Information Notice 1997-38, Level-Sensing System Initiates Common-Mode Faulure of High-Pressure-Injection Pumps: Difference between revisions
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{{#Wiki_filter:UNITED STATES | {{#Wiki_filter:UNITED STATES | ||
NUCLEAR REGULATORY COMMISSION | ===NUCLEAR REGULATORY COMMISSION=== | ||
OFFICE OF NUCLEAR REACTOR REGULATION | |||
WASHINGTON, D.C. 20555-0001 | |||
===June 24, 1997=== | |||
NRC INFORMATION NOTICE 97-38: LEVEL-SENSING SYSTEM INITIATES COMMON- | |||
MODE FAILURE OF HIGH-PRESSURE-INJECTION | |||
PUMPS | PUMPS | ||
| Line 71: | Line 73: | ||
was indicated. | was indicated. | ||
De4e NOrTLdE 1-0o3' | De4e NOrTLdE 1-0o3' | ||
970o6 4 U(WH)oLA | |||
.B~O~ 31O1 lMa | |||
c | |||
rz I | |||
- reP | |||
Undi aqquafac | Undi aqquafac | ||
@) | |||
IN 97-38 | |||
===June 24, 1997 Discussion=== | |||
The HPI pumps at Oconee perform the dual functions of RCS makeup and high-pressure | The HPI pumps at Oconee perform the dual functions of RCS makeup and high-pressure | ||
| Line 161: | Line 175: | ||
below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager. | below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager. | ||
Marylee M. Slosson, Acting Director | ===Marylee M. Slosson, Acting Director=== | ||
Division of Reactor Program Management | Division of Reactor Program Management | ||
Office of Nuclear Reactor Regulation | ===Office of Nuclear Reactor Regulation=== | ||
Technical contacts: Thomas Koshy, NRR | Technical contacts: Thomas Koshy, NRR | ||
301-415-1176 E-mail: txkenrc.gov | 301-415-1176 E-mail: txkenrc.gov | ||
Nick Fields, NRR | ===Nick Fields, NRR=== | ||
301-415-1173 E-mail: enfenrc.gov | 301-415-1173 E-mail: enfenrc.gov | ||
Attachment: List of Recently Issue | Attachment: List of Recently Issue | ||
4' | ===Information Notices=== | ||
4' | |||
ln.44 | |||
I | I | ||
| Line 184: | Line 197: | ||
IN 97-38 | IN 97-38 | ||
.June 24, 1997 LIST OF RECENTLY ISSUED | |||
NRC INFORMATION NOTICES | ===NRC INFORMATION NOTICES=== | ||
Information | |||
Date of | |||
Notice No. | Notice No. | ||
Subject | |||
Issuance | |||
Issued to | |||
97-37 | 96-53, Supp. 1 | ||
97-37 | |||
with Ensuing Oil Spill | ===Retrofit to Amersham 660=== | ||
Posilock Radiography | |||
Camera to Correct Incon- sistency in 10 CFR Part 34 | |||
===Compatibility=== | |||
Main Transformer Fault | |||
with Ensuing Oil Spill | |||
into Turbine Building | into Turbine Building | ||
97 | 06/23/97 | ||
06/20/97 | |||
===All industrial radiography=== | |||
licensees | |||
===All holders of OLs or CPs=== | |||
for nuclear power reactors | |||
97-36 | |||
97-35 | |||
97-34 | |||
===Unplanned Intakes by=== | |||
Worker of Transuranic | |||
===Airborne Radioactive=== | |||
Materials and External | |||
===Exposure Due to Inadequate=== | |||
Control of Work | Control of Work | ||
===Retrofit to Industrial=== | |||
Nuclear Company (INC) | |||
===IR100 Radiography Camera=== | |||
to Correct Inconsistency | |||
in 10 CFR Part 34 | |||
===Compatibility=== | |||
Deficiencies in Licensee | |||
===Submittals Regarding=== | |||
Terminology for Radio- logical Emergency Action | |||
===Levels in Accordance=== | |||
With the New Part 20 | |||
06/20/97 | |||
06/18/97 | |||
06/12/97 | |||
===All holders of OLs and CPs=== | |||
permits. All licensees of | |||
of nuclear power reactors | |||
in the decommissioning | |||
stage and fuel cycle | |||
===All industrial radiography=== | |||
licensees | |||
===All holders of OLs or CPs=== | |||
for test and research | |||
reactors | |||
OL = Operating License | OL = Operating License | ||
| Line 253: | Line 302: | ||
original signed by S.H. Weiss for | original signed by S.H. Weiss for | ||
Marylee M. Slosson, Acting Director | ===Marylee M. Slosson, Acting Director=== | ||
Division of Reactor Program Management | Division of Reactor Program Management | ||
Office of Nuclear Reactor Regulation | ===Office of Nuclear Reactor Regulation=== | ||
Technical contacts: | |||
Technical contacts: | |||
===Thomas Koshy, NRR=== | |||
301-415-1176 E-mail: txk@nrc.gov | 301-415-1176 E-mail: txk@nrc.gov | ||
Nick Fields, NRR | ===Nick Fields, NRR=== | ||
301-415-1173 E-mail: enf@nrc.gov | 301-415-1173 E-mail: enf@nrc.gov | ||
Attachment: List of Recently Issued NRC Information Notices | Attachment: List of Recently Issued NRC Information Notices | ||
Tech Editor has reviewed and concurred on 5/14197 DOCUMENT NAME: G:XNICKIOCONEE.IN | Tech Editor has reviewed and concurred on 5/14197 DOCUMENT NAME: G:XNICKIOCONEE.IN | ||
*SEE PREVIOUS CONCURRENCES | |||
To receive a co | |||
of this document. indicate In the box C=Coov wlo attachmentlendosure E=Coov with attachment/endosure N = No coy | |||
OFFICE | |||
Tech | |||
x | |||
HICB* | |||
x | |||
PECB* | |||
DRPM | |||
Contacts* | Contacts* | ||
NAME | |||
NFields | |||
JWermiel | |||
AChaffee | |||
MSlosson 5 | |||
___ __ | |||
__ | |||
TK oshy | |||
_ | |||
_ | |||
_ | |||
_ | |||
_ | |||
_ | |||
_ | |||
_ | |||
_ | |||
_ | |||
DATE | |||
06/09/97 | |||
06/09/97 | |||
06/12/97 V07 | |||
===OFFICIAL KRCORU COPY=== | |||
- | |||
I | I | ||
S . - | S | ||
. - | |||
-4 K- | |||
IN 97-xx | |||
June xx, 1997 This information notice requires no specific action or written response. If you have any | June xx, 1997 This information notice requires no specific action or written response. If you have any | ||
| Line 294: | Line 383: | ||
below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager. | below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager. | ||
Marylee M. Slosson, Acting Director | ===Marylee M. Slosson, Acting Director=== | ||
Division of Reactor Program Management | Division of Reactor Program Management | ||
Office of Nuclear Reactor Regulation | ===Office of Nuclear Reactor Regulation=== | ||
Technical contacts: Thomas Koshy, NRR | Technical contacts: Thomas Koshy, NRR | ||
301-415-1176 E-mail: txk@nrc.gov | 301-415-1176 E-mail: txk@nrc.gov | ||
Nick Fields, NRR | ===Nick Fields, NRR=== | ||
301-415-1173 E-mail: enfenrc.gov | 301-415-1173 E-mail: enfenrc.gov | ||
Attachment: List of Recently Issued NRC Information Notices | Attachment: List of Recently Issued NRC Information Notices | ||
DOCUMENT NAME: G:%NICKkOCONEE.IN | DOCUMENT NAME: G:%NICKkOCONEE.IN | ||
*SEE PREVIOUS CONCURRENCES | |||
To receive a conv of this document indicate in the box C=Coov wlo attachmentlenclosure E=Coov with attachmentlenclosure N = No copy | To receive a conv of this document indicate in the box C=Coov wlo attachmentlenclosure E=Coov with attachmentlenclosure N = No copy | ||
OFFICE | OFFICE | ||
Tech | |||
x | |||
HICB* | |||
l x | |||
PECB* | |||
DRPM | |||
Contacts* | |||
ll | |||
NAME | |||
NFields | |||
JWermiel | |||
AChaffee | |||
MSlosson | |||
TKoshy | TKoshy | ||
DATE | DATE | ||
06/09/97 | |||
06/09/97 | |||
06112/97 | |||
4/ /97 | |||
===OFFICIAL RECORD COPY=== | |||
~ | |||
6171k | |||
; | |||
I | |||
K'J | K'J | ||
| Line 330: | Line 447: | ||
IN 97-xx | IN 97-xx | ||
June xx, 1997 This information notice requires no specific action or written response. If you have any | |||
questions about information in this notice, please contact on6 of the technical contacts listed | questions about information in this notice, please contact on6 of the technical contacts listed | ||
| Line 336: | Line 453: | ||
below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager. | below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager. | ||
Marylee M. Slosson, Acting Director | ===Marylee M. Slosson, Acting Director=== | ||
Division of Reactor Program Management | Division of Reactor Program Management | ||
Office of Nuclear Reactor Regulation | ===Office of Nuclear Reactor Regulation=== | ||
Technical Contacts: Thomas Koshy, NRR | Technical Contacts: Thomas Koshy, NRR | ||
301-415-1176 e-mail:txk@nrc.gov | 301-415-1176 e-mail:txk@nrc.gov | ||
Nick Fields, NRR | ===Nick Fields, NRR=== | ||
301-415-1173 e-mail:enfenrc.gov | 301-415-1173 e-mail:enfenrc.gov | ||
Attachment: List of Recently Issued NRC Information Notices | Attachment: List of Recently Issued NRC Information Notices | ||
DOCUMENT NAME: G:\NICK\OCONEE.IN | DOCUMENT NAME: G:\\NICK\\OCONEE.IN | ||
To receive a copy of tis document, indicate in the box C=Copy wlo attachment/enclosure E=Copy with attachment/enclosure N = No copy | To receive a copy of tis document, indicate in the box C=Copy wlo attachment/enclosure E=Copy with attachment/enclosure N = No copy | ||
OFFICE | OFFICE | ||
Tech | |||
x | |||
HICB | |||
x | |||
PECB | |||
DRPM | |||
Contacts | |||
l | |||
4.5-A | |||
C)l | |||
NAME | |||
NFields AT | |||
JWermiel | |||
J | |||
A haffee | |||
MSlosson | |||
. | |||
TKoshyA | |||
UW | |||
P | |||
67 DATE | |||
61 | |||
/97 OF | |||
FICAL | |||
7 | |||
41 /97 OFFICIAL RECORD COPY}} | |||
{{Information notice-Nav}} | {{Information notice-Nav}} | ||
Latest revision as of 11:54, 16 January 2025
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C. 20555-0001
June 24, 1997
NRC INFORMATION NOTICE 97-38: LEVEL-SENSING SYSTEM INITIATES COMMON-
MODE FAILURE OF HIGH-PRESSURE-INJECTION
PUMPS
Addressees
All holders of operating licenses or construction permits for nuclear power reactors.
Purpose
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice to alert
addressees to a recent incident in which two high-pressure-injection (HPI) pumps were
damaged as a result of an inaccurate letdown storage tank (LDST) level-sensing system.
The inaccuracy was caused by a drained reference leg. As a result, an incorrect level was
displayed, permitting the pumps to take suction from an empty tank. It is expected that
recipients will review this information for applicability to their facilities and consider actions, as
appropriate. However, suggestions contained in this information notice are not NRC
requirements; therefore, no specific action or written response is required.
Descdrition of Circumstances
On May 3, 1997, the licensee for Oconee Unit 3 was conducting a planned shutdown to
inspect an HPI line. During cooldown of the plant, HPI pump 3B was operating in the reactor
coolant system (RCS) makeup mode. The pump's discharge pressure dropped to the "low'
pressure setpoint initiating the automatic start of standby HPI pump 3A. The operators later
secured pump 3A when reactor coolant pump (RCP) seal injection flow indicated "high". The
HPI header pressure decreased again. HPI pump 3A automatically restarted. The pump's
motor current began oscillating. The operators secured HPI pump 3B because of an
indication of low motor current. Shortly afterwards, HPI pump 3A was also secured when its
motor current decreased sharply. The licensee issued a Notification of an Unusual Event
because of the loss of two of the three HPI pumps.
The licensee later concluded that both HPI pumps became hydrogen bound and possibly
damaged when they took suction from an empty LDST even though adequate tank inventory
was indicated.
De4e NOrTLdE 1-0o3'
970o6 4 U(WH)oLA
.B~O~ 31O1 lMa
c
rz I
- reP
Undi aqquafac
@)
June 24, 1997 Discussion
The HPI pumps at Oconee perform the dual functions of RCS makeup and high-pressure
safety injection. These pumps normally take suction from the LDST (also referred to as the
makeup or volume control tank by other vendors). A 25-psi (172.4 kPa) hydrogen
overpressure is maintained in this tank to scavenge oxygen from the RCS.
During this event, two level transmitters monitored tank level. These transmitters produce
level alarms in the control room. The alarms alert operators to initiate makeup to the LDST.
Both level transmitters shared a common reference leg. Because the shared reference leg
was partially drained, the indicated letdown tank level remained at 9 inches above the
low-level alarm setpoint. The tank was actually empty, its contents having been depleted
during normal charging. Letdown tank level was investigated only after both HPI pumps
developed problems.
Indicated level in the control room was derived from the equivalent pressure difference
between the drained reference leg and the back pressure from the 25 psi hydrogen
overpressure in the LDST. Because both level instruments shared the common reference
leg, both gave the same erroneous indication. Therefore, operators failed to provide makeup
inventory to the LDST. Two of the three HPI pumps became gas-bound, cavitated, and, as a
result, were structurally damaged.
If an actual safety injection actuation occurs, the suction isolation valve to the LDST remains
open while the suction isolation valve to the borated water storage tank (BWST) opens on the
safety injection signal. All three HPI pumps receive a start signal and take suction on both
the LDST and the BWST. With the two tanks cross-tied, the potential existed for this event to
have caused the loss of all HPI pumps as a result of gas binding. Loss of all three HPI
pumps could prevent the successful mitigation of a loss of coolant accident. During normal
operations, loss of all HPI pumps would result in the loss of reactor coolant pump seal
injection, normal RCS makeup, and normal boration.
The level transmitters were last calibrated in February 1997. Sometime between that last
calibration and the event, a leak developed from a scored cap on a test connection that
drained the reference leg. The cap was used to isolate the test connection. A drained
reference leg or a reference leg with entrained air can result in incorrect level indication.
Incorrect level indication will prevent appropriate setpoints being reached when process
conditions demand, defeat critical automatic safety functions, and could mislead plant
operators into taking less than conservative actions.
Pressure and level sensors, in any safety-related application, that rely on a reference leg for
a differential pressure reading, are sensitive to changes in reference leg level. Normal
surveillances that Include only channel checks with other instruments sharing the reference
leg or transmitter calibrations with external hydrostatic test sets will not reveal the true
condition of the reference leg. In the absence of an automatic reference leg fill system, periodic verification of reference leg level based on the plant-specific environment is needed
to ensure the operational integrity of the critical systems that are relied upon for manual and
automatic functions.
IN 97-38 June 24, 1997 This information notice requires no specific action or written response. If you have any
questions about information in this notice, please contact one of the technical contacts listed
below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
Marylee M. Slosson, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical contacts: Thomas Koshy, NRR
301-415-1176 E-mail: txkenrc.gov
Nick Fields, NRR
301-415-1173 E-mail: enfenrc.gov
Attachment: List of Recently Issue
Information Notices
4'
ln.44
I
Attachment
.June 24, 1997 LIST OF RECENTLY ISSUED
NRC INFORMATION NOTICES
Information
Date of
Notice No.
Subject
Issuance
Issued to
96-53, Supp. 1
97-37
Retrofit to Amersham 660
Posilock Radiography
Camera to Correct Incon- sistency in 10 CFR Part 34
Compatibility
Main Transformer Fault
with Ensuing Oil Spill
into Turbine Building
06/23/97
06/20/97
All industrial radiography
licensees
All holders of OLs or CPs
for nuclear power reactors
97-36
97-35
97-34
Unplanned Intakes by
Worker of Transuranic
Airborne Radioactive
Materials and External
Exposure Due to Inadequate
Control of Work
Retrofit to Industrial
Nuclear Company (INC)
IR100 Radiography Camera
to Correct Inconsistency
Compatibility
Deficiencies in Licensee
Submittals Regarding
Terminology for Radio- logical Emergency Action
Levels in Accordance
With the New Part 20
06/20/97
06/18/97
06/12/97
All holders of OLs and CPs
permits. All licensees of
of nuclear power reactors
in the decommissioning
stage and fuel cycle
All industrial radiography
licensees
All holders of OLs or CPs
for test and research
reactors
OL = Operating License
CP = Construction Permit
I
KU
IN 97-38 June 24, 1997 This information notice requires no specific action or written response. If you have any
questions about information in this notice, please contact one of the technical contacts listed
below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
original signed by S.H. Weiss for
Marylee M. Slosson, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical contacts:
Thomas Koshy, NRR
301-415-1176 E-mail: txk@nrc.gov
Nick Fields, NRR
301-415-1173 E-mail: enf@nrc.gov
Attachment: List of Recently Issued NRC Information Notices
Tech Editor has reviewed and concurred on 5/14197 DOCUMENT NAME: G:XNICKIOCONEE.IN
- SEE PREVIOUS CONCURRENCES
To receive a co
of this document. indicate In the box C=Coov wlo attachmentlendosure E=Coov with attachment/endosure N = No coy
OFFICE
Tech
x
HICB*
x
PECB*
DRPM
Contacts*
NAME
NFields
JWermiel
AChaffee
MSlosson 5
___ __
__
TK oshy
_
_
_
_
_
_
_
_
_
_
DATE
06/09/97
06/09/97
06/12/97 V07
OFFICIAL KRCORU COPY
-
I
S
. -
-4 K-
IN 97-xx
June xx, 1997 This information notice requires no specific action or written response. If you have any
questions about information in this notice, please contact one of the technical contacts listed
below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
Marylee M. Slosson, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical contacts: Thomas Koshy, NRR
301-415-1176 E-mail: txk@nrc.gov
Nick Fields, NRR
301-415-1173 E-mail: enfenrc.gov
Attachment: List of Recently Issued NRC Information Notices
DOCUMENT NAME: G:%NICKkOCONEE.IN
- SEE PREVIOUS CONCURRENCES
To receive a conv of this document indicate in the box C=Coov wlo attachmentlenclosure E=Coov with attachmentlenclosure N = No copy
OFFICE
Tech
x
HICB*
l x
PECB*
DRPM
Contacts*
ll
NAME
NFields
JWermiel
AChaffee
MSlosson
TKoshy
DATE
06/09/97
06/09/97
06112/97
4/ /97
OFFICIAL RECORD COPY
~
6171k
I
K'J
IN 97-xx
June xx, 1997 This information notice requires no specific action or written response. If you have any
questions about information in this notice, please contact on6 of the technical contacts listed
below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
Marylee M. Slosson, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical Contacts: Thomas Koshy, NRR
301-415-1176 e-mail:txk@nrc.gov
Nick Fields, NRR
301-415-1173 e-mail:enfenrc.gov
Attachment: List of Recently Issued NRC Information Notices
DOCUMENT NAME: G:\\NICK\\OCONEE.IN
To receive a copy of tis document, indicate in the box C=Copy wlo attachment/enclosure E=Copy with attachment/enclosure N = No copy
OFFICE
Tech
x
HICB
x
PECB
DRPM
Contacts
l
4.5-A
C)l
NAME
NFields AT
JWermiel
J
A haffee
MSlosson
.
TKoshyA
UW
P
67 DATE
61
/97 OF
FICAL
7
41 /97 OFFICIAL RECORD COPY