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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES  
                            NUCLEAR REGULATORY COMMISSION
NUCLEAR REGULATORY COMMISSION  
                                              REGION III
REGION III  
                                2443 WARRENVILLE ROAD, SUITE 210
2443 WARRENVILLE ROAD, SUITE 210  
                                        LISLE, IL 60532-4352
LISLE, IL 60532-4352  
                                        February 10, 2010
Mr. Charles G. Pardee
Senior Vice President, Exelon Generation Company, LLC
February 10, 2010  
President and Chief Nuclear Officer (CNO), Exelon Nuclear
4300 Winfield Road
Warrenville, IL 60555
SUBJECT:       DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3
Mr. Charles G. Pardee  
                INTEGRATED INSPECTION REPORT 05000237/2009-005;
Senior Vice President, Exelon Generation Company, LLC  
                05000249/2009-005
President and Chief Nuclear Officer (CNO), Exelon Nuclear  
Dear Mr. Pardee:
4300 Winfield Road  
On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an
Warrenville, IL 60555  
integrated inspection at your Dresden Nuclear Power Station, Units 2 and 3. The enclosed
report documents the inspection results, which were discussed on January 14, 2010, with
SUBJECT:  
Mr. T. Hanley and other members of your staff.
DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3  
The inspection examined activities conducted under your license as they relate to safety and
INTEGRATED INSPECTION REPORT 05000237/2009-005;  
compliance with the Commissions rules and regulations and with the conditions of your license.
05000249/2009-005  
The inspectors reviewed selected procedures and records, observed activities, and interviewed
Dear Mr. Pardee:  
personnel.
On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an  
The report documents two NRC-identified findings and five self-revealed findings of very low
integrated inspection at your Dresden Nuclear Power Station, Units 2 and 3. The enclosed  
safety significance (Green). All of these findings were determined to involve a violation of
report documents the inspection results, which were discussed on January 14, 2010, with  
NRC requirements. Additionally, one licensee-identified violation is listed in Section 4OA7 of
Mr. T. Hanley and other members of your staff.  
this report. However, because of the very low safety significance and because they are entered
The inspection examined activities conducted under your license as they relate to safety and  
into your corrective action program, the NRC is treating these findings as non-cited violations
compliance with the Commissions rules and regulations and with the conditions of your license.
(NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy.
The inspectors reviewed selected procedures and records, observed activities, and interviewed  
If you contest any NCV, you should provide a response within 30 days of the date of this
personnel.  
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
The report documents two NRC-identified findings and five self-revealed findings of very low  
ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional
safety significance (Green). All of these findings were determined to involve a violation of  
Administrator, Region III; 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352, the Director,
NRC requirements. Additionally, one licensee-identified violation is listed in Section 4OA7 of  
Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and
this report. However, because of the very low safety significance and because they are entered  
the NRC Resident Inspector at Dresden. In addition, if you disagree with the characterization of
into your corrective action program, the NRC is treating these findings as non-cited violations  
any finding in this report, you should provide a response within 30 days of the date of this
(NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy.  
inspection report, with the basis for your disagreement, to the Regional Administrator,
If you contest any NCV, you should provide a response within 30 days of the date of this  
Region III, and the NRC Resident Inspector at Dresden. The information you provide will be
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,  
considered in accordance with Inspection Manual Chapter 0305.
ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional  
Administrator, Region III; 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352, the Director,  
Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and  
the NRC Resident Inspector at Dresden. In addition, if you disagree with the characterization of  
any finding in this report, you should provide a response within 30 days of the date of this  
inspection report, with the basis for your disagreement, to the Regional Administrator,  
Region III, and the NRC Resident Inspector at Dresden. The information you provide will be  
considered in accordance with Inspection Manual Chapter 0305.  


C. Pardee                                   -2-
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its
enclosure, and your response (if any) will be made available electronically for public inspection
in the NRC Public Document Room or from the Publicly Available Records (PARS) component
C. Pardee  
of NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                            Sincerely,
                                            /RA/
                                            Mark A. Ring, Chief
-2-  
                                            Branch 1
                                            Division of Reactor Projects
Docket Nos. 50-237; 50-249
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its  
License Nos. DPR-19; DPR-25
enclosure, and your response (if any) will be made available electronically for public inspection  
Enclosure:     Inspection Report 05000237/2009-005; 05000249/2009-005
in the NRC Public Document Room or from the Publicly Available Records (PARS) component  
                w/Attachment: Supplemental Information
of NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at  
cc w/encl:     Distribution via ListServ
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
Sincerely,  
/RA/  
Mark A. Ring, Chief  
Branch 1  
Division of Reactor Projects  
Docket Nos. 50-237; 50-249  
License Nos. DPR-19; DPR-25  
Enclosure:  
Inspection Report 05000237/2009-005; 05000249/2009-005  
  w/Attachment: Supplemental Information  
cc w/encl:  
Distribution via ListServ  


          U.S. NUCLEAR REGULATORY COMMISSION
                          REGION III
Enclosure
Docket Nos:         50-237; 50-249
U.S. NUCLEAR REGULATORY COMMISSION  
License Nos:       DPR-19; DPR-25
REGION III  
Report No:         05000237/2009-005; 05000249/2009-005
Docket Nos:  
Licensee:           Exelon Generation Company
50-237; 50-249  
Facility:           Dresden Nuclear Power Station, Units 2 and 3
License Nos:  
Location:           Morris, IL
DPR-19; DPR-25  
Dates:             October 1 through December 31, 2009
Report No:  
Inspectors:         C. Phillips, Senior Resident Inspector
05000237/2009-005; 05000249/2009-005  
                    D. Meléndez-Colón, Resident Inspector
Licensee:  
                    J. Benjamin, Project Engineer
Exelon Generation Company  
                    J. Draper, Reactor Engineer
Facility:  
                    D. Sand, Reactor Engineer
Dresden Nuclear Power Station, Units 2 and 3  
                    C. Moore, Operations Engineer
Location:  
                    F. Ramírez, Resident Inspector, LaSalle Station
Morris, IL  
                    J. McGhee, Senior Resident Inspector, Quad Cities
Dates:  
                    M. Holmberg, Reactor Inspector
October 1 through December 31, 2009  
                    M. Mitchell, Health Physicist
Inspectors:  
                    R. Jickling, Senior Emergency Preparedness Inspector
C. Phillips, Senior Resident Inspector  
                    L. Kozak, Senior Reactor Analyst
Approved by:       M. Ring, Chief
D. Meléndez-Colón, Resident Inspector  
                    Projects Branch 1
                    Division of Reactor Projects
J. Benjamin, Project Engineer  
                                                                    Enclosure
J. Draper, Reactor Engineer  
D. Sand, Reactor Engineer  
C. Moore, Operations Engineer  
F. Ramírez, Resident Inspector, LaSalle Station  
J. McGhee, Senior Resident Inspector, Quad Cities  
M. Holmberg, Reactor Inspector  
M. Mitchell, Health Physicist  
R. Jickling, Senior Emergency Preparedness Inspector  
L. Kozak, Senior Reactor Analyst  
Approved by:
M. Ring, Chief  
Projects Branch 1  
Division of Reactor Projects


                                        TABLE OF CONTENTS
SUMMARY OF FINDINGS ...........................................................................................................1
Enclosure
REPORT DETAILS .......................................................................................................................6
TABLE OF CONTENTS  
Summary of Plant Status...........................................................................................................6
SUMMARY OF FINDINGS ...........................................................................................................1  
  1.   REACTOR SAFETY .......................................................................................................6
REPORT DETAILS.......................................................................................................................6  
      1R04   Equipment Alignment (71111.04) ......................................................................6
Summary of Plant Status...........................................................................................................6  
      1R05   Fire Protection (71111.05) .................................................................................9
1.  
      1R08   Inservice Inspection Activities (71111.08G).....................................................10
REACTOR SAFETY .......................................................................................................6  
      1R11   Licensed Operator Requalification Program (71111.11) .................................11
1R04  
      1R12   Maintenance Effectiveness (71111.12) ...........................................................12
Equipment Alignment (71111.04) ......................................................................6  
      1R13   Maintenance Risk Assessments and Emergent Work Control (71111.13)......13
1R05  
      1R15   Operability Evaluations (71111.15)..................................................................13
Fire Protection (71111.05).................................................................................9  
      1R19   Post-Maintenance Testing (71111.19).............................................................16
1R08  
      1R20   Outage Activities (71111.20) ...........................................................................19
Inservice Inspection Activities (71111.08G).....................................................10  
      1R22   Surveillance Testing (71111.22) ......................................................................22
1R11  
      1EP4   Emergency Action Level and Emergency Plan Changes (71114.04)..............25
Licensed Operator Requalification Program (71111.11) .................................11  
  2.   RADIATION SAFETY ...................................................................................................27
1R12  
      2OS1   Access Control to Radiologically Significant Areas (71121.01) .......................27
Maintenance Effectiveness (71111.12) ...........................................................12  
      2OS2   As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)..........28
1R13  
  4.   OTHER ACTIVITIES.....................................................................................................29
Maintenance Risk Assessments and Emergent Work Control (71111.13)......13  
      4OA1   Performance Indicator (PI) Verification (71151) ..............................................29
1R15  
      4OA2   Identification and Resolution of Problems (71152) ..........................................30
Operability Evaluations (71111.15)..................................................................13  
      4OA3   Follow-Up of Events and Notices of Enforcement Discretion (71153).............34
1R19  
      4OA5   Other Activities.................................................................................................42
Post-Maintenance Testing (71111.19).............................................................16  
      4OA6   Management Meetings ....................................................................................44
1R20  
      4OA7   Licensee-Identified Violations ..........................................................................44
Outage Activities (71111.20) ...........................................................................19  
SUPPLEMENTAL INFORMATION ...............................................................................................1
1R22  
KEY POINTS OF CONTACT.....................................................................................................1
Surveillance Testing (71111.22)......................................................................22  
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED ........................................................2
1EP4  
LIST OF DOCUMENTS REVIEWED.........................................................................................4
Emergency Action Level and Emergency Plan Changes (71114.04)..............25  
LIST OF ACRONYMS USED ..................................................................................................10
2.  
                                                                                                                        Enclosure
RADIATION SAFETY ...................................................................................................27  
2OS1  
Access Control to Radiologically Significant Areas (71121.01).......................27  
2OS2  
As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)..........28  
4.  
OTHER ACTIVITIES.....................................................................................................29  
4OA1  
Performance Indicator (PI) Verification (71151) ..............................................29  
4OA2  
Identification and Resolution of Problems (71152)..........................................30  
4OA3  
Follow-Up of Events and Notices of Enforcement Discretion (71153).............34  
4OA5  
Other Activities.................................................................................................42  
4OA6  
Management Meetings ....................................................................................44  
4OA7  
Licensee-Identified Violations..........................................................................44  
SUPPLEMENTAL INFORMATION ...............................................................................................1  
KEY POINTS OF CONTACT.....................................................................................................1  
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED ........................................................2  
LIST OF DOCUMENTS REVIEWED.........................................................................................4  
LIST OF ACRONYMS USED ..................................................................................................10  


                                      SUMMARY OF FINDINGS
IR 05000237/2009-005, 05000249/2009-005; 10/01/2009 - 12/31/2009; Dresden Nuclear Power
Station, Units 2 & 3; Equipment Alignment, Operability Evaluations, Post-Maintenance Testing,
1
Surveillance Testing, Outage, and Event Follow-up.
Enclosure
This report covers a three-month period of inspection by resident inspectors and announced
SUMMARY OF FINDINGS  
baseline inspections by regional inspectors. Two Green findings were identified by the
IR 05000237/2009-005, 05000249/2009-005; 10/01/2009 - 12/31/2009; Dresden Nuclear Power  
inspectors and five findings were self-revealed. All of the findings were considered Non-Cited
Station, Units 2 & 3; Equipment Alignment, Operability Evaluations, Post-Maintenance Testing,  
Violations (NCVs) of NRC regulations. The significance of most findings is indicated by their
Surveillance Testing, Outage, and Event Follow-up.  
color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,
This report covers a three-month period of inspection by resident inspectors and announced  
Significance Determination Process (SDP). Cross-cutting aspects were determined using
baseline inspections by regional inspectors. Two Green findings were identified by the  
IMC 0305, "Operating Reactor Assessment Program." Findings for which the SDP does not
inspectors and five findings were self-revealed. All of the findings were considered Non-Cited  
apply may be Green or be assigned a severity level after NRC management review. The NRCs
Violations (NCVs) of NRC regulations. The significance of most findings is indicated by their  
program for overseeing the safe operation of commercial nuclear power reactors is described in
color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,  
NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.
Significance Determination Process (SDP). Cross-cutting aspects were determined using  
A.     NRC-Identified and Self-Revealed Findings
IMC 0305, "Operating Reactor Assessment Program." Findings for which the SDP does not  
        Cornerstone: Initiating Events
apply may be Green or be assigned a severity level after NRC management review. The NRCs  
    *   Green. A self-revealed finding involving a non-cited violation (NCV) of Technical
program for overseeing the safe operation of commercial nuclear power reactors is described in  
        Specification 5.4.1 was identified on October 3, 2009, due to the licensees failure to
NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.  
        include essential information in DOP 1200-03, RWCU System Operation with the
A.  
        Reactor at Pressure, Revision 51, regarding startup of the reactor water cleanup system
NRC-Identified and Self-Revealed Findings  
        with the reactor at pressure. This procedural deficiency caused a pressure pulse that
Cornerstone: Initiating Events  
        resulted in a reactor water level Low-Low Group 1 Isolation Signal and Unit 3 reactor
*  
        scram. This event was entered into the licensees corrective action program (CAP) as
Green. A self-revealed finding involving a non-cited violation (NCV) of Technical  
        Issue Report (IR) 974426. Corrective actions by the licensee included revising
Specification 5.4.1 was identified on October 3, 2009, due to the licensees failure to  
        procedure DOP 1200-03.
include essential information in DOP 1200-03, RWCU System Operation with the  
        This finding was considered more than minor because it affected the Initiating Events
Reactor at Pressure, Revision 51, regarding startup of the reactor water cleanup system  
        Cornerstone objective to limit the likelihood of those events that upset plant stability and
with the reactor at pressure. This procedural deficiency caused a pressure pulse that  
        challenge critical safety functions during shutdown as well as at power operations.
resulted in a reactor water level Low-Low Group 1 Isolation Signal and Unit 3 reactor  
        The finding was determined to be of very low safety significance because it did not
scram. This event was entered into the licensees corrective action program (CAP) as  
        contribute to both the likelihood of a reactor trip AND the likelihood that mitigating
Issue Report (IR) 974426. Corrective actions by the licensee included revising  
        equipment or functions will not be available. This finding has a cross-cutting aspect in
procedure DOP 1200-03.  
        the area of Human Performance (Resources) because the licensee did not provide
This finding was considered more than minor because it affected the Initiating Events  
        complete, accurate and up-to-date procedures to plant personnel.
Cornerstone objective to limit the likelihood of those events that upset plant stability and  
        H.2(c) (Section 4OA3.2)
challenge critical safety functions during shutdown as well as at power operations.
        Cornerstone: Mitigating Systems
The finding was determined to be of very low safety significance because it did not  
    *   Green. A finding of very low safety significance and associated NCV of Technical
contribute to both the likelihood of a reactor trip AND the likelihood that mitigating  
        Specification 5.4.1 was self-revealed for the failure to meet the requirements of
equipment or functions will not be available. This finding has a cross-cutting aspect in  
        Clearance Order (CO) 69631 by removing shorting links instead of fuses as required by
the area of Human Performance (Resources) because the licensee did not provide  
        the CO on November 12, 2009. As a result, protective relaying was unintentially
complete, accurate and up-to-date procedures to plant personnel.
        removed from the Unit 2 main power transformer TR-2, the unit auxiliary transformer
H.2(c) (Section 4OA3.2)  
        TR-21, and the reserve auxiliary transformer TR-22. This issue was entered into the
Cornerstone: Mitigating Systems  
        licensees CAP as Issue Report 992290. Corrective actions included: coaching of the
*  
        individuals involved with the incorrect placing of the out-of-service and a placard on the
Green. A finding of very low safety significance and associated NCV of Technical  
                                                      1                                    Enclosure
Specification 5.4.1 was self-revealed for the failure to meet the requirements of  
Clearance Order (CO) 69631 by removing shorting links instead of fuses as required by  
the CO on November 12, 2009. As a result, protective relaying was unintentially  
removed from the Unit 2 main power transformer TR-2, the unit auxiliary transformer  
TR-21, and the reserve auxiliary transformer TR-22. This issue was entered into the  
licensees CAP as Issue Report 992290. Corrective actions included: coaching of the  
individuals involved with the incorrect placing of the out-of-service and a placard on the  


  device that was incorrectly repositioned was changed to include the specific equipment
  part number of the shorting links.
  The finding was determined to be more than minor because the finding could reasonably
2
  be viewed as a precursor to a significant event. The finding was evaluated using the
Enclosure
  SDP in accordance with IMC 0609, Appendix G, Attachment 1, Shutdown Operations
device that was incorrectly repositioned was changed to include the specific equipment  
  Significance Determination Process Phase 1 Operational Checklists For Both PWRs and
part number of the shorting links.  
  BWRs, Checklist 6, dated May 25, 2004. This checklist stated that for a finding to
The finding was determined to be more than minor because the finding could reasonably  
  require a Phase 2 or 3 determination, it would require an increase in the likelihood of a
be viewed as a precursor to a significant event. The finding was evaluated using the  
  loss of offsite power or degrade the licensees ability to cope with a loss of offsite power.
SDP in accordance with IMC 0609, Appendix G, Attachment 1, Shutdown Operations  
  The ability of the licensee to cope with a loss of offsite power was not impacted because
Significance Determination Process Phase 1 Operational Checklists For Both PWRs and  
  at least one emergency diesel generator was operable during the entire period. The
BWRs, Checklist 6, dated May 25, 2004. This checklist stated that for a finding to  
  inspectors determined that neither of these conditions were met so the finding screened
require a Phase 2 or 3 determination, it would require an increase in the likelihood of a  
  as Green. This finding had a cross-cutting aspect in the area of Human Performance,
loss of offsite power or degrade the licensees ability to cope with a loss of offsite power.
  Work Practices. H.4(a) (Section 1R04)
The ability of the licensee to cope with a loss of offsite power was not impacted because  
* Green. The inspectors identified a finding of very low safety significance and associated
at least one emergency diesel generator was operable during the entire period. The  
  NCV of Technical Specification 5.4.1 for the licensee failing to follow Dresden procedure
inspectors determined that neither of these conditions were met so the finding screened  
  DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39. On
as Green. This finding had a cross-cutting aspect in the area of Human Performance,  
  September 24, 2009, the inspectors identified valve 2-1501-42A, U2 low pressure
Work Practices. H.4(a) (Section 1R04)  
  coolant injection (LPCI) A pump gland leak-off valve, was closed instead of open as
*  
  required by DOP 2-1500-M1. With this valve closed instead of open, the control room
Green. The inspectors identified a finding of very low safety significance and associated  
  alarm for LPCI pump seal leakage would not have been able to fulfill its function.
NCV of Technical Specification 5.4.1 for the licensee failing to follow Dresden procedure  
  The issue was entered into the licensees CAP as IR 969490. The licensees corrective
DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39. On  
  actions included changing maintenance procedure DMP 1500-05, LPCI Pump
September 24, 2009, the inspectors identified valve 2-1501-42A, U2 low pressure  
  Maintenance, step G.25.d to include the case drain valve equipment numbers and sign
coolant injection (LPCI) A pump gland leak-off valve, was closed instead of open as  
  offs to position and verify the valves; and Operations Department Management
required by DOP 2-1500-M1. With this valve closed instead of open, the control room  
  addressed the operations department personnel about this issue.
alarm for LPCI pump seal leakage would not have been able to fulfill its function.
  The finding was determined to be more than minor because the finding, if left
The issue was entered into the licensees CAP as IR 969490. The licensees corrective  
  uncorrected, would become a more significant safety concern. Specifically, the valve
actions included changing maintenance procedure DMP 1500-05, LPCI Pump  
  isolated an alarm in the control room. The inspectors concluded this finding was
Maintenance, step G.25.d to include the case drain valve equipment numbers and sign  
  associated with the Mitigating Systems Cornerstone using IMC 0609, Significance
offs to position and verify the valves; and Operations Department Management  
  Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and
addressed the operations department personnel about this issue.  
  Characterization of Findings, Table 4a, dated January 10, 2008. This finding has a
The finding was determined to be more than minor because the finding, if left  
  cross-cutting aspect in the area of Human Performance, Work Practices because the
uncorrected, would become a more significant safety concern. Specifically, the valve  
  licensee did not have any documentation as to how or when the valve was placed into
isolated an alarm in the control room. The inspectors concluded this finding was  
  the position it was in. The design and location of the valve precluded that the valve was
associated with the Mitigating Systems Cornerstone using IMC 0609, Significance  
  accidently placed into the position it was found in. Therefore, the inspectors concluded
Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and  
  that either the failure to use human error prevention techniques or maintaining proper
Characterization of Findings, Table 4a, dated January 10, 2008. This finding has a  
  documentation of activities caused the mispositioning of valve 2-1501-42A.
cross-cutting aspect in the area of Human Performance, Work Practices because the  
  H.4.(a) (Section 1R15)
licensee did not have any documentation as to how or when the valve was placed into  
* Green. The inspectors identified a finding of very low significance and associated
the position it was in. The design and location of the valve precluded that the valve was  
  NCV of 10 CFR 50 Appendix B, Criterion XI, Test Control, because the licensee
accidently placed into the position it was found in. Therefore, the inspectors concluded  
  unacceptably preconditioned the Unit 2 Emergency Diesel Generator (EDG) prior to
that either the failure to use human error prevention techniques or maintaining proper  
  performing Technical Specification (TS) Surveillance Requirements (SR) 3.8.1.19.c.4,
documentation of activities caused the mispositioning of valve 2-1501-42A.
  3.8.1.12.c.3, and 3.8.1.10. These TS SRs involved verifying that the EDG supplied
H.4.(a) (Section 1R15)  
  steady state frequency would be acceptable following a loss of offsite power coincident
*  
  with and without a loss of coolant accident, and following the loss of the largest
Green. The inspectors identified a finding of very low significance and associated  
  post-accident load. Specifically, the inspectors identified that the licensee routinely
NCV of 10 CFR 50 Appendix B, Criterion XI, Test Control, because the licensee  
                                                2                                    Enclosure
unacceptably preconditioned the Unit 2 Emergency Diesel Generator (EDG) prior to  
performing Technical Specification (TS) Surveillance Requirements (SR) 3.8.1.19.c.4,  
3.8.1.12.c.3, and 3.8.1.10. These TS SRs involved verifying that the EDG supplied  
steady state frequency would be acceptable following a loss of offsite power coincident  
with and without a loss of coolant accident, and following the loss of the largest  
post-accident load. Specifically, the inspectors identified that the licensee routinely  


  performed governor oil change outage maintenance activities which involved a section
  that tuned the Unit 2 diesel governors response to a load change just prior to performing
  these TS SRs. This issue has been entered into the licensees CAP as IR 1000609.
3
  The licensee had not reached a conclusion on corrective actions by the end of the
Enclosure
  inspection period.
performed governor oil change outage maintenance activities which involved a section  
  This finding was determined to be more than minor because the finding, if left
that tuned the Unit 2 diesel governors response to a load change just prior to performing  
  uncorrected, would become a more significant safety concern. Unacceptable
these TS SRs. This issue has been entered into the licensees CAP as IR 1000609.
  preconditioning the EDG could mask latent performance issues and affect the ability of
The licensee had not reached a conclusion on corrective actions by the end of the  
  the EDG to supply safety-related power to vital loads during an event. The inspectors
inspection period.  
  performed a Phase 1 SDP evaluation and determined that this issue was Green
This finding was determined to be more than minor because the finding, if left  
  because it did not result in an inoperable Unit 2 EDG. The failure to adequately
uncorrected, would become a more significant safety concern. Unacceptable  
  coordinate the work activity of the preventive maintenance and post-maintenance testing
preconditioning the EDG could mask latent performance issues and affect the ability of  
  with the TS SR activities was the principal contributor to this finding and was reflective of
the EDG to supply safety-related power to vital loads during an event. The inspectors  
  recent performance. This finding had a cross-cutting aspect in the area of Work Control.
performed a Phase 1 SDP evaluation and determined that this issue was Green  
  Specifically, the licensee did not appropriately coordinate work activities by incorporating
because it did not result in an inoperable Unit 2 EDG. The failure to adequately  
  actions to address the impact of the work as different job activities. The scheduling of
coordinate the work activity of the preventive maintenance and post-maintenance testing  
  the work activities resulted in the pre-conditioning of the EDG prior to performing the
with the TS SR activities was the principal contributor to this finding and was reflective of  
  surveillance tests. H.3(b) (Section 1R19)
recent performance. This finding had a cross-cutting aspect in the area of Work Control.
* Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,
Specifically, the licensee did not appropriately coordinate work activities by incorporating  
  Appendix B, Criterion IV, Procurement Document Control, was self-revealed for the
actions to address the impact of the work as different job activities. The scheduling of  
  licensee's failure to ensure a safety-related plug was ordered and installed where
the work activities resulted in the pre-conditioning of the EDG prior to performing the  
  required in the 2/3 EDG turbo lube oil Y strainer. Instead, a non-conforming part was
surveillance tests. H.3(b) (Section 1R19)  
  installed, which resulted in a one-half gallon per minute oil leak and removal of the diesel
*  
  generator from service. The issue was entered into the licensees CAP as IR 926605.
Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,  
  Corrective actions included inspection of all other diesel generators to ensure the non-
Appendix B, Criterion IV, Procurement Document Control, was self-revealed for the  
  conforming condition did not exist on another machine, revising the procurement
licensee's failure to ensure a safety-related plug was ordered and installed where  
  documents to ensure that future parts include a pressure retaining pipe plug with
required in the 2/3 EDG turbo lube oil Y strainer. Instead, a non-conforming part was  
  approved material, and adding a requirement for a quality inspection to be performed to
installed, which resulted in a one-half gallon per minute oil leak and removal of the diesel  
  inspect the strainer for metallic pipe plug in blow down port. Individual procedure
generator from service. The issue was entered into the licensees CAP as IR 926605.
  compliance issues were addressed through the stations performance improvement
Corrective actions included inspection of all other diesel generators to ensure the non-
  initiatives.
conforming condition did not exist on another machine, revising the procurement  
  The finding was determined to be more than minor because the finding was similar to
documents to ensure that future parts include a pressure retaining pipe plug with  
  IMC 0612, Appendix E, Example 5 c because an incorrect and inadequate part was
approved material, and adding a requirement for a quality inspection to be performed to  
  installed and the system was returned to service. This performance deficiency impacted
inspect the strainer for metallic pipe plug in blow down port. Individual procedure  
  the Mitigating Systems Cornerstone objective to ensure the availability, reliability, and
compliance issues were addressed through the stations performance improvement  
  capability of systems that respond to initiating events to prevent undesirable
initiatives.  
  consequences. A Phase 3 SDP risk evaluation was performed by the regional
The finding was determined to be more than minor because the finding was similar to  
  Senior Risk Analyst who determined the risk significance of the finding to be less than
IMC 0612, Appendix E, Example 5 c because an incorrect and inadequate part was  
  1.0E-6/yr delta core damage frequency (CDF) and less than 1.0E-7/yr delta LERF, which
installed and the system was returned to service. This performance deficiency impacted  
  represents a finding of very low safety significance. Failure of plant personnel to
the Mitigating Systems Cornerstone objective to ensure the availability, reliability, and  
  question the plastic shipping plug before the equipment was installed and returned to
capability of systems that respond to initiating events to prevent undesirable  
  service was not in compliance with MA-AA-716-008, Foreign Material Exclusion
consequences. A Phase 3 SDP risk evaluation was performed by the regional  
  Program, and, therefore, inspectors determined that this event was cross-cutting in
Senior Risk Analyst who determined the risk significance of the finding to be less than  
  Human Performance, Work Practices, Procedural Compliance for failure of personnel to
1.0E-6/yr delta core damage frequency (CDF) and less than 1.0E-7/yr delta LERF, which  
  follow the procedure. H.4(b) (Section 4OA3.3)
represents a finding of very low safety significance. Failure of plant personnel to  
                                                3                                  Enclosure
question the plastic shipping plug before the equipment was installed and returned to  
service was not in compliance with MA-AA-716-008, Foreign Material Exclusion  
Program, and, therefore, inspectors determined that this event was cross-cutting in  
Human Performance, Work Practices, Procedural Compliance for failure of personnel to  
follow the procedure. H.4(b) (Section 4OA3.3)  


  Cornerstone: Barrier Integrity
* Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,
  Appendix B, Criterion V, was self-revealed for the failure to properly move a fuel
4
  assembly to its specified location, in accordance with DFP 0800-01, Master Refueling
Enclosure
  Procedure. Specifically, on November 5, 2004, fuel assembly JLU569 was placed in
Cornerstone: Barrier Integrity  
  position C4-E5, instead of C4-F5, as required by the procedure. The violation was
*  
  placed into the licensees CAP in IR 990180. As corrective action, the licensee
Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,  
  temporarily suspended all fuel handling activities, conducted a piece count of the spent
Appendix B, Criterion V, was self-revealed for the failure to properly move a fuel  
  fuel and stationed a second Senior Reactor Operator on the refueling bridge as
assembly to its specified location, in accordance with DFP 0800-01, Master Refueling  
  additional oversight for follow-on fuel movements. Additionally the fuel handling crew
Procedure. Specifically, on November 5, 2004, fuel assembly JLU569 was placed in  
  associated with the event was suspended from future fuel moves, pending remedial
position C4-E5, instead of C4-F5, as required by the procedure. The violation was  
  training.
placed into the licensees CAP in IR 990180. As corrective action, the licensee  
  Using the guidance contained in IMC 0612, Power Reactor Inspection Reports,
temporarily suspended all fuel handling activities, conducted a piece count of the spent  
  Appendix B, Issue Disposition Screening, dated December 4, 2008, the inspectors
fuel and stationed a second Senior Reactor Operator on the refueling bridge as  
  determined that the finding was more than minor because the finding was associated
additional oversight for follow-on fuel movements. Additionally the fuel handling crew  
  with the configuration control and human performance attributes of the Barrier Integrity
associated with the event was suspended from future fuel moves, pending remedial  
  Cornerstone and impacted the Barrier Integrity Cornerstone objective to provide
training.  
  reasonable assurance that physical design barriers (i.e., fuel cladding) protect the public
Using the guidance contained in IMC 0612, Power Reactor Inspection Reports,  
  from radionuclide releases caused by an accident or event. Specifically, the shutdown
Appendix B, Issue Disposition Screening, dated December 4, 2008, the inspectors  
  margin and thermal management of the spent fuel pool(s) is affected by fuel assembly
determined that the finding was more than minor because the finding was associated  
  placement inside the pool(s). The inspectors determined the finding could be evaluated
with the configuration control and human performance attributes of the Barrier Integrity  
  using the significance determination process in accordance with IMC 0609,
Cornerstone and impacted the Barrier Integrity Cornerstone objective to provide  
  Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening
reasonable assurance that physical design barriers (i.e., fuel cladding) protect the public  
  and Characterization of Findings, Table 3b, question 6, which directed the inspectors to
from radionuclide releases caused by an accident or event. Specifically, the shutdown  
  Appendix M, Significance Determination Process Using Qualitative Criteria. Because
margin and thermal management of the spent fuel pool(s) is affected by fuel assembly  
  probabilistic risk assessment tools were not well suited for this finding, the criteria for
placement inside the pool(s). The inspectors determined the finding could be evaluated  
  using IMC 0609, Appendix M, were met. In determining the significance of this finding,
using the significance determination process in accordance with IMC 0609,  
  regional management reviewed the licensee's bounding analysis in the UFSAR, which
Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening  
  demonstrated that regardless of the incorrect bundle position in the fuel pool, the design
and Characterization of Findings, Table 3b, question 6, which directed the inspectors to  
  of the pool still maintained pool Keff less than .95. Based on the additional qualitative
Appendix M, Significance Determination Process Using Qualitative Criteria. Because  
  circumstances associated with this finding, regional management concluded the finding
probabilistic risk assessment tools were not well suited for this finding, the criteria for  
  was of very low safety significance (Green). This finding has a cross-cutting aspect in
using IMC 0609, Appendix M, were met. In determining the significance of this finding,  
  the area of Human Performance, Work Practices. Specifically, neither the Senior
regional management reviewed the licensee's bounding analysis in the UFSAR, which  
  Reactor Operator (SRO), nor either of the two members of the fuel handling crew,
demonstrated that regardless of the incorrect bundle position in the fuel pool, the design  
  adequately performed independent verification techniques that ensured the fuel
of the pool still maintained pool Keff less than .95. Based on the additional qualitative  
  assembly move was made in accordance with the Nuclear Component Transfer List, as
circumstances associated with this finding, regional management concluded the finding  
  required by DFP 0800-01. H.4(a) (Section 1R20)
was of very low safety significance (Green). This finding has a cross-cutting aspect in  
* Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,
the area of Human Performance, Work Practices. Specifically, neither the Senior  
  Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed for
Reactor Operator (SRO), nor either of the two members of the fuel handling crew,  
  the mispositioning of a Unit 3 control rod at power. Control rod G-11 was withdrawn one
adequately performed independent verification techniques that ensured the fuel  
  notch contrary to TS SR 3.1.3.3 requirements to insert each withdrawn control rod at
assembly move was made in accordance with the Nuclear Component Transfer List, as  
  least one notch. This was a performance deficiency. The violation was entered into the
required by DFP 0800-01. H.4(a) (Section 1R20)  
  licensees CAP as IR 993634. Corrective actions included inserting control rod G-11
*  
  one notch back to the original position and suspending control rod movement while all
Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,  
  rods were verified to be in their correct position. The operator was removed from shift
Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed for  
  duties and the oncoming shift was briefed of the event.
the mispositioning of a Unit 3 control rod at power. Control rod G-11 was withdrawn one  
                                                4                                    Enclosure
notch contrary to TS SR 3.1.3.3 requirements to insert each withdrawn control rod at  
least one notch. This was a performance deficiency. The violation was entered into the  
licensees CAP as IR 993634. Corrective actions included inserting control rod G-11  
one notch back to the original position and suspending control rod movement while all  
rods were verified to be in their correct position. The operator was removed from shift  
duties and the oncoming shift was briefed of the event.  


  The finding was determined to be more than minor because the finding was associated
  with the Barrier Integrity Cornerstone attributes of human performance and configuration
  control of a control rod, and affected the cornerstone objective of providing reasonable
5
  assurance that physical design barriers protect the public from radionuclide releases
Enclosure
  caused by accidents or events. Specifically, the operator withdrew a control rod contrary
The finding was determined to be more than minor because the finding was associated  
  to expected operation. This added positive reactivity and caused an unanticipated
with the Barrier Integrity Cornerstone attributes of human performance and configuration  
  power increase. The inspectors evaluated the finding using the SDP in accordance with
control of a control rod, and affected the cornerstone objective of providing reasonable  
  IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial
assurance that physical design barriers protect the public from radionuclide releases  
  Screening and Characterization of Findings, Table 4a for the Fuel Barrier Cornerstone.
caused by accidents or events. Specifically, the operator withdrew a control rod contrary  
  Per Table 4a, any issue that involves the fuel barrier is screened as Green. This finding
to expected operation. This added positive reactivity and caused an unanticipated  
  had no cross-cutting aspect. (Section 1R22)
power increase. The inspectors evaluated the finding using the SDP in accordance with  
B. Licensee-Identified Violations
IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial  
  A violation of very low safety significance that was identified by the licensee has been
Screening and Characterization of Findings, Table 4a for the Fuel Barrier Cornerstone.
  reviewed by inspectors. Corrective actions planned or taken by the licensee have been
Per Table 4a, any issue that involves the fuel barrier is screened as Green. This finding  
  entered into the licensees CAP. This violation and corrective action tracking numbers
had no cross-cutting aspect. (Section 1R22)  
  are listed in Section 4OA7 of this report.
B.  
                                                5                                  Enclosure
Licensee-Identified Violations  
A violation of very low safety significance that was identified by the licensee has been  
reviewed by inspectors. Corrective actions planned or taken by the licensee have been  
entered into the licensees CAP. This violation and corrective action tracking numbers  
are listed in Section 4OA7 of this report.  


                                        REPORT DETAILS
Summary of Plant Status
Unit 2
6
On October 18, 2009, the unit began its coastdown to D2R21, and continued to downpower until
Enclosure
the end of the month.
REPORT DETAILS  
On November 1, 2009, the unit was shutdown for the D2R21 Refueling Outage.
Summary of Plant Status  
On December 2, 2009, the unit began ramp-up following D2R21.
Unit 2  
On December 9, 2009, the unit returned to full power.
On October 18, 2009, the unit began its coastdown to D2R21, and continued to downpower until  
Unit 3
the end of the month.  
On October 3, 2009, the unit scrammed due to a Group 1 isolation resulting from a reactor
On November 1, 2009, the unit was shutdown for the D2R21 Refueling Outage.  
water clean-up pressure perturbation. The unit returned to full power on October 8, 2009.
On December 2, 2009, the unit began ramp-up following D2R21.  
On October 18, 2009, power was reduced to approximately 82 percent for a control rod pattern
On December 9, 2009, the unit returned to full power.  
adjustment. The unit returned to full power on the same day.
Unit 3  
On November 6, 2009, the main turbine was manually tripped due to an EHC fluid leak from a
On October 3, 2009, the unit scrammed due to a Group 1 isolation resulting from a reactor  
main stop valve. The unit returned to full power on November 10, 2009.
water clean-up pressure perturbation. The unit returned to full power on October 8, 2009.  
On November 19, 2009, power was reduced to approximately 82 percent for a control rod
On October 18, 2009, power was reduced to approximately 82 percent for a control rod pattern  
pattern adjustment. The unit returned to full power on the same day.
adjustment. The unit returned to full power on the same day.  
On December 12, 2009, power was reduced to approximately 70 percent for control rod testing,
On November 6, 2009, the main turbine was manually tripped due to an EHC fluid leak from a  
scram testing and quarterly valve testing. The unit returned to full power on
main stop valve. The unit returned to full power on November 10, 2009.  
December 13, 2009.
On November 19, 2009, power was reduced to approximately 82 percent for a control rod  
1.     REACTOR SAFETY
pattern adjustment. The unit returned to full power on the same day.  
1R04 Equipment Alignment (71111.04)
On December 12, 2009, power was reduced to approximately 70 percent for control rod testing,  
  .1   Quarterly Partial System Walkdowns
scram testing and quarterly valve testing. The unit returned to full power on  
    a. Inspection Scope
December 13, 2009.  
        The inspectors performed partial system walkdowns of the following risk-significant
1.  
        systems:
REACTOR SAFETY  
        *     Unit 3 250V battery and DC buses during Unit 2 250V battery discharge test;
1R04 Equipment Alignment (71111.04)  
        *     B train of standby gas treatment when A train declared inoperable;
.1  
        *     U2 Division 2 low pressure coolant injection and containment cooling service
Quarterly Partial System Walkdowns  
              water restoration after D2R21; and
a.  
        *     Unit 2 main power transformer clearance order error.
Inspection Scope  
                                                    6                                  Enclosure
The inspectors performed partial system walkdowns of the following risk-significant  
systems:  
*  
Unit 3 250V battery and DC buses during Unit 2 250V battery discharge test;  
*  
B train of standby gas treatment when A train declared inoperable;
*  
U2 Division 2 low pressure coolant injection and containment cooling service  
water restoration after D2R21; and  
*  
Unit 2 main power transformer clearance order error.  


    The inspectors selected these systems based on their risk significance relative to the
    Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted
    to identify any discrepancies that could impact the function of the system, and, therefore,
7
    potentially increase risk. The inspectors reviewed applicable operating procedures,
Enclosure
    system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical
The inspectors selected these systems based on their risk significance relative to the  
    Specification (TS) requirements, outstanding work orders (WOs), condition reports, and
Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted  
    the impact of ongoing work activities on redundant trains of equipment in order to identify
to identify any discrepancies that could impact the function of the system, and, therefore,  
    conditions that could have rendered the systems incapable of performing their intended
potentially increase risk. The inspectors reviewed applicable operating procedures,  
    functions. The inspectors also walked down accessible portions of the systems to verify
system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical  
    that system components and support equipment were aligned correctly and operable.
Specification (TS) requirements, outstanding work orders (WOs), condition reports, and  
    The inspectors examined the material condition of the components and observed
the impact of ongoing work activities on redundant trains of equipment in order to identify  
    operating parameters of equipment to verify that there were no obvious deficiencies.
conditions that could have rendered the systems incapable of performing their intended  
    The inspectors also verified that the licensee had properly identified and resolved
functions. The inspectors also walked down accessible portions of the systems to verify  
    equipment alignment problems that could cause initiating events or impact the capability
that system components and support equipment were aligned correctly and operable.
    of mitigating systems or barriers and entered them into the corrective action program
The inspectors examined the material condition of the components and observed  
    (CAP) with the appropriate significance characterization. Documents reviewed are listed
operating parameters of equipment to verify that there were no obvious deficiencies.
    in the Attachment to this report.
The inspectors also verified that the licensee had properly identified and resolved  
    These activities constituted four partial system walkdown samples as defined in
equipment alignment problems that could cause initiating events or impact the capability  
    Inspection Procedure (IP) 71111.04-05.
of mitigating systems or barriers and entered them into the corrective action program  
b. Findings
(CAP) with the appropriate significance characterization. Documents reviewed are listed  
(1) Operating Personnel Incorrectly Placed Clearance Tags
in the Attachment to this report.  
    Introduction: A finding of very low safety significance and associated Non-Cited
These activities constituted four partial system walkdown samples as defined in  
    Violation (NCV) of TS 5.4.1 was self-revealed for the failure to meet the requirements of
Inspection Procedure (IP) 71111.04-05.  
    Clearance Order (CO) 69631 by removing shorting links instead of fuses as required by
b.  
    the CO (Green). The inspectors determined this finding to be self-revealed because it
Findings  
    required no active and deliberate observation by the licensee or NRC inspectors to
(1) Operating Personnel Incorrectly Placed Clearance Tags  
    determine whether a change in process or equipment capability or function had
Introduction: A finding of very low safety significance and associated Non-Cited  
    occurred. The licensee was in the process of restoring fuses when it was observed the
Violation (NCV) of TS 5.4.1 was self-revealed for the failure to meet the requirements of  
    fuses had not been removed.
Clearance Order (CO) 69631 by removing shorting links instead of fuses as required by  
    Description: Clearance Order 69631 was placed on November 2, 2009. The CO was to
the CO (Green). The inspectors determined this finding to be self-revealed because it  
    remove fuses (2-0902-29-FU1A and 2-0902-29-FU1B) for the U2 main power
required no active and deliberate observation by the licensee or NRC inspectors to  
    transformer protective relays in preparation for the replacement of the main power
determine whether a change in process or equipment capability or function had  
    transformer. The fuses were located in the top of panel 902-29 in the auxiliary electric
occurred. The licensee was in the process of restoring fuses when it was observed the  
    equipment room. On November 12, 2009, direction was given to restore the fuses per
fuses had not been removed.  
    CO 69631. The non-licensed operators (NLOs), assigned to restore the fuses, found
Description: Clearance Order 69631 was placed on November 2, 2009. The CO was to  
    that fuses 2-902-29-FU1A and 2-0902-29-FU1B had not been removed, but that shorting
remove fuses (2-0902-29-FU1A and 2-0902-29-FU1B) for the U2 main power  
    links 2-902-29-F8 and 2-0902-29-F12 had been removed instead. These shorting links
transformer protective relays in preparation for the replacement of the main power  
    removed protective relaying from the main power transformer TR-2, the unit auxiliary
transformer. The fuses were located in the top of panel 902-29 in the auxiliary electric  
    transformer TR-21, and the reserve auxiliary transformer TR-22.
equipment room. On November 12, 2009, direction was given to restore the fuses per  
    Two NLOs were assigned to remove the fuses. One of them was a Dresden operator,
CO 69631. The non-licensed operators (NLOs), assigned to restore the fuses, found  
    the other was a traveler from Braidwood Station. The Braidwood operator had returned
that fuses 2-902-29-FU1A and 2-0902-29-FU1B had not been removed, but that shorting  
    to Braidwood Station by the time this issue was identified. The inspectors interviewed
links 2-902-29-F8 and 2-0902-29-F12 had been removed instead. These shorting links  
    the Dresden operator. The NLO stated that he never saw the fuses that were to be
removed protective relaying from the main power transformer TR-2, the unit auxiliary  
    removed. The labels for the fuses were below the fuses he was required to remove and
transformer TR-21, and the reserve auxiliary transformer TR-22.  
    above a fuse block that contained the shorting links that he did remove. The fuse block
Two NLOs were assigned to remove the fuses. One of them was a Dresden operator,  
                                                  7                                Enclosure
the other was a traveler from Braidwood Station. The Braidwood operator had returned  
to Braidwood Station by the time this issue was identified. The inspectors interviewed  
the Dresden operator. The NLO stated that he never saw the fuses that were to be  
removed. The labels for the fuses were below the fuses he was required to remove and  
above a fuse block that contained the shorting links that he did remove. The fuse block  


containing the shorting links had a placard on it stating that there were shorting links
inside the fuse block. The operator stated that he had not read the placard. In addition,
the operator stated that after the incorrect fuse block was removed he looked inside the
8
fuse block and recognized that they were shorting links and not fuses. The operator
Enclosure
stated that this did not alert him that the wrong equipment had been manipulated. The
containing the shorting links had a placard on it stating that there were shorting links  
operator also stated that he had been trained to recognize the difference between
inside the fuse block. The operator stated that he had not read the placard. In addition,  
shorting links and fuses.
the operator stated that after the incorrect fuse block was removed he looked inside the  
Analysis: The inspectors determined that removal of shorting links instead of fuses was
fuse block and recognized that they were shorting links and not fuses. The operator  
contrary to the requirements of CO 69631 and was a performance deficiency.
stated that this did not alert him that the wrong equipment had been manipulated. The  
The finding was determined to be more than minor because the finding could reasonably
operator also stated that he had been trained to recognize the difference between  
be viewed as a precursor to a significant event. Specifically, the process error by the
shorting links and fuses.  
non-licensed operators involved in the performance of the CO to properly detect that the
Analysis: The inspectors determined that removal of shorting links instead of fuses was  
wrong piece of equipment had been removed, even after observing that the removed
contrary to the requirements of CO 69631 and was a performance deficiency.  
equipment was not what they were assigned to remove (i.e., shorting link versus a fuse),
The finding was determined to be more than minor because the finding could reasonably  
was a failure that, if left uncorrected, could lead to a significant event.
be viewed as a precursor to a significant event. Specifically, the process error by the  
The inspectors determined the finding could be evaluated using the SDP in accordance
non-licensed operators involved in the performance of the CO to properly detect that the  
with IMC 0609, Appendix G, Attachment 1, Shutdown Operations Significance
wrong piece of equipment had been removed, even after observing that the removed  
Determination Process Phase 1 Operational Checklists For Both PWRs AND BWRs,
equipment was not what they were assigned to remove (i.e., shorting link versus a fuse),  
Checklist 6, dated May 25, 2004. This checklist stated that for a finding to require a
was a failure that, if left uncorrected, could lead to a significant event.  
Phase 2 or 3 determination, it would require an increase in the likelihood of a loss of
The inspectors determined the finding could be evaluated using the SDP in accordance  
offsite power or degrade the licensees ability to cope with a loss of offsite power.
with IMC 0609, Appendix G, Attachment 1, Shutdown Operations Significance  
The ability of the licensee to cope with a loss of offsite power was not impacted because
Determination Process Phase 1 Operational Checklists For Both PWRs AND BWRs,  
at least one emergency diesel generator was operable during the entire period. The
Checklist 6, dated May 25, 2004. This checklist stated that for a finding to require a  
inspectors determined that neither of these conditions were met so the finding screened
Phase 2 or 3 determination, it would require an increase in the likelihood of a loss of  
as Green.
offsite power or degrade the licensees ability to cope with a loss of offsite power.
This finding has a cross-cutting aspect in the area of Human Performance,
The ability of the licensee to cope with a loss of offsite power was not impacted because  
Work Practices. The licensee communicates human error prevention techniques, such
at least one emergency diesel generator was operable during the entire period. The  
as self and peer checking. In addition, personnel do not proceed in the face of
inspectors determined that neither of these conditions were met so the finding screened  
uncertainty or unexpected circumstances. Specifically, the NLO: 1) did not read the
as Green.  
placard that was on the component that the NLO removed, which explained that the
This finding has a cross-cutting aspect in the area of Human Performance,  
component was a shorting link and not a fuse; and 2) did not question why the
Work Practices. The licensee communicates human error prevention techniques, such  
component the NLO removed was a shorting link and not a fuse, as identified in the CO.
as self and peer checking. In addition, personnel do not proceed in the face of  
H.4(a)
uncertainty or unexpected circumstances. Specifically, the NLO: 1) did not read the  
Enforcement: Technical Specification Section 5.4.1 states, in part, that
placard that was on the component that the NLO removed, which explained that the  
Written procedures shall be established, implemented, and maintained covering the
component was a shorting link and not a fuse; and 2) did not question why the  
following activities: The applicable procedures recommended in Regulatory Guide 1.33,
component the NLO removed was a shorting link and not a fuse, as identified in the CO.
Revision 2, Appendix A, February 1978. Paragraph 1.c of Regulatory Guide 1.33
H.4(a)  
states, in part, that procedures for equipment control, locking and tagging shall be
Enforcement: Technical Specification Section 5.4.1 states, in part, that  
prepared and activities shall be performed in accordance with these procedures. The
Written procedures shall be established, implemented, and maintained covering the  
licensee established CO 69631 as the implementing procedure for tagging out-of-service
following activities: The applicable procedures recommended in Regulatory Guide 1.33,  
the Unit 2 Main Power Transformer.
Revision 2, Appendix A, February 1978. Paragraph 1.c of Regulatory Guide 1.33  
Contrary to the above, on November 2, 2009, CO 69631 was incorrectly placed, in that,
states, in part, that procedures for equipment control, locking and tagging shall be  
fuses (2-0902-29-FU1A and 2-0902-29-FU1B) for the U2 main power transformer
prepared and activities shall be performed in accordance with these procedures. The  
protective relays were not removed as required by CO 69631. Instead, shorting links
licensee established CO 69631 as the implementing procedure for tagging out-of-service  
2-0902-29-F8 and 2-0902-29-F12 were removed which removed protective relaying to
the Unit 2 Main Power Transformer.  
                                                8                                Enclosure
Contrary to the above, on November 2, 2009, CO 69631 was incorrectly placed, in that,  
fuses (2-0902-29-FU1A and 2-0902-29-FU1B) for the U2 main power transformer  
protective relays were not removed as required by CO 69631. Instead, shorting links  
2-0902-29-F8 and 2-0902-29-F12 were removed which removed protective relaying to  


      the U2 main power transformer, U2 reserve auxiliary transformer, and the U2 unit
      auxiliary transformer. Corrective actions included: coaching of the individuals involved
      with the incorrect placing of the out-of-service, and changing a placard on the device that
9
      was incorrectly repositioned to include the specific equipment part number of the
Enclosure
      shorting links. Because this violation was of very low safety significance and it was
the U2 main power transformer, U2 reserve auxiliary transformer, and the U2 unit  
      entered into the licensees corrective action program as Issue Report 992290 this
auxiliary transformer. Corrective actions included: coaching of the individuals involved  
      violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC
with the incorrect placing of the out-of-service, and changing a placard on the device that  
      Enforcement Policy. (NCV 05000237/2009005-01)
was incorrectly repositioned to include the specific equipment part number of the  
1R05 Fire Protection (71111.05)
shorting links. Because this violation was of very low safety significance and it was  
.1   Routine Resident Inspector Tours (71111.05Q)
entered into the licensees corrective action program as Issue Report 992290 this  
  a. Inspection Scope
violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC  
      The inspectors conducted fire protection walkdowns which were focused on availability,
Enforcement Policy. (NCV 05000237/2009005-01)  
      accessibility, and the condition of firefighting equipment in the following risk-significant
1R05 Fire Protection (71111.05)  
      plant areas:
.1  
      *       Fire Zone 1.1.1.4, Unit 3 Reactor Building Elevation570, Secondary
Routine Resident Inspector Tours (71111.05Q)  
              Containment;
a.  
      *       Fire Zone 8.2.5.B, Unit 2 Turbine Building Elevation 517, Low Pressure Heater
Inspection Scope  
              Bays North Turbine Cavity;
The inspectors conducted fire protection walkdowns which were focused on availability,  
      *       Fire Zone 8.2.5.A, Unit 2 Turbine Building Elevation 517, High Pressure
accessibility, and the condition of firefighting equipment in the following risk-significant  
              Heaters/Steam Lines; and
plant areas:  
      *       Fire Zone 8.2.6.B Multiple Elevations, Low Pressure Heater Bays.
*  
      The inspectors reviewed areas to assess if the licensee had implemented a fire
Fire Zone 1.1.1.4, Unit 3 Reactor Building Elevation570, Secondary  
      protection program that adequately controlled combustibles and ignition sources within
Containment;  
      the plant, effectively maintained fire detection and suppression capability, maintained
*  
      passive fire protection features in good material condition, and implemented adequate
Fire Zone 8.2.5.B, Unit 2 Turbine Building Elevation 517, Low Pressure Heater  
      compensatory measures for out-of-service, degraded or inoperable fire protection
Bays North Turbine Cavity;  
      equipment, systems, or features in accordance with the licensees fire plan. The
*  
      inspectors selected fire areas based on their overall contribution to internal fire risk as
Fire Zone 8.2.5.A, Unit 2 Turbine Building Elevation 517, High Pressure  
      documented in the plants Individual Plant Examination of External Events, their potential
Heaters/Steam Lines; and  
      to impact equipment, which could initiate or mitigate a plant transient, or their impact on
*  
      the plants ability to respond to a security event. Using the documents listed in the
Fire Zone 8.2.6.B Multiple Elevations, Low Pressure Heater Bays.  
      Attachment to this report,, the inspectors verified that fire hoses and extinguishers were
The inspectors reviewed areas to assess if the licensee had implemented a fire  
      in their designated locations and available for immediate use; that fire detectors and
protection program that adequately controlled combustibles and ignition sources within  
      sprinklers were unobstructed; that transient material loading was within the analyzed
the plant, effectively maintained fire detection and suppression capability, maintained  
      limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory
passive fire protection features in good material condition, and implemented adequate  
      condition. The inspectors also verified that minor issues identified during the inspection
compensatory measures for out-of-service, degraded or inoperable fire protection  
      were entered into the licensees CAP. Documents reviewed are listed in the Attachment
equipment, systems, or features in accordance with the licensees fire plan. The  
      to this report.
inspectors selected fire areas based on their overall contribution to internal fire risk as  
      These activities constituted four quarterly fire protection inspection samples as defined in
documented in the plants Individual Plant Examination of External Events, their potential  
      IP 71111.05-05.
to impact equipment, which could initiate or mitigate a plant transient, or their impact on  
  b. Findings
the plants ability to respond to a security event. Using the documents listed in the  
      No findings of significance were identified.
Attachment to this report,, the inspectors verified that fire hoses and extinguishers were  
                                                      9                                  Enclosure
in their designated locations and available for immediate use; that fire detectors and  
sprinklers were unobstructed; that transient material loading was within the analyzed  
limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory  
condition. The inspectors also verified that minor issues identified during the inspection  
were entered into the licensees CAP. Documents reviewed are listed in the Attachment  
to this report.  
These activities constituted four quarterly fire protection inspection samples as defined in  
IP 71111.05-05.  
b.  
Findings  
No findings of significance were identified.  


1R08 Inservice Inspection Activities (71111.08G)
      For Unit 2, from November 2, 2009, through November 13, 2009, the inspectors
      conducted a review of the implementation of the licensees Inservice Inspection (ISI)
10
      Program for monitoring degradation of the reactor coolant system, steam generator
Enclosure
      tubes, emergency feedwater systems, risk-significant piping and components and
1R08 Inservice Inspection Activities (71111.08G)  
      containment systems.
For Unit 2, from November 2, 2009, through November 13, 2009, the inspectors  
      The inspections described in Sections 1R08.1 and 1R08.5 below count as one
conducted a review of the implementation of the licensees Inservice Inspection (ISI)  
      inspection sample as defined in IP 71111.08-05.
Program for monitoring degradation of the reactor coolant system, steam generator  
.1   Piping Systems ISI
tubes, emergency feedwater systems, risk-significant piping and components and  
    a. Inspection Scope
containment systems.  
      The inspectors observed ultrasonic examination (UT) of the following examination
The inspections described in Sections 1R08.1 and 1R08.5 below count as one  
      Category F welds (e.g., welds with known cracks approved by analysis for limited
inspection sample as defined in IP 71111.08-05.  
      additional service without repair) to evaluate compliance with the licensees augmented
.1  
      Stress Corrosion Cracking Program. Specifically, the inspectors evaluated these
Piping Systems ISI  
      examinations to determine if the procedures, equipment, and personnel used were
a. Inspection Scope  
      qualified in accordance with the American Society of Mechanical Engineers (ASME)
The inspectors observed ultrasonic examination (UT) of the following examination  
      Code Section XI, Appendix VIII.
Category F welds (e.g., welds with known cracks approved by analysis for limited  
      *       UT of the valve-to-tee weld (PS2-Tee/202-4B) on the loop B recirculation system.
additional service without repair) to evaluate compliance with the licensees augmented  
      *       UT of the safe end-to-elbow (PS2/201-1) on the loop B recirculation system.
Stress Corrosion Cracking Program. Specifically, the inspectors evaluated these  
      The inspectors observed a video record and reviewed a written report of the following
examinations to determine if the procedures, equipment, and personnel used were  
      containment drywell supports to evaluate compliance with the licensees augmented
qualified in accordance with the American Society of Mechanical Engineers (ASME)  
      inspection program for Code Class MC supports. Specifically, the inspectors evaluated
Code Section XI, Appendix VIII.  
      this examination to determine if the VT-3 procedure, equipment, and personnel used
*  
      were qualified in accordance with the ASME Code Section XI.
UT of the valve-to-tee weld (PS2-Tee/202-4B) on the loop B recirculation system.  
      *       Visual examination (VT-3) of eight male and female drywell shear lug stabilizers
*  
              (support groups 09 and 10).
UT of the safe end-to-elbow (PS2/201-1) on the loop B recirculation system.  
      The inspectors reviewed the following examination record with relevant/recordable
The inspectors observed a video record and reviewed a written report of the following  
      conditions/indications identified by the licensee to determine if acceptance of these
containment drywell supports to evaluate compliance with the licensees augmented  
      indications for continued service was in accordance with the ASME Code Section XI or
inspection program for Code Class MC supports. Specifically, the inspectors evaluated  
      an NRC-approved alternative.
this examination to determine if the VT-3 procedure, equipment, and personnel used  
      *       Report No. D2R20-037, Four Indications on the Reactor Head Flange Weld
were qualified in accordance with the ASME Code Section XI.  
              (2RPV UPP HD/2-THD-FLG). The inspectors observed the following pressure
*  
              boundary weld completed for a risk-significant system to determine if the licensee
Visual examination (VT-3) of eight male and female drywell shear lug stabilizers  
              followed an ASME Code Section IX qualified welding procedure, maintained
(support groups 09 and 10).  
              control of foreign material, and to determine if the welder used qualified weld filler
The inspectors reviewed the following examination record with relevant/recordable  
              material and base material. The inspectors also reviewed the work order for this
conditions/indications identified by the licensee to determine if acceptance of these  
              welding to determine if the post weld nondestructive examinations required by
indications for continued service was in accordance with the ASME Code Section XI or  
              the ASME Code were specified.
an NRC-approved alternative.  
      *       Weld (FW-2) fabricated during installation of the component cooling service
*  
              water system pump discharge elbow replacement.
Report No. D2R20-037, Four Indications on the Reactor Head Flange Weld  
                                                    10                                  Enclosure
(2RPV UPP HD/2-THD-FLG). The inspectors observed the following pressure  
boundary weld completed for a risk-significant system to determine if the licensee  
followed an ASME Code Section IX qualified welding procedure, maintained  
control of foreign material, and to determine if the welder used qualified weld filler  
material and base material. The inspectors also reviewed the work order for this  
welding to determine if the post weld nondestructive examinations required by  
the ASME Code were specified.  
*  
Weld (FW-2) fabricated during installation of the component cooling service  
water system pump discharge elbow replacement.  


    b. Findings
      No findings of significance were identified.
.2   Reactor Pressure Vessel Upper Head Penetration Inspection Activities (Not Applicable)
11
.3   Boric Acid Corrosion Control (Not Applicable)
Enclosure
.4   Steam Generator Tube Inspection Activities (Not Applicable)
b. Findings  
.5   Identification and Resolution of Problems
No findings of significance were identified.  
    a. Inspection Scope
.2  
      The inspectors performed a review of ISI related problems entered into the licensees
Reactor Pressure Vessel Upper Head Penetration Inspection Activities (Not Applicable)  
      corrective action program and conducted interviews with licensee staff to determine if:
.3  
      *       the licensee had established an appropriate threshold for identifying ISI-related
Boric Acid Corrosion Control (Not Applicable)  
                problems;
.4  
      *       the licensee had performed a root cause (if applicable) and taken appropriate
Steam Generator Tube Inspection Activities (Not Applicable)  
                corrective actions; and
.5  
      *       the licensee had evaluated operating experience and industry generic issues
Identification and Resolution of Problems  
                related to ISI and pressure boundary integrity.
a. Inspection Scope  
      The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,
The inspectors performed a review of ISI related problems entered into the licensees  
      Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action
corrective action program and conducted interviews with licensee staff to determine if:  
      documents reviewed by the inspectors are listed in the Attachment to this report.
*  
    b. Findings
the licensee had established an appropriate threshold for identifying ISI-related  
      No findings of significance were identified.
problems;  
1R11 Licensed Operator Requalification Program (71111.11)
*  
  a. Inspection Scope
the licensee had performed a root cause (if applicable) and taken appropriate  
      On August 3, 2009, the inspectors observed a crew of licensed operators in the plants
corrective actions; and  
      simulator during licensed operator requalification examinations to verify that operator
*  
      performance was adequate, evaluators were identifying and documenting crew
the licensee had evaluated operating experience and industry generic issues  
      performance problems and training was being conducted in accordance with licensee
related to ISI and pressure boundary integrity.  
      procedures. The inspectors evaluated the following areas:
The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,  
      *       licensed operator performance;
Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action  
      *       crews clarity and formality of communications;
documents reviewed by the inspectors are listed in the Attachment to this report.  
      *       ability to take timely actions in the conservative direction;
b. Findings  
      *       prioritization, interpretation, and verification of annunciator alarms;
No findings of significance were identified.  
      *       correct use and implementation of abnormal and emergency procedures;
1R11 Licensed Operator Requalification Program (71111.11)  
      *       control board manipulations;
a.  
      *       oversight and direction from supervisors; and
Inspection Scope  
      *       ability to identify and implement appropriate TS actions and Emergency Plan
On August 3, 2009, the inspectors observed a crew of licensed operators in the plants  
                actions and notifications.
simulator during licensed operator requalification examinations to verify that operator  
                                                        11                              Enclosure
performance was adequate, evaluators were identifying and documenting crew  
performance problems and training was being conducted in accordance with licensee  
procedures. The inspectors evaluated the following areas:  
*  
licensed operator performance;  
*  
crews clarity and formality of communications;  
*  
ability to take timely actions in the conservative direction;  
*  
prioritization, interpretation, and verification of annunciator alarms;  
*  
correct use and implementation of abnormal and emergency procedures;  
*  
control board manipulations;  
*  
oversight and direction from supervisors; and  
*  
ability to identify and implement appropriate TS actions and Emergency Plan  
actions and notifications.  


      The crews performance in these areas was compared to pre-established operator action
      expectations and successful critical task completion requirements. Documents reviewed
      are listed in the Attachment to this report.
12
      This inspection constituted one quarterly licensed operator requalification program
Enclosure
      sample as defined in IP 71111.11.
The crews performance in these areas was compared to pre-established operator action  
  b. Findings
expectations and successful critical task completion requirements. Documents reviewed  
      No findings of significance were identified.
are listed in the Attachment to this report.  
1R12 Maintenance Effectiveness (71111.12)
This inspection constituted one quarterly licensed operator requalification program  
.1   Routine Quarterly Evaluations (71111.12Q)
sample as defined in IP 71111.11.  
  a. Inspection Scope
b.  
      The inspectors evaluated degraded performance issues involving the following
Findings  
      risk-significant systems:
No findings of significance were identified.  
      *       Unit 3 control rod drive (Z03); and
1R12 Maintenance Effectiveness (71111.12)  
      *       Unit 2 Shutdown Cooling (Z10).
.1  
      The inspectors reviewed events such as where ineffective equipment maintenance had
Routine Quarterly Evaluations (71111.12Q)  
      resulted in valid or invalid automatic actuations of engineered safeguards systems and
a.  
      independently verified that the licensee's actions to address system performance or
Inspection Scope  
      condition problems in terms of the following:
The inspectors evaluated degraded performance issues involving the following  
      *       implementing appropriate work practices;
risk-significant systems:  
      *       identifying and addressing common cause failures;
*  
      *       scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
Unit 3 control rod drive (Z03); and  
      *       characterizing system reliability issues for performance;
*  
      *       charging unavailability for performance;
Unit 2 Shutdown Cooling (Z10).  
      *       trending key parameters for condition monitoring;
The inspectors reviewed events such as where ineffective equipment maintenance had  
      *       ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
resulted in valid or invalid automatic actuations of engineered safeguards systems and  
      *       verifying appropriate performance criteria for structures, systems, and
independently verified that the licensee's actions to address system performance or  
              components (SSCs)/functions classified as (a)(2) or appropriate and adequate
condition problems in terms of the following:  
              goals and corrective actions for systems classified as (a)(1).
*  
      The inspectors assessed performance issues with respect to the reliability, availability,
implementing appropriate work practices;  
      and condition monitoring of the system. In addition, the inspectors verified that
*  
      maintenance effectiveness issues were entered into the CAP with the appropriate
identifying and addressing common cause failures;  
      significance characterization. Documents reviewed are listed in the Attachment to this
*  
      report.
scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;  
      This inspection constituted two quarterly maintenance effectiveness samples as defined
*  
      in IP 71111.12-05.
characterizing system reliability issues for performance;  
  b. Findings
*  
      No findings of significance were identified.
charging unavailability for performance;  
                                                    12                                  Enclosure
*  
trending key parameters for condition monitoring;  
*  
ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and  
*  
verifying appropriate performance criteria for structures, systems, and  
components (SSCs)/functions classified as (a)(2) or appropriate and adequate  
goals and corrective actions for systems classified as (a)(1).  
The inspectors assessed performance issues with respect to the reliability, availability,  
and condition monitoring of the system. In addition, the inspectors verified that  
maintenance effectiveness issues were entered into the CAP with the appropriate  
significance characterization. Documents reviewed are listed in the Attachment to this  
report.  
This inspection constituted two quarterly maintenance effectiveness samples as defined  
in IP 71111.12-05.  
b.  
Findings  
No findings of significance were identified.  


1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
  a. Inspection Scope
    The inspectors reviewed the licensee's evaluation and management of plant risk for the
13
    maintenance and emergent work activities affecting risk-significant and safety-related
Enclosure
    equipment listed below to verify that the appropriate risk assessments were performed
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)  
    prior to removing equipment for work:
a.  
    *       345 kv Switchyard Bus 4 outage; and
Inspection Scope  
    *       345 kv Line 8014 trip.
The inspectors reviewed the licensee's evaluation and management of plant risk for the  
    These activities were selected based on their potential risk significance relative to the
maintenance and emergent work activities affecting risk-significant and safety-related  
    Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that
equipment listed below to verify that the appropriate risk assessments were performed  
    risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
prior to removing equipment for work:  
    and complete. When emergent work was performed, the inspectors verified that the
*  
    plant risk was promptly reassessed and managed. The inspectors reviewed the scope
345 kv Switchyard Bus 4 outage; and  
    of maintenance work, discussed the results of the assessment with the licensee's
*  
    probabilistic risk analyst or shift technical advisor, and verified plant conditions were
345 kv Line 8014 trip.  
    consistent with the risk assessment. The inspectors also reviewed Technical
These activities were selected based on their potential risk significance relative to the  
    Specification (TS) requirements and walked down portions of redundant safety systems,
Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that  
    when applicable, to verify risk analysis assumptions were valid and applicable
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate  
    requirements were met.
and complete. When emergent work was performed, the inspectors verified that the  
    These maintenance risk assessments and emergent work control activities constituted
plant risk was promptly reassessed and managed. The inspectors reviewed the scope  
    two samples as defined in IP 71111.13-05.
of maintenance work, discussed the results of the assessment with the licensee's  
  b. Findings
probabilistic risk analyst or shift technical advisor, and verified plant conditions were  
    No findings of significance were identified.
consistent with the risk assessment. The inspectors also reviewed Technical  
1R15 Operability Evaluations (71111.15)
Specification (TS) requirements and walked down portions of redundant safety systems,  
  a. Inspection Scope
when applicable, to verify risk analysis assumptions were valid and applicable  
    The inspectors reviewed the following issues:
requirements were met.  
    *       IR 957843, Failed Flowscan on AOV [air operated valve] 3-1599-61;
These maintenance risk assessments and emergent work control activities constituted  
    *       IR 967008, Degraded Thermal Performance of the 2A LPCI [low pressure
two samples as defined in IP 71111.13-05.  
              coolant injection] Hx [heat exchanger];
b.  
    *       IR 987982, Boron Liquid Leak on 3B SBLC [standby liquid control] Pump; and
Findings  
    *       IR 986676, Auto Bypass Sensors Not in Accordance with
No findings of significance were identified.  
              UFSAR Requirements.
1R15 Operability Evaluations (71111.15)  
    The inspectors selected these potential operability issues based on the risk significance
a.  
    of the associated components and systems. The inspectors evaluated the technical
Inspection Scope  
    adequacy of the evaluations to ensure that TS operability was properly justified and the
The inspectors reviewed the following issues:  
    subject component or system remained available such that no unrecognized increase in
*  
    risk occurred. The inspectors compared the operability and design criteria in the
IR 957843, Failed Flowscan on AOV [air operated valve] 3-1599-61;  
    appropriate sections of the TS and UFSAR to the licensees evaluations, to determine
*  
    whether the components or systems were operable. Where compensatory measures
IR 967008, Degraded Thermal Performance of the 2A LPCI [low pressure  
                                                    13                                    Enclosure
coolant injection] Hx [heat exchanger];  
*  
IR 987982, Boron Liquid Leak on 3B SBLC [standby liquid control] Pump; and  
*  
IR 986676, Auto Bypass Sensors Not in Accordance with  
UFSAR Requirements.  
The inspectors selected these potential operability issues based on the risk significance  
of the associated components and systems. The inspectors evaluated the technical  
adequacy of the evaluations to ensure that TS operability was properly justified and the  
subject component or system remained available such that no unrecognized increase in  
risk occurred. The inspectors compared the operability and design criteria in the  
appropriate sections of the TS and UFSAR to the licensees evaluations, to determine  
whether the components or systems were operable. Where compensatory measures  


    were required to maintain operability, the inspectors determined whether the measures
    in place would function as intended and were properly controlled. The inspectors
    determined, where appropriate, compliance with bounding limitations associated with the
14
    evaluations. Additionally, the inspectors also reviewed a sampling of corrective action
Enclosure
    documents to verify that the licensee was identifying and correcting any deficiencies
were required to maintain operability, the inspectors determined whether the measures  
    associated with operability evaluations. Documents reviewed are listed in the
in place would function as intended and were properly controlled. The inspectors  
    Attachment to this report.
determined, where appropriate, compliance with bounding limitations associated with the  
    This operability inspection constituted four samples as defined in IP 71111.15-05.
evaluations. Additionally, the inspectors also reviewed a sampling of corrective action  
b.   Findings
documents to verify that the licensee was identifying and correcting any deficiencies  
  (1) NRC Inspector-Identified Control Room Alarm Isolation Valve Out-of-Position
associated with operability evaluations. Documents reviewed are listed in the  
    Introduction: A finding of very low safety significance and associated NCV of TS 5.4.1
Attachment to this report.  
    was identified by the inspectors for the licensee failing to follow Dresden procedure
This operability inspection constituted four samples as defined in IP 71111.15-05.  
    DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39. The inspectors
b.  
    identified valve 2-1501-42A, U2 low pressure coolant injection (LPCI) A pump gland
Findings  
    leak-off, was out-of-position (closed) and documented an unresolved item (URI) in
(1) NRC Inspector-Identified Control Room Alarm Isolation Valve Out-of-Position  
    inspection report 05000237/2009004; 05000249/2009004.
Introduction: A finding of very low safety significance and associated NCV of TS 5.4.1  
    Description: On September 24, 2009, the inspectors identified that the 2-1501-42A
was identified by the inspectors for the licensee failing to follow Dresden procedure  
    valve was out-of-position. The inspectors were reviewing the 2A LPCI pump seal
DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39. The inspectors  
    leak-off configuration as part of an evaluation of the mechanical seal safety
identified valve 2-1501-42A, U2 low pressure coolant injection (LPCI) A pump gland  
    classification. The inspectors reported the valve position to shift management and
leak-off, was out-of-position (closed) and documented an unresolved item (URI) in  
    operations department personnel verified the valve was not in the open position as
inspection report 05000237/2009004; 05000249/2009004.  
    described in DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39.
Description: On September 24, 2009, the inspectors identified that the 2-1501-42A  
    This issue was documented in IR 969490, LPCI Gland Seal Leak-off Isolation Found
valve was out-of-position. The inspectors were reviewing the 2A LPCI pump seal  
    Closed. With the valve closed instead of open, a control room alarm (902-3 C-6) for
leak-off configuration as part of an evaluation of the mechanical seal safety  
    LPCI pump seal leakage would not have alarmed for the 2A LPCI pump had the seal
classification. The inspectors reported the valve position to shift management and  
    failed during operation.
operations department personnel verified the valve was not in the open position as  
    The issue was considered an unresolved item in Inspection Report 05000237/2009-004;
described in DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39.
    05000249/2009-004 pending NRC review of the licensees evaluation of the valve
This issue was documented in IR 969490, LPCI Gland Seal Leak-off Isolation Found  
    position versus the requirements of DOP 2-1500-M1.
Closed. With the valve closed instead of open, a control room alarm (902-3 C-6) for  
    The licensee performed a prompt investigation into the mispositioning of the valve.
LPCI pump seal leakage would not have alarmed for the 2A LPCI pump had the seal  
    The licensee was unable to determine the reason for, or the time at which the valve
failed during operation.  
    became mispositioned. The licensee did determine that on July 6, 2009, the 2A LPCI
The issue was considered an unresolved item in Inspection Report 05000237/2009-004;  
    pump seal was replaced under Work Order 548808-01 and procedure DMP 1500-05,
05000249/2009-004 pending NRC review of the licensees evaluation of the valve  
    LPCI Pump Maintenance, Revision 8.
position versus the requirements of DOP 2-1500-M1.  
    The inspectors observed that the licensee took a corrective action to change
The licensee performed a prompt investigation into the mispositioning of the valve.
    maintenance procedure DMP 1500-05, LPCI Pump Maintenance, Revision 8,
The licensee was unable to determine the reason for, or the time at which the valve  
    step G.25.d to include the case drain valve equipment numbers. The inspectors
became mispositioned. The licensee did determine that on July 6, 2009, the 2A LPCI  
    reviewed procedure DMP 1500-05, Revision 8, step G.25.d and found that it had
pump seal was replaced under Work Order 548808-01 and procedure DMP 1500-05,  
    directed only that the case drain valves be closed with no specific equipment number
LPCI Pump Maintenance, Revision 8.  
    designations. Since the valve that was found mispositioned was a drain valve and in
The inspectors observed that the licensee took a corrective action to change  
    close proximity to the case drain valves, it was possible that 2-1501-42A was closed at
maintenance procedure DMP 1500-05, LPCI Pump Maintenance, Revision 8,  
    the same time that the case drain valves were closed. There was no step in
step G.25.d to include the case drain valve equipment numbers. The inspectors  
    DMP 1500-05 past step G.25.d to open the case drain valves.
reviewed procedure DMP 1500-05, Revision 8, step G.25.d and found that it had  
                                                  14                                Enclosure
directed only that the case drain valves be closed with no specific equipment number  
designations. Since the valve that was found mispositioned was a drain valve and in  
close proximity to the case drain valves, it was possible that 2-1501-42A was closed at  
the same time that the case drain valves were closed. There was no step in  
DMP 1500-05 past step G.25.d to open the case drain valves.  


Analysis: The inspectors determined that the as found position of 2-1501-42A was
contrary to the requirement of DOP 2-1500-M1, LPCI System Mechanical Checklist,
Revision 39 and was a performance deficiency.
15
The finding was determined to be more than minor because the finding, if left
Enclosure
uncorrected, would become a more significant safety concern. Specifically, the valve
Analysis: The inspectors determined that the as found position of 2-1501-42A was  
isolated an alarm in the control room. The alarm warned the control room operators of a
contrary to the requirement of DOP 2-1500-M1, LPCI System Mechanical Checklist,  
LPCI pump mechanical seal failure. A mechanical seal failure of a LPCI pump during an
Revision 39 and was a performance deficiency.  
accident condition could result in exceeding the limits of the leakage outside the primary
The finding was determined to be more than minor because the finding, if left  
containment as described in TS` 5.5.2. The inspectors concluded this finding was
uncorrected, would become a more significant safety concern. Specifically, the valve  
associated with the Mitigating Systems Cornerstone.
isolated an alarm in the control room. The alarm warned the control room operators of a  
The inspectors determined the finding could be evaluated using the SDP in accordance
LPCI pump mechanical seal failure. A mechanical seal failure of a LPCI pump during an  
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
accident condition could result in exceeding the limits of the leakage outside the primary  
Initial Screening and Characterization of Findings, Table 4a, dated January 10, 2008,
containment as described in TS` 5.5.2. The inspectors concluded this finding was  
for the Mitigating System Cornerstone. The inspectors answered No to all five
associated with the Mitigating Systems Cornerstone.  
questions on Table 4a. This issue screened as Green.
The inspectors determined the finding could be evaluated using the SDP in accordance  
This finding has a cross-cutting aspect in the area of Human Performance, Work
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -  
Practices because the licensee did not have any documentation as to how or when the
Initial Screening and Characterization of Findings, Table 4a, dated January 10, 2008,  
valve was placed into the position it was in. The design and location of the valve
for the Mitigating System Cornerstone. The inspectors answered No to all five  
precluded that the valve was accidently placed into the position it was found in.
questions on Table 4a. This issue screened as Green.  
Therefore, the inspectors concluded that either the failure to use human error prevention
This finding has a cross-cutting aspect in the area of Human Performance, Work  
techniques or maintaining proper documentation of activities caused the mispositioning
Practices because the licensee did not have any documentation as to how or when the  
of valve 2-1501-42A. H.4(a)
valve was placed into the position it was in. The design and location of the valve  
Enforcement: Technical Specification Section 5.4.1.a states, in part, that
precluded that the valve was accidently placed into the position it was found in.
Written procedures shall be established, implemented, and maintained covering the
Therefore, the inspectors concluded that either the failure to use human error prevention  
following activities: The applicable procedures recommended in Regulatory Guide 1.33,
techniques or maintaining proper documentation of activities caused the mispositioning  
Revision 2, Appendix A, February 1978. Paragraph 4 of this Regulatory Guide states,
of valve 2-1501-42A. H.4(a)  
in part, that procedures for energizing, filing, venting, draining, startup, shutdown, and
Enforcement: Technical Specification Section 5.4.1.a states, in part, that  
changing modes of operation for Emergency Core Cooling Systems shall be prepared
Written procedures shall be established, implemented, and maintained covering the  
and activities shall be performed in accordance with these procedures. The licensee
following activities: The applicable procedures recommended in Regulatory Guide 1.33,  
established DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39, as one
Revision 2, Appendix A, February 1978. Paragraph 4 of this Regulatory Guide states,  
of the implementing procedures.
in part, that procedures for energizing, filing, venting, draining, startup, shutdown, and  
Contrary to the above, on September 24, 2009, the inspectors identified that the
changing modes of operation for Emergency Core Cooling Systems shall be prepared  
2-1501-42A valve was not in the open position as required by DOP 2-1500-M1,
and activities shall be performed in accordance with these procedures. The licensee  
LPCI System Mechanical Checklist, Revision 39. The licensee took the following
established DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39, as one  
corrective actions: restored 2-1501-42A to the correct position; changed maintenance
of the implementing procedures.  
procedure DMP 1500-05, LPCI Pump Maintenance, step G.25.d to include the case
Contrary to the above, on September 24, 2009, the inspectors identified that the  
drain valve equipment numbers and sign offs to position and verify the valves; and
2-1501-42A valve was not in the open position as required by DOP 2-1500-M1,  
Operations Department Management addressed the operations department personnel
LPCI System Mechanical Checklist, Revision 39. The licensee took the following  
about this issue. Because this violation was of very low safety significance and it was
corrective actions: restored 2-1501-42A to the correct position; changed maintenance  
entered into the licensees corrective action program as IR 969490, this violation is being
procedure DMP 1500-05, LPCI Pump Maintenance, step G.25.d to include the case  
treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy.
drain valve equipment numbers and sign offs to position and verify the valves; and  
(NCV 05000237/2009005-02) (URI 05000237/2009004-04; 05000249/2009004-04 is
Operations Department Management addressed the operations department personnel  
closed.
about this issue. Because this violation was of very low safety significance and it was  
                                              15                                  Enclosure
entered into the licensees corrective action program as IR 969490, this violation is being  
treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy.
(NCV 05000237/2009005-02) (URI 05000237/2009004-04; 05000249/2009004-04 is  
closed.  


1R19 Post-Maintenance Testing (71111.19)
.1   Post-Maintenance Testing
  a. Inspection Scope
16
      The inspectors reviewed the following post-maintenance (PM) activities to verify that
Enclosure
      procedures and test activities were adequate to ensure system operability and functional
1R19 Post-Maintenance Testing (71111.19)  
      capability:
.1  
      *       WO 1152490-08, OP Perform as Left LLRT [local leak rate test] on 2-0203-2C
Post-Maintenance Testing  
                MSIV [main steam isolation valve];
a.  
      *       WO 1293386, TSC [Technical Support Center] HVAC [heating, ventilation and
Inspection Scope  
                air conditioning] Surveillances Failed;
The inspectors reviewed the following post-maintenance (PM) activities to verify that  
      *       WO 1285845, U2 EDG [emergency diesel generator] Largest Load Reject
procedures and test activities were adequate to ensure system operability and functional  
                (TSR 3.8.1.10);
capability:  
      *       WO 1286397, 2/3 EDG Voltage Transient; and
*  
      *       WO 1098975-02, Perform 2B Condensate Pump Inspections.
WO 1152490-08, OP Perform as Left LLRT [local leak rate test] on 2-0203-2C  
      These activities were selected based upon the structure, system, or component's ability
MSIV [main steam isolation valve];
      to impact risk. The inspectors evaluated these activities for the following (as applicable):
*  
      the effect of testing on the plant had been adequately addressed; testing was adequate
WO 1293386, TSC [Technical Support Center] HVAC [heating, ventilation and  
      for the maintenance performed; acceptance criteria were clear and demonstrated
air conditioning] Surveillances Failed;  
      operational readiness; test instrumentation was appropriate; tests were performed as
*  
      written in accordance with properly reviewed and approved procedures; equipment was
WO 1285845, U2 EDG [emergency diesel generator] Largest Load Reject  
      returned to its operational status following testing (temporary modifications or jumpers
(TSR 3.8.1.10);  
      required for test performance were properly removed after test completion); and test
*  
      documentation was properly evaluated. The inspectors evaluated the activities against
WO 1286397, 2/3 EDG Voltage Transient; and  
      TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various
*  
      NRC generic communications to ensure that the test results adequately ensured that the
WO 1098975-02, Perform 2B Condensate Pump Inspections.  
      equipment met the licensing basis and design requirements. In addition, the inspectors
These activities were selected based upon the structure, system, or component's ability  
      reviewed corrective action documents associated with post-maintenance tests to
to impact risk. The inspectors evaluated these activities for the following (as applicable):
      determine whether the licensee was identifying problems and entering them in the CAP
the effect of testing on the plant had been adequately addressed; testing was adequate  
      and that the problems were being corrected commensurate with their importance to
for the maintenance performed; acceptance criteria were clear and demonstrated  
      safety. Documents reviewed are listed in the Attachment to this report.
operational readiness; test instrumentation was appropriate; tests were performed as  
      This inspection constituted five post-maintenance testing samples as defined in
written in accordance with properly reviewed and approved procedures; equipment was  
      IP 71111.19-05.
returned to its operational status following testing (temporary modifications or jumpers  
  b. Findings
required for test performance were properly removed after test completion); and test  
  (1) Preconditioning the Unit 2 EDG Prior to Performing Technical Specification (TS)
documentation was properly evaluated. The inspectors evaluated the activities against  
      Surveillance Requirements (SRs)
TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various  
      Introduction: The inspectors identified a finding of very low safety significance and an
NRC generic communications to ensure that the test results adequately ensured that the  
      associated NCV of 10 CFR 50 Appendix B, Criterion XI, Test Control, because the
equipment met the licensing basis and design requirements. In addition, the inspectors  
      licensee unacceptably preconditioned the Unit 2 EDG prior to performing TS
reviewed corrective action documents associated with post-maintenance tests to  
      SRs 3.8.1.19.c.4, 3.8.1.12.c.3, and 3.8.1.10 (Green). These TS SRs involved verifying
determine whether the licensee was identifying problems and entering them in the CAP  
      that the EDG supplied steady state frequency would be acceptable following a loss
and that the problems were being corrected commensurate with their importance to  
      offsite power (LOOP) coincident with and without a loss of coolant accident (LOCA), and
safety. Documents reviewed are listed in the Attachment to this report.  
      following the loss of the largest post-accident load. Specifically, the inspectors identified
This inspection constituted five post-maintenance testing samples as defined in  
                                                    16                                  Enclosure
IP 71111.19-05.  
b.  
Findings  
(1) Preconditioning the Unit 2 EDG Prior to Performing Technical Specification (TS)  
Surveillance Requirements (SRs)  
Introduction: The inspectors identified a finding of very low safety significance and an  
associated NCV of 10 CFR 50 Appendix B, Criterion XI, Test Control, because the  
licensee unacceptably preconditioned the Unit 2 EDG prior to performing TS  
SRs 3.8.1.19.c.4, 3.8.1.12.c.3, and 3.8.1.10 (Green). These TS SRs involved verifying  
that the EDG supplied steady state frequency would be acceptable following a loss  
offsite power (LOOP) coincident with and without a loss of coolant accident (LOCA), and  
following the loss of the largest post-accident load. Specifically, the inspectors identified  


that the licensee performed governor oil change outage maintenance activities which
involved a section that tuned the Unit 2 diesel governors response to a load change just
prior to performing these TS SRs. The licensee performed the governor oil change
17
maintenance every six years. The SRs listed above were performed every two years.
Enclosure
Description: On November 13, 2009, during the performance of TS SR 3.8.1.10, under
that the licensee performed governor oil change outage maintenance activities which  
work order (WO) 00634625-01, the Unit 2 EDG did not recover fast enough to satisfy the
involved a section that tuned the Unit 2 diesel governors response to a load change just  
TS SR acceptance criteria. After the largest single post-accident load was shed
prior to performing these TS SRs. The licensee performed the governor oil change  
(i.e., a service water pump), the EDG frequency went up to 62.4 Hz and did not recover
maintenance every six years. The SRs listed above were performed every two years.  
to the allowable band of 58.8-61.2 Hz until 13 seconds had passed. Technical
Description: On November 13, 2009, during the performance of TS SR 3.8.1.10, under  
Specification SR 3.8.1.10 requires the bus frequency to recover in less than 4 seconds.
work order (WO) 00634625-01, the Unit 2 EDG did not recover fast enough to satisfy the  
The licensee entered this condition into the corrective action program (IR 992803).
TS SR acceptance criteria. After the largest single post-accident load was shed  
A second work order (WO 01285845-01) was created, which adjusted the governor
(i.e., a service water pump), the EDG frequency went up to 62.4 Hz and did not recover  
compensator by using work instructions located in station procedure DES 6600-01,
to the allowable band of 58.8-61.2 Hz until 13 seconds had passed. Technical  
Diesel Generator Governor Oil Change and Compensation Adjustment, Revision 23.
Specification SR 3.8.1.10 requires the bus frequency to recover in less than 4 seconds.  
Following the adjustment, the Unit 2 EDG passed TS SR 3.8.1.10 satisfactorily.
The licensee entered this condition into the corrective action program (IR 992803).
The licensee performed a cause evaluation and determined that the Unit 2 EDG failed
A second work order (WO 01285845-01) was created, which adjusted the governor  
the TS SR because the governor compensation was incorrectly set when performing
compensator by using work instructions located in station procedure DES 6600-01,  
WO 634625-01, D2 3RFL PM D/G Governor - Change Oil/Flush/Compensate six days
Diesel Generator Governor Oil Change and Compensation Adjustment, Revision 23.
earlier on November 7, 2009. The licensee determined in their extent of condition
Following the adjustment, the Unit 2 EDG passed TS SR 3.8.1.10 satisfactorily.  
review that the other EDGs were not susceptible to the Unit 2 EDG issue because they
The licensee performed a cause evaluation and determined that the Unit 2 EDG failed  
had been successfully tested by performing TS SR 3.8.1.10 as a post-maintenance test
the TS SR because the governor compensation was incorrectly set when performing  
(PMT) since their respective governor oil change outs. The inspectors identified that it
WO 634625-01, D2 3RFL PM D/G Governor - Change Oil/Flush/Compensate six days  
was the practice for the licensee to utilize TS SR 4.8.1.10 as a PMT when performing
earlier on November 7, 2009. The licensee determined in their extent of condition  
these oil changes on a six year interval.
review that the other EDGs were not susceptible to the Unit 2 EDG issue because they  
The inspectors questioned the practice of performing preventative maintenance (PM)
had been successfully tested by performing TS SR 3.8.1.10 as a post-maintenance test  
activities which involved tuning the EDG governor response just prior to the EDGs
(PMT) since their respective governor oil change outs. The inspectors identified that it  
biennial design basis loading/load shedding tests. Furthermore, the inspectors noted
was the practice for the licensee to utilize TS SR 4.8.1.10 as a PMT when performing  
that the maintenance activity utilized to resolve the failed TS SR was to re-perform the
these oil changes on a six year interval.  
governor compensator adjustment section of the PM activity used on November 7, 2009.
The inspectors questioned the practice of performing preventative maintenance (PM)  
The licensee stated that, after evaluating the issue under IR 1000609, Assignment 1,
activities which involved tuning the EDG governor response just prior to the EDGs  
that the inspectors issue was an example of acceptable pre-conditioning, primarily for
biennial design basis loading/load shedding tests. Furthermore, the inspectors noted  
two reasons. The licensee agreed that the PM and PMT could mask the as-found EDG
that the maintenance activity utilized to resolve the failed TS SR was to re-perform the  
governors response during the performance of TS SR 3.8.1.10, but was acceptable
governor compensator adjustment section of the PM activity used on November 7, 2009.  
because the TS SR is usually performed without the PM/PMT activity the majority of the
The licensee stated that, after evaluating the issue under IR 1000609, Assignment 1,  
time (oil change/flush every six years, and TS SR is performed every two years.).
that the inspectors issue was an example of acceptable pre-conditioning, primarily for  
In addition the licensee determined that a second diesel run would be required, and that
two reasons. The licensee agreed that the PM and PMT could mask the as-found EDG  
this run would unnecessarily stress the machine.
governors response during the performance of TS SR 3.8.1.10, but was acceptable  
The inspectors disagreed with the licensees CAP evaluation and conclusions and
because the TS SR is usually performed without the PM/PMT activity the majority of the  
communicated the issue through Dresden management. The inspectors consulted the
time (oil change/flush every six years, and TS SR is performed every two years.).
NRR Quality Assurance, Vendor Inspection, and Maintenance Branch as recommended
In addition the licensee determined that a second diesel run would be required, and that  
in the NRCs Inspection Manual Part 9900 guidance regarding preconditioning.
this run would unnecessarily stress the machine.  
The NRR Branch agreed that this issue was not consistent with the guidance outlined in
The inspectors disagreed with the licensees CAP evaluation and conclusions and  
the NRC technical guidance or Information Notice 97-16, Preconditioning of Plant
communicated the issue through Dresden management. The inspectors consulted the  
Structures, Systems, and Components before ASME Code Inservice Testing or
NRR Quality Assurance, Vendor Inspection, and Maintenance Branch as recommended  
Technical Specification Surveillance Testing.
in the NRCs Inspection Manual Part 9900 guidance regarding preconditioning.
                                              17                                Enclosure
The NRR Branch agreed that this issue was not consistent with the guidance outlined in  
the NRC technical guidance or Information Notice 97-16, Preconditioning of Plant  
Structures, Systems, and Components before ASME Code Inservice Testing or  
Technical Specification Surveillance Testing.  


    Analysis: The inspectors determined that the licensee did not establish suitable test
    conditions during the Unit 2 EDG TS SRs 3.8.1.19.c.4, 3.8.1.12.c.3, and 3.8.1.10.
    The inspectors identified that this was a performance deficiency based on the
18
    10 CFR 50, Appendix B, Criterion XI, Test Control regulatory requirements and the
Enclosure
    NRCs generic communication to licensees regarding preconditioning. The failure to
Analysis: The inspectors determined that the licensee did not establish suitable test  
    properly test the EDG is considered more than minor because, if left uncorrected, the
conditions during the Unit 2 EDG TS SRs 3.8.1.19.c.4, 3.8.1.12.c.3, and 3.8.1.10.
    finding would become a more significant safety concern. Unacceptable preconditioning
The inspectors identified that this was a performance deficiency based on the  
    of the EDG could mask latent performance issues and affect the ability of the EDG to
10 CFR 50, Appendix B, Criterion XI, Test Control regulatory requirements and the  
    supply safety-related power to vital loads during an event. The inspectors determined
NRCs generic communication to licensees regarding preconditioning. The failure to  
    that traditional enforcement was not appropriate because it was not apparent that the
properly test the EDG is considered more than minor because, if left uncorrected, the  
    performance deficiency affected the ability of the NRC to regulate. However, the
finding would become a more significant safety concern. Unacceptable preconditioning  
    inspectors noted that this issue could mask failed TS SRs, which would directly feed into
of the EDG could mask latent performance issues and affect the ability of the EDG to  
    the NRC assessment process. This issue was determined to be Green because it did
supply safety-related power to vital loads during an event. The inspectors determined  
    not result in an inoperable Unit 2 EDG.
that traditional enforcement was not appropriate because it was not apparent that the  
    The inspectors determined that the failure to adequately coordinate the work activity of
performance deficiency affected the ability of the NRC to regulate. However, the  
    the PM/PMT and TS SR activities was the principal contributor to this finding and was
inspectors noted that this issue could mask failed TS SRs, which would directly feed into  
    reflective of recent performance. This finding had a cross-cutting aspect in the area of
the NRC assessment process. This issue was determined to be Green because it did  
    Work Control. Specifically the licensee did not appropriately coordinate work activities
not result in an inoperable Unit 2 EDG.  
    by incorporating actions to address the impact of the work as different job activities. The
The inspectors determined that the failure to adequately coordinate the work activity of  
    scheduling of the work activities resulted in the pre-conditioning of the EDG prior to the
the PM/PMT and TS SR activities was the principal contributor to this finding and was  
    surveillance tests. H.3(b)
reflective of recent performance. This finding had a cross-cutting aspect in the area of  
    Enforcement: 10 CFR 50, Appendix B, Criterion XI, Test Control, requires, in part,
Work Control. Specifically the licensee did not appropriately coordinate work activities  
    that the test is performed under suitable environmental conditions. Suitable
by incorporating actions to address the impact of the work as different job activities. The  
    environment conditions include conditions representative of the expected conditions
scheduling of the work activities resulted in the pre-conditioning of the EDG prior to the  
    when the equipment is required to perform its safety function. The adjustment of the
surveillance tests. H.3(b)  
    Unit 2 EDG governor compensator affects how the EDG governor will respond when
Enforcement: 10 CFR 50, Appendix B, Criterion XI, Test Control, requires, in part,  
    TS SRs 3.8.1.19.c.4, 3.8.1.12.c.3, and 3.8.1.10. are performed and, therefore,
that the test is performed under suitable environmental conditions. Suitable  
    preconditions the EDG. The licensee agreed to change the method by which their
environment conditions include conditions representative of the expected conditions  
    maintenance and testing was performed, but had not reached a conclusion on corrective
when the equipment is required to perform its safety function. The adjustment of the  
    actions by the end of the inspection period. Because the finding is of very low safety
Unit 2 EDG governor compensator affects how the EDG governor will respond when  
    significance, and has been entered into the corrective action program as IR 01000609, it
TS SRs 3.8.1.19.c.4, 3.8.1.12.c.3, and 3.8.1.10. are performed and, therefore,  
    is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy,
preconditions the EDG. The licensee agreed to change the method by which their  
    NUREG 1600. (NCV 05000237/2009005-03)
maintenance and testing was performed, but had not reached a conclusion on corrective  
(2) 2/3 Emergency Diesel Generator (EDG) Overvoltage during Division I Undervoltage
actions by the end of the inspection period. Because the finding is of very low safety  
    Surveillance
significance, and has been entered into the corrective action program as IR 01000609, it  
a. Inspection Scope
is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy,  
    The inspectors reviewed the licensees equipment apparent cause evaluation (EACE) in
NUREG 1600. (NCV 05000237/2009005-03)  
    response to a 2/3 EDG overvoltage during performance of DOS 6600-06,
(2) 2/3 Emergency Diesel Generator (EDG) Overvoltage during Division I Undervoltage  
    Bus Undervoltage and ECCS Integrated Functional Test for Unit 2/3 Diesel Generator
Surveillance  
    to Unit 2, Revision 46. Documents reviewed in this inspection are listed in the
a.  
    Attachment to this report.
Inspection Scope  
    This post-maintenance testing review constituted one sample as defined in IP 71111.19.
The inspectors reviewed the licensees equipment apparent cause evaluation (EACE) in  
                                                18                                  Enclosure
response to a 2/3 EDG overvoltage during performance of DOS 6600-06,  
Bus Undervoltage and ECCS Integrated Functional Test for Unit 2/3 Diesel Generator  
to Unit 2, Revision 46. Documents reviewed in this inspection are listed in the  
Attachment to this report.  
This post-maintenance testing review constituted one sample as defined in IP 71111.19.  


  b. Findings
      Introduction: The inspectors identified an URI regarding the regulatory requirements
      associated with the circumstances surrounding the 2/3 EDG overvoltage event on
19
      November 16, 2009.
Enclosure
      Description: On November 16, 2009, at 10:53 a.m., a nuclear station operator (NSO)
b.  
      was performing step I.11.c per DOS 6600-06, Bus Undervoltage and ECCS Integrated
Findings
      Functional Test for Unit 2/3 Diesel Generator to Unit 2, Revision 46. At this time, the
Introduction: The inspectors identified an URI regarding the regulatory requirements  
      operator was attempting to synchronize Bus 23-1 (powered from 2/3 EDG) to Bus 23
associated with the circumstances surrounding the 2/3 EDG overvoltage event on  
      (powered from reserve auxiliary transformer 22). The operator stated that he was only
November 16, 2009.  
      monitoring running versus on-coming bus voltage meters, which are transformed down
Description: On November 16, 2009, at 10:53 a.m., a nuclear station operator (NSO)  
      and are only relative to actual bus voltages. The operator stated that a loud pop noise
was performing step I.11.c per DOS 6600-06, Bus Undervoltage and ECCS Integrated  
      was heard from the 902-3 panel. At this time, the operator noticed that the 23-1/24-1
Functional Test for Unit 2/3 Diesel Generator to Unit 2, Revision 46. At this time, the  
      digital volt meter read around 5600 volts (was previously around 4100 volts). The 2/3
operator was attempting to synchronize Bus 23-1 (powered from 2/3 EDG) to Bus 23  
      EDG was then shutdown per DOS 6600-06 step I.12. On step I.12.c, the voltage
(powered from reserve auxiliary transformer 22). The operator stated that he was only  
      regulator would not lower (remained upscale). The EDG stopped after the 6-minute cool
monitoring running versus on-coming bus voltage meters, which are transformed down  
      down and DOS 6600-06 was stopped.
and are only relative to actual bus voltages. The operator stated that a loud pop noise  
      The licensee generated EACE 994101-07, 2/3 Emergency Diesel Generator (EDG)
was heard from the 902-3 panel. At this time, the operator noticed that the 23-1/24-1  
      Voltage Transient, to determine the cause, extent of condition and corrective actions for
digital volt meter read around 5600 volts (was previously around 4100 volts). The 2/3  
      this event. The inspectors reviewed EACE 994101-07 and interviewed the NSO who
EDG was then shutdown per DOS 6600-06 step I.12. On step I.12.c, the voltage  
      had performed DOS 6600-06. The inspectors raised more questions regarding the
regulator would not lower (remained upscale). The EDG stopped after the 6-minute cool  
      capabilities of the control room simulator used for training, procedure adequacy and the
down and DOS 6600-06 was stopped.  
      corrective actions in place. The inspectors plan to review the licensees response to
The licensee generated EACE 994101-07, 2/3 Emergency Diesel Generator (EDG)  
      their questions to determine if there were any violations of NRC requirements and that
Voltage Transient, to determine the cause, extent of condition and corrective actions for  
      appropriate corrective actions were applied. (URI 05000237/2009005-04;
this event. The inspectors reviewed EACE 994101-07 and interviewed the NSO who  
      05000249/2009005-04)
had performed DOS 6600-06. The inspectors raised more questions regarding the  
1R20 Outage Activities (71111.20)
capabilities of the control room simulator used for training, procedure adequacy and the  
.1   Other Outage Activities
corrective actions in place. The inspectors plan to review the licensees response to  
  a. Inspection Scope
their questions to determine if there were any violations of NRC requirements and that  
      The inspectors evaluated outage activities for a Unit 3 forced outage that began on
appropriate corrective actions were applied. (URI 05000237/2009005-04;  
      October 3, 2009, and continued through October 8, 2009. The forced outage was
05000249/2009005-04)  
      caused by a Group 1 isolation and reactor scram caused by a pressure pulse caused by
1R20 Outage Activities (71111.20)  
      the restoration of the Unit 3 reactor water clean-up system. The inspectors reviewed
.1  
      activities to ensure that the licensee considered risk in developing, planning, and
Other Outage Activities  
      implementing the outage schedule.
a.  
      The inspectors observed or reviewed the reactor shutdown and cooldown, outage
Inspection Scope  
      equipment configuration and risk management, electrical lineups, selected clearances,
The inspectors evaluated outage activities for a Unit 3 forced outage that began on  
      control and monitoring of decay heat removal, control of containment activities, startup
October 3, 2009, and continued through October 8, 2009. The forced outage was  
      and heatup activities, and identification and resolution of problems associated with the
caused by a Group 1 isolation and reactor scram caused by a pressure pulse caused by  
      outage.
the restoration of the Unit 3 reactor water clean-up system. The inspectors reviewed  
      This inspection constituted one other outage sample as defined in IP 71111.20-05.
activities to ensure that the licensee considered risk in developing, planning, and  
                                                    19                                  Enclosure
implementing the outage schedule.  
The inspectors observed or reviewed the reactor shutdown and cooldown, outage  
equipment configuration and risk management, electrical lineups, selected clearances,  
control and monitoring of decay heat removal, control of containment activities, startup  
and heatup activities, and identification and resolution of problems associated with the  
outage.  
This inspection constituted one other outage sample as defined in IP 71111.20-05.  


  b. Findings
    No findings of significance were identified.
.2   Refueling Outage Activities
20
  a. Inspection Scope
Enclosure
    The inspectors reviewed the Outage Safety Plan (OSP) and contingency plans for the
b.  
    Unit 2 refueling outage (RFO), conducted November 1, 2009, through
Findings  
    December 9, 2009, to confirm that the licensee had appropriately considered risk,
No findings of significance were identified.  
    industry experience, and previous site-specific problems in developing and implementing
.2  
    a plan that assured maintenance of defense-in-depth. During the RFO, the inspectors
Refueling Outage Activities  
    observed portions of the shutdown and cooldown processes and monitored licensee
a.  
    controls over the outage activities listed below. Documents reviewed during the
Inspection Scope  
    inspection are listed in the Attachment to this report.
The inspectors reviewed the Outage Safety Plan (OSP) and contingency plans for the  
    *       Licensee configuration management, including maintenance of defense-in-depth
Unit 2 refueling outage (RFO), conducted November 1, 2009, through  
            commensurate with the OSP for key safety functions and compliance with the
December 9, 2009, to confirm that the licensee had appropriately considered risk,  
            applicable TS when taking equipment out-of-service.
industry experience, and previous site-specific problems in developing and implementing  
    *       Implementation of clearance activities and confirmation that tags were properly
a plan that assured maintenance of defense-in-depth. During the RFO, the inspectors  
            hung and equipment appropriately configured to safely support the work or
observed portions of the shutdown and cooldown processes and monitored licensee  
            testing.
controls over the outage activities listed below. Documents reviewed during the  
    *       Installation and configuration of reactor coolant pressure, level, and temperature
inspection are listed in the Attachment to this report.  
            instruments to provide accurate indication, accounting for instrument error.
*  
    *       Controls over the status and configuration of electrical systems to ensure that
Licensee configuration management, including maintenance of defense-in-depth  
            TS and OSP requirements were met, and controls over switchyard activities.
commensurate with the OSP for key safety functions and compliance with the  
    *       Monitoring of decay heat removal processes, systems, and components.
applicable TS when taking equipment out-of-service.  
    *       Controls to ensure that outage work was not impacting the ability of the operators
*  
            to operate the spent fuel pool cooling system.
Implementation of clearance activities and confirmation that tags were properly  
    *       Reactor water inventory controls including flow paths, configurations, and
hung and equipment appropriately configured to safely support the work or  
            alternative means for inventory addition, and controls to prevent inventory loss.
testing.  
    *       Controls over activities that could affect reactivity.
*  
    *       Maintenance of secondary containment as required by TS.
Installation and configuration of reactor coolant pressure, level, and temperature  
    *       Refueling activities, including fuel handling and sipping to detect fuel assembly
instruments to provide accurate indication, accounting for instrument error.  
            leakage.
*  
    *       Startup and ascension to full power operation, tracking of startup prerequisites,
Controls over the status and configuration of electrical systems to ensure that  
            walkdown of the drywell (primary containment) to verify that debris had not been
TS and OSP requirements were met, and controls over switchyard activities.  
            left, which could block emergency core cooling system suction strainers, and
*  
            reactor physics testing.
Monitoring of decay heat removal processes, systems, and components.  
    *       Licensee identification and resolution of problems related to RFO activities.
*  
    This inspection constituted one RFO sample as defined in IP 71111.20-05.
Controls to ensure that outage work was not impacting the ability of the operators  
                                                  20                                  Enclosure
to operate the spent fuel pool cooling system.  
*  
Reactor water inventory controls including flow paths, configurations, and  
alternative means for inventory addition, and controls to prevent inventory loss.  
*  
Controls over activities that could affect reactivity.  
*  
Maintenance of secondary containment as required by TS.  
*  
Refueling activities, including fuel handling and sipping to detect fuel assembly  
leakage.  
*  
Startup and ascension to full power operation, tracking of startup prerequisites,  
walkdown of the drywell (primary containment) to verify that debris had not been  
left, which could block emergency core cooling system suction strainers, and  
reactor physics testing.  
*  
Licensee identification and resolution of problems related to RFO activities.  
This inspection constituted one RFO sample as defined in IP 71111.20-05.  


b. Findings
(1) Failure to Follow the Master Refueling Procedure During Movement of Fuel Assembly
    JLU569
21
    Introduction: A finding of very low significance (Green) was self-revealed involving a
Enclosure
    NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and
b.  
    Drawings, for failing to follow DFP 0800-01, Master Refueling Procedure, Revision 45,
Findings  
    Page 12, Step 2.b, when the licensee moved fuel assembly JLU569 to the wrong
(1) Failure to Follow the Master Refueling Procedure During Movement of Fuel Assembly  
    position in the Unit 2 Spent Fuel Pool during D2R21, on November 5, 2009.
JLU569  
    Description: On November 6, 2009, during fuel shuffle 1, the fuel handling crew was
Introduction: A finding of very low significance (Green) was self-revealed involving a  
    moving a fuel assembly from the reactor to location C4-E5 of the spent fuel pool, per
NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and  
    step 475 of the Nuclear Component Transfer List (Move Sheet), in accordance with
Drawings, for failing to follow DFP 0800-01, Master Refueling Procedure, Revision 45,  
    DFP 0800-01, Master Refueling Procedure. While making the move the refueling crew
Page 12, Step 2.b, when the licensee moved fuel assembly JLU569 to the wrong  
    identified a fuel assembly was already in location C4-E5. The fuel assembly being
position in the Unit 2 Spent Fuel Pool during D2R21, on November 5, 2009.  
    moved was then placed in the designated Emergency Set Down Location.
Description: On November 6, 2009, during fuel shuffle 1, the fuel handling crew was  
    It was immediately determined that the same fuel handling crew had incorrectly
moving a fuel assembly from the reactor to location C4-E5 of the spent fuel pool, per  
    performed step 294 of the Nuclear Component Transfer List the previous night,
step 475 of the Nuclear Component Transfer List (Move Sheet), in accordance with  
    November 5, 2009, where they positioned fuel assembly JLU569 into C4-E5, vice the
DFP 0800-01, Master Refueling Procedure. While making the move the refueling crew  
    correct location of C4-F5, each location was located in the same fuel rack.
identified a fuel assembly was already in location C4-E5. The fuel assembly being  
    DFP 0800-01, Master Refueling Procedure, Revision 45, Step 8.d directs the
moved was then placed in the designated Emergency Set Down Location.  
    Senior Reactor Operator (SRO) on the refueling bridge to verify a fuel assembly is
It was immediately determined that the same fuel handling crew had incorrectly  
    placed in the correct spent fuel pool location by observing rack coordinates in the spent
performed step 294 of the Nuclear Component Transfer List the previous night,  
    fuel pool. During interviews with the inspector, it was determined that the crane
November 5, 2009, where they positioned fuel assembly JLU569 into C4-E5, vice the  
    operator, fuel-handling supervisor and the SRO had each independently
correct location of C4-F5, each location was located in the same fuel rack.  
    (and incorrectly) identified spent fuel pool location C4-F5 as C4-E5.
DFP 0800-01, Master Refueling Procedure, Revision 45, Step 8.d directs the  
    Analysis: The inspectors determined that the licensees failure to move fuel assembly
Senior Reactor Operator (SRO) on the refueling bridge to verify a fuel assembly is  
    JLU569 to the correct location in accordance with the Nuclear Component Transfer List
placed in the correct spent fuel pool location by observing rack coordinates in the spent  
    (Move Sheet) was contrary to 10 CFR 50, Appendix B, Criteria V, Instructions,
fuel pool. During interviews with the inspector, it was determined that the crane  
    Procedures, and Drawings, which, in part, requires that activities affecting quality shall
operator, fuel-handling supervisor and the SRO had each independently  
    be accomplished in accordance with prescribed instructions, and was a performance
(and incorrectly) identified spent fuel pool location C4-F5 as C4-E5.  
    deficiency.
Analysis: The inspectors determined that the licensees failure to move fuel assembly  
    The finding was determined to be more than minor because the finding was associated
JLU569 to the correct location in accordance with the Nuclear Component Transfer List  
    with the configuration control and human performance attributes of the Barrier Integrity
(Move Sheet) was contrary to 10 CFR 50, Appendix B, Criteria V, Instructions,  
    Cornerstone and impacted the Barrier Integrity Cornerstone objective to provide
Procedures, and Drawings, which, in part, requires that activities affecting quality shall  
    reasonable assurance the physical design barriers (i.e., fuel cladding) protect the public
be accomplished in accordance with prescribed instructions, and was a performance  
    from radionuclide releases caused by an accident or event. Specifically, the shutdown
deficiency.  
    margin and thermal management of the spent fuel pool(s) is affected by fuel assembly
The finding was determined to be more than minor because the finding was associated  
    placement inside the pool(s).
with the configuration control and human performance attributes of the Barrier Integrity  
    The inspectors determined the finding could be evaluated using the SDP in accordance
Cornerstone and impacted the Barrier Integrity Cornerstone objective to provide  
    with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
reasonable assurance the physical design barriers (i.e., fuel cladding) protect the public  
    Initial Screening and Characterization of Findings, Table 3b, question 6, which directed
from radionuclide releases caused by an accident or event. Specifically, the shutdown  
    the inspectors to Appendix M, Significance Determination Process Using Qualitative
margin and thermal management of the spent fuel pool(s) is affected by fuel assembly  
    Criteria. Because probabilistic risk assessment tools were not well suited for this
placement inside the pool(s).  
    finding, the criteria for using IMC 0609, Appendix M, were met. In determining the
The inspectors determined the finding could be evaluated using the SDP in accordance  
                                                  21                                Enclosure
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -  
Initial Screening and Characterization of Findings, Table 3b, question 6, which directed  
the inspectors to Appendix M, Significance Determination Process Using Qualitative  
Criteria. Because probabilistic risk assessment tools were not well suited for this  
finding, the criteria for using IMC 0609, Appendix M, were met. In determining the  


      significance of this finding, regional management reviewed the licensee's bounding
      analysis in the UFSAR which demonstrated that regardless of the incorrect bundle
      position in the spent fuel pool, the design of the pool still maintained pool Keff less
22
      than .95. Based on the additional qualitative circumstances associated with this finding,
Enclosure
      regional management concluded the finding was very low safety significance (Green).
significance of this finding, regional management reviewed the licensee's bounding  
      This finding has a cross-cutting aspect in the area of Human Performance, Work
analysis in the UFSAR which demonstrated that regardless of the incorrect bundle  
      Practices. Specifically, neither the SRO, nor either of the two members of the fuel
position in the spent fuel pool, the design of the pool still maintained pool Keff less  
      handling crew, adequately performed independent verification techniques that ensured
than .95.   Based on the additional qualitative circumstances associated with this finding,  
      the fuel assembly move was made in accordance with the Nuclear Component Transfer
regional management concluded the finding was very low safety significance (Green).  
      List, as required by DFP 0800-01, Revision 45, Page 12, Step 2.b. H.4(a)
This finding has a cross-cutting aspect in the area of Human Performance, Work  
      Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and
Practices. Specifically, neither the SRO, nor either of the two members of the fuel  
      Drawings, requires, in part, that activities affecting quality shall be prescribed by
handling crew, adequately performed independent verification techniques that ensured  
      documented instructions, procedures, or drawings, of a type appropriate to the
the fuel assembly move was made in accordance with the Nuclear Component Transfer  
      circumstances and shall be accomplished in accordance with these instructions,
List, as required by DFP 0800-01, Revision 45, Page 12, Step 2.b. H.4(a)  
      procedures, or drawings.
Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and  
      Dresden procedure DFP 0800-01, Master Refueling Procedure, Revision 45 is a
Drawings, requires, in part, that activities affecting quality shall be prescribed by  
      procedure affecting quality. Specifically, it governs fuel movements between the spent
documented instructions, procedures, or drawings, of a type appropriate to the  
      fuel pool and the reactor. Dresden Procedure DFP 0800-01 Step 2.b required the SRO
circumstances and shall be accomplished in accordance with these instructions,  
      to ensure that the fuel assembly was moved in accordance with the Nuclear Component
procedures, or drawings.  
      Transfer List (Move Sheet).
Dresden procedure DFP 0800-01, Master Refueling Procedure, Revision 45 is a  
      Contrary to the above, on November 5, 2009, the licensee failed to follow DFP 0800-01,
procedure affecting quality. Specifically, it governs fuel movements between the spent  
      Master Refueling Procedure, Revision 45, Step 2.b. Specifically, the fuel handling
fuel pool and the reactor. Dresden Procedure DFP 0800-01 Step 2.b required the SRO  
      crew positioned fuel assembly JLU569 in location C4-E5 of the U2 spent fuel pool
to ensure that the fuel assembly was moved in accordance with the Nuclear Component  
      instead of location C4-F5. Because this violation was of very low safety significance and
Transfer List (Move Sheet).  
      it was entered into the licensees correction action program as IR 990180, this violation
Contrary to the above, on November 5, 2009, the licensee failed to follow DFP 0800-01,  
      is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement
Master Refueling Procedure, Revision 45, Step 2.b. Specifically, the fuel handling  
      Policy. (NCV 05000237/2009005-05)
crew positioned fuel assembly JLU569 in location C4-E5 of the U2 spent fuel pool  
      Corrective actions for this event included a temporary stand down of all fuel handling
instead of location C4-F5. Because this violation was of very low safety significance and  
      activities, a piece count of the spent fuel was performed to identify any errors associated
it was entered into the licensees correction action program as IR 990180, this violation  
      with fuel handling up to step 475 of the nuclear transfer list, a second SRO and a fuel
is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement  
      handling supervisor were stationed on the refuel bridge to provide additional oversight
Policy. (NCV 05000237/2009005-05)  
      during the remaining fuel moves, and the crew associated with the event were not to
Corrective actions for this event included a temporary stand down of all fuel handling  
      resume fuel handling duties until the completion of remedial training.
activities, a piece count of the spent fuel was performed to identify any errors associated  
1R22 Surveillance Testing (71111.22)
with fuel handling up to step 475 of the nuclear transfer list, a second SRO and a fuel  
.1   Surveillance Testing
handling supervisor were stationed on the refuel bridge to provide additional oversight  
  a. Inspection Scope
during the remaining fuel moves, and the crew associated with the event were not to  
      The inspectors reviewed the test results for the following activities to determine whether
resume fuel handling duties until the completion of remedial training.  
      risk-significant systems and equipment were capable of performing their intended safety
1R22 Surveillance Testing (71111.22)  
      function and to verify testing was conducted in accordance with applicable procedural
.1  
      and TS requirements:
Surveillance Testing  
                                                    22                                    Enclosure
a.  
Inspection Scope  
The inspectors reviewed the test results for the following activities to determine whether  
risk-significant systems and equipment were capable of performing their intended safety  
function and to verify testing was conducted in accordance with applicable procedural  
and TS requirements:  


*     WO 1077723-01, D2 20M/RFL [20 month/refuel] TS LLRT [local leak rate test]
      MSIV 203-1A & 203-2A Dry Test;
*     WO 1257282-01, D2 QTR SBO [station black out] Diesel Generator Surveillance
23
      Test;
Enclosure
*     WO 1251254-01, D3 Qtr TS Reactor Low Pressure (350 PSIG) ECCS
*  
      [emergency core cooling system] Permissive Ca; and
WO 1077723-01, D2 20M/RFL [20 month/refuel] TS LLRT [local leak rate test]  
*     WO 1277976-01, D3 1M TS Partially Withdrawn Control Rod Drive Exercise.
MSIV 203-1A & 203-2A Dry Test;  
      (IST Sample).
*  
The inspectors observed in plant activities and reviewed procedures and associated
WO 1257282-01, D2 QTR SBO [station black out] Diesel Generator Surveillance  
records to determine the following:
Test;  
*     did unacceptable preconditioning occur;
*  
*     were the effects of the testing adequately addressed by control room personnel
WO 1251254-01, D3 Qtr TS Reactor Low Pressure (350 PSIG) ECCS  
      or engineers prior to the commencement of the testing;
[emergency core cooling system] Permissive Ca; and  
*     were acceptance criteria clearly stated, demonstrated operational readiness, and
*  
      consistent with the system design basis;
WO 1277976-01, D3 1M TS Partially Withdrawn Control Rod Drive Exercise.  
*     plant equipment calibration was correct, accurate, and properly documented;
(IST Sample).  
*     as-left setpoints were within required ranges; and the calibration frequencies
The inspectors observed in plant activities and reviewed procedures and associated  
      were in accordance with TSs, the UFSAR, procedures, and applicable
records to determine the following:  
      commitments;
*  
*     measuring and test equipment calibration was current;
did unacceptable preconditioning occur;  
*     test equipment was used within the required range and accuracy; applicable
*  
      prerequisites described in the test procedures were satisfied;
were the effects of the testing adequately addressed by control room personnel  
*     test frequencies met TS requirements to demonstrate operability and reliability;
or engineers prior to the commencement of the testing;  
      tests were performed in accordance with the test procedures and other
*  
      applicable procedures; jumpers and lifted leads were controlled and restored
were acceptance criteria clearly stated, demonstrated operational readiness, and  
      where used;
consistent with the system design basis;  
*     test data and results were accurate, complete, within limits, and valid;
*  
*     test equipment was removed after testing;
plant equipment calibration was correct, accurate, and properly documented;  
*     where applicable for in-service testing activities, testing was performed in
*  
      accordance with the applicable version of Section XI, ASME code, and reference
as-left setpoints were within required ranges; and the calibration frequencies  
      values were consistent with the system design basis;
were in accordance with TSs, the UFSAR, procedures, and applicable  
*     where applicable, test results not meeting acceptance criteria were addressed
commitments;  
      with an adequate operability evaluation or the system or component was
*  
      declared inoperable;
measuring and test equipment calibration was current;  
*     where applicable for safety-related instrument control surveillance tests,
*  
      reference setting data were accurately incorporated in the test procedure;
test equipment was used within the required range and accuracy; applicable  
*     where applicable, actual conditions encountering high resistance electrical
prerequisites described in the test procedures were satisfied;  
      contacts were such that the intended safety function could still be accomplished;
*  
*     prior procedure changes had not provided an opportunity to identify problems
test frequencies met TS requirements to demonstrate operability and reliability;  
      encountered during the performance of the surveillance or calibration test;
tests were performed in accordance with the test procedures and other  
*     equipment was returned to a position or status required to support the
applicable procedures; jumpers and lifted leads were controlled and restored  
      performance of its safety functions; and
where used;  
*     all problems identified during the testing were appropriately documented and
*  
      dispositioned in the CAP.
test data and results were accurate, complete, within limits, and valid;  
Documents reviewed are listed in the Attachment to this report.
*  
                                            23                                  Enclosure
test equipment was removed after testing;  
*  
where applicable for in-service testing activities, testing was performed in  
accordance with the applicable version of Section XI, ASME code, and reference  
values were consistent with the system design basis;  
*  
where applicable, test results not meeting acceptance criteria were addressed  
with an adequate operability evaluation or the system or component was  
declared inoperable;  
*  
where applicable for safety-related instrument control surveillance tests,  
reference setting data were accurately incorporated in the test procedure;  
*  
where applicable, actual conditions encountering high resistance electrical  
contacts were such that the intended safety function could still be accomplished;  
*  
prior procedure changes had not provided an opportunity to identify problems  
encountered during the performance of the surveillance or calibration test;  
*  
equipment was returned to a position or status required to support the  
performance of its safety functions; and  
*  
all problems identified during the testing were appropriately documented and  
dispositioned in the CAP.  
Documents reviewed are listed in the Attachment to this report.  


    This inspection constituted two routine surveillance testing samples, one in-service
    testing sample, and one isolation valve inspection sample as defined in IP 71111.22,
    Sections -02 and -05.
24
b. Findings
Enclosure
(1) Mispositioning of Unit 3 Control Rod G-11
This inspection constituted two routine surveillance testing samples, one in-service  
    Introduction: A finding of very low safety significance and associated NCV of
testing sample, and one isolation valve inspection sample as defined in IP 71111.22,  
    10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was
Sections -02 and -05.  
    self-revealed for the mispositioning of a Unit 3 control rod at power.
b.  
    Description: On November 15, 2009, during performance of DOS 0300-01, Control Rod
Findings  
    Exercise, Revision 48, control rod CRD G-11 was withdrawn by the reactor operator to
(1) Mispositioning of Unit 3 Control Rod G-11  
    position 16 from position 14 instead of being inserted to position 12 as required by
Introduction: A finding of very low safety significance and associated NCV of  
    procedure. The licensee entered DOA 0300-12, Mispositioned Control Rod, Revision
10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was  
    14; and DGA 7, Unpredicted Reactivity Addition, Revision 20. Control rod G-11 was
self-revealed for the mispositioning of a Unit 3 control rod at power.  
    inserted back to the initial position of 14 and DOA 0300-12 was exited.
Description: On November 15, 2009, during performance of DOS 0300-01, Control Rod  
    Analysis: The inspectors determined that the withdrawal of the control rod was contrary
Exercise, Revision 48, control rod CRD G-11 was withdrawn by the reactor operator to  
    to Technical Specification Surveillance Requirement 3.1.3.3 to insert each withdrawn
position 16 from position 14 instead of being inserted to position 12 as required by  
    control rod at least one notch and was a performance deficiency.
procedure. The licensee entered DOA 0300-12, Mispositioned Control Rod, Revision  
    The finding was determined to be more than minor because the finding was associated
14; and DGA 7, Unpredicted Reactivity Addition, Revision 20. Control rod G-11 was  
    with the Fuel Barrier Cornerstone attributes of human performance and configuration
inserted back to the initial position of 14 and DOA 0300-12 was exited.  
    control of a control rod, and affected the cornerstone objective of providing reasonable
Analysis: The inspectors determined that the withdrawal of the control rod was contrary  
    assurance that physical design barriers protect the public from radionuclide releases
to Technical Specification Surveillance Requirement 3.1.3.3 to insert each withdrawn  
    caused by accidents or events. Specifically, the operator withdrew a control rod contrary
control rod at least one notch and was a performance deficiency.  
    to the expected operation of insertion. This added positive reactivity and caused an
The finding was determined to be more than minor because the finding was associated  
    unanticipated power increase. No thermal or power limits were exceeded.
with the Fuel Barrier Cornerstone attributes of human performance and configuration  
    The inspectors determined the finding could be evaluated using the SDP in accordance
control of a control rod, and affected the cornerstone objective of providing reasonable  
    with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
assurance that physical design barriers protect the public from radionuclide releases  
    Initial Screening and Characterization of Findings, Table 4a for the Fuel Barrier
caused by accidents or events. Specifically, the operator withdrew a control rod contrary  
    Cornerstone. Per Table 4a any issue that involves the fuel barrier is screened as Green.
to the expected operation of insertion. This added positive reactivity and caused an  
    This finding had no cross-cutting aspect. The inspectors determined that the licensee
unanticipated power increase. No thermal or power limits were exceeded.  
    had taken every precaution possible to prevent this error in advance, in that, the licensee
The inspectors determined the finding could be evaluated using the SDP in accordance  
    has briefed the evolution and stationed additional personnel to ensure correct
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -  
    movement. Notwithstanding, the operator moved the rod in the wrong direction.
Initial Screening and Characterization of Findings, Table 4a for the Fuel Barrier  
    Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,
Cornerstone. Per Table 4a any issue that involves the fuel barrier is screened as Green.  
    and Drawings, requires, in part, that activities affecting quality shall be prescribed by
This finding had no cross-cutting aspect. The inspectors determined that the licensee  
    documented instructions, procedures, or drawings, of a type appropriate to the
had taken every precaution possible to prevent this error in advance, in that, the licensee  
    circumstances and shall be accomplished in accordance with these instructions,
has briefed the evolution and stationed additional personnel to ensure correct  
    procedures, or drawings.
movement. Notwithstanding, the operator moved the rod in the wrong direction.  
    Contrary to the above, on November 15, 2009, the licensee failed to perform an activity
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,  
    affecting quality in accordance with the appropriate procedure during performance of
and Drawings, requires, in part, that activities affecting quality shall be prescribed by  
    DOS 0300-01, Control Rod Exercise, Revision 48, in that, control rod CRD G-11 was
documented instructions, procedures, or drawings, of a type appropriate to the  
    withdrawn to position 16 from position 14 instead of being inserted to position 12.
circumstances and shall be accomplished in accordance with these instructions,  
                                                  24                                    Enclosure
procedures, or drawings.  
Contrary to the above, on November 15, 2009, the licensee failed to perform an activity  
affecting quality in accordance with the appropriate procedure during performance of  
DOS 0300-01, Control Rod Exercise, Revision 48, in that, control rod CRD G-11 was  
withdrawn to position 16 from position 14 instead of being inserted to position 12.


      Specifically, the licensed operator moving the control rod did not follow procedure
      DOS 0300-01, Step I.4.a, which stated to insert the control rod one notch. The licensee
      took a series of corrective actions: control rod G-11 was inserted one notch back to the
25
      original position and then control room operators suspended control rod movement. All
Enclosure
      control rods were verified to be in their correct position. The operator was removed from
Specifically, the licensed operator moving the control rod did not follow procedure  
      shift duties and the oncoming shift was briefed of the event. Because this violation was
DOS 0300-01, Step I.4.a, which stated to insert the control rod one notch. The licensee  
      of very low safety significance and it was entered into the licensees corrective action
took a series of corrective actions: control rod G-11 was inserted one notch back to the  
      program as IR 993634, this violation is being treated as an NCV, consistent with
original position and then control room operators suspended control rod movement. All  
      Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000249/2009005-06)
control rods were verified to be in their correct position. The operator was removed from  
      Cornerstone: Emergency Preparedness
shift duties and the oncoming shift was briefed of the event. Because this violation was  
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
of very low safety significance and it was entered into the licensees corrective action  
.1   Emergency Action Level and Emergency Plan Changes
program as IR 993634, this violation is being treated as an NCV, consistent with  
  a. Inspection Scope
Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000249/2009005-06)  
      Since the last NRC inspection of this program area, Emergency Plan Annex,
Cornerstone: Emergency Preparedness  
      Revisions 24 and 25 were implemented based on licensee determination, in accordance
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)  
      with 10 CFR 50.54(q), that the changes resulted in no decrease in effectiveness of the
.1  
      Plan, and that the revised Plan continues to meet the requirements of 10 CFR 50.47(b)
Emergency Action Level and Emergency Plan Changes  
      and Appendix E to 10 CFR Part 50. The inspectors conducted a sampling review of the
a.  
      Emergency Plan changes and a review of the Emergency Action Level (EAL) changes to
Inspection Scope  
      evaluate for potential decreases in effectiveness of the Plan. However, this review does
Since the last NRC inspection of this program area, Emergency Plan Annex,  
      not constitute formal NRC approval of the changes. Therefore, these changes remain
Revisions 24 and 25 were implemented based on licensee determination, in accordance  
      subject to future NRC inspection in their entirety.
with 10 CFR 50.54(q), that the changes resulted in no decrease in effectiveness of the  
      This emergency action level and emergency plan changes inspection constituted one
Plan, and that the revised Plan continues to meet the requirements of 10 CFR 50.47(b)  
      sample as defined in IP 71114.04-05.
and Appendix E to 10 CFR Part 50. The inspectors conducted a sampling review of the  
  b. Findings
Emergency Plan changes and a review of the Emergency Action Level (EAL) changes to  
  (1) Changes to EAL HU6 Potentially Decrease the Effectiveness of the Plans without Prior
evaluate for potential decreases in effectiveness of the Plan. However, this review does  
      NRC Approval
not constitute formal NRC approval of the changes. Therefore, these changes remain  
      Introduction: The inspectors reviewed changes implemented to the Dresden Station
subject to future NRC inspection in their entirety.  
      Radiological Emergency Plan Annex EALs and EAL Basis. In Revision 24, the licensee
This emergency action level and emergency plan changes inspection constituted one  
      changed the basis of EAL HU6, "Fire not extinguished within 15 minutes of detection
sample as defined in IP 71114.04-05.  
      within the protected area boundary," by adding two statements. The two changes added
b.  
      to the EAL basis stated that if the alarm could not be verified by redundant control room
Findings  
      or nearby fire panel indications, notification from the field that a fire exists starts the
(1) Changes to EAL HU6 Potentially Decrease the Effectiveness of the Plans without Prior  
      15-minute classification and fire extinguishment clocks. The second change stated the
NRC Approval  
      15-minute period to extinguish the fire does not start until either the fire alarm is verified
Introduction: The inspectors reviewed changes implemented to the Dresden Station  
      to be valid by additional control room or nearby fire panel instrumentation, or upon
Radiological Emergency Plan Annex EALs and EAL Basis. In Revision 24, the licensee  
      notification of a fire from the field. These statements conflict with the previous
changed the basis of EAL HU6, "Fire not extinguished within 15 minutes of detection  
      Dresden Station Annex, Revision 23, basis statements and potentially decrease the
within the protected area boundary," by adding two statements. The two changes added  
      effectiveness of the Plans.
to the EAL basis stated that if the alarm could not be verified by redundant control room  
      Description: Dresden Station Radiological Emergency Plan Annex, Revision 23,
or nearby fire panel indications, notification from the field that a fire exists starts the  
      EAL HU6, initiating condition stated, "Fire not extinguished within 15 minutes of
15-minute classification and fire extinguishment clocks. The second change stated the  
                                                      25                                      Enclosure
15-minute period to extinguish the fire does not start until either the fire alarm is verified  
to be valid by additional control room or nearby fire panel instrumentation, or upon  
notification of a fire from the field. These statements conflict with the previous  
Dresden Station Annex, Revision 23, basis statements and potentially decrease the  
effectiveness of the Plans.  
Description: Dresden Station Radiological Emergency Plan Annex, Revision 23,  
EAL HU6, initiating condition stated, "Fire not extinguished within 15 minutes of  


detection, or explosion, within the protected area boundary." The threshold values for
HU6 were, in part: 1) Fire in any Table H2 area not extinguished within 15 minutes of
Control Room notification or verification of a Control Room alarm, or 2) Fire outside any
26
Table H2 area with the potential to damage safety systems in any Table H2 area not
Enclosure
extinguished within 15 minutes of Control Room notification or verification of a Control
detection, or explosion, within the protected area boundary." The threshold values for  
Room alarm. Table H2, Vital Areas, were identified as reactor building, auxiliary electric
HU6 were, in part: 1) Fire in any Table H2 area not extinguished within 15 minutes of  
room, control room, diesel generator rooms, 4 kilovolt emergency core cooling system
Control Room notification or verification of a Control Room alarm, or 2) Fire outside any  
switchgear area, battery rooms, control rod drive and component cooling service water
Table H2 area with the potential to damage safety systems in any Table H2 area not  
pump rooms, turbine building cable tunnel, turbine building safe shutdown areas, and
extinguished within 15 minutes of Control Room notification or verification of a Control  
crib house. The basis defined fire as "combustion characterized by heat and light.
Room alarm. Table H2, Vital Areas, were identified as reactor building, auxiliary electric  
Sources of smoke such as slipping drive belts or overheated electrical equipment do not
room, control room, diesel generator rooms, 4 kilovolt emergency core cooling system  
constitute fires. Observation of flame is preferred but is not required if large quantities of
switchgear area, battery rooms, control rod drive and component cooling service water  
smoke and heat are observed."
pump rooms, turbine building cable tunnel, turbine building safe shutdown areas, and  
The basis for Revision 23, EAL HU6 thresholds 1 and 2 stated, in part, the purpose of
crib house. The basis defined fire as "combustion characterized by heat and light.
this threshold is to address the magnitude and extent of fires that may be potentially
Sources of smoke such as slipping drive belts or overheated electrical equipment do not  
significant precursors to damage to safety systems. As used here, notification is visual
constitute fires. Observation of flame is preferred but is not required if large quantities of  
observation and report by plant personnel or sensor alarm indication. The 15-minute
smoke and heat are observed."  
period begins with a credible notification that a fire is occurring or indication of a valid fire
The basis for Revision 23, EAL HU6 thresholds 1 and 2 stated, in part, the purpose of  
detection system alarm. A verified alarm is assumed to be an indication of a fire unless
this threshold is to address the magnitude and extent of fires that may be potentially  
personnel dispatched to the scene disprove the alarm within the 15-minute period. The
significant precursors to damage to safety systems. As used here, notification is visual  
report, however, shall not be required to verify the alarm. The intent of the 15-minute
observation and report by plant personnel or sensor alarm indication. The 15-minute  
period is to size the fire and discriminate against small fires that are readily extinguished
period begins with a credible notification that a fire is occurring or indication of a valid fire  
(e.g., smoldering waste paper basket, etc.).
detection system alarm. A verified alarm is assumed to be an indication of a fire unless  
Revision 24 of the Dresden Station Radiological Emergency Plan Annex, changed the
personnel dispatched to the scene disprove the alarm within the 15-minute period. The  
threshold basis for EAL HU6 by adding the following two statements: 1) If the alarm
report, however, shall not be required to verify the alarm. The intent of the 15-minute  
cannot be verified by redundant control room or nearby fire panel indications, notification
period is to size the fire and discriminate against small fires that are readily extinguished  
from the field that a fire exists starts the 15-minute classification and fire extinguishment
(e.g., smoldering waste paper basket, etc.).  
clocks, and 2) The 15-minute period to extinguish the fire does not start until either the
Revision 24 of the Dresden Station Radiological Emergency Plan Annex, changed the  
fire alarm is verified to be valid by utilization of additional control room or nearby fire
threshold basis for EAL HU6 by adding the following two statements: 1) If the alarm  
panel instrumentation, or upon notification of a fire from the field."
cannot be verified by redundant control room or nearby fire panel indications, notification  
The two statements added to the basis in Revision 24 conflict with the Revision 23
from the field that a fire exists starts the 15-minute classification and fire extinguishment  
threshold basis and initiating condition. The changed threshold basis in Revision 24
clocks, and 2) The 15-minute period to extinguish the fire does not start until either the  
could add an indeterminate amount of time to declaring an actual emergency until a
fire alarm is verified to be valid by utilization of additional control room or nearby fire  
person responded to the area of the fire and made a notification to the control room of a
panel instrumentation, or upon notification of a fire from the field."  
fire in the event that redundant control room or nearby fire panel indications were not
The two statements added to the basis in Revision 24 conflict with the Revision 23  
available.
threshold basis and initiating condition. The changed threshold basis in Revision 24  
Pending further review and verification by the NRC to determine if the changes to
could add an indeterminate amount of time to declaring an actual emergency until a  
EAL HU6 threshold basis potentially decreased the effectiveness of the Plans, this issue
person responded to the area of the fire and made a notification to the control room of a  
was considered an Unresolved Item. (URI 05000237/2009005-07)
fire in the event that redundant control room or nearby fire panel indications were not  
                                                26                                  Enclosure
available.  
Pending further review and verification by the NRC to determine if the changes to  
EAL HU6 threshold basis potentially decreased the effectiveness of the Plans, this issue  
was considered an Unresolved Item. (URI 05000237/2009005-07)  


2.     RADIATION SAFETY
      Cornerstone: Occupational Radiation Safety
2OS1 Access Control to Radiologically Significant Areas (71121.01)
27
.1   Plant Walkdowns and Radiation Work Permit Reviews
Enclosure
    a. Inspection Scope
2.  
      The inspectors reviewed licensee controls and surveys in the following radiologically
RADIATION SAFETY  
      significant work areas within radiation areas, high radiation areas, and airborne
Cornerstone: Occupational Radiation Safety
      radioactivity areas in the plant to determine if radiological controls including surveys,
2OS1 Access Control to Radiologically Significant Areas (71121.01)  
      postings, and barricades were acceptable:
.1  
      *       Drywell Nuclear Instrumentation System Maintenance;
Plant Walkdowns and Radiation Work Permit Reviews  
      *       Drywell In-Service Inspection;
a. Inspection Scope  
      *       Drywell Control Rod Drive System Maintenance and Support.
The inspectors reviewed licensee controls and surveys in the following radiologically  
      The inspectors walked down and surveyed (using an NRC survey meter) these areas to
significant work areas within radiation areas, high radiation areas, and airborne  
      verify that the prescribed RWP, procedure, and engineering controls were in place; that
radioactivity areas in the plant to determine if radiological controls including surveys,  
      licensee surveys and postings were complete and accurate; and that air samplers were
postings, and barricades were acceptable:  
      properly located.
*  
      This sample was documented and credited in Inspection Report 05000237/2009003;
Drywell Nuclear Instrumentation System Maintenance;  
      05000249/2009003; therefore, this review does not represent a sample.
*  
    b. Findings
Drywell In-Service Inspection;  
      No findings of significance were identified.
*  
.2   Radiation Worker Performance
Drywell Control Rod Drive System Maintenance and Support.  
    a. Inspection Scope
The inspectors walked down and surveyed (using an NRC survey meter) these areas to  
      During job performance observations, the inspectors evaluated radiation worker
verify that the prescribed RWP, procedure, and engineering controls were in place; that  
      performance with respect to stated radiation safety work requirements. The inspectors
licensee surveys and postings were complete and accurate; and that air samplers were  
      evaluated whether workers were aware of any significant radiological conditions in their
properly located.  
      workplace, of the RWP controls and limits in place, and of the level of radiological
This sample was documented and credited in Inspection Report 05000237/2009003;  
      hazards present. The inspectors also observed worker performance to determine if
05000249/2009003; therefore, this review does not represent a sample.  
      workers accounted for these radiological hazards.
b. Findings  
      This sample was documented and credited in Inspection Report 05000237/2009003;
No findings of significance were identified.  
      05000249/2009003; therefore, this review does not represent a sample.
.2  
    b. Findings
Radiation Worker Performance  
      No findings of significance were identified.
a. Inspection Scope  
                                                    27                                    Enclosure
During job performance observations, the inspectors evaluated radiation worker  
performance with respect to stated radiation safety work requirements. The inspectors  
evaluated whether workers were aware of any significant radiological conditions in their  
workplace, of the RWP controls and limits in place, and of the level of radiological  
hazards present. The inspectors also observed worker performance to determine if  
workers accounted for these radiological hazards.  
This sample was documented and credited in Inspection Report 05000237/2009003;  
05000249/2009003; therefore, this review does not represent a sample.  
b. Findings  
No findings of significance were identified.  


2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)
.1   Inspection Planning
  a. Inspection Scope
28
      The inspectors reviewed plant collective exposure history, current exposure trends, and
Enclosure
      ongoing and planned activities in order to assess current performance and exposure
2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)  
      challenges. The inspectors reviewed the plants current 3-year rolling average for
.1  
      collective exposure in order to help establish resource allocations and to provide a
Inspection Planning  
      perspective of significance for any resulting inspection finding assessment.
a.  
      This inspection constituted one required sample as defined in IP 71121.02-5.
Inspection Scope  
  b. Findings
The inspectors reviewed plant collective exposure history, current exposure trends, and  
      No findings of significance were identified.
ongoing and planned activities in order to assess current performance and exposure  
.2   Radiological Work Planning
challenges. The inspectors reviewed the plants current 3-year rolling average for  
  a. Inspection Scope
collective exposure in order to help establish resource allocations and to provide a  
      The inspectors evaluated the licensees list of work activities ranked by estimated
perspective of significance for any resulting inspection finding assessment.  
      exposure that were in progress and reviewed the following three work activities of
This inspection constituted one required sample as defined in IP 71121.02-5.  
      highest exposure significance:
b.  
      *       Drywell Nuclear Instrumentation System Maintenance;
Findings  
      *       Drywell In-Service Inspection; and
No findings of significance were identified.  
      *       Drywell Control Rod Drive System Maintenance and Support.
.2  
      This sample was documented and credited in Inspection Report 05000237/2008005;
Radiological Work Planning  
      05000249/2008005; therefore, this review does not represent a sample.
a.  
      For these three activities, the inspectors reviewed the As-Low-As-Reasonably-
Inspection Scope  
      Achievable (ALARA) work activity evaluations, exposure estimates, and exposure
The inspectors evaluated the licensees list of work activities ranked by estimated  
      mitigation requirements in order to verify that the licensee had established procedures
exposure that were in progress and reviewed the following three work activities of  
      and engineering and work controls that were based on sound radiation protection
highest exposure significance:  
      principles in order to achieve occupational exposures that were ALARA. The inspectors
*  
      also determined if the licensee had reasonably grouped the radiological work into work
Drywell Nuclear Instrumentation System Maintenance;  
      activities, based on historical precedence, industry norms, and/or special circumstances.
*  
      This sample was documented and credited in Inspection Report 05000237/2008005;
Drywell In-Service Inspection; and  
      05000249/2008005; therefore, this review does not represent a sample.
*  
    b. Findings
Drywell Control Rod Drive System Maintenance and Support.  
      No findings of significance were identified.
This sample was documented and credited in Inspection Report 05000237/2008005;  
                                                    28                                  Enclosure
05000249/2008005; therefore, this review does not represent a sample.  
For these three activities, the inspectors reviewed the As-Low-As-Reasonably-
Achievable (ALARA) work activity evaluations, exposure estimates, and exposure  
mitigation requirements in order to verify that the licensee had established procedures  
and engineering and work controls that were based on sound radiation protection  
principles in order to achieve occupational exposures that were ALARA. The inspectors  
also determined if the licensee had reasonably grouped the radiological work into work  
activities, based on historical precedence, industry norms, and/or special circumstances.  
This sample was documented and credited in Inspection Report 05000237/2008005;  
05000249/2008005; therefore, this review does not represent a sample.  
b. Findings  
No findings of significance were identified.  


  .3   Source-Term Reduction and Control
   
    b. Inspection Scope
      The inspectors reviewed licensee records to evaluate the historical trends and the
29
      current status of tracked plant source terms. The inspectors determined if the licensee
Enclosure
      was making allowances and had developing contingency plans for expected changes in
.3  
      the source term due to changes in plant fuel performance issues or changes in plant
Source-Term Reduction and Control  
      primary chemistry.
b. Inspection Scope  
      This inspection constituted one required sample as defined in IP 71121.02-5.
The inspectors reviewed licensee records to evaluate the historical trends and the  
    c. Findings
current status of tracked plant source terms. The inspectors determined if the licensee  
      No findings of significance were identified.
was making allowances and had developing contingency plans for expected changes in  
4.     OTHER ACTIVITIES
the source term due to changes in plant fuel performance issues or changes in plant  
4OA1 Performance Indicator (PI) Verification (71151)
primary chemistry.  
      Cornerstone: Barrier Integrity
This inspection constituted one required sample as defined in IP 71121.02-5.  
.1   Reactor Coolant System Leakage
c. Findings  
  a. Inspection Scope
No findings of significance were identified.  
      The inspectors sampled licensee submittals for the reactor coolant system (RCS)
4.  
      leakage performance indicator for Units 2 and 3 for the period from the fourth
OTHER ACTIVITIES  
      quarter 2008 through the third quarter 2009. To determine the accuracy of the PI data
4OA1 Performance Indicator (PI) Verification (71151)  
      reported during those periods, PI definitions and guidance contained in the Nuclear
Cornerstone: Barrier Integrity  
      Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator
.1  
      Guideline, Revision 5, were used. The inspectors reviewed the licensees operator
Reactor Coolant System Leakage  
      logs, RCS leakage tracking data, issue reports, event reports and NRC Integrated
a.  
      Inspection Reports for the period of January 2009 through November 2009 to validate
Inspection Scope  
      the accuracy of the submittals. The inspectors also reviewed the licensees issue report
The inspectors sampled licensee submittals for the reactor coolant system (RCS)  
      (IR) database to determine if any problems had been identified with the PI data collected
leakage performance indicator for Units 2 and 3 for the period from the fourth  
      or transmitted for this indicator and none were identified. Documents reviewed are listed
quarter 2008 through the third quarter 2009. To determine the accuracy of the PI data  
      in the Attachment to this report.
reported during those periods, PI definitions and guidance contained in the Nuclear  
      This inspection constituted two reactor coolant system leakage samples as defined in
Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator  
      IP 71151-05.
Guideline, Revision 5, were used. The inspectors reviewed the licensees operator  
  b. Findings
logs, RCS leakage tracking data, issue reports, event reports and NRC Integrated  
      No findings of significance were identified.
Inspection Reports for the period of January 2009 through November 2009 to validate  
                                                    29                                Enclosure
the accuracy of the submittals. The inspectors also reviewed the licensees issue report  
(IR) database to determine if any problems had been identified with the PI data collected  
or transmitted for this indicator and none were identified. Documents reviewed are listed  
in the Attachment to this report.  
This inspection constituted two reactor coolant system leakage samples as defined in  
IP 71151-05.  
b.  
Findings  
No findings of significance were identified.  


      Cornerstone: Occupational Radiation Safety
.2   Occupational Exposure Control Effectiveness
    a. Inspection Scope
30
      The inspectors sampled licensee submittals for the Occupational Radiological
Enclosure
      Occurrences performance indicator for the period from the third quarter 2008 through the
Cornerstone: Occupational Radiation Safety  
      third quarter 2009, to determine the accuracy of the PI data reported during those
.2  
      periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory
Occupational Exposure Control Effectiveness  
      Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors
a. Inspection Scope  
      reviewed the licensees assessment of the PI for occupational radiation safety to
The inspectors sampled licensee submittals for the Occupational Radiological  
      determine if indicator related data was adequately assessed and reported. To assess
Occurrences performance indicator for the period from the third quarter 2008 through the  
      the adequacy of the licensees PI data collection and analyses, the inspectors discussed
third quarter 2009, to determine the accuracy of the PI data reported during those  
      with radiation protection staff, the scope and breadth of its data review, and the results of
periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory  
      those reviews. The inspectors independently reviewed electronic dosimetry dose rate
Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors  
      and accumulated dose alarm and dose reports and the dose assignments for any
reviewed the licensees assessment of the PI for occupational radiation safety to  
      intakes that occurred during the time period reviewed to determine if there were
determine if indicator related data was adequately assessed and reported. To assess  
      potentially unrecognized occurrences. The inspectors also conducted walkdowns of
the adequacy of the licensees PI data collection and analyses, the inspectors discussed  
      numerous locked high and very high radiation area entrances to determine the adequacy
with radiation protection staff, the scope and breadth of its data review, and the results of  
      of the controls in place for these areas. Documents reviewed are listed in the
those reviews. The inspectors independently reviewed electronic dosimetry dose rate  
      Attachment to this report.
and accumulated dose alarm and dose reports and the dose assignments for any  
      This inspection constituted one occupational radiological occurrences sample as defined
intakes that occurred during the time period reviewed to determine if there were  
      in IP 71151-05.
potentially unrecognized occurrences. The inspectors also conducted walkdowns of  
    b. Findings
numerous locked high and very high radiation area entrances to determine the adequacy  
      No findings of significance were identified.
of the controls in place for these areas. Documents reviewed are listed in the  
4OA2 Identification and Resolution of Problems (71152)
Attachment to this report.  
.1   Routine Review of Items Entered Into the CAP
This inspection constituted one occupational radiological occurrences sample as defined  
  a. Scope
in IP 71151-05.  
      As part of the various baseline inspection procedures discussed in previous sections of
b. Findings  
      this report, the inspectors routinely reviewed issues during baseline inspection activities
No findings of significance were identified.  
      and plant status reviews to verify that they were being entered into the licensees CAP at
4OA2 Identification and Resolution of Problems (71152)  
      an appropriate threshold, that adequate attention was being given to timely corrective
.1  
      actions, and that adverse trends were identified and addressed. Attributes reviewed
Routine Review of Items Entered Into the CAP  
      included: the complete and accurate identification of the problem; that timeliness was
a.  
      commensurate with the safety significance; that evaluation and disposition of
Scope  
      performance issues, generic implications, common causes, contributing factors, root
As part of the various baseline inspection procedures discussed in previous sections of  
      causes, extent of condition reviews, and previous occurrences reviews were proper and
this report, the inspectors routinely reviewed issues during baseline inspection activities  
      adequate; and that the classification, prioritization, focus, and timeliness of corrective
and plant status reviews to verify that they were being entered into the licensees CAP at  
      actions were commensurate with safety and sufficient to prevent recurrence of the issue.
an appropriate threshold, that adequate attention was being given to timely corrective  
      Minor issues entered into the licensees CAP as a result of the inspectors observations
actions, and that adverse trends were identified and addressed. Attributes reviewed  
      are included in the attached List of Documents Reviewed.
included: the complete and accurate identification of the problem; that timeliness was  
                                                    30                                    Enclosure
commensurate with the safety significance; that evaluation and disposition of  
performance issues, generic implications, common causes, contributing factors, root  
causes, extent of condition reviews, and previous occurrences reviews were proper and  
adequate; and that the classification, prioritization, focus, and timeliness of corrective  
actions were commensurate with safety and sufficient to prevent recurrence of the issue.
Minor issues entered into the licensees CAP as a result of the inspectors observations  
are included in the attached List of Documents Reviewed.  


    These routine reviews for the identification and resolution of problems did not constitute
    any additional inspection samples. Instead, by procedure, they were considered an
    integral part of the inspections performed during the quarter and documented in
31
    Section 1 of this report.
Enclosure
  b. Findings
These routine reviews for the identification and resolution of problems did not constitute  
    No findings of significance were identified.
any additional inspection samples. Instead, by procedure, they were considered an  
.2   Daily CAP Reviews
integral part of the inspections performed during the quarter and documented in  
  a. Inspection Scope
Section 1 of this report.  
    In order to assist with the identification of repetitive equipment failures and specific
b.  
    human performance issues for follow-up, the inspectors performed a daily screening of
Findings  
    items entered into the licensees CAP. This review was accomplished through
No findings of significance were identified.  
    inspection of the stations daily condition report packages.
.2  
    These daily reviews were performed by procedure as part of the inspectors daily plant
Daily CAP Reviews  
    status monitoring activities and, as such, did not constitute any separate inspection
a.  
    samples.
Inspection Scope  
  b. Findings
In order to assist with the identification of repetitive equipment failures and specific  
    No findings of significance were identified.
human performance issues for follow-up, the inspectors performed a daily screening of  
.3   Semi-Annual Trend Review
items entered into the licensees CAP. This review was accomplished through  
  a. Inspection Scope
inspection of the stations daily condition report packages.  
    The inspectors performed a review of the licensees CAP and associated documents to
These daily reviews were performed by procedure as part of the inspectors daily plant  
    identify trends that could indicate the existence of a more significant safety issue.
status monitoring activities and, as such, did not constitute any separate inspection  
    The inspectors review was focused on repetitive equipment issues, but also considered
samples.  
    the results of daily inspector CAP item screening discussed in Section 4OA2.2 above,
b.  
    licensee trending efforts, and licensee human performance results. Specifically, the
Findings  
    inspectors performed a review of the licensees corrective actions program documents
No findings of significance were identified.  
    related to the areas of instrument air systems, heating, ventilation and air conditioning,
.3  
    and instruments and controls. The inspectors review nominally considered IRs that
Semi-Annual Trend Review  
    were generated in the six month period of July 2009 through December 2009, although
a.  
    some examples expanded beyond those dates where the scope of the trend warranted.
Inspection Scope  
    In addition to reviewing the IR documents for trends, the inspectors compared their
The inspectors performed a review of the licensees CAP and associated documents to  
    results with issues identified in the licensees trending reports. A sample of the licensee
identify trends that could indicate the existence of a more significant safety issue.
    IRs associated with trends was reviewed for corrective action adequacy.
The inspectors review was focused on repetitive equipment issues, but also considered  
    This review constituted a single semi-annual trend inspection sample as defined in
the results of daily inspector CAP item screening discussed in Section 4OA2.2 above,  
    IP 71152-05.
licensee trending efforts, and licensee human performance results. Specifically, the  
  b. Findings
inspectors performed a review of the licensees corrective actions program documents  
    No findings of significance were identified.
related to the areas of instrument air systems, heating, ventilation and air conditioning,  
                                                    31                                Enclosure
and instruments and controls. The inspectors review nominally considered IRs that  
were generated in the six month period of July 2009 through December 2009, although  
some examples expanded beyond those dates where the scope of the trend warranted.
In addition to reviewing the IR documents for trends, the inspectors compared their  
results with issues identified in the licensees trending reports. A sample of the licensee  
IRs associated with trends was reviewed for corrective action adequacy.  
This review constituted a single semi-annual trend inspection sample as defined in  
IP 71152-05.  
b.  
Findings  
No findings of significance were identified.  


.4   In-Depth Review - Corrective Actions Associated With Tube Blockages of the Unit 2 and
      Unit 3 LPCI Heat Exchangers
  a. Inspection Scope
32
      The inspectors performed a focused review of root cause report (RCR) 967008-03,
Enclosure
      Dresden 2-1503-A, 2A Low Pressure Coolant Injection (LPCI) / Containment Cooling
.4  
      Heat Exchanger (Hx) Failure to Meet Design Basis Heat Removal Capability due to
In-Depth Review - Corrective Actions Associated With Tube Blockages of the Unit 2 and  
      Asiatic Clam Macrofouling resulting from 2-1501-3A Valve Leakage and Subsequent
Unit 3 LPCI Heat Exchangers  
      Untreated Service Water Make-up via the CCSW Keepfill Diluting the Biocide Treatment
a.  
      below the Asiatic Clam Lethal Concentration, revision 0, to evaluate the corrective
Inspection Scope  
      actions that the licensee had taken to address the introduction of Asiatic clam relics into
The inspectors performed a focused review of root cause report (RCR) 967008-03,  
      the containment cooling heat exchangers.
Dresden 2-1503-A, 2A Low Pressure Coolant Injection (LPCI) / Containment Cooling  
      Containment cooling is the operating mode of the low pressure coolant injection (LPCI)
Heat Exchanger (Hx) Failure to Meet Design Basis Heat Removal Capability due to  
      subsystem initiated to cool the containment in the event of a loss-of-coolant accident
Asiatic Clam Macrofouling resulting from 2-1501-3A Valve Leakage and Subsequent  
      (LOCA). Each containment cooling subsystem consists of two LPCI pumps, one
Untreated Service Water Make-up via the CCSW Keepfill Diluting the Biocide Treatment  
      containment cooling Hx (also called LPCI Hx), one drywell spray header and a separate
below the Asiatic Clam Lethal Concentration, revision 0, to evaluate the corrective  
      suppression chamber spray header. Heat exchanger cooling water is provided by two
actions that the licensee had taken to address the introduction of Asiatic clam relics into  
      containment cooling service water (CCSW) pumps in each containment cooling
the containment cooling heat exchangers.  
      subsystem. The water source for the CCSW pumps is the cribhouse, specifically
Containment cooling is the operating mode of the low pressure coolant injection (LPCI)  
      Bay 13. If the heat exchanger is significantly fouled, then the Hx may be unable to
subsystem initiated to cool the containment in the event of a loss-of-coolant accident  
      remove sufficient heat from the containment, which could result in primary containment
(LOCA). Each containment cooling subsystem consists of two LPCI pumps, one  
      failure.
containment cooling Hx (also called LPCI Hx), one drywell spray header and a separate  
      In addition, the inspectors performed a focused review to evaluate the licensees
suppression chamber spray header. Heat exchanger cooling water is provided by two  
      assessment of a number of IRs related to the failure to meet biocide residual
containment cooling service water (CCSW) pumps in each containment cooling  
      concentration after chemical addition into the containment cooling service water system.
subsystem. The water source for the CCSW pumps is the cribhouse, specifically  
      The inspectors reviewed these issues to determine if the licensee has taken adequate
Bay 13. If the heat exchanger is significantly fouled, then the Hx may be unable to  
      corrective actions both individually and collectively. This review constituted one sample
remove sufficient heat from the containment, which could result in primary containment  
      as defined in IP 71152.
failure.  
      The inspectors reviewed several documents that are listed in the Attachment of the
In addition, the inspectors performed a focused review to evaluate the licensees  
      report.
assessment of a number of IRs related to the failure to meet biocide residual  
      Issues
concentration after chemical addition into the containment cooling service water system.
  (1) Effectiveness of Problem Identification
The inspectors reviewed these issues to determine if the licensee has taken adequate  
      The licensees thermal performance testing of the LPCI heat exchangers has been
corrective actions both individually and collectively. This review constituted one sample  
      effective in identifying heat exchanger degradation prior to the Hx becoming inoperable.
as defined in IP 71152.  
      On September 18, 2009, a thermal performance test was performed on the 2A LPCI Hx.
The inspectors reviewed several documents that are listed in the Attachment of the  
      The test results indicated a heat removal capability of 67.49 MBtu/hr, which was
report.  
      4.9 percent below the design heat removal rate of 71 MBtu/hr at design conditions per
Issues  
      the updated final safety analysis report (UFSAR) Table 6.2-3b, Heat Exchanger Heat
(1) Effectiveness of Problem Identification  
      Transfer Rate. This issue was documented in IR 967008. Further evaluation
The licensees thermal performance testing of the LPCI heat exchangers has been  
      determined that with a heat removal capability of 67.49 MBtu/hr the new maximum
effective in identifying heat exchanger degradation prior to the Hx becoming inoperable.
      allowable inlet water temperatures for the 3 months following the test performed on
On September 18, 2009, a thermal performance test was performed on the 2A LPCI Hx.
      September 18, were 90.2 degrees F, 89.7 degrees F and 88 degrees F, respectively.
The test results indicated a heat removal capability of 67.49 MBtu/hr, which was  
      Actual CCSW temperatures for the time period, including previous summer months,
4.9 percent below the design heat removal rate of 71 MBtu/hr at design conditions per  
      were below the design basis parameter of 95 degrees F, therefore, the licensee
the updated final safety analysis report (UFSAR) Table 6.2-3b, Heat Exchanger Heat  
                                                  32                                  Enclosure
Transfer Rate. This issue was documented in IR 967008. Further evaluation  
determined that with a heat removal capability of 67.49 MBtu/hr the new maximum  
allowable inlet water temperatures for the 3 months following the test performed on  
September 18, were 90.2 degrees F, 89.7 degrees F and 88 degrees F, respectively.
Actual CCSW temperatures for the time period, including previous summer months,  
were below the design basis parameter of 95 degrees F, therefore, the licensee  


    determined that the 2A LPCI Hx, although degraded, was able to perform the required
    design functions. Also, the licensee reviewed the results for the most recent thermal
    performance tests performed for the other three heat exchangers and based on these
33
    results the licensee determined that the heat exchangers were operable.
Enclosure
    On November 5, 2009, the 2A LPCI Hx was opened for inspection and cleaning.
determined that the 2A LPCI Hx, although degraded, was able to perform the required  
    Approximately 50 percent of the 1256 CCSW inlet tubes were partially or fully
design functions. Also, the licensee reviewed the results for the most recent thermal  
    obstructed. The primary macrofouling mechanism was Asiatic clam relics coupled with
performance tests performed for the other three heat exchangers and based on these  
    silt microfouling. Issue report 989609, D2R21 Inspection Results for 2A LPCI
results the licensee determined that the heat exchangers were operable.  
    Heat Exchanger, was generated to document the as-found condition. The 2A LPCI Hx
On November 5, 2009, the 2A LPCI Hx was opened for inspection and cleaning.
    was cleaned and the thermal performance testing was re-performed in December 2009.
Approximately 50 percent of the 1256 CCSW inlet tubes were partially or fully  
    The new test results indicated a heat removal capability of 78.08 MBtu/hr at design
obstructed. The primary macrofouling mechanism was Asiatic clam relics coupled with  
    conditions which is 10 percent above the design heat removal rate.
silt microfouling. Issue report 989609, D2R21 Inspection Results for 2A LPCI  
(2) Prioritization and Evaluation of Problems
Heat Exchanger, was generated to document the as-found condition. The 2A LPCI Hx  
    The licensees evaluation of the cause of the repetitive LPCI Hx blockages and
was cleaned and the thermal performance testing was re-performed in December 2009.
    prioritization of corrective actions were ineffective. This was the third blockage of a LPCI
The new test results indicated a heat removal capability of 78.08 MBtu/hr at design  
    Hx by Asiatic clams. The first event occurred on the 3B LPCI Hx in September of 2006.
conditions which is 10 percent above the design heat removal rate.  
    At that time the build up of Asiatic clams was thought to be due to a change in the
(2) Prioritization and Evaluation of Problems  
    frequency of Bay 13 cleaning. The second event took place in March 2008, when the 3B
The licensees evaluation of the cause of the repetitive LPCI Hx blockages and  
    LPCI Hx failed its thermal performance test (70.586 vice 71 MBtu/hr). Root Cause
prioritization of corrective actions were ineffective. This was the third blockage of a LPCI  
    Report 776598-08, Dresden 3-1503-B, 3B Low Pressure Coolant Injection (LPCI) /
Hx by Asiatic clams. The first event occurred on the 3B LPCI Hx in September of 2006.
    Containment Cooling Heat Exchanger (HX) Failure to Meet Design Basis Heat Removal
At that time the build up of Asiatic clams was thought to be due to a change in the  
    Capability Due to Inadequate Programmatic Control of Macrofoulants, revision 0,
frequency of Bay 13 cleaning. The second event took place in March 2008, when the 3B  
    attributed the failure of the 3B LPCI Hx to meet the design basis heat removal capability
LPCI Hx failed its thermal performance test (70.586 vice 71 MBtu/hr). Root Cause  
    to inadequate programmatic control of macrofoulants. Specifically, the licensee failed to
Report 776598-08, Dresden 3-1503-B, 3B Low Pressure Coolant Injection (LPCI) /  
    inject biocide into the containment cooling service water pumps' intake during normally
Containment Cooling Heat Exchanger (HX) Failure to Meet Design Basis Heat Removal  
    scheduled operability surveillances and sample to verify biocide residual concentration.
Capability Due to Inadequate Programmatic Control of Macrofoulants, revision 0,  
    This was contrary to the licensees Generic Letter 89-13 Program commitments (refer to
attributed the failure of the 3B LPCI Hx to meet the design basis heat removal capability  
    inspection report 05000237/2008-005; 05000249/2008-005 Section 1R15 for more
to inadequate programmatic control of macrofoulants. Specifically, the licensee failed to  
    details). Corrective actions included injection of biocide into the containment cooling
inject biocide into the containment cooling service water pumps' intake during normally  
    service water pumps' intake (e.g., Bay 13) during normally scheduled surveillances and
scheduled operability surveillances and sample to verify biocide residual concentration.  
    sample to verify biocide residual concentration.
This was contrary to the licensees Generic Letter 89-13 Program commitments (refer to  
    Root cause report 776598-08 was revised on January 9, 2009. Revision 1 included an
inspection report 05000237/2008-005; 05000249/2008-005 Section 1R15 for more  
    additional causal factor which stated that a potential existed for a significant section of
details). Corrective actions included injection of biocide into the containment cooling  
    the CCSW pump discharge piping to not receive a lethal biocide concentration for the
service water pumps' intake (e.g., Bay 13) during normally scheduled surveillances and  
    required contact time to ensure a 100 percent mortality rate for the control of
sample to verify biocide residual concentration.  
    macrofoulants. This was due to the leak-by of the 2(3)-1501-3A(B), Unit 2(3) LPCI Hx
Root cause report 776598-08 was revised on January 9, 2009. Revision 1 included an  
    A(B) tube side discharge motor operated valves (MOVs). If leakage past these valves
additional causal factor which stated that a potential existed for a significant section of  
    occurs, then the untreated service water CCSW keepfill (strained river water) will supply
the CCSW pump discharge piping to not receive a lethal biocide concentration for the  
    an equivalent volume of makeup water into the CCSW pump common discharge header
required contact time to ensure a 100 percent mortality rate for the control of  
    and result in the dilution of any chemical biocide present in the piping. This portion of
macrofoulants. This was due to the leak-by of the 2(3)-1501-3A(B), Unit 2(3) LPCI Hx  
    the pipe is located upstream of the LPCI Hxs and it is in this portion of the pipe where
A(B) tube side discharge motor operated valves (MOVs). If leakage past these valves  
    the licensee postulates the Asiatic clams are growing and eventually getting transported
occurs, then the untreated service water CCSW keepfill (strained river water) will supply  
    to the Hxs.
an equivalent volume of makeup water into the CCSW pump common discharge header  
    On May 22, 2009, RCR 776598-08 was revised again. Revision 2 added action
and result in the dilution of any chemical biocide present in the piping. This portion of  
    number 776598-50 to track a Unit 2(3) biocide chemical injection configuration change to
the pipe is located upstream of the LPCI Hxs and it is in this portion of the pipe where  
    completion. This configuration change shall inject biocide into the CCSW keepfill service
the licensee postulates the Asiatic clams are growing and eventually getting transported  
                                                  33                                  Enclosure
to the Hxs.  
On May 22, 2009, RCR 776598-08 was revised again. Revision 2 added action  
number 776598-50 to track a Unit 2(3) biocide chemical injection configuration change to  
completion. This configuration change shall inject biocide into the CCSW keepfill service  


      water to eliminate biocide dilution resulting from leak-by of the 2-1501-3A, 2-1501-3B,
      3-1501-3A and 3-1501-3B valves. This configuration change is schedule to be installed
      in April 2010 on Unit 2 and May of 2010 on Unit 3. The purpose of this new biocide
34
      injection skid is to eliminate the Asiatic clam population residing in the Unit 2 and Unit 3
Enclosure
      CCSW piping.
water to eliminate biocide dilution resulting from leak-by of the 2-1501-3A, 2-1501-3B,  
      The inspectors inquired why there was such a long lead time for the injection skid
3-1501-3A and 3-1501-3B valves. This configuration change is schedule to be installed  
      modification. Through discussions with engineering management in December 2009, it
in April 2010 on Unit 2 and May of 2010 on Unit 3. The purpose of this new biocide  
      became clear that the modification was thought to be for budgetary reasons only, and
injection skid is to eliminate the Asiatic clam population residing in the Unit 2 and Unit 3  
      that the skid was to reduce the amount, and therefore the cost, of biocide that was being
CCSW piping.  
      injected. Engineering management thought that sufficient amounts of biocide were
The inspectors inquired why there was such a long lead time for the injection skid  
      being injected to adequately kill the Asiatic clams in the piping even though root cause
modification. Through discussions with engineering management in December 2009, it  
      report 776598-08, revision 1 dated January 9, 2009, stated that an additional causal
became clear that the modification was thought to be for budgetary reasons only, and  
      factor potential existed for a significant section of the CCSW pump discharge piping to
that the skid was to reduce the amount, and therefore the cost, of biocide that was being  
      not receive a lethal biocide concentration for the required contact time to ensure a
injected. Engineering management thought that sufficient amounts of biocide were  
      100 percent mortality rate for the control of macrofoulants.
being injected to adequately kill the Asiatic clams in the piping even though root cause  
  (3) Effectiveness of Corrective Actions to Preclude Repetition
report 776598-08, revision 1 dated January 9, 2009, stated that an additional causal  
      From January through September 2009, the licensee failed to take corrective actions to
factor potential existed for a significant section of the CCSW pump discharge piping to  
      prelude repetition of a condition meeting the licensee's definition of a significant
not receive a lethal biocide concentration for the required contact time to ensure a  
      condition adverse to quality, associated with both Unit 2 and Unit 3 CCSW systems
100 percent mortality rate for the control of macrofoulants.  
      which affected the performance of the LPCI heat exchangers. Specifically, the licensee
(3) Effectiveness of Corrective Actions to Preclude Repetition  
      failed to provide a sufficient Asiatic clam lethal concentration of 8 PPM for the required
From January through September 2009, the licensee failed to take corrective actions to  
      minimum 18 hour contact time to ensure a 100 percent mortality rate for Asiatic clams
prelude repetition of a condition meeting the licensee's definition of a significant  
      which was necessary to ensure that the heat exchangers continued to meet their design
condition adverse to quality, associated with both Unit 2 and Unit 3 CCSW systems  
      basis heat removal requirements. The failure to perform these actions caused the
which affected the performance of the LPCI heat exchangers. Specifically, the licensee  
      blocking of the 2A LPCI Hx tubes by Asiatic clams which resulted in the degraded
failed to provide a sufficient Asiatic clam lethal concentration of 8 PPM for the required  
      thermal performance of the Hx. Licensee planned corrective actions include the
minimum 18 hour contact time to ensure a 100 percent mortality rate for Asiatic clams  
      installation of a temporary modification to provide temporary keepfill that is expected to
which was necessary to ensure that the heat exchangers continued to meet their design  
      provide better chemical treatment of the CCSW piping upstream of the LPCI Hxs. This
basis heat removal requirements. The failure to perform these actions caused the  
      violation was determined to be of very low safety significance because even though the
blocking of the 2A LPCI Hx tubes by Asiatic clams which resulted in the degraded  
      2A LPCI Hx was degraded it was able to perform the required design safety function.
thermal performance of the Hx. Licensee planned corrective actions include the  
  b. Findings
installation of a temporary modification to provide temporary keepfill that is expected to  
      The inspectors determined that the failure to take corrective action to preclude repetition
provide better chemical treatment of the CCSW piping upstream of the LPCI Hxs. This  
      of heat exchanger blockage by providing a sufficient Asiatic clam lethal concentration of
violation was determined to be of very low safety significance because even though the  
      8PPM for the required minimum 18 hour contact time to ensure a 100 percent mortality
2A LPCI Hx was degraded it was able to perform the required design safety function.  
      rate was a licensee-identified violation and is documented in Section 4OA7 of this report.
b.  
4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)
Findings  
.1   (Closed) Licensee Event Report (LER) 05000237/2009-001-00; 05000249/2009-001-00,
The inspectors determined that the failure to take corrective action to preclude repetition  
      Common Mode Failure of Reactor Building Isolation Dampers
of heat exchanger blockage by providing a sufficient Asiatic clam lethal concentration of  
      This event, which occurred on February 6, 2009, was identified as a result of a licensee
8PPM for the required minimum 18 hour contact time to ensure a 100 percent mortality  
      review of failures of reactor building ventilation isolation dampers at Dresden and
rate was a licensee-identified violation and is documented in Section 4OA7 of this report.  
      another Exelon facility. Licensee failure analysis determined the damper failure
4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)  
      mechanism to be the result of inadequate lubrication of internal parts and installation of
.1  
      upgraded solenoid valves that was completed in January of 2009. The NRC identified
(Closed) Licensee Event Report (LER) 05000237/2009-001-00; 05000249/2009-001-00,  
                                                      34                                  Enclosure
Common Mode Failure of Reactor Building Isolation Dampers  
This event, which occurred on February 6, 2009, was identified as a result of a licensee  
review of failures of reactor building ventilation isolation dampers at Dresden and  
another Exelon facility. Licensee failure analysis determined the damper failure  
mechanism to be the result of inadequate lubrication of internal parts and installation of  
upgraded solenoid valves that was completed in January of 2009. The NRC identified  


    the slow response to identifying the common mode failure and failure to write trending
    condition reports to document the adverse trend. Inspectors verified replacement
    solenoid valves continued to perform correctly and other corrective actions put in place
35
    were appropriate to correct the procedural non-compliance issues. Documents reviewed
Enclosure
    as part of this inspection are listed in the Attachment to this report. A NCV was written in
the slow response to identifying the common mode failure and failure to write trending  
    inspection report 05000237/2009002; 05000249/2009002 as 05000237/2009002-04.
condition reports to document the adverse trend. Inspectors verified replacement  
    This LER is closed.
solenoid valves continued to perform correctly and other corrective actions put in place  
    This event follow-up review constituted one sample as defined in IP 71153-05.
were appropriate to correct the procedural non-compliance issues. Documents reviewed  
.2   (Closed) LER 249/2009-001-00, Unit 3 Group 1 Isolation and Automatic Reactor Scram
as part of this inspection are listed in the Attachment to this report. A NCV was written in  
  a. Inspection Scope
inspection report 05000237/2009002; 05000249/2009002 as 05000237/2009002-04.
    The inspectors reviewed LER 249/2009-001-00, Unit 3 Group 1 Isolation and Automatic
This LER is closed.  
    Reactor Scram, to ensure that the issues documented in the report were adequately
This event follow-up review constituted one sample as defined in IP 71153-05.  
    addressed in the licensees corrective action program. The inspectors interviewed plant
.2  
    personnel and reviewed operating and maintenance procedures to ensure that generic
(Closed) LER 249/2009-001-00, Unit 3 Group 1 Isolation and Automatic Reactor Scram  
    issues were captured appropriately. The inspectors reviewed operator logs, issue
a.  
    reports, the Updated Final Safety Analysis Report, and other documents to verify the
Inspection Scope  
    statements contained in the LER. This LER is closed.
The inspectors reviewed LER 249/2009-001-00, Unit 3 Group 1 Isolation and Automatic  
    This event follow-up review constituted one sample as defined in IP 71153-05.
Reactor Scram, to ensure that the issues documented in the report were adequately  
  b. Findings
addressed in the licensees corrective action program. The inspectors interviewed plant  
    Introduction: A finding of very low significance (Green) involving a NCV of TS 5.4.1 was
personnel and reviewed operating and maintenance procedures to ensure that generic  
    self-revealed when Unit 3 experienced an automatic reactor scram and Group 1 primary
issues were captured appropriately. The inspectors reviewed operator logs, issue  
    containment isolation signal (PCIS) when operators were restoring the reactor water
reports, the Updated Final Safety Analysis Report, and other documents to verify the  
    cleanup (RWCU) system with the reactor at pressure. Station procedure DOP 1200-03,
statements contained in the LER. This LER is closed.  
    RWCU System Operation with the Reactor at Pressure, Revision 51, failed to identify
This event follow-up review constituted one sample as defined in IP 71153-05.  
    the correct position of motor operated valve (MOV), 3-1201-7, RWCU System Return to
b.  
    Reactor. This procedural deficiency caused a pressure pulse that resulted in a reactor
Findings  
    water level Low-Low Group 1 Isolation Signal and Unit 3 reactor scram.
Introduction: A finding of very low significance (Green) involving a NCV of TS 5.4.1 was  
    Description: On October 3, 2009, Unit 3 experienced an automatic reactor scram and
self-revealed when Unit 3 experienced an automatic reactor scram and Group 1 primary  
    Group 1 PCIS. Due to the Group 1 PCIS, the inboard and outboard main steam
containment isolation signal (PCIS) when operators were restoring the reactor water  
    isolation valves closed as designed. In addition, PCIS Group 2 and Group 3 isolations
cleanup (RWCU) system with the reactor at pressure. Station procedure DOP 1200-03,  
    were received and verified complete. Operators manually initiated the isolation
RWCU System Operation with the Reactor at Pressure, Revision 51, failed to identify  
    condenser to control reactor pressure within limits.
the correct position of motor operated valve (MOV), 3-1201-7, RWCU System Return to  
    The RWCU system had tripped earlier on October 2, 2009. On October 3, 2009, prior to
Reactor. This procedural deficiency caused a pressure pulse that resulted in a reactor  
    the reactor scram, operators were restoring the reactor water cleanup system per station
water level Low-Low Group 1 Isolation Signal and Unit 3 reactor scram.  
    procedure DOP 1200-03, RWCU System Operation with the Reactor at Pressure,
Description: On October 3, 2009, Unit 3 experienced an automatic reactor scram and  
    Revision 51. Per the procedure, RWCU was being filled and heated in the blowdown
Group 1 PCIS. Due to the Group 1 PCIS, the inboard and outboard main steam  
    mode with a flow path from the reactor pressure vessel (RPV) to the main condenser.
isolation valves closed as designed. In addition, PCIS Group 2 and Group 3 isolations  
    While the fill was being performed, the 3-1201-7 valve, Unit 3 RWCU System Return to
were received and verified complete. Operators manually initiated the isolation  
    Reactor, was closed. Reactor water cleanup system operation in the blowdown mode
condenser to control reactor pressure within limits.  
    with the 3-1201-7 valve closed resulted in: (1) heat up and expansion of the water
The RWCU system had tripped earlier on October 2, 2009. On October 3, 2009, prior to  
    volume upstream of the 3-1201-7 valve (area of high pressure), and (2) cooling and
the reactor scram, operators were restoring the reactor water cleanup system per station  
                                                    35                                Enclosure
procedure DOP 1200-03, RWCU System Operation with the Reactor at Pressure,  
Revision 51. Per the procedure, RWCU was being filled and heated in the blowdown  
mode with a flow path from the reactor pressure vessel (RPV) to the main condenser.  
While the fill was being performed, the 3-1201-7 valve, Unit 3 RWCU System Return to  
Reactor, was closed. Reactor water cleanup system operation in the blowdown mode  
with the 3-1201-7 valve closed resulted in: (1) heat up and expansion of the water  
volume upstream of the 3-1201-7 valve (area of high pressure), and (2) cooling and  


contraction of the water volume downstream of the 3-1201-7 valve (area of low
pressure). This condition created a high differential pressure across the valve.
A root cause investigation determined that under these conditions, when the 3-1201-7
36
valve was opened, the pressurized water upstream of the valve flashed to steam in the
Enclosure
lower pressure region downstream of the valve. The resulting pressure pulse was
contraction of the water volume downstream of the 3-1201-7 valve (area of low  
sensed by the RPV level transmitters, resulting in a Reactor Water Level Low SCRAM
pressure). This condition created a high differential pressure across the valve.  
Signal and Reactor Water Level Low-Low Group 1 Isolation Signal.
The licensee determined that the probable cause for the pressure pulse initiating the
A root cause investigation determined that under these conditions, when the 3-1201-7  
Reactor Water Level Low-Low Group 1 Isolation Signal and Unit 3 Reactor SCRAM was
valve was opened, the pressurized water upstream of the valve flashed to steam in the  
a latent procedural deficiency. DOP 1200-03 provided inadequate guidance for the
lower pressure region downstream of the valve. The resulting pressure pulse was  
3-1201-7 valve position during system startup with the RPV at pressure. In GEK-32399,
sensed by the RPV level transmitters, resulting in a Reactor Water Level Low SCRAM  
Dresden 3 Instrumentation Subsystem of the Reactor Water Cleanup System,
Signal and Reactor Water Level Low-Low Group 1 Isolation Signal.  
Section 3-11, Normal Operation, Table 3-6, Valve Positions for Cleanup System
Startup during Normal Operations, the reactor vendor, General Electric, recommended
The licensee determined that the probable cause for the pressure pulse initiating the  
that the Reactor Return Isolation Valve 1201-7 be in the open position for RWCU system
Reactor Water Level Low-Low Group 1 Isolation Signal and Unit 3 Reactor SCRAM was  
startup when the reactor is at power. This recommendation was not incorporated in
a latent procedural deficiency. DOP 1200-03 provided inadequate guidance for the  
DOP 1200-03. Procedure DOP 1200-03, step G.1.g.(2) , gave the option to the operator
3-1201-7 valve position during system startup with the RPV at pressure. In GEK-32399,  
to open MOV 3-1201-7 at that step or later on in the procedure. During this event, the
Dresden 3 Instrumentation Subsystem of the Reactor Water Cleanup System,  
3-1201-7 valve was opened later on in the procedure.
Section 3-11, Normal Operation, Table 3-6, Valve Positions for Cleanup System  
Analysis: The inspectors determined that the licensees failure to include pertinent
Startup during Normal Operations, the reactor vendor, General Electric, recommended  
information regarding valve position during RWCU system startup with the RPV at
that the Reactor Return Isolation Valve 1201-7 be in the open position for RWCU system  
pressure in DOP 1200-03 was a performance deficiency warranting a significance
startup when the reactor is at power. This recommendation was not incorporated in  
evaluation. Using IMC 0612, Appendix B, Issue Screening, issued on
DOP 1200-03. Procedure DOP 1200-03, step G.1.g.(2) , gave the option to the operator  
December 4, 2008, the inspectors determined that this finding was more than minor
to open MOV 3-1201-7 at that step or later on in the procedure. During this event, the  
because it impacted the Initiating Events Cornerstone objective to limit the likelihood of
3-1201-7 valve was opened later on in the procedure.  
those events that upset plant stability and challenge critical safety functions during
shutdown as well as at power operations. The failure to maintain adequate procedures
Analysis: The inspectors determined that the licensees failure to include pertinent  
for the restoration of systems can result in events (i.e., reactor scram) that upset plant
information regarding valve position during RWCU system startup with the RPV at  
stability. This condition caused a pressure pulse that was sensed by the RPV level
pressure in DOP 1200-03 was a performance deficiency warranting a significance  
transmitters, resulting in a Reactor Water Level Low SCRAM Signal and Reactor Water
evaluation. Using IMC 0612, Appendix B, Issue Screening, issued on  
Level Low-Low Group 1 Isolation Signal. This finding had a cross-cutting aspect in the
December 4, 2008, the inspectors determined that this finding was more than minor  
area of Human Performance Resources because the licensee did not provide complete,
because it impacted the Initiating Events Cornerstone objective to limit the likelihood of  
accurate and up-to-date procedures to plant personnel. H.2(c)
those events that upset plant stability and challenge critical safety functions during  
The inspectors completed a Phase 1 significance determination of this issue using
shutdown as well as at power operations. The failure to maintain adequate procedures  
IMC 0609, Significance Determination Process, Attachment 0609.04, dated
for the restoration of systems can result in events (i.e., reactor scram) that upset plant  
January 10, 2008. The inspectors determined that the finding impacted the Initiating
stability. This condition caused a pressure pulse that was sensed by the RPV level  
Events Cornerstone. The inspectors answered No to the question on Transient
transmitters, resulting in a Reactor Water Level Low SCRAM Signal and Reactor Water  
Initiators under the Initiating Events Cornerstone column on Table 4a because the
Level Low-Low Group 1 Isolation Signal. This finding had a cross-cutting aspect in the  
finding did not contribute to both the likelihood of a reactor trip AND the likelihood that
area of Human Performance Resources because the licensee did not provide complete,  
mitigating equipment or functions will not be available. Therefore, the issue screened as
accurate and up-to-date procedures to plant personnel. H.2(c)  
having very low safety significance (Green).
The inspectors completed a Phase 1 significance determination of this issue using  
Enforcement: The inspectors determined that the licensees failure to include pertinent
IMC 0609, Significance Determination Process, Attachment 0609.04, dated  
information, regarding valve position during RWCU system startup with the RPV at
January 10, 2008. The inspectors determined that the finding impacted the Initiating  
pressure, in DOP 1200-03 was a violation of Dresden Nuclear Power Station Technical
Events Cornerstone. The inspectors answered No to the question on Transient  
Specification Section 5.4.1, Procedures. Section 5.4.1 states, in part, that written
Initiators under the Initiating Events Cornerstone column on Table 4a because the  
procedures shall be established, implemented, and maintained covering applicable
finding did not contribute to both the likelihood of a reactor trip AND the likelihood that  
                                              36                                  Enclosure
mitigating equipment or functions will not be available. Therefore, the issue screened as  
having very low safety significance (Green).  
Enforcement: The inspectors determined that the licensees failure to include pertinent  
information, regarding valve position during RWCU system startup with the RPV at  
pressure, in DOP 1200-03 was a violation of Dresden Nuclear Power Station Technical  
Specification Section 5.4.1, Procedures. Section 5.4.1 states, in part, that written  
procedures shall be established, implemented, and maintained covering applicable  


  procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, issued
  February 1978. Procedures addressing startup of boiling water reactor (BWR) systems,
  including the reactor cleanup system, are recommended in Section 4. of Appendix A to
37
  this Regulatory Guide.
Enclosure
  Contrary to the above, on October 3, 2009, the licensee failed to include pertinent
procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, issued  
  guidance regarding 3-1201-7 valve position during system startup with the RPV at
February 1978. Procedures addressing startup of boiling water reactor (BWR) systems,  
  pressure. This failure resulted in an automatic reactor scram and Group 1 primary
including the reactor cleanup system, are recommended in Section 4. of Appendix A to  
  containment isolation signal. This event was entered into the licensees corrective action
this Regulatory Guide.  
  program as IR 974426, U3 Group 1 Isolation and Reactor Scram. Corrective actions
Contrary to the above, on October 3, 2009, the licensee failed to include pertinent  
  by the licensee included revising procedure DOP 1200-03, requiring the 3-1201-7 valve
guidance regarding 3-1201-7 valve position during system startup with the RPV at  
  to be open prior to initiating RWCU system fill and vent activities. Because this violation
pressure. This failure resulted in an automatic reactor scram and Group 1 primary  
  was of very low safety significance and it was entered into the licensees corrective
containment isolation signal. This event was entered into the licensees corrective action  
  action program, this violation is being treated as a NCV, consistent with Section VI.A.1 of
program as IR 974426, U3 Group 1 Isolation and Reactor Scram. Corrective actions  
  the NRC Enforcement Policy. (NCV 05000249/2009005-08)
by the licensee included revising procedure DOP 1200-03, requiring the 3-1201-7 valve  
.3 (Closed) Licensee Event Report (LER) 05000237/2009-003-00; 05000249/2009-003-00,
to be open prior to initiating RWCU system fill and vent activities. Because this violation  
  Emergency Diesel Generator Oil Leak and Unresolved Item (URI)
was of very low safety significance and it was entered into the licensees corrective  
  05000237/2009003-01; 05000249/2009003-01, Failure of 2/3 Emergency Diesel
action program, this violation is being treated as a NCV, consistent with Section VI.A.1 of  
  Generator Due to Lube Oil Leak on Y Strainer
the NRC Enforcement Policy. (NCV 05000249/2009005-08)  
  This event, which occurred on June 2, 2009, during performance of the monthly
.3  
  surveillance on the Unit 2/3 Emergency Diesel Generator (EDG), resulted in an oil leak
(Closed) Licensee Event Report (LER) 05000237/2009-003-00; 05000249/2009-003-00,  
  of approximately one-half gallon per minute from the turbocharger lubricating oil Y
Emergency Diesel Generator Oil Leak and Unresolved Item (URI)  
  strainer end cap plug. The initial event was documented in Section 1R12 of report
05000237/2009003-01; 05000249/2009003-01, Failure of 2/3 Emergency Diesel  
  05000237/2009003; 05000249/2009003 as an Unresolved Item
Generator Due to Lube Oil Leak on Y Strainer  
  (URI 05000237/2009003-01; 05000249/2009003-01.)
This event, which occurred on June 2, 2009, during performance of the monthly  
  Documents reviewed as part of this inspection are listed in the Attachment to this report.
surveillance on the Unit 2/3 Emergency Diesel Generator (EDG), resulted in an oil leak  
  Both the above referenced URI and this LER are closed.
of approximately one-half gallon per minute from the turbocharger lubricating oil Y  
  This event follow-up review constituted one sample as defined in IP 71153-05.
strainer end cap plug. The initial event was documented in Section 1R12 of report  
  Introduction: A finding of very low safety significance and associated NCV of
05000237/2009003; 05000249/2009003 as an Unresolved Item  
  10 CFR Part 50, Appendix B, Criterion IV, Procurement Document Control, was
(URI 05000237/2009003-01; 05000249/2009003-01.)  
  self-revealed for the failure to ensure a safety-related plug was ordered and installed
Documents reviewed as part of this inspection are listed in the Attachment to this report.
  where required in the 2/3 EDG turbo lube oil Y strainer.
Both the above referenced URI and this LER are closed.  
  Description: On June 02, 2009, the 2/3 EDG was operating in support of the monthly
This event follow-up review constituted one sample as defined in IP 71153-05.  
  surveillance run in accordance with DOS 6600-01, Diesel Generator Surveillance
Introduction: A finding of very low safety significance and associated NCV of  
  Tests. At approximately 3:39 am the 2/3 EDG was 25 minutes into the loaded run when
10 CFR Part 50, Appendix B, Criterion IV, Procurement Document Control, was  
  an oil leak of approximately 1/2 gallon per minute was identified at the Turbo Lube Oil
self-revealed for the failure to ensure a safety-related plug was ordered and installed  
  System Y strainer.
where required in the 2/3 EDG turbo lube oil Y strainer.  
  The 2/3 EDG was secured at approximately 3:47 a.m., and the turbo oil circulating pump
Description: On June 02, 2009, the 2/3 EDG was operating in support of the monthly  
  was secured approximately 45 minutes after the engine shutdown to allow heat removal
surveillance run in accordance with DOS 6600-01, Diesel Generator Surveillance  
  from the engines turbo charger to prevent damage. Inspection of the turbo lube oil
Tests. At approximately 3:39 am the 2/3 EDG was 25 minutes into the loaded run when  
  system Y strainer identified the source of the leakage to be coming from a pipe plug on
an oil leak of approximately 1/2 gallon per minute was identified at the Turbo Lube Oil  
  the Y strainer end cap. Further investigation revealed the pipe plug installed in the
System Y strainer.  
  strainer end cap to be a black 3/8 inch NPT plastic shipping plug instead of the
The 2/3 EDG was secured at approximately 3:47 a.m., and the turbo oil circulating pump  
  safety-related steel plug required by design documents.
was secured approximately 45 minutes after the engine shutdown to allow heat removal  
                                                37                                  Enclosure
from the engines turbo charger to prevent damage. Inspection of the turbo lube oil  
system Y strainer identified the source of the leakage to be coming from a pipe plug on  
the Y strainer end cap. Further investigation revealed the pipe plug installed in the  
strainer end cap to be a black 3/8 inch NPT plastic shipping plug instead of the  
safety-related steel plug required by design documents.  


As immediate corrective action, the licensee installed a 3/8 inch NPT ASTM A-105
carbon steel hex head threaded pipe plug, Cat ID 43255-1 in the strainer end cap of the
2/3 EDG using work order (WO) 1240346-01 and approximately 30 gallons of oil were
38
added to the engine reservoir. Surveillance procedure DOS 6600-01, Diesel Generator
Enclosure
Surveillance Tests, was completed satisfactorily with no leakage observed from the
As immediate corrective action, the licensee installed a 3/8 inch NPT ASTM A-105  
Turbo Lube Oil System Y strainer. The 2/3 EDG was declared operable at 11:05 p.m.
carbon steel hex head threaded pipe plug, Cat ID 43255-1 in the strainer end cap of the  
on June 2, 2009. Extent of condition reviews were performed on the four other similar
2/3 EDG using work order (WO) 1240346-01 and approximately 30 gallons of oil were  
diesel generators; two safety-related and two station blackout emergency diesels.
added to the engine reservoir. Surveillance procedure DOS 6600-01, Diesel Generator  
No other non-conforming conditions were identified.
Surveillance Tests, was completed satisfactorily with no leakage observed from the  
During the subsequent root cause investigation, the licensee determined that the
Turbo Lube Oil System Y strainer. The 2/3 EDG was declared operable at 11:05 p.m.  
Unit 2/3 EDG Turbo Lube Oil Y Strainer (EPN 2/3-6661) and Circulating Oil Y Strainer
on June 2, 2009. Extent of condition reviews were performed on the four other similar  
(EPN 2/3-6672) were replaced on March 24, 2008, under WO 922770-01 due to wear on
diesel generators; two safety-related and two station blackout emergency diesels.
the strainer blowdown caps. On March 24, 2008, the licensee completed steps 8, 9
No other non-conforming conditions were identified.  
and 10 of WO 922770-01. This work scope removed the old lube oil strainer 2/3-6661
During the subsequent root cause investigation, the licensee determined that the  
from the system, cleaned piping and pipe nipples prior to installing the strainer
Unit 2/3 EDG Turbo Lube Oil Y Strainer (EPN 2/3-6661) and Circulating Oil Y Strainer  
(replacing pipe nipples as required), and installed the new Mueller strainer snug tight
(EPN 2/3-6672) were replaced on March 24, 2008, under WO 922770-01 due to wear on  
using site approved sealant. On March 25, 2008, the license performed step 11 of the
the strainer blowdown caps. On March 24, 2008, the licensee completed steps 8, 9  
work package requiring the strainers to be painted with designated orange paint once
and 10 of WO 922770-01. This work scope removed the old lube oil strainer 2/3-6661  
the strainers have been installed. The painting step was important because from this
from the system, cleaned piping and pipe nipples prior to installing the strainer  
step on there is no way to visually identify the non-conforming condition. Interviews with
(replacing pipe nipples as required), and installed the new Mueller strainer snug tight  
the individual performing the installation and painting indicated that they did not identify
using site approved sealant. On March 25, 2008, the license performed step 11 of the  
the plug as a plastic foreign material exclusion (FME) plug and therefore took no action
work package requiring the strainers to be painted with designated orange paint once  
to replace it as was required by procedure MA-AA-716-008, Foreign Material Exclusion
the strainers have been installed. The painting step was important because from this  
Program.
step on there is no way to visually identify the non-conforming condition. Interviews with  
The post-maintenance test (PMT) was performed on the Y strainers on
the individual performing the installation and painting indicated that they did not identify  
March 27, 2008, per WO 922770-02. The licensee performed visual inspections of the
the plug as a plastic foreign material exclusion (FME) plug and therefore took no action  
Y strainers at system pressure. The inspections passed with no identified leakage.
to replace it as was required by procedure MA-AA-716-008, Foreign Material Exclusion  
Subsequent investigation revealed that Turbo Lube Oil Strainer replaced under
Program.  
WO 922770-01 in March 2008 was assigned Exelon Catalog Identification
The post-maintenance test (PMT) was performed on the Y strainers on  
Number 38412-1. The Y strainer was manufactured commercial grade by Mueller
March 27, 2008, per WO 922770-02. The licensee performed visual inspections of the  
Steam Specialty under Model No. 352M. Exelon purchased the Y strainer from
Y strainers at system pressure. The inspections passed with no identified leakage.
Engine Systems Incorporated (ESI) under Purchase Order (PO) 00000703 Revision 001
Subsequent investigation revealed that Turbo Lube Oil Strainer replaced under  
as a Quality Level 1 Nuclear Safety-Related Item. The PO stated, Strainer, Y-Type,
WO 922770-01 in March 2008 was assigned Exelon Catalog Identification  
1 IN, Bronze ASTM B62, Threaded (FNPT), Class 250, 20 Mesh Size Stainless Steel
Number 38412-1. The Y strainer was manufactured commercial grade by Mueller  
Screen, supplied with threaded gasketed cap and plug; and rated for 400 PSI @ 150 F
Steam Specialty under Model No. 352M. Exelon purchased the Y strainer from  
(WOG); and seismically qualified per Report Number ST-MSS-352M-1 issued by ESI.
Engine Systems Incorporated (ESI) under Purchase Order (PO) 00000703 Revision 001  
The Mueller Steam Specialty catalog Cut Sheet that was pasted in the supply database
as a Quality Level 1 Nuclear Safety-Related Item. The PO stated, Strainer, Y-Type,  
for CAT ID 38412-1 on July 3, 2006, indicated Y strainer Blowoff Outlets are
1 IN, Bronze ASTM B62, Threaded (FNPT), Class 250, 20 Mesh Size Stainless Steel  
unplugged. Additionally, the current Mueller Steam Specialty online specification sheet
Screen, supplied with threaded gasketed cap and plug; and rated for 400 PSI @ 150 F  
for Y Strainers (ES-MS-351M-358) states Blow Off Outlets: Not normally furnished
(WOG); and seismically qualified per Report Number ST-MSS-352M-1 issued by ESI.  
with plug. Plug available, specify with order.
The Mueller Steam Specialty catalog Cut Sheet that was pasted in the supply database  
Since the part number specified by Dresden in the procurement document does not
for CAT ID 38412-1 on July 3, 2006, indicated Y strainer Blowoff Outlets are  
include a plug in the end cap, Engine Systems Incorporated (ESI) included the plastic
unplugged. Additionally, the current Mueller Steam Specialty online specification sheet  
plug for FME purposes. The plug is black only because that was the color that ESI had
for Y Strainers (ES-MS-351M-358) states Blow Off Outlets: Not normally furnished  
on hand at the time. Personnel from ESI stated that when performing the qualification
with plug. Plug available, specify with order.  
testing for the part two strainers are ordered, one for the testing and one to ship to the
Since the part number specified by Dresden in the procurement document does not  
customer. An appropriate plug is installed in the one used for qualification testing.
include a plug in the end cap, Engine Systems Incorporated (ESI) included the plastic  
                                              38                                  Enclosure
plug for FME purposes. The plug is black only because that was the color that ESI had  
on hand at the time. Personnel from ESI stated that when performing the qualification  
testing for the part two strainers are ordered, one for the testing and one to ship to the  
customer. An appropriate plug is installed in the one used for qualification testing.  


The strainer purchased for WO 922770-01 was shipped to Dresden Site Supply and had
a receipt inspection performed on December 19, 2007. The inspection accepted the
strainer with no discrepancies noted in the Quality Receipt Inspection Package and
39
without questioning if the plug installed in the strainer end cap should have been a
Enclosure
suitable pressure retaining pipe plug or a shipping plug.
The strainer purchased for WO 922770-01 was shipped to Dresden Site Supply and had  
The licensee concluded from their investigation that the root cause for this issue was the
a receipt inspection performed on December 19, 2007. The inspection accepted the  
failure to have a purchase order that clearly documented the need for the safety-related
strainer with no discrepancies noted in the Quality Receipt Inspection Package and  
strainer cap plugs.
without questioning if the plug installed in the strainer end cap should have been a  
Analysis: The inspectors determined that the failure to document the requirement for a
suitable pressure retaining pipe plug or a shipping plug.  
safety-related strainer cap plug in the purchase order was a performance deficiency.
The licensee concluded from their investigation that the root cause for this issue was the  
The finding was determined to be more than minor because the finding was similar to
failure to have a purchase order that clearly documented the need for the safety-related  
IMC 0612, Appendix E, Example 5 c, in that, an incorrect and inadequate part was
strainer cap plugs.  
installed and the system was returned to service. Therefore, this performance deficiency
Analysis: The inspectors determined that the failure to document the requirement for a  
also impacted the Mitigating Systems Cornerstone objective to ensure the availability,
safety-related strainer cap plug in the purchase order was a performance deficiency.
reliability, and capability of systems that respond to initiating events to prevent
The finding was determined to be more than minor because the finding was similar to  
undesirable consequences.
IMC 0612, Appendix E, Example 5 c, in that, an incorrect and inadequate part was  
The inspectors determined the finding could be evaluated using the SDP in accordance
installed and the system was returned to service. Therefore, this performance deficiency  
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
also impacted the Mitigating Systems Cornerstone objective to ensure the availability,  
Initial Screening and Characterization of Findings, Table 4a, dated January 10, 2008,
reliability, and capability of systems that respond to initiating events to prevent  
for Mitigating Systems because the 2/3 EDG is a mitigating system that could impact the
undesirable consequences.  
long term or short term decay heat removal capability during a loss of offsite power
The inspectors determined the finding could be evaluated using the SDP in accordance  
event. The inspectors answered yes to the question, Does the finding represent
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -  
actual loss of safety function of a single train for greater than its Technical Specification
Initial Screening and Characterization of Findings, Table 4a, dated January 10, 2008,  
Allowed Outage Time? The inspectors performed a SDP phase 2 evaluation using the
for Mitigating Systems because the 2/3 EDG is a mitigating system that could impact the  
pre-solved spreadsheet for the Risk-Informed Inspection Notebook for Dresden Nuclear
long term or short term decay heat removal capability during a loss of offsite power  
Power Station. The assumption that EDG 2/3 was unavailable for greater than 30 days
event. The inspectors answered yes to the question, Does the finding represent  
resulted in a finding of low to moderate risk significance (White). The Region III senior
actual loss of safety function of a single train for greater than its Technical Specification  
reactor analyst (SRA) performed a SDP phase 3 evaluation of the EDG 2/3 failure to run.
Allowed Outage Time? The inspectors performed a SDP phase 2 evaluation using the  
The SRA used the Dresden Standardized Plant Analysis Risk (SPAR) Model,
pre-solved spreadsheet for the Risk-Informed Inspection Notebook for Dresden Nuclear  
Revision 3.50, and assumed that the EDG would have failed to run in response to any
Power Station. The assumption that EDG 2/3 was unavailable for greater than 30 days  
demand that would have occurred since the last successful 24 hour endurance run.
resulted in a finding of low to moderate risk significance (White). The Region III senior  
This exposure period was approximately 89 days. The delta CDF for internal events
reactor analyst (SRA) performed a SDP phase 3 evaluation of the EDG 2/3 failure to run.
was estimated to be 4.0E-7/yr. The dominant sequence was a loss of offsite power
The SRA used the Dresden Standardized Plant Analysis Risk (SPAR) Model,  
event followed by common cause failure of all emergency power and the failure to
Revision 3.50, and assumed that the EDG would have failed to run in response to any  
recover either offsite or onsite power.
demand that would have occurred since the last successful 24 hour endurance run.
Since the delta CDF was greater than 1.0E-7/yr, the SRA evaluated the risk contribution
This exposure period was approximately 89 days. The delta CDF for internal events  
from external events. The risk contribution from seismic events was determined to be
was estimated to be 4.0E-7/yr. The dominant sequence was a loss of offsite power  
negligible because the frequency of seismically-induced loss of offsite power events was
event followed by common cause failure of all emergency power and the failure to  
estimated to be much less than plant-centered, switchyard-centered, or grid-related loss
recover either offsite or onsite power.  
of offsite power events. The fire risk contribution was estimated using information from
Since the delta CDF was greater than 1.0E-7/yr, the SRA evaluated the risk contribution  
the licensees Individual Plant Examination for External Events (IPEEE) submitted
from external events. The risk contribution from seismic events was determined to be  
in 2000. Fire-induced loss of offsite power events were assumed to occur for fires in
negligible because the frequency of seismically-induced loss of offsite power events was  
control room panel 902-8 (Unit 3 panel 903-8), panel 923-2, and for fires in the auxiliary
estimated to be much less than plant-centered, switchyard-centered, or grid-related loss  
electric equipment room (AEER). The SRA used the fire ignition frequencies from the
of offsite power events. The fire risk contribution was estimated using information from  
IPEEE and calculated conditional core damage probabilities using the SPAR model for
the licensees Individual Plant Examination for External Events (IPEEE) submitted  
plant-centered loss of offsite power events with the failure of the 2/3 EDG to estimate the
in 2000. Fire-induced loss of offsite power events were assumed to occur for fires in  
change in core damage frequency for fire events that did not result in control room
control room panel 902-8 (Unit 3 panel 903-8), panel 923-2, and for fires in the auxiliary  
                                              39                                  Enclosure
electric equipment room (AEER). The SRA used the fire ignition frequencies from the  
IPEEE and calculated conditional core damage probabilities using the SPAR model for  
plant-centered loss of offsite power events with the failure of the 2/3 EDG to estimate the  
change in core damage frequency for fire events that did not result in control room  


evacuation. Fires in the AEER contributed less than 1.0E-7/yr to the change in CDF.
For the control room, fires in panel 902-8 (903-8) were evaluated and determined to be
potential risk contributors because the fire damage caused a loss of offsite power and
40
resulted in the unavailability of the Division II power supplies. For panel fires that were
Enclosure
not suppressed within 15 minutes, the SRA used a non-suppression probability of 3.4E-3
evacuation. Fires in the AEER contributed less than 1.0E-7/yr to the change in CDF.
from the licensees IPEEE and concluded that operators would evacuate the control
For the control room, fires in panel 902-8 (903-8) were evaluated and determined to be  
room and use the fire-specific safe shutdown procedures. With the 2/3 EDG unavailable
potential risk contributors because the fire damage caused a loss of offsite power and  
due to the performance deficiency, only the station blackout (SBO) diesel generator
resulted in the unavailability of the Division II power supplies. For panel fires that were  
would remain available to provide power. The SRA used SPAR-H to estimate the
not suppressed within 15 minutes, the SRA used a non-suppression probability of 3.4E-3  
human error probability (HEP) for aligning the SBO diesel generator during fire scenarios
from the licensees IPEEE and concluded that operators would evacuate the control  
and estimated a value of 0.4 assuming that diagnosis of the loss of power and need for
room and use the fire-specific safe shutdown procedures. With the 2/3 EDG unavailable  
the SBO diesel generator would dominate the HEP. The performance-shaping factors
due to the performance deficiency, only the station blackout (SBO) diesel generator  
for stress and procedures were adjusted in the HEP calculation. The procedures for
would remain available to provide power. The SRA used SPAR-H to estimate the  
using the SBO DG were considered to be incomplete because the Dresden fire safe
human error probability (HEP) for aligning the SBO diesel generator during fire scenarios  
shutdown procedures do not address the use of the SBO diesel generator and operators
and estimated a value of 0.4 assuming that diagnosis of the loss of power and need for  
would be required to use separate procedures for non-fire scenarios to line-up the SBO
the SBO diesel generator would dominate the HEP. The performance-shaping factors  
DG. Also, the stress of the fire-induced LOOP with failure of the 2/3 EDG was assumed
for stress and procedures were adjusted in the HEP calculation. The procedures for  
to be high. The risk contribution from control room fire scenarios was estimated to be
using the SBO DG were considered to be incomplete because the Dresden fire safe  
approximately 4.0E-7/yr. The total delta CDF from internal and external scenarios was
shutdown procedures do not address the use of the SBO diesel generator and operators  
estimated to be approximately 8.0E-7/yr. The risk estimate is conservative because it
would be required to use separate procedures for non-fire scenarios to line-up the SBO  
does not account for any successful run time of the diesel generators and provides only
DG. Also, the stress of the fire-induced LOOP with failure of the 2/3 EDG was assumed  
limited credit for the use of SBO diesel generators in fire scenarios.
to be high. The risk contribution from control room fire scenarios was estimated to be  
The risk contribution from large early release frequency (LERF) was also evaluated.
approximately 4.0E-7/yr. The total delta CDF from internal and external scenarios was  
IMC 0609, Appendix H, Containment Integrity Significance Determination Process
estimated to be approximately 8.0E-7/yr. The risk estimate is conservative because it  
assigns a screening LERF factor of 1.0 to station blackout core damage sequences for
does not account for any successful run time of the diesel generators and provides only  
BWRs with Mark I containments. This would result in a delta LERF estimate of
limited credit for the use of SBO diesel generators in fire scenarios.  
8.0E-7/yr, which represents low to moderate significance. However, based on a
The risk contribution from large early release frequency (LERF) was also evaluated.
previous Dresden phase 3 SDP evaluation and other SDP evaluations of plants with
IMC 0609, Appendix H, Containment Integrity Significance Determination Process  
Mark 1 containments, a much lower LERF factor of 0.1 is judged to be appropriate for
assigns a screening LERF factor of 1.0 to station blackout core damage sequences for  
this SDP phase 3 evaluation. As a result, the risk significance of the finding is estimated
BWRs with Mark I containments. This would result in a delta LERF estimate of  
to be less than 1.0E-6/yr delta CDF and less than 1.0E-7/yr delta LERF, which
8.0E-7/yr, which represents low to moderate significance. However, based on a  
represents a finding of very low safety significance (Green).
previous Dresden phase 3 SDP evaluation and other SDP evaluations of plants with  
In addition, the failure of plant maintenance personnel to identify and remove the plastic
Mark 1 containments, a much lower LERF factor of 0.1 is judged to be appropriate for  
foreign material exclusion plug prior to equipment return to service was a significant
this SDP phase 3 evaluation. As a result, the risk significance of the finding is estimated  
contributor to the finding. Step 4.2.5.3.B of MA-AA-716-008, Foreign Material Exclusion
to be less than 1.0E-6/yr delta CDF and less than 1.0E-7/yr delta LERF, which  
Program, states, in part, New parts/components/equipment to be installed in the plant
represents a finding of very low safety significance (Green).  
should be carefully inspected to ensure that no foreign material (e.g., packaging
In addition, the failure of plant maintenance personnel to identify and remove the plastic  
material, shipping plugs, desiccants, and lubricant/preservatives used for shipping or
foreign material exclusion plug prior to equipment return to service was a significant  
storage) are present to prevent introduction to the system. Failure of plant personnel to
contributor to the finding. Step 4.2.5.3.B of MA-AA-716-008, Foreign Material Exclusion  
question the plastic shipping plug before the equipment was installed and returned to
Program, states, in part, New parts/components/equipment to be installed in the plant  
service was not in compliance with the procedure and, therefore, inspectors determined
should be carefully inspected to ensure that no foreign material (e.g., packaging  
that this event was cross-cutting in Human Performance, Work Practices, Procedural
material, shipping plugs, desiccants, and lubricant/preservatives used for shipping or  
Compliance for failure to follow of personnel to follow the procedure. H.4(b)
storage) are present to prevent introduction to the system. Failure of plant personnel to  
Enforcement: 10 CFR Part 50, Appendix B, Criterion IV, Procurement Document
question the plastic shipping plug before the equipment was installed and returned to  
Control, requires, in part, that measures shall be established to assure that applicable
service was not in compliance with the procedure and, therefore, inspectors determined  
regulatory requirements, design bases, and other requirements which are necessary to
that this event was cross-cutting in Human Performance, Work Practices, Procedural  
assure adequate quality are suitably included or referenced in the documents for
Compliance for failure to follow of personnel to follow the procedure. H.4(b)  
                                              40                                  Enclosure
Enforcement: 10 CFR Part 50, Appendix B, Criterion IV, Procurement Document  
Control, requires, in part, that measures shall be established to assure that applicable  
regulatory requirements, design bases, and other requirements which are necessary to  
assure adequate quality are suitably included or referenced in the documents for  


    procurement of material, equipment, and services, whether purchased by the applicant
    or by its contractors or subcontractors.
    Contrary to the above, from December 2007 until June 2009, the licensee did not include
41
    a requirement which was necessary to assure adequate quality in the document for
Enclosure
    procurement of the 2/3 EDG Turbo Lube Oil Y Strainer, CAT ID 38412-1. Specifically,
procurement of material, equipment, and services, whether purchased by the applicant  
    the purchase order did not specify what type of plug was required to be supplied and
or by its contractors or subcontractors.  
    installed in the strainer cap prior to installation. The strainer was supplied with a plug
Contrary to the above, from December 2007 until June 2009, the licensee did not include  
    installed that was neither designed nor constructed sufficiently to prevent a leak that
a requirement which was necessary to assure adequate quality in the document for  
    resulted in the inoperability of the 2/3 EDG for greater than 30 days. Immediate
procurement of the 2/3 EDG Turbo Lube Oil Y Strainer, CAT ID 38412-1. Specifically,  
    corrective action to correct the leak included installation of a qualified plug in the strainer,
the purchase order did not specify what type of plug was required to be supplied and  
    post-maintenance testing of the 2/3 EDG, and inspection of all other diesel generators to
installed in the strainer cap prior to installation. The strainer was supplied with a plug  
    ensure the same condition did not exist on another machine. The catalogue ID was
installed that was neither designed nor constructed sufficiently to prevent a leak that  
    revised to include a pressure retaining pipe plug with approved material and a
resulted in the inoperability of the 2/3 EDG for greater than 30 days. Immediate  
    requirement was added for a quality inspection to be performed to inspect the strainer
corrective action to correct the leak included installation of a qualified plug in the strainer,
    for metallic pipe plug in blow down port. Individual procedure compliance issues were
post-maintenance testing of the 2/3 EDG, and inspection of all other diesel generators to  
    addressed through the stations performance improvement initiatives. Because this
ensure the same condition did not exist on another machine. The catalogue ID was  
    violation was of very low safety significance and it was entered into the licensees
revised to include a pressure retaining pipe plug with approved material and a  
    corrective action program as IR 926605, this violation is being treated as an NCV,
requirement was added for a quality inspection to be performed to inspect the strainer  
    consistent with Section VI.A.1 of the NRC Enforcement Policy.
for metallic pipe plug in blow down port. Individual procedure compliance issues were  
    (NCV 05000237/2009005-09; 05000249/2009005-09)
addressed through the stations performance improvement initiatives. Because this  
.4   Electro-Hydraulic Control (EHC) Fluid Leaking From Stop Valve 3-5699-MSV4-FA
violation was of very low safety significance and it was entered into the licensees  
    Resulting in Forced Outage D3F49
corrective action program as IR 926605, this violation is being treated as an NCV,  
  a. Inspection Scope
consistent with Section VI.A.1 of the NRC Enforcement Policy.
    The inspectors reviewed the plants response to an EHC leak on Dresden Unit 3 that
(NCV 05000237/2009005-09; 05000249/2009005-09)  
    caused the unit to come offline. Documents reviewed in this inspection are listed in the
.4  
    Attachment to this report.
Electro-Hydraulic Control (EHC) Fluid Leaking From Stop Valve 3-5699-MSV4-FA  
    This event follow-up review constituted one sample as defined in IP 71153-05.
Resulting in Forced Outage D3F49  
  b. Findings
a.  
    Introduction: The inspectors identified an unresolved item regarding the regulatory
Inspection Scope  
    requirements associated with the circumstances surrounding the Unit 3 turbine trip on
The inspectors reviewed the plants response to an EHC leak on Dresden Unit 3 that  
    November 6, 2009.
caused the unit to come offline. Documents reviewed in this inspection are listed in the  
    Description: On November 5, 2009, at 8:53 p.m., Unit 3 Control Room received the
Attachment to this report.  
    following alarm: 903-7 B-6, EHC [electro-hydraulic control] RESERVOIR LVL HI/LO
This event follow-up review constituted one sample as defined in IP 71153-05.  
    (reference IR 989641) indicating a rate of change in the EHC reservoir at 1.3" in 100 hrs
b.  
    or greater. A non-licensed operator (NLO) was dispatched to stage a barrel of EHC fluid
Findings  
    for addition. Preparations were made for a heater bay entry to look for leaks.
Introduction: The inspectors identified an unresolved item regarding the regulatory  
    A Unit 3 heater bay entry was made and it was determined that the Unit 3 Main Turbine
requirements associated with the circumstances surrounding the Unit 3 turbine trip on  
    Stop Valve (MSV) # 4 had an EHC leak from the fast-acting solenoid valve
November 6, 2009.  
    (3-5699-MSV4-FA). The leak was determined to be approximately 4-5 gallons of fluid
Description: On November 5, 2009, at 8:53 p.m., Unit 3 Control Room received the  
    per hour. A report from the field was that reservoir level had dropped about 1.1" in the
following alarm: 903-7 B-6, EHC [electro-hydraulic control] RESERVOIR LVL HI/LO  
    last 12 hours. Between 12:50 a.m. and 3:43 a.m. on November 6, 2009, the licensee
(reference IR 989641) indicating a rate of change in the EHC reservoir at 1.3" in 100 hrs  
    added two barrels of EHC fluid to the EHC reservoir.
or greater. A non-licensed operator (NLO) was dispatched to stage a barrel of EHC fluid  
                                                      41                                  Enclosure
for addition. Preparations were made for a heater bay entry to look for leaks.  
A Unit 3 heater bay entry was made and it was determined that the Unit 3 Main Turbine  
Stop Valve (MSV) # 4 had an EHC leak from the fast-acting solenoid valve  
(3-5699-MSV4-FA). The leak was determined to be approximately 4-5 gallons of fluid  
per hour. A report from the field was that reservoir level had dropped about 1.1" in the  
last 12 hours. Between 12:50 a.m. and 3:43 a.m. on November 6, 2009, the licensee  
added two barrels of EHC fluid to the EHC reservoir.  


      On November 6, 2009, between 9:00 a.m. and 2:00 p.m., licensee management
      conducted meetings regarding the repair of the leak on MSV #4. The plan called for
      starting to down power Unit 3 to 650 Mwe for a planned 3:00 p.m. entry into the heater
42
      bay to repair the valve. The decision to go to 650 Mwe was to reduce the dose rate in
Enclosure
      the area and extend stay time for the repair.
On November 6, 2009, between 9:00 a.m. and 2:00 p.m., licensee management  
      At approximately 3:00 p.m., while staging for entry to repair the leak, Operations
conducted meetings regarding the repair of the leak on MSV #4. The plan called for  
      personnel informed the NLO, staged to isolate the oil supply to the leaking valve, that
starting to down power Unit 3 to 650 Mwe for a planned 3:00 p.m. entry into the heater  
      level in the EHC reservoir was dropping quickly, and requested the NLO to enter the
bay to repair the valve. The decision to go to 650 Mwe was to reduce the dose rate in  
      pipeway as soon as possible.
the area and extend stay time for the repair.  
      At approximately 3:05 p.m., the NLO observed oil spraying profusely from the bottom
At approximately 3:00 p.m., while staging for entry to repair the leak, Operations  
      area of #4 Main Stop Valve and the area of the solenoid that was going to be changed
personnel informed the NLO, staged to isolate the oil supply to the leaking valve, that  
      out. The NLO immediately contacted the control room to report what was observed and
level in the EHC reservoir was dropping quickly, and requested the NLO to enter the  
      a decision was made to take the turbine offline. At 3:32 p.m., the Unit 3 Turbine was
pipeway as soon as possible.  
      tripped.
At approximately 3:05 p.m., the NLO observed oil spraying profusely from the bottom  
      The licensee had not completed their root cause investigation by the end of the
area of #4 Main Stop Valve and the area of the solenoid that was going to be changed  
      inspection period. The inspectors planned to review the root cause investigation to
out. The NLO immediately contacted the control room to report what was observed and  
      determine if there were any violations of NRC requirements and that appropriate
a decision was made to take the turbine offline. At 3:32 p.m., the Unit 3 Turbine was  
      corrective actions were applied. (URI 05000249/2009005-10)
tripped.  
4OA5 Other Activities
The licensee had not completed their root cause investigation by the end of the  
.1   Quarterly Resident Inspector Observations of Security Personnel and Activities
inspection period. The inspectors planned to review the root cause investigation to  
  a. Inspection Scope
determine if there were any violations of NRC requirements and that appropriate  
      During the inspection period, the inspectors conducted observations of security force
corrective actions were applied. (URI 05000249/2009005-10)  
      personnel and activities to ensure that the activities were consistent with licensee
4OA5 Other Activities  
      security procedures and regulatory requirements relating to nuclear plant security.
.1  
      These observations took place during both normal and off-normal plant working hours.
Quarterly Resident Inspector Observations of Security Personnel and Activities  
      These quarterly resident inspector observations of security force personnel and activities
a.  
      did not constitute any additional inspection samples. Rather, they were considered an
Inspection Scope  
      integral part of the inspectors' normal plant status review and inspection activities.
During the inspection period, the inspectors conducted observations of security force  
  b. Findings
personnel and activities to ensure that the activities were consistent with licensee  
      No findings of significance were identified.
security procedures and regulatory requirements relating to nuclear plant security.
.2   Institute of Nuclear Power Operations (INPO) Plant Assessment Report Review
These observations took place during both normal and off-normal plant working hours.  
  a. Inspection Scope
These quarterly resident inspector observations of security force personnel and activities  
      The inspectors reviewed the interim report for the INPO plant assessment of Dresden
did not constitute any additional inspection samples. Rather, they were considered an  
      Station conducted in September 2009. The inspectors reviewed the report to ensure
integral part of the inspectors' normal plant status review and inspection activities.  
      that issues identified were consistent with the NRC perspectives of licensee
b.  
      performance and to verify if any significant safety issues were identified that required
Findings  
      further NRC follow-up.
No findings of significance were identified.  
                                                    42                                  Enclosure
.2  
Institute of Nuclear Power Operations (INPO) Plant Assessment Report Review  
a.  
Inspection Scope  
The inspectors reviewed the interim report for the INPO plant assessment of Dresden  
Station conducted in September 2009. The inspectors reviewed the report to ensure  
that issues identified were consistent with the NRC perspectives of licensee  
performance and to verify if any significant safety issues were identified that required  
further NRC follow-up.


  b. Findings
    No findings of significance were identified.
.3   Open) NRC TI 2515/177, Managing Gas Accumulation in Emergency Core Cooling,
43
    Decay Heat Removal and Containment Spray Systems (NRC Generic Letter 2008-01)
Enclosure
  a. Inspection Scope
b.  
    On November 10, 2008, the inspectors conducted a walkdown of the Unit 2 High
Findings
    Pressure Coolant Injection (HPCI) discharge piping inside the Unit 2 X-Area in sufficient
No findings of significance were identified.  
    detail to reasonably assure the acceptability of the licensees walkdowns (TI 2515/177,
.3  
    Section 04.02.d). The inspectors also verified that the information obtained during the
Open) NRC TI 2515/177, Managing Gas Accumulation in Emergency Core Cooling,  
    licensees walkdown was consistent with the items identified during the inspectors
Decay Heat Removal and Containment Spray Systems (NRC Generic Letter 2008-01)  
    independent walkdown (TI 2515/177, Section 04.02.c.3).
a.  
    The inspectors verified that Piping and Instrumentation Diagrams (P&IDs) accurately
Inspection Scope  
    described the subject system, that the P&IDs were up-to-date with respect to recent
On November 10, 2008, the inspectors conducted a walkdown of the Unit 2 High  
    hardware changes, and any discrepancies between as-built configurations and the
Pressure Coolant Injection (HPCI) discharge piping inside the Unit 2 X-Area in sufficient  
    P&IDs were documented and entered into the CAP for resolution (TI 2515/177, Section
detail to reasonably assure the acceptability of the licensees walkdowns (TI 2515/177,  
    04.02.b).
Section 04.02.d). The inspectors also verified that the information obtained during the  
    In addition, the inspectors reviewed the licensees isometric drawings that describe the
licensees walkdown was consistent with the items identified during the inspectors  
    HPCI system configurations to verify that the licensee had acceptably confirmed the
independent walkdown (TI 2515/177, Section 04.02.c.3).  
    accuracy of the drawings (TI 2515/177, Section 04.02.a). The inspectors considered the
The inspectors verified that Piping and Instrumentation Diagrams (P&IDs) accurately  
    following related to the isometric drawings:
described the subject system, that the P&IDs were up-to-date with respect to recent  
    *       High point vents were identified.
hardware changes, and any discrepancies between as-built configurations and the  
    *       High points that do not have vents were acceptably recognizable.
P&IDs were documented and entered into the CAP for resolution (TI 2515/177, Section  
    *       Other areas where gas can accumulate and potentially impact subject system
04.02.b).  
              operability, such as at orifices in horizontal pipes, isolated branch lines, heat
In addition, the inspectors reviewed the licensees isometric drawings that describe the  
              exchangers, improperly sloped piping, and under closed valves, were acceptably
HPCI system configurations to verify that the licensee had acceptably confirmed the  
              described in the drawings or in referenced documentation.
accuracy of the drawings (TI 2515/177, Section 04.02.a). The inspectors considered the  
    *       Horizontal pipe centerline elevation deviations and pipe slopes in nominally
following related to the isometric drawings:  
              horizontal lines that exceed specified criteria were identified.
*  
    *       All pipes and fittings were clearly shown.
High point vents were identified.  
    *       The drawings were up-to-date with respect to recent hardware changes and that
*  
              any discrepancies between as-built configurations and the drawings were
High points that do not have vents were acceptably recognizable.  
              documented and entered into the CAP for resolution.
*  
    The licensee indicated that even though they possess isometric drawings of the HPCI
Other areas where gas can accumulate and potentially impact subject system  
    system, they do not rely upon any isometric drawings for gas management in that
operability, such as at orifices in horizontal pipes, isolated branch lines, heat  
    system. Therefore, the inspectors were unable to verify the above considerations.
exchangers, improperly sloped piping, and under closed valves, were acceptably  
    In their review, the inspectors did identify discrepancies in the available isometric
described in the drawings or in referenced documentation.  
    drawings between what was shown on the drawing and the as-built condition of the
*  
    system. The discrepancies identified were in drawings M-1151C-2 and ISI-510 Sheet 2
Horizontal pipe centerline elevation deviations and pipe slopes in nominally  
    and were associated with the 2-23126-3/4-L vent line. The licensee determined that
horizontal lines that exceed specified criteria were identified.  
    drawing M-1151C-2 does not need to be updated because it was created to support a
*  
    seismic analysis done before the 2-23126-3/4-L vent line was installed and was not
All pipes and fittings were clearly shown.  
    intended to be updated. They determined that drawing ISI-510 Sheet 2 does not need to
*  
                                                    43                                    Enclosure
The drawings were up-to-date with respect to recent hardware changes and that  
any discrepancies between as-built configurations and the drawings were  
documented and entered into the CAP for resolution.  
The licensee indicated that even though they possess isometric drawings of the HPCI  
system, they do not rely upon any isometric drawings for gas management in that  
system. Therefore, the inspectors were unable to verify the above considerations.  
In their review, the inspectors did identify discrepancies in the available isometric  
drawings between what was shown on the drawing and the as-built condition of the  
system. The discrepancies identified were in drawings M-1151C-2 and ISI-510 Sheet 2  
and were associated with the 2-23126-3/4-L vent line. The licensee determined that  
drawing M-1151C-2 does not need to be updated because it was created to support a  
seismic analysis done before the 2-23126-3/4-L vent line was installed and was not  
intended to be updated. They determined that drawing ISI-510 Sheet 2 does not need to  


      be updated because it is a system pressure testing walkdown isometric drawing,
      therefore, the discrepancy does not impact the purpose and use of the drawing. These
      conclusions were documented in AR 1014280.
44
      Documents reviewed are listed in the Attachment to this report.
Enclosure
      This inspection effort counts towards the completion of TI 2515/177, which will be closed
be updated because it is a system pressure testing walkdown isometric drawing,  
      in a later Inspection Report.
therefore, the discrepancy does not impact the purpose and use of the drawing. These  
  b. Findings
conclusions were documented in AR 1014280.  
      No findings of significance were identified.
Documents reviewed are listed in the Attachment to this report.  
4OA6 Management Meetings
This inspection effort counts towards the completion of TI 2515/177, which will be closed  
.1   Exit Meeting Summary
in a later Inspection Report.  
      On January 14, 2010, the inspectors presented the inspection results to Mr. T. Hanley,
b.  
      and other members of the licensee staff. The licensee acknowledged the issues
Findings  
      presented. The inspectors confirmed that none of the potential report input discussed
No findings of significance were identified.  
      was considered proprietary.
4OA6 Management Meetings  
.2   Interim Exit Meeting
.1  
      Interim exits were conducted for:
Exit Meeting Summary  
      *       The results of the inservice inspection with Site Vice-President T. Hanley on
On January 14, 2010, the inspectors presented the inspection results to Mr. T. Hanley,  
              November 13, 2009.
and other members of the licensee staff. The licensee acknowledged the issues  
      *       The results of the As-Low-As-Reasonably-Achievable Planning and Controls
presented. The inspectors confirmed that none of the potential report input discussed  
              inspection with the Site Vice President, Mr. T. Hanley, on November 17, 2009.
was considered proprietary.  
      *       The annual review of Emergency Action Level and Emergency Plan changes
.2  
              with the licensee's Emergency Preparedness Manager, Mr. P. Quealy, via
Interim Exit Meeting  
              telephone on December 21, 2009.
Interim exits were conducted for:  
      The inspectors confirmed that none of the potential report input discussed was
*  
      considered proprietary.
The results of the inservice inspection with Site Vice-President T. Hanley on  
4OA7 Licensee-Identified Violations
November 13, 2009.  
      The following violation of very low safety significance (Green) was identified by the
*  
      licensee and is a violation of NRC requirements which meets the criteria of Section
The results of the As-Low-As-Reasonably-Achievable Planning and Controls  
      VI.A.1 of the NRC Enforcement Policy, for being dispositioned as an NCV.
inspection with the Site Vice President, Mr. T. Hanley, on November 17, 2009.  
          *   Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Criterion XVI,
*  
              Corrective Action, states, in part, Measures shall be established to assure that
The annual review of Emergency Action Level and Emergency Plan changes  
              conditions adverse to quality, such as failures, malfunctions, deficiencies,
with the licensee's Emergency Preparedness Manager, Mr. P. Quealy, via  
              deviations, defective material and equipment, and non-conformances are
telephone on December 21, 2009.  
              promptly identified and corrected. In the case of significant conditions adverse to
              quality, the measures shall assure that the cause of the condition is determined
The inspectors confirmed that none of the potential report input discussed was  
              and corrective action taken to preclude repetition. A significant condition
considered proprietary.  
              adverse to quality for both Unit 2 and Unit 3 containment cooling service water
                                                      44                                Enclosure
4OA7 Licensee-Identified Violations  
The following violation of very low safety significance (Green) was identified by the  
licensee and is a violation of NRC requirements which meets the criteria of Section  
VI.A.1 of the NRC Enforcement Policy, for being dispositioned as an NCV.  
*  
Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Criterion XVI,  
Corrective Action, states, in part, Measures shall be established to assure that  
conditions adverse to quality, such as failures, malfunctions, deficiencies,  
deviations, defective material and equipment, and non-conformances are  
promptly identified and corrected. In the case of significant conditions adverse to  
quality, the measures shall assure that the cause of the condition is determined  
and corrective action taken to preclude repetition. A significant condition  
adverse to quality for both Unit 2 and Unit 3 containment cooling service water  


          (CCSW) systems was identified by the licensee in RCR 776598-08,
          Dresden 3-1503-B, 3B Low Pressure Coolant Injection (LPCI) / Containment
          Cooling Heat Exchanger (HX) Failure to Meet Design Basis Heat Removal
45
          Capability Due to Inadequate Programmatic Control of Macrofoulants,
Enclosure
          Revision 1, on January 9, 2009. Procedure LS-AA-125, Corrective Action
(CCSW) systems was identified by the licensee in RCR 776598-08,  
          Program (CAP) Procedure, revision 13, defines significant condition adverse to
Dresden 3-1503-B, 3B Low Pressure Coolant Injection (LPCI) / Containment  
          quality (SCAQ), in part, as A condition which, if left uncorrected, could have a
Cooling Heat Exchanger (HX) Failure to Meet Design Basis Heat Removal  
          serious effect on safety or reliability. In addition, recurring deficiencies or errors
Capability Due to Inadequate Programmatic Control of Macrofoulants,  
          that cannot be dispositioned or brought into conformance by established
Revision 1, on January 9, 2009. Procedure LS-AA-125, Corrective Action  
          corrective action systems," are considered SCAQs. The inspectors determined
Program (CAP) Procedure, revision 13, defines significant condition adverse to  
          that the conditions described in RCR 776598-08, met the licensee's definition of
quality (SCAQ), in part, as A condition which, if left uncorrected, could have a  
          a significant condition adverse to quality. Contrary to the above requirements,
serious effect on safety or reliability. In addition, recurring deficiencies or errors  
          from January through September 2009, the licensee failed to take measures to
that cannot be dispositioned or brought into conformance by established  
          assure that the cause of the condition (blockage of the LPCI heat exchangers)
corrective action systems," are considered SCAQs. The inspectors determined  
          was determined and corrective action taken to preclude the repetition for a
that the conditions described in RCR 776598-08, met the licensee's definition of  
          significant condition adverse to quality on both Unit 2 and Unit 3 CCSW systems.
a significant condition adverse to quality. Contrary to the above requirements,  
          Specifically, the licensee failed to prevent the recurrence of Asiatic clam
from January through September 2009, the licensee failed to take measures to  
          blockage in the 2A LPCI Hx tubes which resulted in the degraded thermal
assure that the cause of the condition (blockage of the LPCI heat exchangers)  
          performance of the Hx. Licensee planned corrective actions included installation
was determined and corrective action taken to preclude the repetition for a  
          of a temporary modification to provide temporary keepfill that was expected to
significant condition adverse to quality on both Unit 2 and Unit 3 CCSW systems.
          provide better chemical treatment of the CCSW piping upstream of the LPCI Hxs,
Specifically, the licensee failed to prevent the recurrence of Asiatic clam  
          and a permanent injection skid for biocide to provide for long term assurance of
blockage in the 2A LPCI Hx tubes which resulted in the degraded thermal  
          effective chemical treatment. This violation was determined to be of very low
performance of the Hx. Licensee planned corrective actions included installation  
          safety significance because even though the 2A LPCI Hx was degraded it was
of a temporary modification to provide temporary keepfill that was expected to  
          able to perform the required design safety function.
provide better chemical treatment of the CCSW piping upstream of the LPCI Hxs,  
ATTACHMENT: SUPPLEMENTAL INFORMATION
and a permanent injection skid for biocide to provide for long term assurance of  
                                                  45                                    Enclosure
effective chemical treatment. This violation was determined to be of very low  
safety significance because even though the 2A LPCI Hx was degraded it was  
able to perform the required design safety function.
ATTACHMENT: SUPPLEMENTAL INFORMATION  


                              SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
Licensee
1
T. Hanley, Site Vice President
Attachment
S. Marik, Station Plant Manager
SUPPLEMENTAL INFORMATION  
H. Bush, Radiation Protection Manager
KEY POINTS OF CONTACT  
B. Casey, Engineering Programs (Braidwood)
Licensee  
H. Do, Exelon Corporate ISI
T. Hanley, Site Vice President  
B. Finley, Security Manager
S. Marik, Station Plant Manager  
D. Glick, Shipping Specialist
H. Bush, Radiation Protection Manager  
T. Green, Nondestructive Examination Services
B. Casey, Engineering Programs (Braidwood)  
J. Griffin, Regulatory Assurance - NRC Coordinator
H. Do, Exelon Corporate ISI  
D. Gronek, Operations Director
B. Finley, Security Manager  
J. Hansen, Corporate Licensing
D. Glick, Shipping Specialist  
L. Jordan, Training Director
T. Green, Nondestructive Examination Services  
R. Kalb, Chemistry
J. Griffin, Regulatory Assurance - NRC Coordinator  
P. Karaba, Maintenance Director
D. Gronek, Operations Director  
J. Kish, Engineering Programs
J. Hansen, Corporate Licensing  
M. Kluge, Design Engineer
L. Jordan, Training Director  
D. Leggett, Nuclear Oversight Manager
R. Kalb, Chemistry  
R. Laburn, Radiation Protection
P. Karaba, Maintenance Director  
M. Marchionda, Regulatory Assurance Manager
J. Kish, Engineering Programs  
J. Miller, Nondestructive Examination Services
M. Kluge, Design Engineer  
P. OConnor, Licensed Operator Requalification Training Lead
D. Leggett, Nuclear Oversight Manager  
M. Overstreet, Lead Radiation Protection Supervisor
R. Laburn, Radiation Protection  
C. Podczerwinski, Maintenance Rule Coordinator
M. Marchionda, Regulatory Assurance Manager  
P. Quealy, Emergency Preparedness Manager
J. Miller, Nondestructive Examination Services  
E. Rowley, Chemistry
P. OConnor, Licensed Operator Requalification Training Lead  
R. Rybak, Regulatory Assurance
M. Overstreet, Lead Radiation Protection Supervisor  
J. Sipek, Engineering Director
C. Podczerwinski, Maintenance Rule Coordinator  
N. Starcevich, Radiation Protection Instrumentation Coordinator
P. Quealy, Emergency Preparedness Manager  
J. Strmec, Chemistry Manager
E. Rowley, Chemistry  
S. Vercelli, Work Management Director
R. Rybak, Regulatory Assurance  
NRC
J. Sipek, Engineering Director  
M. Ring, Chief, Division of Reactor Projects, Branch 1
N. Starcevich, Radiation Protection Instrumentation Coordinator  
IEMA
J. Strmec, Chemistry Manager  
R. Zuffa, Illinois Emergency Management Agency
S. Vercelli, Work Management Director  
R. Schulz, Illinois Emergency Management Agency
                                                    1          Attachment
NRC  
M. Ring, Chief, Division of Reactor Projects, Branch 1  
IEMA  
R. Zuffa, Illinois Emergency Management Agency  
R. Schulz, Illinois Emergency Management Agency  


                  LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened:
05000237/2009005-01         NCV Operating Personnel Incorrectly Placed Clearance Tags
2
                                (Section 1R04)
Attachment
05000237/2009009-02         NCV NRC Inspector-Identified Control Room Alarm Isolation
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED  
                                Valve Out-of-Position (Section 1R15)
Opened:  
05000237/2009005-03         NCV Preconditioning the Unit 2 Emergency Diesel Generator
05000237/2009005-01  
                                Prior to Performing TS Surveillance Requirements
NCV  
                                (Section 1R19)
Operating Personnel Incorrectly Placed Clearance Tags  
05000237/2009005-04         URI 2/3 Emergency Diesel Generator (EDG) Overvoltage
05000249/2009005-04             During Division I Undervoltage Surveillance (1R19)
05000237/2005009-05         NCV Failure to Follow the Master Refueling Procedure During
                                Movement of Fuel Assembly JLU569 (Section 1R20)
05000249/2009005-06         NCV Mispositioning of a Unit 3 Control Rod at Power
                                (Section 1R22)
(Section 1R04)  
05000237/2009005-07         URI Changes to EAL HU6 Potentially Decreased the
05000237/2009009-02  
                                Effectiveness of the Plans without Prior NRC Approval
NCV  
                                (1EP4)
NRC Inspector-Identified Control Room Alarm Isolation  
05000249/2009005-08         NCV Procedural Deficiency Causing a Pressure Pulse
                                Resulting in a Reactor Water Level Low-Low Group 1
                                Isolation Signal and Unit 3 Reactor Scram
                                (Section 4OA3.2)
05000237/2009005-09         NCV Failure to Ensure a Safety-Related Plug was Ordered and
05000249/2009005-09             Installed in the 2/3 Emergency Diesel Generator
Valve Out-of-Position (Section 1R15)  
                                Turbo Lube Oil Y Strainer (Section 4OA3.3)
05000237/2009005-03  
05000249/2009005-10         URI Electro-Hydraulic Control (EHC) Fluid Leaking From Stop
NCV  
                                Valve 3-5699-MSV4-FA Resulting in Forced Outage
Preconditioning the Unit 2 Emergency Diesel Generator  
                                D3F49 (Section 4OA3.4)
Temporary Instruction 2515/177   Managing Gas Accumulation in Emergency Core Cooling,
                                Decay Heat Removal and Containment Spray Systems
                                (NRC Generic Letter 2008-01) (Section 4OA5.3)
                                                2                              Attachment
Prior to Performing TS Surveillance Requirements  
(Section 1R19)  
05000237/2009005-04  
URI  
2/3 Emergency Diesel Generator (EDG) Overvoltage  
05000249/2009005-04  
During Division I Undervoltage Surveillance (1R19)  
05000237/2005009-05  
NCV  
Failure to Follow the Master Refueling Procedure During  
Movement of Fuel Assembly JLU569 (Section 1R20)  
05000249/2009005-06  
NCV  
Mispositioning of a Unit 3 Control Rod at Power  
(Section 1R22)  
05000237/2009005-07  
URI  
Changes to EAL HU6 Potentially Decreased the  
Effectiveness of the Plans without Prior NRC Approval  
(1EP4)  
05000249/2009005-08  
NCV  
Procedural Deficiency Causing a Pressure Pulse
Resulting in a Reactor Water Level Low-Low Group 1  
Isolation Signal and Unit 3 Reactor Scram  
(Section 4OA3.2)  
05000237/2009005-09  
NCV  
Failure to Ensure a Safety-Related Plug was Ordered and  
05000249/2009005-09  
Installed in the 2/3 Emergency Diesel Generator
Turbo Lube Oil Y Strainer (Section 4OA3.3)  
05000249/2009005-10  
URI  
Electro-Hydraulic Control (EHC) Fluid Leaking From Stop  
Valve 3-5699-MSV4-FA Resulting in Forced Outage
D3F49 (Section 4OA3.4)  
Temporary Instruction 2515/177  
Managing Gas Accumulation in Emergency Core Cooling,  
Decay Heat Removal and Containment Spray Systems  
(NRC Generic Letter 2008-01) (Section 4OA5.3)  


Closed:
05000237/2009005-01       NCV   Operating Personnel Incorrectly Placed Clearance Tags
                                (Section 1R04)
3
05000237/2009009-02       NCV   NRC Inspector-Identified Control Room Alarm Isolation
Attachment
                                Valve Out-of-Position (Section 1R15)
Closed:  
05000237/2009005-03       NCV   Preconditioning the Unit 2 Emergency Diesel Generator
05000237/2009005-01  
                                Prior to Performing TS Surveillance Requirements
NCV  
                                (Section 1R19)
Operating Personnel Incorrectly Placed Clearance Tags  
05000237/2005009-05       NCV   Failure to Follow the Master Refueling Procedure During
                                Movement of Fuel Assembly JLU569 (Section 1R20)
05000249/2009005-06       NCV   Mispositioning of a Unit 3 Control Rod at Power
                                (Section 1R22)
05000249/2009005-08       NCV   Procedural Deficiency Causing a Pressure Pulse
                                Resulting in a Reactor Water Level Low-Low Group 1
(Section 1R04)  
                                Isolation Signal and Unit 3 Reactor Scram
05000237/2009009-02  
                                (Section 4OA3.2)
NCV  
05000237/2009005-09       NCV   Failure to Ensure a Safety-Related Plug was Ordered and
NRC Inspector-Identified Control Room Alarm Isolation  
05000249/2009005-09             Installed in the 2/3 Emergency Diesel Generator
                                Turbo Lube Oil Y Strainer (Section 4OA3.3)
05000237/2009004-04       URI   Inspector Identified Control Room Alarm Isolation Valve
05000249/2009004-04             Out-of-Position (1R15)
05000237/2009003-01       URI   Failure of 2/3 Emergency Diesel Generator (EDG) Due to
05000249/2009003-01             Lube Oil Leak On Y-Strainer (4OA3.3)
Valve Out-of-Position (Section 1R15)  
05000237/2009-001-00       LER   Common Mode Failure of Reactor Building Isolation
05000237/2009005-03  
05000249/2009-001-00             Dampers (4OA3.1)
NCV  
05000249/2009-001-00       LER   Unit 3 Group 1 Isolation and Automatic Reactor Scram
Preconditioning the Unit 2 Emergency Diesel Generator  
                                (4OA3.2)
05000237/2009-003-00       LER   Emergency Diesel Generator Oil Leak (4OA3.3)
05000249/2009-003-00
Discussed:
Inspection Report 05000237/2008005; 05000249/2008005, Section 1R15 (4OA2.4)
05000237/2009002-04       NCV   Failure to Take Corrective Actions to Replace a Degraded
Prior to Performing TS Surveillance Requirements
                                Valve in a Timely Manner (4OA3.1)
                                                3                              Attachment
(Section 1R19)  
05000237/2005009-05  
NCV  
Failure to Follow the Master Refueling Procedure During  
Movement of Fuel Assembly JLU569 (Section 1R20)  
05000249/2009005-06  
NCV  
Mispositioning of a Unit 3 Control Rod at Power  
(Section 1R22)  
05000249/2009005-08  
NCV  
Procedural Deficiency Causing a Pressure Pulse
Resulting in a Reactor Water Level Low-Low Group 1  
Isolation Signal and Unit 3 Reactor Scram
(Section 4OA3.2)  
05000237/2009005-09  
NCV  
Failure to Ensure a Safety-Related Plug was Ordered and  
05000249/2009005-09  
Installed in the 2/3 Emergency Diesel Generator
Turbo Lube Oil Y Strainer (Section 4OA3.3)  
05000237/2009004-04  
URI  
Inspector Identified Control Room Alarm Isolation Valve  
05000249/2009004-04  
Out-of-Position (1R15)  
05000237/2009003-01  
URI  
Failure of 2/3 Emergency Diesel Generator (EDG) Due to  
05000249/2009003-01  
Lube Oil Leak On Y-Strainer (4OA3.3)  
05000237/2009-001-00  
LER  
Common Mode Failure of Reactor Building Isolation  
05000249/2009-001-00  
Dampers (4OA3.1)  
05000249/2009-001-00  
LER  
Unit 3 Group 1 Isolation and Automatic Reactor Scram
(4OA3.2)  
05000237/2009-003-00  
LER  
Emergency Diesel Generator Oil Leak (4OA3.3)  
05000249/2009-003-00  
Discussed:  
Inspection Report 05000237/2008005; 05000249/2008005, Section 1R15 (4OA2.4)  
05000237/2009002-04  
NCV  
Failure to Take Corrective Actions to Replace a Degraded  
Valve in a Timely Manner (4OA3.1)  


                                  LIST OF DOCUMENTS REVIEWED
The following is a partial list of documents reviewed during the inspection. Inclusion on this list
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that
4
selected sections or portions of the documents were evaluated as part of the overall inspection
Attachment
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
LIST OF DOCUMENTS REVIEWED  
any part of it, unless this is stated in the body of the inspection report.
The following is a partial list of documents reviewed during the inspection. Inclusion on this list  
1R04 Equipment Alignment (71111.04)
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that  
- WO 1079566-01, Perform 250V Station Battery Service Test
selected sections or portions of the documents were evaluated as part of the overall inspection  
- C/O 76319, (ASSY) Battery 250V U2
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or  
- DOP 7500-M1/E1, Unit 2/3 Standby Gas Treatment, Revision 6
any part of it, unless this is stated in the body of the inspection report.  
1R05 Fire Protection (71111.05)
- IR 976782, NRC Observations from U3 Rx Bldg. 570 Pre-Plan Review
1R04 Equipment Alignment (71111.04)  
1R08 Inservice Inspection Activities (71111.08G)
- WO 1079566-01, Perform 250V Station Battery Service Test  
- IR 00992912; Material Certification of Recirc Piping Could not be Found; November 13, 2009
- C/O 76319, (ASSY) Battery 250V U2  
- IR 00911408; Section XI Class 2 Boundary; April 28, 2009
- DOP 7500-M1/E1, Unit 2/3 Standby Gas Treatment, Revision 6  
- IR 00889729; LPCI Heat Exchanger Recordable Indications; March 6, 2009
1R05 Fire Protection (71111.05)  
- IR 00782956; Corrosion Pipe Elbow B CST Tank; June 6, 2008
- IR 976782, NRC Observations from U3 Rx Bldg. 570 Pre-Plan Review  
- IR 00755744; 2/3 EDG Leak on Engine Block; March 28, 2008
1R08 Inservice Inspection Activities (71111.08G)  
- IR 00711323; 2/3 DGCW Pump Suction Pipe Corrosion; December 14, 2007
- IR 00992912; Material Certification of Recirc Piping Could not be Found; November 13, 2009  
- IR 00705912; Unit 2 CCSW System Corrosion; December 2, 2007
- IR 00911408; Section XI Class 2 Boundary; April 28, 2009  
- IR 00705639; DGCW Pipe Corrosion; December 2, 2007
- IR 00889729; LPCI Heat Exchanger Recordable Indications; March 6, 2009  
- IR 00695137; Unit 2 Reactor Head Flange MT Indication; November 8, 2007
- IR 00782956; Corrosion Pipe Elbow B CST Tank; June 6, 2008  
- IR 00691069; Loose Anchor Bolt on CS Line; October 31, 2007
- IR 00755744; 2/3 EDG Leak on Engine Block; March 28, 2008  
- IR 00681657; PT Rejectable Indication; October 22, 2007
- IR 00711323; 2/3 DGCW Pump Suction Pipe Corrosion; December 14, 2007  
- ASME Section XI Repair/Replacement Plan 2-1505A-12-0; April 1, 2009
- IR 00705912; Unit 2 CCSW System Corrosion; December 2, 2007  
- Certified Mill Test Report (Consolidated Power Supply); 12 Safety-Related 90 Elbow;
- IR 00705639; DGCW Pipe Corrosion; December 2, 2007  
  September 15, 2009
- IR 00695137; Unit 2 Reactor Head Flange MT Indication; November 8, 2007  
- EC 368360; Evaluation of Leakage at Bolted Connections and other Recordable Indications;
- IR 00691069; Loose Anchor Bolt on CS Line; October 31, 2007  
  Revision 0
- IR 00681657; PT Rejectable Indication; October 22, 2007  
- Examination Summary Sheet; D2R21-028 UT of PS2/201-1; November 7, 2009
- ASME Section XI Repair/Replacement Plan 2-1505A-12-0; April 1, 2009  
- Examination Summary Sheet; D2R21-029 UT of PS2-Tee/202-4B; November 7, 2009
- Certified Mill Test Report (Consolidated Power Supply); 12 Safety-Related 90 Elbow;  
- NDE Report No. 09-294; VT-3 Visual Examination; November 13, 2009
September 15, 2009  
- NDE Certification; Scott R. Erickson; UT Level III; October 6, 2009
- EC 368360; Evaluation of Leakage at Bolted Connections and other Recordable Indications;  
- Procedure GE-PDI-UT-2; PDI Generic Procedure for the Ultrasonic Examination of Austenitic
Revision 0  
  Pipe Welds; Revision 4
- Examination Summary Sheet; D2R21-028 UT of PS2/201-1; November 7, 2009  
- Procedure GE-PDI-UT-3, PDI Generic Procedure for the Ultrasonic Thru Wall Sizing in Piping
- Examination Summary Sheet; D2R21-029 UT of PS2-Tee/202-4B; November 7, 2009  
  Welds, Revision 2
- NDE Report No. 09-294; VT-3 Visual Examination; November 13, 2009  
- Procedure ER-AA-335-018, Detailed General VT-1, VT-1C, VT-3 and VT-3C Visual
- NDE Certification; Scott R. Erickson; UT Level III; October 6, 2009  
  Examination of ASME Class MC and CC Containment Surfaces and Components; Revision 5
- Procedure GE-PDI-UT-2; PDI Generic Procedure for the Ultrasonic Examination of Austenitic  
- Procedure ER-AA-335-1008; Code Acceptance and Recording Criteria for Nondestructive
Pipe Welds; Revision 4  
  Surface Examination; Revision 1
- Procedure GE-PDI-UT-3, PDI Generic Procedure for the Ultrasonic Thru Wall Sizing in Piping  
- Procedure Qualification Record; A-001; October 19, 1998
Welds, Revision 2  
- Procedure Qualification Record; A-002; March 9, 1997
- Procedure ER-AA-335-018, Detailed General VT-1, VT-1C, VT-3 and VT-3C Visual  
- Procedure Qualification Record; 1-50C; January 3, 1984
Examination of ASME Class MC and CC Containment Surfaces and Components; Revision 5  
                                                        4                              Attachment
- Procedure ER-AA-335-1008; Code Acceptance and Recording Criteria for Nondestructive  
Surface Examination; Revision 1  
- Procedure Qualification Record; A-001; October 19, 1998  
- Procedure Qualification Record; A-002; March 9, 1997  
- Procedure Qualification Record; 1-50C; January 3, 1984  


- Report No. D2R20-037; Four Indications on the Reactor Head Flange Weld (2RPV UPP
  HD/2-THD-FLG); November 11, 2007
- Weld Procedure Specification; 1-1-GTSM-PWHT; Revision 1
5
- Welder Qualification Record; W2677; October 5, 2009
Attachment
- Work Order 01189798; Replace Degraded Elbow on 2A CCSW Pump; October 22, 2009
- Report No. D2R20-037; Four Indications on the Reactor Head Flange Weld (2RPV UPP  
1R12 Maintenance Effectiveness (71111.12)
HD/2-THD-FLG); November 11, 2007  
- Z03, "Control Rod Drive Maintenance Rule Performance Criteria"
- Weld Procedure Specification; 1-1-GTSM-PWHT; Revision 1  
- IR 845878, "Scram Dump Valve Leaking", 11/17/2008
- Welder Qualification Record; W2677; October 5, 2009  
- IR 763023, "Review Maintenance Rule Functions Perform review described in In-Progress
- Work Order 01189798; Replace Degraded Elbow on 2A CCSW Pump; October 22, 2009  
  Notes", 5/30/2008
1R12 Maintenance Effectiveness (71111.12)  
- IR 842585, "Handwheel Spins with no Valve Movement", 11/09/2008
- Z03, "Control Rod Drive Maintenance Rule Performance Criteria"  
- IR 842587, "Valve Handwheel Broken", 11/09/2008
- IR 845878, "Scram Dump Valve Leaking", 11/17/2008  
- IR 843592, "HCU P6 Scram Valve Packing Leak", 11/11/2008
- IR 763023, "Review Maintenance Rule Functions Perform review described in In-Progress  
- IR 700134, "Relief Valve Continuously Lifted", 11/16/2007
Notes", 5/30/2008  
- IR 976292, "CRD Exercising and Condenser Vacuum Scram Impact U3 Restart", 10/05/2009
- IR 842585, "Handwheel Spins with no Valve Movement", 11/09/2008  
- WO 1186809, "Scram Dump Valve Leaking", 11/17/2008
- IR 842587, "Valve Handwheel Broken", 11/09/2008  
- M-34, "Diagram of Control Rod Drive Hydraulic Piping", Revision W
- IR 843592, "HCU P6 Scram Valve Packing Leak", 11/11/2008  
- TS 3.1.3, Control Rod Operability
- IR 700134, "Relief Valve Continuously Lifted", 11/16/2007  
- TS 3.1.4, Control Rod Scram Times
- IR 976292, "CRD Exercising and Condenser Vacuum Scram Impact U3 Restart", 10/05/2009  
- TS 3.1.5, Control Rod Scram Accumulators
- WO 1186809, "Scram Dump Valve Leaking", 11/17/2008  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
- M-34, "Diagram of Control Rod Drive Hydraulic Piping", Revision W  
- IR 1009039, 345 kv Line 8014 trip
- TS 3.1.3, Control Rod Operability  
1R15 Operability Evaluations (71111.15)
- TS 3.1.4, Control Rod Scram Times  
- Operability Evaluation No. 09-007, 2A LPCI Heat Exchanger (2-1503-A)
- TS 3.1.5, Control Rod Scram Accumulators  
- EC 372200, Perform Evaluation of Thermal Performance Test Data of 2A LPCI Hx
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)  
- EC 377036, 2A LPCI Heat Exchanger September 18, 2009 Thermal Performance Test
- IR 1009039, 345 kv Line 8014 trip  
- IR 978203, GL 89-13 Program Health Color Change
1R15 Operability Evaluations (71111.15)  
- IR 989609, D2R21 Inspection Results for 2A LPCI Heat Exchanger
- Operability Evaluation No. 09-007, 2A LPCI Heat Exchanger (2-1503-A)  
- IR 990189, 2A LPCI Heat Exchanger Tubesheet Corrosion
- EC 372200, Perform Evaluation of Thermal Performance Test Data of 2A LPCI Hx  
- IR 990209, 2A LPCI Hx Top Coverplate Coating Bubbled
- EC 377036, 2A LPCI Heat Exchanger September 18, 2009 Thermal Performance Test  
- IR 996991, A LPCI HT Exchanger Shell Side RV Lifting
- IR 978203, GL 89-13 Program Health Color Change  
- CY-DR-110-220, LPCI Service Water (CCSW) and Torus Water Sampling, Revision 3
- IR 989609, D2R21 Inspection Results for 2A LPCI Heat Exchanger  
- CY-DR0120-413, Cooling and Service Water Chemical Injection System, Revision 8
- IR 990189, 2A LPCI Heat Exchanger Tubesheet Corrosion  
- Root Cause Report 967008-03, Dresden 2-1503-A, 2A Low Pressure Coolant Injection
- IR 990209, 2A LPCI Hx Top Coverplate Coating Bubbled  
  (LPCI)/Containment Cooling Heat Exchanger (Hx) Failure to Meet Design Basis Heat Removal
- IR 996991, A LPCI HT Exchanger Shell Side RV Lifting  
  Capability due to Asiatic Clam Macrofouling Resulting from 2-1501-3A Valve Leakage and
- CY-DR-110-220, LPCI Service Water (CCSW) and Torus Water Sampling, Revision 3  
  Subsequent Untreated Service Water Make-Up via the CCSW Keepfill Diluting the Biocide
- CY-DR0120-413, Cooling and Service Water Chemical Injection System, Revision 8  
  Treatment below the Asiatic Clam Lethal Concentration
- Root Cause Report 967008-03, Dresden 2-1503-A, 2A Low Pressure Coolant Injection  
- Focus Area Assessment, Dresden Station, CCSW System Asiatic Clam Fouling. Performed
(LPCI)/Containment Cooling Heat Exchanger (Hx) Failure to Meet Design Basis Heat Removal  
  by Water Technology Consultants, Inc.
Capability due to Asiatic Clam Macrofouling Resulting from 2-1501-3A Valve Leakage and  
- EC Evaluation 373443, Evaluation of Leakage From Cylinder Head Covers on 2A SBLC
Subsequent Untreated Service Water Make-Up via the CCSW Keepfill Diluting the Biocide  
  Pump
Treatment below the Asiatic Clam Lethal Concentration  
- WO1001541-76, 3B SBLC System Pump Test for Operability Verification
- Focus Area Assessment, Dresden Station, CCSW System Asiatic Clam Fouling. Performed  
                                                    5                            Attachment
by Water Technology Consultants, Inc.  
- EC Evaluation 373443, Evaluation of Leakage From Cylinder Head Covers on 2A SBLC  
Pump  
- WO1001541-76, 3B SBLC System Pump Test for Operability Verification  


1R19 Post-Maintenance Testing (71111.19)
- IR 1003797, TSC HVAC Surveillances Failed
- WO 1294151, D1/2/3 SAN PM Operability Surv for the TSC AFUs
6
- DOS 5750-05, Semi-Annual Technical Support Center (TSC) Air Filtration Unit (AFU)
Attachment
  Operability Test, Revision 15
1R19 Post-Maintenance Testing (71111.19)  
- IR 348426, FIC-2/3-5748-93 Airflow Indication Not Actual Airflow
- IR 1003797, TSC HVAC Surveillances Failed  
- WO 826129, FIC-2/3-5748-93 Airflow Indication Not Actual Airflow
- WO 1294151, D1/2/3 SAN PM Operability Surv for the TSC AFUs  
- IR 1005336, TSC Flow Controller Range Issue
- DOS 5750-05, Semi-Annual Technical Support Center (TSC) Air Filtration Unit (AFU)  
- EP-AA-1000, Standardized Radiological Emergency Plan, Revision 19
Operability Test, Revision 15  
- EP-AA-112-200-F-01, Station Emergency Director Checklist, Revision F
- IR 348426, FIC-2/3-5748-93 Airflow Indication Not Actual Airflow  
- NUREG-0696, Functional Criteria for Emergency Response Facilities, February 1981
- WO 826129, FIC-2/3-5748-93 Airflow Indication Not Actual Airflow  
- NUREG-0737, Clarification of TMI Action Plan Requirements, Supplement No. 1,
- IR 1005336, TSC Flow Controller Range Issue  
  January 1983.
- EP-AA-1000, Standardized Radiological Emergency Plan, Revision 19  
- M-3006, Technical Support Center HVAC & Plumbing Layout, Revision F
- EP-AA-112-200-F-01, Station Emergency Director Checklist, Revision F  
- DOS 6600-01, Diesel Generator Governor Oil Change and Compensating Adjustment,
- NUREG-0696, Functional Criteria for Emergency Response Facilities, February 1981  
  Revision 23
- NUREG-0737, Clarification of TMI Action Plan Requirements, Supplement No. 1,  
- IR 992803, U2 EDG Largest Load Reject (TSR 3.8.1.10)
January 1983.  
- IR 994101, 2/3 EDG Voltage Transient
- M-3006, Technical Support Center HVAC & Plumbing Layout, Revision F  
- DOS 6600-06, Bus Undervoltage and ECCS Integrated Functional Test for Unit 2/3 Diesel
- DOS 6600-01, Diesel Generator Governor Oil Change and Compensating Adjustment,  
  Generator to Unit 2, Revision 46
Revision 23  
- IR 997244, Recirc Pump Instruments not Functioning Reqd for Hydro
- IR 992803, U2 EDG Largest Load Reject (TSR 3.8.1.10)  
- IR 997142, CCP: MCR Panel 923-5 Lost Ventilation Equip Indications
- IR 994101, 2/3 EDG Voltage Transient  
- EC 378040, 2/3 EDG Overvoltage during Division I Undervoltage Surveillance, Revision 0
- DOS 6600-06, Bus Undervoltage and ECCS Integrated Functional Test for Unit 2/3 Diesel  
- IR 1005291, Inaccurate Information Included in IR 994101
Generator to Unit 2, Revision 46  
- IR 1006989, Control Room Indicators Deenergized
- IR 997244, Recirc Pump Instruments not Functioning Reqd for Hydro  
- EACE 994101-07, 2/3 Emergency Diesel Generator (EDG) Voltage Transient
- IR 997142, CCP: MCR Panel 923-5 Lost Ventilation Equip Indications  
- IR 987850, D2R21 As Found LLRT on 2-0203-2C Exceeded Leakage Limit
- EC 378040, 2/3 EDG Overvoltage during Division I Undervoltage Surveillance, Revision 0  
- DOS 0250-02, Full Closure Timing and Exercising of Main Steam Isolation Valves, Rev 26
- IR 1005291, Inaccurate Information Included in IR 994101  
- DOS 0250-03, Main Steam Isolation Valve Fail-Safe Closure Test, Rev 21
- IR 1006989, Control Room Indicators Deenergized
- IR 1001725, Higher than Expected Vibrations on 2B Cond Pp.
- EACE 994101-07, 2/3 Emergency Diesel Generator (EDG) Voltage Transient  
- IR 1002609, FME: Found in 2B Condensate Pump Suction Piping
- IR 987850, D2R21 As Found LLRT on 2-0203-2C Exceeded Leakage Limit  
- ER-AA-2006, Lost Parts Evaluations, Revision 6
- DOS 0250-02, Full Closure Timing and Exercising of Main Steam Isolation Valves, Rev 26  
- WO 1098975, 2B Condensate Booster Motor Alignment
- DOS 0250-03, Main Steam Isolation Valve Fail-Safe Closure Test, Rev 21  
- DOP 3300-02, Condensate System Startup, Revision 50
- IR 1001725, Higher than Expected Vibrations on 2B Cond Pp.  
- M-15, Diagram of Condensate Piping, Revision J
- IR 1002609, FME: Found in 2B Condensate Pump Suction Piping  
- MA-AA-716-012, Post-Maintenance Testing, Revision 11
- ER-AA-2006, Lost Parts Evaluations, Revision 6  
- MA-AA-716-230-1002, Vibration Analysis/Acceptance Guideline, Revision 2
- WO 1098975, 2B Condensate Booster Motor Alignment  
1R20 Outage (71111.20)
- DOP 3300-02, Condensate System Startup, Revision 50  
- DGP 01-01, Unit Startup, Revision 153
- M-15, Diagram of Condensate Piping, Revision J  
- IR 975280, 3B CRD FCV Failed to Operate Remotely
- MA-AA-716-012, Post-Maintenance Testing, Revision 11  
- IR 975813, D3F48LL: DEHC Alarms During U3 Chest Warming
- MA-AA-716-230-1002, Vibration Analysis/Acceptance Guideline, Revision 2  
- IR 975830, D3F48LL: DEHC Issues During Turbine Roll
1R20 Outage (71111.20)  
- IR 976410, CIV #1 Indicates 57% Open. LVDT Position Indication Failure
- DGP 01-01, Unit Startup, Revision 153  
                                                  6                              Attachment
- IR 975280, 3B CRD FCV Failed to Operate Remotely  
- IR 975813, D3F48LL: DEHC Alarms During U3 Chest Warming  
- IR 975830, D3F48LL: DEHC Issues During Turbine Roll  
- IR 976410, CIV #1 Indicates 57% Open. LVDT Position Indication Failure  


1R22 Surveillance Testing (71111.22)
- IR 984934, DOS 6620-07 SBO Surveillance Need Revision
- IR 745855, "Unable to Close SBO Diesel Onto Bus"
7
- IR 984179, "Unit 2 SBO Preparation for Standby Readiness Deficiency"
Attachment
- DOS 6620-07, "SBO 2(3) Diesel Generator Surveillance Tests, Revision 28
1R22 Surveillance Testing (71111.22)  
- DOP 6620-20, "SBO D/G 2(3) Prelubrication and Barring for Normal Start", Revision 06
- IR 984934, DOS 6620-07 SBO Surveillance Need Revision  
- DOA 6500-11, "4 KV Bus Overvoltage," Revision 05
- IR 745855, "Unable to Close SBO Diesel Onto Bus"  
- WO 1257282, "Perform DOS 6620-07, D2 SBO Surveillance," 10/26/2009
- IR 984179, "Unit 2 SBO Preparation for Standby Readiness Deficiency"  
- WO 1079209-01, D2 30M/RFL TS LLRT MSIV 203-1B & 203-2B Dry Test
- DOS 6620-07, "SBO 2(3) Diesel Generator Surveillance Tests, Revision 28  
- WO 1077724-01, D2 30M/RFL TS LLRT MSIV 203-1C & 203-2C Dry Test
- DOP 6620-20, "SBO D/G 2(3) Prelubrication and Barring for Normal Start", Revision 06  
- WO 1077725-01, D2 30M/RFL TS LLRT MSIV 203-1D & 203-2D Dry Test
- DOA 6500-11, "4 KV Bus Overvoltage," Revision 05  
- WO 1081285-01, D2 20M/RFL TS LLRT MSIV 203-2A Wet Test
- WO 1257282, "Perform DOS 6620-07, D2 SBO Surveillance," 10/26/2009  
- WO 1079266-01, D2 30M/RFL TS LLRT MSIV 203-2B Wet Test
- WO 1079209-01, D2 30M/RFL TS LLRT MSIV 203-1B & 203-2B Dry Test  
- WO 1081288-01, D2 30M/RFL TS LLRT MSIV 203-2C Wet Test
- WO 1077724-01, D2 30M/RFL TS LLRT MSIV 203-1C & 203-2C Dry Test  
- WO 1081313-01, D2 30M/RFL TS LLRT MSIV 203-2D Wet Test
- WO 1077725-01, D2 30M/RFL TS LLRT MSIV 203-1D & 203-2D Dry Test  
- DOS 7000-01, Local Leak Rate Testing of Main Steam Isolation Valves (Dry Tests), Rev 5
- WO 1081285-01, D2 20M/RFL TS LLRT MSIV 203-2A Wet Test  
- DOS 7000-02, Local Leak Rate Testing of Main Steam Isolation Valves (Wet Test), Rev 2
- WO 1079266-01, D2 30M/RFL TS LLRT MSIV 203-2B Wet Test  
- IR 987850, D2R21 As Found LLRT on 2-0203-2C Exceeded Leakage Limit
- WO 1081288-01, D2 30M/RFL TS LLRT MSIV 203-2C Wet Test  
- IR 987852, D2R21 As Found LLRT on 2-0203-1D Exceeded Leakage Limit
- WO 1081313-01, D2 30M/RFL TS LLRT MSIV 203-2D Wet Test  
- DIS 1500-01, Reactor Low Pressure (350 PSIG) ECCS Permissive, Revision 27
- DOS 7000-01, Local Leak Rate Testing of Main Steam Isolation Valves (Dry Tests), Rev 5  
- IR 944688, Test Valves Not Installed on CST Level Switches (HPCI Logic)
- DOS 7000-02, Local Leak Rate Testing of Main Steam Isolation Valves (Wet Test), Rev 2  
1EP4 Emergency Action Level and Emergency Plan Changes
- IR 987850, D2R21 As Found LLRT on 2-0203-2C Exceeded Leakage Limit  
- Dresden Station Radiological Emergency Plan Annex; Revisions 23, 24, and 25
- IR 987852, D2R21 As Found LLRT on 2-0203-1D Exceeded Leakage Limit  
2OS1 Access Control to Radiologically Significant Areas (71121.01)
- DIS 1500-01, Reactor Low Pressure (350 PSIG) ECCS Permissive, Revision 27  
- AR 987949; Operator PCE in Clean Area above Drywell Bullpen; November 3, 2009
- IR 944688, Test Valves Not Installed on CST Level Switches (HPCI Logic)  
- AR 993194; Responding to Guardhouse Portal Monitor Alarm; November 13, 2009
1EP4 Emergency Action Level and Emergency Plan Changes  
- RP-AA-203-1001; Personnel Exposure Investigation, Revision 6
- Dresden Station Radiological Emergency Plan Annex; Revisions 23, 24, and 25  
- RP-AA-210; Dosimetry Issue, Usage and Control; Revision 15
2OS1 Access Control to Radiologically Significant Areas (71121.01)  
- RP-AA-220; Intake Investigation, Revision 5
- AR 987949; Operator PCE in Clean Area above Drywell Bullpen; November 3, 2009  
- RP-AA-350-1001; Response to Guardhouse Portal Monitor Alarms, Revision 0
- AR 993194; Responding to Guardhouse Portal Monitor Alarm; November 13, 2009  
- Underwater Construction Corporation Safe Practices Manual, Attachment A: Safety Hazard
- RP-AA-203-1001; Personnel Exposure Investigation, Revision 6  
  Analysis/Dive Plan; November 3, 2009
- RP-AA-210; Dosimetry Issue, Usage and Control; Revision 15  
2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)
- RP-AA-220; Intake Investigation, Revision 5  
- RWP 10010408; D2R21 Drywell Nuclear Instrumentation System Maintenance; Revision 0
- RP-AA-350-1001; Response to Guardhouse Portal Monitor Alarms, Revision 0  
- RWP 10010420; D2R21 Drywell Control Rod Drive System Maintenance; Revision 0
- Underwater Construction Corporation Safe Practices Manual, Attachment A: Safety Hazard  
- RWP 10010421; D2R21 Drywell Control Rod Drive System Support; Revision 0
Analysis/Dive Plan; November 3, 2009  
- RWP 10010426; D2R21 Drywell In-Service Inspection; Revision 0
2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)  
- RWP 10010437; D2R21 Torus Diving Activities; Revision 1
- RWP 10010408; D2R21 Drywell Nuclear Instrumentation System Maintenance; Revision 0  
- RWP 10010452; D2R21 Reactor Disassembly/Reassembly and Related Activities; Revision 1
- RWP 10010420; D2R21 Drywell Control Rod Drive System Maintenance; Revision 0
- AR 870602-03; Focused Area Self-Assessment: ALARA Planning for Outage Readiness and
- RWP 10010421; D2R21 Drywell Control Rod Drive System Support; Revision 0  
  Preparation; August 27, 2009
- RWP 10010426; D2R21 Drywell In-Service Inspection; Revision 0  
- AR 988447; Unit 2 Refuel Floor and Reactor Building Low Level Contamination;
- RWP 10010437; D2R21 Torus Diving Activities; Revision 1  
  November 3, 2009
- RWP 10010452; D2R21 Reactor Disassembly/Reassembly and Related Activities; Revision 1  
                                                  7                              Attachment
- AR 870602-03; Focused Area Self-Assessment: ALARA Planning for Outage Readiness and  
Preparation; August 27, 2009  
- AR 988447; Unit 2 Refuel Floor and Reactor Building Low Level Contamination;  
November 3, 2009  


- AR 990061; Under Vessel General Electric Worker Receives Small Ingestion;
  November 5, 2009
- AR 993319; Shaw Laborer Wiping Down cords on RB 613 300K Particle on Scrubs;
8
  November 11, 1009
Attachment
- RWP-WIP-10010388; D2 R21 Scaffold Installation/Removal Activities (Excluding Drywell);
- AR 990061; Under Vessel General Electric Worker Receives Small Ingestion;  
  November 7, 2009
November 5, 2009  
- RP-AA-461; Radiological Controls for Contaminated Water Diving Operations; Revision 2
- AR 993319; Shaw Laborer Wiping Down cords on RB 613 300K Particle on Scrubs;  
- RWP-WIP-10010403; D2 R21 Drywell Radiation Protection Department Activities;
November 11, 1009  
  November 6, 2009
- RWP-WIP-10010388; D2 R21 Scaffold Installation/Removal Activities (Excluding Drywell);  
- RWP-WIP-10010403; D2 R21 Drywell Radiation Protection Department Activities;
November 7, 2009  
  November 10, 2009
- RP-AA-461; Radiological Controls for Contaminated Water Diving Operations; Revision 2  
- RWP-WIP-10010437; D2 R21 Torus Diving Activities; November 10, 2009
- RWP-WIP-10010403; D2 R21 Drywell Radiation Protection Department Activities;  
- RWP-WIP-10010453; D2 R21 Refuel Floor IVVI Activities; November 7, 2009
November 6, 2009  
4OA1 Performance Indicator (PI) Verification (71151)
- RWP-WIP-10010403; D2 R21 Drywell Radiation Protection Department Activities;  
- LS-AA-2140; Monthly Data Elements for NRC Occupational Exposure Control Effectiveness;
November 10, 2009  
  Revision 4
- RWP-WIP-10010437; D2 R21 Torus Diving Activities; November 10, 2009  
4OA2 Identification and Resolution of Problems (71152)
- RWP-WIP-10010453; D2 R21 Refuel Floor IVVI Activities; November 7, 2009  
- RCR 776598-08, Dresden 3-1503-B, 3B Low Pressure Coolant Injection (LPCI) / Containment
4OA1 Performance Indicator (PI) Verification (71151)  
  Cooling Heat Exchanger (HX) Failure to Meet Design Basis Heat Removal Capability Due to
- LS-AA-2140; Monthly Data Elements for NRC Occupational Exposure Control Effectiveness;  
  Inadequate Programmatic Control of Macrofoulants, Revision 0
Revision 4  
- IR 868703, 2A and 2B LPCI Heat Exchanger Samples Tested 0 PPM Biocide
4OA2 Identification and Resolution of Problems (71152)  
- IR 871271, Biocide Injection Unavailable for CCSW System PMT Run
- RCR 776598-08, Dresden 3-1503-B, 3B Low Pressure Coolant Injection (LPCI) / Containment  
- IR 877889, Biocide Injection Not Available During U3 CCSW Run
Cooling Heat Exchanger (HX) Failure to Meet Design Basis Heat Removal Capability Due to  
- IR 880708, CCSW Biocide/Clam-Trol Chemical Injection Result Low
Inadequate Programmatic Control of Macrofoulants, Revision 0  
- IR 881043, CCSW Biocide/Clamtrol Chemical Injection Result Low
- IR 868703, 2A and 2B LPCI Heat Exchanger Samples Tested 0 PPM Biocide  
- IR 883155, 3A and 3B LPCI Fail Clam-Trol Test
- IR 871271, Biocide Injection Unavailable for CCSW System PMT Run  
- IR 884613, 2B LPCI Failed Clam-Trol Test
- IR 877889, Biocide Injection Not Available During U3 CCSW Run  
- IR 887406, Inadequate Biocide Retention
- IR 880708, CCSW Biocide/Clam-Trol Chemical Injection Result Low  
- IR 888462, 0 PPM Biocide Results for 2/3 EDG
- IR 881043, CCSW Biocide/Clamtrol Chemical Injection Result Low  
- IR 889598, No Biocide Found in Unit 2B LPCI CCSW Hx Lay-up Sample
- IR 883155, 3A and 3B LPCI Fail Clam-Trol Test  
- IR 891286, No Biocide Found in 2B LPCI CCSW Hx Lay-up Sample
- IR 884613, 2B LPCI Failed Clam-Trol Test  
- IR 892241, Procedure change and Eval of Biocide Injection to DGCWPs
- IR 887406, Inadequate Biocide Retention  
- IR 905027, 2B LPCI No Clamtrol Present
- IR 888462, 0 PPM Biocide Results for 2/3 EDG  
- IR 905224, No Biocide Detected in 2/3 DGCSW
- IR 889598, No Biocide Found in Unit 2B LPCI CCSW Hx Lay-up Sample  
- IR 908886, 2A LPCI Biocide Results Less than 8 PPM
- IR 891286, No Biocide Found in 2B LPCI CCSW Hx Lay-up Sample  
- IR 914398, Revision to RCR 776598-08, 3B LPCI Hx Macrofouling Required
- IR 892241, Procedure change and Eval of Biocide Injection to DGCWPs  
- IR 915033, 2A LPCI SW Biocide 24 hr. Sample < 8PPM
- IR 905027, 2B LPCI No Clamtrol Present  
- IR 917133, 2B LPCI Failed Clam-Trol Test
- IR 905224, No Biocide Detected in 2/3 DGCSW  
- IR 920498, 2A and 2B LPCI SW Biocide <8PPM (24hr Sample)
- IR 908886, 2A LPCI Biocide Results Less than 8 PPM  
- IR 923788, Clam-Trol Analysis Failed on 3DGCSW
- IR 914398, Revision to RCR 776598-08, 3B LPCI Hx Macrofouling Required  
- IR 999766, 2B LPCI Failed for Biocide
- IR 915033, 2A LPCI SW Biocide 24 hr. Sample < 8PPM  
- IR 1000791, 2B LPCI Heat Exchanger Failed Clam-Trol Analysis
- IR 917133, 2B LPCI Failed Clam-Trol Test  
- IR 1006553, No Biocide Detected in CCSW from 3B LPCI Hx
- IR 920498, 2A and 2B LPCI SW Biocide <8PPM (24hr Sample)  
- IR 1007918, Unit 2 A and B LPCI Heat Exchangers Fail 18-24 hr Biocide
- IR 923788, Clam-Trol Analysis Failed on 3DGCSW  
                                                    8                            Attachment
- IR 999766, 2B LPCI Failed for Biocide  
- IR 1000791, 2B LPCI Heat Exchanger Failed Clam-Trol Analysis  
- IR 1006553, No Biocide Detected in CCSW from 3B LPCI Hx  
- IR 1007918, Unit 2 A and B LPCI Heat Exchangers Fail 18-24 hr Biocide  


4OA3 Follow-Up of Events (71153)
- Licensee Event Report 237/2009-003-00, Emergency Diesel Generator Oil Leak, Revision 00
- IR 926605, Oil Leak on the 2/3 DG Turbo Lube Oil Y-strainer
9
- MA-AA-716-008, Foreign Material Exclusion Program, Revision 4
Attachment
- Licensee Event Report 237/2009-001-00, Common Mode Failure of Reactor Building Isolation
4OA3 Follow-Up of Events (71153)  
  Dampers, Revision 00
- Licensee Event Report 237/2009-003-00, Emergency Diesel Generator Oil Leak, Revision 00  
- IR 877591, Potential 10CFR50 Part 21 Notification of Versa Air Solenoid
- IR 926605, Oil Leak on the 2/3 DG Turbo Lube Oil Y-strainer
- IR 838034, RBV Damper 2-5742-A Slow to Close
- MA-AA-716-008, Foreign Material Exclusion Program, Revision 4  
- IR 842305, 3-5742-B Damper 90 Seconds to Close
- Licensee Event Report 237/2009-001-00, Common Mode Failure of Reactor Building Isolation  
- IR 888338, RBV Isolation Damper Solenoid Valve Incorrect Component Classification
Dampers, Revision 00  
- IR 975779, Post Transient/Scram Walkdown Observation by NRC
- IR 877591, Potential 10CFR50 Part 21 Notification of Versa Air Solenoid  
- IR 975076, U2/3 EDG Started on Rx Trip when Aux Power Transferred
- IR 838034, RBV Damper 2-5742-A Slow to Close  
- IR 974426, U3 Group 1 Isolation and Reactor Scram
- IR 842305, 3-5742-B Damper 90 Seconds to Close  
- IR 973968, 3A RWCU Pump Tripped and DOA Entry
- IR 888338, RBV Isolation Damper Solenoid Valve Incorrect Component Classification  
- IR 973144, RWCU Isolate on High Temperature
- IR 975779, Post Transient/Scram Walkdown Observation by NRC  
- IR 973104, 3A RWCU Tripped
- IR 975076, U2/3 EDG Started on Rx Trip when Aux Power Transferred  
- Root Cause Report 974426-04, U3 Reactor SCRAM and Group 1 Isolation Resulting in
- IR 974426, U3 Group 1 Isolation and Reactor Scram  
  Forced Outage D3F48 Due to DOP 1200-03, titled RWCU System Operation with the Reactor
- IR 973968, 3A RWCU Pump Tripped and DOA Entry  
  at Pressure Latent Procedural Deficiency
- IR 973144, RWCU Isolate on High Temperature
- LER 249/2009-001-00, Unit 3 Group 1 Isolation and Automatic Reactor Scram
- IR 973104, 3A RWCU Tripped  
- IR 990113, U3 from 650 MWe to 0 and a Turbine Trip
- Root Cause Report 974426-04, U3 Reactor SCRAM and Group 1 Isolation Resulting in  
- IR 990160, 2/3 EDG Auto Started when U3 Main Generator was Tripped
Forced Outage D3F48 Due to DOP 1200-03, titled RWCU System Operation with the Reactor  
- IR 990112, Need WO Rolled for Repair to U3 EHC Filter Pump Bkr
at Pressure Latent Procedural Deficiency  
- IR 990110, U3 EHC Filter Pmp Trip
- LER 249/2009-001-00, Unit 3 Group 1 Isolation and Automatic Reactor Scram  
- IR 990661,  MSV #4 Did Not Open During Initial Turbine Roll
- IR 990113, U3 from 650 MWe to 0 and a Turbine Trip
4OA5 Other Activities (TI 2515/177)
- IR 990160, 2/3 EDG Auto Started when U3 Main Generator was Tripped  
- IR 994774, Procedures for Venting ECCS/SDC Systems Should Be Revised
- IR 990112, Need WO Rolled for Repair to U3 EHC Filter Pump Bkr  
- IR 999625, Air Found in HPCI Discharge Piping During UT
- IR 990110, U3 EHC Filter Pmp Trip  
- IR 999762, Air Found in Second Location in HPCI Discharge Piping
- IR 990661,  MSV #4 Did Not Open During Initial Turbine Roll  
- IR 1014280, Question from NRC Inspector on ISI Drawing
4OA5 Other Activities (TI 2515/177)  
- EC 371153, Rev 2, NRC GL 2008-01 HPCI System Evaluation
- IR 994774, Procedures for Venting ECCS/SDC Systems Should Be Revised  
- DOP 2300-01, HPCI Standby Operation, Rev 41
- IR 999625, Air Found in HPCI Discharge Piping During UT  
- M-51, Diagram of High Pressure Coolant Injection Piping, Rev CL
- IR 999762, Air Found in Second Location in HPCI Discharge Piping  
- ISI-504, System Pressure Test Walkdown Isometric MSIV Room - X Area, Rev B
- IR 1014280, Question from NRC Inspector on ISI Drawing  
- ISI-510, System Pressure Test Walkdown Isometric H.P. Coolant Injection Piping, Sheet 2,
- EC 371153, Rev 2, NRC GL 2008-01 HPCI System Evaluation  
  Rev D
- DOP 2300-01, HPCI Standby Operation, Rev 41  
- M-1151C-2, Computer Math Model High Pressure Coolant Injection System, Sheet 1, Rev 2
- M-51, Diagram of High Pressure Coolant Injection Piping, Rev CL  
- M-4455, HPCI High Point Vent Line, Sheet 3, Rev A
- ISI-504, System Pressure Test Walkdown Isometric MSIV Room - X Area, Rev B  
                                                  9                              Attachment
- ISI-510, System Pressure Test Walkdown Isometric H.P. Coolant Injection Piping, Sheet 2,  
Rev D  
- M-1151C-2, Computer Math Model High Pressure Coolant Injection System, Sheet 1, Rev 2  
- M-4455, HPCI High Point Vent Line, Sheet 3, Rev A  


                          LIST OF ACRONYMS USED
ADAMS Agencywide Document Access Management System
AEER Auxiliary Electric Equipment Room
10
ALARA As-Low-As-Reasonably-Achievable
Attachment
ASME American Society of Mechanical Engineers
LIST OF ACRONYMS USED  
BWR   Boiling Water Reactor
ADAMS  
CAP   Corrective Action Program
Agencywide Document Access Management System  
CCSW Containment Cooling Service Water
AEER  
CDF   Core Damage Frequency
Auxiliary Electric Equipment Room  
CFR   Code of Federal Regulations
ALARA  
CO   Clearance Order
As-Low-As-Reasonably-Achievable  
CRD   Control Rod Drive
ASME  
D2   Dresden Unit 2
American Society of Mechanical Engineers  
DRP   Division of Reactor Projects
BWR  
EACE Equipment Apparent Cause Evaluation
Boiling Water Reactor  
EAL   Emergency Action Level
CAP  
EC   Engineering Change
Corrective Action Program  
EDG   Emergency Diesel Generator
CCSW  
ESI   Engine Systems Incorporated
Containment Cooling Service Water  
FME   Foreign Material Exclusion
CDF  
GE   General Electric
Core Damage Frequency  
HEP   Human Error Probability
CFR  
HEPA High Efficiency Particulate Air
Code of Federal Regulations  
HPCI High Pressure Coolant Injection
CO  
HCU   Hydraulic Control Unit
Clearance Order  
Hx   Heat Exchanger
CRD  
IPEEE Individual Plant Examination for External Events
Control Rod Drive  
IMC   Inspection Manual Chapter
D2  
INPO Institute of Nuclear Power Operations
Dresden Unit 2  
IP   Inspection Procedure
DRP  
IR   Issue Report
Division of Reactor Projects  
ISI   Inservice Inspection
EACE  
IST   In-service Test
Equipment Apparent Cause Evaluation  
LER   Licensee Event Report
EAL  
LERF Large Early Release Frequency
Emergency Action Level  
LOCA Loss of Coolant Accident
EC  
LOOP Loss of OffSite Power
Engineering Change  
LPCI Low Pressure Coolant Injection
EDG  
MOV   Motor Operated Valves
Emergency Diesel Generator  
MSV   Main Stop Valve
ESI  
NCV   Non-Cited Violation
Engine Systems Incorporated  
NEI   Nuclear Energy Institute
FME  
NLO   Non-Licensed Operator
Foreign Material Exclusion  
NRC   Nuclear Regulatory Commission
GE  
NRR   Office of Nuclear Reactor Regulation
General Electric  
NSO   Nuclear Station Operator
HEP  
OSF   Outage Safety Plan
Human Error Probability  
PARS Publicly Available Records
HEPA  
PCIS Primary Containment Isolation Signal
High Efficiency Particulate Air  
PI   Performance Indicator
HPCI  
                                          10          Attachment
High Pressure Coolant Injection  
HCU  
Hydraulic Control Unit  
Hx  
Heat Exchanger  
IPEEE  
Individual Plant Examination for External Events  
IMC  
Inspection Manual Chapter  
INPO  
Institute of Nuclear Power Operations  
IP  
Inspection Procedure  
IR  
Issue Report  
ISI  
Inservice Inspection  
IST  
In-service Test  
LER  
Licensee Event Report  
LERF  
Large Early Release Frequency  
LOCA  
Loss of Coolant Accident  
LOOP  
Loss of OffSite Power  
LPCI  
Low Pressure Coolant Injection  
MOV  
Motor Operated Valves  
MSV  
Main Stop Valve  
NCV  
Non-Cited Violation  
NEI  
Nuclear Energy Institute  
NLO  
Non-Licensed Operator  
NRC  
Nuclear Regulatory Commission  
NRR  
Office of Nuclear Reactor Regulation  
NSO  
Nuclear Station Operator  
OSF  
Outage Safety Plan  
PARS  
Publicly Available Records  
PCIS  
Primary Containment Isolation Signal  
PI  
Performance Indicator  


P&ID Piping and Instrumentation Diagrams
PM   Planned or Preventative Maintenance, or Post-Maintenance
PO   Purchase Order
11
RCR   Root Cause Report
Attachment
RCS   Reactor Coolant System
P&ID  
RFO   Refueling Outage
Piping and Instrumentation Diagrams  
RPV   Reactor Pressure Vessel
PM  
RWCU Reactor Water Cleanup
Planned or Preventative Maintenance, or Post-Maintenance  
SBLC Standby Liquid Control
PO  
SBO   Station Blackout
Purchase Order  
SCAQ Significant Condition Adverse to Quality
RCR  
SDP   Significance Determination Process
Root Cause Report  
SPAR Standardized Plant Analysis Risk
RCS  
SR   Surveillance Requirements
Reactor Coolant System  
SRO   Senior Reactor Operator
RFO  
SSC   Structures, Systems and Components
Refueling Outage  
TS   Technical Specification
RPV  
U2   Unit 2
Reactor Pressure Vessel  
U3   Unit 3
RWCU  
UFSAR Updated Final Safety Analysis Report
Reactor Water Cleanup  
URI   Unresolved Item
SBLC  
UT   Ultrasonic Examination
Standby Liquid Control  
WO   Work Order
SBO  
                                        11                    Attachment
Station Blackout  
SCAQ  
Significant Condition Adverse to Quality  
SDP  
Significance Determination Process  
SPAR  
Standardized Plant Analysis Risk  
SR  
Surveillance Requirements  
SRO  
Senior Reactor Operator  
SSC  
Structures, Systems and Components  
TS  
Technical Specification  
U2  
Unit 2  
U3  
Unit 3  
UFSAR  
Updated Final Safety Analysis Report  
URI  
Unresolved Item  
UT  
Ultrasonic Examination  
WO  
Work Order  


C. Pardee                                           -2-
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its
enclosure, and your response (if any) will be made available electronically for public inspection
C. Pardee  
in the NRC Public Document Room or from the Publicly Available Records (PARS) component
of NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                                    Sincerely,
                                                    /RA/
-2-  
                                                    Mark A. Ring, Chief
                                                    Branch 1
                                                    Division of Reactor Projects
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its  
Docket Nos. 50-237; 50-249
enclosure, and your response (if any) will be made available electronically for public inspection  
License Nos. DPR-19; DPR-25
in the NRC Public Document Room or from the Publicly Available Records (PARS) component  
Enclosure:       Inspection Report 05000237/2009-005; 05000249/2009-005
of NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at  
                    w/Attachment: Supplemental Information
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
cc w/encl:       Distribution via ListServ
DOCUMENT NAME: G:\1-SECY\1-WORK IN PROGRESS\DRE 2009 005.DOC
G Publicly Available         G Non-Publicly Available     G Sensitive   G Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl
"E" = Copy with attach/encl "N" = No copy
  OFFICE       RIII                     RIII                 RIII                 RIII
  NAME         MRing:cms
Sincerely,  
  DATE         02/10/2010
                                          OFFICIAL RECORD COPY
/RA/  
Mark A. Ring, Chief  
Branch 1  
Division of Reactor Projects  
Docket Nos. 50-237; 50-249  
License Nos. DPR-19; DPR-25  
Enclosure:  
Inspection Report 05000237/2009-005; 05000249/2009-005  
  w/Attachment: Supplemental Information  
cc w/encl:  
Distribution via ListServ  
DOCUMENT NAME: G:\\1-SECY\\1-WORK IN PROGRESS\\DRE 2009 005.DOC  
G Publicly Available  
G Non-Publicly Available  
G Sensitive  
G Non-Sensitive  
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl  
"E" = Copy with attach/encl "N" = No copy  
   
OFFICE  
RIII  
RIII  
RIII  
RIII  
   
NAME  
MRing:cms  
   
DATE  
02/10/2010  
OFFICIAL RECORD COPY  


Letter to C. Pardee from M. Ring dated February 10, 2010
SUBJECT:       DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3
              INTEGRATED INSPECTION REPORT 05000237/2009-005;
Letter to C. Pardee from M. Ring dated February 10, 2010  
              05000249/2009-005
DISTRIBUTION:
SUBJECT:  
Susan Bagley
DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3  
RidsNrrDorlLpl3-2
INTEGRATED INSPECTION REPORT 05000237/2009-005;  
RidsNrrPMDresden Resource
05000249/2009-005  
RidsNrrDirsIrib Resource
DISTRIBUTION:  
Cynthia Pederson
Susan Bagley  
Steven Orth
RidsNrrDorlLpl3-2  
Jared Heck
RidsNrrPMDresden Resource  
Allan Barker
RidsNrrDirsIrib Resource  
Carole Ariano
Cynthia Pederson  
Linda Linn
Steven Orth  
DRPIII
Jared Heck  
DRSIII
Allan Barker  
Patricia Buckley
Carole Ariano  
Tammy Tomczak
Linda Linn  
DRPIII  
DRSIII  
Patricia Buckley  
Tammy Tomczak  
ROPreports Resource
ROPreports Resource
}}
}}

Latest revision as of 06:38, 14 January 2025

IR 05000237-09-005, 05000249-09-005, on 10/01/09 - 12/31/09; Dresden Nuclear Power Station, Units 2 & 3; Equipment Alignment, Operability Evaluations, Post-Maintenance Testing, Surveillance Testing, Outage, and Event Follow-up
ML100410121
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 02/10/2010
From: Ring M
NRC/RGN-III/DRP/B1
To: Pardee C
Exelon Generation Co, Exelon Nuclear
References
IR-09-005
Download: ML100410121 (62)


See also: IR 05000237/2009005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

February 10, 2010

Mr. Charles G. Pardee

Senior Vice President, Exelon Generation Company, LLC

President and Chief Nuclear Officer (CNO), Exelon Nuclear

4300 Winfield Road

Warrenville, IL 60555

SUBJECT:

DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3

INTEGRATED INSPECTION REPORT 05000237/2009-005;

05000249/2009-005

Dear Mr. Pardee:

On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an

integrated inspection at your Dresden Nuclear Power Station, Units 2 and 3. The enclosed

report documents the inspection results, which were discussed on January 14, 2010, with

Mr. T. Hanley and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

The report documents two NRC-identified findings and five self-revealed findings of very low

safety significance (Green). All of these findings were determined to involve a violation of

NRC requirements. Additionally, one licensee-identified violation is listed in Section 4OA7 of

this report. However, because of the very low safety significance and because they are entered

into your corrective action program, the NRC is treating these findings as non-cited violations

(NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy.

If you contest any NCV, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional

Administrator, Region III; 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352, the Director,

Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and

the NRC Resident Inspector at Dresden. In addition, if you disagree with the characterization of

any finding in this report, you should provide a response within 30 days of the date of this

inspection report, with the basis for your disagreement, to the Regional Administrator,

Region III, and the NRC Resident Inspector at Dresden. The information you provide will be

considered in accordance with Inspection Manual Chapter 0305.

C. Pardee

-2-

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response (if any) will be made available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket Nos. 50-237; 50-249

License Nos. DPR-19; DPR-25

Enclosure:

Inspection Report 05000237/2009-005; 05000249/2009-005

w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServ

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-237; 50-249

License Nos:

DPR-19; DPR-25

Report No:

05000237/2009-005; 05000249/2009-005

Licensee:

Exelon Generation Company

Facility:

Dresden Nuclear Power Station, Units 2 and 3

Location:

Morris, IL

Dates:

October 1 through December 31, 2009

Inspectors:

C. Phillips, Senior Resident Inspector

D. Meléndez-Colón, Resident Inspector

J. Benjamin, Project Engineer

J. Draper, Reactor Engineer

D. Sand, Reactor Engineer

C. Moore, Operations Engineer

F. Ramírez, Resident Inspector, LaSalle Station

J. McGhee, Senior Resident Inspector, Quad Cities

M. Holmberg, Reactor Inspector

M. Mitchell, Health Physicist

R. Jickling, Senior Emergency Preparedness Inspector

L. Kozak, Senior Reactor Analyst

Approved by:

M. Ring, Chief

Projects Branch 1

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ...........................................................................................................1

REPORT DETAILS.......................................................................................................................6

Summary of Plant Status...........................................................................................................6

1.

REACTOR SAFETY .......................................................................................................6

1R04

Equipment Alignment (71111.04) ......................................................................6

1R05

Fire Protection (71111.05).................................................................................9

1R08

Inservice Inspection Activities (71111.08G).....................................................10

1R11

Licensed Operator Requalification Program (71111.11) .................................11

1R12

Maintenance Effectiveness (71111.12) ...........................................................12

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13)......13

1R15

Operability Evaluations (71111.15)..................................................................13

1R19

Post-Maintenance Testing (71111.19).............................................................16

1R20

Outage Activities (71111.20) ...........................................................................19

1R22

Surveillance Testing (71111.22)......................................................................22

1EP4

Emergency Action Level and Emergency Plan Changes (71114.04)..............25

2.

RADIATION SAFETY ...................................................................................................27

2OS1

Access Control to Radiologically Significant Areas (71121.01).......................27

2OS2

As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)..........28

4.

OTHER ACTIVITIES.....................................................................................................29

4OA1

Performance Indicator (PI) Verification (71151) ..............................................29

4OA2

Identification and Resolution of Problems (71152)..........................................30

4OA3

Follow-Up of Events and Notices of Enforcement Discretion (71153).............34

4OA5

Other Activities.................................................................................................42

4OA6

Management Meetings ....................................................................................44

4OA7

Licensee-Identified Violations..........................................................................44

SUPPLEMENTAL INFORMATION ...............................................................................................1

KEY POINTS OF CONTACT.....................................................................................................1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED ........................................................2

LIST OF DOCUMENTS REVIEWED.........................................................................................4

LIST OF ACRONYMS USED ..................................................................................................10

1

Enclosure

SUMMARY OF FINDINGS

IR 05000237/2009-005, 05000249/2009-005; 10/01/2009 - 12/31/2009; Dresden Nuclear Power

Station, Units 2 & 3; Equipment Alignment, Operability Evaluations, Post-Maintenance Testing,

Surveillance Testing, Outage, and Event Follow-up.

This report covers a three-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Two Green findings were identified by the

inspectors and five findings were self-revealed. All of the findings were considered Non-Cited

Violations (NCVs) of NRC regulations. The significance of most findings is indicated by their

color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process (SDP). Cross-cutting aspects were determined using

IMC 0305, "Operating Reactor Assessment Program." Findings for which the SDP does not

apply may be Green or be assigned a severity level after NRC management review. The NRCs

program for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

A.

NRC-Identified and Self-Revealed Findings

Cornerstone: Initiating Events

Green. A self-revealed finding involving a non-cited violation (NCV) of Technical

Specification 5.4.1 was identified on October 3, 2009, due to the licensees failure to

include essential information in DOP 1200-03, RWCU System Operation with the

Reactor at Pressure, Revision 51, regarding startup of the reactor water cleanup system

with the reactor at pressure. This procedural deficiency caused a pressure pulse that

resulted in a reactor water level Low-Low Group 1 Isolation Signal and Unit 3 reactor

scram. This event was entered into the licensees corrective action program (CAP) as

Issue Report (IR) 974426. Corrective actions by the licensee included revising

procedure DOP 1200-03.

This finding was considered more than minor because it affected the Initiating Events

Cornerstone objective to limit the likelihood of those events that upset plant stability and

challenge critical safety functions during shutdown as well as at power operations.

The finding was determined to be of very low safety significance because it did not

contribute to both the likelihood of a reactor trip AND the likelihood that mitigating

equipment or functions will not be available. This finding has a cross-cutting aspect in

the area of Human Performance (Resources) because the licensee did not provide

complete, accurate and up-to-date procedures to plant personnel.

H.2(c) (Section 4OA3.2)

Cornerstone: Mitigating Systems

Green. A finding of very low safety significance and associated NCV of Technical

Specification 5.4.1 was self-revealed for the failure to meet the requirements of

Clearance Order (CO) 69631 by removing shorting links instead of fuses as required by

the CO on November 12, 2009. As a result, protective relaying was unintentially

removed from the Unit 2 main power transformer TR-2, the unit auxiliary transformer

TR-21, and the reserve auxiliary transformer TR-22. This issue was entered into the

licensees CAP as Issue Report 992290. Corrective actions included: coaching of the

individuals involved with the incorrect placing of the out-of-service and a placard on the

2

Enclosure

device that was incorrectly repositioned was changed to include the specific equipment

part number of the shorting links.

The finding was determined to be more than minor because the finding could reasonably

be viewed as a precursor to a significant event. The finding was evaluated using the

SDP in accordance with IMC 0609, Appendix G, Attachment 1, Shutdown Operations

Significance Determination Process Phase 1 Operational Checklists For Both PWRs and

BWRs, Checklist 6, dated May 25, 2004. This checklist stated that for a finding to

require a Phase 2 or 3 determination, it would require an increase in the likelihood of a

loss of offsite power or degrade the licensees ability to cope with a loss of offsite power.

The ability of the licensee to cope with a loss of offsite power was not impacted because

at least one emergency diesel generator was operable during the entire period. The

inspectors determined that neither of these conditions were met so the finding screened

as Green. This finding had a cross-cutting aspect in the area of Human Performance,

Work Practices. H.4(a) (Section 1R04)

Green. The inspectors identified a finding of very low safety significance and associated

NCV of Technical Specification 5.4.1 for the licensee failing to follow Dresden procedure

DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39. On

September 24, 2009, the inspectors identified valve 2-1501-42A, U2 low pressure

coolant injection (LPCI) A pump gland leak-off valve, was closed instead of open as

required by DOP 2-1500-M1. With this valve closed instead of open, the control room

alarm for LPCI pump seal leakage would not have been able to fulfill its function.

The issue was entered into the licensees CAP as IR 969490. The licensees corrective

actions included changing maintenance procedure DMP 1500-05, LPCI Pump

Maintenance, step G.25.d to include the case drain valve equipment numbers and sign

offs to position and verify the valves; and Operations Department Management

addressed the operations department personnel about this issue.

The finding was determined to be more than minor because the finding, if left

uncorrected, would become a more significant safety concern. Specifically, the valve

isolated an alarm in the control room. The inspectors concluded this finding was

associated with the Mitigating Systems Cornerstone using IMC 0609, Significance

Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, Table 4a, dated January 10, 2008. This finding has a

cross-cutting aspect in the area of Human Performance, Work Practices because the

licensee did not have any documentation as to how or when the valve was placed into

the position it was in. The design and location of the valve precluded that the valve was

accidently placed into the position it was found in. Therefore, the inspectors concluded

that either the failure to use human error prevention techniques or maintaining proper

documentation of activities caused the mispositioning of valve 2-1501-42A.

H.4.(a) (Section 1R15)

Green. The inspectors identified a finding of very low significance and associated

NCV of 10 CFR 50 Appendix B, Criterion XI, Test Control, because the licensee

unacceptably preconditioned the Unit 2 Emergency Diesel Generator (EDG) prior to

performing Technical Specification (TS) Surveillance Requirements (SR) 3.8.1.19.c.4,

3.8.1.12.c.3, and 3.8.1.10. These TS SRs involved verifying that the EDG supplied

steady state frequency would be acceptable following a loss of offsite power coincident

with and without a loss of coolant accident, and following the loss of the largest

post-accident load. Specifically, the inspectors identified that the licensee routinely

3

Enclosure

performed governor oil change outage maintenance activities which involved a section

that tuned the Unit 2 diesel governors response to a load change just prior to performing

these TS SRs. This issue has been entered into the licensees CAP as IR 1000609.

The licensee had not reached a conclusion on corrective actions by the end of the

inspection period.

This finding was determined to be more than minor because the finding, if left

uncorrected, would become a more significant safety concern. Unacceptable

preconditioning the EDG could mask latent performance issues and affect the ability of

the EDG to supply safety-related power to vital loads during an event. The inspectors

performed a Phase 1 SDP evaluation and determined that this issue was Green

because it did not result in an inoperable Unit 2 EDG. The failure to adequately

coordinate the work activity of the preventive maintenance and post-maintenance testing

with the TS SR activities was the principal contributor to this finding and was reflective of

recent performance. This finding had a cross-cutting aspect in the area of Work Control.

Specifically, the licensee did not appropriately coordinate work activities by incorporating

actions to address the impact of the work as different job activities. The scheduling of

the work activities resulted in the pre-conditioning of the EDG prior to performing the

surveillance tests. H.3(b) (Section 1R19)

Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,

Appendix B, Criterion IV, Procurement Document Control, was self-revealed for the

licensee's failure to ensure a safety-related plug was ordered and installed where

required in the 2/3 EDG turbo lube oil Y strainer. Instead, a non-conforming part was

installed, which resulted in a one-half gallon per minute oil leak and removal of the diesel

generator from service. The issue was entered into the licensees CAP as IR 926605.

Corrective actions included inspection of all other diesel generators to ensure the non-

conforming condition did not exist on another machine, revising the procurement

documents to ensure that future parts include a pressure retaining pipe plug with

approved material, and adding a requirement for a quality inspection to be performed to

inspect the strainer for metallic pipe plug in blow down port. Individual procedure

compliance issues were addressed through the stations performance improvement

initiatives.

The finding was determined to be more than minor because the finding was similar to

IMC 0612, Appendix E, Example 5 c because an incorrect and inadequate part was

installed and the system was returned to service. This performance deficiency impacted

the Mitigating Systems Cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. A Phase 3 SDP risk evaluation was performed by the regional

Senior Risk Analyst who determined the risk significance of the finding to be less than

1.0E-6/yr delta core damage frequency (CDF) and less than 1.0E-7/yr delta LERF, which

represents a finding of very low safety significance. Failure of plant personnel to

question the plastic shipping plug before the equipment was installed and returned to

service was not in compliance with MA-AA-716-008, Foreign Material Exclusion

Program, and, therefore, inspectors determined that this event was cross-cutting in

Human Performance, Work Practices, Procedural Compliance for failure of personnel to

follow the procedure. H.4(b) (Section 4OA3.3)

4

Enclosure

Cornerstone: Barrier Integrity

Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,

Appendix B, Criterion V, was self-revealed for the failure to properly move a fuel

assembly to its specified location, in accordance with DFP 0800-01, Master Refueling

Procedure. Specifically, on November 5, 2004, fuel assembly JLU569 was placed in

position C4-E5, instead of C4-F5, as required by the procedure. The violation was

placed into the licensees CAP in IR 990180. As corrective action, the licensee

temporarily suspended all fuel handling activities, conducted a piece count of the spent

fuel and stationed a second Senior Reactor Operator on the refueling bridge as

additional oversight for follow-on fuel movements. Additionally the fuel handling crew

associated with the event was suspended from future fuel moves, pending remedial

training.

Using the guidance contained in IMC 0612, Power Reactor Inspection Reports,

Appendix B, Issue Disposition Screening, dated December 4, 2008, the inspectors

determined that the finding was more than minor because the finding was associated

with the configuration control and human performance attributes of the Barrier Integrity

Cornerstone and impacted the Barrier Integrity Cornerstone objective to provide

reasonable assurance that physical design barriers (i.e., fuel cladding) protect the public

from radionuclide releases caused by an accident or event. Specifically, the shutdown

margin and thermal management of the spent fuel pool(s) is affected by fuel assembly

placement inside the pool(s). The inspectors determined the finding could be evaluated

using the significance determination process in accordance with IMC 0609,

Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening

and Characterization of Findings, Table 3b, question 6, which directed the inspectors to

Appendix M, Significance Determination Process Using Qualitative Criteria. Because

probabilistic risk assessment tools were not well suited for this finding, the criteria for

using IMC 0609, Appendix M, were met. In determining the significance of this finding,

regional management reviewed the licensee's bounding analysis in the UFSAR, which

demonstrated that regardless of the incorrect bundle position in the fuel pool, the design

of the pool still maintained pool Keff less than .95. Based on the additional qualitative

circumstances associated with this finding, regional management concluded the finding

was of very low safety significance (Green). This finding has a cross-cutting aspect in

the area of Human Performance, Work Practices. Specifically, neither the Senior

Reactor Operator (SRO), nor either of the two members of the fuel handling crew,

adequately performed independent verification techniques that ensured the fuel

assembly move was made in accordance with the Nuclear Component Transfer List, as

required by DFP 0800-01. H.4(a) (Section 1R20)

Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed for

the mispositioning of a Unit 3 control rod at power. Control rod G-11 was withdrawn one

notch contrary to TS SR 3.1.3.3 requirements to insert each withdrawn control rod at

least one notch. This was a performance deficiency. The violation was entered into the

licensees CAP as IR 993634. Corrective actions included inserting control rod G-11

one notch back to the original position and suspending control rod movement while all

rods were verified to be in their correct position. The operator was removed from shift

duties and the oncoming shift was briefed of the event.

5

Enclosure

The finding was determined to be more than minor because the finding was associated

with the Barrier Integrity Cornerstone attributes of human performance and configuration

control of a control rod, and affected the cornerstone objective of providing reasonable

assurance that physical design barriers protect the public from radionuclide releases

caused by accidents or events. Specifically, the operator withdrew a control rod contrary

to expected operation. This added positive reactivity and caused an unanticipated

power increase. The inspectors evaluated the finding using the SDP in accordance with

IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial

Screening and Characterization of Findings, Table 4a for the Fuel Barrier Cornerstone.

Per Table 4a, any issue that involves the fuel barrier is screened as Green. This finding

had no cross-cutting aspect. (Section 1R22)

B.

Licensee-Identified Violations

A violation of very low safety significance that was identified by the licensee has been

reviewed by inspectors. Corrective actions planned or taken by the licensee have been

entered into the licensees CAP. This violation and corrective action tracking numbers

are listed in Section 4OA7 of this report.

6

Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 2

On October 18, 2009, the unit began its coastdown to D2R21, and continued to downpower until

the end of the month.

On November 1, 2009, the unit was shutdown for the D2R21 Refueling Outage.

On December 2, 2009, the unit began ramp-up following D2R21.

On December 9, 2009, the unit returned to full power.

Unit 3

On October 3, 2009, the unit scrammed due to a Group 1 isolation resulting from a reactor

water clean-up pressure perturbation. The unit returned to full power on October 8, 2009.

On October 18, 2009, power was reduced to approximately 82 percent for a control rod pattern

adjustment. The unit returned to full power on the same day.

On November 6, 2009, the main turbine was manually tripped due to an EHC fluid leak from a

main stop valve. The unit returned to full power on November 10, 2009.

On November 19, 2009, power was reduced to approximately 82 percent for a control rod

pattern adjustment. The unit returned to full power on the same day.

On December 12, 2009, power was reduced to approximately 70 percent for control rod testing,

scram testing and quarterly valve testing. The unit returned to full power on

December 13, 2009.

1.

REACTOR SAFETY

1R04 Equipment Alignment (71111.04)

.1

Quarterly Partial System Walkdowns

a.

Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

Unit 3 250V battery and DC buses during Unit 2 250V battery discharge test;

B train of standby gas treatment when A train declared inoperable;

U2 Division 2 low pressure coolant injection and containment cooling service

water restoration after D2R21; and

Unit 2 main power transformer clearance order error.

7

Enclosure

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical

Specification (TS) requirements, outstanding work orders (WOs), condition reports, and

the impact of ongoing work activities on redundant trains of equipment in order to identify

conditions that could have rendered the systems incapable of performing their intended

functions. The inspectors also walked down accessible portions of the systems to verify

that system components and support equipment were aligned correctly and operable.

The inspectors examined the material condition of the components and observed

operating parameters of equipment to verify that there were no obvious deficiencies.

The inspectors also verified that the licensee had properly identified and resolved

equipment alignment problems that could cause initiating events or impact the capability

of mitigating systems or barriers and entered them into the corrective action program

(CAP) with the appropriate significance characterization. Documents reviewed are listed

in the Attachment to this report.

These activities constituted four partial system walkdown samples as defined in

Inspection Procedure (IP) 71111.04-05.

b.

Findings

(1) Operating Personnel Incorrectly Placed Clearance Tags

Introduction: A finding of very low safety significance and associated Non-Cited

Violation (NCV) of TS 5.4.1 was self-revealed for the failure to meet the requirements of

Clearance Order (CO) 69631 by removing shorting links instead of fuses as required by

the CO (Green). The inspectors determined this finding to be self-revealed because it

required no active and deliberate observation by the licensee or NRC inspectors to

determine whether a change in process or equipment capability or function had

occurred. The licensee was in the process of restoring fuses when it was observed the

fuses had not been removed.

Description: Clearance Order 69631 was placed on November 2, 2009. The CO was to

remove fuses (2-0902-29-FU1A and 2-0902-29-FU1B) for the U2 main power

transformer protective relays in preparation for the replacement of the main power

transformer. The fuses were located in the top of panel 902-29 in the auxiliary electric

equipment room. On November 12, 2009, direction was given to restore the fuses per

CO 69631. The non-licensed operators (NLOs), assigned to restore the fuses, found

that fuses 2-902-29-FU1A and 2-0902-29-FU1B had not been removed, but that shorting

links 2-902-29-F8 and 2-0902-29-F12 had been removed instead. These shorting links

removed protective relaying from the main power transformer TR-2, the unit auxiliary

transformer TR-21, and the reserve auxiliary transformer TR-22.

Two NLOs were assigned to remove the fuses. One of them was a Dresden operator,

the other was a traveler from Braidwood Station. The Braidwood operator had returned

to Braidwood Station by the time this issue was identified. The inspectors interviewed

the Dresden operator. The NLO stated that he never saw the fuses that were to be

removed. The labels for the fuses were below the fuses he was required to remove and

above a fuse block that contained the shorting links that he did remove. The fuse block

8

Enclosure

containing the shorting links had a placard on it stating that there were shorting links

inside the fuse block. The operator stated that he had not read the placard. In addition,

the operator stated that after the incorrect fuse block was removed he looked inside the

fuse block and recognized that they were shorting links and not fuses. The operator

stated that this did not alert him that the wrong equipment had been manipulated. The

operator also stated that he had been trained to recognize the difference between

shorting links and fuses.

Analysis: The inspectors determined that removal of shorting links instead of fuses was

contrary to the requirements of CO 69631 and was a performance deficiency.

The finding was determined to be more than minor because the finding could reasonably

be viewed as a precursor to a significant event. Specifically, the process error by the

non-licensed operators involved in the performance of the CO to properly detect that the

wrong piece of equipment had been removed, even after observing that the removed

equipment was not what they were assigned to remove (i.e., shorting link versus a fuse),

was a failure that, if left uncorrected, could lead to a significant event.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Appendix G, Attachment 1, Shutdown Operations Significance

Determination Process Phase 1 Operational Checklists For Both PWRs AND BWRs,

Checklist 6, dated May 25, 2004. This checklist stated that for a finding to require a

Phase 2 or 3 determination, it would require an increase in the likelihood of a loss of

offsite power or degrade the licensees ability to cope with a loss of offsite power.

The ability of the licensee to cope with a loss of offsite power was not impacted because

at least one emergency diesel generator was operable during the entire period. The

inspectors determined that neither of these conditions were met so the finding screened

as Green.

This finding has a cross-cutting aspect in the area of Human Performance,

Work Practices. The licensee communicates human error prevention techniques, such

as self and peer checking. In addition, personnel do not proceed in the face of

uncertainty or unexpected circumstances. Specifically, the NLO: 1) did not read the

placard that was on the component that the NLO removed, which explained that the

component was a shorting link and not a fuse; and 2) did not question why the

component the NLO removed was a shorting link and not a fuse, as identified in the CO.

H.4(a)

Enforcement: Technical Specification Section 5.4.1 states, in part, that

Written procedures shall be established, implemented, and maintained covering the

following activities: The applicable procedures recommended in Regulatory Guide 1.33,

Revision 2, Appendix A, February 1978. Paragraph 1.c of Regulatory Guide 1.33

states, in part, that procedures for equipment control, locking and tagging shall be

prepared and activities shall be performed in accordance with these procedures. The

licensee established CO 69631 as the implementing procedure for tagging out-of-service

the Unit 2 Main Power Transformer.

Contrary to the above, on November 2, 2009, CO 69631 was incorrectly placed, in that,

fuses (2-0902-29-FU1A and 2-0902-29-FU1B) for the U2 main power transformer

protective relays were not removed as required by CO 69631. Instead, shorting links

2-0902-29-F8 and 2-0902-29-F12 were removed which removed protective relaying to

9

Enclosure

the U2 main power transformer, U2 reserve auxiliary transformer, and the U2 unit

auxiliary transformer. Corrective actions included: coaching of the individuals involved

with the incorrect placing of the out-of-service, and changing a placard on the device that

was incorrectly repositioned to include the specific equipment part number of the

shorting links. Because this violation was of very low safety significance and it was

entered into the licensees corrective action program as Issue Report 992290 this

violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC

Enforcement Policy. (NCV 05000237/2009005-01)

1R05 Fire Protection (71111.05)

.1

Routine Resident Inspector Tours (71111.05Q)

a.

Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

Fire Zone 1.1.1.4, Unit 3 Reactor Building Elevation570, Secondary

Containment;

Fire Zone 8.2.5.B, Unit 2 Turbine Building Elevation 517, Low Pressure Heater

Bays North Turbine Cavity;

Fire Zone 8.2.5.A, Unit 2 Turbine Building Elevation 517, High Pressure

Heaters/Steam Lines; and

Fire Zone 8.2.6.B Multiple Elevations, Low Pressure Heater Bays.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and implemented adequate

compensatory measures for out-of-service, degraded or inoperable fire protection

equipment, systems, or features in accordance with the licensees fire plan. The

inspectors selected fire areas based on their overall contribution to internal fire risk as

documented in the plants Individual Plant Examination of External Events, their potential

to impact equipment, which could initiate or mitigate a plant transient, or their impact on

the plants ability to respond to a security event. Using the documents listed in the

Attachment to this report,, the inspectors verified that fire hoses and extinguishers were

in their designated locations and available for immediate use; that fire detectors and

sprinklers were unobstructed; that transient material loading was within the analyzed

limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory

condition. The inspectors also verified that minor issues identified during the inspection

were entered into the licensees CAP. Documents reviewed are listed in the Attachment

to this report.

These activities constituted four quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b.

Findings

No findings of significance were identified.

10

Enclosure

1R08 Inservice Inspection Activities (71111.08G)

For Unit 2, from November 2, 2009, through November 13, 2009, the inspectors

conducted a review of the implementation of the licensees Inservice Inspection (ISI)

Program for monitoring degradation of the reactor coolant system, steam generator

tubes, emergency feedwater systems, risk-significant piping and components and

containment systems.

The inspections described in Sections 1R08.1 and 1R08.5 below count as one

inspection sample as defined in IP 71111.08-05.

.1

Piping Systems ISI

a. Inspection Scope

The inspectors observed ultrasonic examination (UT) of the following examination

Category F welds (e.g., welds with known cracks approved by analysis for limited

additional service without repair) to evaluate compliance with the licensees augmented

Stress Corrosion Cracking Program. Specifically, the inspectors evaluated these

examinations to determine if the procedures, equipment, and personnel used were

qualified in accordance with the American Society of Mechanical Engineers (ASME)

Code Section XI, Appendix VIII.

UT of the valve-to-tee weld (PS2-Tee/202-4B) on the loop B recirculation system.

UT of the safe end-to-elbow (PS2/201-1) on the loop B recirculation system.

The inspectors observed a video record and reviewed a written report of the following

containment drywell supports to evaluate compliance with the licensees augmented

inspection program for Code Class MC supports. Specifically, the inspectors evaluated

this examination to determine if the VT-3 procedure, equipment, and personnel used

were qualified in accordance with the ASME Code Section XI.

Visual examination (VT-3) of eight male and female drywell shear lug stabilizers

(support groups 09 and 10).

The inspectors reviewed the following examination record with relevant/recordable

conditions/indications identified by the licensee to determine if acceptance of these

indications for continued service was in accordance with the ASME Code Section XI or

an NRC-approved alternative.

Report No. D2R20-037, Four Indications on the Reactor Head Flange Weld

(2RPV UPP HD/2-THD-FLG). The inspectors observed the following pressure

boundary weld completed for a risk-significant system to determine if the licensee

followed an ASME Code Section IX qualified welding procedure, maintained

control of foreign material, and to determine if the welder used qualified weld filler

material and base material. The inspectors also reviewed the work order for this

welding to determine if the post weld nondestructive examinations required by

the ASME Code were specified.

Weld (FW-2) fabricated during installation of the component cooling service

water system pump discharge elbow replacement.

11

Enclosure

b. Findings

No findings of significance were identified.

.2

Reactor Pressure Vessel Upper Head Penetration Inspection Activities (Not Applicable)

.3

Boric Acid Corrosion Control (Not Applicable)

.4

Steam Generator Tube Inspection Activities (Not Applicable)

.5

Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a review of ISI related problems entered into the licensees

corrective action program and conducted interviews with licensee staff to determine if:

the licensee had established an appropriate threshold for identifying ISI-related

problems;

the licensee had performed a root cause (if applicable) and taken appropriate

corrective actions; and

the licensee had evaluated operating experience and industry generic issues

related to ISI and pressure boundary integrity.

The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action

documents reviewed by the inspectors are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

a.

Inspection Scope

On August 3, 2009, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification examinations to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

licensed operator performance;

crews clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of abnormal and emergency procedures;

control board manipulations;

oversight and direction from supervisors; and

ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

12

Enclosure

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program

sample as defined in IP 71111.11.

b.

Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

.1

Routine Quarterly Evaluations (71111.12Q)

a.

Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant systems:

Unit 3 control rod drive (Z03); and

Unit 2 Shutdown Cooling (Z10).

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified that the licensee's actions to address system performance or

condition problems in terms of the following:

implementing appropriate work practices;

identifying and addressing common cause failures;

scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;

characterizing system reliability issues for performance;

charging unavailability for performance;

trending key parameters for condition monitoring;

ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and

verifying appropriate performance criteria for structures, systems, and

components (SSCs)/functions classified as (a)(2) or appropriate and adequate

goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified that

maintenance effectiveness issues were entered into the CAP with the appropriate

significance characterization. Documents reviewed are listed in the Attachment to this

report.

This inspection constituted two quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b.

Findings

No findings of significance were identified.

13

Enclosure

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

345 kv Switchyard Bus 4 outage; and

345 kv Line 8014 trip.

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed Technical

Specification (TS) requirements and walked down portions of redundant safety systems,

when applicable, to verify risk analysis assumptions were valid and applicable

requirements were met.

These maintenance risk assessments and emergent work control activities constituted

two samples as defined in IP 71111.13-05.

b.

Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a.

Inspection Scope

The inspectors reviewed the following issues:

IR 957843, Failed Flowscan on AOV [air operated valve] 3-1599-61;

IR 967008, Degraded Thermal Performance of the 2A LPCI [low pressure

coolant injection] Hx [heat exchanger];

IR 987982, Boron Liquid Leak on 3B SBLC [standby liquid control] Pump; and

IR 986676, Auto Bypass Sensors Not in Accordance with

UFSAR Requirements.

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and UFSAR to the licensees evaluations, to determine

whether the components or systems were operable. Where compensatory measures

14

Enclosure

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors also reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment to this report.

This operability inspection constituted four samples as defined in IP 71111.15-05.

b.

Findings

(1) NRC Inspector-Identified Control Room Alarm Isolation Valve Out-of-Position

Introduction: A finding of very low safety significance and associated NCV of TS 5.4.1

was identified by the inspectors for the licensee failing to follow Dresden procedure

DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39. The inspectors

identified valve 2-1501-42A, U2 low pressure coolant injection (LPCI) A pump gland

leak-off, was out-of-position (closed) and documented an unresolved item (URI) in

inspection report 05000237/2009004; 05000249/2009004.

Description: On September 24, 2009, the inspectors identified that the 2-1501-42A

valve was out-of-position. The inspectors were reviewing the 2A LPCI pump seal

leak-off configuration as part of an evaluation of the mechanical seal safety

classification. The inspectors reported the valve position to shift management and

operations department personnel verified the valve was not in the open position as

described in DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39.

This issue was documented in IR 969490, LPCI Gland Seal Leak-off Isolation Found

Closed. With the valve closed instead of open, a control room alarm (902-3 C-6) for

LPCI pump seal leakage would not have alarmed for the 2A LPCI pump had the seal

failed during operation.

The issue was considered an unresolved item in Inspection Report 05000237/2009-004;

05000249/2009-004 pending NRC review of the licensees evaluation of the valve

position versus the requirements of DOP 2-1500-M1.

The licensee performed a prompt investigation into the mispositioning of the valve.

The licensee was unable to determine the reason for, or the time at which the valve

became mispositioned. The licensee did determine that on July 6, 2009, the 2A LPCI

pump seal was replaced under Work Order 548808-01 and procedure DMP 1500-05,

LPCI Pump Maintenance, Revision 8.

The inspectors observed that the licensee took a corrective action to change

maintenance procedure DMP 1500-05, LPCI Pump Maintenance, Revision 8,

step G.25.d to include the case drain valve equipment numbers. The inspectors

reviewed procedure DMP 1500-05, Revision 8, step G.25.d and found that it had

directed only that the case drain valves be closed with no specific equipment number

designations. Since the valve that was found mispositioned was a drain valve and in

close proximity to the case drain valves, it was possible that 2-1501-42A was closed at

the same time that the case drain valves were closed. There was no step in

DMP 1500-05 past step G.25.d to open the case drain valves.

15

Enclosure

Analysis: The inspectors determined that the as found position of 2-1501-42A was

contrary to the requirement of DOP 2-1500-M1, LPCI System Mechanical Checklist,

Revision 39 and was a performance deficiency.

The finding was determined to be more than minor because the finding, if left

uncorrected, would become a more significant safety concern. Specifically, the valve

isolated an alarm in the control room. The alarm warned the control room operators of a

LPCI pump mechanical seal failure. A mechanical seal failure of a LPCI pump during an

accident condition could result in exceeding the limits of the leakage outside the primary

containment as described in TS` 5.5.2. The inspectors concluded this finding was

associated with the Mitigating Systems Cornerstone.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of Findings, Table 4a, dated January 10, 2008,

for the Mitigating System Cornerstone. The inspectors answered No to all five

questions on Table 4a. This issue screened as Green.

This finding has a cross-cutting aspect in the area of Human Performance, Work

Practices because the licensee did not have any documentation as to how or when the

valve was placed into the position it was in. The design and location of the valve

precluded that the valve was accidently placed into the position it was found in.

Therefore, the inspectors concluded that either the failure to use human error prevention

techniques or maintaining proper documentation of activities caused the mispositioning

of valve 2-1501-42A. H.4(a)

Enforcement: Technical Specification Section 5.4.1.a states, in part, that

Written procedures shall be established, implemented, and maintained covering the

following activities: The applicable procedures recommended in Regulatory Guide 1.33,

Revision 2, Appendix A, February 1978. Paragraph 4 of this Regulatory Guide states,

in part, that procedures for energizing, filing, venting, draining, startup, shutdown, and

changing modes of operation for Emergency Core Cooling Systems shall be prepared

and activities shall be performed in accordance with these procedures. The licensee

established DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39, as one

of the implementing procedures.

Contrary to the above, on September 24, 2009, the inspectors identified that the

2-1501-42A valve was not in the open position as required by DOP 2-1500-M1,

LPCI System Mechanical Checklist, Revision 39. The licensee took the following

corrective actions: restored 2-1501-42A to the correct position; changed maintenance

procedure DMP 1500-05, LPCI Pump Maintenance, step G.25.d to include the case

drain valve equipment numbers and sign offs to position and verify the valves; and

Operations Department Management addressed the operations department personnel

about this issue. Because this violation was of very low safety significance and it was

entered into the licensees corrective action program as IR 969490, this violation is being

treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy.

(NCV 05000237/2009005-02) (URI 05000237/2009004-04; 05000249/2009004-04 is

closed.

16

Enclosure

1R19 Post-Maintenance Testing (71111.19)

.1

Post-Maintenance Testing

a.

Inspection Scope

The inspectors reviewed the following post-maintenance (PM) activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

WO 1152490-08, OP Perform as Left LLRT [local leak rate test] on 2-0203-2C

MSIV [main steam isolation valve];

WO 1293386, TSC [Technical Support Center] HVAC [heating, ventilation and

air conditioning] Surveillances Failed;

WO 1285845, U2 EDG [emergency diesel generator] Largest Load Reject

(TSR 3.8.1.10);

WO 1286397, 2/3 EDG Voltage Transient; and

WO 1098975-02, Perform 2B Condensate Pump Inspections.

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted five post-maintenance testing samples as defined in

IP 71111.19-05.

b.

Findings

(1) Preconditioning the Unit 2 EDG Prior to Performing Technical Specification (TS)

Surveillance Requirements (SRs)

Introduction: The inspectors identified a finding of very low safety significance and an

associated NCV of 10 CFR 50 Appendix B, Criterion XI, Test Control, because the

licensee unacceptably preconditioned the Unit 2 EDG prior to performing TS

SRs 3.8.1.19.c.4, 3.8.1.12.c.3, and 3.8.1.10 (Green). These TS SRs involved verifying

that the EDG supplied steady state frequency would be acceptable following a loss

offsite power (LOOP) coincident with and without a loss of coolant accident (LOCA), and

following the loss of the largest post-accident load. Specifically, the inspectors identified

17

Enclosure

that the licensee performed governor oil change outage maintenance activities which

involved a section that tuned the Unit 2 diesel governors response to a load change just

prior to performing these TS SRs. The licensee performed the governor oil change

maintenance every six years. The SRs listed above were performed every two years.

Description: On November 13, 2009, during the performance of TS SR 3.8.1.10, under

work order (WO) 00634625-01, the Unit 2 EDG did not recover fast enough to satisfy the

TS SR acceptance criteria. After the largest single post-accident load was shed

(i.e., a service water pump), the EDG frequency went up to 62.4 Hz and did not recover

to the allowable band of 58.8-61.2 Hz until 13 seconds had passed. Technical

Specification SR 3.8.1.10 requires the bus frequency to recover in less than 4 seconds.

The licensee entered this condition into the corrective action program (IR 992803).

A second work order (WO 01285845-01) was created, which adjusted the governor

compensator by using work instructions located in station procedure DES 6600-01,

Diesel Generator Governor Oil Change and Compensation Adjustment, Revision 23.

Following the adjustment, the Unit 2 EDG passed TS SR 3.8.1.10 satisfactorily.

The licensee performed a cause evaluation and determined that the Unit 2 EDG failed

the TS SR because the governor compensation was incorrectly set when performing

WO 634625-01, D2 3RFL PM D/G Governor - Change Oil/Flush/Compensate six days

earlier on November 7, 2009. The licensee determined in their extent of condition

review that the other EDGs were not susceptible to the Unit 2 EDG issue because they

had been successfully tested by performing TS SR 3.8.1.10 as a post-maintenance test

(PMT) since their respective governor oil change outs. The inspectors identified that it

was the practice for the licensee to utilize TS SR 4.8.1.10 as a PMT when performing

these oil changes on a six year interval.

The inspectors questioned the practice of performing preventative maintenance (PM)

activities which involved tuning the EDG governor response just prior to the EDGs

biennial design basis loading/load shedding tests. Furthermore, the inspectors noted

that the maintenance activity utilized to resolve the failed TS SR was to re-perform the

governor compensator adjustment section of the PM activity used on November 7, 2009.

The licensee stated that, after evaluating the issue under IR 1000609, Assignment 1,

that the inspectors issue was an example of acceptable pre-conditioning, primarily for

two reasons. The licensee agreed that the PM and PMT could mask the as-found EDG

governors response during the performance of TS SR 3.8.1.10, but was acceptable

because the TS SR is usually performed without the PM/PMT activity the majority of the

time (oil change/flush every six years, and TS SR is performed every two years.).

In addition the licensee determined that a second diesel run would be required, and that

this run would unnecessarily stress the machine.

The inspectors disagreed with the licensees CAP evaluation and conclusions and

communicated the issue through Dresden management. The inspectors consulted the

NRR Quality Assurance, Vendor Inspection, and Maintenance Branch as recommended

in the NRCs Inspection Manual Part 9900 guidance regarding preconditioning.

The NRR Branch agreed that this issue was not consistent with the guidance outlined in

the NRC technical guidance or Information Notice 97-16, Preconditioning of Plant

Structures, Systems, and Components before ASME Code Inservice Testing or

Technical Specification Surveillance Testing.

18

Enclosure

Analysis: The inspectors determined that the licensee did not establish suitable test

conditions during the Unit 2 EDG TS SRs 3.8.1.19.c.4, 3.8.1.12.c.3, and 3.8.1.10.

The inspectors identified that this was a performance deficiency based on the

10 CFR 50, Appendix B, Criterion XI, Test Control regulatory requirements and the

NRCs generic communication to licensees regarding preconditioning. The failure to

properly test the EDG is considered more than minor because, if left uncorrected, the

finding would become a more significant safety concern. Unacceptable preconditioning

of the EDG could mask latent performance issues and affect the ability of the EDG to

supply safety-related power to vital loads during an event. The inspectors determined

that traditional enforcement was not appropriate because it was not apparent that the

performance deficiency affected the ability of the NRC to regulate. However, the

inspectors noted that this issue could mask failed TS SRs, which would directly feed into

the NRC assessment process. This issue was determined to be Green because it did

not result in an inoperable Unit 2 EDG.

The inspectors determined that the failure to adequately coordinate the work activity of

the PM/PMT and TS SR activities was the principal contributor to this finding and was

reflective of recent performance. This finding had a cross-cutting aspect in the area of

Work Control. Specifically the licensee did not appropriately coordinate work activities

by incorporating actions to address the impact of the work as different job activities. The

scheduling of the work activities resulted in the pre-conditioning of the EDG prior to the

surveillance tests. H.3(b)

Enforcement: 10 CFR 50, Appendix B, Criterion XI, Test Control, requires, in part,

that the test is performed under suitable environmental conditions. Suitable

environment conditions include conditions representative of the expected conditions

when the equipment is required to perform its safety function. The adjustment of the

Unit 2 EDG governor compensator affects how the EDG governor will respond when

TS SRs 3.8.1.19.c.4, 3.8.1.12.c.3, and 3.8.1.10. are performed and, therefore,

preconditions the EDG. The licensee agreed to change the method by which their

maintenance and testing was performed, but had not reached a conclusion on corrective

actions by the end of the inspection period. Because the finding is of very low safety

significance, and has been entered into the corrective action program as IR 01000609, it

is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy,

NUREG 1600. (NCV 05000237/2009005-03)

(2) 2/3 Emergency Diesel Generator (EDG) Overvoltage during Division I Undervoltage

Surveillance

a.

Inspection Scope

The inspectors reviewed the licensees equipment apparent cause evaluation (EACE) in

response to a 2/3 EDG overvoltage during performance of DOS 6600-06,

Bus Undervoltage and ECCS Integrated Functional Test for Unit 2/3 Diesel Generator

to Unit 2, Revision 46. Documents reviewed in this inspection are listed in the

Attachment to this report.

This post-maintenance testing review constituted one sample as defined in IP 71111.19.

19

Enclosure

b.

Findings

Introduction: The inspectors identified an URI regarding the regulatory requirements

associated with the circumstances surrounding the 2/3 EDG overvoltage event on

November 16, 2009.

Description: On November 16, 2009, at 10:53 a.m., a nuclear station operator (NSO)

was performing step I.11.c per DOS 6600-06, Bus Undervoltage and ECCS Integrated

Functional Test for Unit 2/3 Diesel Generator to Unit 2, Revision 46. At this time, the

operator was attempting to synchronize Bus 23-1 (powered from 2/3 EDG) to Bus 23

(powered from reserve auxiliary transformer 22). The operator stated that he was only

monitoring running versus on-coming bus voltage meters, which are transformed down

and are only relative to actual bus voltages. The operator stated that a loud pop noise

was heard from the 902-3 panel. At this time, the operator noticed that the 23-1/24-1

digital volt meter read around 5600 volts (was previously around 4100 volts). The 2/3

EDG was then shutdown per DOS 6600-06 step I.12. On step I.12.c, the voltage

regulator would not lower (remained upscale). The EDG stopped after the 6-minute cool

down and DOS 6600-06 was stopped.

The licensee generated EACE 994101-07, 2/3 Emergency Diesel Generator (EDG)

Voltage Transient, to determine the cause, extent of condition and corrective actions for

this event. The inspectors reviewed EACE 994101-07 and interviewed the NSO who

had performed DOS 6600-06. The inspectors raised more questions regarding the

capabilities of the control room simulator used for training, procedure adequacy and the

corrective actions in place. The inspectors plan to review the licensees response to

their questions to determine if there were any violations of NRC requirements and that

appropriate corrective actions were applied. (URI 05000237/2009005-04; 05000249/2009005-04)

1R20 Outage Activities (71111.20)

.1

Other Outage Activities

a.

Inspection Scope

The inspectors evaluated outage activities for a Unit 3 forced outage that began on

October 3, 2009, and continued through October 8, 2009. The forced outage was

caused by a Group 1 isolation and reactor scram caused by a pressure pulse caused by

the restoration of the Unit 3 reactor water clean-up system. The inspectors reviewed

activities to ensure that the licensee considered risk in developing, planning, and

implementing the outage schedule.

The inspectors observed or reviewed the reactor shutdown and cooldown, outage

equipment configuration and risk management, electrical lineups, selected clearances,

control and monitoring of decay heat removal, control of containment activities, startup

and heatup activities, and identification and resolution of problems associated with the

outage.

This inspection constituted one other outage sample as defined in IP 71111.20-05.

20

Enclosure

b.

Findings

No findings of significance were identified.

.2

Refueling Outage Activities

a.

Inspection Scope

The inspectors reviewed the Outage Safety Plan (OSP) and contingency plans for the

Unit 2 refueling outage (RFO), conducted November 1, 2009, through

December 9, 2009, to confirm that the licensee had appropriately considered risk,

industry experience, and previous site-specific problems in developing and implementing

a plan that assured maintenance of defense-in-depth. During the RFO, the inspectors

observed portions of the shutdown and cooldown processes and monitored licensee

controls over the outage activities listed below. Documents reviewed during the

inspection are listed in the Attachment to this report.

Licensee configuration management, including maintenance of defense-in-depth

commensurate with the OSP for key safety functions and compliance with the

applicable TS when taking equipment out-of-service.

Implementation of clearance activities and confirmation that tags were properly

hung and equipment appropriately configured to safely support the work or

testing.

Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error.

Controls over the status and configuration of electrical systems to ensure that

TS and OSP requirements were met, and controls over switchyard activities.

Monitoring of decay heat removal processes, systems, and components.

Controls to ensure that outage work was not impacting the ability of the operators

to operate the spent fuel pool cooling system.

Reactor water inventory controls including flow paths, configurations, and

alternative means for inventory addition, and controls to prevent inventory loss.

Controls over activities that could affect reactivity.

Maintenance of secondary containment as required by TS.

Refueling activities, including fuel handling and sipping to detect fuel assembly

leakage.

Startup and ascension to full power operation, tracking of startup prerequisites,

walkdown of the drywell (primary containment) to verify that debris had not been

left, which could block emergency core cooling system suction strainers, and

reactor physics testing.

Licensee identification and resolution of problems related to RFO activities.

This inspection constituted one RFO sample as defined in IP 71111.20-05.

21

Enclosure

b.

Findings

(1) Failure to Follow the Master Refueling Procedure During Movement of Fuel Assembly

JLU569

Introduction: A finding of very low significance (Green) was self-revealed involving a

NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, for failing to follow DFP 0800-01, Master Refueling Procedure, Revision 45,

Page 12, Step 2.b, when the licensee moved fuel assembly JLU569 to the wrong

position in the Unit 2 Spent Fuel Pool during D2R21, on November 5, 2009.

Description: On November 6, 2009, during fuel shuffle 1, the fuel handling crew was

moving a fuel assembly from the reactor to location C4-E5 of the spent fuel pool, per

step 475 of the Nuclear Component Transfer List (Move Sheet), in accordance with

DFP 0800-01, Master Refueling Procedure. While making the move the refueling crew

identified a fuel assembly was already in location C4-E5. The fuel assembly being

moved was then placed in the designated Emergency Set Down Location.

It was immediately determined that the same fuel handling crew had incorrectly

performed step 294 of the Nuclear Component Transfer List the previous night,

November 5, 2009, where they positioned fuel assembly JLU569 into C4-E5, vice the

correct location of C4-F5, each location was located in the same fuel rack.

DFP 0800-01, Master Refueling Procedure, Revision 45, Step 8.d directs the

Senior Reactor Operator (SRO) on the refueling bridge to verify a fuel assembly is

placed in the correct spent fuel pool location by observing rack coordinates in the spent

fuel pool. During interviews with the inspector, it was determined that the crane

operator, fuel-handling supervisor and the SRO had each independently

(and incorrectly) identified spent fuel pool location C4-F5 as C4-E5.

Analysis: The inspectors determined that the licensees failure to move fuel assembly

JLU569 to the correct location in accordance with the Nuclear Component Transfer List

(Move Sheet) was contrary to 10 CFR 50, Appendix B, Criteria V, Instructions,

Procedures, and Drawings, which, in part, requires that activities affecting quality shall

be accomplished in accordance with prescribed instructions, and was a performance

deficiency.

The finding was determined to be more than minor because the finding was associated

with the configuration control and human performance attributes of the Barrier Integrity

Cornerstone and impacted the Barrier Integrity Cornerstone objective to provide

reasonable assurance the physical design barriers (i.e., fuel cladding) protect the public

from radionuclide releases caused by an accident or event. Specifically, the shutdown

margin and thermal management of the spent fuel pool(s) is affected by fuel assembly

placement inside the pool(s).

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of Findings, Table 3b, question 6, which directed

the inspectors to Appendix M, Significance Determination Process Using Qualitative

Criteria. Because probabilistic risk assessment tools were not well suited for this

finding, the criteria for using IMC 0609, Appendix M, were met. In determining the

22

Enclosure

significance of this finding, regional management reviewed the licensee's bounding

analysis in the UFSAR which demonstrated that regardless of the incorrect bundle

position in the spent fuel pool, the design of the pool still maintained pool Keff less

than .95. Based on the additional qualitative circumstances associated with this finding,

regional management concluded the finding was very low safety significance (Green).

This finding has a cross-cutting aspect in the area of Human Performance, Work

Practices. Specifically, neither the SRO, nor either of the two members of the fuel

handling crew, adequately performed independent verification techniques that ensured

the fuel assembly move was made in accordance with the Nuclear Component Transfer

List, as required by DFP 0800-01, Revision 45, Page 12, Step 2.b. H.4(a)

Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and

Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings, of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions,

procedures, or drawings.

Dresden procedure DFP 0800-01, Master Refueling Procedure, Revision 45 is a

procedure affecting quality. Specifically, it governs fuel movements between the spent

fuel pool and the reactor. Dresden Procedure DFP 0800-01 Step 2.b required the SRO

to ensure that the fuel assembly was moved in accordance with the Nuclear Component

Transfer List (Move Sheet).

Contrary to the above, on November 5, 2009, the licensee failed to follow DFP 0800-01,

Master Refueling Procedure, Revision 45, Step 2.b. Specifically, the fuel handling

crew positioned fuel assembly JLU569 in location C4-E5 of the U2 spent fuel pool

instead of location C4-F5. Because this violation was of very low safety significance and

it was entered into the licensees correction action program as IR 990180, this violation

is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement

Policy. (NCV 05000237/2009005-05)

Corrective actions for this event included a temporary stand down of all fuel handling

activities, a piece count of the spent fuel was performed to identify any errors associated

with fuel handling up to step 475 of the nuclear transfer list, a second SRO and a fuel

handling supervisor were stationed on the refuel bridge to provide additional oversight

during the remaining fuel moves, and the crew associated with the event were not to

resume fuel handling duties until the completion of remedial training.

1R22 Surveillance Testing (71111.22)

.1

Surveillance Testing

a.

Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

23

Enclosure

WO 1077723-01, D2 20M/RFL [20 month/refuel] TS LLRT [local leak rate test]

MSIV 203-1A & 203-2A Dry Test;

WO 1257282-01, D2 QTR SBO [station black out] Diesel Generator Surveillance

Test;

WO 1251254-01, D3 Qtr TS Reactor Low Pressure (350 PSIG) ECCS

[emergency core cooling system] Permissive Ca; and

WO 1277976-01, D3 1M TS Partially Withdrawn Control Rod Drive Exercise.

(IST Sample).

The inspectors observed in plant activities and reviewed procedures and associated

records to determine the following:

did unacceptable preconditioning occur;

were the effects of the testing adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

plant equipment calibration was correct, accurate, and properly documented;

as-left setpoints were within required ranges; and the calibration frequencies

were in accordance with TSs, the UFSAR, procedures, and applicable

commitments;

measuring and test equipment calibration was current;

test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

test data and results were accurate, complete, within limits, and valid;

test equipment was removed after testing;

where applicable for in-service testing activities, testing was performed in

accordance with the applicable version of Section XI, ASME code, and reference

values were consistent with the system design basis;

where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

equipment was returned to a position or status required to support the

performance of its safety functions; and

all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

24

Enclosure

This inspection constituted two routine surveillance testing samples, one in-service

testing sample, and one isolation valve inspection sample as defined in IP 71111.22,

Sections -02 and -05.

b.

Findings

(1) Mispositioning of Unit 3 Control Rod G-11

Introduction: A finding of very low safety significance and associated NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was

self-revealed for the mispositioning of a Unit 3 control rod at power.

Description: On November 15, 2009, during performance of DOS 0300-01, Control Rod

Exercise, Revision 48, control rod CRD G-11 was withdrawn by the reactor operator to

position 16 from position 14 instead of being inserted to position 12 as required by

procedure. The licensee entered DOA 0300-12, Mispositioned Control Rod, Revision

14; and DGA 7, Unpredicted Reactivity Addition, Revision 20. Control rod G-11 was

inserted back to the initial position of 14 and DOA 0300-12 was exited.

Analysis: The inspectors determined that the withdrawal of the control rod was contrary

to Technical Specification Surveillance Requirement 3.1.3.3 to insert each withdrawn

control rod at least one notch and was a performance deficiency.

The finding was determined to be more than minor because the finding was associated

with the Fuel Barrier Cornerstone attributes of human performance and configuration

control of a control rod, and affected the cornerstone objective of providing reasonable

assurance that physical design barriers protect the public from radionuclide releases

caused by accidents or events. Specifically, the operator withdrew a control rod contrary

to the expected operation of insertion. This added positive reactivity and caused an

unanticipated power increase. No thermal or power limits were exceeded.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of Findings, Table 4a for the Fuel Barrier

Cornerstone. Per Table 4a any issue that involves the fuel barrier is screened as Green.

This finding had no cross-cutting aspect. The inspectors determined that the licensee

had taken every precaution possible to prevent this error in advance, in that, the licensee

has briefed the evolution and stationed additional personnel to ensure correct

movement. Notwithstanding, the operator moved the rod in the wrong direction.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings, of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions,

procedures, or drawings.

Contrary to the above, on November 15, 2009, the licensee failed to perform an activity

affecting quality in accordance with the appropriate procedure during performance of

DOS 0300-01, Control Rod Exercise, Revision 48, in that, control rod CRD G-11 was

withdrawn to position 16 from position 14 instead of being inserted to position 12.

25

Enclosure

Specifically, the licensed operator moving the control rod did not follow procedure

DOS 0300-01, Step I.4.a, which stated to insert the control rod one notch. The licensee

took a series of corrective actions: control rod G-11 was inserted one notch back to the

original position and then control room operators suspended control rod movement. All

control rods were verified to be in their correct position. The operator was removed from

shift duties and the oncoming shift was briefed of the event. Because this violation was

of very low safety significance and it was entered into the licensees corrective action

program as IR 993634, this violation is being treated as an NCV, consistent with

Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000249/2009005-06)

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

.1

Emergency Action Level and Emergency Plan Changes

a.

Inspection Scope

Since the last NRC inspection of this program area, Emergency Plan Annex,

Revisions 24 and 25 were implemented based on licensee determination, in accordance

with 10 CFR 50.54(q), that the changes resulted in no decrease in effectiveness of the

Plan, and that the revised Plan continues to meet the requirements of 10 CFR 50.47(b)

and Appendix E to 10 CFR Part 50. The inspectors conducted a sampling review of the

Emergency Plan changes and a review of the Emergency Action Level (EAL) changes to

evaluate for potential decreases in effectiveness of the Plan. However, this review does

not constitute formal NRC approval of the changes. Therefore, these changes remain

subject to future NRC inspection in their entirety.

This emergency action level and emergency plan changes inspection constituted one

sample as defined in IP 71114.04-05.

b.

Findings

(1) Changes to EAL HU6 Potentially Decrease the Effectiveness of the Plans without Prior

NRC Approval

Introduction: The inspectors reviewed changes implemented to the Dresden Station

Radiological Emergency Plan Annex EALs and EAL Basis. In Revision 24, the licensee

changed the basis of EAL HU6, "Fire not extinguished within 15 minutes of detection

within the protected area boundary," by adding two statements. The two changes added

to the EAL basis stated that if the alarm could not be verified by redundant control room

or nearby fire panel indications, notification from the field that a fire exists starts the

15-minute classification and fire extinguishment clocks. The second change stated the

15-minute period to extinguish the fire does not start until either the fire alarm is verified

to be valid by additional control room or nearby fire panel instrumentation, or upon

notification of a fire from the field. These statements conflict with the previous

Dresden Station Annex, Revision 23, basis statements and potentially decrease the

effectiveness of the Plans.

Description: Dresden Station Radiological Emergency Plan Annex, Revision 23,

EAL HU6, initiating condition stated, "Fire not extinguished within 15 minutes of

26

Enclosure

detection, or explosion, within the protected area boundary." The threshold values for

HU6 were, in part: 1) Fire in any Table H2 area not extinguished within 15 minutes of

Control Room notification or verification of a Control Room alarm, or 2) Fire outside any

Table H2 area with the potential to damage safety systems in any Table H2 area not

extinguished within 15 minutes of Control Room notification or verification of a Control

Room alarm. Table H2, Vital Areas, were identified as reactor building, auxiliary electric

room, control room, diesel generator rooms, 4 kilovolt emergency core cooling system

switchgear area, battery rooms, control rod drive and component cooling service water

pump rooms, turbine building cable tunnel, turbine building safe shutdown areas, and

crib house. The basis defined fire as "combustion characterized by heat and light.

Sources of smoke such as slipping drive belts or overheated electrical equipment do not

constitute fires. Observation of flame is preferred but is not required if large quantities of

smoke and heat are observed."

The basis for Revision 23, EAL HU6 thresholds 1 and 2 stated, in part, the purpose of

this threshold is to address the magnitude and extent of fires that may be potentially

significant precursors to damage to safety systems. As used here, notification is visual

observation and report by plant personnel or sensor alarm indication. The 15-minute

period begins with a credible notification that a fire is occurring or indication of a valid fire

detection system alarm. A verified alarm is assumed to be an indication of a fire unless

personnel dispatched to the scene disprove the alarm within the 15-minute period. The

report, however, shall not be required to verify the alarm. The intent of the 15-minute

period is to size the fire and discriminate against small fires that are readily extinguished

(e.g., smoldering waste paper basket, etc.).

Revision 24 of the Dresden Station Radiological Emergency Plan Annex, changed the

threshold basis for EAL HU6 by adding the following two statements: 1) If the alarm

cannot be verified by redundant control room or nearby fire panel indications, notification

from the field that a fire exists starts the 15-minute classification and fire extinguishment

clocks, and 2) The 15-minute period to extinguish the fire does not start until either the

fire alarm is verified to be valid by utilization of additional control room or nearby fire

panel instrumentation, or upon notification of a fire from the field."

The two statements added to the basis in Revision 24 conflict with the Revision 23

threshold basis and initiating condition. The changed threshold basis in Revision 24

could add an indeterminate amount of time to declaring an actual emergency until a

person responded to the area of the fire and made a notification to the control room of a

fire in the event that redundant control room or nearby fire panel indications were not

available.

Pending further review and verification by the NRC to determine if the changes to

EAL HU6 threshold basis potentially decreased the effectiveness of the Plans, this issue

was considered an Unresolved Item. (URI 05000237/2009005-07)

27

Enclosure

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1

Plant Walkdowns and Radiation Work Permit Reviews

a. Inspection Scope

The inspectors reviewed licensee controls and surveys in the following radiologically

significant work areas within radiation areas, high radiation areas, and airborne

radioactivity areas in the plant to determine if radiological controls including surveys,

postings, and barricades were acceptable:

Drywell Nuclear Instrumentation System Maintenance;

Drywell In-Service Inspection;

Drywell Control Rod Drive System Maintenance and Support.

The inspectors walked down and surveyed (using an NRC survey meter) these areas to

verify that the prescribed RWP, procedure, and engineering controls were in place; that

licensee surveys and postings were complete and accurate; and that air samplers were

properly located.

This sample was documented and credited in Inspection Report 05000237/2009003;

05000249/2009003; therefore, this review does not represent a sample.

b. Findings

No findings of significance were identified.

.2

Radiation Worker Performance

a. Inspection Scope

During job performance observations, the inspectors evaluated radiation worker

performance with respect to stated radiation safety work requirements. The inspectors

evaluated whether workers were aware of any significant radiological conditions in their

workplace, of the RWP controls and limits in place, and of the level of radiological

hazards present. The inspectors also observed worker performance to determine if

workers accounted for these radiological hazards.

This sample was documented and credited in Inspection Report 05000237/2009003;

05000249/2009003; therefore, this review does not represent a sample.

b. Findings

No findings of significance were identified.

28

Enclosure

2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)

.1

Inspection Planning

a.

Inspection Scope

The inspectors reviewed plant collective exposure history, current exposure trends, and

ongoing and planned activities in order to assess current performance and exposure

challenges. The inspectors reviewed the plants current 3-year rolling average for

collective exposure in order to help establish resource allocations and to provide a

perspective of significance for any resulting inspection finding assessment.

This inspection constituted one required sample as defined in IP 71121.02-5.

b.

Findings

No findings of significance were identified.

.2

Radiological Work Planning

a.

Inspection Scope

The inspectors evaluated the licensees list of work activities ranked by estimated

exposure that were in progress and reviewed the following three work activities of

highest exposure significance:

Drywell Nuclear Instrumentation System Maintenance;

Drywell In-Service Inspection; and

Drywell Control Rod Drive System Maintenance and Support.

This sample was documented and credited in Inspection Report 05000237/2008005;

05000249/2008005; therefore, this review does not represent a sample.

For these three activities, the inspectors reviewed the As-Low-As-Reasonably-

Achievable (ALARA) work activity evaluations, exposure estimates, and exposure

mitigation requirements in order to verify that the licensee had established procedures

and engineering and work controls that were based on sound radiation protection

principles in order to achieve occupational exposures that were ALARA. The inspectors

also determined if the licensee had reasonably grouped the radiological work into work

activities, based on historical precedence, industry norms, and/or special circumstances.

This sample was documented and credited in Inspection Report 05000237/2008005;

05000249/2008005; therefore, this review does not represent a sample.

b. Findings

No findings of significance were identified.

29

Enclosure

.3

Source-Term Reduction and Control

b. Inspection Scope

The inspectors reviewed licensee records to evaluate the historical trends and the

current status of tracked plant source terms. The inspectors determined if the licensee

was making allowances and had developing contingency plans for expected changes in

the source term due to changes in plant fuel performance issues or changes in plant

primary chemistry.

This inspection constituted one required sample as defined in IP 71121.02-5.

c. Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification (71151)

Cornerstone: Barrier Integrity

.1

Reactor Coolant System Leakage

a.

Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system (RCS)

leakage performance indicator for Units 2 and 3 for the period from the fourth

quarter 2008 through the third quarter 2009. To determine the accuracy of the PI data

reported during those periods, PI definitions and guidance contained in the Nuclear

Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 5, were used. The inspectors reviewed the licensees operator

logs, RCS leakage tracking data, issue reports, event reports and NRC Integrated

Inspection Reports for the period of January 2009 through November 2009 to validate

the accuracy of the submittals. The inspectors also reviewed the licensees issue report

(IR) database to determine if any problems had been identified with the PI data collected

or transmitted for this indicator and none were identified. Documents reviewed are listed

in the Attachment to this report.

This inspection constituted two reactor coolant system leakage samples as defined in

IP 71151-05.

b.

Findings

No findings of significance were identified.

30

Enclosure

Cornerstone: Occupational Radiation Safety

.2

Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors sampled licensee submittals for the Occupational Radiological

Occurrences performance indicator for the period from the third quarter 2008 through the

third quarter 2009, to determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors

reviewed the licensees assessment of the PI for occupational radiation safety to

determine if indicator related data was adequately assessed and reported. To assess

the adequacy of the licensees PI data collection and analyses, the inspectors discussed

with radiation protection staff, the scope and breadth of its data review, and the results of

those reviews. The inspectors independently reviewed electronic dosimetry dose rate

and accumulated dose alarm and dose reports and the dose assignments for any

intakes that occurred during the time period reviewed to determine if there were

potentially unrecognized occurrences. The inspectors also conducted walkdowns of

numerous locked high and very high radiation area entrances to determine the adequacy

of the controls in place for these areas. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted one occupational radiological occurrences sample as defined

in IP 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1

Routine Review of Items Entered Into the CAP

a.

Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees CAP at

an appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: the complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent of condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the attached List of Documents Reviewed.

31

Enclosure

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b.

Findings

No findings of significance were identified.

.2

Daily CAP Reviews

a.

Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b.

Findings

No findings of significance were identified.

.3

Semi-Annual Trend Review

a.

Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue.

The inspectors review was focused on repetitive equipment issues, but also considered

the results of daily inspector CAP item screening discussed in Section 4OA2.2 above,

licensee trending efforts, and licensee human performance results. Specifically, the

inspectors performed a review of the licensees corrective actions program documents

related to the areas of instrument air systems, heating, ventilation and air conditioning,

and instruments and controls. The inspectors review nominally considered IRs that

were generated in the six month period of July 2009 through December 2009, although

some examples expanded beyond those dates where the scope of the trend warranted.

In addition to reviewing the IR documents for trends, the inspectors compared their

results with issues identified in the licensees trending reports. A sample of the licensee

IRs associated with trends was reviewed for corrective action adequacy.

This review constituted a single semi-annual trend inspection sample as defined in

IP 71152-05.

b.

Findings

No findings of significance were identified.

32

Enclosure

.4

In-Depth Review - Corrective Actions Associated With Tube Blockages of the Unit 2 and

Unit 3 LPCI Heat Exchangers

a.

Inspection Scope

The inspectors performed a focused review of root cause report (RCR) 967008-03,

Dresden 2-1503-A, 2A Low Pressure Coolant Injection (LPCI) / Containment Cooling

Heat Exchanger (Hx) Failure to Meet Design Basis Heat Removal Capability due to

Asiatic Clam Macrofouling resulting from 2-1501-3A Valve Leakage and Subsequent

Untreated Service Water Make-up via the CCSW Keepfill Diluting the Biocide Treatment

below the Asiatic Clam Lethal Concentration, revision 0, to evaluate the corrective

actions that the licensee had taken to address the introduction of Asiatic clam relics into

the containment cooling heat exchangers.

Containment cooling is the operating mode of the low pressure coolant injection (LPCI)

subsystem initiated to cool the containment in the event of a loss-of-coolant accident

(LOCA). Each containment cooling subsystem consists of two LPCI pumps, one

containment cooling Hx (also called LPCI Hx), one drywell spray header and a separate

suppression chamber spray header. Heat exchanger cooling water is provided by two

containment cooling service water (CCSW) pumps in each containment cooling

subsystem. The water source for the CCSW pumps is the cribhouse, specifically

Bay 13. If the heat exchanger is significantly fouled, then the Hx may be unable to

remove sufficient heat from the containment, which could result in primary containment

failure.

In addition, the inspectors performed a focused review to evaluate the licensees

assessment of a number of IRs related to the failure to meet biocide residual

concentration after chemical addition into the containment cooling service water system.

The inspectors reviewed these issues to determine if the licensee has taken adequate

corrective actions both individually and collectively. This review constituted one sample

as defined in IP 71152.

The inspectors reviewed several documents that are listed in the Attachment of the

report.

Issues

(1) Effectiveness of Problem Identification

The licensees thermal performance testing of the LPCI heat exchangers has been

effective in identifying heat exchanger degradation prior to the Hx becoming inoperable.

On September 18, 2009, a thermal performance test was performed on the 2A LPCI Hx.

The test results indicated a heat removal capability of 67.49 MBtu/hr, which was

4.9 percent below the design heat removal rate of 71 MBtu/hr at design conditions per

the updated final safety analysis report (UFSAR) Table 6.2-3b, Heat Exchanger Heat

Transfer Rate. This issue was documented in IR 967008. Further evaluation

determined that with a heat removal capability of 67.49 MBtu/hr the new maximum

allowable inlet water temperatures for the 3 months following the test performed on

September 18, were 90.2 degrees F, 89.7 degrees F and 88 degrees F, respectively.

Actual CCSW temperatures for the time period, including previous summer months,

were below the design basis parameter of 95 degrees F, therefore, the licensee

33

Enclosure

determined that the 2A LPCI Hx, although degraded, was able to perform the required

design functions. Also, the licensee reviewed the results for the most recent thermal

performance tests performed for the other three heat exchangers and based on these

results the licensee determined that the heat exchangers were operable.

On November 5, 2009, the 2A LPCI Hx was opened for inspection and cleaning.

Approximately 50 percent of the 1256 CCSW inlet tubes were partially or fully

obstructed. The primary macrofouling mechanism was Asiatic clam relics coupled with

silt microfouling. Issue report 989609, D2R21 Inspection Results for 2A LPCI

Heat Exchanger, was generated to document the as-found condition. The 2A LPCI Hx

was cleaned and the thermal performance testing was re-performed in December 2009.

The new test results indicated a heat removal capability of 78.08 MBtu/hr at design

conditions which is 10 percent above the design heat removal rate.

(2) Prioritization and Evaluation of Problems

The licensees evaluation of the cause of the repetitive LPCI Hx blockages and

prioritization of corrective actions were ineffective. This was the third blockage of a LPCI

Hx by Asiatic clams. The first event occurred on the 3B LPCI Hx in September of 2006.

At that time the build up of Asiatic clams was thought to be due to a change in the

frequency of Bay 13 cleaning. The second event took place in March 2008, when the 3B

LPCI Hx failed its thermal performance test (70.586 vice 71 MBtu/hr). Root Cause

Report 776598-08, Dresden 3-1503-B, 3B Low Pressure Coolant Injection (LPCI) /

Containment Cooling Heat Exchanger (HX) Failure to Meet Design Basis Heat Removal

Capability Due to Inadequate Programmatic Control of Macrofoulants, revision 0,

attributed the failure of the 3B LPCI Hx to meet the design basis heat removal capability

to inadequate programmatic control of macrofoulants. Specifically, the licensee failed to

inject biocide into the containment cooling service water pumps' intake during normally

scheduled operability surveillances and sample to verify biocide residual concentration.

This was contrary to the licensees Generic Letter 89-13 Program commitments (refer to

inspection report 05000237/2008-005; 05000249/2008-005 Section 1R15 for more

details). Corrective actions included injection of biocide into the containment cooling

service water pumps' intake (e.g., Bay 13) during normally scheduled surveillances and

sample to verify biocide residual concentration.

Root cause report 776598-08 was revised on January 9, 2009. Revision 1 included an

additional causal factor which stated that a potential existed for a significant section of

the CCSW pump discharge piping to not receive a lethal biocide concentration for the

required contact time to ensure a 100 percent mortality rate for the control of

macrofoulants. This was due to the leak-by of the 2(3)-1501-3A(B), Unit 2(3) LPCI Hx

A(B) tube side discharge motor operated valves (MOVs). If leakage past these valves

occurs, then the untreated service water CCSW keepfill (strained river water) will supply

an equivalent volume of makeup water into the CCSW pump common discharge header

and result in the dilution of any chemical biocide present in the piping. This portion of

the pipe is located upstream of the LPCI Hxs and it is in this portion of the pipe where

the licensee postulates the Asiatic clams are growing and eventually getting transported

to the Hxs.

On May 22, 2009, RCR 776598-08 was revised again. Revision 2 added action

number 776598-50 to track a Unit 2(3) biocide chemical injection configuration change to

completion. This configuration change shall inject biocide into the CCSW keepfill service

34

Enclosure

water to eliminate biocide dilution resulting from leak-by of the 2-1501-3A, 2-1501-3B,

3-1501-3A and 3-1501-3B valves. This configuration change is schedule to be installed

in April 2010 on Unit 2 and May of 2010 on Unit 3. The purpose of this new biocide

injection skid is to eliminate the Asiatic clam population residing in the Unit 2 and Unit 3

CCSW piping.

The inspectors inquired why there was such a long lead time for the injection skid

modification. Through discussions with engineering management in December 2009, it

became clear that the modification was thought to be for budgetary reasons only, and

that the skid was to reduce the amount, and therefore the cost, of biocide that was being

injected. Engineering management thought that sufficient amounts of biocide were

being injected to adequately kill the Asiatic clams in the piping even though root cause

report 776598-08, revision 1 dated January 9, 2009, stated that an additional causal

factor potential existed for a significant section of the CCSW pump discharge piping to

not receive a lethal biocide concentration for the required contact time to ensure a

100 percent mortality rate for the control of macrofoulants.

(3) Effectiveness of Corrective Actions to Preclude Repetition

From January through September 2009, the licensee failed to take corrective actions to

prelude repetition of a condition meeting the licensee's definition of a significant

condition adverse to quality, associated with both Unit 2 and Unit 3 CCSW systems

which affected the performance of the LPCI heat exchangers. Specifically, the licensee

failed to provide a sufficient Asiatic clam lethal concentration of 8 PPM for the required

minimum 18 hour2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> contact time to ensure a 100 percent mortality rate for Asiatic clams

which was necessary to ensure that the heat exchangers continued to meet their design

basis heat removal requirements. The failure to perform these actions caused the

blocking of the 2A LPCI Hx tubes by Asiatic clams which resulted in the degraded

thermal performance of the Hx. Licensee planned corrective actions include the

installation of a temporary modification to provide temporary keepfill that is expected to

provide better chemical treatment of the CCSW piping upstream of the LPCI Hxs. This

violation was determined to be of very low safety significance because even though the

2A LPCI Hx was degraded it was able to perform the required design safety function.

b.

Findings

The inspectors determined that the failure to take corrective action to preclude repetition

of heat exchanger blockage by providing a sufficient Asiatic clam lethal concentration of

8PPM for the required minimum 18 hour2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> contact time to ensure a 100 percent mortality

rate was a licensee-identified violation and is documented in Section 4OA7 of this report.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)

.1

(Closed) Licensee Event Report (LER) 05000237/2009-001-00; 05000249/2009-001-00,

Common Mode Failure of Reactor Building Isolation Dampers

This event, which occurred on February 6, 2009, was identified as a result of a licensee

review of failures of reactor building ventilation isolation dampers at Dresden and

another Exelon facility. Licensee failure analysis determined the damper failure

mechanism to be the result of inadequate lubrication of internal parts and installation of

upgraded solenoid valves that was completed in January of 2009. The NRC identified

35

Enclosure

the slow response to identifying the common mode failure and failure to write trending

condition reports to document the adverse trend. Inspectors verified replacement

solenoid valves continued to perform correctly and other corrective actions put in place

were appropriate to correct the procedural non-compliance issues. Documents reviewed

as part of this inspection are listed in the Attachment to this report. A NCV was written in

inspection report 05000237/2009002; 05000249/2009002 as05000237/2009002-04.

This LER is closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

.2

(Closed) LER 249/2009-001-00, Unit 3 Group 1 Isolation and Automatic Reactor Scram

a.

Inspection Scope

The inspectors reviewed LER 249/2009-001-00, Unit 3 Group 1 Isolation and Automatic

Reactor Scram, to ensure that the issues documented in the report were adequately

addressed in the licensees corrective action program. The inspectors interviewed plant

personnel and reviewed operating and maintenance procedures to ensure that generic

issues were captured appropriately. The inspectors reviewed operator logs, issue

reports, the Updated Final Safety Analysis Report, and other documents to verify the

statements contained in the LER. This LER is closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

b.

Findings

Introduction: A finding of very low significance (Green) involving a NCV of TS 5.4.1 was

self-revealed when Unit 3 experienced an automatic reactor scram and Group 1 primary

containment isolation signal (PCIS) when operators were restoring the reactor water

cleanup (RWCU) system with the reactor at pressure. Station procedure DOP 1200-03,

RWCU System Operation with the Reactor at Pressure, Revision 51, failed to identify

the correct position of motor operated valve (MOV), 3-1201-7, RWCU System Return to

Reactor. This procedural deficiency caused a pressure pulse that resulted in a reactor

water level Low-Low Group 1 Isolation Signal and Unit 3 reactor scram.

Description: On October 3, 2009, Unit 3 experienced an automatic reactor scram and

Group 1 PCIS. Due to the Group 1 PCIS, the inboard and outboard main steam

isolation valves closed as designed. In addition, PCIS Group 2 and Group 3 isolations

were received and verified complete. Operators manually initiated the isolation

condenser to control reactor pressure within limits.

The RWCU system had tripped earlier on October 2, 2009. On October 3, 2009, prior to

the reactor scram, operators were restoring the reactor water cleanup system per station

procedure DOP 1200-03, RWCU System Operation with the Reactor at Pressure,

Revision 51. Per the procedure, RWCU was being filled and heated in the blowdown

mode with a flow path from the reactor pressure vessel (RPV) to the main condenser.

While the fill was being performed, the 3-1201-7 valve, Unit 3 RWCU System Return to

Reactor, was closed. Reactor water cleanup system operation in the blowdown mode

with the 3-1201-7 valve closed resulted in: (1) heat up and expansion of the water

volume upstream of the 3-1201-7 valve (area of high pressure), and (2) cooling and

36

Enclosure

contraction of the water volume downstream of the 3-1201-7 valve (area of low

pressure). This condition created a high differential pressure across the valve.

A root cause investigation determined that under these conditions, when the 3-1201-7

valve was opened, the pressurized water upstream of the valve flashed to steam in the

lower pressure region downstream of the valve. The resulting pressure pulse was

sensed by the RPV level transmitters, resulting in a Reactor Water Level Low SCRAM

Signal and Reactor Water Level Low-Low Group 1 Isolation Signal.

The licensee determined that the probable cause for the pressure pulse initiating the

Reactor Water Level Low-Low Group 1 Isolation Signal and Unit 3 Reactor SCRAM was

a latent procedural deficiency. DOP 1200-03 provided inadequate guidance for the

3-1201-7 valve position during system startup with the RPV at pressure. In GEK-32399,

Dresden 3 Instrumentation Subsystem of the Reactor Water Cleanup System,

Section 3-11, Normal Operation, Table 3-6, Valve Positions for Cleanup System

Startup during Normal Operations, the reactor vendor, General Electric, recommended

that the Reactor Return Isolation Valve 1201-7 be in the open position for RWCU system

startup when the reactor is at power. This recommendation was not incorporated in

DOP 1200-03. Procedure DOP 1200-03, step G.1.g.(2) , gave the option to the operator

to open MOV 3-1201-7 at that step or later on in the procedure. During this event, the

3-1201-7 valve was opened later on in the procedure.

Analysis: The inspectors determined that the licensees failure to include pertinent

information regarding valve position during RWCU system startup with the RPV at

pressure in DOP 1200-03 was a performance deficiency warranting a significance

evaluation. Using IMC 0612, Appendix B, Issue Screening, issued on

December 4, 2008, the inspectors determined that this finding was more than minor

because it impacted the Initiating Events Cornerstone objective to limit the likelihood of

those events that upset plant stability and challenge critical safety functions during

shutdown as well as at power operations. The failure to maintain adequate procedures

for the restoration of systems can result in events (i.e., reactor scram) that upset plant

stability. This condition caused a pressure pulse that was sensed by the RPV level

transmitters, resulting in a Reactor Water Level Low SCRAM Signal and Reactor Water

Level Low-Low Group 1 Isolation Signal. This finding had a cross-cutting aspect in the

area of Human Performance Resources because the licensee did not provide complete,

accurate and up-to-date procedures to plant personnel. H.2(c)

The inspectors completed a Phase 1 significance determination of this issue using

IMC 0609, Significance Determination Process, Attachment 0609.04, dated

January 10, 2008. The inspectors determined that the finding impacted the Initiating

Events Cornerstone. The inspectors answered No to the question on Transient

Initiators under the Initiating Events Cornerstone column on Table 4a because the

finding did not contribute to both the likelihood of a reactor trip AND the likelihood that

mitigating equipment or functions will not be available. Therefore, the issue screened as

having very low safety significance (Green).

Enforcement: The inspectors determined that the licensees failure to include pertinent

information, regarding valve position during RWCU system startup with the RPV at

pressure, in DOP 1200-03 was a violation of Dresden Nuclear Power Station Technical

Specification Section 5.4.1, Procedures. Section 5.4.1 states, in part, that written

procedures shall be established, implemented, and maintained covering applicable

37

Enclosure

procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, issued

February 1978. Procedures addressing startup of boiling water reactor (BWR) systems,

including the reactor cleanup system, are recommended in Section 4. of Appendix A to

this Regulatory Guide.

Contrary to the above, on October 3, 2009, the licensee failed to include pertinent

guidance regarding 3-1201-7 valve position during system startup with the RPV at

pressure. This failure resulted in an automatic reactor scram and Group 1 primary

containment isolation signal. This event was entered into the licensees corrective action

program as IR 974426, U3 Group 1 Isolation and Reactor Scram. Corrective actions

by the licensee included revising procedure DOP 1200-03, requiring the 3-1201-7 valve

to be open prior to initiating RWCU system fill and vent activities. Because this violation

was of very low safety significance and it was entered into the licensees corrective

action program, this violation is being treated as a NCV, consistent with Section VI.A.1 of

the NRC Enforcement Policy. (NCV 05000249/2009005-08)

.3

(Closed) Licensee Event Report (LER) 05000237/2009-003-00; 05000249/2009-003-00,

Emergency Diesel Generator Oil Leak and Unresolved Item (URI)05000237/2009003-01; 05000249/2009003-01, Failure of 2/3 Emergency Diesel

Generator Due to Lube Oil Leak on Y Strainer

This event, which occurred on June 2, 2009, during performance of the monthly

surveillance on the Unit 2/3 Emergency Diesel Generator (EDG), resulted in an oil leak

of approximately one-half gallon per minute from the turbocharger lubricating oil Y

strainer end cap plug. The initial event was documented in Section 1R12 of report

05000237/2009003; 05000249/2009003 as an Unresolved Item

(URI 05000237/2009003-01; 05000249/2009003-01.)

Documents reviewed as part of this inspection are listed in the Attachment to this report.

Both the above referenced URI and this LER are closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

Introduction: A finding of very low safety significance and associated NCV of

10 CFR Part 50, Appendix B, Criterion IV, Procurement Document Control, was

self-revealed for the failure to ensure a safety-related plug was ordered and installed

where required in the 2/3 EDG turbo lube oil Y strainer.

Description: On June 02, 2009, the 2/3 EDG was operating in support of the monthly

surveillance run in accordance with DOS 6600-01, Diesel Generator Surveillance

Tests. At approximately 3:39 am the 2/3 EDG was 25 minutes into the loaded run when

an oil leak of approximately 1/2 gallon per minute was identified at the Turbo Lube Oil

System Y strainer.

The 2/3 EDG was secured at approximately 3:47 a.m., and the turbo oil circulating pump

was secured approximately 45 minutes after the engine shutdown to allow heat removal

from the engines turbo charger to prevent damage. Inspection of the turbo lube oil

system Y strainer identified the source of the leakage to be coming from a pipe plug on

the Y strainer end cap. Further investigation revealed the pipe plug installed in the

strainer end cap to be a black 3/8 inch NPT plastic shipping plug instead of the

safety-related steel plug required by design documents.

38

Enclosure

As immediate corrective action, the licensee installed a 3/8 inch NPT ASTM A-105

carbon steel hex head threaded pipe plug, Cat ID 43255-1 in the strainer end cap of the

2/3 EDG using work order (WO) 1240346-01 and approximately 30 gallons of oil were

added to the engine reservoir. Surveillance procedure DOS 6600-01, Diesel Generator

Surveillance Tests, was completed satisfactorily with no leakage observed from the

Turbo Lube Oil System Y strainer. The 2/3 EDG was declared operable at 11:05 p.m.

on June 2, 2009. Extent of condition reviews were performed on the four other similar

diesel generators; two safety-related and two station blackout emergency diesels.

No other non-conforming conditions were identified.

During the subsequent root cause investigation, the licensee determined that the

Unit 2/3 EDG Turbo Lube Oil Y Strainer (EPN 2/3-6661) and Circulating Oil Y Strainer

(EPN 2/3-6672) were replaced on March 24, 2008, under WO 922770-01 due to wear on

the strainer blowdown caps. On March 24, 2008, the licensee completed steps 8, 9

and 10 of WO 922770-01. This work scope removed the old lube oil strainer 2/3-6661

from the system, cleaned piping and pipe nipples prior to installing the strainer

(replacing pipe nipples as required), and installed the new Mueller strainer snug tight

using site approved sealant. On March 25, 2008, the license performed step 11 of the

work package requiring the strainers to be painted with designated orange paint once

the strainers have been installed. The painting step was important because from this

step on there is no way to visually identify the non-conforming condition. Interviews with

the individual performing the installation and painting indicated that they did not identify

the plug as a plastic foreign material exclusion (FME) plug and therefore took no action

to replace it as was required by procedure MA-AA-716-008, Foreign Material Exclusion

Program.

The post-maintenance test (PMT) was performed on the Y strainers on

March 27, 2008, per WO 922770-02. The licensee performed visual inspections of the

Y strainers at system pressure. The inspections passed with no identified leakage.

Subsequent investigation revealed that Turbo Lube Oil Strainer replaced under

WO 922770-01 in March 2008 was assigned Exelon Catalog Identification

Number 38412-1. The Y strainer was manufactured commercial grade by Mueller

Steam Specialty under Model No. 352M. Exelon purchased the Y strainer from

Engine Systems Incorporated (ESI) under Purchase Order (PO) 00000703 Revision 001

as a Quality Level 1 Nuclear Safety-Related Item. The PO stated, Strainer, Y-Type,

1 IN, Bronze ASTM B62, Threaded (FNPT), Class 250, 20 Mesh Size Stainless Steel

Screen, supplied with threaded gasketed cap and plug; and rated for 400 PSI @ 150 F

(WOG); and seismically qualified per Report Number ST-MSS-352M-1 issued by ESI.

The Mueller Steam Specialty catalog Cut Sheet that was pasted in the supply database

for CAT ID 38412-1 on July 3, 2006, indicated Y strainer Blowoff Outlets are

unplugged. Additionally, the current Mueller Steam Specialty online specification sheet

for Y Strainers (ES-MS-351M-358) states Blow Off Outlets: Not normally furnished

with plug. Plug available, specify with order.

Since the part number specified by Dresden in the procurement document does not

include a plug in the end cap, Engine Systems Incorporated (ESI) included the plastic

plug for FME purposes. The plug is black only because that was the color that ESI had

on hand at the time. Personnel from ESI stated that when performing the qualification

testing for the part two strainers are ordered, one for the testing and one to ship to the

customer. An appropriate plug is installed in the one used for qualification testing.

39

Enclosure

The strainer purchased for WO 922770-01 was shipped to Dresden Site Supply and had

a receipt inspection performed on December 19, 2007. The inspection accepted the

strainer with no discrepancies noted in the Quality Receipt Inspection Package and

without questioning if the plug installed in the strainer end cap should have been a

suitable pressure retaining pipe plug or a shipping plug.

The licensee concluded from their investigation that the root cause for this issue was the

failure to have a purchase order that clearly documented the need for the safety-related

strainer cap plugs.

Analysis: The inspectors determined that the failure to document the requirement for a

safety-related strainer cap plug in the purchase order was a performance deficiency.

The finding was determined to be more than minor because the finding was similar to

IMC 0612, Appendix E, Example 5 c, in that, an incorrect and inadequate part was

installed and the system was returned to service. Therefore, this performance deficiency

also impacted the Mitigating Systems Cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of Findings, Table 4a, dated January 10, 2008,

for Mitigating Systems because the 2/3 EDG is a mitigating system that could impact the

long term or short term decay heat removal capability during a loss of offsite power

event. The inspectors answered yes to the question, Does the finding represent

actual loss of safety function of a single train for greater than its Technical Specification

Allowed Outage Time? The inspectors performed a SDP phase 2 evaluation using the

pre-solved spreadsheet for the Risk-Informed Inspection Notebook for Dresden Nuclear

Power Station. The assumption that EDG 2/3 was unavailable for greater than 30 days

resulted in a finding of low to moderate risk significance (White). The Region III senior

reactor analyst (SRA) performed a SDP phase 3 evaluation of the EDG 2/3 failure to run.

The SRA used the Dresden Standardized Plant Analysis Risk (SPAR) Model,

Revision 3.50, and assumed that the EDG would have failed to run in response to any

demand that would have occurred since the last successful 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> endurance run.

This exposure period was approximately 89 days. The delta CDF for internal events

was estimated to be 4.0E-7/yr. The dominant sequence was a loss of offsite power

event followed by common cause failure of all emergency power and the failure to

recover either offsite or onsite power.

Since the delta CDF was greater than 1.0E-7/yr, the SRA evaluated the risk contribution

from external events. The risk contribution from seismic events was determined to be

negligible because the frequency of seismically-induced loss of offsite power events was

estimated to be much less than plant-centered, switchyard-centered, or grid-related loss

of offsite power events. The fire risk contribution was estimated using information from

the licensees Individual Plant Examination for External Events (IPEEE) submitted

in 2000. Fire-induced loss of offsite power events were assumed to occur for fires in

control room panel 902-8 (Unit 3 panel 903-8), panel 923-2, and for fires in the auxiliary

electric equipment room (AEER). The SRA used the fire ignition frequencies from the

IPEEE and calculated conditional core damage probabilities using the SPAR model for

plant-centered loss of offsite power events with the failure of the 2/3 EDG to estimate the

change in core damage frequency for fire events that did not result in control room

40

Enclosure

evacuation. Fires in the AEER contributed less than 1.0E-7/yr to the change in CDF.

For the control room, fires in panel 902-8 (903-8) were evaluated and determined to be

potential risk contributors because the fire damage caused a loss of offsite power and

resulted in the unavailability of the Division II power supplies. For panel fires that were

not suppressed within 15 minutes, the SRA used a non-suppression probability of 3.4E-3

from the licensees IPEEE and concluded that operators would evacuate the control

room and use the fire-specific safe shutdown procedures. With the 2/3 EDG unavailable

due to the performance deficiency, only the station blackout (SBO) diesel generator

would remain available to provide power. The SRA used SPAR-H to estimate the

human error probability (HEP) for aligning the SBO diesel generator during fire scenarios

and estimated a value of 0.4 assuming that diagnosis of the loss of power and need for

the SBO diesel generator would dominate the HEP. The performance-shaping factors

for stress and procedures were adjusted in the HEP calculation. The procedures for

using the SBO DG were considered to be incomplete because the Dresden fire safe

shutdown procedures do not address the use of the SBO diesel generator and operators

would be required to use separate procedures for non-fire scenarios to line-up the SBO

DG. Also, the stress of the fire-induced LOOP with failure of the 2/3 EDG was assumed

to be high. The risk contribution from control room fire scenarios was estimated to be

approximately 4.0E-7/yr. The total delta CDF from internal and external scenarios was

estimated to be approximately 8.0E-7/yr. The risk estimate is conservative because it

does not account for any successful run time of the diesel generators and provides only

limited credit for the use of SBO diesel generators in fire scenarios.

The risk contribution from large early release frequency (LERF) was also evaluated.

IMC 0609, Appendix H, Containment Integrity Significance Determination Process

assigns a screening LERF factor of 1.0 to station blackout core damage sequences for

BWRs with Mark I containments. This would result in a delta LERF estimate of

8.0E-7/yr, which represents low to moderate significance. However, based on a

previous Dresden phase 3 SDP evaluation and other SDP evaluations of plants with

Mark 1 containments, a much lower LERF factor of 0.1 is judged to be appropriate for

this SDP phase 3 evaluation. As a result, the risk significance of the finding is estimated

to be less than 1.0E-6/yr delta CDF and less than 1.0E-7/yr delta LERF, which

represents a finding of very low safety significance (Green).

In addition, the failure of plant maintenance personnel to identify and remove the plastic

foreign material exclusion plug prior to equipment return to service was a significant

contributor to the finding. Step 4.2.5.3.B of MA-AA-716-008, Foreign Material Exclusion

Program, states, in part, New parts/components/equipment to be installed in the plant

should be carefully inspected to ensure that no foreign material (e.g., packaging

material, shipping plugs, desiccants, and lubricant/preservatives used for shipping or

storage) are present to prevent introduction to the system. Failure of plant personnel to

question the plastic shipping plug before the equipment was installed and returned to

service was not in compliance with the procedure and, therefore, inspectors determined

that this event was cross-cutting in Human Performance, Work Practices, Procedural

Compliance for failure to follow of personnel to follow the procedure. H.4(b)

Enforcement: 10 CFR Part 50, Appendix B, Criterion IV, Procurement Document

Control, requires, in part, that measures shall be established to assure that applicable

regulatory requirements, design bases, and other requirements which are necessary to

assure adequate quality are suitably included or referenced in the documents for

41

Enclosure

procurement of material, equipment, and services, whether purchased by the applicant

or by its contractors or subcontractors.

Contrary to the above, from December 2007 until June 2009, the licensee did not include

a requirement which was necessary to assure adequate quality in the document for

procurement of the 2/3 EDG Turbo Lube Oil Y Strainer, CAT ID 38412-1. Specifically,

the purchase order did not specify what type of plug was required to be supplied and

installed in the strainer cap prior to installation. The strainer was supplied with a plug

installed that was neither designed nor constructed sufficiently to prevent a leak that

resulted in the inoperability of the 2/3 EDG for greater than 30 days. Immediate

corrective action to correct the leak included installation of a qualified plug in the strainer,

post-maintenance testing of the 2/3 EDG, and inspection of all other diesel generators to

ensure the same condition did not exist on another machine. The catalogue ID was

revised to include a pressure retaining pipe plug with approved material and a

requirement was added for a quality inspection to be performed to inspect the strainer

for metallic pipe plug in blow down port. Individual procedure compliance issues were

addressed through the stations performance improvement initiatives. Because this

violation was of very low safety significance and it was entered into the licensees

corrective action program as IR 926605, this violation is being treated as an NCV,

consistent with Section VI.A.1 of the NRC Enforcement Policy.

(NCV 05000237/2009005-09; 05000249/2009005-09)

.4

Electro-Hydraulic Control (EHC) Fluid Leaking From Stop Valve 3-5699-MSV4-FA

Resulting in Forced Outage D3F49

a.

Inspection Scope

The inspectors reviewed the plants response to an EHC leak on Dresden Unit 3 that

caused the unit to come offline. Documents reviewed in this inspection are listed in the

Attachment to this report.

This event follow-up review constituted one sample as defined in IP 71153-05.

b.

Findings

Introduction: The inspectors identified an unresolved item regarding the regulatory

requirements associated with the circumstances surrounding the Unit 3 turbine trip on

November 6, 2009.

Description: On November 5, 2009, at 8:53 p.m., Unit 3 Control Room received the

following alarm: 903-7 B-6, EHC [electro-hydraulic control] RESERVOIR LVL HI/LO

(reference IR 989641) indicating a rate of change in the EHC reservoir at 1.3" in 100 hrs

or greater. A non-licensed operator (NLO) was dispatched to stage a barrel of EHC fluid

for addition. Preparations were made for a heater bay entry to look for leaks.

A Unit 3 heater bay entry was made and it was determined that the Unit 3 Main Turbine

Stop Valve (MSV) # 4 had an EHC leak from the fast-acting solenoid valve

(3-5699-MSV4-FA). The leak was determined to be approximately 4-5 gallons of fluid

per hour. A report from the field was that reservoir level had dropped about 1.1" in the

last 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Between 12:50 a.m. and 3:43 a.m. on November 6, 2009, the licensee

added two barrels of EHC fluid to the EHC reservoir.

42

Enclosure

On November 6, 2009, between 9:00 a.m. and 2:00 p.m., licensee management

conducted meetings regarding the repair of the leak on MSV #4. The plan called for

starting to down power Unit 3 to 650 Mwe for a planned 3:00 p.m. entry into the heater

bay to repair the valve. The decision to go to 650 Mwe was to reduce the dose rate in

the area and extend stay time for the repair.

At approximately 3:00 p.m., while staging for entry to repair the leak, Operations

personnel informed the NLO, staged to isolate the oil supply to the leaking valve, that

level in the EHC reservoir was dropping quickly, and requested the NLO to enter the

pipeway as soon as possible.

At approximately 3:05 p.m., the NLO observed oil spraying profusely from the bottom

area of #4 Main Stop Valve and the area of the solenoid that was going to be changed

out. The NLO immediately contacted the control room to report what was observed and

a decision was made to take the turbine offline. At 3:32 p.m., the Unit 3 Turbine was

tripped.

The licensee had not completed their root cause investigation by the end of the

inspection period. The inspectors planned to review the root cause investigation to

determine if there were any violations of NRC requirements and that appropriate

corrective actions were applied. (URI 05000249/2009005-10)

4OA5 Other Activities

.1

Quarterly Resident Inspector Observations of Security Personnel and Activities

a.

Inspection Scope

During the inspection period, the inspectors conducted observations of security force

personnel and activities to ensure that the activities were consistent with licensee

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors' normal plant status review and inspection activities.

b.

Findings

No findings of significance were identified.

.2

Institute of Nuclear Power Operations (INPO) Plant Assessment Report Review

a.

Inspection Scope

The inspectors reviewed the interim report for the INPO plant assessment of Dresden

Station conducted in September 2009. The inspectors reviewed the report to ensure

that issues identified were consistent with the NRC perspectives of licensee

performance and to verify if any significant safety issues were identified that required

further NRC follow-up.

43

Enclosure

b.

Findings

No findings of significance were identified.

.3

Open) NRC TI 2515/177, Managing Gas Accumulation in Emergency Core Cooling,

Decay Heat Removal and Containment Spray Systems (NRC Generic Letter 2008-01)

a.

Inspection Scope

On November 10, 2008, the inspectors conducted a walkdown of the Unit 2 High

Pressure Coolant Injection (HPCI) discharge piping inside the Unit 2 X-Area in sufficient

detail to reasonably assure the acceptability of the licensees walkdowns (TI 2515/177,

Section 04.02.d). The inspectors also verified that the information obtained during the

licensees walkdown was consistent with the items identified during the inspectors

independent walkdown (TI 2515/177, Section 04.02.c.3).

The inspectors verified that Piping and Instrumentation Diagrams (P&IDs) accurately

described the subject system, that the P&IDs were up-to-date with respect to recent

hardware changes, and any discrepancies between as-built configurations and the

P&IDs were documented and entered into the CAP for resolution (TI 2515/177, Section

04.02.b).

In addition, the inspectors reviewed the licensees isometric drawings that describe the

HPCI system configurations to verify that the licensee had acceptably confirmed the

accuracy of the drawings (TI 2515/177, Section 04.02.a). The inspectors considered the

following related to the isometric drawings:

High point vents were identified.

High points that do not have vents were acceptably recognizable.

Other areas where gas can accumulate and potentially impact subject system

operability, such as at orifices in horizontal pipes, isolated branch lines, heat

exchangers, improperly sloped piping, and under closed valves, were acceptably

described in the drawings or in referenced documentation.

Horizontal pipe centerline elevation deviations and pipe slopes in nominally

horizontal lines that exceed specified criteria were identified.

All pipes and fittings were clearly shown.

The drawings were up-to-date with respect to recent hardware changes and that

any discrepancies between as-built configurations and the drawings were

documented and entered into the CAP for resolution.

The licensee indicated that even though they possess isometric drawings of the HPCI

system, they do not rely upon any isometric drawings for gas management in that

system. Therefore, the inspectors were unable to verify the above considerations.

In their review, the inspectors did identify discrepancies in the available isometric

drawings between what was shown on the drawing and the as-built condition of the

system. The discrepancies identified were in drawings M-1151C-2 and ISI-510 Sheet 2

and were associated with the 2-23126-3/4-L vent line. The licensee determined that

drawing M-1151C-2 does not need to be updated because it was created to support a

seismic analysis done before the 2-23126-3/4-L vent line was installed and was not

intended to be updated. They determined that drawing ISI-510 Sheet 2 does not need to

44

Enclosure

be updated because it is a system pressure testing walkdown isometric drawing,

therefore, the discrepancy does not impact the purpose and use of the drawing. These

conclusions were documented in AR 1014280.

Documents reviewed are listed in the Attachment to this report.

This inspection effort counts towards the completion of TI 2515/177, which will be closed

in a later Inspection Report.

b.

Findings

No findings of significance were identified.

4OA6 Management Meetings

.1

Exit Meeting Summary

On January 14, 2010, the inspectors presented the inspection results to Mr. T. Hanley,

and other members of the licensee staff. The licensee acknowledged the issues

presented. The inspectors confirmed that none of the potential report input discussed

was considered proprietary.

.2

Interim Exit Meeting

Interim exits were conducted for:

The results of the inservice inspection with Site Vice-President T. Hanley on

November 13, 2009.

The results of the As-Low-As-Reasonably-Achievable Planning and Controls

inspection with the Site Vice President, Mr. T. Hanley, on November 17, 2009.

The annual review of Emergency Action Level and Emergency Plan changes

with the licensee's Emergency Preparedness Manager, Mr. P. Quealy, via

telephone on December 21, 2009.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements which meets the criteria of Section

VI.A.1 of the NRC Enforcement Policy, for being dispositioned as an NCV.

Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Criterion XVI,

Corrective Action, states, in part, Measures shall be established to assure that

conditions adverse to quality, such as failures, malfunctions, deficiencies,

deviations, defective material and equipment, and non-conformances are

promptly identified and corrected. In the case of significant conditions adverse to

quality, the measures shall assure that the cause of the condition is determined

and corrective action taken to preclude repetition. A significant condition

adverse to quality for both Unit 2 and Unit 3 containment cooling service water

45

Enclosure

(CCSW) systems was identified by the licensee in RCR 776598-08,

Dresden 3-1503-B, 3B Low Pressure Coolant Injection (LPCI) / Containment

Cooling Heat Exchanger (HX) Failure to Meet Design Basis Heat Removal

Capability Due to Inadequate Programmatic Control of Macrofoulants,

Revision 1, on January 9, 2009. Procedure LS-AA-125, Corrective Action

Program (CAP) Procedure, revision 13, defines significant condition adverse to

quality (SCAQ), in part, as A condition which, if left uncorrected, could have a

serious effect on safety or reliability. In addition, recurring deficiencies or errors

that cannot be dispositioned or brought into conformance by established

corrective action systems," are considered SCAQs. The inspectors determined

that the conditions described in RCR 776598-08, met the licensee's definition of

a significant condition adverse to quality. Contrary to the above requirements,

from January through September 2009, the licensee failed to take measures to

assure that the cause of the condition (blockage of the LPCI heat exchangers)

was determined and corrective action taken to preclude the repetition for a

significant condition adverse to quality on both Unit 2 and Unit 3 CCSW systems.

Specifically, the licensee failed to prevent the recurrence of Asiatic clam

blockage in the 2A LPCI Hx tubes which resulted in the degraded thermal

performance of the Hx. Licensee planned corrective actions included installation

of a temporary modification to provide temporary keepfill that was expected to

provide better chemical treatment of the CCSW piping upstream of the LPCI Hxs,

and a permanent injection skid for biocide to provide for long term assurance of

effective chemical treatment. This violation was determined to be of very low

safety significance because even though the 2A LPCI Hx was degraded it was

able to perform the required design safety function.

ATTACHMENT: SUPPLEMENTAL INFORMATION

1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

T. Hanley, Site Vice President

S. Marik, Station Plant Manager

H. Bush, Radiation Protection Manager

B. Casey, Engineering Programs (Braidwood)

H. Do, Exelon Corporate ISI

B. Finley, Security Manager

D. Glick, Shipping Specialist

T. Green, Nondestructive Examination Services

J. Griffin, Regulatory Assurance - NRC Coordinator

D. Gronek, Operations Director

J. Hansen, Corporate Licensing

L. Jordan, Training Director

R. Kalb, Chemistry

P. Karaba, Maintenance Director

J. Kish, Engineering Programs

M. Kluge, Design Engineer

D. Leggett, Nuclear Oversight Manager

R. Laburn, Radiation Protection

M. Marchionda, Regulatory Assurance Manager

J. Miller, Nondestructive Examination Services

P. OConnor, Licensed Operator Requalification Training Lead

M. Overstreet, Lead Radiation Protection Supervisor

C. Podczerwinski, Maintenance Rule Coordinator

P. Quealy, Emergency Preparedness Manager

E. Rowley, Chemistry

R. Rybak, Regulatory Assurance

J. Sipek, Engineering Director

N. Starcevich, Radiation Protection Instrumentation Coordinator

J. Strmec, Chemistry Manager

S. Vercelli, Work Management Director

NRC

M. Ring, Chief, Division of Reactor Projects, Branch 1

IEMA

R. Zuffa, Illinois Emergency Management Agency

R. Schulz, Illinois Emergency Management Agency

2

Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened: 05000237/2009005-01

NCV

Operating Personnel Incorrectly Placed Clearance Tags

(Section 1R04)05000237/2009009-02

NCV

NRC Inspector-Identified Control Room Alarm Isolation

Valve Out-of-Position (Section 1R15)05000237/2009005-03

NCV

Preconditioning the Unit 2 Emergency Diesel Generator

Prior to Performing TS Surveillance Requirements

(Section 1R19)05000237/2009005-04

URI

2/3 Emergency Diesel Generator (EDG) Overvoltage 05000249/2009005-04

During Division I Undervoltage Surveillance (1R19)05000237/2005009-05

NCV

Failure to Follow the Master Refueling Procedure During

Movement of Fuel Assembly JLU569 (Section 1R20)05000249/2009005-06

NCV

Mispositioning of a Unit 3 Control Rod at Power

(Section 1R22)05000237/2009005-07

URI

Changes to EAL HU6 Potentially Decreased the

Effectiveness of the Plans without Prior NRC Approval

(1EP4)05000249/2009005-08

NCV

Procedural Deficiency Causing a Pressure Pulse

Resulting in a Reactor Water Level Low-Low Group 1

Isolation Signal and Unit 3 Reactor Scram

(Section 4OA3.2)05000237/2009005-09

NCV

Failure to Ensure a Safety-Related Plug was Ordered and 05000249/2009005-09

Installed in the 2/3 Emergency Diesel Generator

Turbo Lube Oil Y Strainer (Section 4OA3.3)05000249/2009005-10

URI

Electro-Hydraulic Control (EHC) Fluid Leaking From Stop

Valve 3-5699-MSV4-FA Resulting in Forced Outage

D3F49 (Section 4OA3.4)

Temporary Instruction 2515/177

Managing Gas Accumulation in Emergency Core Cooling,

Decay Heat Removal and Containment Spray Systems

(NRC Generic Letter 2008-01) (Section 4OA5.3)

3

Attachment

Closed: 05000237/2009005-01

NCV

Operating Personnel Incorrectly Placed Clearance Tags

(Section 1R04)05000237/2009009-02

NCV

NRC Inspector-Identified Control Room Alarm Isolation

Valve Out-of-Position (Section 1R15)05000237/2009005-03

NCV

Preconditioning the Unit 2 Emergency Diesel Generator

Prior to Performing TS Surveillance Requirements

(Section 1R19)05000237/2005009-05

NCV

Failure to Follow the Master Refueling Procedure During

Movement of Fuel Assembly JLU569 (Section 1R20)05000249/2009005-06

NCV

Mispositioning of a Unit 3 Control Rod at Power

(Section 1R22)05000249/2009005-08

NCV

Procedural Deficiency Causing a Pressure Pulse

Resulting in a Reactor Water Level Low-Low Group 1

Isolation Signal and Unit 3 Reactor Scram

(Section 4OA3.2)05000237/2009005-09

NCV

Failure to Ensure a Safety-Related Plug was Ordered and 05000249/2009005-09

Installed in the 2/3 Emergency Diesel Generator

Turbo Lube Oil Y Strainer (Section 4OA3.3)05000237/2009004-04

URI

Inspector Identified Control Room Alarm Isolation Valve 05000249/2009004-04

Out-of-Position (1R15)05000237/2009003-01

URI

Failure of 2/3 Emergency Diesel Generator (EDG) Due to 05000249/2009003-01

Lube Oil Leak On Y-Strainer (4OA3.3)

05000237/2009-001-00

LER

Common Mode Failure of Reactor Building Isolation

05000249/2009-001-00

Dampers (4OA3.1)

05000249/2009-001-00

LER

Unit 3 Group 1 Isolation and Automatic Reactor Scram

(4OA3.2)

05000237/2009-003-00

LER

Emergency Diesel Generator Oil Leak (4OA3.3)

05000249/2009-003-00

Discussed:

Inspection Report 05000237/2008005; 05000249/2008005, Section 1R15 (4OA2.4)05000237/2009002-04

NCV

Failure to Take Corrective Actions to Replace a Degraded

Valve in a Timely Manner (4OA3.1)

4

Attachment

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R04 Equipment Alignment (71111.04)

- WO 1079566-01, Perform 250V Station Battery Service Test

- C/O 76319, (ASSY) Battery 250V U2

- DOP 7500-M1/E1, Unit 2/3 Standby Gas Treatment, Revision 6

1R05 Fire Protection (71111.05)

- IR 976782, NRC Observations from U3 Rx Bldg. 570 Pre-Plan Review

1R08 Inservice Inspection Activities (71111.08G)

- IR 00992912; Material Certification of Recirc Piping Could not be Found; November 13, 2009

- IR 00911408;Section XI Class 2 Boundary; April 28, 2009

- IR 00889729; LPCI Heat Exchanger Recordable Indications; March 6, 2009

- IR 00782956; Corrosion Pipe Elbow B CST Tank; June 6, 2008

- IR 00755744; 2/3 EDG Leak on Engine Block; March 28, 2008

- IR 00711323; 2/3 DGCW Pump Suction Pipe Corrosion; December 14, 2007

- IR 00705912; Unit 2 CCSW System Corrosion; December 2, 2007

- IR 00705639; DGCW Pipe Corrosion; December 2, 2007

- IR 00695137; Unit 2 Reactor Head Flange MT Indication; November 8, 2007

- IR 00691069; Loose Anchor Bolt on CS Line; October 31, 2007

- IR 00681657; PT Rejectable Indication; October 22, 2007

- ASME Section XI Repair/Replacement Plan 2-1505A-12-0; April 1, 2009

- Certified Mill Test Report (Consolidated Power Supply); 12 Safety-Related 90 Elbow;

September 15, 2009

- EC 368360; Evaluation of Leakage at Bolted Connections and other Recordable Indications;

Revision 0

- Examination Summary Sheet; D2R21-028 UT of PS2/201-1; November 7, 2009

- Examination Summary Sheet; D2R21-029 UT of PS2-Tee/202-4B; November 7, 2009

- NDE Report No.09-294; VT-3 Visual Examination; November 13, 2009

- NDE Certification; Scott R. Erickson; UT Level III; October 6, 2009

- Procedure GE-PDI-UT-2; PDI Generic Procedure for the Ultrasonic Examination of Austenitic

Pipe Welds; Revision 4

- Procedure GE-PDI-UT-3, PDI Generic Procedure for the Ultrasonic Thru Wall Sizing in Piping

Welds, Revision 2

- Procedure ER-AA-335-018, Detailed General VT-1, VT-1C, VT-3 and VT-3C Visual

Examination of ASME Class MC and CC Containment Surfaces and Components; Revision 5

- Procedure ER-AA-335-1008; Code Acceptance and Recording Criteria for Nondestructive

Surface Examination; Revision 1

- Procedure Qualification Record; A-001; October 19, 1998

- Procedure Qualification Record; A-002; March 9, 1997

- Procedure Qualification Record; 1-50C; January 3, 1984

5

Attachment

- Report No. D2R20-037; Four Indications on the Reactor Head Flange Weld (2RPV UPP

HD/2-THD-FLG); November 11, 2007

- Weld Procedure Specification; 1-1-GTSM-PWHT; Revision 1

- Welder Qualification Record; W2677; October 5, 2009

- Work Order 01189798; Replace Degraded Elbow on 2A CCSW Pump; October 22, 2009

1R12 Maintenance Effectiveness (71111.12)

- Z03, "Control Rod Drive Maintenance Rule Performance Criteria"

- IR 845878, "Scram Dump Valve Leaking", 11/17/2008

- IR 763023, "Review Maintenance Rule Functions Perform review described in In-Progress

Notes", 5/30/2008

- IR 842585, "Handwheel Spins with no Valve Movement", 11/09/2008

- IR 842587, "Valve Handwheel Broken", 11/09/2008

- IR 843592, "HCU P6 Scram Valve Packing Leak", 11/11/2008

- IR 700134, "Relief Valve Continuously Lifted", 11/16/2007

- IR 976292, "CRD Exercising and Condenser Vacuum Scram Impact U3 Restart", 10/05/2009

- WO 1186809, "Scram Dump Valve Leaking", 11/17/2008

- M-34, "Diagram of Control Rod Drive Hydraulic Piping", Revision W

- TS 3.1.3, Control Rod Operability

- TS 3.1.4, Control Rod Scram Times

- TS 3.1.5, Control Rod Scram Accumulators

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

- IR 1009039, 345 kv Line 8014 trip

1R15 Operability Evaluations (71111.15)

- Operability Evaluation No.09-007, 2A LPCI Heat Exchanger (2-1503-A)

- EC 372200, Perform Evaluation of Thermal Performance Test Data of 2A LPCI Hx

- EC 377036, 2A LPCI Heat Exchanger September 18, 2009 Thermal Performance Test

- IR 978203, GL 89-13 Program Health Color Change

- IR 989609, D2R21 Inspection Results for 2A LPCI Heat Exchanger

- IR 990189, 2A LPCI Heat Exchanger Tubesheet Corrosion

- IR 990209, 2A LPCI Hx Top Coverplate Coating Bubbled

- IR 996991, A LPCI HT Exchanger Shell Side RV Lifting

- CY-DR-110-220, LPCI Service Water (CCSW) and Torus Water Sampling, Revision 3

- CY-DR0120-413, Cooling and Service Water Chemical Injection System, Revision 8

- Root Cause Report 967008-03, Dresden 2-1503-A, 2A Low Pressure Coolant Injection

(LPCI)/Containment Cooling Heat Exchanger (Hx) Failure to Meet Design Basis Heat Removal

Capability due to Asiatic Clam Macrofouling Resulting from 2-1501-3A Valve Leakage and

Subsequent Untreated Service Water Make-Up via the CCSW Keepfill Diluting the Biocide

Treatment below the Asiatic Clam Lethal Concentration

- Focus Area Assessment, Dresden Station, CCSW System Asiatic Clam Fouling. Performed

by Water Technology Consultants, Inc.

- EC Evaluation 373443, Evaluation of Leakage From Cylinder Head Covers on 2A SBLC

Pump

- WO1001541-76, 3B SBLC System Pump Test for Operability Verification

6

Attachment

1R19 Post-Maintenance Testing (71111.19)

- IR 1003797, TSC HVAC Surveillances Failed

- WO 1294151, D1/2/3 SAN PM Operability Surv for the TSC AFUs

- DOS 5750-05, Semi-Annual Technical Support Center (TSC) Air Filtration Unit (AFU)

Operability Test, Revision 15

- IR 348426, FIC-2/3-5748-93 Airflow Indication Not Actual Airflow

- WO 826129, FIC-2/3-5748-93 Airflow Indication Not Actual Airflow

- IR 1005336, TSC Flow Controller Range Issue

- EP-AA-1000, Standardized Radiological Emergency Plan, Revision 19

- EP-AA-112-200-F-01, Station Emergency Director Checklist, Revision F

- NUREG-0696, Functional Criteria for Emergency Response Facilities, February 1981

- NUREG-0737, Clarification of TMI Action Plan Requirements, Supplement No. 1,

January 1983.

- M-3006, Technical Support Center HVAC & Plumbing Layout, Revision F

- DOS 6600-01, Diesel Generator Governor Oil Change and Compensating Adjustment,

Revision 23

- IR 992803, U2 EDG Largest Load Reject (TSR 3.8.1.10)

- IR 994101, 2/3 EDG Voltage Transient

- DOS 6600-06, Bus Undervoltage and ECCS Integrated Functional Test for Unit 2/3 Diesel

Generator to Unit 2, Revision 46

- IR 997244, Recirc Pump Instruments not Functioning Reqd for Hydro

- IR 997142, CCP: MCR Panel 923-5 Lost Ventilation Equip Indications

- EC 378040, 2/3 EDG Overvoltage during Division I Undervoltage Surveillance, Revision 0

- IR 1005291, Inaccurate Information Included in IR 994101

- IR 1006989, Control Room Indicators Deenergized

- EACE 994101-07, 2/3 Emergency Diesel Generator (EDG) Voltage Transient

- IR 987850, D2R21 As Found LLRT on 2-0203-2C Exceeded Leakage Limit

- DOS 0250-02, Full Closure Timing and Exercising of Main Steam Isolation Valves, Rev 26

- DOS 0250-03, Main Steam Isolation Valve Fail-Safe Closure Test, Rev 21

- IR 1001725, Higher than Expected Vibrations on 2B Cond Pp.

- IR 1002609, FME: Found in 2B Condensate Pump Suction Piping

- ER-AA-2006, Lost Parts Evaluations, Revision 6

- WO 1098975, 2B Condensate Booster Motor Alignment

- DOP 3300-02, Condensate System Startup, Revision 50

- M-15, Diagram of Condensate Piping, Revision J

- MA-AA-716-012, Post-Maintenance Testing, Revision 11

- MA-AA-716-230-1002, Vibration Analysis/Acceptance Guideline, Revision 2

1R20 Outage (71111.20)

- DGP 01-01, Unit Startup, Revision 153

- IR 975280, 3B CRD FCV Failed to Operate Remotely

- IR 975813, D3F48LL: DEHC Alarms During U3 Chest Warming

- IR 975830, D3F48LL: DEHC Issues During Turbine Roll

- IR 976410, CIV #1 Indicates 57% Open. LVDT Position Indication Failure

7

Attachment

1R22 Surveillance Testing (71111.22)

- IR 984934, DOS 6620-07 SBO Surveillance Need Revision

- IR 745855, "Unable to Close SBO Diesel Onto Bus"

- IR 984179, "Unit 2 SBO Preparation for Standby Readiness Deficiency"

- DOS 6620-07, "SBO 2(3) Diesel Generator Surveillance Tests, Revision 28

- DOP 6620-20, "SBO D/G 2(3) Prelubrication and Barring for Normal Start", Revision 06

- DOA 6500-11, "4 KV Bus Overvoltage," Revision 05

- WO 1257282, "Perform DOS 6620-07, D2 SBO Surveillance," 10/26/2009

- WO 1079209-01, D2 30M/RFL TS LLRT MSIV 203-1B & 203-2B Dry Test

- WO 1077724-01, D2 30M/RFL TS LLRT MSIV 203-1C & 203-2C Dry Test

- WO 1077725-01, D2 30M/RFL TS LLRT MSIV 203-1D & 203-2D Dry Test

- WO 1081285-01, D2 20M/RFL TS LLRT MSIV 203-2A Wet Test

- WO 1079266-01, D2 30M/RFL TS LLRT MSIV 203-2B Wet Test

- WO 1081288-01, D2 30M/RFL TS LLRT MSIV 203-2C Wet Test

- WO 1081313-01, D2 30M/RFL TS LLRT MSIV 203-2D Wet Test

- DOS 7000-01, Local Leak Rate Testing of Main Steam Isolation Valves (Dry Tests), Rev 5

- DOS 7000-02, Local Leak Rate Testing of Main Steam Isolation Valves (Wet Test), Rev 2

- IR 987850, D2R21 As Found LLRT on 2-0203-2C Exceeded Leakage Limit

- IR 987852, D2R21 As Found LLRT on 2-0203-1D Exceeded Leakage Limit

- DIS 1500-01, Reactor Low Pressure (350 PSIG) ECCS Permissive, Revision 27

- IR 944688, Test Valves Not Installed on CST Level Switches (HPCI Logic)

1EP4 Emergency Action Level and Emergency Plan Changes

- Dresden Station Radiological Emergency Plan Annex; Revisions 23, 24, and 25

2OS1 Access Control to Radiologically Significant Areas (71121.01)

- AR 987949987949 Operator PCE in Clean Area above Drywell Bullpen; November 3, 2009

- AR 993194993194 Responding to Guardhouse Portal Monitor Alarm; November 13, 2009

- RP-AA-203-1001; Personnel Exposure Investigation, Revision 6

- RP-AA-210; Dosimetry Issue, Usage and Control; Revision 15

- RP-AA-220; Intake Investigation, Revision 5

- RP-AA-350-1001; Response to Guardhouse Portal Monitor Alarms, Revision 0

- Underwater Construction Corporation Safe Practices Manual, Attachment A: Safety Hazard

Analysis/Dive Plan; November 3, 2009

2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)

- RWP 10010408; D2R21 Drywell Nuclear Instrumentation System Maintenance; Revision 0

- RWP 10010420; D2R21 Drywell Control Rod Drive System Maintenance; Revision 0

- RWP 10010421; D2R21 Drywell Control Rod Drive System Support; Revision 0

- RWP 10010426; D2R21 Drywell In-Service Inspection; Revision 0

- RWP 10010437; D2R21 Torus Diving Activities; Revision 1

- RWP 10010452; D2R21 Reactor Disassembly/Reassembly and Related Activities; Revision 1

- AR 870602-03; Focused Area Self-Assessment: ALARA Planning for Outage Readiness and

Preparation; August 27, 2009

- AR 988447988447 Unit 2 Refuel Floor and Reactor Building Low Level Contamination;

November 3, 2009

8

Attachment

- AR 990061990061 Under Vessel General Electric Worker Receives Small Ingestion;

November 5, 2009

- AR 993319993319 Shaw Laborer Wiping Down cords on RB 613 300K Particle on Scrubs;

November 11, 1009

- RWP-WIP-10010388; D2 R21 Scaffold Installation/Removal Activities (Excluding Drywell);

November 7, 2009

- RP-AA-461; Radiological Controls for Contaminated Water Diving Operations; Revision 2

- RWP-WIP-10010403; D2 R21 Drywell Radiation Protection Department Activities;

November 6, 2009

- RWP-WIP-10010403; D2 R21 Drywell Radiation Protection Department Activities;

November 10, 2009

- RWP-WIP-10010437; D2 R21 Torus Diving Activities; November 10, 2009

- RWP-WIP-10010453; D2 R21 Refuel Floor IVVI Activities; November 7, 2009

4OA1 Performance Indicator (PI) Verification (71151)

- LS-AA-2140; Monthly Data Elements for NRC Occupational Exposure Control Effectiveness;

Revision 4

4OA2 Identification and Resolution of Problems (71152)

- RCR 776598-08, Dresden 3-1503-B, 3B Low Pressure Coolant Injection (LPCI) / Containment

Cooling Heat Exchanger (HX) Failure to Meet Design Basis Heat Removal Capability Due to

Inadequate Programmatic Control of Macrofoulants, Revision 0

- IR 868703, 2A and 2B LPCI Heat Exchanger Samples Tested 0 PPM Biocide

- IR 871271, Biocide Injection Unavailable for CCSW System PMT Run

- IR 877889, Biocide Injection Not Available During U3 CCSW Run

- IR 880708, CCSW Biocide/Clam-Trol Chemical Injection Result Low

- IR 881043, CCSW Biocide/Clamtrol Chemical Injection Result Low

- IR 883155, 3A and 3B LPCI Fail Clam-Trol Test

- IR 884613, 2B LPCI Failed Clam-Trol Test

- IR 887406, Inadequate Biocide Retention

- IR 888462, 0 PPM Biocide Results for 2/3 EDG

- IR 889598, No Biocide Found in Unit 2B LPCI CCSW Hx Lay-up Sample

- IR 891286, No Biocide Found in 2B LPCI CCSW Hx Lay-up Sample

- IR 892241, Procedure change and Eval of Biocide Injection to DGCWPs

- IR 905027, 2B LPCI No Clamtrol Present

- IR 905224, No Biocide Detected in 2/3 DGCSW

- IR 908886, 2A LPCI Biocide Results Less than 8 PPM

- IR 914398, Revision to RCR 776598-08, 3B LPCI Hx Macrofouling Required

- IR 915033, 2A LPCI SW Biocide 24 hr. Sample < 8PPM

- IR 917133, 2B LPCI Failed Clam-Trol Test

- IR 920498, 2A and 2B LPCI SW Biocide <8PPM (24hr Sample)

- IR 923788, Clam-Trol Analysis Failed on 3DGCSW

- IR 999766, 2B LPCI Failed for Biocide

- IR 1000791, 2B LPCI Heat Exchanger Failed Clam-Trol Analysis

- IR 1006553, No Biocide Detected in CCSW from 3B LPCI Hx

- IR 1007918, Unit 2 A and B LPCI Heat Exchangers Fail 18-24 hr Biocide

9

Attachment

4OA3 Follow-Up of Events (71153)

- Licensee Event Report 237/2009-003-00, Emergency Diesel Generator Oil Leak, Revision 00

- IR 926605, Oil Leak on the 2/3 DG Turbo Lube Oil Y-strainer

- MA-AA-716-008, Foreign Material Exclusion Program, Revision 4

- Licensee Event Report 237/2009-001-00, Common Mode Failure of Reactor Building Isolation

Dampers, Revision 00

- IR 877591, Potential 10CFR50 Part 21 Notification of Versa Air Solenoid

- IR 838034, RBV Damper 2-5742-A Slow to Close

- IR 842305, 3-5742-B Damper 90 Seconds to Close

- IR 888338, RBV Isolation Damper Solenoid Valve Incorrect Component Classification

- IR 975779, Post Transient/Scram Walkdown Observation by NRC

- IR 975076, U2/3 EDG Started on Rx Trip when Aux Power Transferred

- IR 974426, U3 Group 1 Isolation and Reactor Scram

- IR 973968, 3A RWCU Pump Tripped and DOA Entry

- IR 973144, RWCU Isolate on High Temperature

- IR 973104, 3A RWCU Tripped

- Root Cause Report 974426-04, U3 Reactor SCRAM and Group 1 Isolation Resulting in

Forced Outage D3F48 Due to DOP 1200-03, titled RWCU System Operation with the Reactor

at Pressure Latent Procedural Deficiency

- LER 249/2009-001-00, Unit 3 Group 1 Isolation and Automatic Reactor Scram

- IR 990113, U3 from 650 MWe to 0 and a Turbine Trip

- IR 990160, 2/3 EDG Auto Started when U3 Main Generator was Tripped

- IR 990112, Need WO Rolled for Repair to U3 EHC Filter Pump Bkr

- IR 990110, U3 EHC Filter Pmp Trip

- IR 990661, MSV #4 Did Not Open During Initial Turbine Roll

4OA5 Other Activities (TI 2515/177)

- IR 994774, Procedures for Venting ECCS/SDC Systems Should Be Revised

- IR 999625, Air Found in HPCI Discharge Piping During UT

- IR 999762, Air Found in Second Location in HPCI Discharge Piping

- IR 1014280, Question from NRC Inspector on ISI Drawing

- EC 371153, Rev 2, NRC GL 2008-01 HPCI System Evaluation

- DOP 2300-01, HPCI Standby Operation, Rev 41

- M-51, Diagram of High Pressure Coolant Injection Piping, Rev CL

- ISI-504, System Pressure Test Walkdown Isometric MSIV Room - X Area, Rev B

- ISI-510, System Pressure Test Walkdown Isometric H.P. Coolant Injection Piping, Sheet 2,

Rev D

- M-1151C-2, Computer Math Model High Pressure Coolant Injection System, Sheet 1, Rev 2

- M-4455, HPCI High Point Vent Line, Sheet 3, Rev A

10

Attachment

LIST OF ACRONYMS USED

ADAMS

Agencywide Document Access Management System

AEER

Auxiliary Electric Equipment Room

ALARA

As-Low-As-Reasonably-Achievable

ASME

American Society of Mechanical Engineers

BWR

Boiling Water Reactor

CAP

Corrective Action Program

CCSW

Containment Cooling Service Water

CDF

Core Damage Frequency

CFR

Code of Federal Regulations

CO

Clearance Order

CRD

Control Rod Drive

D2

Dresden Unit 2

DRP

Division of Reactor Projects

EACE

Equipment Apparent Cause Evaluation

EAL

Emergency Action Level

EC

Engineering Change

EDG

Emergency Diesel Generator

ESI

Engine Systems Incorporated

FME

Foreign Material Exclusion

GE

General Electric

HEP

Human Error Probability

HEPA

High Efficiency Particulate Air

HPCI

High Pressure Coolant Injection

HCU

Hydraulic Control Unit

Hx

Heat Exchanger

IPEEE

Individual Plant Examination for External Events

IMC

Inspection Manual Chapter

INPO

Institute of Nuclear Power Operations

IP

Inspection Procedure

IR

Issue Report

ISI

Inservice Inspection

IST

In-service Test

LER

Licensee Event Report

LERF

Large Early Release Frequency

LOCA

Loss of Coolant Accident

LOOP

Loss of OffSite Power

LPCI

Low Pressure Coolant Injection

MOV

Motor Operated Valves

MSV

Main Stop Valve

NCV

Non-Cited Violation

NEI

Nuclear Energy Institute

NLO

Non-Licensed Operator

NRC

Nuclear Regulatory Commission

NRR

Office of Nuclear Reactor Regulation

NSO

Nuclear Station Operator

OSF

Outage Safety Plan

PARS

Publicly Available Records

PCIS

Primary Containment Isolation Signal

PI

Performance Indicator

11

Attachment

P&ID

Piping and Instrumentation Diagrams

PM

Planned or Preventative Maintenance, or Post-Maintenance

PO

Purchase Order

RCR

Root Cause Report

RCS

Reactor Coolant System

RFO

Refueling Outage

RPV

Reactor Pressure Vessel

RWCU

Reactor Water Cleanup

SBLC

Standby Liquid Control

SBO

Station Blackout

SCAQ

Significant Condition Adverse to Quality

SDP

Significance Determination Process

SPAR

Standardized Plant Analysis Risk

SR

Surveillance Requirements

SRO

Senior Reactor Operator

SSC

Structures, Systems and Components

TS

Technical Specification

U2

Unit 2

U3

Unit 3

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

UT

Ultrasonic Examination

WO

Work Order

C. Pardee

-2-

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response (if any) will be made available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket Nos. 50-237; 50-249

License Nos. DPR-19; DPR-25

Enclosure:

Inspection Report 05000237/2009-005; 05000249/2009-005

w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServ

DOCUMENT NAME: G:\\1-SECY\\1-WORK IN PROGRESS\\DRE 2009 005.DOC

G Publicly Available

G Non-Publicly Available

G Sensitive

G Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl

"E" = Copy with attach/encl "N" = No copy

OFFICE

RIII

RIII

RIII

RIII

NAME

MRing:cms

DATE

02/10/2010

OFFICIAL RECORD COPY

Letter to C. Pardee from M. Ring dated February 10, 2010

SUBJECT:

DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3

INTEGRATED INSPECTION REPORT 05000237/2009-005;

05000249/2009-005

DISTRIBUTION:

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