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| {{#Wiki_filter:ACCELEBRATED91S'JUUBUTIONDEMONS~TJONSY~gMREGULATINFORMATIONDISTRIBUTIOIYSTEM(RIDE))",ACCESSIONNBR:8807060119DOC.DATE:88/06/24NOTARIZED:NODOCKETFACZL:50-316DonaldC.CookNuclearPowerPlant,Unit2,Indiana&05000316AUTH.NAMEAUTHORAFFILIATIONPOSTLEWAZT,T.K.IndianaMichiganPowerCo.SMITH,W.G.IndianaMichiganPoweCo.RECIP.NAMERECIPIENTAFFILIATION | | {{#Wiki_filter:ACCELEBRATED 91S'JUUBUTION DEMONS~TJON SY~gMREGULATINFORMATION DISTRIBUTIOIYSTEM (RIDE))",ACCESSION NBR:8807060119 DOC.DATE: |
| | 88/06/24NOTARIZED: |
| | NODOCKETFACZL:50-316 DonaldC.CookNuclearPowerPlant,Unit2,Indiana&05000316AUTH.NAMEAUTHORAFFILIATION POSTLEWAZT,T.K. |
| | IndianaMichiganPowerCo.SMITH,W.G. |
| | IndianaMichiganPoweCo.RECIP.NAME RECIPIENT AFFILIATION |
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER86-023-02:on860715,erroneousaccumulatorlevelindicationresultinginlowaccumulatorvolume.W/8DISTRIBUTIONCODE:ZE22DCOPIESRECEIVED:LTRtENCL/SIZE:TITLE:50.73LicenseeEventReport(LER),IncidentRpt,etc.NOTES:RRECIPIENTZDCODE/NAMEPD3-1LASTANGFJINTERNAL:ACRSMICHELSONAEOD/DOAAEOD/DSP/ROABARM/DCTS/DABNRR/DEST/ADS7ENRR/DEST/ESB8DNRR/DEST/MEB9HNRR/DEST/PSB8DNRR/DEST/SGB8DNRR/DLPQ/QAB10NRR/DREP/RAB10DR<IB9ARES/DE/EIBRGN3FILE01EXTERNALEGSrGWILLIAMSFSHSTLOBBYWARDNRCPDRNSICMAYSFGCOPIESLTTRENCL111111112211101111111111111111111144111111RECIPIENTIDCODE/NAMEPD3-1PDACRSMOELLERAEOD/DSP/NASAEOD/DSP/TPABDEDRONRR/DEST/CEB8HNRR/DEST/ICSB7NRR/DEST/MTB9HNRR/DEST/RSB8ENRR/DLPQ/HFB10NRR/DOEA/EAB11NRR/DREP/RPB10NUDOCS-ABSTRACTRESTELFORD,JRES/DRPSDEPYFORDBLDGHOYFALPDRNSICHARRZSFJCOPIESLTTRENCL11221111'1111111111111122111111111111hDhTOTALNUMBEROFCOPIESREQUIRED:LTTR45ENCL44 NRCForm355(9.83)LICENSEEEVENTREPORTILER)U.S.NUCLEARREOULATOAYCOMMISSIONAPPAOVEOOMBNO,31504101EXPIRES:8/31/88FACILITYNAME(I)D.C.CookNuclearPlant-Unit2DOCKETNUMBER(2)PAE3)o5ooo316>OF07TITLE(IlErroneousAccumulatorLevelIndicationResultinginLowAccumulatorVolumeMONTHDAYYEAREVENTDATE(5)LERNUMBER(5)YEARÃ~'.SEQVSNtIALPr~REVOKENVM888X5IIVM88RREPORTDATE(7)MONTHOAYYEARFACILITYNAMESDOCKETNUMBER(SI05000OTHERFACILITIESINVOLVED(8)071586860230206248805000OPERATINOMODE(8)POWERLEVELTHISREPORTISSUBMITTEDPURSUANTT50.73(e)(2)(ivl50.73(e)12)(vl50.nN)(2)(vB)50.n(el(2)(vBII(A)50,73(el(2)(v)5)(BI9),73(~)(2)(el20A05(c)50.38(cl(1)50.38(c)(2)50,73(eIl2)0)5073(el(2)(EI50.73(e)(2)(51120.802(8)20405(~)(1)(l)20A05(el(I)(8)20A05(e)(1)(BII20A05(el(1)(tvl20A05(~)(I)(vlLICENSEECONTACTFORTHISLER(12)0THEREOUIREMENTSOF10CFR()I(CheckoneormoriOfthefollovffnfl(Ill73.7)(8)73.71(c)OTHERfSpeclfyInAhttrectOelowendInFeet,NRCForm3BBAINAMET.K.Postlewait-TechnicalEnineerinSuerintendentTELEPHONENUMBERAREACODE616465-5901COMPLETEONELINEFOREACHCOMPONENTFAILUREDESCRIBEDINTHISREPORT(13)CAUSESYSTEMCOMPONENTMANUFACTUREREP0RTA8L~',It~IIiCAUSESYSTEMCOMPONENTMANUFAC.TURERTONPROSXXBPECBDBPTDI204I204@~IXBPPITI204SUPPLEMENTALAEPOATEXPECTED(lelEXPECTEDSU5MlSSIONDATE(15)MONTHOAYYEARYESf/fyet,completeEXPECTEDSUBMISSIOND4FE)NOABBTRAcT(Llmlttote00tpecet,I.e.,eppronlmetelyfifteentlncleepecetypewrittenllnnl08)ThisrevisionisbeingsubmittedtoincludetheresultsofdiagnostictestingperformedduringtheSeptember1987outage.BetweenJuly15and18,1986,problemswereencounteredwiththeprocessinstrumentationmonitoringthevolumewithinaccumulator)jj'2.Complicationsdevelopedduringultrasonictesting(UT)conductedtoverifyaccumulatoroperabilitywhichresultedinthefailuretoidentifyaviolationoftheactionstatementassociatedwithlowaccumulatorvolumeandamissedsurveillanceforboronconcentration.TheadministrativeproblemsassociatedwithaccumulatorlevelverificationbyUTwerecorrected.andthismethodwasusedinlieuoftheprocessinstrumentationtoverifyaccumulatoroperabilityuntilunitshutdownforanoutageMarch3,1987.TestingperformedduringtheMarch1987outage,determinedthatthreeinstrumentcomponentsweredefective;allwerereplacedinkind.OnApril26,1987ILA<<121begantodriftupwards.OnApril30,1987,asaprecautionarymeasure,ILA-121wasdeclaredinoperable.AccumulatorlevelwasmonitoredusingUTuntilunitshutdownonAugust27,1987.TestingperformedduringtheSeptember1987outagedeterminedthatoneinstrumentcomponentwasdefective.Thecomponentwasreplacedinkindandtheprocessinstrumentationhassubsequentlyfunctionednormally.NRCForm388(Be)3I8807060}}9880624PDRADOCK050003}6SPNU$6ZZ NRCForm3BBA(943(LICENSEENTREPORT(LER)TEXTCONTINUANU.S.NUCLEARREGULATORYCOMMISSIONAPPROVEDOMBNO,3I50-0104EXPIRES:8/3'I/88FACILITYNAME(I(DOCKETNUMBER(2)LERNUMBER(8(PAGE(3iD.C.CookNuclearPlant-Unit2TE/ET/~RRE>><<~,~~//RCr3SBA<</(mYEARosooo31686SEOUENTIALNUMBER023REVISIONNUMBER0202QF07ThisrevisionisbeingsubmittedtoincludetheresultsofdiagnostictestingperformedduringtheSeptember1987outage.ConditionsPriortoOccurrenceUnit2inMode1,RTPat48percent(91330hourson7-15-86)DescritionofEventTechnicalSpecification3.5.lbrequiresthateachaccumulator(EIIS/BP-TK)mustmaintainbetween929and971cubicfeetofboratedwaterwhiletheunitisinModes1-3(PowerOperation,Startup,andHotStandby,respectively).Iftheaccumulatorvolumedeviatesfromtheprescribedlimits,thevolumemustberestoredwithin1hourortheunitmustbeinhotshutdown(Mode4)withinthenext12hours.Processinstrumentationmonitoringaccumulatorinventory(EIIS/BP-LIT)displayswatervolumeincubicfeet.Thesystemiscomprisedof2indicatorsforeachaccumulator,onewiderange(300-1000cubicfeet)andonenarrowrange(900-1000cubicfeet).OnJuly15,1986,operatorsonshiftbecamesuspectoftheaccumulator82volumeindicationandrequestedanultrasonictest(UT)beperformedtoverifywaterinventory.QualityControlpersonnellocatedthewaterlevelusingultrasoundandthenmarked/datedthetankaccordingly;however,duringthisprocesstheirdatasheetbecamecontaminatedandwasdiscardedbeforeleavingaccesscontrol.AnewdatasheetwassubsequentlyfilledoutfrommemoryandtheControlRoomwasinformedat1330hoursonJuly15thataccumulator(/(2wasat115.75inches.Whenmathematicallyconvertedtovolume,thislevelcorrespondsto969.58cubicfeet;which,bycoincidenceonly,happenedtocloselyagreewiththeprocessinstrumentationindicationatthattime.OnJuly18,1986,at0800hoursanotherUTwasrequestedforaccumulator/!2becauseofquestionablevolumeindication.WhenQCarrivedataccumulator(/'2theydiscovereda10incherrorwasmadeintheJuly15report.Thelevelwasactually105.75inches(909.58cubicfeet)onJuly15,andnot115.75(969.58cubicfeet)asreported.Itcanthereforebededucedthatthelowerlimitforcontinuedoperation(929cubicfeet)hadbeenviolatedsinceatleastJuly15withouttheappropriatecompensatoryactionsbeingtaken.NRCFORMSBBA(EBSI*U.S.GPO:(BBB0824538/455 NRCForm366A(84)3)LICENSEENTREPORT(LER)TEXTCONTINUANV.S.NUCLEARREGULATORYCOMMISSIONAPPROVEOOMBNO.3(50-0104EXPIRES:8/31/88FACILITYNAMEl()D.C.CookNuclearPlant-Unit2OOCKETNUMBER(2)31686LFRNUMBER(6)SEQUENTIALNUMBER023REVISIONNUMBER020PAGE(3)OFTUCT(lmrsoEpsos/4rBEM)BI(,BBB///orrr/HRC/ronn36543)l17)DescritionofEvent(cont'd)ThiserrorwascompoundedduringcommunicationsbetweenQualityControlandOperationsfollowingtheUTperformedthemorningofJuly18.At0945hoursonthatmorning,QualityControlreportedthelevelofaccumulatorf32hadrisen3inchessincethelasttestperformedonJuly15.Operationswasnotmadeawareofthe10incherrordiscoveredearlier.Consequently,actingundertheimpressionthataccumulator((I2hadrisenfrom115.75inches(969.58cubicfeet)toavolumeexceedingtheupperlimitingconditionforcontinuedoperation,'perationspersonneldeclaredaccumulator82inoperablebaseduponhighlevel(itwasactuallylow)andmeasuresweretakentobegindrainingthetank.WithrespecttothevolumeincreasewhichoccurredsometimebetweenJuly15andJuly18,noconclusiveevidencecanbeproducedconfirmingthatsaidincreaseactuallyhappenedwithinasixhourtimespanprecedingboronsamplingperformedat0925hoursonJuly18.Therefore,theplantmustassumetheboronconcentrationwasnotverifiedfollowingasolutionincrease>/1percentoftankvolumeasrequiredbyTechnicalSpecification4.5.1b.Itshouldbenotedthatat0952hoursonJuly18,whilepreparationswereunderwayfordrainingaccumulator82,Unit2trippedonasteamgeneratorlevelhigh-highsignalthusplacingtheunitinMode3.Thiseventwasfurthercomplicatedat1447hoursonJuly18whentheControlRoomwasinformedthatUTresultsplaced82accumulator'slevel3inchesbelowthelastmeasurementtakenearlierthatmorning(duetodraining).Withthisinformation,andstillunawareofthe10incherrormadeonJuly15,Operationsdeclaredtheaccumulatoroperablebecausetheybelievedtheapparentlyhighvolumeofwaterhadbeenreducedtowithinacceptablelimitsforcontinuedoperation.Inreality,theaccumulatorvolumewasdraineddownfromanalreadytoolowconditiontoanevenlowerstatus.At1620hoursonJuly18,Operationsbecamecognizantofthe10incherrormadeonJuly15.Itwasrecognizedatthistimethataccumulator$!2was,andhadbeensinceatleast1330hoursonJuly15,inviolationofthelowervolumelimitrequiredbyTechnicalSpecification3.5.1b.Accumulator/f2wasimmediatelydeclaredinoperable.Coolingofthereactorcoolantsystem(EIIS/BP-AB)toachieveMode4beganat1720hoursandtheNRCwasnotifiedoftheeventbyphoneat1808hours.Effortstowardsfillingaccumulatorf/2viatherefuelingwaterstoragetank(EIIS/BP-TK)commencedat1839hoursandtheeventwasterminatedat2120hoursonJuly18whentheaccumulatorvolumeandboronconcentrationwereverifiedtobewithinthelimitingconditionforoperationasdescribedinTechnicalSpecification3.5.1band3.5.1crespectively.CooldownwashaltedpriortoreachingMode4.Withtheexceptionoftheloop2accumulatorvolumeinstrumentation,therewerenoinoperablestructures,systems,orcomponentsatthestartofthiseventwhichcouldhavecontributedtoitsoccurrence.NRCFORM366A(()4)3)oU,S.GPO.19880824538/455 0<iII NRCForm388A(943)LICENSEENTREPORT(LER)TEXTCONTINUA~NU.S.NUCLEARREGULATORYCOMMISSIONAPPROVEDOMSNO3150-0104EXPIRES8/31/88FACILITYNAME(11DOCKETNUMBER(2)LERNUMBER(BlPAGE(3)D.C.CookNuclearFlant-Unit27%XT/4/m<<oNMoo/sIFEo8or/,IrsoI/8/ooo/HRCR<<m35843/(17)osooo316YEAR@IrI86SEQUENTIALNUMBER8rV023IIEVISIONNUMSER0204OF07CauseofEventThecauseofthiseventhasbeenattributedtotheinabilityoftheprocessinstrumentationtoaccuratelyreflectthevolumewithinaccumulator82,whichresultedintheneedforultrasonictestingtoverifyaccumulatoroperability.Threedefectivecomponentswithinthesystemwerediagnosedastherootcausefortheinstrumentationfailure.theinstrumentationconsistsofacircuitboard(EIIS/BP-ECBD),straingauge(EIIS/BP-TD),potentiometerspan(EIIS/BP-EC),potentiometerzero(EIIS/BP-EC)andanarrowrangedifferentialpressureunit(DPU)(EIIS/BP-PIT).Theinitialinvestigationindicatedthatthe"zero"wasdrifting,whichresultsfromafaultycircuitboardandstraingauge.Subsequently,thesecomponentswerereplaced.Theinstrumentationsubsequentlyzeroedproperly,butdatawasnotrepeatablevhenrangedupandbackdownthemeasurementscale.Asaresult,theDPUnarrowrangewasreplacedwhicheliminatedtherepeatabilityproblem.Later,'hespanandzeropotentiometersverereplacedtoensureproperinstrumentationoperation.ThecalibratedinstrumentwasreturnedtoserviceonApril2,1987,andfunctionednormallyuntilApril26,atwhichtimethesystembegantoexhibitsignsofdriftingupwards.UltrasonicmeasurementstakenafterApril26confirmedtheactualvolumewithinaccumulatorf/2wassteadyandwellwithintheTechnicalSpecificationallowablerange,however,theresultsalsoconfirmedthatILA-121wascontinuingaslowbutsteadyupwarddrifttowardstheadministrativelimitforoperability.Asaprecautionarymeasure,ILA-121wasdeclaredinoperableat1328hoursonApril30,1987.FurtherinvestigationconductedduringtheSeptember1987outageindicatedthattherootcauseofthesecondinstrumentfailurewasafaultyDPUnarrowrange.TheDPUnarrowrangewasreplacedandthecalibratedinstrumentwasreturnedtoserviceonSeptember24,1987.Theinstrumenthassubsequentlyfunctionednormally.ContributingtothiseventwasthefactthatQualityControlpersonnelwhoperformedtheoriginalUTonJuly15didnotimplementsoundworkpracticeswhileconductingactivitiesinaradioactiveenvironment.Thisresultedinthelossofhard.copydatasupportingtestresultsforcingthoseinvolvedtorelysolelyuponmemoryrecall.ItshouldbenotedthattheUTwasperformedwithin-anextremelyharshenvironmentconsistingofelevatedtemperatureandairborneradioactivity.Theseadverseconditionscomplicatedeffortsofthetestcrewbecausefullfacemaskwasrequiredandthefatigueprocesswasaccelerated.InadequatecommunicationbetweentheControlRoomandQualityControlpersonnelfurthercomplicatedthisevent.NoformalmechanismhadbeenestablishedtoverifythatoperatorsonshifthadacompleteandaccurateunderstandingoftheUTresults.NRCFORMSBBA(948)*U.S.GPO:)988%.824538/455 NRCForm366A(94)3)LICENSEENTREPORT(LER)TEXTCONTINUNU.S.NUCLEARREGULATORYCOMMISSIONAPPROVEDOMBNO.3(9)&104EXPIRES:8/31/88FACILITYNAME(llDOCKETNUMBER(2)LERNUMBER(6)PAGE(3)D.C.CookNuclearPlant-Unit2TEXT/kmcY8<<>>48lrnr/I/EerEI/88T/I/or>>/HRC%%dnn35549/(17)YEAR3168602302(jar,SEGVENTIALjZ':REVISION49NUM88Rv>errNUMSER05OF07AnalsisofEventThiseventisreportableunderthecriteriaof10CFR50.73(a)(2)(i)asdescribedbelow.-Forapproximately3dayspriortoJuly18,1986,thevolumeofaccumulator82wasbelowitslowerlimitingconditionforoperationandthecorrespondingactionstatementassociatedwithTechnicalSpecification3.5.1bwasnotsatisfied.-BetweenJuly15andJuly18,1986,accumulator82experiencedasolutionincreasegreater>/m1percentofthetankvolumeandtheboronconcentrationwasnotverifiedtobeacceptablewithinthenext6hoursasrequiredbyTechnicalSpecification4.5.1b.Thesafetysignificanceofpoweroperationwithaccumulatorvolumeofoneaccumulatorat909.6cubicfeetratherthan929cubicfeetislimitedtoimpactontheloss-of-coolantaccidentanalysis.Thelimitingloss-of-coolantaccidentanalysisforUnit2Cycle6predictsapeakcladtemperatureof2079degreeFwitha121degreeFmargintothe2200degreeFlimitspecifiedin10CFR50.46.ExxonNuclearCompany,thefuelvendorforCycle6,wasrequestedtoevaluatetheimpactofthiseventonpublichealthandsafety.Theirresponsestated:itisExxon'sopinionthatasignificantsafetyhazardtothepublicdidnotexistforthefollowingreason.Thelimitingcaseinthereferenceindicatedapeakcladdingtemperature(PCT)of2079degreeFforoperationatlOOXpower.Operationat90percentpowerwouldresultinareductioninthePCTandwouldtendtooffsetanyincreaseinPCTduetothereducedaccumulatorliquidvolume.ThereducedaccumulatorliquidvolumealoneisexpectedtohaveaverysmalleffectonthePCT.Theaccumulatorflowwouldendapproximately1secondsoonerthanthetimeindicatedinthereference.Sincethisoccursafterthebeginningofcorerecoverytime(BOCREC)whenthedowncomerisfull,averysmalladverseeffectonrefloodrateandPCTwouldoccurandwouldbemuchlessthanthe121degreeFmarginindicatedinthereference."Itisofnotethatthedifferencebetweentheas-foundcondition(909.6cubicfeet)andthevaluespecifiedintheTechnicalSpecificationof929cubicfeetis19.4cubicfeet,orapproximately960lbs.ofwater.Inordertoconservativelyevaluatetheeffectonpeakcladtemperature,ahypotheticalscenariowasevaluatedinwhichitwasassumedthatthiswaterwasdeficientduringtherefillperiod,andhadtobemadeupbypumpedin5ectionwater.Itwouldhavetakenthepumpsapproximately1.1secondstomakeupthiswater.SincethePCTrateofheatupduringtheearlyreflood/refillperiodisabout13degree/sec.,thiswouldhaveresultedinaPCTincreaseofabout15degreeF.Adding15degreeFtothecalculatedPCTresultsinanewPCTof2094degreeF,whichisstillwellwithinthelimitsof10CFR50.46.NRCFORMSStA(94)3)8U.S.GPO:1986.0.624538/455 NRCForm388A(943)L'ICENSEENTREPORT(LER)TEXTCONTINUANU.S.NUCLEARREGULATORYCOMMISSIONAPPROVEDOMSNO.3150M)84EXPIRES:8/31/88FACILITYNAME{1)DOCKETNUMBER(2)LERNUMBER(8)PACE(3)D.C.CookNuclearPlant-Unit2TEXT/Smroodraco/rorR/)or/,I/44/8/orro/NRCFarm35(LE'4/(IT)050003]YEARP~r~+86SEQUENTIALgj<NUMBER023REVISIONNUMBER0206OFAnalsisofEvent(cont'd)Theactualchangeinpeakcladtemperature,hadanewanalysisbeenperformed,wouldhavebeenwellbelowtheabove15degreesFvaluebecausethedeficit,inwaterwouldhaveoccurredafterthebeginningofcorerecoverywhenheattransfermechanismsassociatedwithrefloodwereinplace,andtheneedforaccumulatorwaterhadsignificantlylessened.Itisalsoconcludedthatthemissedboronsurveillancewasnotofsignificance,sinceaboronsampletakenat0925hoursonJuly18containedaconcentrationof1975partspermillion(ppm),whichiswellwithintherequiredlimitsof1900and2100ppm.Basedonalloftheaboveinformation,itisconcludedthattheeventdidnotconstituteanunreviewedsafetyquestionasdefinedin10CFR50.59nordiditadverselyimpactpublichealthandsafety.CorrectiveActionsImmediatecorrective/preventativeactionconsistedof:1)promptlyincreasingaccumulatorvolumetowi.thinTechnicalSpecificationlimitsandverifyingacceptableboronconcentration;and2)obtainingindependentlyverifiedUTlevelindication,atleastonceevery10hours,toensureTechnicalSpecificationcompliancewhiletheprocessinstrumentationwas/isoutofservice.LongtermpreventativeactionwillbetoreplacealloftheaccumulatorlevelinstrumentationwithFoxboroinstrumentationassimilarproblemshavebeenexperiencedwithseveraloftheotherITT-Bartoninstruments.ThereplacementisscheduledforUnit1duringitsscheduled1989RefuelingOutageandforUnit2duringitsnextscheduledrefuelingoutagein1990.ThepersonnelresponsiblefortheinaccuratereportonJuly15havebeeninstructedintheappropriatemethodsformaintainingcleanlinessofwrittendocumentswhileinacontaminatedenvironment,andtheimportanceoftransmittingaccurateinformationutilizedtoevaluateplantconditions.Thesepersonshavesincedemonstratedthenecessaryskillstopreventarecurrenceofthiseventduringactivitiesperformedundersimilarcircumstances.ToenhancetheeffectivenessofcommunicationsbetweenQualityControlandOperationspersonnel,thedatasheet(s)withintheultrasonictestprocedurehavebeenrevisedtorequire:1)independentverificationoftestresults;and2)UnitSupervisor/SROreviewandsignature.NRCFORM3BBA(943)*U.S.GPO.'(9880824538/455 NRCFORR35BA(983)LICENSEENTREPORT(LER)TEXTCONTINUNU.S,NUCLEARREGULATORYCOMMISSIONAPPROVEOOMBNO.3150&104EXPIRES:8/31/88FACILITYNAME(1)D.C.CookNuclearPlant-Unit2OOCKETNUMBER(2)osooo31686023-02LERNUMBER(6)YEAR~+.SEQVENTIAL>y'EVISIONNUMBER.~%NUMBERPAGE(3)07QF07TEXTN/R/FBBP44B/4BqvlBI/IIFB//I/BIBBn/HRC%%dnII35549/(17)FailedComonentIdentificationComponent:EIIS:Manufacturer:ModelNumber:CircuitBoardECBDITT-Barton384Component:EIIS:Manufacturer:ModelNumber:StrainGaugeTDITT-Barton386Component:EIIS:Manufacturer:ModelNumber:DifferentialPressureUnitPITITT-Barton224-352PreviousSimilarEventsTherehavebeennosimilareventsinthepastwheretheplanthasfailedtomeettheactionstatementassociatedwithaccumulatorvolumesbeingoutofspecification.Also,theplanthasneverfailedinthepasttoverifyboronconcentrationintheaccumulatorswithin6hoursfollowingasolutionincreaseof>/J'percentoftankvolume.NRCFORMSBBA(94)3)*U.S.GPO:1985.O.B24538/455 IndianaMichiganPower".ompanyCookNuclearPlanlP.O,Box458Bridgman.MI491066164655901INDIANANICMIGANPOWERJune24,1988UnitedStatesNuclearRegulatoryCommissionDocumentControlDeskWashington,D.C.20555OperatingLicenseDPR-58DocketNo.50-316DocumentControlManager:Inaccordancewiththecriteriaestablishedby10CFR50.73entitledLicenseeEventReortinSstem,thefollowingreportisbeingsubmitted:86-023-02Sincerely,W.G.Smith,Jr.PlantManagerWGS:clwAttachmentcc:D.H.Williams,Jr.A.B.,Davis,RegionIIIM.P.AlexichP.A.BarrettH.B.BruggerR.W.JurgensenNRCResidentInspectorJ.F.Stang,NRCR.C.CallenG.Charnoff,Esq.DottieSherman,ANILibraryD.HahnINPOPNSRCA.A.BlindS.J.Brewer/B.P.Lauzau}} | | LER86-023-02:on 860715,erroneous accumulator levelindication resulting inlowaccumulator volume.W/8DISTRIBUTION CODE:ZE22DCOPIESRECEIVED:LTR tENCL/SIZE:TITLE:50.73LicenseeEventReport(LER),IncidentRpt,etc.NOTES:RRECIPIENT ZDCODE/NAME PD3-1LASTANGFJINTERNAL: |
| | ACRSMICHELSON AEOD/DOAAEOD/DSP/ROAB ARM/DCTS/DAB NRR/DEST/ADS 7ENRR/DEST/ESB 8DNRR/DEST/MEB 9HNRR/DEST/PSB 8DNRR/DEST/SGB 8DNRR/DLPQ/QAB 10NRR/DREP/RAB 10DR<IB9ARES/DE/EIB RGN3FILE01EXTERNALEGSrGWILLIAMSFSHSTLOBBYWARDNRCPDRNSICMAYSFGCOPIESLTTRENCL111111112211101111111111111111111144111111RECIPIENT IDCODE/NAME PD3-1PDACRSMOELLERAEOD/DSP/NAS AEOD/DSP/TPAB DEDRONRR/DEST/CEB 8HNRR/DEST/ICSB 7NRR/DEST/MTB 9HNRR/DEST/RSB 8ENRR/DLPQ/HFB 10NRR/DOEA/EAB 11NRR/DREP/RPB 10NUDOCS-ABSTRACT RESTELFORD,J RES/DRPSDEPYFORDBLDGHOYFALPDRNSICHARRZSFJCOPIESLTTRENCL11221111'1111111111111122111111111111hDhTOTALNUMBEROFCOPIESREQUIRED: |
| | LTTR45ENCL44 NRCForm355(9.83)LICENSEEEVENTREPORTILER)U.S.NUCLEARREOULATOAY COMMISSION APPAOVEOOMBNO,31504101EXPIRES:8/31/88FACILITYNAME(I)D.C.CookNuclearPlant-Unit2DOCKETNUMBER(2)PAE3)o5ooo316>OF07TITLE(IlErroneous Accumulator LevelIndication Resulting inLowAccumulator VolumeMONTHDAYYEAREVENTDATE(5)LERNUMBER(5)YEARÃ~'.SEQVSNtIAL Pr~REVOKENVM888X5IIVM88RREPORTDATE(7)MONTHOAYYEARFACILITYNAMESDOCKETNUMBER(SI 05000OTHERFACILITIES INVOLVED(8)071586860230206248805000OPERATINO MODE(8)POWERLEVELTHISREPORTISSUBMITTED PURSUANTT50.73(e)(2)(ivl50.73(e)12)(vl50.nN)(2)(vB) 50.n(el(2)(vBII(A) 50,73(el(2) |
| | (v)5)(BI9),73(~)(2)(el20A05(c)50.38(cl(1) 50.38(c)(2)50,73(eIl2)0)5073(el(2)(EI 50.73(e)(2)(51120.802(8)20405(~)(1)(l)20A05(el(I)(8)20A05(e)(1)(BII 20A05(el(1)(tvl 20A05(~)(I)(vlLICENSEECONTACTFORTHISLER(12)0THEREOUIREMENTS OF10CFR()I(CheckoneormoriOfthefollovffnfl (Ill73.7)(8)73.71(c)OTHERfSpeclfyInAhttrectOelowendInFeet,NRCForm3BBAINAMET.K.Postlewait-Technical EnineerinSuerintendent TELEPHONE NUMBERAREACODE616465-5901COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT(13)CAUSESYSTEMCOMPONENT MANUFACTUREREP0RTA8L~',It~IIiCAUSESYSTEMCOMPONENT MANUFAC.TURERTONPROSXXBPECBDBPTDI204I204@~IXBPPITI204SUPPLEMENTAL AEPOATEXPECTED(lelEXPECTEDSU5MlSSIONDATE(15)MONTHOAYYEARYESf/fyet,completeEXPECTEDSUBMISSION D4FE)NOABBTRAcT(Llmlttote00tpecet,I.e.,eppronlmetely fifteentlncleepece typewritten llnnl08)Thisrevisionisbeingsubmitted toincludetheresultsofdiagnostic testingperformed duringtheSeptember 1987outage.BetweenJuly15and18,1986,problemswereencountered withtheprocessinstrumentation monitoring thevolumewithinaccumulator |
| | )jj'2.Complications developed duringultrasonic testing(UT)conducted toverifyaccumulator operability whichresultedinthefailuretoidentifyaviolation oftheactionstatement associated withlowaccumulator volumeandamissedsurveillance forboronconcentration. |
| | Theadministrative problemsassociated withaccumulator levelverification byUTwerecorrected.and thismethodwasusedinlieuoftheprocessinstrumentation toverifyaccumulator operability untilunitshutdownforanoutageMarch3,1987.Testingperformed duringtheMarch1987outage,determined thatthreeinstrument components weredefective; allwerereplacedinkind.OnApril26,1987ILA<<121begantodriftupwards.OnApril30,1987,asaprecautionary measure,ILA-121wasdeclaredinoperable. |
| | Accumulator levelwasmonitored usingUTuntilunitshutdownonAugust27,1987.Testingperformed duringtheSeptember 1987outagedetermined thatoneinstrument component wasdefective. |
| | Thecomponent wasreplacedinkindandtheprocessinstrumentation hassubsequently functioned normally. |
| | NRCForm388(Be)3I8807060}}9 880624PDRADOCK050003}6SPNU$6ZZ NRCForm3BBA(943(LICENSEENTREPORT(LER)TEXTCONTINUANU.S.NUCLEARREGULATORY COMMISSION APPROVEDOMBNO,3I50-0104 EXPIRES:8/3'I/88FACILITYNAME(I(DOCKETNUMBER(2)LERNUMBER(8(PAGE(3iD.C.CookNuclearPlant-Unit2TE/ET/~RRE>> |
| | <<~,~~//RCr3SBA<</(mYEARosooo31686SEOUENTIAL NUMBER023REVISIONNUMBER0202QF07Thisrevisionisbeingsubmitted toincludetheresultsofdiagnostic testingperformed duringtheSeptember 1987outage.Conditions PriortoOccurrence Unit2inMode1,RTPat48percent(91330hourson7-15-86)DescritionofEventTechnical Specification 3.5.lbrequiresthateachaccumulator (EIIS/BP-TK) mustmaintainbetween929and971cubicfeetofboratedwaterwhiletheunitisinModes1-3(PowerOperation, Startup,andHotStandby,respectively). |
| | Iftheaccumulator volumedeviatesfromtheprescribed limits,thevolumemustberestoredwithin1hourortheunitmustbeinhotshutdown(Mode4)withinthenext12hours.Processinstrumentation monitoring accumulator inventory (EIIS/BP-LIT) displayswatervolumeincubicfeet.Thesystemiscomprised of2indicators foreachaccumulator, onewiderange(300-1000cubicfeet)andonenarrowrange(900-1000cubicfeet).OnJuly15,1986,operators onshiftbecamesuspectoftheaccumulator 82volumeindication andrequested anultrasonic test(UT)beperformed toverifywaterinventory. |
| | QualityControlpersonnel locatedthewaterlevelusingultrasound andthenmarked/dated thetankaccordingly; however,duringthisprocesstheirdatasheetbecamecontaminated andwasdiscarded beforeleavingaccesscontrol.Anewdatasheetwassubsequently filledoutfrommemoryandtheControlRoomwasinformedat1330hoursonJuly15thataccumulator |
| | (/(2wasat115.75inches.Whenmathematically converted tovolume,thislevelcorresponds to969.58cubicfeet;which,bycoincidence only,happenedtocloselyagreewiththeprocessinstrumentation indication atthattime.OnJuly18,1986,at0800hoursanotherUTwasrequested foraccumulator |
| | /!2becauseofquestionable volumeindication. |
| | WhenQCarrivedataccumulator |
| | (/'2theydiscovered a10incherrorwasmadeintheJuly15report.Thelevelwasactually105.75inches(909.58cubicfeet)onJuly15,andnot115.75(969.58cubicfeet)asreported. |
| | Itcantherefore bededucedthatthelowerlimitforcontinued operation (929cubicfeet)hadbeenviolatedsinceatleastJuly15withouttheappropriate compensatory actionsbeingtaken.NRCFORMSBBA(EBSI*U.S.GPO:(BBB 0824538/455 NRCForm366A(84)3)LICENSEENTREPORT(LER)TEXTCONTINUANV.S.NUCLEARREGULATORY COMMISSION APPROVEOOMBNO.3(50-0104 EXPIRES:8/31/88FACILITYNAMEl()D.C.CookNuclearPlant-Unit2OOCKETNUMBER(2)31686LFRNUMBER(6)SEQUENTIAL NUMBER023REVISIONNUMBER020PAGE(3)OFTUCT(lmrsoEpsos/4rBEM)BI(, |
| | BBB///orrr/HRC |
| | /ronn36543)l17)DescritionofEvent(cont'd)Thiserrorwascompounded duringcommunications betweenQualityControlandOperations following theUTperformed themorningofJuly18.At0945hoursonthatmorning,QualityControlreportedthelevelofaccumulator f32hadrisen3inchessincethelasttestperformed onJuly15.Operations wasnotmadeawareofthe10incherrordiscovered earlier.Consequently, actingundertheimpression thataccumulator |
| | ((I2hadrisenfrom115.75inches(969.58cubicfeet)toavolumeexceeding theupperlimitingcondition forcontinued operation,'perations personnel declaredaccumulator 82inoperable baseduponhighlevel(itwasactuallylow)andmeasuresweretakentobegindrainingthetank.WithrespecttothevolumeincreasewhichoccurredsometimebetweenJuly15andJuly18,noconclusive evidencecanbeproducedconfirming thatsaidincreaseactuallyhappenedwithinasixhourtimespanpreceding boronsamplingperformed at0925hoursonJuly18.Therefore, theplantmustassumetheboronconcentration wasnotverifiedfollowing asolutionincrease>/1percentoftankvolumeasrequiredbyTechnical Specification 4.5.1b.Itshouldbenotedthatat0952hoursonJuly18,whilepreparations wereunderwayfordrainingaccumulator 82,Unit2trippedonasteamgenerator levelhigh-high signalthusplacingtheunitinMode3.Thiseventwasfurthercomplicated at1447hoursonJuly18whentheControlRoomwasinformedthatUTresultsplaced82accumulator's level3inchesbelowthelastmeasurement takenearlierthatmorning(duetodraining). |
| | Withthisinformation, andstillunawareofthe10incherrormadeonJuly15,Operations declaredtheaccumulator operablebecausetheybelievedtheapparently highvolumeofwaterhadbeenreducedtowithinacceptable limitsforcontinued operation. |
| | Inreality,theaccumulator volumewasdraineddownfromanalreadytoolowcondition toanevenlowerstatus.At1620hoursonJuly18,Operations becamecognizant ofthe10incherrormadeonJuly15.Itwasrecognized atthistimethataccumulator |
| | $!2was,andhadbeensinceatleast1330hoursonJuly15,inviolation ofthelowervolumelimitrequiredbyTechnical Specification 3.5.1b.Accumulator |
| | /f2wasimmediately declaredinoperable. |
| | Coolingofthereactorcoolantsystem(EIIS/BP-AB) toachieveMode4beganat1720hoursandtheNRCwasnotifiedoftheeventbyphoneat1808hours.Effortstowardsfillingaccumulator f/2viatherefueling waterstoragetank(EIIS/BP-TK) commenced at1839hoursandtheeventwasterminated at2120hoursonJuly18whentheaccumulator volumeandboronconcentration wereverifiedtobewithinthelimitingcondition foroperation asdescribed inTechnical Specification 3.5.1band3.5.1crespectively. |
| | CooldownwashaltedpriortoreachingMode4.Withtheexception oftheloop2accumulator volumeinstrumentation, therewerenoinoperable structures, systems,orcomponents atthestartofthiseventwhichcouldhavecontributed toitsoccurrence. |
| | NRCFORM366A(()4)3)oU,S.GPO.1 9880824538/455 0<iII NRCForm388A(943)LICENSEENTREPORT(LER)TEXTCONTINUA~NU.S.NUCLEARREGULATORY COMMISSION APPROVEDOMSNO3150-0104 EXPIRES8/31/88FACILITYNAME(11DOCKETNUMBER(2)LERNUMBER(BlPAGE(3)D.C.CookNuclearFlant-Unit27%XT/4/m<<oNMoo/sIFEo8or/, |
| | IrsoI/8/ooo/HRC R<<m35843/(17)osooo316YEAR@IrI86SEQUENTIAL NUMBER8rV023IIEVISION NUMSER0204OF07CauseofEventThecauseofthiseventhasbeenattributed totheinability oftheprocessinstrumentation toaccurately reflectthevolumewithinaccumulator 82,whichresultedintheneedforultrasonic testingtoverifyaccumulator operability. |
| | Threedefective components withinthesystemwerediagnosed astherootcausefortheinstrumentation failure.theinstrumentation consistsofacircuitboard(EIIS/BP-ECBD), |
| | straingauge(EIIS/BP-TD), |
| | potentiometer span(EIIS/BP-EC), |
| | potentiometer zero(EIIS/BP-EC) andanarrowrangedifferential pressureunit(DPU)(EIIS/BP-PIT). |
| | Theinitialinvestigation indicated thatthe"zero"wasdrifting, whichresultsfromafaultycircuitboardandstraingauge.Subsequently, thesecomponents werereplaced. |
| | Theinstrumentation subsequently zeroedproperly, butdatawasnotrepeatable vhenrangedupandbackdownthemeasurement scale.Asaresult,theDPUnarrowrangewasreplacedwhicheliminated therepeatability problem.Later,'he spanandzeropotentiometers verereplacedtoensureproperinstrumentation operation. |
| | Thecalibrated instrument wasreturnedtoserviceonApril2,1987,andfunctioned normallyuntilApril26,atwhichtimethesystembegantoexhibitsignsofdriftingupwards.Ultrasonic measurements takenafterApril26confirmed theactualvolumewithinaccumulator f/2wassteadyandwellwithintheTechnical Specification allowable range,however,theresultsalsoconfirmed thatILA-121wascontinuing aslowbutsteadyupwarddrifttowardstheadministrative limitforoperability. |
| | Asaprecautionary measure,ILA-121wasdeclaredinoperable at1328hoursonApril30,1987.Furtherinvestigation conducted duringtheSeptember 1987outageindicated thattherootcauseofthesecondinstrument failurewasafaultyDPUnarrowrange.TheDPUnarrowrangewasreplacedandthecalibrated instrument wasreturnedtoserviceonSeptember 24,1987.Theinstrument hassubsequently functioned normally. |
| | Contributing tothiseventwasthefactthatQualityControlpersonnel whoperformed theoriginalUTonJuly15didnotimplement soundworkpractices whileconducting activities inaradioactive environment. |
| | Thisresultedinthelossofhard.copydatasupporting testresultsforcingthoseinvolvedtorelysolelyuponmemoryrecall.ItshouldbenotedthattheUTwasperformed within-anextremely harshenvironment consisting ofelevatedtemperature andairborneradioactivity. |
| | Theseadverseconditions complicated effortsofthetestcrewbecausefullfacemaskwasrequiredandthefatigueprocesswasaccelerated. |
| | Inadequate communication betweentheControlRoomandQualityControlpersonnel furthercomplicated thisevent.Noformalmechanism hadbeenestablished toverifythatoperators onshifthadacompleteandaccurateunderstanding oftheUTresults.NRCFORMSBBA(948)*U.S.GPO:)988%.824 538/455 NRCForm366A(94)3)LICENSEENTREPORT(LER)TEXTCONTINUNU.S.NUCLEARREGULATORY COMMISSION APPROVEDOMBNO.3(9)&104EXPIRES:8/31/88FACILITYNAME(llDOCKETNUMBER(2)LERNUMBER(6)PAGE(3)D.C.CookNuclearPlant-Unit2TEXT/kmcY8<<>>48lrnr/I/EerE I/88T/I/or>>/HRC |
| | %%dnn35549/(17)YEAR3168602302(jar,SEGVENTIAL jZ':REVISION49NUM88Rv>errNUMSER05OF07AnalsisofEventThiseventisreportable underthecriteriaof10CFR50.73(a)(2)(i) asdescribed below.-Forapproximately 3dayspriortoJuly18,1986,thevolumeofaccumulator 82wasbelowitslowerlimitingcondition foroperation andthecorresponding actionstatement associated withTechnical Specification 3.5.1bwasnotsatisfied. |
| | -BetweenJuly15andJuly18,1986,accumulator 82experienced asolutionincreasegreater>/m1percentofthetankvolumeandtheboronconcentration wasnotverifiedtobeacceptable withinthenext6hoursasrequiredbyTechnical Specification 4.5.1b.Thesafetysignificance ofpoweroperation withaccumulator volumeofoneaccumulator at909.6cubicfeetratherthan929cubicfeetislimitedtoimpactontheloss-of-coolant accidentanalysis. |
| | Thelimitingloss-of-coolant accidentanalysisforUnit2Cycle6predictsapeakcladtemperature of2079degreeFwitha121degreeFmargintothe2200degreeFlimitspecified in10CFR50.46.ExxonNuclearCompany,thefuelvendorforCycle6,wasrequested toevaluatetheimpactofthiseventonpublichealthandsafety.Theirresponsestated:itisExxon'sopinionthatasignificant safetyhazardtothepublicdidnotexistforthefollowing reason.Thelimitingcaseinthereference indicated apeakcladdingtemperature (PCT)of2079degreeFforoperation atlOOXpower.Operation at90percentpowerwouldresultinareduction inthePCTandwouldtendtooffsetanyincreaseinPCTduetothereducedaccumulator liquidvolume.Thereducedaccumulator liquidvolumealoneisexpectedtohaveaverysmalleffectonthePCT.Theaccumulator flowwouldendapproximately 1secondsoonerthanthetimeindicated inthereference. |
| | Sincethisoccursafterthebeginning ofcorerecoverytime(BOCREC)whenthedowncomer isfull,averysmalladverseeffectonrefloodrateandPCTwouldoccurandwouldbemuchlessthanthe121degreeFmarginindicated inthereference." |
| | Itisofnotethatthedifference betweentheas-foundcondition (909.6cubicfeet)andthevaluespecified intheTechnical Specification of929cubicfeetis19.4cubicfeet,orapproximately 960lbs.ofwater.Inordertoconservatively evaluatetheeffectonpeakcladtemperature, ahypothetical scenariowasevaluated inwhichitwasassumedthatthiswaterwasdeficient duringtherefillperiod,andhadtobemadeupbypumpedin5ection water.Itwouldhavetakenthepumpsapproximately 1.1secondstomakeupthiswater.SincethePCTrateofheatupduringtheearlyreflood/refill periodisabout13degree/sec., |
| | thiswouldhaveresultedinaPCTincreaseofabout15degreeF.Adding15degreeFtothecalculated PCTresultsinanewPCTof2094degreeF,whichisstillwellwithinthelimitsof10CFR50.46.NRCFORMSStA(94)3)8U.S.GPO:1986.0.624 538/455 NRCForm388A(943)L'ICENSEE NTREPORT(LER)TEXTCONTINUANU.S.NUCLEARREGULATORY COMMISSION APPROVEDOMSNO.3150M)84EXPIRES:8/31/88FACILITYNAME{1)DOCKETNUMBER(2)LERNUMBER(8)PACE(3)D.C.CookNuclearPlant-Unit2TEXT/Smroodraco/rorR/)or/, |
| | I/44/8/orro/NRC Farm35(LE'4/(IT) 050003]YEARP~r~+86SEQUENTIAL gj<NUMBER023REVISIONNUMBER0206OFAnalsisofEvent(cont'd)Theactualchangeinpeakcladtemperature, hadanewanalysisbeenperformed, wouldhavebeenwellbelowtheabove15degreesFvaluebecausethedeficit,in waterwouldhaveoccurredafterthebeginning ofcorerecoverywhenheattransfermechanisms associated withrefloodwereinplace,andtheneedforaccumulator waterhadsignificantly lessened. |
| | Itisalsoconcluded thatthemissedboronsurveillance wasnotofsignificance, sinceaboronsampletakenat0925hoursonJuly18contained aconcentration of1975partspermillion(ppm),whichiswellwithintherequiredlimitsof1900and2100ppm.Basedonalloftheaboveinformation, itisconcluded thattheeventdidnotconstitute anunreviewed safetyquestionasdefinedin10CFR50.59nordiditadversely impactpublichealthandsafety.Corrective ActionsImmediate corrective/preventative actionconsisted of:1)promptlyincreasing accumulator volumetowi.thinTechnical Specification limitsandverifying acceptable boronconcentration; and2)obtaining independently verifiedUTlevelindication, atleastonceevery10hours,toensureTechnical Specification compliance whiletheprocessinstrumentation was/isoutofservice.Longtermpreventative actionwillbetoreplacealloftheaccumulator levelinstrumentation withFoxboroinstrumentation assimilarproblemshavebeenexperienced withseveraloftheotherITT-Barton instruments. |
| | Thereplacement isscheduled forUnit1duringitsscheduled 1989Refueling OutageandforUnit2duringitsnextscheduled refueling outagein1990.Thepersonnel responsible fortheinaccurate reportonJuly15havebeeninstructed intheappropriate methodsformaintaining cleanliness ofwrittendocuments whileinacontaminated environment, andtheimportance oftransmitting accurateinformation utilizedtoevaluateplantconditions. |
| | Thesepersonshavesincedemonstrated thenecessary skillstopreventarecurrence ofthiseventduringactivities performed undersimilarcircumstances. |
| | Toenhancetheeffectiveness ofcommunications betweenQualityControlandOperations personnel, thedatasheet(s)withintheultrasonic testprocedure havebeenrevisedtorequire:1)independent verification oftestresults;and2)UnitSupervisor/SRO reviewandsignature. |
| | NRCFORM3BBA(943)*U.S.GPO.'(988 0824538/455 NRCFORR35BA(983)LICENSEENTREPORT(LER)TEXTCONTINUNU.S,NUCLEARREGULATORY COMMISSION APPROVEOOMBNO.3150&104EXPIRES:8/31/88FACILITYNAME(1)D.C.CookNuclearPlant-Unit2OOCKETNUMBER(2)osooo31686023-02LERNUMBER(6)YEAR~+.SEQVENTIAL |
| | >y'EVISIONNUMBER.~%NUMBERPAGE(3)07QF07TEXTN/R/FBBP44B/4BqvlBI/IIFB//I/BIBBn/ |
| | HRC%%dnII35549/(17)FailedComonentIdentification Component: |
| | EIIS:Manufacturer: |
| | ModelNumber:CircuitBoardECBDITT-Barton 384Component: |
| | EIIS:Manufacturer: |
| | ModelNumber:StrainGaugeTDITT-Barton 386Component: |
| | EIIS:Manufacturer: |
| | ModelNumber:Differential PressureUnitPITITT-Barton 224-352PreviousSimilarEventsTherehavebeennosimilareventsinthepastwheretheplanthasfailedtomeettheactionstatement associated withaccumulator volumesbeingoutofspecification. |
| | Also,theplanthasneverfailedinthepasttoverifyboronconcentration intheaccumulators within6hoursfollowing asolutionincreaseof>/J'percentoftankvolume.NRCFORMSBBA(94)3)*U.S.GPO:1985.O.B24 538/455 IndianaMichiganPower".ompanyCookNuclearPlanlP.O,Box458Bridgman. |
| | MI491066164655901INDIANANICMIGANPOWERJune24,1988UnitedStatesNuclearRegulatory Commission DocumentControlDeskWashington, D.C.20555Operating LicenseDPR-58DocketNo.50-316DocumentControlManager:Inaccordance withthecriteriaestablished by10CFR50.73entitledLicenseeEventReortinSstem,thefollowing reportisbeingsubmitted: |
| | 86-023-02 Sincerely, W.G.Smith,Jr.PlantManagerWGS:clwAttachment cc:D.H.Williams, Jr.A.B.,Davis, RegionIIIM.P.AlexichP.A.BarrettH.B.BruggerR.W.Jurgensen NRCResidentInspector J.F.Stang,NRCR.C.CallenG.Charnoff, Esq.DottieSherman,ANILibraryD.HahnINPOPNSRCA.A.BlindS.J.Brewer/B. |
| | P.Lauzau}} |
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Updated LER Will Be Submittted by 990415.With 990127 Ltr ML17335A4921999-01-19019 January 1999 LER 98-052-01:on 981128,no Analysis for NSR Sc Manual Loader for Tdafwp Could Be Found in Original Design.Cause Due to All Failure Modes Not Considered When Compressed Air Sys Originally Designed.Performed Review of Components ML17335A4721999-01-0606 January 1999 LER 98-055-00:on 981207,potential for Condition Outside of Design Bases for Rod Control Sys Was Noted.Caused by Calibration Error Coupled with Single Rod Failure.Condition Rept Investigation Is Ongoing ML17335A4691999-01-0606 January 1999 LER 98-056-00:on 981211,hot Leg Nozzle Gaps Resulted in Plant Being in Unanalyzed Condition.Analyses Are Being Performed by W to Resolve Problem.Updated LER Will Be Submitted by 990211.With 990106 Ltr ML17335A4661999-01-0505 January 1999 LER 98-049-00:on 981020,emergency Boron Injection Flow Path Was Inoperable.Caused by Original Design Deficiency. Engineering Evaluation of Event Is Continuing ML17335A4631999-01-0404 January 1999 LER 98-054-00:on 981202,discovered That at Least One MSSV Had Not Been Reset as Required by Ts.Engineering Is Continuing Review of Extent of Condition for Event.Updated LER Will Be Submitted by 990129.With 990104 Ltr ML17335A4481998-12-30030 December 1998 LER 98-053-00:on 981130,discovered Use of Inoperable Substitute Subcooling Margin Monitor.Caused by Condition Existing Since Installation of Plant Process Computer in 1992.Updated LER Will Be Submitted.With 981230 Ltr ML17335A4581998-12-28028 December 1998 LER 98-052-00:on 981128,turbine Driven AFW Pump Speed Controller Failure Mode Occurred.Caused Because Not All Failure Modes Were Considered When Compressed Air Sys Was Originally Designed.Verified Current Design Change Process ML17335A4281998-12-22022 December 1998 LER 98-051-00:on 981122,reactor Trip Signal from Manual Safety Injection Not Verified as Required by TS Surveillance,Was Discovered.Maintenance Currently Evaluating Significance & Cause of Event ML17335A4111998-12-17017 December 1998 LER 98-047-00:on 981117,potential for Increase Leakage from Reactor Coolant Pump Seals Was Identified.Util Is Working with W to Resolve Issue.Current Expectations Are to Submit Update to LER by 990215.With 981217 Ltr ML17335A4141998-12-16016 December 1998 LER 98-058-00:on 981216,postulated High Line Break Could Result in Condition Outside Design Bases for AF Occurred. Caused by Deficiencies Associated with Administration of HELB Program.Analysis of AF Will Be Completed by 990122 ML17335A4181998-12-16016 December 1998 LER 98-050-00:on 980814,ancillary Equipment Installed in Ice Condenser Was Not Designed to Withstand Design Basis Accident/Earthquake Loads.Caused by Lack of Established Design Criteria.Developed Design Criteria ML17335A3871998-12-11011 December 1998 LER 98-031-01:on 980610,potential Common Mode Failure of RHR Pumps Were Noted.Caused by Inaccurate Values.Accurate Miniflow Numbers Have Been Determined by Flow Testing ML17335A3821998-12-0808 December 1998 LER 98-039-01 Re EOP Step Conflicts with Small Break LOCA Analysis.Ler 98-039-00 Has Been Canceled.With 981208 Ltr ML17335A3781998-12-0707 December 1998 LER 98-007-00:on 981106,high Energy Line Break Effects in Auxiliary FW Sys Was Noted.Cause of Event Is Under Investigation & Will Be Completed by 990220.Updated LER Will Be Submitted by 990310.With 981207 Ltr ML17335A3771998-12-0303 December 1998 LER 98-046-00:on 981103,determined That Afs Was Unable to Meet Design Flow Requirements During Special Test.Caused by Failure to Consider All Aspects of Sys Operation in Design of Suction Basket Strainers.Sys Will Be Redesigned ML17335A3741998-12-0202 December 1998 LER 97-011-02:on 970822,operation Was Noted Outside Design Bases for ECCS & CSP for Switchover to Recirculation Sump Suction.Caused by Ineffective Change Mgt.Revised Procedure for Switchover 01(02) Ohp 4023.ES-1.3 1999-09-17
[Table view] Category:RO)
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors ML17335A5171999-02-11011 February 1999 LER 99-002-00:on 990112,determined That RCS Pressurizer PORVs Had Not Been Tested,Per Ts.Caused by Inadequate Scheduling Controls Allowing Personnel Error.Surveillance Procedure Was Completed & Updated LER Will Be Submitted ML17335A5141999-02-10010 February 1999 LER 99-001-00:on 990106,noted That GE Hfa Relays Installed in EDGs May Not Meet Seismic Qualification.Caused by Operating Experience Info Incorrectly Dispositioned in 1985. Updated LER Will Be Submitted by 990405 ML17335A5011999-02-0101 February 1999 LER 98-060-00:on 981231,identified That Rt Sys Response Time Testing Did Not Comply with TS Definition.Caused by Inadequate Procedures.Corrective Actions Will Be Developed & Update to LER Will Be Submitted by 990415.With 990201 Ltr ML17335A4951999-01-29029 January 1999 LER 98-059-00:on 981230,interim LER -single Failure in Containment Spray Sys Could Result in Containment Spray Ph Outside Design Occurred.Investigation Into Condition Continuing.Update Will Be Submitted by 990514 Ltr ML17335A4961999-01-27027 January 1999 LER 98-057-00:on 981228,discovered That AFW Valves Were Not Tested IAW Inservice Testing Program.Caused by Failure to Recognize Design Bases Features Re Afws by Personnel. Updated LER Will Be Submittted by 990415.With 990127 Ltr ML17335A4921999-01-19019 January 1999 LER 98-052-01:on 981128,no Analysis for NSR Sc Manual Loader for Tdafwp Could Be Found in Original Design.Cause Due to All Failure Modes Not Considered When Compressed Air Sys Originally Designed.Performed Review of Components ML17335A4721999-01-0606 January 1999 LER 98-055-00:on 981207,potential for Condition Outside of Design Bases for Rod Control Sys Was Noted.Caused by Calibration Error Coupled with Single Rod Failure.Condition Rept Investigation Is Ongoing ML17335A4691999-01-0606 January 1999 LER 98-056-00:on 981211,hot Leg Nozzle Gaps Resulted in Plant Being in Unanalyzed Condition.Analyses Are Being Performed by W to Resolve Problem.Updated LER Will Be Submitted by 990211.With 990106 Ltr ML17335A4661999-01-0505 January 1999 LER 98-049-00:on 981020,emergency Boron Injection Flow Path Was Inoperable.Caused by Original Design Deficiency. Engineering Evaluation of Event Is Continuing ML17335A4631999-01-0404 January 1999 LER 98-054-00:on 981202,discovered That at Least One MSSV Had Not Been Reset as Required by Ts.Engineering Is Continuing Review of Extent of Condition for Event.Updated LER Will Be Submitted by 990129.With 990104 Ltr ML17335A4481998-12-30030 December 1998 LER 98-053-00:on 981130,discovered Use of Inoperable Substitute Subcooling Margin Monitor.Caused by Condition Existing Since Installation of Plant Process Computer in 1992.Updated LER Will Be Submitted.With 981230 Ltr ML17335A4581998-12-28028 December 1998 LER 98-052-00:on 981128,turbine Driven AFW Pump Speed Controller Failure Mode Occurred.Caused Because Not All Failure Modes Were Considered When Compressed Air Sys Was Originally Designed.Verified Current Design Change Process ML17335A4281998-12-22022 December 1998 LER 98-051-00:on 981122,reactor Trip Signal from Manual Safety Injection Not Verified as Required by TS Surveillance,Was Discovered.Maintenance Currently Evaluating Significance & Cause of Event ML17335A4111998-12-17017 December 1998 LER 98-047-00:on 981117,potential for Increase Leakage from Reactor Coolant Pump Seals Was Identified.Util Is Working with W to Resolve Issue.Current Expectations Are to Submit Update to LER by 990215.With 981217 Ltr ML17335A4141998-12-16016 December 1998 LER 98-058-00:on 981216,postulated High Line Break Could Result in Condition Outside Design Bases for AF Occurred. Caused by Deficiencies Associated with Administration of HELB Program.Analysis of AF Will Be Completed by 990122 ML17335A4181998-12-16016 December 1998 LER 98-050-00:on 980814,ancillary Equipment Installed in Ice Condenser Was Not Designed to Withstand Design Basis Accident/Earthquake Loads.Caused by Lack of Established Design Criteria.Developed Design Criteria ML17335A3871998-12-11011 December 1998 LER 98-031-01:on 980610,potential Common Mode Failure of RHR Pumps Were Noted.Caused by Inaccurate Values.Accurate Miniflow Numbers Have Been Determined by Flow Testing ML17335A3821998-12-0808 December 1998 LER 98-039-01 Re EOP Step Conflicts with Small Break LOCA Analysis.Ler 98-039-00 Has Been Canceled.With 981208 Ltr ML17335A3781998-12-0707 December 1998 LER 98-007-00:on 981106,high Energy Line Break Effects in Auxiliary FW Sys Was Noted.Cause of Event Is Under Investigation & Will Be Completed by 990220.Updated LER Will Be Submitted by 990310.With 981207 Ltr ML17335A3771998-12-0303 December 1998 LER 98-046-00:on 981103,determined That Afs Was Unable to Meet Design Flow Requirements During Special Test.Caused by Failure to Consider All Aspects of Sys Operation in Design of Suction Basket Strainers.Sys Will Be Redesigned ML17335A3741998-12-0202 December 1998 LER 97-011-02:on 970822,operation Was Noted Outside Design Bases for ECCS & CSP for Switchover to Recirculation Sump Suction.Caused by Ineffective Change Mgt.Revised Procedure for Switchover 01(02) Ohp 4023.ES-1.3 1999-09-17
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
[Table view] |
Text
ACCELEBRATED 91S'JUUBUTION DEMONS~TJON SY~gMREGULATINFORMATION DISTRIBUTIOIYSTEM (RIDE))",ACCESSION NBR:8807060119 DOC.DATE:
88/06/24NOTARIZED:
NODOCKETFACZL:50-316 DonaldC.CookNuclearPowerPlant,Unit2,Indiana&05000316AUTH.NAMEAUTHORAFFILIATION POSTLEWAZT,T.K.
IndianaMichiganPowerCo.SMITH,W.G.
IndianaMichiganPoweCo.RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER86-023-02:on 860715,erroneous accumulator levelindication resulting inlowaccumulator volume.W/8DISTRIBUTION CODE:ZE22DCOPIESRECEIVED:LTR tENCL/SIZE:TITLE:50.73LicenseeEventReport(LER),IncidentRpt,etc.NOTES:RRECIPIENT ZDCODE/NAME PD3-1LASTANGFJINTERNAL:
ACRSMICHELSON AEOD/DOAAEOD/DSP/ROAB ARM/DCTS/DAB NRR/DEST/ADS 7ENRR/DEST/ESB 8DNRR/DEST/MEB 9HNRR/DEST/PSB 8DNRR/DEST/SGB 8DNRR/DLPQ/QAB 10NRR/DREP/RAB 10DR<IB9ARES/DE/EIB RGN3FILE01EXTERNALEGSrGWILLIAMSFSHSTLOBBYWARDNRCPDRNSICMAYSFGCOPIESLTTRENCL111111112211101111111111111111111144111111RECIPIENT IDCODE/NAME PD3-1PDACRSMOELLERAEOD/DSP/NAS AEOD/DSP/TPAB DEDRONRR/DEST/CEB 8HNRR/DEST/ICSB 7NRR/DEST/MTB 9HNRR/DEST/RSB 8ENRR/DLPQ/HFB 10NRR/DOEA/EAB 11NRR/DREP/RPB 10NUDOCS-ABSTRACT RESTELFORD,J RES/DRPSDEPYFORDBLDGHOYFALPDRNSICHARRZSFJCOPIESLTTRENCL11221111'1111111111111122111111111111hDhTOTALNUMBEROFCOPIESREQUIRED:
LTTR45ENCL44 NRCForm355(9.83)LICENSEEEVENTREPORTILER)U.S.NUCLEARREOULATOAY COMMISSION APPAOVEOOMBNO,31504101EXPIRES:8/31/88FACILITYNAME(I)D.C.CookNuclearPlant-Unit2DOCKETNUMBER(2)PAE3)o5ooo316>OF07TITLE(IlErroneous Accumulator LevelIndication Resulting inLowAccumulator VolumeMONTHDAYYEAREVENTDATE(5)LERNUMBER(5)YEARÃ~'.SEQVSNtIAL Pr~REVOKENVM888X5IIVM88RREPORTDATE(7)MONTHOAYYEARFACILITYNAMESDOCKETNUMBER(SI 05000OTHERFACILITIES INVOLVED(8)071586860230206248805000OPERATINO MODE(8)POWERLEVELTHISREPORTISSUBMITTED PURSUANTT50.73(e)(2)(ivl50.73(e)12)(vl50.nN)(2)(vB) 50.n(el(2)(vBII(A) 50,73(el(2)
(v)5)(BI9),73(~)(2)(el20A05(c)50.38(cl(1) 50.38(c)(2)50,73(eIl2)0)5073(el(2)(EI 50.73(e)(2)(51120.802(8)20405(~)(1)(l)20A05(el(I)(8)20A05(e)(1)(BII 20A05(el(1)(tvl 20A05(~)(I)(vlLICENSEECONTACTFORTHISLER(12)0THEREOUIREMENTS OF10CFR()I(CheckoneormoriOfthefollovffnfl (Ill73.7)(8)73.71(c)OTHERfSpeclfyInAhttrectOelowendInFeet,NRCForm3BBAINAMET.K.Postlewait-Technical EnineerinSuerintendent TELEPHONE NUMBERAREACODE616465-5901COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT(13)CAUSESYSTEMCOMPONENT MANUFACTUREREP0RTA8L~',It~IIiCAUSESYSTEMCOMPONENT MANUFAC.TURERTONPROSXXBPECBDBPTDI204I204@~IXBPPITI204SUPPLEMENTAL AEPOATEXPECTED(lelEXPECTEDSU5MlSSIONDATE(15)MONTHOAYYEARYESf/fyet,completeEXPECTEDSUBMISSION D4FE)NOABBTRAcT(Llmlttote00tpecet,I.e.,eppronlmetely fifteentlncleepece typewritten llnnl08)Thisrevisionisbeingsubmitted toincludetheresultsofdiagnostic testingperformed duringtheSeptember 1987outage.BetweenJuly15and18,1986,problemswereencountered withtheprocessinstrumentation monitoring thevolumewithinaccumulator
)jj'2.Complications developed duringultrasonic testing(UT)conducted toverifyaccumulator operability whichresultedinthefailuretoidentifyaviolation oftheactionstatement associated withlowaccumulator volumeandamissedsurveillance forboronconcentration.
Theadministrative problemsassociated withaccumulator levelverification byUTwerecorrected.and thismethodwasusedinlieuoftheprocessinstrumentation toverifyaccumulator operability untilunitshutdownforanoutageMarch3,1987.Testingperformed duringtheMarch1987outage,determined thatthreeinstrument components weredefective; allwerereplacedinkind.OnApril26,1987ILA<<121begantodriftupwards.OnApril30,1987,asaprecautionary measure,ILA-121wasdeclaredinoperable.
Accumulator levelwasmonitored usingUTuntilunitshutdownonAugust27,1987.Testingperformed duringtheSeptember 1987outagedetermined thatoneinstrument component wasdefective.
Thecomponent wasreplacedinkindandtheprocessinstrumentation hassubsequently functioned normally.
NRCForm388(Be)3I88070609 880624PDRADOCK050003}6SPNU$6ZZ NRCForm3BBA(943(LICENSEENTREPORT(LER)TEXTCONTINUANU.S.NUCLEARREGULATORY COMMISSION APPROVEDOMBNO,3I50-0104 EXPIRES:8/3'I/88FACILITYNAME(I(DOCKETNUMBER(2)LERNUMBER(8(PAGE(3iD.C.CookNuclearPlant-Unit2TE/ET/~RRE>>
<<~,~~//RCr3SBA<</(mYEARosooo31686SEOUENTIAL NUMBER023REVISIONNUMBER0202QF07Thisrevisionisbeingsubmitted toincludetheresultsofdiagnostic testingperformed duringtheSeptember 1987outage.Conditions PriortoOccurrence Unit2inMode1,RTPat48percent(91330hourson7-15-86)DescritionofEventTechnical Specification 3.5.lbrequiresthateachaccumulator (EIIS/BP-TK) mustmaintainbetween929and971cubicfeetofboratedwaterwhiletheunitisinModes1-3(PowerOperation, Startup,andHotStandby,respectively).
Iftheaccumulator volumedeviatesfromtheprescribed limits,thevolumemustberestoredwithin1hourortheunitmustbeinhotshutdown(Mode4)withinthenext12hours.Processinstrumentation monitoring accumulator inventory (EIIS/BP-LIT) displayswatervolumeincubicfeet.Thesystemiscomprised of2indicators foreachaccumulator, onewiderange(300-1000cubicfeet)andonenarrowrange(900-1000cubicfeet).OnJuly15,1986,operators onshiftbecamesuspectoftheaccumulator 82volumeindication andrequested anultrasonic test(UT)beperformed toverifywaterinventory.
QualityControlpersonnel locatedthewaterlevelusingultrasound andthenmarked/dated thetankaccordingly; however,duringthisprocesstheirdatasheetbecamecontaminated andwasdiscarded beforeleavingaccesscontrol.Anewdatasheetwassubsequently filledoutfrommemoryandtheControlRoomwasinformedat1330hoursonJuly15thataccumulator
(/(2wasat115.75inches.Whenmathematically converted tovolume,thislevelcorresponds to969.58cubicfeet;which,bycoincidence only,happenedtocloselyagreewiththeprocessinstrumentation indication atthattime.OnJuly18,1986,at0800hoursanotherUTwasrequested foraccumulator
/!2becauseofquestionable volumeindication.
WhenQCarrivedataccumulator
(/'2theydiscovered a10incherrorwasmadeintheJuly15report.Thelevelwasactually105.75inches(909.58cubicfeet)onJuly15,andnot115.75(969.58cubicfeet)asreported.
Itcantherefore bededucedthatthelowerlimitforcontinued operation (929cubicfeet)hadbeenviolatedsinceatleastJuly15withouttheappropriate compensatory actionsbeingtaken.NRCFORMSBBA(EBSI*U.S.GPO:(BBB 0824538/455 NRCForm366A(84)3)LICENSEENTREPORT(LER)TEXTCONTINUANV.S.NUCLEARREGULATORY COMMISSION APPROVEOOMBNO.3(50-0104 EXPIRES:8/31/88FACILITYNAMEl()D.C.CookNuclearPlant-Unit2OOCKETNUMBER(2)31686LFRNUMBER(6)SEQUENTIAL NUMBER023REVISIONNUMBER020PAGE(3)OFTUCT(lmrsoEpsos/4rBEM)BI(,
BBB///orrr/HRC
/ronn36543)l17)DescritionofEvent(cont'd)Thiserrorwascompounded duringcommunications betweenQualityControlandOperations following theUTperformed themorningofJuly18.At0945hoursonthatmorning,QualityControlreportedthelevelofaccumulator f32hadrisen3inchessincethelasttestperformed onJuly15.Operations wasnotmadeawareofthe10incherrordiscovered earlier.Consequently, actingundertheimpression thataccumulator
((I2hadrisenfrom115.75inches(969.58cubicfeet)toavolumeexceeding theupperlimitingcondition forcontinued operation,'perations personnel declaredaccumulator 82inoperable baseduponhighlevel(itwasactuallylow)andmeasuresweretakentobegindrainingthetank.WithrespecttothevolumeincreasewhichoccurredsometimebetweenJuly15andJuly18,noconclusive evidencecanbeproducedconfirming thatsaidincreaseactuallyhappenedwithinasixhourtimespanpreceding boronsamplingperformed at0925hoursonJuly18.Therefore, theplantmustassumetheboronconcentration wasnotverifiedfollowing asolutionincrease>/1percentoftankvolumeasrequiredbyTechnical Specification 4.5.1b.Itshouldbenotedthatat0952hoursonJuly18,whilepreparations wereunderwayfordrainingaccumulator 82,Unit2trippedonasteamgenerator levelhigh-high signalthusplacingtheunitinMode3.Thiseventwasfurthercomplicated at1447hoursonJuly18whentheControlRoomwasinformedthatUTresultsplaced82accumulator's level3inchesbelowthelastmeasurement takenearlierthatmorning(duetodraining).
Withthisinformation, andstillunawareofthe10incherrormadeonJuly15,Operations declaredtheaccumulator operablebecausetheybelievedtheapparently highvolumeofwaterhadbeenreducedtowithinacceptable limitsforcontinued operation.
Inreality,theaccumulator volumewasdraineddownfromanalreadytoolowcondition toanevenlowerstatus.At1620hoursonJuly18,Operations becamecognizant ofthe10incherrormadeonJuly15.Itwasrecognized atthistimethataccumulator
$!2was,andhadbeensinceatleast1330hoursonJuly15,inviolation ofthelowervolumelimitrequiredbyTechnical Specification 3.5.1b.Accumulator
/f2wasimmediately declaredinoperable.
Coolingofthereactorcoolantsystem(EIIS/BP-AB) toachieveMode4beganat1720hoursandtheNRCwasnotifiedoftheeventbyphoneat1808hours.Effortstowardsfillingaccumulator f/2viatherefueling waterstoragetank(EIIS/BP-TK) commenced at1839hoursandtheeventwasterminated at2120hoursonJuly18whentheaccumulator volumeandboronconcentration wereverifiedtobewithinthelimitingcondition foroperation asdescribed inTechnical Specification 3.5.1band3.5.1crespectively.
CooldownwashaltedpriortoreachingMode4.Withtheexception oftheloop2accumulator volumeinstrumentation, therewerenoinoperable structures, systems,orcomponents atthestartofthiseventwhichcouldhavecontributed toitsoccurrence.
NRCFORM366A(()4)3)oU,S.GPO.1 9880824538/455 0<iII NRCForm388A(943)LICENSEENTREPORT(LER)TEXTCONTINUA~NU.S.NUCLEARREGULATORY COMMISSION APPROVEDOMSNO3150-0104 EXPIRES8/31/88FACILITYNAME(11DOCKETNUMBER(2)LERNUMBER(BlPAGE(3)D.C.CookNuclearFlant-Unit27%XT/4/m<<oNMoo/sIFEo8or/,
IrsoI/8/ooo/HRC R<<m35843/(17)osooo316YEAR@IrI86SEQUENTIAL NUMBER8rV023IIEVISION NUMSER0204OF07CauseofEventThecauseofthiseventhasbeenattributed totheinability oftheprocessinstrumentation toaccurately reflectthevolumewithinaccumulator 82,whichresultedintheneedforultrasonic testingtoverifyaccumulator operability.
Threedefective components withinthesystemwerediagnosed astherootcausefortheinstrumentation failure.theinstrumentation consistsofacircuitboard(EIIS/BP-ECBD),
straingauge(EIIS/BP-TD),
potentiometer span(EIIS/BP-EC),
potentiometer zero(EIIS/BP-EC) andanarrowrangedifferential pressureunit(DPU)(EIIS/BP-PIT).
Theinitialinvestigation indicated thatthe"zero"wasdrifting, whichresultsfromafaultycircuitboardandstraingauge.Subsequently, thesecomponents werereplaced.
Theinstrumentation subsequently zeroedproperly, butdatawasnotrepeatable vhenrangedupandbackdownthemeasurement scale.Asaresult,theDPUnarrowrangewasreplacedwhicheliminated therepeatability problem.Later,'he spanandzeropotentiometers verereplacedtoensureproperinstrumentation operation.
Thecalibrated instrument wasreturnedtoserviceonApril2,1987,andfunctioned normallyuntilApril26,atwhichtimethesystembegantoexhibitsignsofdriftingupwards.Ultrasonic measurements takenafterApril26confirmed theactualvolumewithinaccumulator f/2wassteadyandwellwithintheTechnical Specification allowable range,however,theresultsalsoconfirmed thatILA-121wascontinuing aslowbutsteadyupwarddrifttowardstheadministrative limitforoperability.
Asaprecautionary measure,ILA-121wasdeclaredinoperable at1328hoursonApril30,1987.Furtherinvestigation conducted duringtheSeptember 1987outageindicated thattherootcauseofthesecondinstrument failurewasafaultyDPUnarrowrange.TheDPUnarrowrangewasreplacedandthecalibrated instrument wasreturnedtoserviceonSeptember 24,1987.Theinstrument hassubsequently functioned normally.
Contributing tothiseventwasthefactthatQualityControlpersonnel whoperformed theoriginalUTonJuly15didnotimplement soundworkpractices whileconducting activities inaradioactive environment.
Thisresultedinthelossofhard.copydatasupporting testresultsforcingthoseinvolvedtorelysolelyuponmemoryrecall.ItshouldbenotedthattheUTwasperformed within-anextremely harshenvironment consisting ofelevatedtemperature andairborneradioactivity.
Theseadverseconditions complicated effortsofthetestcrewbecausefullfacemaskwasrequiredandthefatigueprocesswasaccelerated.
Inadequate communication betweentheControlRoomandQualityControlpersonnel furthercomplicated thisevent.Noformalmechanism hadbeenestablished toverifythatoperators onshifthadacompleteandaccurateunderstanding oftheUTresults.NRCFORMSBBA(948)*U.S.GPO:)988%.824 538/455 NRCForm366A(94)3)LICENSEENTREPORT(LER)TEXTCONTINUNU.S.NUCLEARREGULATORY COMMISSION APPROVEDOMBNO.3(9)&104EXPIRES:8/31/88FACILITYNAME(llDOCKETNUMBER(2)LERNUMBER(6)PAGE(3)D.C.CookNuclearPlant-Unit2TEXT/kmcY8<<>>48lrnr/I/EerE I/88T/I/or>>/HRC
%%dnn35549/(17)YEAR3168602302(jar,SEGVENTIAL jZ':REVISION49NUM88Rv>errNUMSER05OF07AnalsisofEventThiseventisreportable underthecriteriaof10CFR50.73(a)(2)(i) asdescribed below.-Forapproximately 3dayspriortoJuly18,1986,thevolumeofaccumulator 82wasbelowitslowerlimitingcondition foroperation andthecorresponding actionstatement associated withTechnical Specification 3.5.1bwasnotsatisfied.
-BetweenJuly15andJuly18,1986,accumulator 82experienced asolutionincreasegreater>/m1percentofthetankvolumeandtheboronconcentration wasnotverifiedtobeacceptable withinthenext6hoursasrequiredbyTechnical Specification 4.5.1b.Thesafetysignificance ofpoweroperation withaccumulator volumeofoneaccumulator at909.6cubicfeetratherthan929cubicfeetislimitedtoimpactontheloss-of-coolant accidentanalysis.
Thelimitingloss-of-coolant accidentanalysisforUnit2Cycle6predictsapeakcladtemperature of2079degreeFwitha121degreeFmargintothe2200degreeFlimitspecified in10CFR50.46.ExxonNuclearCompany,thefuelvendorforCycle6,wasrequested toevaluatetheimpactofthiseventonpublichealthandsafety.Theirresponsestated:itisExxon'sopinionthatasignificant safetyhazardtothepublicdidnotexistforthefollowing reason.Thelimitingcaseinthereference indicated apeakcladdingtemperature (PCT)of2079degreeFforoperation atlOOXpower.Operation at90percentpowerwouldresultinareduction inthePCTandwouldtendtooffsetanyincreaseinPCTduetothereducedaccumulator liquidvolume.Thereducedaccumulator liquidvolumealoneisexpectedtohaveaverysmalleffectonthePCT.Theaccumulator flowwouldendapproximately 1secondsoonerthanthetimeindicated inthereference.
Sincethisoccursafterthebeginning ofcorerecoverytime(BOCREC)whenthedowncomer isfull,averysmalladverseeffectonrefloodrateandPCTwouldoccurandwouldbemuchlessthanthe121degreeFmarginindicated inthereference."
Itisofnotethatthedifference betweentheas-foundcondition (909.6cubicfeet)andthevaluespecified intheTechnical Specification of929cubicfeetis19.4cubicfeet,orapproximately 960lbs.ofwater.Inordertoconservatively evaluatetheeffectonpeakcladtemperature, ahypothetical scenariowasevaluated inwhichitwasassumedthatthiswaterwasdeficient duringtherefillperiod,andhadtobemadeupbypumpedin5ection water.Itwouldhavetakenthepumpsapproximately 1.1secondstomakeupthiswater.SincethePCTrateofheatupduringtheearlyreflood/refill periodisabout13degree/sec.,
thiswouldhaveresultedinaPCTincreaseofabout15degreeF.Adding15degreeFtothecalculated PCTresultsinanewPCTof2094degreeF,whichisstillwellwithinthelimitsof10CFR50.46.NRCFORMSStA(94)3)8U.S.GPO:1986.0.624 538/455 NRCForm388A(943)L'ICENSEE NTREPORT(LER)TEXTCONTINUANU.S.NUCLEARREGULATORY COMMISSION APPROVEDOMSNO.3150M)84EXPIRES:8/31/88FACILITYNAME{1)DOCKETNUMBER(2)LERNUMBER(8)PACE(3)D.C.CookNuclearPlant-Unit2TEXT/Smroodraco/rorR/)or/,
I/44/8/orro/NRC Farm35(LE'4/(IT) 050003]YEARP~r~+86SEQUENTIAL gj<NUMBER023REVISIONNUMBER0206OFAnalsisofEvent(cont'd)Theactualchangeinpeakcladtemperature, hadanewanalysisbeenperformed, wouldhavebeenwellbelowtheabove15degreesFvaluebecausethedeficit,in waterwouldhaveoccurredafterthebeginning ofcorerecoverywhenheattransfermechanisms associated withrefloodwereinplace,andtheneedforaccumulator waterhadsignificantly lessened.
Itisalsoconcluded thatthemissedboronsurveillance wasnotofsignificance, sinceaboronsampletakenat0925hoursonJuly18contained aconcentration of1975partspermillion(ppm),whichiswellwithintherequiredlimitsof1900and2100ppm.Basedonalloftheaboveinformation, itisconcluded thattheeventdidnotconstitute anunreviewed safetyquestionasdefinedin10CFR50.59nordiditadversely impactpublichealthandsafety.Corrective ActionsImmediate corrective/preventative actionconsisted of:1)promptlyincreasing accumulator volumetowi.thinTechnical Specification limitsandverifying acceptable boronconcentration; and2)obtaining independently verifiedUTlevelindication, atleastonceevery10hours,toensureTechnical Specification compliance whiletheprocessinstrumentation was/isoutofservice.Longtermpreventative actionwillbetoreplacealloftheaccumulator levelinstrumentation withFoxboroinstrumentation assimilarproblemshavebeenexperienced withseveraloftheotherITT-Barton instruments.
Thereplacement isscheduled forUnit1duringitsscheduled 1989Refueling OutageandforUnit2duringitsnextscheduled refueling outagein1990.Thepersonnel responsible fortheinaccurate reportonJuly15havebeeninstructed intheappropriate methodsformaintaining cleanliness ofwrittendocuments whileinacontaminated environment, andtheimportance oftransmitting accurateinformation utilizedtoevaluateplantconditions.
Thesepersonshavesincedemonstrated thenecessary skillstopreventarecurrence ofthiseventduringactivities performed undersimilarcircumstances.
Toenhancetheeffectiveness ofcommunications betweenQualityControlandOperations personnel, thedatasheet(s)withintheultrasonic testprocedure havebeenrevisedtorequire:1)independent verification oftestresults;and2)UnitSupervisor/SRO reviewandsignature.
NRCFORM3BBA(943)*U.S.GPO.'(988 0824538/455 NRCFORR35BA(983)LICENSEENTREPORT(LER)TEXTCONTINUNU.S,NUCLEARREGULATORY COMMISSION APPROVEOOMBNO.3150&104EXPIRES:8/31/88FACILITYNAME(1)D.C.CookNuclearPlant-Unit2OOCKETNUMBER(2)osooo31686023-02LERNUMBER(6)YEAR~+.SEQVENTIAL
>y'EVISIONNUMBER.~%NUMBERPAGE(3)07QF07TEXTN/R/FBBP44B/4BqvlBI/IIFB//I/BIBBn/
HRC%%dnII35549/(17)FailedComonentIdentification Component:
EIIS:Manufacturer:
ModelNumber:CircuitBoardECBDITT-Barton 384Component:
EIIS:Manufacturer:
ModelNumber:StrainGaugeTDITT-Barton 386Component:
EIIS:Manufacturer:
ModelNumber:Differential PressureUnitPITITT-Barton 224-352PreviousSimilarEventsTherehavebeennosimilareventsinthepastwheretheplanthasfailedtomeettheactionstatement associated withaccumulator volumesbeingoutofspecification.
Also,theplanthasneverfailedinthepasttoverifyboronconcentration intheaccumulators within6hoursfollowing asolutionincreaseof>/J'percentoftankvolume.NRCFORMSBBA(94)3)*U.S.GPO:1985.O.B24 538/455 IndianaMichiganPower".ompanyCookNuclearPlanlP.O,Box458Bridgman.
MI491066164655901INDIANANICMIGANPOWERJune24,1988UnitedStatesNuclearRegulatory Commission DocumentControlDeskWashington, D.C.20555Operating LicenseDPR-58DocketNo.50-316DocumentControlManager:Inaccordance withthecriteriaestablished by10CFR50.73entitledLicenseeEventReortinSstem,thefollowing reportisbeingsubmitted:
86-023-02 Sincerely, W.G.Smith,Jr.PlantManagerWGS:clwAttachment cc:D.H.Williams, Jr.A.B.,Davis, RegionIIIM.P.AlexichP.A.BarrettH.B.BruggerR.W.Jurgensen NRCResidentInspector J.F.Stang,NRCR.C.CallenG.Charnoff, Esq.DottieSherman,ANILibraryD.HahnINPOPNSRCA.A.BlindS.J.Brewer/B.
P.Lauzau}}