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| {{#Wiki_filter:ACCEIERDDOCUMENTDISIBVTIONSYSTEMREGULRYINFORMATIONDISTRIBUTSYSTEM(RIDS)ACCESSIONNBR:9302110293DOC.DATE:93/02/05NOTARIZED:NOFACIL:50-389St.LuciePlant,Unit2,FloridaPower&LightCo.AUTH.NAMEAUTHORAFFILIATIONHURCHALLA,J.A.FloridaPowerELightCo.SAGER,D.A.-FloridaPower6LightCo.RECIP.NAMERECIPIENTAFFILIATIONDOCKET05000389 | | {{#Wiki_filter:ACCEIERDDOCUMENTDISIBVTIONSYSTEMREGULRYINFORMATION DISTRIBUT SYSTEM(RIDS)ACCESSION NBR:9302110293 DOC.DATE: |
| | 93/02/05NOTARIZED: |
| | NOFACIL:50-389 St.LuciePlant,Unit2,FloridaPower&LightCo.AUTH.NAMEAUTHORAFFILIATION HURCHALLA,J.A. |
| | FloridaPowerELightCo.SAGER,D.A. |
| | -FloridaPower6LightCo.RECIP.NAME RECIPIENT AFFILIATION DOCKET05000389 |
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER93-001-00:on930108,chemistrytechnicianfailedtosamplethirdSItank6samplingofSItank2A1notperformedwithinTSrequiredintervalafterfillingtank.Causedbypersonnelerror.Personnelcounseled.W/930205ltr.DISTRIBUTIONCODE:IE22TCOPIESRECEIVED:LTRgENCLgSIZE:TITLE:50.73/50.9LicenseeEventReport(LER)-,IncidentRpt,etc.NOTES:RECiPIENTIDCODE/NAMEPD2-2LANORRIS,JINTERNAL:ACNWAEOD/DOA.AEOD/ROAB/DSPNRR/DLPQ/LHFB10NRR/DOEA/OEABNRR/DST/SELB8DNR~SPLB8DlREGFILE02GN2~LE01EXTERNAL:EGErGBRYCE,J.HNRCPDRNSICPOORE,W.COPIESLTTRENCL1111221122111111111111221111RECIPIENTIDCODE/NAMEPD2-2PDACRSAEOD/DSP/TPABNRR/DET/EMEB7ENRR/DLPQ/LPEB10NRR/DREP/PRPB11NRR/DST/SICB8H3NRR/DST/SRXB8ERES/DSIR/EIBLSTLOBBYWARDNSICMURPHY,G.ANUDOCSFULLTXTCOPIESLTTRENCL1-12211111122111111111111RNOTETOALL"RIDS"RECIPIENTS:PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2065)TOELIMINATEYOURNAMEFROMDISTRIBUTIONLISTSFORDOCUMENTSYOUDON'TNEED!LSFULLTEXTCONVERSIONREQUIREDTOTALNUMBEROFCOPIESREQUIRED:LTTR31ENCL31 P.O.Box128,Ft.Pierce,FL3o954-0128February5,1993L-'93-3010CFR50.73U.S.NuclearRegulatoryCommissionAttn:DocumentControlDeskWashington,D.C.20555Re:St.LucieUnit2DocketNo.50-389ReportableEvent:93-001DateofEvent:January8,1993MissedSurveillanceforSafetyInectionTankSamlinDuetoPersonnelErrorTheattachedLicenseeEventReportisbeingsubmittedpursuanttotherequirementsof10CFR50.73toprovidenotificationofthesubjectevent.Verytrulyyours,D.A.SVicePSt.LugersidentePlantDAS/JWH/kwAttachmentcc:StewartD.Ebneter,RegionalAdministrator,USNRCRegionII.SeniorResident,Inspector,USNRC,St.LuciePlantDAS/PSLN857-933.000429302110293930205PDRADOCK050003B98PDRanFPLGroupcompany~/gJI FPLFscsirriisoiNRCFormS68(e.es)VS.NLCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)APPITCYT0CNSISA$150010lEXP'.l1500tESTNEEDNATCEN005PESPONSEToCOWLYWITHTHEPPOISAATIONCOLLECTONINOLEST150ll550$,TONWAAOCONMENTSPECAIEANO55505tH5STNAATETOTIEPECOPOSANCINPCTTTSIIANAOENENTTTLFNCH(P~LLS,IACLENLINQAATOIYCONLPSSCFLWANANCTCN.CCt05NLAIOTOTHEPAPENFICFIAFETACTCNPNCVECTOl50010PACF5IcEoFNANAEELENTNoNAxft.wASFNIOTIPLoct05NLFACILITYNAME(1)DOCKETNUMBER(2)St.LucieUnit2A05000389103T'TLE{)MissedSurveillanceforSafetyInjectionTankSamplingDuetoPersonnelErrorEVENTDATE(5)LERNUMBER(6)REPORTDATE(7)OTHERFACILITIESINVOLVED(8)01DAY08YEAR93YEAR93,.'IAL001gR0002DAYYEAR0593FACILITYNAMESN/AN/ADOCKETNUMBER(S)050005000OPERATINGMODE(9)POWERLEVEL(10)100;Cgjlr20.402(b)20.405(a)(1)(i)20.405(c)50.36(c)(1)20A05(a)(1)(II)50.36(c)(2)20.405(a)(1)(iii)20.405(a)(1)(iv)20.405(a)(1)(v)50.73(a)(2)(I)50.73(a)(2)(ii)50.73(a)(2)(iii)LICENSEECONTACTFORTHISLER1250.73(a)(2)(iv)50.73(a){2){v)50.73(a)(2)(vii)50.73(a)(2)(viii)(A)50.73(a)(2)(viii)(B)50.73(a)(2)(x)THISREPORTISSUBMITTEDPURSUANTTOTHEREQUIREMENTSOF10CFR:Checkoneormoreofthefollowin,(11)73.71(b)73;71{c)OTHER(SpecifyinAbstractbelowandinTextNRCForm366A)NAMEJamesA.Hurchalla,ShiftTechnicalAdvisorTELEPONENUMBERAREACODE407465-3550COMPLETEONELINEFOREACHCOMPONENTFAILUREDESCRIBEDINTHISREPORT13CAUSESYSTEMCOMPONENTREPORTABLETONPRDSSYSTEMCOMPONENTMANUFACREPORTABLETURERTONPRDSSUPPLEMENTALREPORTEXPECTED14YES(Ifyes,completeEXPECTEDSUBMISSIONDATE)XNOIIIEXPECTEDMONTHDAYYEARSUBMISSIONDATE(15)ABSTRACT'(Limitto1400spaces.i.e.approximatelyfifteensingle-spacetypewrittenlines)(16)OnJanuary8,at0500aReactorControlOperator(RCO)filledthe2A1,2A2,and2B2SafetytnjectionTanks'SITs)andsubsequentlynotifiedChemistry.AChemistrytechniciansamptedtwooftheSITspertherequiredsurveillancebutfaitedtosamplethethird.OnJanuary8,1993,at2300theUnit2AssistantNuclearPlantSupervisordiscoveredthatthesamplingofthe2A1SafetyInjectionTankhadnotbeenperformedbyChemistrywithintherequiredtimeintervalatterfillingthetank.Using,the25%maximumallowableextensionpermittedby.TechnicalSpecification(TS)4.0.2,thelatesttimeatwhichthesamplingcouldhavebeenperformedontimewasJanuary8,at1230.TherootcauseoftheeventwaspersonnelerrorbyaChemistrytechnicianresponsibleforthesampling.WheninformedbyOperationsthatspecificSITshavebeenfilleditistheresponsibilityoftheChemistrydepartmentpersonnelonshifttosampletheseSITsfortherequiredboronconcentrationperTS4.5.1.1.b.Inaddition,therewasafailureonthepartofthecontrolroompersonneltorealizethatoneofthethreefilledSITshadnotbeensampledwhenChemistrynotifiedthemthattwoSITswerewithinspecification.Correctiveactionswere;1)Performthe2A1SITsutveiltance.2)CreateastatusboardbywhichChemistrycaninsurethattheappropriateSITshavebeensampled.3)TheChemistrypersonnelinvolvedwerecounselled.4)Operationspersonnelhavebeencounselled.5)AHumanPerformanceEvaluationSystemevaluationwassubsequentlyconductedwhosefindingsagreewiththisreport.FPLFacsimileofNRCForm366(6-89) | | LER93-001-00:on 930108,chemistry technician failedtosamplethirdSItank6samplingofSItank2A1notperformed withinTSrequiredintervalafterfillingtank.Causedbypersonnel error.Personnel counseled.W/930205 ltr.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:LTR gENCLgSIZE:TITLE:50.73/50.9 LicenseeEventReport(LER)-,IncidentRpt,etc.NOTES:RECiPIENT IDCODE/NAME PD2-2LANORRIS,JINTERNAL: |
| PPLPSCSIITTleOtNRCFOTm&OSl689)U.S.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATlON'APPROITOCAATKLSITCSIPAlsplpaaACGITTSTPAATTOIMICTNPTRRTSPONSlTOOOINTTWITHTIPSPPOISAAOCNCOIlfCTONRTOUTSTIISAIPTSIORNNOCCANRNT0RTGARTNICTAPSXNTSTINATlTOPICRTCORCSAICIISPORTSNANAGTASNTSRANCHTP000AU0,IAICI0AITRlOIAATORYOAA+CSSN70WANTNCTON,OCT000SNAPTOTIRPAPTRWOPNRTOVCTIONPRORCTI'TIICCISPAOIIICCOPNANAKNTNTAM)TANCTT.WANSNCTOIAOCPPNOFACILITYNAME(1)St.LucieUnit2DOCKETNUMBER(2)YEAREQUENTIALNUMBER."T',."REVISIONvlNUMBERLERNUMBER(6)PAGE(3)05000389TEXT(Ifmorespaceisreqoired,tjseadditionalNRCForm366A's)(17)9300000203OperationsfillsSafetyInjectionTanks(SIT)(EIIS:BP)asnecessarytomaintaintherequiredTechnicalSpecification(TS)level.SubsequentlytheseSITsmustbesampledinaccordancewith-ChemistryOperatingProcedure2-C-60within6hourstoensurethattherequiredTSboronconcentrationhasbeenmaintained.OnJanuary8,1993,at0500aReactorControlOperator(RCO)filledthe2A1,2A2,and2B2SITs.At0530henotifiedtheonshiftChemistrytechnician.TheChemistrytechnicianwhoreceivedthecallturnedthesamplingresponsibilityovertoanoncomingtechnicianonthenextshift.ThistechnicianreceivedtheappropriateverbalinstructionsofwhichSITstocheckbutonlysampledthe2A2and2B2SITs.At0830henotifiedthecontrolroomthattheseSITsweresatisfactorywilhrespecttoboronconcentration.OperationspersonnelreceivedthecallandfailedtonoticethatoneoftheSITshadnotbeensampled.At2314theoncomingAssistantNuclearPlantSupervisorwasreviewingtheRCOchronologicalloganddiscoveredthe2A1SIThadnotbeensampled.TheSITwasadministrativelydeclaredoutofserviceandChemistrywasnotifiedtosampleit.Thesampleshowedsatisfactoryboronconcentrationandthe2A1SITwasdeclaredbackinserviceat2345.VTherootcauseoftheeventiscognitivepersonnelerrorbyautilityChemistrytechnicianbyfailingtoensurethesamplingoftheappropriateSITs.AcontributingfactoristhattherewasnomethodotherthanverbalrequestturnoverbetweenChemistrytechnicianstoinsurethatthecorrectSITsaresampled.ThisplacesthefullresponsibilityforthecorrectnessandtimelinessofthisTSsurveillanceonverbalcommunicationwithnorecordedinformationfortheChemistrytechniciantoreference.Inaddition,therewasafailureonthepartofcontrolroompersonneltorealizethatoneofthethreeSITshadnotbeensampledwhenChemistrynotifiedthemthattwoSITswerewithinspecification.Therewerenounusualcharacteristicsoftheworklocationwhichcontributedtothisevent.TVThiseventisreportableunder10CFR50.73.a.2.i.b,asamissedsurveillancerequiredbyTechnicalSpecifications.TechnicalSpecification4.5.1.1.bstatesthateachSafetyInjectionTankshallbedemonstratedoperablewithin6hoursaftereachsolutionvolumeincreasegreaterthanorequalto1%oftankvolumebyverifyingtheboronconcentrationofthesolution.ThepurposeofthissamplingistoprovideassurancethattheboronconcentrationoftheSITshasnotbeenchangedtoavalue-outsidethebandoftheTechnicalSpecificationrequirements.ThisassuresthattheassumptionsusedfortheSITsintheFinalUpdatedSafetyAnalysisReport(FUSAR)arevalid.Thesurveillanceofthe2A1SITwascompletedat2340,or12hoursand40minutespasttherequiredTechnicalSpecificationsampletime.FPLFacsimileofNRCForm366(6-89)
| | ACNWAEOD/DOA. |
| FPLFacsimrootrNRCForm666(669t.U.S.NUCLEARREGULATORYCOMMISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATlONAPPAOVTOCallNCI0ll00IOI000TIES.0000000TAAATTOnvexNPTfrfE0PONTEToCOAWlvvATNTI0000aNAAOONCcuTCTEPIIEOIE00I0000000fCTIWATErCCANENT0IECANONCTAPCTN00TINATKToOETECOII0AlafEPTNTCNANACTAENTCPlANCNIP0000uaIAcTTArlTEaAATONT~WASHNCTON,OC00000APATToTIE0APTfrWONATECOCTIONPNOEC'0fll000IOl00ÃfICTOfNANACTIENTAIOTANCET.WACIIAOT000OC00NO.FACILITYNAME{1)St.LUCieUnit2DOCKETNUMBER(2)YEARLERNUMBER{6)EQUENTIALNUMBERREVISIONNUMBERPAGE(3)0500038993TEXT(Ifmorespaceisrequired,useadditionalNRCForm366A's)(17)0010003003TheresultsofthechemistrysampleshowedtheboronconcentrationtobewithinTechnicalSpecification3.5.1.c.The2A1SafetyInjectionTankwascapableofperformingitsintendedsafetyfunctionassetforthintheassumptionsoftheFUSAR,sections6.3.2.2.1and6.3.3.4.3.f.TI;erefore,lhehealthandsafetyofthepublicwasnotaffectedbythisevent.1)The2A1SafetyInjectionTank(SIT)ChemistrySurveillancewasperformedwithsatisfactoryresultsJanuary8,1993at2340hours.2)TheChemistrydepartmentnowusesastatusboardtotrackregulatoryrequiredsurveillancesthatarenotperiodicallyscheduled..3)ThepersonnelinvolvedinthiseventhavebeencounselledbytheChemistrysupervisorontheimportanceofmeetingsurveillancerequirements.-4)TheOperationssupervisorhasissuedaNightOrderonthiseventwhichemphasizestheneedforoperatorstotracksurveillancessuchastheonedescribedintheLERviatheoperatorturnoversheet,andtheneedfortheoncomingcrewstocarefullyreviewthechronologicallog.5)AHumanPerformanceEnhancementSystem(HPES)evaluationwasperformed.TheresultsagreewiththeconclusionsofthisLicenseeEventReport.ITINAFnnFilTherewerenocomponentfailuresinvolvedinthisevent.VIAprevioussimilareventisdescribedinLER389-89-008,whichdescribesamissedsurveillanceforSafetyInjectionLoopHeadervalvesfollowingthefillingoftwoSITs.FPLFacsimileofNRCForm366(6.89)}} | | AEOD/ROAB/DSP NRR/DLPQ/LHFB10 NRR/DOEA/OEAB NRR/DST/SELB 8DNR~SPLB8DlREGFILE02GN2~LE01EXTERNAL: |
| | EGErGBRYCE,J.H NRCPDRNSICPOORE,W.COPIESLTTRENCL1111221122111111111111221111RECIPIENT IDCODE/NAME PD2-2PDACRSAEOD/DSP/TPAB NRR/DET/EMEB 7ENRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB8H3 NRR/DST/SRXB 8ERES/DSIR/EIB LSTLOBBYWARDNSICMURPHY,G.A NUDOCSFULLTXTCOPIESLTTRENCL1-12211111122111111111111RNOTETOALL"RIDS"RECIPIENTS: |
| | PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2065) |
| | TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!LSFULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED: |
| | LTTR31ENCL31 P.O.Box128,Ft.Pierce,FL3o954-0128 February5,1993L-'93-3010CFR50.73U.S.NuclearRegulatory Commission Attn:DocumentControlDeskWashington, D.C.20555Re:St.LucieUnit2DocketNo.50-389Reportable Event:93-001DateofEvent:January8,1993MissedSurveillance forSafetyInectionTankSamlinDuetoPersonnel ErrorTheattachedLicenseeEventReportisbeingsubmitted pursuanttotherequirements of10CFR50.73toprovidenotification ofthesubjectevent.Verytrulyyours,D.A.SVicePSt.LugersidentePlantDAS/JWH/kw Attachment cc:StewartD.Ebneter,RegionalAdministrator, USNRCRegionII.SeniorResident, Inspector, USNRC,St.LuciePlantDAS/PSLN857-933.000429302110293 930205PDRADOCK050003B98PDRanFPLGroupcompany~/gJI FPLFscsirriis oiNRCFormS68(e.es)VS.NLCLEARREGULATORY COMMISSION LICENSEEEVENTREPORT(LER)APPITCYT0CNSISA$150010lEXP'.l1500tESTNEEDNATCEN005PESPONSEToCOWLYWITHTHEPPOISAATION COLLECTONINOLEST150 ll550$,TONWAAOCONMENTSPECAIEANO 55505tH5STNAATETOTIEPECOPOSANC INPCTTTSIIANAOENENT TTLFNCH(P~LLS, IACLENLINQAATOIY CONLPSSCFL WANANCTCN. |
| | CCt05NLAIOTOTHEPAPENFICFIA FETACTCNPNCVECTOl50010PACF5IcEoFNANAEELENTNoNAxft.wASFNIOTIPL oct05NLFACILITYNAME(1)DOCKETNUMBER(2)St.LucieUnit2A050003891 03T'TLE{)MissedSurveillance forSafetyInjection TankSamplingDuetoPersonnel ErrorEVENTDATE(5)LERNUMBER(6)REPORTDATE(7)OTHERFACILITIES INVOLVED(8)01DAY08YEAR93YEAR93,.'IAL001gR0002DAYYEAR0593FACILITYNAMESN/AN/ADOCKETNUMBER(S) 050005000OPERATING MODE(9)POWERLEVEL(10)100;Cgjlr20.402(b) 20.405(a)(1)(i) 20.405(c) 50.36(c)(1) 20A05(a)(1)(II) 50.36(c)(2) 20.405(a)(1)(iii) 20.405(a)(1)(iv) 20.405(a)(1)(v) 50.73(a)(2)(I)50.73(a)(2)(ii) 50.73(a)(2) |
| | (iii)LICENSEECONTACTFORTHISLER1250.73(a)(2)(iv) 50.73(a){2){v) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(x) |
| | THISREPORTISSUBMITTED PURSUANTTOTHEREQUIREMENTS OF10CFR:Checkoneormoreofthefollowin, (11)73.71(b)73;71{c)OTHER(SpecifyinAbstractbelowandinTextNRCForm366A)NAMEJamesA.Hurchalla, ShiftTechnical AdvisorTELEPONENUMBERAREACODE407465-3550COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT13CAUSESYSTEMCOMPONENT REPORTABLE TONPRDSSYSTEMCOMPONENT MANUFACREPORTABLE TURERTONPRDSSUPPLEMENTAL REPORTEXPECTED14YES(Ifyes,completeEXPECTEDSUBMISSION DATE)XNOIIIEXPECTEDMONTHDAYYEARSUBMISSION DATE(15)ABSTRACT'(Limitto1400spaces.i.e. |
| | approximately fifteensingle-space typewritten lines)(16)OnJanuary8,at0500aReactorControlOperator(RCO)filledthe2A1,2A2,and2B2Safetytnjection Tanks'SITs) andsubsequently notifiedChemistry. |
| | AChemistry technician samptedtwooftheSITspertherequiredsurveillance butfaitedtosamplethethird.OnJanuary8,1993,at2300theUnit2Assistant NuclearPlantSupervisor discovered thatthesamplingofthe2A1SafetyInjection Tankhadnotbeenperformed byChemistry withintherequiredtimeintervalatterfillingthetank.Using,the25%maximumallowable extension permitted by.Technical Specification (TS)4.0.2,thelatesttimeatwhichthesamplingcouldhavebeenperformed ontimewasJanuary8,at1230.Therootcauseoftheeventwaspersonnel errorbyaChemistry technician responsible forthesampling. |
| | WheninformedbyOperations thatspecificSITshavebeenfilleditistheresponsibility oftheChemistry department personnel onshifttosampletheseSITsfortherequiredboronconcentration perTS4.5.1.1.b. |
| | Inaddition, therewasafailureonthepartofthecontrolroompersonnel torealizethatoneofthethreefilledSITshadnotbeensampledwhenChemistry notifiedthemthattwoSITswerewithinspecification. |
| | Corrective actionswere;1)Performthe2A1SITsutveiltance. |
| | 2)CreateastatusboardbywhichChemistry caninsurethattheappropriate SITshavebeensampled.3)TheChemistry personnel involvedwerecounselled. |
| | 4)Operations personnel havebeencounselled. |
| | 5)AHumanPerformance Evaluation Systemevaluation wassubsequently conducted whosefindingsagreewiththisreport.FPLFacsimile ofNRCForm366(6-89) |
| | PPLPSCSIITTle OtNRCFOTm&OSl689)U.S.NUCLEARREGULATORY COMMISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATlON |
| | 'APPROITOCAAT KLSITCSIPA lsplpaaACGITTSTPAATTOIMICTNPTRRTSPONSl TOOOINTTWITH TIPSPPOISAAOCNCOIlf CTONRTOUTSTIISAIPTSIORNNOCCANRNT0RTGARTNIC TAPSXNTSTINATlTOPICRTCORCSAICIISPORTSNANAGTASNTSRANCHTP000AU0,IAICI0AITRlOIAATORYOAA+CSSN70 WANTNCTON,OCT000S NAPTOTIRPAPTRWOPNRTOVCTIONPRORCTI'TIICCISPAOIIICC OPNANAKNTNTAM)TANCTT.WANSNCTOIAOCPPNOFACILITYNAME(1)St.LucieUnit2DOCKETNUMBER(2)YEAREQUENTIAL NUMBER."T',."REVISIONvlNUMBERLERNUMBER(6)PAGE(3)05000389TEXT(Ifmorespaceisreqoired, tjseadditional NRCForm366A's)(17)9300000203Operations fillsSafetyInjection Tanks(SIT)(EIIS: |
| | BP)asnecessary tomaintaintherequiredTechnical Specification (TS)level.Subsequently theseSITsmustbesampledinaccordance with-Chemistry Operating Procedure 2-C-60within6hourstoensurethattherequiredTSboronconcentration hasbeenmaintained. |
| | OnJanuary8,1993,at0500aReactorControlOperator(RCO)filledthe2A1,2A2,and2B2SITs.At0530henotifiedtheonshiftChemistry technician. |
| | TheChemistry technician whoreceivedthecallturnedthesamplingresponsibility overtoanoncomingtechnician onthenextshift.Thistechnician receivedtheappropriate verbalinstructions ofwhichSITstocheckbutonlysampledthe2A2and2B2SITs.At0830henotifiedthecontrolroomthattheseSITsweresatisfactory wilhrespecttoboronconcentration. |
| | Operations personnel receivedthecallandfailedtonoticethatoneoftheSITshadnotbeensampled.At2314theoncomingAssistant NuclearPlantSupervisor wasreviewing theRCOchronological loganddiscovered the2A1SIThadnotbeensampled.TheSITwasadministratively declaredoutofserviceandChemistry wasnotifiedtosampleit.Thesampleshowedsatisfactory boronconcentration andthe2A1SITwasdeclaredbackinserviceat2345.VTherootcauseoftheeventiscognitive personnel errorbyautilityChemistry technician byfailingtoensurethesamplingoftheappropriate SITs.Acontributing factoristhattherewasnomethodotherthanverbalrequestturnoverbetweenChemistry technicians toinsurethatthecorrectSITsaresampled.Thisplacesthefullresponsibility forthecorrectness andtimeliness ofthisTSsurveillance onverbalcommunication withnorecordedinformation fortheChemistry technician toreference. |
| | Inaddition, therewasafailureonthepartofcontrolroompersonnel torealizethatoneofthethreeSITshadnotbeensampledwhenChemistry notifiedthemthattwoSITswerewithinspecification. |
| | Therewerenounusualcharacteristics oftheworklocationwhichcontributed tothisevent.TVThiseventisreportable under10CFR50.73.a.2.i.b, asamissedsurveillance requiredbyTechnical Specifications. |
| | Technical Specification 4.5.1.1.b statesthateachSafetyInjection Tankshallbedemonstrated operablewithin6hoursaftereachsolutionvolumeincreasegreaterthanorequalto1%oftankvolumebyverifying theboronconcentration ofthesolution. |
| | Thepurposeofthissamplingistoprovideassurance thattheboronconcentration oftheSITshasnotbeenchangedtoavalue-outsidethebandoftheTechnical Specification requirements. |
| | Thisassuresthattheassumptions usedfortheSITsintheFinalUpdatedSafetyAnalysisReport(FUSAR)arevalid.Thesurveillance ofthe2A1SITwascompleted at2340,or12hoursand40minutespasttherequiredTechnical Specification sampletime.FPLFacsimile ofNRCForm366(6-89) |
| | FPLFacsimrootrNRCForm666(669t.U.S.NUCLEARREGULATORY COMMISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATlON APPAOVTOCallNCI 0ll00IOI000TIES.0000000TAAATTO nvexNPTfrfE0PONTE ToCOAWlvvATN TI0000aNAAOONCcuTCTEPI IEOIE00I0000000fCTIWATErCCANENT0IECANONCTAPCTN00TINATKToOETECOII0AlafEPTNTCNANACTAENTCPlANCNIP0000ua IAcTTArlTEaAATONT~ |
| | WASHNCTON,OC00000APATToTIE0APTfrWONATECOCTIONPNOEC'0fll000IOl00ÃfICTOfNANACTIENT AIOTANCET.WACIIAOT000 OC00NO.FACILITYNAME{1)St.LUCieUnit2DOCKETNUMBER(2)YEARLERNUMBER{6)EQUENTIAL NUMBERREVISIONNUMBERPAGE(3)0500038993TEXT(Ifmorespaceisrequired, useadditional NRCForm366A's)(17)0010003003Theresultsofthechemistry sampleshowedtheboronconcentration tobewithinTechnical Specification 3.5.1.c.The2A1SafetyInjection Tankwascapableofperforming itsintendedsafetyfunctionassetforthintheassumptions oftheFUSAR,sections6.3.2.2.1 and6.3.3.4.3.f. |
| | TI;erefore, lhehealthandsafetyofthepublicwasnotaffectedbythisevent.1)The2A1SafetyInjection Tank(SIT)Chemistry Surveillance wasperformed withsatisfactory resultsJanuary8,1993at2340hours.2)TheChemistry department nowusesastatusboardtotrackregulatory requiredsurveillances thatarenotperiodically scheduled.. |
| | 3)Thepersonnel involvedinthiseventhavebeencounselled bytheChemistry supervisor ontheimportance ofmeetingsurveillance requirements. |
| | -4)TheOperations supervisor hasissuedaNightOrderonthiseventwhichemphasizes theneedforoperators totracksurveillances suchastheonedescribed intheLERviatheoperatorturnoversheet,andtheneedfortheoncomingcrewstocarefully reviewthechronological log.5)AHumanPerformance Enhancement System(HPES)evaluation wasperformed. |
| | Theresultsagreewiththeconclusions ofthisLicenseeEventReport.ITINAFnnFilTherewerenocomponent failuresinvolvedinthisevent.VIAprevioussimilareventisdescribed inLER389-89-008, whichdescribes amissedsurveillance forSafetyInjection LoopHeadervalvesfollowing thefillingoftwoSITs.FPLFacsimile ofNRCForm366(6.89)}} |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17241A4891999-10-0707 October 1999 LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr ML17241A4111999-07-16016 July 1999 LER 99-007-00:on 990610,unplanned Cooldown Transient Occurred Due to Personnel Error.Trained & Briefed Personnel & Revised Procedures.With 990716 Ltr ML17241A4031999-07-0606 July 1999 LER 99-006-00:on 990605,sub-critical Reactor Trip Occurred Due to Inadvertent MSIV Opening.Caused by Personnel Error. Provided Operation Supervision Instruction to Operating Crews,Stand Down Meetings & Operator Aids.With 990706 Ltr ML17241A4041999-07-0606 July 1999 LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr ML17241A3941999-06-30030 June 1999 LER 99-004-01:on 990415,as Found Cycle 10 Psv Setpoints Were Outside TS Limits.Caused by Manufacturing Process Defect. All Three Psvs Were Replaced with pre-tested Valves During Cycle 11 Refueling Outage.With 990630 Ltr ML17241A3551999-06-0404 June 1999 LER 99-002-00:on 990505,both Trains of Safety Injection Actuation Were Blocked During Surveillance.Caused by Procedure Error.Procedure Revised.With 990604 Ltr ML17241A3321999-05-17017 May 1999 LER 99-004-00:on 990415,determined That as Found Cycle 10 Psv Setpoints Outside TS Limits.Root Cause Under Investigation.Psvs Replaced with pe-tested Valves During Cycle 11 ML17241A3271999-05-0606 May 1999 LER 99-003-00:on 990406,ECCS Suction Header Leak Resulted in Both ECCS Trains Being Inoperable & Entry Into TS 3.0.3. Caused by Chloride Induced OD Stress Corrosion Cracking of Piping.Made Code Repairs & Coated Piping.With 990506 Ltr ML17229B0791999-04-0707 April 1999 LER 99-001-00:on 990309,discovered Inadequate Design & IST SRs for Iodine Removal Sys (Irs).Caused by Original Design Inadequacies & Personnel Error.Naoh Tank Vent Valve V07233 Was Tagged Open.With 990407 Ltr ML17229B0801999-04-0707 April 1999 LER 99-002-00:on 990311,SG ECT Error Caused Operation with Condition Prohibited by Ts.Caused by Deficiencies in Data Analysis Guideline Instructions.Licensee Will Change Data Analysis Guidelines for Lead Analysts.With 990407 Ltr ML17229B0541999-03-10010 March 1999 LER 99-001-00:on 990211,inadequate TS SRs for SIT & SDC Isolation Valves Were Noted.Caused by Failure to Correctly Implement TS Srs.Submitted LAR to Align Required TS SR with Design Bases Requirements Being Verified.With 990310 Ltr ML17229A9901999-01-20020 January 1999 LER 98-009-00:on 981223,noted That Facility Operated Outside of Design Basis.Caused by non-conservative MSLB Analysis Inputs.Will Review SR Component Differences Between Units & Will re-baseline LTOP Analysis.With 990120 Ltr ML17229A9821999-01-0404 January 1999 LER 98-010-00:on 981207,RCS Boron Sample Frequency Required by Ts,Was Exceeded by Twelve Minutes.Caused by Personnel Error.Equipment Clearance Order Was Lifted to Draw Required Sample & Operations Procedure Was Changed.With 990104 Ltr ML17229A9611998-12-22022 December 1998 LER 97-002-01:on 981204,containment Sump Debris Screen Was Not IAW Design.Caused by Inadequate C/As for Sump Screen Anamolies.All Identified Sump Screen Deficiencies Were Dispositioned &/Or Repaired.With 981222 Ltr ML17229A9561998-12-15015 December 1998 LER 98-008-00:on 981118,missed TS SG U Tube Insp.Caused by Encoding Errors While Using Remote Positioning Fixtures.All SG Tube Surveyed.With 981215 Ltr ML17229A9301998-11-25025 November 1998 LER 98-005-01:on 980807,discovered That New MOV Methodology Caused Past PORV Block Valve Operability Problem.Caused by Inadequacies in Original Vendor MOV Methodology.Planned Valve Mods Will Be Implemented During Cycle 11 1998 Outage ML17229A9021998-11-0404 November 1998 LER 98-008-00:on 981008,inadequate Reactor Protection Sys Trip Bypass TS Was Noted.Caused by Poorly Worded Ts. Submitted LAR to Clarify Power Requirements for High Rate of Power Trips.With 981104 Ltr ML17229A8771998-10-14014 October 1998 LER 98-006-00:on 980918,inadvertent Afas Actuation Was Noted.Caused by Degradation of Multiple Afas Power Supplies. Replaced Afas Power Supplies & Revised Procedures.With 981014 Ltr ML17229A8761998-10-14014 October 1998 LER 98-007-00:on 980918,identified Discrepancies Between Fire Protection Design Requirements & Field Conditions. Caused by Inadequate Translation & Implementation of Fire Protection Requirements.Procedures Revised.With 981014 Ltr ML17229A8511998-09-0202 September 1998 LER 98-005-00:on 980807,discovered That PORV Margins Were Insufficient to Accommodate Addl Conservatism.Caused by Inadequacies in Original Vendor MOV Methodology.Will Implement Planned Valve Actuator mods.W/980902 Ltr ML17229A8201998-07-29029 July 1998 LER 98-007-00:on 980630,inadequate Procedure May Have Resulted in SBO Recovery Complications.Caused by Inadequate Procedures.Attached Caution Tags to Appropriate Control switches.W/980729 Ltr ML17229A7411998-05-28028 May 1998 LER 98-004-00:on 980430,discovered Waste Gas Decay Tank Operation W/O Available Oxygen Analyzers,Which Is Prohibited by Ts.Caused by Inadequate Licensee Review of License Amend. Oxygen Analyzer recalibrated.W/980528 Ltr ML17229A7381998-05-21021 May 1998 LER 98-006-00:on 980421,missed EDG Fuel Oil Sample Surveillance Was Noted.Caused by Personnel Error.Revised Fuel Oil Sampling Service Purchase Order & Revised Site procedure.W/980521 Ltr ML17229A7011998-04-27027 April 1998 LER 98-003-00:on 980326,discovered Containment Pressure Instrumentation Design Single Failure Vulnerability.Caused by Inadequate Design by Personnel Error.Removed RPS & ESFAS Containment Pressure Bypass Keys immediately.W/980427 Ltr ML17229A6761998-04-0202 April 1998 LER 98-005-00:on 980305,identified Two Conditions That Were Outside App R Design Bases.Caused by Design Oversight During Development of Original App R Safe SD Design.Established 30 Minute Roving Fire Watches & Provided training.W/980402 Ltr ML17229A6731998-03-26026 March 1998 LER 98-002-00:on 980224,radiation Monitor Surveillance Inadequacies Led to Operating of Facility Prohibited by Tss. Caused by Congnitive Personnel Error.Permanent Procedure Changes Were implemented.W/980326 Ltr ML17229A6551998-03-0505 March 1998 LER 98-001-00:on 980206,high/low Pressure Shutdown Cooling Interface Was Noted Outside App R Design Bases.Caused by Personnel Error.Addl Guidance Was Provided to Engineering Dept personnel.W/980305 Ltr ML17229A6281998-02-19019 February 1998 LER 98-004-00:on 980121,emergency Lighting Outside App R Design Bases Occurred.Caused by Congnitive Personnel Error During Translation of App R Section Iii.Procedures Onop 1 & 2 ONP-100.01 Were Issued for Use on 980206.W/980219 Ltr ML17229A6211998-02-0909 February 1998 LER 98-003-00:on 980110,manual Rt Due to DEH Leak at Turbine Test Block Was Noted.Caused by o-ring Extrusion.Shortened Bolts by About 0.125 & Reinstalled at Correct Torque values.W/980209 Ltr ML17229A6191998-02-0404 February 1998 LER 98-002-00:on 980105,CIS Bistable in Bypass Resulted in Condition Prohibited by Tss.Caused by Personnel Error. Radiation Monitor Was Restored to service.W/980204 Ltr ML17229A6161998-02-0303 February 1998 LER 98-001-00:on 980104,inadvertent RPS Actuation Occurred Due to Personnel Error.Caused by Procedural Inadequacies & Inadequate self-checking by Licensed Utility Personnel. Placards Have Been Placed in CRs.W/980203 Ltr ML17229A6051998-01-27027 January 1998 LER 97-010-01:on 971027,inadvertent Core Alteration Prohibited by TSs Were Noted Due to Stuck Cea.Caused by Personnel Error.Cea #24 Was Dislodged & Transferred to Spent Pool for insp.W/980127 Ltr ML17229A5501997-12-0505 December 1997 LER 97-008-00:on 971107,inadequate CR Ventilation Surveillance Resulted in Condition Prohibited by Ts.Caused by non-cognitive Personnel Error.Operating Procedure 2-1900050 Was revised.W/971205 Ltr ML17309A9091997-12-0202 December 1997 LER 97-011-00:on 971102,non-conservative RAS Set Point Resulted in Operation Prohibited by Ts.Caused by Inadequate Set Point & Instrument Loop Scaling Process.Revised ESFAS Functional Tp W/Proper Set point.W/971202 Ltr ML17229A5391997-11-26026 November 1997 LER 97-010-00:on 971027,inadvertant Core Alteration Prohibited by TS Occurred.Caused by CEA Failure to Detach from Ugs.Safety Evaluation Was Performed & Procedural Rev Made to Continue Upper Guide Structure move.W/971126 Ltr ML17229A5151997-11-0707 November 1997 LER 97-007-00:on 971008,inoperable Containment Cooling Fan Resulted in Operation of Facility Outside Design Basis. Caused by non-cognitive Personnel Error.Ccs Operation Was Revised & Issued on 971013.W/971107 Ltr ML17229A4991997-10-17017 October 1997 LER 97-009-00:on 970917,inoperable PORV Block Valve Resulted in Operation Prohibited by Tech Specs Occurred.Caused by Plant GL 89-10 Program Plan to Review Plant Manager Action Item Sys.Porv Block Valve V-1403 restored.W/971017 Ltr ML17309A9011997-08-27027 August 1997 LER 97-008-00:on 970728,mechanical Fire Penetrations Were Inoperable & Outside App R Design Bases.Caused by Seal Mfg Not Providing Formal Documentation for Installed Seals. Modified Inoperable Fire penetrations.W/970827 Ltr ML17229A4311997-07-29029 July 1997 LER 97-006-00:on 970630,discovered Inadequate Testing of Engineered Safety Features Subgroup Relays.Caused by Inadequacy in Implementing TS Requirements in Surveillance Procedures.Revised Surveillance procedures.W/970729 Ltr ML17229A4241997-07-25025 July 1997 LER 97-005-00:on 970625,discovered That Hot Shutdown Control Panel Shutdown Cooling Flow indicator,FI-3306 Inoperable. Caused by Weakness in Work Order & Procedure Used to Repair FI-3306.Section Meeting W/I&C Planners held.W/970725 Ltr ML17229A3971997-07-11011 July 1997 LER 97-004-00:on 970611,discovered Incorrect Original Cable Tray Fire Stop Assembly Installation Was Outside App R Design Basis.Caused by Personnel Error.Hourly Fire Watch Patrols Will Be posted.W/970711 Ltr ML17229A3871997-06-19019 June 1997 LER 97-003-00:on 970521,determined Required Post Maint Open Stroke Test for Valve V3245,2B2 SIT Discharge Check Valve, Had Not Been Performed.Caused by Personnel Error.Procedure revised.W/970619 Ltr ML17229A3841997-06-17017 June 1997 LER 97-002-00:on 970518,containment Sump Debris Screen Was Not IAW Design Due to Gaps in Screen Encl.Performed SER to Document Containment Sump Design requirements.W/970617 Ltr ML17229A3751997-06-0202 June 1997 LER 97-006-00:on 970501,operation Was Prohibited by TS Due to Inadequately Tested Degraded Voltage Sys.Revised Unit 1 ESFAS Surveillance Test procedure.W/970602 Ltr ML17229A3611997-05-29029 May 1997 LER 97-007-00:on 970502,reactor Coolant Pump Oil Collection Sys Was Outside App R Design Bases.Identified Leak Sites Were Repaired & Mods to RCP Oil Collection Sys to Capture Any Future Leakage from areas.W/970529 Ltr ML17229A3491997-05-21021 May 1997 LER 97-001-00:on 970423,containment Isolation Actuation Occurred.Caused by Increased Radiation Levels During Removal of Upper Guide Structure.Proper Actuation of Containment Isolation Components Was verified.W/970521 Ltr ML17229A3441997-05-13013 May 1997 LER 97-005-00:on 970419,reactor Was Shutdown Due to Reactor Coolant Pressure Boundary Leakage.Hot Cracking Was Caused by Weld Contamination.Repairs to RCPB Were Completed & 1A SDC Train Was Restored to Svc ML17229A3141997-04-30030 April 1997 LER 97-004-00:on 970402,refueling Machine Was Operating in Manner Prohibited by TS Due to Original Design of Refueling Machine Bypass Feature Conflicting W/Ts Requirements. Eliminated Overload Cut Off Limit bypass.W/970430 Ltr ML17229A2951997-03-31031 March 1997 LER 97-003-00:on 970304,automatic Rt Resulted from Loss of Electrical Power to 1A2 Rc Pump.Rcp Breaker Was Replaced & Pump Was Returned to svc.W/970331 Ltr ML17229A2721997-03-21021 March 1997 LER 97-002-00:on 970221,operation in Excess of Max Rated Thermal Power Occurred Due to Digital Data Processing Sys (Ddps) Calorimetric Error.Verified Acceptable Performance of Ddps Functions & Reviewed Software mods.W/970321 Ltr 1999-07-06
[Table view] Category:RO)
MONTHYEARML17241A4891999-10-0707 October 1999 LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr ML17241A4111999-07-16016 July 1999 LER 99-007-00:on 990610,unplanned Cooldown Transient Occurred Due to Personnel Error.Trained & Briefed Personnel & Revised Procedures.With 990716 Ltr ML17241A4031999-07-0606 July 1999 LER 99-006-00:on 990605,sub-critical Reactor Trip Occurred Due to Inadvertent MSIV Opening.Caused by Personnel Error. Provided Operation Supervision Instruction to Operating Crews,Stand Down Meetings & Operator Aids.With 990706 Ltr ML17241A4041999-07-0606 July 1999 LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr ML17241A3941999-06-30030 June 1999 LER 99-004-01:on 990415,as Found Cycle 10 Psv Setpoints Were Outside TS Limits.Caused by Manufacturing Process Defect. All Three Psvs Were Replaced with pre-tested Valves During Cycle 11 Refueling Outage.With 990630 Ltr ML17241A3551999-06-0404 June 1999 LER 99-002-00:on 990505,both Trains of Safety Injection Actuation Were Blocked During Surveillance.Caused by Procedure Error.Procedure Revised.With 990604 Ltr ML17241A3321999-05-17017 May 1999 LER 99-004-00:on 990415,determined That as Found Cycle 10 Psv Setpoints Outside TS Limits.Root Cause Under Investigation.Psvs Replaced with pe-tested Valves During Cycle 11 ML17241A3271999-05-0606 May 1999 LER 99-003-00:on 990406,ECCS Suction Header Leak Resulted in Both ECCS Trains Being Inoperable & Entry Into TS 3.0.3. Caused by Chloride Induced OD Stress Corrosion Cracking of Piping.Made Code Repairs & Coated Piping.With 990506 Ltr ML17229B0791999-04-0707 April 1999 LER 99-001-00:on 990309,discovered Inadequate Design & IST SRs for Iodine Removal Sys (Irs).Caused by Original Design Inadequacies & Personnel Error.Naoh Tank Vent Valve V07233 Was Tagged Open.With 990407 Ltr ML17229B0801999-04-0707 April 1999 LER 99-002-00:on 990311,SG ECT Error Caused Operation with Condition Prohibited by Ts.Caused by Deficiencies in Data Analysis Guideline Instructions.Licensee Will Change Data Analysis Guidelines for Lead Analysts.With 990407 Ltr ML17229B0541999-03-10010 March 1999 LER 99-001-00:on 990211,inadequate TS SRs for SIT & SDC Isolation Valves Were Noted.Caused by Failure to Correctly Implement TS Srs.Submitted LAR to Align Required TS SR with Design Bases Requirements Being Verified.With 990310 Ltr ML17229A9901999-01-20020 January 1999 LER 98-009-00:on 981223,noted That Facility Operated Outside of Design Basis.Caused by non-conservative MSLB Analysis Inputs.Will Review SR Component Differences Between Units & Will re-baseline LTOP Analysis.With 990120 Ltr ML17229A9821999-01-0404 January 1999 LER 98-010-00:on 981207,RCS Boron Sample Frequency Required by Ts,Was Exceeded by Twelve Minutes.Caused by Personnel Error.Equipment Clearance Order Was Lifted to Draw Required Sample & Operations Procedure Was Changed.With 990104 Ltr ML17229A9611998-12-22022 December 1998 LER 97-002-01:on 981204,containment Sump Debris Screen Was Not IAW Design.Caused by Inadequate C/As for Sump Screen Anamolies.All Identified Sump Screen Deficiencies Were Dispositioned &/Or Repaired.With 981222 Ltr ML17229A9561998-12-15015 December 1998 LER 98-008-00:on 981118,missed TS SG U Tube Insp.Caused by Encoding Errors While Using Remote Positioning Fixtures.All SG Tube Surveyed.With 981215 Ltr ML17229A9301998-11-25025 November 1998 LER 98-005-01:on 980807,discovered That New MOV Methodology Caused Past PORV Block Valve Operability Problem.Caused by Inadequacies in Original Vendor MOV Methodology.Planned Valve Mods Will Be Implemented During Cycle 11 1998 Outage ML17229A9021998-11-0404 November 1998 LER 98-008-00:on 981008,inadequate Reactor Protection Sys Trip Bypass TS Was Noted.Caused by Poorly Worded Ts. Submitted LAR to Clarify Power Requirements for High Rate of Power Trips.With 981104 Ltr ML17229A8771998-10-14014 October 1998 LER 98-006-00:on 980918,inadvertent Afas Actuation Was Noted.Caused by Degradation of Multiple Afas Power Supplies. Replaced Afas Power Supplies & Revised Procedures.With 981014 Ltr ML17229A8761998-10-14014 October 1998 LER 98-007-00:on 980918,identified Discrepancies Between Fire Protection Design Requirements & Field Conditions. Caused by Inadequate Translation & Implementation of Fire Protection Requirements.Procedures Revised.With 981014 Ltr ML17229A8511998-09-0202 September 1998 LER 98-005-00:on 980807,discovered That PORV Margins Were Insufficient to Accommodate Addl Conservatism.Caused by Inadequacies in Original Vendor MOV Methodology.Will Implement Planned Valve Actuator mods.W/980902 Ltr ML17229A8201998-07-29029 July 1998 LER 98-007-00:on 980630,inadequate Procedure May Have Resulted in SBO Recovery Complications.Caused by Inadequate Procedures.Attached Caution Tags to Appropriate Control switches.W/980729 Ltr ML17229A7411998-05-28028 May 1998 LER 98-004-00:on 980430,discovered Waste Gas Decay Tank Operation W/O Available Oxygen Analyzers,Which Is Prohibited by Ts.Caused by Inadequate Licensee Review of License Amend. Oxygen Analyzer recalibrated.W/980528 Ltr ML17229A7381998-05-21021 May 1998 LER 98-006-00:on 980421,missed EDG Fuel Oil Sample Surveillance Was Noted.Caused by Personnel Error.Revised Fuel Oil Sampling Service Purchase Order & Revised Site procedure.W/980521 Ltr ML17229A7011998-04-27027 April 1998 LER 98-003-00:on 980326,discovered Containment Pressure Instrumentation Design Single Failure Vulnerability.Caused by Inadequate Design by Personnel Error.Removed RPS & ESFAS Containment Pressure Bypass Keys immediately.W/980427 Ltr ML17229A6761998-04-0202 April 1998 LER 98-005-00:on 980305,identified Two Conditions That Were Outside App R Design Bases.Caused by Design Oversight During Development of Original App R Safe SD Design.Established 30 Minute Roving Fire Watches & Provided training.W/980402 Ltr ML17229A6731998-03-26026 March 1998 LER 98-002-00:on 980224,radiation Monitor Surveillance Inadequacies Led to Operating of Facility Prohibited by Tss. Caused by Congnitive Personnel Error.Permanent Procedure Changes Were implemented.W/980326 Ltr ML17229A6551998-03-0505 March 1998 LER 98-001-00:on 980206,high/low Pressure Shutdown Cooling Interface Was Noted Outside App R Design Bases.Caused by Personnel Error.Addl Guidance Was Provided to Engineering Dept personnel.W/980305 Ltr ML17229A6281998-02-19019 February 1998 LER 98-004-00:on 980121,emergency Lighting Outside App R Design Bases Occurred.Caused by Congnitive Personnel Error During Translation of App R Section Iii.Procedures Onop 1 & 2 ONP-100.01 Were Issued for Use on 980206.W/980219 Ltr ML17229A6211998-02-0909 February 1998 LER 98-003-00:on 980110,manual Rt Due to DEH Leak at Turbine Test Block Was Noted.Caused by o-ring Extrusion.Shortened Bolts by About 0.125 & Reinstalled at Correct Torque values.W/980209 Ltr ML17229A6191998-02-0404 February 1998 LER 98-002-00:on 980105,CIS Bistable in Bypass Resulted in Condition Prohibited by Tss.Caused by Personnel Error. Radiation Monitor Was Restored to service.W/980204 Ltr ML17229A6161998-02-0303 February 1998 LER 98-001-00:on 980104,inadvertent RPS Actuation Occurred Due to Personnel Error.Caused by Procedural Inadequacies & Inadequate self-checking by Licensed Utility Personnel. Placards Have Been Placed in CRs.W/980203 Ltr ML17229A6051998-01-27027 January 1998 LER 97-010-01:on 971027,inadvertent Core Alteration Prohibited by TSs Were Noted Due to Stuck Cea.Caused by Personnel Error.Cea #24 Was Dislodged & Transferred to Spent Pool for insp.W/980127 Ltr ML17229A5501997-12-0505 December 1997 LER 97-008-00:on 971107,inadequate CR Ventilation Surveillance Resulted in Condition Prohibited by Ts.Caused by non-cognitive Personnel Error.Operating Procedure 2-1900050 Was revised.W/971205 Ltr ML17309A9091997-12-0202 December 1997 LER 97-011-00:on 971102,non-conservative RAS Set Point Resulted in Operation Prohibited by Ts.Caused by Inadequate Set Point & Instrument Loop Scaling Process.Revised ESFAS Functional Tp W/Proper Set point.W/971202 Ltr ML17229A5391997-11-26026 November 1997 LER 97-010-00:on 971027,inadvertant Core Alteration Prohibited by TS Occurred.Caused by CEA Failure to Detach from Ugs.Safety Evaluation Was Performed & Procedural Rev Made to Continue Upper Guide Structure move.W/971126 Ltr ML17229A5151997-11-0707 November 1997 LER 97-007-00:on 971008,inoperable Containment Cooling Fan Resulted in Operation of Facility Outside Design Basis. Caused by non-cognitive Personnel Error.Ccs Operation Was Revised & Issued on 971013.W/971107 Ltr ML17229A4991997-10-17017 October 1997 LER 97-009-00:on 970917,inoperable PORV Block Valve Resulted in Operation Prohibited by Tech Specs Occurred.Caused by Plant GL 89-10 Program Plan to Review Plant Manager Action Item Sys.Porv Block Valve V-1403 restored.W/971017 Ltr ML17309A9011997-08-27027 August 1997 LER 97-008-00:on 970728,mechanical Fire Penetrations Were Inoperable & Outside App R Design Bases.Caused by Seal Mfg Not Providing Formal Documentation for Installed Seals. Modified Inoperable Fire penetrations.W/970827 Ltr ML17229A4311997-07-29029 July 1997 LER 97-006-00:on 970630,discovered Inadequate Testing of Engineered Safety Features Subgroup Relays.Caused by Inadequacy in Implementing TS Requirements in Surveillance Procedures.Revised Surveillance procedures.W/970729 Ltr ML17229A4241997-07-25025 July 1997 LER 97-005-00:on 970625,discovered That Hot Shutdown Control Panel Shutdown Cooling Flow indicator,FI-3306 Inoperable. Caused by Weakness in Work Order & Procedure Used to Repair FI-3306.Section Meeting W/I&C Planners held.W/970725 Ltr ML17229A3971997-07-11011 July 1997 LER 97-004-00:on 970611,discovered Incorrect Original Cable Tray Fire Stop Assembly Installation Was Outside App R Design Basis.Caused by Personnel Error.Hourly Fire Watch Patrols Will Be posted.W/970711 Ltr ML17229A3871997-06-19019 June 1997 LER 97-003-00:on 970521,determined Required Post Maint Open Stroke Test for Valve V3245,2B2 SIT Discharge Check Valve, Had Not Been Performed.Caused by Personnel Error.Procedure revised.W/970619 Ltr ML17229A3841997-06-17017 June 1997 LER 97-002-00:on 970518,containment Sump Debris Screen Was Not IAW Design Due to Gaps in Screen Encl.Performed SER to Document Containment Sump Design requirements.W/970617 Ltr ML17229A3751997-06-0202 June 1997 LER 97-006-00:on 970501,operation Was Prohibited by TS Due to Inadequately Tested Degraded Voltage Sys.Revised Unit 1 ESFAS Surveillance Test procedure.W/970602 Ltr ML17229A3611997-05-29029 May 1997 LER 97-007-00:on 970502,reactor Coolant Pump Oil Collection Sys Was Outside App R Design Bases.Identified Leak Sites Were Repaired & Mods to RCP Oil Collection Sys to Capture Any Future Leakage from areas.W/970529 Ltr ML17229A3491997-05-21021 May 1997 LER 97-001-00:on 970423,containment Isolation Actuation Occurred.Caused by Increased Radiation Levels During Removal of Upper Guide Structure.Proper Actuation of Containment Isolation Components Was verified.W/970521 Ltr ML17229A3441997-05-13013 May 1997 LER 97-005-00:on 970419,reactor Was Shutdown Due to Reactor Coolant Pressure Boundary Leakage.Hot Cracking Was Caused by Weld Contamination.Repairs to RCPB Were Completed & 1A SDC Train Was Restored to Svc ML17229A3141997-04-30030 April 1997 LER 97-004-00:on 970402,refueling Machine Was Operating in Manner Prohibited by TS Due to Original Design of Refueling Machine Bypass Feature Conflicting W/Ts Requirements. Eliminated Overload Cut Off Limit bypass.W/970430 Ltr ML17229A2951997-03-31031 March 1997 LER 97-003-00:on 970304,automatic Rt Resulted from Loss of Electrical Power to 1A2 Rc Pump.Rcp Breaker Was Replaced & Pump Was Returned to svc.W/970331 Ltr ML17229A2721997-03-21021 March 1997 LER 97-002-00:on 970221,operation in Excess of Max Rated Thermal Power Occurred Due to Digital Data Processing Sys (Ddps) Calorimetric Error.Verified Acceptable Performance of Ddps Functions & Reviewed Software mods.W/970321 Ltr 1999-07-06
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17241A4891999-10-0707 October 1999 LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr ML17241A4951999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for St Lucie,Units 1 & 2.With 991014 Ltr ML17241A4741999-08-31031 August 1999 Rev 1 to PCM 99016, St Lucie Unit 1,Cycle 16 Colr. ML17241A4591999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for St Lucie,Units 1 & 2.With 990913 Ltr ML17241A4301999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for St Lucie Units 1 & 2.With 990805 Ltr ML17241A4111999-07-16016 July 1999 LER 99-007-00:on 990610,unplanned Cooldown Transient Occurred Due to Personnel Error.Trained & Briefed Personnel & Revised Procedures.With 990716 Ltr ML17241A4031999-07-0606 July 1999 LER 99-006-00:on 990605,sub-critical Reactor Trip Occurred Due to Inadvertent MSIV Opening.Caused by Personnel Error. Provided Operation Supervision Instruction to Operating Crews,Stand Down Meetings & Operator Aids.With 990706 Ltr ML17241A4041999-07-0606 July 1999 LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr ML17241A4091999-06-30030 June 1999 Monthly Operating Repts for June 1999 for St Lucie,Units 1 & 2.With 990712 Ltr ML17241A3941999-06-30030 June 1999 LER 99-004-01:on 990415,as Found Cycle 10 Psv Setpoints Were Outside TS Limits.Caused by Manufacturing Process Defect. All Three Psvs Were Replaced with pre-tested Valves During Cycle 11 Refueling Outage.With 990630 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17241A3551999-06-0404 June 1999 LER 99-002-00:on 990505,both Trains of Safety Injection Actuation Were Blocked During Surveillance.Caused by Procedure Error.Procedure Revised.With 990604 Ltr ML17241A3631999-05-31031 May 1999 Monthly Operating Repts for May 1999 for St Lucie Units 1 & 2.With 990610 Ltr ML17241A3321999-05-17017 May 1999 LER 99-004-00:on 990415,determined That as Found Cycle 10 Psv Setpoints Outside TS Limits.Root Cause Under Investigation.Psvs Replaced with pe-tested Valves During Cycle 11 ML17241A3271999-05-0606 May 1999 LER 99-003-00:on 990406,ECCS Suction Header Leak Resulted in Both ECCS Trains Being Inoperable & Entry Into TS 3.0.3. Caused by Chloride Induced OD Stress Corrosion Cracking of Piping.Made Code Repairs & Coated Piping.With 990506 Ltr ML17241A3331999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for St Lucie,Units 1 & 2.With 990517 Ltr ML17229B0801999-04-0707 April 1999 LER 99-002-00:on 990311,SG ECT Error Caused Operation with Condition Prohibited by Ts.Caused by Deficiencies in Data Analysis Guideline Instructions.Licensee Will Change Data Analysis Guidelines for Lead Analysts.With 990407 Ltr ML17229B0841999-04-0707 April 1999 Rev 2 to PSL-ENG-SEMS-98-102, Engineering Evaluation of ECCS Suction Lines. ML17229B0791999-04-0707 April 1999 LER 99-001-00:on 990309,discovered Inadequate Design & IST SRs for Iodine Removal Sys (Irs).Caused by Original Design Inadequacies & Personnel Error.Naoh Tank Vent Valve V07233 Was Tagged Open.With 990407 Ltr ML17229B0961999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for St Lucie,Units 1 & 2.With 990408 Ltr ML17229B0541999-03-10010 March 1999 LER 99-001-00:on 990211,inadequate TS SRs for SIT & SDC Isolation Valves Were Noted.Caused by Failure to Correctly Implement TS Srs.Submitted LAR to Align Required TS SR with Design Bases Requirements Being Verified.With 990310 Ltr ML17229B0461999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for St Lucie,Units 1 & 2.With 990310 Ltr ML17229B0051999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for St Lucie,Units 1 & 2.With 990211 Ltr ML17229A9901999-01-20020 January 1999 LER 98-009-00:on 981223,noted That Facility Operated Outside of Design Basis.Caused by non-conservative MSLB Analysis Inputs.Will Review SR Component Differences Between Units & Will re-baseline LTOP Analysis.With 990120 Ltr ML17229A9961999-01-14014 January 1999 SG Tube Inservice Insp Special Rept. ML17229A9821999-01-0404 January 1999 LER 98-010-00:on 981207,RCS Boron Sample Frequency Required by Ts,Was Exceeded by Twelve Minutes.Caused by Personnel Error.Equipment Clearance Order Was Lifted to Draw Required Sample & Operations Procedure Was Changed.With 990104 Ltr ML17229A9831998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for St Lucie,Units 1 & 2.With 990111 Ltr ML17229A9611998-12-22022 December 1998 LER 97-002-01:on 981204,containment Sump Debris Screen Was Not IAW Design.Caused by Inadequate C/As for Sump Screen Anamolies.All Identified Sump Screen Deficiencies Were Dispositioned &/Or Repaired.With 981222 Ltr ML17229A9561998-12-15015 December 1998 LER 98-008-00:on 981118,missed TS SG U Tube Insp.Caused by Encoding Errors While Using Remote Positioning Fixtures.All SG Tube Surveyed.With 981215 Ltr ML17241A3581998-12-0909 December 1998 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period of 970526-981209. ML17229A9421998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for St Lucie,Units 1 & 2.With 981215 Ltr ML17229A9301998-11-25025 November 1998 LER 98-005-01:on 980807,discovered That New MOV Methodology Caused Past PORV Block Valve Operability Problem.Caused by Inadequacies in Original Vendor MOV Methodology.Planned Valve Mods Will Be Implemented During Cycle 11 1998 Outage ML17229A9021998-11-0404 November 1998 LER 98-008-00:on 981008,inadequate Reactor Protection Sys Trip Bypass TS Was Noted.Caused by Poorly Worded Ts. Submitted LAR to Clarify Power Requirements for High Rate of Power Trips.With 981104 Ltr ML17241A4931998-11-0101 November 1998 Statement of Account for Period of 981101-990930 for Suntrust Bank,As Trustee for Florida Municipal Power Agency Nuclear Decommissioning Trust (St Lucie Project). ML17229A9051998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for St Lucie,Units 1 & 2.With 981110 Ltr ML17229A8871998-10-19019 October 1998 Part 21 Rept Re Potential Defect in Swagelok Stainless Steel Front Ferrule,Part Number SS-503-1 Which Was Machined with Improper Length.C/A Includes Insp Equipment That Will 100% Identify Short Length ML17229A8781998-10-19019 October 1998 Part 21 Rept Re Potential Defect in Swagelok Stainless Steel Front Ferrule,Part Number SS-503-1,which Was Machined with Improper Length.Insp Equipment That Will 100% Identify Short Length ML17229A8771998-10-14014 October 1998 LER 98-006-00:on 980918,inadvertent Afas Actuation Was Noted.Caused by Degradation of Multiple Afas Power Supplies. Replaced Afas Power Supplies & Revised Procedures.With 981014 Ltr ML17229A8761998-10-14014 October 1998 LER 98-007-00:on 980918,identified Discrepancies Between Fire Protection Design Requirements & Field Conditions. Caused by Inadequate Translation & Implementation of Fire Protection Requirements.Procedures Revised.With 981014 Ltr ML17229A8721998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for St Lucie Units 1 & 2.With 981009 Ltr ML17229A8511998-09-0202 September 1998 LER 98-005-00:on 980807,discovered That PORV Margins Were Insufficient to Accommodate Addl Conservatism.Caused by Inadequacies in Original Vendor MOV Methodology.Will Implement Planned Valve Actuator mods.W/980902 Ltr ML17229A8611998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for St Lucie,Units 1 & 2.With 980911 Ltr ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17229A8481998-08-0707 August 1998 Rev 1 to PSL-ENG-SEFJ-98-013, St Lucie Unit 2,Cycle 10 Colr. ML17229A9461998-08-0707 August 1998 Rev 0 to PCM 98016, St Lucie Unit 2,Cycle 11 Colr. ML17229A8301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for St Lucie,Units 1 & 2.W/980814 Ltr ML17229A8201998-07-29029 July 1998 LER 98-007-00:on 980630,inadequate Procedure May Have Resulted in SBO Recovery Complications.Caused by Inadequate Procedures.Attached Caution Tags to Appropriate Control switches.W/980729 Ltr ML17229A7981998-06-30030 June 1998 Monthly Operating Repts for June 1998 for St Lucie,Units 1 & 2.W/980713 Ltr ML17229A7701998-05-31031 May 1998 Monthly Operating Repts for May 1998 for St Lucie,Units 1 & 2.W/980612 Ltr ML17229A7411998-05-28028 May 1998 LER 98-004-00:on 980430,discovered Waste Gas Decay Tank Operation W/O Available Oxygen Analyzers,Which Is Prohibited by Ts.Caused by Inadequate Licensee Review of License Amend. Oxygen Analyzer recalibrated.W/980528 Ltr 1999-09-30
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ACCEIERDDOCUMENTDISIBVTIONSYSTEMREGULRYINFORMATION DISTRIBUT SYSTEM(RIDS)ACCESSION NBR:9302110293 DOC.DATE:
93/02/05NOTARIZED:
NOFACIL:50-389 St.LuciePlant,Unit2,FloridaPower&LightCo.AUTH.NAMEAUTHORAFFILIATION HURCHALLA,J.A.
FloridaPowerELightCo.SAGER,D.A.
-FloridaPower6LightCo.RECIP.NAME RECIPIENT AFFILIATION DOCKET05000389
SUBJECT:
LER93-001-00:on 930108,chemistry technician failedtosamplethirdSItank6samplingofSItank2A1notperformed withinTSrequiredintervalafterfillingtank.Causedbypersonnel error.Personnel counseled.W/930205 ltr.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:LTR gENCLgSIZE:TITLE:50.73/50.9 LicenseeEventReport(LER)-,IncidentRpt,etc.NOTES:RECiPIENT IDCODE/NAME PD2-2LANORRIS,JINTERNAL:
ACNWAEOD/DOA.
AEOD/ROAB/DSP NRR/DLPQ/LHFB10 NRR/DOEA/OEAB NRR/DST/SELB 8DNR~SPLB8DlREGFILE02GN2~LE01EXTERNAL:
EGErGBRYCE,J.H NRCPDRNSICPOORE,W.COPIESLTTRENCL1111221122111111111111221111RECIPIENT IDCODE/NAME PD2-2PDACRSAEOD/DSP/TPAB NRR/DET/EMEB 7ENRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB8H3 NRR/DST/SRXB 8ERES/DSIR/EIB LSTLOBBYWARDNSICMURPHY,G.A NUDOCSFULLTXTCOPIESLTTRENCL1-12211111122111111111111RNOTETOALL"RIDS"RECIPIENTS:
PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2065)
TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!LSFULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:
LTTR31ENCL31 P.O.Box128,Ft.Pierce,FL3o954-0128 February5,1993L-'93-3010CFR50.73U.S.NuclearRegulatory Commission Attn:DocumentControlDeskWashington, D.C.20555Re:St.LucieUnit2DocketNo.50-389Reportable Event:93-001DateofEvent:January8,1993MissedSurveillance forSafetyInectionTankSamlinDuetoPersonnel ErrorTheattachedLicenseeEventReportisbeingsubmitted pursuanttotherequirements of10CFR50.73toprovidenotification ofthesubjectevent.Verytrulyyours,D.A.SVicePSt.LugersidentePlantDAS/JWH/kw Attachment cc:StewartD.Ebneter,RegionalAdministrator, USNRCRegionII.SeniorResident, Inspector, USNRC,St.LuciePlantDAS/PSLN857-933.000429302110293 930205PDRADOCK050003B98PDRanFPLGroupcompany~/gJI FPLFscsirriis oiNRCFormS68(e.es)VS.NLCLEARREGULATORY COMMISSION LICENSEEEVENTREPORT(LER)APPITCYT0CNSISA$150010lEXP'.l1500tESTNEEDNATCEN005PESPONSEToCOWLYWITHTHEPPOISAATION COLLECTONINOLEST150 ll550$,TONWAAOCONMENTSPECAIEANO 55505tH5STNAATETOTIEPECOPOSANC INPCTTTSIIANAOENENT TTLFNCH(P~LLS, IACLENLINQAATOIY CONLPSSCFL WANANCTCN.
CCt05NLAIOTOTHEPAPENFICFIA FETACTCNPNCVECTOl50010PACF5IcEoFNANAEELENTNoNAxft.wASFNIOTIPL oct05NLFACILITYNAME(1)DOCKETNUMBER(2)St.LucieUnit2A050003891 03T'TLE{)MissedSurveillance forSafetyInjection TankSamplingDuetoPersonnel ErrorEVENTDATE(5)LERNUMBER(6)REPORTDATE(7)OTHERFACILITIES INVOLVED(8)01DAY08YEAR93YEAR93,.'IAL001gR0002DAYYEAR0593FACILITYNAMESN/AN/ADOCKETNUMBER(S) 050005000OPERATING MODE(9)POWERLEVEL(10)100;Cgjlr20.402(b) 20.405(a)(1)(i) 20.405(c) 50.36(c)(1) 20A05(a)(1)(II) 50.36(c)(2) 20.405(a)(1)(iii) 20.405(a)(1)(iv) 20.405(a)(1)(v) 50.73(a)(2)(I)50.73(a)(2)(ii) 50.73(a)(2)
(iii)LICENSEECONTACTFORTHISLER1250.73(a)(2)(iv) 50.73(a){2){v) 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(x)
THISREPORTISSUBMITTED PURSUANTTOTHEREQUIREMENTS OF10CFR:Checkoneormoreofthefollowin, (11)73.71(b)73;71{c)OTHER(SpecifyinAbstractbelowandinTextNRCForm366A)NAMEJamesA.Hurchalla, ShiftTechnical AdvisorTELEPONENUMBERAREACODE407465-3550COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT13CAUSESYSTEMCOMPONENT REPORTABLE TONPRDSSYSTEMCOMPONENT MANUFACREPORTABLE TURERTONPRDSSUPPLEMENTAL REPORTEXPECTED14YES(Ifyes,completeEXPECTEDSUBMISSION DATE)XNOIIIEXPECTEDMONTHDAYYEARSUBMISSION DATE(15)ABSTRACT'(Limitto1400spaces.i.e.
approximately fifteensingle-space typewritten lines)(16)OnJanuary8,at0500aReactorControlOperator(RCO)filledthe2A1,2A2,and2B2Safetytnjection Tanks'SITs) andsubsequently notifiedChemistry.
AChemistry technician samptedtwooftheSITspertherequiredsurveillance butfaitedtosamplethethird.OnJanuary8,1993,at2300theUnit2Assistant NuclearPlantSupervisor discovered thatthesamplingofthe2A1SafetyInjection Tankhadnotbeenperformed byChemistry withintherequiredtimeintervalatterfillingthetank.Using,the25%maximumallowable extension permitted by.Technical Specification (TS)4.0.2,thelatesttimeatwhichthesamplingcouldhavebeenperformed ontimewasJanuary8,at1230.Therootcauseoftheeventwaspersonnel errorbyaChemistry technician responsible forthesampling.
WheninformedbyOperations thatspecificSITshavebeenfilleditistheresponsibility oftheChemistry department personnel onshifttosampletheseSITsfortherequiredboronconcentration perTS4.5.1.1.b.
Inaddition, therewasafailureonthepartofthecontrolroompersonnel torealizethatoneofthethreefilledSITshadnotbeensampledwhenChemistry notifiedthemthattwoSITswerewithinspecification.
Corrective actionswere;1)Performthe2A1SITsutveiltance.
2)CreateastatusboardbywhichChemistry caninsurethattheappropriate SITshavebeensampled.3)TheChemistry personnel involvedwerecounselled.
4)Operations personnel havebeencounselled.
5)AHumanPerformance Evaluation Systemevaluation wassubsequently conducted whosefindingsagreewiththisreport.FPLFacsimile ofNRCForm366(6-89)
PPLPSCSIITTle OtNRCFOTm&OSl689)U.S.NUCLEARREGULATORY COMMISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATlON
'APPROITOCAAT KLSITCSIPA lsplpaaACGITTSTPAATTOIMICTNPTRRTSPONSl TOOOINTTWITH TIPSPPOISAAOCNCOIlf CTONRTOUTSTIISAIPTSIORNNOCCANRNT0RTGARTNIC TAPSXNTSTINATlTOPICRTCORCSAICIISPORTSNANAGTASNTSRANCHTP000AU0,IAICI0AITRlOIAATORYOAA+CSSN70 WANTNCTON,OCT000S NAPTOTIRPAPTRWOPNRTOVCTIONPRORCTI'TIICCISPAOIIICC OPNANAKNTNTAM)TANCTT.WANSNCTOIAOCPPNOFACILITYNAME(1)St.LucieUnit2DOCKETNUMBER(2)YEAREQUENTIAL NUMBER."T',."REVISIONvlNUMBERLERNUMBER(6)PAGE(3)05000389TEXT(Ifmorespaceisreqoired, tjseadditional NRCForm366A's)(17)9300000203Operations fillsSafetyInjection Tanks(SIT)(EIIS:
BP)asnecessary tomaintaintherequiredTechnical Specification (TS)level.Subsequently theseSITsmustbesampledinaccordance with-Chemistry Operating Procedure 2-C-60within6hourstoensurethattherequiredTSboronconcentration hasbeenmaintained.
OnJanuary8,1993,at0500aReactorControlOperator(RCO)filledthe2A1,2A2,and2B2SITs.At0530henotifiedtheonshiftChemistry technician.
TheChemistry technician whoreceivedthecallturnedthesamplingresponsibility overtoanoncomingtechnician onthenextshift.Thistechnician receivedtheappropriate verbalinstructions ofwhichSITstocheckbutonlysampledthe2A2and2B2SITs.At0830henotifiedthecontrolroomthattheseSITsweresatisfactory wilhrespecttoboronconcentration.
Operations personnel receivedthecallandfailedtonoticethatoneoftheSITshadnotbeensampled.At2314theoncomingAssistant NuclearPlantSupervisor wasreviewing theRCOchronological loganddiscovered the2A1SIThadnotbeensampled.TheSITwasadministratively declaredoutofserviceandChemistry wasnotifiedtosampleit.Thesampleshowedsatisfactory boronconcentration andthe2A1SITwasdeclaredbackinserviceat2345.VTherootcauseoftheeventiscognitive personnel errorbyautilityChemistry technician byfailingtoensurethesamplingoftheappropriate SITs.Acontributing factoristhattherewasnomethodotherthanverbalrequestturnoverbetweenChemistry technicians toinsurethatthecorrectSITsaresampled.Thisplacesthefullresponsibility forthecorrectness andtimeliness ofthisTSsurveillance onverbalcommunication withnorecordedinformation fortheChemistry technician toreference.
Inaddition, therewasafailureonthepartofcontrolroompersonnel torealizethatoneofthethreeSITshadnotbeensampledwhenChemistry notifiedthemthattwoSITswerewithinspecification.
Therewerenounusualcharacteristics oftheworklocationwhichcontributed tothisevent.TVThiseventisreportable under10CFR50.73.a.2.i.b, asamissedsurveillance requiredbyTechnical Specifications.
Technical Specification 4.5.1.1.b statesthateachSafetyInjection Tankshallbedemonstrated operablewithin6hoursaftereachsolutionvolumeincreasegreaterthanorequalto1%oftankvolumebyverifying theboronconcentration ofthesolution.
Thepurposeofthissamplingistoprovideassurance thattheboronconcentration oftheSITshasnotbeenchangedtoavalue-outsidethebandoftheTechnical Specification requirements.
Thisassuresthattheassumptions usedfortheSITsintheFinalUpdatedSafetyAnalysisReport(FUSAR)arevalid.Thesurveillance ofthe2A1SITwascompleted at2340,or12hoursand40minutespasttherequiredTechnical Specification sampletime.FPLFacsimile ofNRCForm366(6-89)
FPLFacsimrootrNRCForm666(669t.U.S.NUCLEARREGULATORY COMMISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATlON APPAOVTOCallNCI 0ll00IOI000TIES.0000000TAAATTO nvexNPTfrfE0PONTE ToCOAWlvvATN TI0000aNAAOONCcuTCTEPI IEOIE00I0000000fCTIWATErCCANENT0IECANONCTAPCTN00TINATKToOETECOII0AlafEPTNTCNANACTAENTCPlANCNIP0000ua IAcTTArlTEaAATONT~
WASHNCTON,OC00000APATToTIE0APTfrWONATECOCTIONPNOEC'0fll000IOl00ÃfICTOfNANACTIENT AIOTANCET.WACIIAOT000 OC00NO.FACILITYNAME{1)St.LUCieUnit2DOCKETNUMBER(2)YEARLERNUMBER{6)EQUENTIAL NUMBERREVISIONNUMBERPAGE(3)0500038993TEXT(Ifmorespaceisrequired, useadditional NRCForm366A's)(17)0010003003Theresultsofthechemistry sampleshowedtheboronconcentration tobewithinTechnical Specification 3.5.1.c.The2A1SafetyInjection Tankwascapableofperforming itsintendedsafetyfunctionassetforthintheassumptions oftheFUSAR,sections6.3.2.2.1 and6.3.3.4.3.f.
TI;erefore, lhehealthandsafetyofthepublicwasnotaffectedbythisevent.1)The2A1SafetyInjection Tank(SIT)Chemistry Surveillance wasperformed withsatisfactory resultsJanuary8,1993at2340hours.2)TheChemistry department nowusesastatusboardtotrackregulatory requiredsurveillances thatarenotperiodically scheduled..
3)Thepersonnel involvedinthiseventhavebeencounselled bytheChemistry supervisor ontheimportance ofmeetingsurveillance requirements.
-4)TheOperations supervisor hasissuedaNightOrderonthiseventwhichemphasizes theneedforoperators totracksurveillances suchastheonedescribed intheLERviatheoperatorturnoversheet,andtheneedfortheoncomingcrewstocarefully reviewthechronological log.5)AHumanPerformance Enhancement System(HPES)evaluation wasperformed.
Theresultsagreewiththeconclusions ofthisLicenseeEventReport.ITINAFnnFilTherewerenocomponent failuresinvolvedinthisevent.VIAprevioussimilareventisdescribed inLER389-89-008, whichdescribes amissedsurveillance forSafetyInjection LoopHeadervalvesfollowing thefillingoftwoSITs.FPLFacsimile ofNRCForm366(6.89)