ML100410121
ML100410121 | |
Person / Time | |
---|---|
Site: | Dresden |
Issue date: | 02/10/2010 |
From: | Ring M NRC/RGN-III/DRP/B1 |
To: | Pardee C Exelon Generation Co, Exelon Nuclear |
References | |
IR-09-005 | |
Download: ML100410121 (62) | |
See also: IR 05000237/2009005
Text
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION III
2443 WARRENVILLE ROAD, SUITE 210
LISLE, IL 60532-4352
February 10, 2010
Mr. Charles G. Pardee
Senior Vice President, Exelon Generation Company, LLC
President and Chief Nuclear Officer (CNO), Exelon Nuclear
4300 Winfield Road
Warrenville, IL 60555
SUBJECT: DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3
INTEGRATED INSPECTION REPORT 05000237/2009-005;
Dear Mr. Pardee:
On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an
integrated inspection at your Dresden Nuclear Power Station, Units 2 and 3. The enclosed
report documents the inspection results, which were discussed on January 14, 2010, with
Mr. T. Hanley and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
The report documents two NRC-identified findings and five self-revealed findings of very low
safety significance (Green). All of these findings were determined to involve a violation of
NRC requirements. Additionally, one licensee-identified violation is listed in Section 4OA7 of
this report. However, because of the very low safety significance and because they are entered
into your corrective action program, the NRC is treating these findings as non-cited violations
(NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy.
If you contest any NCV, you should provide a response within 30 days of the date of this
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional
Administrator, Region III; 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352, the Director,
Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and
the NRC Resident Inspector at Dresden. In addition, if you disagree with the characterization of
any finding in this report, you should provide a response within 30 days of the date of this
inspection report, with the basis for your disagreement, to the Regional Administrator,
Region III, and the NRC Resident Inspector at Dresden. The information you provide will be
considered in accordance with Inspection Manual Chapter 0305.
C. Pardee -2-
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its
enclosure, and your response (if any) will be made available electronically for public inspection
in the NRC Public Document Room or from the Publicly Available Records (PARS) component
of NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Mark A. Ring, Chief
Branch 1
Division of Reactor Projects
Docket Nos. 50-237; 50-249
Enclosure: Inspection Report 05000237/2009-005; 05000249/2009-005
w/Attachment: Supplemental Information
cc w/encl: Distribution via ListServ
U.S. NUCLEAR REGULATORY COMMISSION
REGION III
Docket Nos: 50-237; 50-249
Report No: 05000237/2009-005; 05000249/2009-005
Licensee: Exelon Generation Company
Facility: Dresden Nuclear Power Station, Units 2 and 3
Location: Morris, IL
Dates: October 1 through December 31, 2009
Inspectors: C. Phillips, Senior Resident Inspector
D. Meléndez-Colón, Resident Inspector
J. Benjamin, Project Engineer
J. Draper, Reactor Engineer
D. Sand, Reactor Engineer
C. Moore, Operations Engineer
F. Ramírez, Resident Inspector, LaSalle Station
J. McGhee, Senior Resident Inspector, Quad Cities
M. Holmberg, Reactor Inspector
M. Mitchell, Health Physicist
R. Jickling, Senior Emergency Preparedness Inspector
L. Kozak, Senior Reactor Analyst
Approved by: M. Ring, Chief
Projects Branch 1
Division of Reactor Projects
Enclosure
TABLE OF CONTENTS
SUMMARY OF FINDINGS ...........................................................................................................1
REPORT DETAILS .......................................................................................................................6
Summary of Plant Status...........................................................................................................6
1. REACTOR SAFETY .......................................................................................................6
1R04 Equipment Alignment (71111.04) ......................................................................6
1R05 Fire Protection (71111.05) .................................................................................9
1R08 Inservice Inspection Activities (71111.08G).....................................................10
1R11 Licensed Operator Requalification Program (71111.11) .................................11
1R12 Maintenance Effectiveness (71111.12) ...........................................................12
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)......13
1R15 Operability Evaluations (71111.15)..................................................................13
1R19 Post-Maintenance Testing (71111.19).............................................................16
1R20 Outage Activities (71111.20) ...........................................................................19
1R22 Surveillance Testing (71111.22) ......................................................................22
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)..............25
2. RADIATION SAFETY ...................................................................................................27
2OS1 Access Control to Radiologically Significant Areas (71121.01) .......................27
2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)..........28
4. OTHER ACTIVITIES.....................................................................................................29
4OA1 Performance Indicator (PI) Verification (71151) ..............................................29
4OA2 Identification and Resolution of Problems (71152) ..........................................30
4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153).............34
4OA5 Other Activities.................................................................................................42
4OA6 Management Meetings ....................................................................................44
4OA7 Licensee-Identified Violations ..........................................................................44
SUPPLEMENTAL INFORMATION ...............................................................................................1
KEY POINTS OF CONTACT.....................................................................................................1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED ........................................................2
LIST OF DOCUMENTS REVIEWED.........................................................................................4
LIST OF ACRONYMS USED ..................................................................................................10
Enclosure
SUMMARY OF FINDINGS
IR 05000237/2009-005, 05000249/2009-005; 10/01/2009 - 12/31/2009; Dresden Nuclear Power
Station, Units 2 & 3; Equipment Alignment, Operability Evaluations, Post-Maintenance Testing,
Surveillance Testing, Outage, and Event Follow-up.
This report covers a three-month period of inspection by resident inspectors and announced
baseline inspections by regional inspectors. Two Green findings were identified by the
inspectors and five findings were self-revealed. All of the findings were considered Non-Cited
Violations (NCVs) of NRC regulations. The significance of most findings is indicated by their
color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,
Significance Determination Process (SDP). Cross-cutting aspects were determined using
IMC 0305, "Operating Reactor Assessment Program." Findings for which the SDP does not
apply may be Green or be assigned a severity level after NRC management review. The NRCs
program for overseeing the safe operation of commercial nuclear power reactors is described in
NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.
A. NRC-Identified and Self-Revealed Findings
Cornerstone: Initiating Events
- Green. A self-revealed finding involving a non-cited violation (NCV) of Technical
Specification 5.4.1 was identified on October 3, 2009, due to the licensees failure to
include essential information in DOP 1200-03, RWCU System Operation with the
Reactor at Pressure, Revision 51, regarding startup of the reactor water cleanup system
with the reactor at pressure. This procedural deficiency caused a pressure pulse that
resulted in a reactor water level Low-Low Group 1 Isolation Signal and Unit 3 reactor
scram. This event was entered into the licensees corrective action program (CAP) as
Issue Report (IR) 974426. Corrective actions by the licensee included revising
procedure DOP 1200-03.
This finding was considered more than minor because it affected the Initiating Events
Cornerstone objective to limit the likelihood of those events that upset plant stability and
challenge critical safety functions during shutdown as well as at power operations.
The finding was determined to be of very low safety significance because it did not
contribute to both the likelihood of a reactor trip AND the likelihood that mitigating
equipment or functions will not be available. This finding has a cross-cutting aspect in
the area of Human Performance (Resources) because the licensee did not provide
complete, accurate and up-to-date procedures to plant personnel.
H.2(c) (Section 4OA3.2)
Cornerstone: Mitigating Systems
- Green. A finding of very low safety significance and associated NCV of Technical
Specification 5.4.1 was self-revealed for the failure to meet the requirements of
Clearance Order (CO) 69631 by removing shorting links instead of fuses as required by
the CO on November 12, 2009. As a result, protective relaying was unintentially
removed from the Unit 2 main power transformer TR-2, the unit auxiliary transformer
TR-21, and the reserve auxiliary transformer TR-22. This issue was entered into the
licensees CAP as Issue Report 992290. Corrective actions included: coaching of the
individuals involved with the incorrect placing of the out-of-service and a placard on the
1 Enclosure
device that was incorrectly repositioned was changed to include the specific equipment
part number of the shorting links.
The finding was determined to be more than minor because the finding could reasonably
be viewed as a precursor to a significant event. The finding was evaluated using the
SDP in accordance with IMC 0609, Appendix G, Attachment 1, Shutdown Operations
Significance Determination Process Phase 1 Operational Checklists For Both PWRs and
BWRs, Checklist 6, dated May 25, 2004. This checklist stated that for a finding to
require a Phase 2 or 3 determination, it would require an increase in the likelihood of a
loss of offsite power or degrade the licensees ability to cope with a loss of offsite power.
The ability of the licensee to cope with a loss of offsite power was not impacted because
at least one emergency diesel generator was operable during the entire period. The
inspectors determined that neither of these conditions were met so the finding screened
as Green. This finding had a cross-cutting aspect in the area of Human Performance,
Work Practices. H.4(a) (Section 1R04)
- Green. The inspectors identified a finding of very low safety significance and associated
NCV of Technical Specification 5.4.1 for the licensee failing to follow Dresden procedure
DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39. On
September 24, 2009, the inspectors identified valve 2-1501-42A, U2 low pressure
coolant injection (LPCI) A pump gland leak-off valve, was closed instead of open as
required by DOP 2-1500-M1. With this valve closed instead of open, the control room
alarm for LPCI pump seal leakage would not have been able to fulfill its function.
The issue was entered into the licensees CAP as IR 969490. The licensees corrective
actions included changing maintenance procedure DMP 1500-05, LPCI Pump
Maintenance, step G.25.d to include the case drain valve equipment numbers and sign
offs to position and verify the valves; and Operations Department Management
addressed the operations department personnel about this issue.
The finding was determined to be more than minor because the finding, if left
uncorrected, would become a more significant safety concern. Specifically, the valve
isolated an alarm in the control room. The inspectors concluded this finding was
associated with the Mitigating Systems Cornerstone using IMC 0609, Significance
Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and
Characterization of Findings, Table 4a, dated January 10, 2008. This finding has a
cross-cutting aspect in the area of Human Performance, Work Practices because the
licensee did not have any documentation as to how or when the valve was placed into
the position it was in. The design and location of the valve precluded that the valve was
accidently placed into the position it was found in. Therefore, the inspectors concluded
that either the failure to use human error prevention techniques or maintaining proper
documentation of activities caused the mispositioning of valve 2-1501-42A.
H.4.(a) (Section 1R15)
- Green. The inspectors identified a finding of very low significance and associated
NCV of 10 CFR 50 Appendix B, Criterion XI, Test Control, because the licensee
unacceptably preconditioned the Unit 2 Emergency Diesel Generator (EDG) prior to
performing Technical Specification (TS) Surveillance Requirements (SR) 3.8.1.19.c.4,
3.8.1.12.c.3, and 3.8.1.10. These TS SRs involved verifying that the EDG supplied
steady state frequency would be acceptable following a loss of offsite power coincident
with and without a loss of coolant accident, and following the loss of the largest
post-accident load. Specifically, the inspectors identified that the licensee routinely
2 Enclosure
performed governor oil change outage maintenance activities which involved a section
that tuned the Unit 2 diesel governors response to a load change just prior to performing
these TS SRs. This issue has been entered into the licensees CAP as IR 1000609.
The licensee had not reached a conclusion on corrective actions by the end of the
inspection period.
This finding was determined to be more than minor because the finding, if left
uncorrected, would become a more significant safety concern. Unacceptable
preconditioning the EDG could mask latent performance issues and affect the ability of
the EDG to supply safety-related power to vital loads during an event. The inspectors
performed a Phase 1 SDP evaluation and determined that this issue was Green
because it did not result in an inoperable Unit 2 EDG. The failure to adequately
coordinate the work activity of the preventive maintenance and post-maintenance testing
with the TS SR activities was the principal contributor to this finding and was reflective of
recent performance. This finding had a cross-cutting aspect in the area of Work Control.
Specifically, the licensee did not appropriately coordinate work activities by incorporating
actions to address the impact of the work as different job activities. The scheduling of
the work activities resulted in the pre-conditioning of the EDG prior to performing the
surveillance tests. H.3(b) (Section 1R19)
- Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,
Appendix B, Criterion IV, Procurement Document Control, was self-revealed for the
licensee's failure to ensure a safety-related plug was ordered and installed where
required in the 2/3 EDG turbo lube oil Y strainer. Instead, a non-conforming part was
installed, which resulted in a one-half gallon per minute oil leak and removal of the diesel
generator from service. The issue was entered into the licensees CAP as IR 926605.
Corrective actions included inspection of all other diesel generators to ensure the non-
conforming condition did not exist on another machine, revising the procurement
documents to ensure that future parts include a pressure retaining pipe plug with
approved material, and adding a requirement for a quality inspection to be performed to
inspect the strainer for metallic pipe plug in blow down port. Individual procedure
compliance issues were addressed through the stations performance improvement
initiatives.
The finding was determined to be more than minor because the finding was similar to
IMC 0612, Appendix E, Example 5 c because an incorrect and inadequate part was
installed and the system was returned to service. This performance deficiency impacted
the Mitigating Systems Cornerstone objective to ensure the availability, reliability, and
capability of systems that respond to initiating events to prevent undesirable
consequences. A Phase 3 SDP risk evaluation was performed by the regional
Senior Risk Analyst who determined the risk significance of the finding to be less than
1.0E-6/yr delta core damage frequency (CDF) and less than 1.0E-7/yr delta LERF, which
represents a finding of very low safety significance. Failure of plant personnel to
question the plastic shipping plug before the equipment was installed and returned to
service was not in compliance with MA-AA-716-008, Foreign Material Exclusion
Program, and, therefore, inspectors determined that this event was cross-cutting in
Human Performance, Work Practices, Procedural Compliance for failure of personnel to
follow the procedure. H.4(b) (Section 4OA3.3)
3 Enclosure
Cornerstone: Barrier Integrity
- Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,
Appendix B, Criterion V, was self-revealed for the failure to properly move a fuel
assembly to its specified location, in accordance with DFP 0800-01, Master Refueling
Procedure. Specifically, on November 5, 2004, fuel assembly JLU569 was placed in
position C4-E5, instead of C4-F5, as required by the procedure. The violation was
placed into the licensees CAP in IR 990180. As corrective action, the licensee
temporarily suspended all fuel handling activities, conducted a piece count of the spent
fuel and stationed a second Senior Reactor Operator on the refueling bridge as
additional oversight for follow-on fuel movements. Additionally the fuel handling crew
associated with the event was suspended from future fuel moves, pending remedial
training.
Using the guidance contained in IMC 0612, Power Reactor Inspection Reports,
Appendix B, Issue Disposition Screening, dated December 4, 2008, the inspectors
determined that the finding was more than minor because the finding was associated
with the configuration control and human performance attributes of the Barrier Integrity
Cornerstone and impacted the Barrier Integrity Cornerstone objective to provide
reasonable assurance that physical design barriers (i.e., fuel cladding) protect the public
from radionuclide releases caused by an accident or event. Specifically, the shutdown
margin and thermal management of the spent fuel pool(s) is affected by fuel assembly
placement inside the pool(s). The inspectors determined the finding could be evaluated
using the significance determination process in accordance with IMC 0609,
Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening
and Characterization of Findings, Table 3b, question 6, which directed the inspectors to
Appendix M, Significance Determination Process Using Qualitative Criteria. Because
probabilistic risk assessment tools were not well suited for this finding, the criteria for
using IMC 0609, Appendix M, were met. In determining the significance of this finding,
regional management reviewed the licensee's bounding analysis in the UFSAR, which
demonstrated that regardless of the incorrect bundle position in the fuel pool, the design
of the pool still maintained pool Keff less than .95. Based on the additional qualitative
circumstances associated with this finding, regional management concluded the finding
was of very low safety significance (Green). This finding has a cross-cutting aspect in
the area of Human Performance, Work Practices. Specifically, neither the Senior
Reactor Operator (SRO), nor either of the two members of the fuel handling crew,
adequately performed independent verification techniques that ensured the fuel
assembly move was made in accordance with the Nuclear Component Transfer List, as
required by DFP 0800-01. H.4(a) (Section 1R20)
- Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,
Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed for
the mispositioning of a Unit 3 control rod at power. Control rod G-11 was withdrawn one
notch contrary to TS SR 3.1.3.3 requirements to insert each withdrawn control rod at
least one notch. This was a performance deficiency. The violation was entered into the
licensees CAP as IR 993634. Corrective actions included inserting control rod G-11
one notch back to the original position and suspending control rod movement while all
rods were verified to be in their correct position. The operator was removed from shift
duties and the oncoming shift was briefed of the event.
4 Enclosure
The finding was determined to be more than minor because the finding was associated
with the Barrier Integrity Cornerstone attributes of human performance and configuration
control of a control rod, and affected the cornerstone objective of providing reasonable
assurance that physical design barriers protect the public from radionuclide releases
caused by accidents or events. Specifically, the operator withdrew a control rod contrary
to expected operation. This added positive reactivity and caused an unanticipated
power increase. The inspectors evaluated the finding using the SDP in accordance with
IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial
Screening and Characterization of Findings, Table 4a for the Fuel Barrier Cornerstone.
Per Table 4a, any issue that involves the fuel barrier is screened as Green. This finding
had no cross-cutting aspect. (Section 1R22)
B. Licensee-Identified Violations
A violation of very low safety significance that was identified by the licensee has been
reviewed by inspectors. Corrective actions planned or taken by the licensee have been
entered into the licensees CAP. This violation and corrective action tracking numbers
are listed in Section 4OA7 of this report.
5 Enclosure
REPORT DETAILS
Summary of Plant Status
Unit 2
On October 18, 2009, the unit began its coastdown to D2R21, and continued to downpower until
the end of the month.
On November 1, 2009, the unit was shutdown for the D2R21 Refueling Outage.
On December 2, 2009, the unit began ramp-up following D2R21.
On December 9, 2009, the unit returned to full power.
Unit 3
On October 3, 2009, the unit scrammed due to a Group 1 isolation resulting from a reactor
water clean-up pressure perturbation. The unit returned to full power on October 8, 2009.
On October 18, 2009, power was reduced to approximately 82 percent for a control rod pattern
adjustment. The unit returned to full power on the same day.
On November 6, 2009, the main turbine was manually tripped due to an EHC fluid leak from a
main stop valve. The unit returned to full power on November 10, 2009.
On November 19, 2009, power was reduced to approximately 82 percent for a control rod
pattern adjustment. The unit returned to full power on the same day.
On December 12, 2009, power was reduced to approximately 70 percent for control rod testing,
scram testing and quarterly valve testing. The unit returned to full power on
December 13, 2009.
1. REACTOR SAFETY
1R04 Equipment Alignment (71111.04)
.1 Quarterly Partial System Walkdowns
a. Inspection Scope
The inspectors performed partial system walkdowns of the following risk-significant
systems:
- Unit 3 250V battery and DC buses during Unit 2 250V battery discharge test;
- B train of standby gas treatment when A train declared inoperable;
- U2 Division 2 low pressure coolant injection and containment cooling service
water restoration after D2R21; and
- Unit 2 main power transformer clearance order error.
6 Enclosure
The inspectors selected these systems based on their risk significance relative to the
Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted
to identify any discrepancies that could impact the function of the system, and, therefore,
potentially increase risk. The inspectors reviewed applicable operating procedures,
system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical
Specification (TS) requirements, outstanding work orders (WOs), condition reports, and
the impact of ongoing work activities on redundant trains of equipment in order to identify
conditions that could have rendered the systems incapable of performing their intended
functions. The inspectors also walked down accessible portions of the systems to verify
that system components and support equipment were aligned correctly and operable.
The inspectors examined the material condition of the components and observed
operating parameters of equipment to verify that there were no obvious deficiencies.
The inspectors also verified that the licensee had properly identified and resolved
equipment alignment problems that could cause initiating events or impact the capability
of mitigating systems or barriers and entered them into the corrective action program
(CAP) with the appropriate significance characterization. Documents reviewed are listed
in the Attachment to this report.
These activities constituted four partial system walkdown samples as defined in
Inspection Procedure (IP) 71111.04-05.
b. Findings
(1) Operating Personnel Incorrectly Placed Clearance Tags
Introduction: A finding of very low safety significance and associated Non-Cited
Violation (NCV) of TS 5.4.1 was self-revealed for the failure to meet the requirements of
Clearance Order (CO) 69631 by removing shorting links instead of fuses as required by
the CO (Green). The inspectors determined this finding to be self-revealed because it
required no active and deliberate observation by the licensee or NRC inspectors to
determine whether a change in process or equipment capability or function had
occurred. The licensee was in the process of restoring fuses when it was observed the
fuses had not been removed.
Description: Clearance Order 69631 was placed on November 2, 2009. The CO was to
remove fuses (2-0902-29-FU1A and 2-0902-29-FU1B) for the U2 main power
transformer protective relays in preparation for the replacement of the main power
transformer. The fuses were located in the top of panel 902-29 in the auxiliary electric
equipment room. On November 12, 2009, direction was given to restore the fuses per
CO 69631. The non-licensed operators (NLOs), assigned to restore the fuses, found
that fuses 2-902-29-FU1A and 2-0902-29-FU1B had not been removed, but that shorting
links 2-902-29-F8 and 2-0902-29-F12 had been removed instead. These shorting links
removed protective relaying from the main power transformer TR-2, the unit auxiliary
transformer TR-21, and the reserve auxiliary transformer TR-22.
Two NLOs were assigned to remove the fuses. One of them was a Dresden operator,
the other was a traveler from Braidwood Station. The Braidwood operator had returned
to Braidwood Station by the time this issue was identified. The inspectors interviewed
the Dresden operator. The NLO stated that he never saw the fuses that were to be
removed. The labels for the fuses were below the fuses he was required to remove and
above a fuse block that contained the shorting links that he did remove. The fuse block
7 Enclosure
containing the shorting links had a placard on it stating that there were shorting links
inside the fuse block. The operator stated that he had not read the placard. In addition,
the operator stated that after the incorrect fuse block was removed he looked inside the
fuse block and recognized that they were shorting links and not fuses. The operator
stated that this did not alert him that the wrong equipment had been manipulated. The
operator also stated that he had been trained to recognize the difference between
shorting links and fuses.
Analysis: The inspectors determined that removal of shorting links instead of fuses was
contrary to the requirements of CO 69631 and was a performance deficiency.
The finding was determined to be more than minor because the finding could reasonably
be viewed as a precursor to a significant event. Specifically, the process error by the
non-licensed operators involved in the performance of the CO to properly detect that the
wrong piece of equipment had been removed, even after observing that the removed
equipment was not what they were assigned to remove (i.e., shorting link versus a fuse),
was a failure that, if left uncorrected, could lead to a significant event.
The inspectors determined the finding could be evaluated using the SDP in accordance
with IMC 0609, Appendix G, Attachment 1, Shutdown Operations Significance
Determination Process Phase 1 Operational Checklists For Both PWRs AND BWRs,
Checklist 6, dated May 25, 2004. This checklist stated that for a finding to require a
Phase 2 or 3 determination, it would require an increase in the likelihood of a loss of
offsite power or degrade the licensees ability to cope with a loss of offsite power.
The ability of the licensee to cope with a loss of offsite power was not impacted because
at least one emergency diesel generator was operable during the entire period. The
inspectors determined that neither of these conditions were met so the finding screened
as Green.
This finding has a cross-cutting aspect in the area of Human Performance,
Work Practices. The licensee communicates human error prevention techniques, such
as self and peer checking. In addition, personnel do not proceed in the face of
uncertainty or unexpected circumstances. Specifically, the NLO: 1) did not read the
placard that was on the component that the NLO removed, which explained that the
component was a shorting link and not a fuse; and 2) did not question why the
component the NLO removed was a shorting link and not a fuse, as identified in the CO.
Enforcement: Technical Specification Section 5.4.1 states, in part, that
Written procedures shall be established, implemented, and maintained covering the
following activities: The applicable procedures recommended in Regulatory Guide 1.33,
Revision 2, Appendix A, February 1978. Paragraph 1.c of Regulatory Guide 1.33
states, in part, that procedures for equipment control, locking and tagging shall be
prepared and activities shall be performed in accordance with these procedures. The
licensee established CO 69631 as the implementing procedure for tagging out-of-service
the Unit 2 Main Power Transformer.
Contrary to the above, on November 2, 2009, CO 69631 was incorrectly placed, in that,
fuses (2-0902-29-FU1A and 2-0902-29-FU1B) for the U2 main power transformer
protective relays were not removed as required by CO 69631. Instead, shorting links
2-0902-29-F8 and 2-0902-29-F12 were removed which removed protective relaying to
8 Enclosure
the U2 main power transformer, U2 reserve auxiliary transformer, and the U2 unit
auxiliary transformer. Corrective actions included: coaching of the individuals involved
with the incorrect placing of the out-of-service, and changing a placard on the device that
was incorrectly repositioned to include the specific equipment part number of the
shorting links. Because this violation was of very low safety significance and it was
entered into the licensees corrective action program as Issue Report 992290 this
violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC
Enforcement Policy. (NCV 05000237/2009005-01)
1R05 Fire Protection (71111.05)
.1 Routine Resident Inspector Tours (71111.05Q)
a. Inspection Scope
The inspectors conducted fire protection walkdowns which were focused on availability,
accessibility, and the condition of firefighting equipment in the following risk-significant
plant areas:
- Fire Zone 1.1.1.4, Unit 3 Reactor Building Elevation570, Secondary
Containment;
- Fire Zone 8.2.5.B, Unit 2 Turbine Building Elevation 517, Low Pressure Heater
Bays North Turbine Cavity;
- Fire Zone 8.2.5.A, Unit 2 Turbine Building Elevation 517, High Pressure
Heaters/Steam Lines; and
- Fire Zone 8.2.6.B Multiple Elevations, Low Pressure Heater Bays.
The inspectors reviewed areas to assess if the licensee had implemented a fire
protection program that adequately controlled combustibles and ignition sources within
the plant, effectively maintained fire detection and suppression capability, maintained
passive fire protection features in good material condition, and implemented adequate
compensatory measures for out-of-service, degraded or inoperable fire protection
equipment, systems, or features in accordance with the licensees fire plan. The
inspectors selected fire areas based on their overall contribution to internal fire risk as
documented in the plants Individual Plant Examination of External Events, their potential
to impact equipment, which could initiate or mitigate a plant transient, or their impact on
the plants ability to respond to a security event. Using the documents listed in the
Attachment to this report,, the inspectors verified that fire hoses and extinguishers were
in their designated locations and available for immediate use; that fire detectors and
sprinklers were unobstructed; that transient material loading was within the analyzed
limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory
condition. The inspectors also verified that minor issues identified during the inspection
were entered into the licensees CAP. Documents reviewed are listed in the Attachment
to this report.
These activities constituted four quarterly fire protection inspection samples as defined in
IP 71111.05-05.
b. Findings
No findings of significance were identified.
9 Enclosure
1R08 Inservice Inspection Activities (71111.08G)
For Unit 2, from November 2, 2009, through November 13, 2009, the inspectors
conducted a review of the implementation of the licensees Inservice Inspection (ISI)
Program for monitoring degradation of the reactor coolant system, steam generator
tubes, emergency feedwater systems, risk-significant piping and components and
containment systems.
The inspections described in Sections 1R08.1 and 1R08.5 below count as one
inspection sample as defined in IP 71111.08-05.
.1 Piping Systems ISI
a. Inspection Scope
The inspectors observed ultrasonic examination (UT) of the following examination
Category F welds (e.g., welds with known cracks approved by analysis for limited
additional service without repair) to evaluate compliance with the licensees augmented
Stress Corrosion Cracking Program. Specifically, the inspectors evaluated these
examinations to determine if the procedures, equipment, and personnel used were
qualified in accordance with the American Society of Mechanical Engineers (ASME)
Code Section XI, Appendix VIII.
- UT of the safe end-to-elbow (PS2/201-1) on the loop B recirculation system.
The inspectors observed a video record and reviewed a written report of the following
containment drywell supports to evaluate compliance with the licensees augmented
inspection program for Code Class MC supports. Specifically, the inspectors evaluated
this examination to determine if the VT-3 procedure, equipment, and personnel used
were qualified in accordance with the ASME Code Section XI.
- Visual examination (VT-3) of eight male and female drywell shear lug stabilizers
(support groups 09 and 10).
The inspectors reviewed the following examination record with relevant/recordable
conditions/indications identified by the licensee to determine if acceptance of these
indications for continued service was in accordance with the ASME Code Section XI or
an NRC-approved alternative.
(2RPV UPP HD/2-THD-FLG). The inspectors observed the following pressure
boundary weld completed for a risk-significant system to determine if the licensee
followed an ASME Code Section IX qualified welding procedure, maintained
control of foreign material, and to determine if the welder used qualified weld filler
material and base material. The inspectors also reviewed the work order for this
welding to determine if the post weld nondestructive examinations required by
the ASME Code were specified.
- Weld (FW-2) fabricated during installation of the component cooling service
water system pump discharge elbow replacement.
10 Enclosure
b. Findings
No findings of significance were identified.
.2 Reactor Pressure Vessel Upper Head Penetration Inspection Activities (Not Applicable)
.3 Boric Acid Corrosion Control (Not Applicable)
.4 Steam Generator Tube Inspection Activities (Not Applicable)
.5 Identification and Resolution of Problems
a. Inspection Scope
The inspectors performed a review of ISI related problems entered into the licensees
corrective action program and conducted interviews with licensee staff to determine if:
- the licensee had established an appropriate threshold for identifying ISI-related
problems;
- the licensee had performed a root cause (if applicable) and taken appropriate
corrective actions; and
- the licensee had evaluated operating experience and industry generic issues
related to ISI and pressure boundary integrity.
The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,
Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action
documents reviewed by the inspectors are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification Program (71111.11)
a. Inspection Scope
On August 3, 2009, the inspectors observed a crew of licensed operators in the plants
simulator during licensed operator requalification examinations to verify that operator
performance was adequate, evaluators were identifying and documenting crew
performance problems and training was being conducted in accordance with licensee
procedures. The inspectors evaluated the following areas:
- licensed operator performance;
- crews clarity and formality of communications;
- ability to take timely actions in the conservative direction;
- prioritization, interpretation, and verification of annunciator alarms;
- correct use and implementation of abnormal and emergency procedures;
- control board manipulations;
- oversight and direction from supervisors; and
- ability to identify and implement appropriate TS actions and Emergency Plan
actions and notifications.
11 Enclosure
The crews performance in these areas was compared to pre-established operator action
expectations and successful critical task completion requirements. Documents reviewed
are listed in the Attachment to this report.
This inspection constituted one quarterly licensed operator requalification program
sample as defined in IP 71111.11.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12)
.1 Routine Quarterly Evaluations (71111.12Q)
a. Inspection Scope
The inspectors evaluated degraded performance issues involving the following
risk-significant systems:
- Unit 3 control rod drive (Z03); and
- Unit 2 Shutdown Cooling (Z10).
The inspectors reviewed events such as where ineffective equipment maintenance had
resulted in valid or invalid automatic actuations of engineered safeguards systems and
independently verified that the licensee's actions to address system performance or
condition problems in terms of the following:
- implementing appropriate work practices;
- identifying and addressing common cause failures;
- scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
- characterizing system reliability issues for performance;
- charging unavailability for performance;
- trending key parameters for condition monitoring;
- ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
- verifying appropriate performance criteria for structures, systems, and
components (SSCs)/functions classified as (a)(2) or appropriate and adequate
goals and corrective actions for systems classified as (a)(1).
The inspectors assessed performance issues with respect to the reliability, availability,
and condition monitoring of the system. In addition, the inspectors verified that
maintenance effectiveness issues were entered into the CAP with the appropriate
significance characterization. Documents reviewed are listed in the Attachment to this
report.
This inspection constituted two quarterly maintenance effectiveness samples as defined
in IP 71111.12-05.
b. Findings
No findings of significance were identified.
12 Enclosure
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
a. Inspection Scope
The inspectors reviewed the licensee's evaluation and management of plant risk for the
maintenance and emergent work activities affecting risk-significant and safety-related
equipment listed below to verify that the appropriate risk assessments were performed
prior to removing equipment for work:
- 345 kv Switchyard Bus 4 outage; and
- 345 kv Line 8014 trip.
These activities were selected based on their potential risk significance relative to the
Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
and complete. When emergent work was performed, the inspectors verified that the
plant risk was promptly reassessed and managed. The inspectors reviewed the scope
of maintenance work, discussed the results of the assessment with the licensee's
probabilistic risk analyst or shift technical advisor, and verified plant conditions were
consistent with the risk assessment. The inspectors also reviewed Technical
Specification (TS) requirements and walked down portions of redundant safety systems,
when applicable, to verify risk analysis assumptions were valid and applicable
requirements were met.
These maintenance risk assessments and emergent work control activities constituted
two samples as defined in IP 71111.13-05.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations (71111.15)
a. Inspection Scope
The inspectors reviewed the following issues:
- IR 957843, Failed Flowscan on AOV [air operated valve] 3-1599-61;
- IR 967008, Degraded Thermal Performance of the 2A LPCI [low pressure
coolant injection] Hx [heat exchanger];
- IR 987982, Boron Liquid Leak on 3B SBLC [standby liquid control] Pump; and
- IR 986676, Auto Bypass Sensors Not in Accordance with
UFSAR Requirements.
The inspectors selected these potential operability issues based on the risk significance
of the associated components and systems. The inspectors evaluated the technical
adequacy of the evaluations to ensure that TS operability was properly justified and the
subject component or system remained available such that no unrecognized increase in
risk occurred. The inspectors compared the operability and design criteria in the
appropriate sections of the TS and UFSAR to the licensees evaluations, to determine
whether the components or systems were operable. Where compensatory measures
13 Enclosure
were required to maintain operability, the inspectors determined whether the measures
in place would function as intended and were properly controlled. The inspectors
determined, where appropriate, compliance with bounding limitations associated with the
evaluations. Additionally, the inspectors also reviewed a sampling of corrective action
documents to verify that the licensee was identifying and correcting any deficiencies
associated with operability evaluations. Documents reviewed are listed in the
Attachment to this report.
This operability inspection constituted four samples as defined in IP 71111.15-05.
b. Findings
(1) NRC Inspector-Identified Control Room Alarm Isolation Valve Out-of-Position
Introduction: A finding of very low safety significance and associated NCV of TS 5.4.1
was identified by the inspectors for the licensee failing to follow Dresden procedure
DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39. The inspectors
identified valve 2-1501-42A, U2 low pressure coolant injection (LPCI) A pump gland
leak-off, was out-of-position (closed) and documented an unresolved item (URI) in
inspection report 05000237/2009004; 05000249/2009004.
Description: On September 24, 2009, the inspectors identified that the 2-1501-42A
valve was out-of-position. The inspectors were reviewing the 2A LPCI pump seal
leak-off configuration as part of an evaluation of the mechanical seal safety
classification. The inspectors reported the valve position to shift management and
operations department personnel verified the valve was not in the open position as
described in DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39.
This issue was documented in IR 969490, LPCI Gland Seal Leak-off Isolation Found
Closed. With the valve closed instead of open, a control room alarm (902-3 C-6) for
LPCI pump seal leakage would not have alarmed for the 2A LPCI pump had the seal
failed during operation.
The issue was considered an unresolved item in Inspection Report 05000237/2009-004;
05000249/2009-004 pending NRC review of the licensees evaluation of the valve
position versus the requirements of DOP 2-1500-M1.
The licensee performed a prompt investigation into the mispositioning of the valve.
The licensee was unable to determine the reason for, or the time at which the valve
became mispositioned. The licensee did determine that on July 6, 2009, the 2A LPCI
pump seal was replaced under Work Order 548808-01 and procedure DMP 1500-05,
LPCI Pump Maintenance, Revision 8.
The inspectors observed that the licensee took a corrective action to change
maintenance procedure DMP 1500-05, LPCI Pump Maintenance, Revision 8,
step G.25.d to include the case drain valve equipment numbers. The inspectors
reviewed procedure DMP 1500-05, Revision 8, step G.25.d and found that it had
directed only that the case drain valves be closed with no specific equipment number
designations. Since the valve that was found mispositioned was a drain valve and in
close proximity to the case drain valves, it was possible that 2-1501-42A was closed at
the same time that the case drain valves were closed. There was no step in
DMP 1500-05 past step G.25.d to open the case drain valves.
14 Enclosure
Analysis: The inspectors determined that the as found position of 2-1501-42A was
contrary to the requirement of DOP 2-1500-M1, LPCI System Mechanical Checklist,
Revision 39 and was a performance deficiency.
The finding was determined to be more than minor because the finding, if left
uncorrected, would become a more significant safety concern. Specifically, the valve
isolated an alarm in the control room. The alarm warned the control room operators of a
LPCI pump mechanical seal failure. A mechanical seal failure of a LPCI pump during an
accident condition could result in exceeding the limits of the leakage outside the primary
containment as described in TS` 5.5.2. The inspectors concluded this finding was
associated with the Mitigating Systems Cornerstone.
The inspectors determined the finding could be evaluated using the SDP in accordance
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
Initial Screening and Characterization of Findings, Table 4a, dated January 10, 2008,
for the Mitigating System Cornerstone. The inspectors answered No to all five
questions on Table 4a. This issue screened as Green.
This finding has a cross-cutting aspect in the area of Human Performance, Work
Practices because the licensee did not have any documentation as to how or when the
valve was placed into the position it was in. The design and location of the valve
precluded that the valve was accidently placed into the position it was found in.
Therefore, the inspectors concluded that either the failure to use human error prevention
techniques or maintaining proper documentation of activities caused the mispositioning
of valve 2-1501-42A. H.4(a)
Enforcement: Technical Specification Section 5.4.1.a states, in part, that
Written procedures shall be established, implemented, and maintained covering the
following activities: The applicable procedures recommended in Regulatory Guide 1.33,
Revision 2, Appendix A, February 1978. Paragraph 4 of this Regulatory Guide states,
in part, that procedures for energizing, filing, venting, draining, startup, shutdown, and
changing modes of operation for Emergency Core Cooling Systems shall be prepared
and activities shall be performed in accordance with these procedures. The licensee
established DOP 2-1500-M1, LPCI System Mechanical Checklist, Revision 39, as one
of the implementing procedures.
Contrary to the above, on September 24, 2009, the inspectors identified that the
2-1501-42A valve was not in the open position as required by DOP 2-1500-M1,
LPCI System Mechanical Checklist, Revision 39. The licensee took the following
corrective actions: restored 2-1501-42A to the correct position; changed maintenance
procedure DMP 1500-05, LPCI Pump Maintenance, step G.25.d to include the case
drain valve equipment numbers and sign offs to position and verify the valves; and
Operations Department Management addressed the operations department personnel
about this issue. Because this violation was of very low safety significance and it was
entered into the licensees corrective action program as IR 969490, this violation is being
treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy.
(NCV 05000237/2009005-02) (URI 05000237/2009004-04; 05000249/2009004-04 is
closed.
15 Enclosure
1R19 Post-Maintenance Testing (71111.19)
.1 Post-Maintenance Testing
a. Inspection Scope
The inspectors reviewed the following post-maintenance (PM) activities to verify that
procedures and test activities were adequate to ensure system operability and functional
capability:
- WO 1152490-08, OP Perform as Left LLRT [local leak rate test] on 2-0203-2C
MSIV [main steam isolation valve];
- WO 1293386, TSC [Technical Support Center] HVAC [heating, ventilation and
air conditioning] Surveillances Failed;
- WO 1285845, U2 EDG [emergency diesel generator] Largest Load Reject
(TSR 3.8.1.10);
- WO 1286397, 2/3 EDG Voltage Transient; and
- WO 1098975-02, Perform 2B Condensate Pump Inspections.
These activities were selected based upon the structure, system, or component's ability
to impact risk. The inspectors evaluated these activities for the following (as applicable):
the effect of testing on the plant had been adequately addressed; testing was adequate
for the maintenance performed; acceptance criteria were clear and demonstrated
operational readiness; test instrumentation was appropriate; tests were performed as
written in accordance with properly reviewed and approved procedures; equipment was
returned to its operational status following testing (temporary modifications or jumpers
required for test performance were properly removed after test completion); and test
documentation was properly evaluated. The inspectors evaluated the activities against
TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various
NRC generic communications to ensure that the test results adequately ensured that the
equipment met the licensing basis and design requirements. In addition, the inspectors
reviewed corrective action documents associated with post-maintenance tests to
determine whether the licensee was identifying problems and entering them in the CAP
and that the problems were being corrected commensurate with their importance to
safety. Documents reviewed are listed in the Attachment to this report.
This inspection constituted five post-maintenance testing samples as defined in
IP 71111.19-05.
b. Findings
(1) Preconditioning the Unit 2 EDG Prior to Performing Technical Specification (TS)
Surveillance Requirements (SRs)
Introduction: The inspectors identified a finding of very low safety significance and an
associated NCV of 10 CFR 50 Appendix B, Criterion XI, Test Control, because the
licensee unacceptably preconditioned the Unit 2 EDG prior to performing TS
SRs 3.8.1.19.c.4, 3.8.1.12.c.3, and 3.8.1.10 (Green). These TS SRs involved verifying
that the EDG supplied steady state frequency would be acceptable following a loss
offsite power (LOOP) coincident with and without a loss of coolant accident (LOCA), and
following the loss of the largest post-accident load. Specifically, the inspectors identified
16 Enclosure
that the licensee performed governor oil change outage maintenance activities which
involved a section that tuned the Unit 2 diesel governors response to a load change just
prior to performing these TS SRs. The licensee performed the governor oil change
maintenance every six years. The SRs listed above were performed every two years.
Description: On November 13, 2009, during the performance of TS SR 3.8.1.10, under
work order (WO) 00634625-01, the Unit 2 EDG did not recover fast enough to satisfy the
TS SR acceptance criteria. After the largest single post-accident load was shed
(i.e., a service water pump), the EDG frequency went up to 62.4 Hz and did not recover
to the allowable band of 58.8-61.2 Hz until 13 seconds had passed. Technical
Specification SR 3.8.1.10 requires the bus frequency to recover in less than 4 seconds.
The licensee entered this condition into the corrective action program (IR 992803).
A second work order (WO 01285845-01) was created, which adjusted the governor
compensator by using work instructions located in station procedure DES 6600-01,
Diesel Generator Governor Oil Change and Compensation Adjustment, Revision 23.
Following the adjustment, the Unit 2 EDG passed TS SR 3.8.1.10 satisfactorily.
The licensee performed a cause evaluation and determined that the Unit 2 EDG failed
the TS SR because the governor compensation was incorrectly set when performing
WO 634625-01, D2 3RFL PM D/G Governor - Change Oil/Flush/Compensate six days
earlier on November 7, 2009. The licensee determined in their extent of condition
review that the other EDGs were not susceptible to the Unit 2 EDG issue because they
had been successfully tested by performing TS SR 3.8.1.10 as a post-maintenance test
(PMT) since their respective governor oil change outs. The inspectors identified that it
was the practice for the licensee to utilize TS SR 4.8.1.10 as a PMT when performing
these oil changes on a six year interval.
The inspectors questioned the practice of performing preventative maintenance (PM)
activities which involved tuning the EDG governor response just prior to the EDGs
biennial design basis loading/load shedding tests. Furthermore, the inspectors noted
that the maintenance activity utilized to resolve the failed TS SR was to re-perform the
governor compensator adjustment section of the PM activity used on November 7, 2009.
The licensee stated that, after evaluating the issue under IR 1000609, Assignment 1,
that the inspectors issue was an example of acceptable pre-conditioning, primarily for
two reasons. The licensee agreed that the PM and PMT could mask the as-found EDG
governors response during the performance of TS SR 3.8.1.10, but was acceptable
because the TS SR is usually performed without the PM/PMT activity the majority of the
time (oil change/flush every six years, and TS SR is performed every two years.).
In addition the licensee determined that a second diesel run would be required, and that
this run would unnecessarily stress the machine.
The inspectors disagreed with the licensees CAP evaluation and conclusions and
communicated the issue through Dresden management. The inspectors consulted the
NRR Quality Assurance, Vendor Inspection, and Maintenance Branch as recommended
in the NRCs Inspection Manual Part 9900 guidance regarding preconditioning.
The NRR Branch agreed that this issue was not consistent with the guidance outlined in
the NRC technical guidance or Information Notice 97-16, Preconditioning of Plant
Structures, Systems, and Components before ASME Code Inservice Testing or
Technical Specification Surveillance Testing.
17 Enclosure
Analysis: The inspectors determined that the licensee did not establish suitable test
conditions during the Unit 2 EDG TS SRs 3.8.1.19.c.4, 3.8.1.12.c.3, and 3.8.1.10.
The inspectors identified that this was a performance deficiency based on the
10 CFR 50, Appendix B, Criterion XI, Test Control regulatory requirements and the
NRCs generic communication to licensees regarding preconditioning. The failure to
properly test the EDG is considered more than minor because, if left uncorrected, the
finding would become a more significant safety concern. Unacceptable preconditioning
of the EDG could mask latent performance issues and affect the ability of the EDG to
supply safety-related power to vital loads during an event. The inspectors determined
that traditional enforcement was not appropriate because it was not apparent that the
performance deficiency affected the ability of the NRC to regulate. However, the
inspectors noted that this issue could mask failed TS SRs, which would directly feed into
the NRC assessment process. This issue was determined to be Green because it did
not result in an inoperable Unit 2 EDG.
The inspectors determined that the failure to adequately coordinate the work activity of
the PM/PMT and TS SR activities was the principal contributor to this finding and was
reflective of recent performance. This finding had a cross-cutting aspect in the area of
Work Control. Specifically the licensee did not appropriately coordinate work activities
by incorporating actions to address the impact of the work as different job activities. The
scheduling of the work activities resulted in the pre-conditioning of the EDG prior to the
surveillance tests. H.3(b)
Enforcement: 10 CFR 50, Appendix B, Criterion XI, Test Control, requires, in part,
that the test is performed under suitable environmental conditions. Suitable
environment conditions include conditions representative of the expected conditions
when the equipment is required to perform its safety function. The adjustment of the
Unit 2 EDG governor compensator affects how the EDG governor will respond when
TS SRs 3.8.1.19.c.4, 3.8.1.12.c.3, and 3.8.1.10. are performed and, therefore,
preconditions the EDG. The licensee agreed to change the method by which their
maintenance and testing was performed, but had not reached a conclusion on corrective
actions by the end of the inspection period. Because the finding is of very low safety
significance, and has been entered into the corrective action program as IR 01000609, it
is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy,
NUREG 1600. (NCV 05000237/2009005-03)
(2) 2/3 Emergency Diesel Generator (EDG) Overvoltage during Division I Undervoltage
Surveillance
a. Inspection Scope
The inspectors reviewed the licensees equipment apparent cause evaluation (EACE) in
response to a 2/3 EDG overvoltage during performance of DOS 6600-06,
Bus Undervoltage and ECCS Integrated Functional Test for Unit 2/3 Diesel Generator
to Unit 2, Revision 46. Documents reviewed in this inspection are listed in the
Attachment to this report.
This post-maintenance testing review constituted one sample as defined in IP 71111.19.
18 Enclosure
b. Findings
Introduction: The inspectors identified an URI regarding the regulatory requirements
associated with the circumstances surrounding the 2/3 EDG overvoltage event on
November 16, 2009.
Description: On November 16, 2009, at 10:53 a.m., a nuclear station operator (NSO)
was performing step I.11.c per DOS 6600-06, Bus Undervoltage and ECCS Integrated
Functional Test for Unit 2/3 Diesel Generator to Unit 2, Revision 46. At this time, the
operator was attempting to synchronize Bus 23-1 (powered from 2/3 EDG) to Bus 23
(powered from reserve auxiliary transformer 22). The operator stated that he was only
monitoring running versus on-coming bus voltage meters, which are transformed down
and are only relative to actual bus voltages. The operator stated that a loud pop noise
was heard from the 902-3 panel. At this time, the operator noticed that the 23-1/24-1
digital volt meter read around 5600 volts (was previously around 4100 volts). The 2/3
EDG was then shutdown per DOS 6600-06 step I.12. On step I.12.c, the voltage
regulator would not lower (remained upscale). The EDG stopped after the 6-minute cool
down and DOS 6600-06 was stopped.
The licensee generated EACE 994101-07, 2/3 Emergency Diesel Generator (EDG)
Voltage Transient, to determine the cause, extent of condition and corrective actions for
this event. The inspectors reviewed EACE 994101-07 and interviewed the NSO who
had performed DOS 6600-06. The inspectors raised more questions regarding the
capabilities of the control room simulator used for training, procedure adequacy and the
corrective actions in place. The inspectors plan to review the licensees response to
their questions to determine if there were any violations of NRC requirements and that
appropriate corrective actions were applied. (URI 05000237/2009005-04;
1R20 Outage Activities (71111.20)
.1 Other Outage Activities
a. Inspection Scope
The inspectors evaluated outage activities for a Unit 3 forced outage that began on
October 3, 2009, and continued through October 8, 2009. The forced outage was
caused by a Group 1 isolation and reactor scram caused by a pressure pulse caused by
the restoration of the Unit 3 reactor water clean-up system. The inspectors reviewed
activities to ensure that the licensee considered risk in developing, planning, and
implementing the outage schedule.
The inspectors observed or reviewed the reactor shutdown and cooldown, outage
equipment configuration and risk management, electrical lineups, selected clearances,
control and monitoring of decay heat removal, control of containment activities, startup
and heatup activities, and identification and resolution of problems associated with the
outage.
This inspection constituted one other outage sample as defined in IP 71111.20-05.
19 Enclosure
b. Findings
No findings of significance were identified.
.2 Refueling Outage Activities
a. Inspection Scope
The inspectors reviewed the Outage Safety Plan (OSP) and contingency plans for the
Unit 2 refueling outage (RFO), conducted November 1, 2009, through
December 9, 2009, to confirm that the licensee had appropriately considered risk,
industry experience, and previous site-specific problems in developing and implementing
a plan that assured maintenance of defense-in-depth. During the RFO, the inspectors
observed portions of the shutdown and cooldown processes and monitored licensee
controls over the outage activities listed below. Documents reviewed during the
inspection are listed in the Attachment to this report.
- Licensee configuration management, including maintenance of defense-in-depth
commensurate with the OSP for key safety functions and compliance with the
applicable TS when taking equipment out-of-service.
- Implementation of clearance activities and confirmation that tags were properly
hung and equipment appropriately configured to safely support the work or
testing.
- Installation and configuration of reactor coolant pressure, level, and temperature
instruments to provide accurate indication, accounting for instrument error.
- Controls over the status and configuration of electrical systems to ensure that
TS and OSP requirements were met, and controls over switchyard activities.
- Monitoring of decay heat removal processes, systems, and components.
- Controls to ensure that outage work was not impacting the ability of the operators
to operate the spent fuel pool cooling system.
- Reactor water inventory controls including flow paths, configurations, and
alternative means for inventory addition, and controls to prevent inventory loss.
- Controls over activities that could affect reactivity.
- Maintenance of secondary containment as required by TS.
- Refueling activities, including fuel handling and sipping to detect fuel assembly
leakage.
- Startup and ascension to full power operation, tracking of startup prerequisites,
walkdown of the drywell (primary containment) to verify that debris had not been
left, which could block emergency core cooling system suction strainers, and
reactor physics testing.
- Licensee identification and resolution of problems related to RFO activities.
This inspection constituted one RFO sample as defined in IP 71111.20-05.
20 Enclosure
b. Findings
(1) Failure to Follow the Master Refueling Procedure During Movement of Fuel Assembly
JLU569
Introduction: A finding of very low significance (Green) was self-revealed involving a
NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and
Drawings, for failing to follow DFP 0800-01, Master Refueling Procedure, Revision 45,
Page 12, Step 2.b, when the licensee moved fuel assembly JLU569 to the wrong
position in the Unit 2 Spent Fuel Pool during D2R21, on November 5, 2009.
Description: On November 6, 2009, during fuel shuffle 1, the fuel handling crew was
moving a fuel assembly from the reactor to location C4-E5 of the spent fuel pool, per
step 475 of the Nuclear Component Transfer List (Move Sheet), in accordance with
DFP 0800-01, Master Refueling Procedure. While making the move the refueling crew
identified a fuel assembly was already in location C4-E5. The fuel assembly being
moved was then placed in the designated Emergency Set Down Location.
It was immediately determined that the same fuel handling crew had incorrectly
performed step 294 of the Nuclear Component Transfer List the previous night,
November 5, 2009, where they positioned fuel assembly JLU569 into C4-E5, vice the
correct location of C4-F5, each location was located in the same fuel rack.
DFP 0800-01, Master Refueling Procedure, Revision 45, Step 8.d directs the
Senior Reactor Operator (SRO) on the refueling bridge to verify a fuel assembly is
placed in the correct spent fuel pool location by observing rack coordinates in the spent
fuel pool. During interviews with the inspector, it was determined that the crane
operator, fuel-handling supervisor and the SRO had each independently
(and incorrectly) identified spent fuel pool location C4-F5 as C4-E5.
Analysis: The inspectors determined that the licensees failure to move fuel assembly
JLU569 to the correct location in accordance with the Nuclear Component Transfer List
(Move Sheet) was contrary to 10 CFR 50, Appendix B, Criteria V, Instructions,
Procedures, and Drawings, which, in part, requires that activities affecting quality shall
be accomplished in accordance with prescribed instructions, and was a performance
deficiency.
The finding was determined to be more than minor because the finding was associated
with the configuration control and human performance attributes of the Barrier Integrity
Cornerstone and impacted the Barrier Integrity Cornerstone objective to provide
reasonable assurance the physical design barriers (i.e., fuel cladding) protect the public
from radionuclide releases caused by an accident or event. Specifically, the shutdown
margin and thermal management of the spent fuel pool(s) is affected by fuel assembly
placement inside the pool(s).
The inspectors determined the finding could be evaluated using the SDP in accordance
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
Initial Screening and Characterization of Findings, Table 3b, question 6, which directed
the inspectors to Appendix M, Significance Determination Process Using Qualitative
Criteria. Because probabilistic risk assessment tools were not well suited for this
finding, the criteria for using IMC 0609, Appendix M, were met. In determining the
21 Enclosure
significance of this finding, regional management reviewed the licensee's bounding
analysis in the UFSAR which demonstrated that regardless of the incorrect bundle
position in the spent fuel pool, the design of the pool still maintained pool Keff less
than .95. Based on the additional qualitative circumstances associated with this finding,
regional management concluded the finding was very low safety significance (Green).
This finding has a cross-cutting aspect in the area of Human Performance, Work
Practices. Specifically, neither the SRO, nor either of the two members of the fuel
handling crew, adequately performed independent verification techniques that ensured
the fuel assembly move was made in accordance with the Nuclear Component Transfer
List, as required by DFP 0800-01, Revision 45, Page 12, Step 2.b. H.4(a)
Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures and
Drawings, requires, in part, that activities affecting quality shall be prescribed by
documented instructions, procedures, or drawings, of a type appropriate to the
circumstances and shall be accomplished in accordance with these instructions,
procedures, or drawings.
Dresden procedure DFP 0800-01, Master Refueling Procedure, Revision 45 is a
procedure affecting quality. Specifically, it governs fuel movements between the spent
fuel pool and the reactor. Dresden Procedure DFP 0800-01 Step 2.b required the SRO
to ensure that the fuel assembly was moved in accordance with the Nuclear Component
Transfer List (Move Sheet).
Contrary to the above, on November 5, 2009, the licensee failed to follow DFP 0800-01,
Master Refueling Procedure, Revision 45, Step 2.b. Specifically, the fuel handling
crew positioned fuel assembly JLU569 in location C4-E5 of the U2 spent fuel pool
instead of location C4-F5. Because this violation was of very low safety significance and
it was entered into the licensees correction action program as IR 990180, this violation
is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement
Policy. (NCV 05000237/2009005-05)
Corrective actions for this event included a temporary stand down of all fuel handling
activities, a piece count of the spent fuel was performed to identify any errors associated
with fuel handling up to step 475 of the nuclear transfer list, a second SRO and a fuel
handling supervisor were stationed on the refuel bridge to provide additional oversight
during the remaining fuel moves, and the crew associated with the event were not to
resume fuel handling duties until the completion of remedial training.
1R22 Surveillance Testing (71111.22)
.1 Surveillance Testing
a. Inspection Scope
The inspectors reviewed the test results for the following activities to determine whether
risk-significant systems and equipment were capable of performing their intended safety
function and to verify testing was conducted in accordance with applicable procedural
and TS requirements:
22 Enclosure
- WO 1077723-01, D2 20M/RFL [20 month/refuel] TS LLRT [local leak rate test]
MSIV 203-1A & 203-2A Dry Test;
- WO 1257282-01, D2 QTR SBO [station black out] Diesel Generator Surveillance
Test;
- WO 1251254-01, D3 Qtr TS Reactor Low Pressure (350 PSIG) ECCS
[emergency core cooling system] Permissive Ca; and
- WO 1277976-01, D3 1M TS Partially Withdrawn Control Rod Drive Exercise.
(IST Sample).
The inspectors observed in plant activities and reviewed procedures and associated
records to determine the following:
- did unacceptable preconditioning occur;
- were the effects of the testing adequately addressed by control room personnel
or engineers prior to the commencement of the testing;
- were acceptance criteria clearly stated, demonstrated operational readiness, and
consistent with the system design basis;
- plant equipment calibration was correct, accurate, and properly documented;
- as-left setpoints were within required ranges; and the calibration frequencies
were in accordance with TSs, the UFSAR, procedures, and applicable
commitments;
- measuring and test equipment calibration was current;
- test equipment was used within the required range and accuracy; applicable
prerequisites described in the test procedures were satisfied;
- test frequencies met TS requirements to demonstrate operability and reliability;
tests were performed in accordance with the test procedures and other
applicable procedures; jumpers and lifted leads were controlled and restored
where used;
- test data and results were accurate, complete, within limits, and valid;
- test equipment was removed after testing;
- where applicable for in-service testing activities, testing was performed in
accordance with the applicable version of Section XI, ASME code, and reference
values were consistent with the system design basis;
- where applicable, test results not meeting acceptance criteria were addressed
with an adequate operability evaluation or the system or component was
declared inoperable;
- where applicable for safety-related instrument control surveillance tests,
reference setting data were accurately incorporated in the test procedure;
- where applicable, actual conditions encountering high resistance electrical
contacts were such that the intended safety function could still be accomplished;
- prior procedure changes had not provided an opportunity to identify problems
encountered during the performance of the surveillance or calibration test;
- equipment was returned to a position or status required to support the
performance of its safety functions; and
- all problems identified during the testing were appropriately documented and
dispositioned in the CAP.
Documents reviewed are listed in the Attachment to this report.
23 Enclosure
This inspection constituted two routine surveillance testing samples, one in-service
testing sample, and one isolation valve inspection sample as defined in IP 71111.22,
Sections -02 and -05.
b. Findings
(1) Mispositioning of Unit 3 Control Rod G-11
Introduction: A finding of very low safety significance and associated NCV of
10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was
self-revealed for the mispositioning of a Unit 3 control rod at power.
Description: On November 15, 2009, during performance of DOS 0300-01, Control Rod
Exercise, Revision 48, control rod CRD G-11 was withdrawn by the reactor operator to
position 16 from position 14 instead of being inserted to position 12 as required by
procedure. The licensee entered DOA 0300-12, Mispositioned Control Rod, Revision
14; and DGA 7, Unpredicted Reactivity Addition, Revision 20. Control rod G-11 was
inserted back to the initial position of 14 and DOA 0300-12 was exited.
Analysis: The inspectors determined that the withdrawal of the control rod was contrary
to Technical Specification Surveillance Requirement 3.1.3.3 to insert each withdrawn
control rod at least one notch and was a performance deficiency.
The finding was determined to be more than minor because the finding was associated
with the Fuel Barrier Cornerstone attributes of human performance and configuration
control of a control rod, and affected the cornerstone objective of providing reasonable
assurance that physical design barriers protect the public from radionuclide releases
caused by accidents or events. Specifically, the operator withdrew a control rod contrary
to the expected operation of insertion. This added positive reactivity and caused an
unanticipated power increase. No thermal or power limits were exceeded.
The inspectors determined the finding could be evaluated using the SDP in accordance
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
Initial Screening and Characterization of Findings, Table 4a for the Fuel Barrier
Cornerstone. Per Table 4a any issue that involves the fuel barrier is screened as Green.
This finding had no cross-cutting aspect. The inspectors determined that the licensee
had taken every precaution possible to prevent this error in advance, in that, the licensee
has briefed the evolution and stationed additional personnel to ensure correct
movement. Notwithstanding, the operator moved the rod in the wrong direction.
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,
and Drawings, requires, in part, that activities affecting quality shall be prescribed by
documented instructions, procedures, or drawings, of a type appropriate to the
circumstances and shall be accomplished in accordance with these instructions,
procedures, or drawings.
Contrary to the above, on November 15, 2009, the licensee failed to perform an activity
affecting quality in accordance with the appropriate procedure during performance of
DOS 0300-01, Control Rod Exercise, Revision 48, in that, control rod CRD G-11 was
withdrawn to position 16 from position 14 instead of being inserted to position 12.
24 Enclosure
Specifically, the licensed operator moving the control rod did not follow procedure
DOS 0300-01, Step I.4.a, which stated to insert the control rod one notch. The licensee
took a series of corrective actions: control rod G-11 was inserted one notch back to the
original position and then control room operators suspended control rod movement. All
control rods were verified to be in their correct position. The operator was removed from
shift duties and the oncoming shift was briefed of the event. Because this violation was
of very low safety significance and it was entered into the licensees corrective action
program as IR 993634, this violation is being treated as an NCV, consistent with
Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000249/2009005-06)
Cornerstone: Emergency Preparedness
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
.1 Emergency Action Level and Emergency Plan Changes
a. Inspection Scope
Since the last NRC inspection of this program area, Emergency Plan Annex,
Revisions 24 and 25 were implemented based on licensee determination, in accordance
with 10 CFR 50.54(q), that the changes resulted in no decrease in effectiveness of the
Plan, and that the revised Plan continues to meet the requirements of 10 CFR 50.47(b)
and Appendix E to 10 CFR Part 50. The inspectors conducted a sampling review of the
Emergency Plan changes and a review of the Emergency Action Level (EAL) changes to
evaluate for potential decreases in effectiveness of the Plan. However, this review does
not constitute formal NRC approval of the changes. Therefore, these changes remain
subject to future NRC inspection in their entirety.
This emergency action level and emergency plan changes inspection constituted one
sample as defined in IP 71114.04-05.
b. Findings
(1) Changes to EAL HU6 Potentially Decrease the Effectiveness of the Plans without Prior
NRC Approval
Introduction: The inspectors reviewed changes implemented to the Dresden Station
Radiological Emergency Plan Annex EALs and EAL Basis. In Revision 24, the licensee
changed the basis of EAL HU6, "Fire not extinguished within 15 minutes of detection
within the protected area boundary," by adding two statements. The two changes added
to the EAL basis stated that if the alarm could not be verified by redundant control room
or nearby fire panel indications, notification from the field that a fire exists starts the
15-minute classification and fire extinguishment clocks. The second change stated the
15-minute period to extinguish the fire does not start until either the fire alarm is verified
to be valid by additional control room or nearby fire panel instrumentation, or upon
notification of a fire from the field. These statements conflict with the previous
Dresden Station Annex, Revision 23, basis statements and potentially decrease the
effectiveness of the Plans.
Description: Dresden Station Radiological Emergency Plan Annex, Revision 23,
EAL HU6, initiating condition stated, "Fire not extinguished within 15 minutes of
25 Enclosure
detection, or explosion, within the protected area boundary." The threshold values for
HU6 were, in part: 1) Fire in any Table H2 area not extinguished within 15 minutes of
Control Room notification or verification of a Control Room alarm, or 2) Fire outside any
Table H2 area with the potential to damage safety systems in any Table H2 area not
extinguished within 15 minutes of Control Room notification or verification of a Control
Room alarm. Table H2, Vital Areas, were identified as reactor building, auxiliary electric
room, control room, diesel generator rooms, 4 kilovolt emergency core cooling system
switchgear area, battery rooms, control rod drive and component cooling service water
pump rooms, turbine building cable tunnel, turbine building safe shutdown areas, and
crib house. The basis defined fire as "combustion characterized by heat and light.
Sources of smoke such as slipping drive belts or overheated electrical equipment do not
constitute fires. Observation of flame is preferred but is not required if large quantities of
smoke and heat are observed."
The basis for Revision 23, EAL HU6 thresholds 1 and 2 stated, in part, the purpose of
this threshold is to address the magnitude and extent of fires that may be potentially
significant precursors to damage to safety systems. As used here, notification is visual
observation and report by plant personnel or sensor alarm indication. The 15-minute
period begins with a credible notification that a fire is occurring or indication of a valid fire
detection system alarm. A verified alarm is assumed to be an indication of a fire unless
personnel dispatched to the scene disprove the alarm within the 15-minute period. The
report, however, shall not be required to verify the alarm. The intent of the 15-minute
period is to size the fire and discriminate against small fires that are readily extinguished
(e.g., smoldering waste paper basket, etc.).
Revision 24 of the Dresden Station Radiological Emergency Plan Annex, changed the
threshold basis for EAL HU6 by adding the following two statements: 1) If the alarm
cannot be verified by redundant control room or nearby fire panel indications, notification
from the field that a fire exists starts the 15-minute classification and fire extinguishment
clocks, and 2) The 15-minute period to extinguish the fire does not start until either the
fire alarm is verified to be valid by utilization of additional control room or nearby fire
panel instrumentation, or upon notification of a fire from the field."
The two statements added to the basis in Revision 24 conflict with the Revision 23
threshold basis and initiating condition. The changed threshold basis in Revision 24
could add an indeterminate amount of time to declaring an actual emergency until a
person responded to the area of the fire and made a notification to the control room of a
fire in the event that redundant control room or nearby fire panel indications were not
available.
Pending further review and verification by the NRC to determine if the changes to
EAL HU6 threshold basis potentially decreased the effectiveness of the Plans, this issue
was considered an Unresolved Item. (URI 05000237/2009005-07)
26 Enclosure
2. RADIATION SAFETY
Cornerstone: Occupational Radiation Safety
2OS1 Access Control to Radiologically Significant Areas (71121.01)
.1 Plant Walkdowns and Radiation Work Permit Reviews
a. Inspection Scope
The inspectors reviewed licensee controls and surveys in the following radiologically
significant work areas within radiation areas, high radiation areas, and airborne
radioactivity areas in the plant to determine if radiological controls including surveys,
postings, and barricades were acceptable:
- Drywell Nuclear Instrumentation System Maintenance;
- Drywell In-Service Inspection;
- Drywell Control Rod Drive System Maintenance and Support.
The inspectors walked down and surveyed (using an NRC survey meter) these areas to
verify that the prescribed RWP, procedure, and engineering controls were in place; that
licensee surveys and postings were complete and accurate; and that air samplers were
properly located.
This sample was documented and credited in Inspection Report 05000237/2009003;
05000249/2009003; therefore, this review does not represent a sample.
b. Findings
No findings of significance were identified.
.2 Radiation Worker Performance
a. Inspection Scope
During job performance observations, the inspectors evaluated radiation worker
performance with respect to stated radiation safety work requirements. The inspectors
evaluated whether workers were aware of any significant radiological conditions in their
workplace, of the RWP controls and limits in place, and of the level of radiological
hazards present. The inspectors also observed worker performance to determine if
workers accounted for these radiological hazards.
This sample was documented and credited in Inspection Report 05000237/2009003;
05000249/2009003; therefore, this review does not represent a sample.
b. Findings
No findings of significance were identified.
27 Enclosure
2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)
.1 Inspection Planning
a. Inspection Scope
The inspectors reviewed plant collective exposure history, current exposure trends, and
ongoing and planned activities in order to assess current performance and exposure
challenges. The inspectors reviewed the plants current 3-year rolling average for
collective exposure in order to help establish resource allocations and to provide a
perspective of significance for any resulting inspection finding assessment.
This inspection constituted one required sample as defined in IP 71121.02-5.
b. Findings
No findings of significance were identified.
.2 Radiological Work Planning
a. Inspection Scope
The inspectors evaluated the licensees list of work activities ranked by estimated
exposure that were in progress and reviewed the following three work activities of
highest exposure significance:
- Drywell Nuclear Instrumentation System Maintenance;
- Drywell In-Service Inspection; and
- Drywell Control Rod Drive System Maintenance and Support.
This sample was documented and credited in Inspection Report 05000237/2008005;
05000249/2008005; therefore, this review does not represent a sample.
For these three activities, the inspectors reviewed the As-Low-As-Reasonably-
Achievable (ALARA) work activity evaluations, exposure estimates, and exposure
mitigation requirements in order to verify that the licensee had established procedures
and engineering and work controls that were based on sound radiation protection
principles in order to achieve occupational exposures that were ALARA. The inspectors
also determined if the licensee had reasonably grouped the radiological work into work
activities, based on historical precedence, industry norms, and/or special circumstances.
This sample was documented and credited in Inspection Report 05000237/2008005;
05000249/2008005; therefore, this review does not represent a sample.
b. Findings
No findings of significance were identified.
28 Enclosure
.3 Source-Term Reduction and Control
b. Inspection Scope
The inspectors reviewed licensee records to evaluate the historical trends and the
current status of tracked plant source terms. The inspectors determined if the licensee
was making allowances and had developing contingency plans for expected changes in
the source term due to changes in plant fuel performance issues or changes in plant
primary chemistry.
This inspection constituted one required sample as defined in IP 71121.02-5.
c. Findings
No findings of significance were identified.
4. OTHER ACTIVITIES
4OA1 Performance Indicator (PI) Verification (71151)
Cornerstone: Barrier Integrity
.1 Reactor Coolant System Leakage
a. Inspection Scope
The inspectors sampled licensee submittals for the reactor coolant system (RCS)
leakage performance indicator for Units 2 and 3 for the period from the fourth
quarter 2008 through the third quarter 2009. To determine the accuracy of the PI data
reported during those periods, PI definitions and guidance contained in the Nuclear
Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator
Guideline, Revision 5, were used. The inspectors reviewed the licensees operator
logs, RCS leakage tracking data, issue reports, event reports and NRC Integrated
Inspection Reports for the period of January 2009 through November 2009 to validate
the accuracy of the submittals. The inspectors also reviewed the licensees issue report
(IR) database to determine if any problems had been identified with the PI data collected
or transmitted for this indicator and none were identified. Documents reviewed are listed
in the Attachment to this report.
This inspection constituted two reactor coolant system leakage samples as defined in
IP 71151-05.
b. Findings
No findings of significance were identified.
29 Enclosure
Cornerstone: Occupational Radiation Safety
.2 Occupational Exposure Control Effectiveness
a. Inspection Scope
The inspectors sampled licensee submittals for the Occupational Radiological
Occurrences performance indicator for the period from the third quarter 2008 through the
third quarter 2009, to determine the accuracy of the PI data reported during those
periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory
Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors
reviewed the licensees assessment of the PI for occupational radiation safety to
determine if indicator related data was adequately assessed and reported. To assess
the adequacy of the licensees PI data collection and analyses, the inspectors discussed
with radiation protection staff, the scope and breadth of its data review, and the results of
those reviews. The inspectors independently reviewed electronic dosimetry dose rate
and accumulated dose alarm and dose reports and the dose assignments for any
intakes that occurred during the time period reviewed to determine if there were
potentially unrecognized occurrences. The inspectors also conducted walkdowns of
numerous locked high and very high radiation area entrances to determine the adequacy
of the controls in place for these areas. Documents reviewed are listed in the
Attachment to this report.
This inspection constituted one occupational radiological occurrences sample as defined
in IP 71151-05.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems (71152)
.1 Routine Review of Items Entered Into the CAP
a. Scope
As part of the various baseline inspection procedures discussed in previous sections of
this report, the inspectors routinely reviewed issues during baseline inspection activities
and plant status reviews to verify that they were being entered into the licensees CAP at
an appropriate threshold, that adequate attention was being given to timely corrective
actions, and that adverse trends were identified and addressed. Attributes reviewed
included: the complete and accurate identification of the problem; that timeliness was
commensurate with the safety significance; that evaluation and disposition of
performance issues, generic implications, common causes, contributing factors, root
causes, extent of condition reviews, and previous occurrences reviews were proper and
adequate; and that the classification, prioritization, focus, and timeliness of corrective
actions were commensurate with safety and sufficient to prevent recurrence of the issue.
Minor issues entered into the licensees CAP as a result of the inspectors observations
are included in the attached List of Documents Reviewed.
30 Enclosure
These routine reviews for the identification and resolution of problems did not constitute
any additional inspection samples. Instead, by procedure, they were considered an
integral part of the inspections performed during the quarter and documented in
Section 1 of this report.
b. Findings
No findings of significance were identified.
.2 Daily CAP Reviews
a. Inspection Scope
In order to assist with the identification of repetitive equipment failures and specific
human performance issues for follow-up, the inspectors performed a daily screening of
items entered into the licensees CAP. This review was accomplished through
inspection of the stations daily condition report packages.
These daily reviews were performed by procedure as part of the inspectors daily plant
status monitoring activities and, as such, did not constitute any separate inspection
samples.
b. Findings
No findings of significance were identified.
.3 Semi-Annual Trend Review
a. Inspection Scope
The inspectors performed a review of the licensees CAP and associated documents to
identify trends that could indicate the existence of a more significant safety issue.
The inspectors review was focused on repetitive equipment issues, but also considered
the results of daily inspector CAP item screening discussed in Section 4OA2.2 above,
licensee trending efforts, and licensee human performance results. Specifically, the
inspectors performed a review of the licensees corrective actions program documents
related to the areas of instrument air systems, heating, ventilation and air conditioning,
and instruments and controls. The inspectors review nominally considered IRs that
were generated in the six month period of July 2009 through December 2009, although
some examples expanded beyond those dates where the scope of the trend warranted.
In addition to reviewing the IR documents for trends, the inspectors compared their
results with issues identified in the licensees trending reports. A sample of the licensee
IRs associated with trends was reviewed for corrective action adequacy.
This review constituted a single semi-annual trend inspection sample as defined in
IP 71152-05.
b. Findings
No findings of significance were identified.
31 Enclosure
.4 In-Depth Review - Corrective Actions Associated With Tube Blockages of the Unit 2 and
Unit 3 LPCI Heat Exchangers
a. Inspection Scope
The inspectors performed a focused review of root cause report (RCR) 967008-03,
Dresden 2-1503-A, 2A Low Pressure Coolant Injection (LPCI) / Containment Cooling
Heat Exchanger (Hx) Failure to Meet Design Basis Heat Removal Capability due to
Asiatic Clam Macrofouling resulting from 2-1501-3A Valve Leakage and Subsequent
Untreated Service Water Make-up via the CCSW Keepfill Diluting the Biocide Treatment
below the Asiatic Clam Lethal Concentration, revision 0, to evaluate the corrective
actions that the licensee had taken to address the introduction of Asiatic clam relics into
the containment cooling heat exchangers.
Containment cooling is the operating mode of the low pressure coolant injection (LPCI)
subsystem initiated to cool the containment in the event of a loss-of-coolant accident
(LOCA). Each containment cooling subsystem consists of two LPCI pumps, one
containment cooling Hx (also called LPCI Hx), one drywell spray header and a separate
suppression chamber spray header. Heat exchanger cooling water is provided by two
containment cooling service water (CCSW) pumps in each containment cooling
subsystem. The water source for the CCSW pumps is the cribhouse, specifically
Bay 13. If the heat exchanger is significantly fouled, then the Hx may be unable to
remove sufficient heat from the containment, which could result in primary containment
failure.
In addition, the inspectors performed a focused review to evaluate the licensees
assessment of a number of IRs related to the failure to meet biocide residual
concentration after chemical addition into the containment cooling service water system.
The inspectors reviewed these issues to determine if the licensee has taken adequate
corrective actions both individually and collectively. This review constituted one sample
as defined in IP 71152.
The inspectors reviewed several documents that are listed in the Attachment of the
report.
Issues
(1) Effectiveness of Problem Identification
The licensees thermal performance testing of the LPCI heat exchangers has been
effective in identifying heat exchanger degradation prior to the Hx becoming inoperable.
On September 18, 2009, a thermal performance test was performed on the 2A LPCI Hx.
The test results indicated a heat removal capability of 67.49 MBtu/hr, which was
4.9 percent below the design heat removal rate of 71 MBtu/hr at design conditions per
the updated final safety analysis report (UFSAR) Table 6.2-3b, Heat Exchanger Heat
Transfer Rate. This issue was documented in IR 967008. Further evaluation
determined that with a heat removal capability of 67.49 MBtu/hr the new maximum
allowable inlet water temperatures for the 3 months following the test performed on
September 18, were 90.2 degrees F, 89.7 degrees F and 88 degrees F, respectively.
Actual CCSW temperatures for the time period, including previous summer months,
were below the design basis parameter of 95 degrees F, therefore, the licensee
32 Enclosure
determined that the 2A LPCI Hx, although degraded, was able to perform the required
design functions. Also, the licensee reviewed the results for the most recent thermal
performance tests performed for the other three heat exchangers and based on these
results the licensee determined that the heat exchangers were operable.
On November 5, 2009, the 2A LPCI Hx was opened for inspection and cleaning.
Approximately 50 percent of the 1256 CCSW inlet tubes were partially or fully
obstructed. The primary macrofouling mechanism was Asiatic clam relics coupled with
silt microfouling. Issue report 989609, D2R21 Inspection Results for 2A LPCI
Heat Exchanger, was generated to document the as-found condition. The 2A LPCI Hx
was cleaned and the thermal performance testing was re-performed in December 2009.
The new test results indicated a heat removal capability of 78.08 MBtu/hr at design
conditions which is 10 percent above the design heat removal rate.
(2) Prioritization and Evaluation of Problems
The licensees evaluation of the cause of the repetitive LPCI Hx blockages and
prioritization of corrective actions were ineffective. This was the third blockage of a LPCI
Hx by Asiatic clams. The first event occurred on the 3B LPCI Hx in September of 2006.
At that time the build up of Asiatic clams was thought to be due to a change in the
frequency of Bay 13 cleaning. The second event took place in March 2008, when the 3B
LPCI Hx failed its thermal performance test (70.586 vice 71 MBtu/hr). Root Cause
Report 776598-08, Dresden 3-1503-B, 3B Low Pressure Coolant Injection (LPCI) /
Containment Cooling Heat Exchanger (HX) Failure to Meet Design Basis Heat Removal
Capability Due to Inadequate Programmatic Control of Macrofoulants, revision 0,
attributed the failure of the 3B LPCI Hx to meet the design basis heat removal capability
to inadequate programmatic control of macrofoulants. Specifically, the licensee failed to
inject biocide into the containment cooling service water pumps' intake during normally
scheduled operability surveillances and sample to verify biocide residual concentration.
This was contrary to the licensees Generic Letter 89-13 Program commitments (refer to
inspection report 05000237/2008-005; 05000249/2008-005 Section 1R15 for more
details). Corrective actions included injection of biocide into the containment cooling
service water pumps' intake (e.g., Bay 13) during normally scheduled surveillances and
sample to verify biocide residual concentration.
Root cause report 776598-08 was revised on January 9, 2009. Revision 1 included an
additional causal factor which stated that a potential existed for a significant section of
the CCSW pump discharge piping to not receive a lethal biocide concentration for the
required contact time to ensure a 100 percent mortality rate for the control of
macrofoulants. This was due to the leak-by of the 2(3)-1501-3A(B), Unit 2(3) LPCI Hx
A(B) tube side discharge motor operated valves (MOVs). If leakage past these valves
occurs, then the untreated service water CCSW keepfill (strained river water) will supply
an equivalent volume of makeup water into the CCSW pump common discharge header
and result in the dilution of any chemical biocide present in the piping. This portion of
the pipe is located upstream of the LPCI Hxs and it is in this portion of the pipe where
the licensee postulates the Asiatic clams are growing and eventually getting transported
to the Hxs.
On May 22, 2009, RCR 776598-08 was revised again. Revision 2 added action
number 776598-50 to track a Unit 2(3) biocide chemical injection configuration change to
completion. This configuration change shall inject biocide into the CCSW keepfill service
33 Enclosure
water to eliminate biocide dilution resulting from leak-by of the 2-1501-3A, 2-1501-3B,
3-1501-3A and 3-1501-3B valves. This configuration change is schedule to be installed
in April 2010 on Unit 2 and May of 2010 on Unit 3. The purpose of this new biocide
injection skid is to eliminate the Asiatic clam population residing in the Unit 2 and Unit 3
CCSW piping.
The inspectors inquired why there was such a long lead time for the injection skid
modification. Through discussions with engineering management in December 2009, it
became clear that the modification was thought to be for budgetary reasons only, and
that the skid was to reduce the amount, and therefore the cost, of biocide that was being
injected. Engineering management thought that sufficient amounts of biocide were
being injected to adequately kill the Asiatic clams in the piping even though root cause
report 776598-08, revision 1 dated January 9, 2009, stated that an additional causal
factor potential existed for a significant section of the CCSW pump discharge piping to
not receive a lethal biocide concentration for the required contact time to ensure a
100 percent mortality rate for the control of macrofoulants.
(3) Effectiveness of Corrective Actions to Preclude Repetition
From January through September 2009, the licensee failed to take corrective actions to
prelude repetition of a condition meeting the licensee's definition of a significant
condition adverse to quality, associated with both Unit 2 and Unit 3 CCSW systems
which affected the performance of the LPCI heat exchangers. Specifically, the licensee
failed to provide a sufficient Asiatic clam lethal concentration of 8 PPM for the required
minimum 18 hour2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> contact time to ensure a 100 percent mortality rate for Asiatic clams
which was necessary to ensure that the heat exchangers continued to meet their design
basis heat removal requirements. The failure to perform these actions caused the
blocking of the 2A LPCI Hx tubes by Asiatic clams which resulted in the degraded
thermal performance of the Hx. Licensee planned corrective actions include the
installation of a temporary modification to provide temporary keepfill that is expected to
provide better chemical treatment of the CCSW piping upstream of the LPCI Hxs. This
violation was determined to be of very low safety significance because even though the
2A LPCI Hx was degraded it was able to perform the required design safety function.
b. Findings
The inspectors determined that the failure to take corrective action to preclude repetition
of heat exchanger blockage by providing a sufficient Asiatic clam lethal concentration of
8PPM for the required minimum 18 hour2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> contact time to ensure a 100 percent mortality
rate was a licensee-identified violation and is documented in Section 4OA7 of this report.
4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)
.1 (Closed) Licensee Event Report (LER) 05000237/2009-001-00; 05000249/2009-001-00,
Common Mode Failure of Reactor Building Isolation Dampers
This event, which occurred on February 6, 2009, was identified as a result of a licensee
review of failures of reactor building ventilation isolation dampers at Dresden and
another Exelon facility. Licensee failure analysis determined the damper failure
mechanism to be the result of inadequate lubrication of internal parts and installation of
upgraded solenoid valves that was completed in January of 2009. The NRC identified
34 Enclosure
the slow response to identifying the common mode failure and failure to write trending
condition reports to document the adverse trend. Inspectors verified replacement
solenoid valves continued to perform correctly and other corrective actions put in place
were appropriate to correct the procedural non-compliance issues. Documents reviewed
as part of this inspection are listed in the Attachment to this report. A NCV was written in
inspection report 05000237/2009002; 05000249/2009002 as05000237/2009002-04.
This LER is closed.
This event follow-up review constituted one sample as defined in IP 71153-05.
.2 (Closed) LER 249/2009-001-00, Unit 3 Group 1 Isolation and Automatic Reactor Scram
a. Inspection Scope
The inspectors reviewed LER 249/2009-001-00, Unit 3 Group 1 Isolation and Automatic
Reactor Scram, to ensure that the issues documented in the report were adequately
addressed in the licensees corrective action program. The inspectors interviewed plant
personnel and reviewed operating and maintenance procedures to ensure that generic
issues were captured appropriately. The inspectors reviewed operator logs, issue
reports, the Updated Final Safety Analysis Report, and other documents to verify the
statements contained in the LER. This LER is closed.
This event follow-up review constituted one sample as defined in IP 71153-05.
b. Findings
Introduction: A finding of very low significance (Green) involving a NCV of TS 5.4.1 was
self-revealed when Unit 3 experienced an automatic reactor scram and Group 1 primary
containment isolation signal (PCIS) when operators were restoring the reactor water
cleanup (RWCU) system with the reactor at pressure. Station procedure DOP 1200-03,
RWCU System Operation with the Reactor at Pressure, Revision 51, failed to identify
the correct position of motor operated valve (MOV), 3-1201-7, RWCU System Return to
Reactor. This procedural deficiency caused a pressure pulse that resulted in a reactor
water level Low-Low Group 1 Isolation Signal and Unit 3 reactor scram.
Description: On October 3, 2009, Unit 3 experienced an automatic reactor scram and
Group 1 PCIS. Due to the Group 1 PCIS, the inboard and outboard main steam
isolation valves closed as designed. In addition, PCIS Group 2 and Group 3 isolations
were received and verified complete. Operators manually initiated the isolation
condenser to control reactor pressure within limits.
The RWCU system had tripped earlier on October 2, 2009. On October 3, 2009, prior to
the reactor scram, operators were restoring the reactor water cleanup system per station
procedure DOP 1200-03, RWCU System Operation with the Reactor at Pressure,
Revision 51. Per the procedure, RWCU was being filled and heated in the blowdown
mode with a flow path from the reactor pressure vessel (RPV) to the main condenser.
While the fill was being performed, the 3-1201-7 valve, Unit 3 RWCU System Return to
Reactor, was closed. Reactor water cleanup system operation in the blowdown mode
with the 3-1201-7 valve closed resulted in: (1) heat up and expansion of the water
volume upstream of the 3-1201-7 valve (area of high pressure), and (2) cooling and
35 Enclosure
contraction of the water volume downstream of the 3-1201-7 valve (area of low
pressure). This condition created a high differential pressure across the valve.
A root cause investigation determined that under these conditions, when the 3-1201-7
valve was opened, the pressurized water upstream of the valve flashed to steam in the
lower pressure region downstream of the valve. The resulting pressure pulse was
sensed by the RPV level transmitters, resulting in a Reactor Water Level Low SCRAM
Signal and Reactor Water Level Low-Low Group 1 Isolation Signal.
The licensee determined that the probable cause for the pressure pulse initiating the
Reactor Water Level Low-Low Group 1 Isolation Signal and Unit 3 Reactor SCRAM was
a latent procedural deficiency. DOP 1200-03 provided inadequate guidance for the
3-1201-7 valve position during system startup with the RPV at pressure. In GEK-32399,
Dresden 3 Instrumentation Subsystem of the Reactor Water Cleanup System,
Section 3-11, Normal Operation, Table 3-6, Valve Positions for Cleanup System
Startup during Normal Operations, the reactor vendor, General Electric, recommended
that the Reactor Return Isolation Valve 1201-7 be in the open position for RWCU system
startup when the reactor is at power. This recommendation was not incorporated in
DOP 1200-03. Procedure DOP 1200-03, step G.1.g.(2) , gave the option to the operator
to open MOV 3-1201-7 at that step or later on in the procedure. During this event, the
3-1201-7 valve was opened later on in the procedure.
Analysis: The inspectors determined that the licensees failure to include pertinent
information regarding valve position during RWCU system startup with the RPV at
pressure in DOP 1200-03 was a performance deficiency warranting a significance
evaluation. Using IMC 0612, Appendix B, Issue Screening, issued on
December 4, 2008, the inspectors determined that this finding was more than minor
because it impacted the Initiating Events Cornerstone objective to limit the likelihood of
those events that upset plant stability and challenge critical safety functions during
shutdown as well as at power operations. The failure to maintain adequate procedures
for the restoration of systems can result in events (i.e., reactor scram) that upset plant
stability. This condition caused a pressure pulse that was sensed by the RPV level
transmitters, resulting in a Reactor Water Level Low SCRAM Signal and Reactor Water
Level Low-Low Group 1 Isolation Signal. This finding had a cross-cutting aspect in the
area of Human Performance Resources because the licensee did not provide complete,
accurate and up-to-date procedures to plant personnel. H.2(c)
The inspectors completed a Phase 1 significance determination of this issue using
IMC 0609, Significance Determination Process, Attachment 0609.04, dated
January 10, 2008. The inspectors determined that the finding impacted the Initiating
Events Cornerstone. The inspectors answered No to the question on Transient
Initiators under the Initiating Events Cornerstone column on Table 4a because the
finding did not contribute to both the likelihood of a reactor trip AND the likelihood that
mitigating equipment or functions will not be available. Therefore, the issue screened as
having very low safety significance (Green).
Enforcement: The inspectors determined that the licensees failure to include pertinent
information, regarding valve position during RWCU system startup with the RPV at
pressure, in DOP 1200-03 was a violation of Dresden Nuclear Power Station Technical
Specification Section 5.4.1, Procedures. Section 5.4.1 states, in part, that written
procedures shall be established, implemented, and maintained covering applicable
36 Enclosure
procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, issued
February 1978. Procedures addressing startup of boiling water reactor (BWR) systems,
including the reactor cleanup system, are recommended in Section 4. of Appendix A to
this Regulatory Guide.
Contrary to the above, on October 3, 2009, the licensee failed to include pertinent
guidance regarding 3-1201-7 valve position during system startup with the RPV at
pressure. This failure resulted in an automatic reactor scram and Group 1 primary
containment isolation signal. This event was entered into the licensees corrective action
program as IR 974426, U3 Group 1 Isolation and Reactor Scram. Corrective actions
by the licensee included revising procedure DOP 1200-03, requiring the 3-1201-7 valve
to be open prior to initiating RWCU system fill and vent activities. Because this violation
was of very low safety significance and it was entered into the licensees corrective
action program, this violation is being treated as a NCV, consistent with Section VI.A.1 of
the NRC Enforcement Policy. (NCV 05000249/2009005-08)
.3 (Closed) Licensee Event Report (LER) 05000237/2009-003-00; 05000249/2009-003-00,
Emergency Diesel Generator Oil Leak and Unresolved Item (URI)05000237/2009003-01; 05000249/2009003-01, Failure of 2/3 Emergency Diesel
Generator Due to Lube Oil Leak on Y Strainer
This event, which occurred on June 2, 2009, during performance of the monthly
surveillance on the Unit 2/3 Emergency Diesel Generator (EDG), resulted in an oil leak
of approximately one-half gallon per minute from the turbocharger lubricating oil Y
strainer end cap plug. The initial event was documented in Section 1R12 of report
05000237/2009003; 05000249/2009003 as an Unresolved Item
(URI 05000237/2009003-01; 05000249/2009003-01.)
Documents reviewed as part of this inspection are listed in the Attachment to this report.
Both the above referenced URI and this LER are closed.
This event follow-up review constituted one sample as defined in IP 71153-05.
Introduction: A finding of very low safety significance and associated NCV of
10 CFR Part 50, Appendix B, Criterion IV, Procurement Document Control, was
self-revealed for the failure to ensure a safety-related plug was ordered and installed
where required in the 2/3 EDG turbo lube oil Y strainer.
Description: On June 02, 2009, the 2/3 EDG was operating in support of the monthly
surveillance run in accordance with DOS 6600-01, Diesel Generator Surveillance
Tests. At approximately 3:39 am the 2/3 EDG was 25 minutes into the loaded run when
an oil leak of approximately 1/2 gallon per minute was identified at the Turbo Lube Oil
System Y strainer.
The 2/3 EDG was secured at approximately 3:47 a.m., and the turbo oil circulating pump
was secured approximately 45 minutes after the engine shutdown to allow heat removal
from the engines turbo charger to prevent damage. Inspection of the turbo lube oil
system Y strainer identified the source of the leakage to be coming from a pipe plug on
the Y strainer end cap. Further investigation revealed the pipe plug installed in the
strainer end cap to be a black 3/8 inch NPT plastic shipping plug instead of the
safety-related steel plug required by design documents.
37 Enclosure
As immediate corrective action, the licensee installed a 3/8 inch NPT ASTM A-105
carbon steel hex head threaded pipe plug, Cat ID 43255-1 in the strainer end cap of the
2/3 EDG using work order (WO) 1240346-01 and approximately 30 gallons of oil were
added to the engine reservoir. Surveillance procedure DOS 6600-01, Diesel Generator
Surveillance Tests, was completed satisfactorily with no leakage observed from the
Turbo Lube Oil System Y strainer. The 2/3 EDG was declared operable at 11:05 p.m.
on June 2, 2009. Extent of condition reviews were performed on the four other similar
diesel generators; two safety-related and two station blackout emergency diesels.
No other non-conforming conditions were identified.
During the subsequent root cause investigation, the licensee determined that the
Unit 2/3 EDG Turbo Lube Oil Y Strainer (EPN 2/3-6661) and Circulating Oil Y Strainer
(EPN 2/3-6672) were replaced on March 24, 2008, under WO 922770-01 due to wear on
the strainer blowdown caps. On March 24, 2008, the licensee completed steps 8, 9
and 10 of WO 922770-01. This work scope removed the old lube oil strainer 2/3-6661
from the system, cleaned piping and pipe nipples prior to installing the strainer
(replacing pipe nipples as required), and installed the new Mueller strainer snug tight
using site approved sealant. On March 25, 2008, the license performed step 11 of the
work package requiring the strainers to be painted with designated orange paint once
the strainers have been installed. The painting step was important because from this
step on there is no way to visually identify the non-conforming condition. Interviews with
the individual performing the installation and painting indicated that they did not identify
the plug as a plastic foreign material exclusion (FME) plug and therefore took no action
to replace it as was required by procedure MA-AA-716-008, Foreign Material Exclusion
Program.
The post-maintenance test (PMT) was performed on the Y strainers on
March 27, 2008, per WO 922770-02. The licensee performed visual inspections of the
Y strainers at system pressure. The inspections passed with no identified leakage.
Subsequent investigation revealed that Turbo Lube Oil Strainer replaced under
WO 922770-01 in March 2008 was assigned Exelon Catalog Identification
Number 38412-1. The Y strainer was manufactured commercial grade by Mueller
Steam Specialty under Model No. 352M. Exelon purchased the Y strainer from
Engine Systems Incorporated (ESI) under Purchase Order (PO) 00000703 Revision 001
as a Quality Level 1 Nuclear Safety-Related Item. The PO stated, Strainer, Y-Type,
1 IN, Bronze ASTM B62, Threaded (FNPT), Class 250, 20 Mesh Size Stainless Steel
Screen, supplied with threaded gasketed cap and plug; and rated for 400 PSI @ 150 F
(WOG); and seismically qualified per Report Number ST-MSS-352M-1 issued by ESI.
The Mueller Steam Specialty catalog Cut Sheet that was pasted in the supply database
for CAT ID 38412-1 on July 3, 2006, indicated Y strainer Blowoff Outlets are
unplugged. Additionally, the current Mueller Steam Specialty online specification sheet
for Y Strainers (ES-MS-351M-358) states Blow Off Outlets: Not normally furnished
with plug. Plug available, specify with order.
Since the part number specified by Dresden in the procurement document does not
include a plug in the end cap, Engine Systems Incorporated (ESI) included the plastic
plug for FME purposes. The plug is black only because that was the color that ESI had
on hand at the time. Personnel from ESI stated that when performing the qualification
testing for the part two strainers are ordered, one for the testing and one to ship to the
customer. An appropriate plug is installed in the one used for qualification testing.
38 Enclosure
The strainer purchased for WO 922770-01 was shipped to Dresden Site Supply and had
a receipt inspection performed on December 19, 2007. The inspection accepted the
strainer with no discrepancies noted in the Quality Receipt Inspection Package and
without questioning if the plug installed in the strainer end cap should have been a
suitable pressure retaining pipe plug or a shipping plug.
The licensee concluded from their investigation that the root cause for this issue was the
failure to have a purchase order that clearly documented the need for the safety-related
strainer cap plugs.
Analysis: The inspectors determined that the failure to document the requirement for a
safety-related strainer cap plug in the purchase order was a performance deficiency.
The finding was determined to be more than minor because the finding was similar to
IMC 0612, Appendix E, Example 5 c, in that, an incorrect and inadequate part was
installed and the system was returned to service. Therefore, this performance deficiency
also impacted the Mitigating Systems Cornerstone objective to ensure the availability,
reliability, and capability of systems that respond to initiating events to prevent
undesirable consequences.
The inspectors determined the finding could be evaluated using the SDP in accordance
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
Initial Screening and Characterization of Findings, Table 4a, dated January 10, 2008,
for Mitigating Systems because the 2/3 EDG is a mitigating system that could impact the
long term or short term decay heat removal capability during a loss of offsite power
event. The inspectors answered yes to the question, Does the finding represent
actual loss of safety function of a single train for greater than its Technical Specification
Allowed Outage Time? The inspectors performed a SDP phase 2 evaluation using the
pre-solved spreadsheet for the Risk-Informed Inspection Notebook for Dresden Nuclear
Power Station. The assumption that EDG 2/3 was unavailable for greater than 30 days
resulted in a finding of low to moderate risk significance (White). The Region III senior
reactor analyst (SRA) performed a SDP phase 3 evaluation of the EDG 2/3 failure to run.
The SRA used the Dresden Standardized Plant Analysis Risk (SPAR) Model,
Revision 3.50, and assumed that the EDG would have failed to run in response to any
demand that would have occurred since the last successful 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> endurance run.
This exposure period was approximately 89 days. The delta CDF for internal events
was estimated to be 4.0E-7/yr. The dominant sequence was a loss of offsite power
event followed by common cause failure of all emergency power and the failure to
recover either offsite or onsite power.
Since the delta CDF was greater than 1.0E-7/yr, the SRA evaluated the risk contribution
from external events. The risk contribution from seismic events was determined to be
negligible because the frequency of seismically-induced loss of offsite power events was
estimated to be much less than plant-centered, switchyard-centered, or grid-related loss
of offsite power events. The fire risk contribution was estimated using information from
the licensees Individual Plant Examination for External Events (IPEEE) submitted
in 2000. Fire-induced loss of offsite power events were assumed to occur for fires in
control room panel 902-8 (Unit 3 panel 903-8), panel 923-2, and for fires in the auxiliary
electric equipment room (AEER). The SRA used the fire ignition frequencies from the
IPEEE and calculated conditional core damage probabilities using the SPAR model for
plant-centered loss of offsite power events with the failure of the 2/3 EDG to estimate the
change in core damage frequency for fire events that did not result in control room
39 Enclosure
evacuation. Fires in the AEER contributed less than 1.0E-7/yr to the change in CDF.
For the control room, fires in panel 902-8 (903-8) were evaluated and determined to be
potential risk contributors because the fire damage caused a loss of offsite power and
resulted in the unavailability of the Division II power supplies. For panel fires that were
not suppressed within 15 minutes, the SRA used a non-suppression probability of 3.4E-3
from the licensees IPEEE and concluded that operators would evacuate the control
room and use the fire-specific safe shutdown procedures. With the 2/3 EDG unavailable
due to the performance deficiency, only the station blackout (SBO) diesel generator
would remain available to provide power. The SRA used SPAR-H to estimate the
human error probability (HEP) for aligning the SBO diesel generator during fire scenarios
and estimated a value of 0.4 assuming that diagnosis of the loss of power and need for
the SBO diesel generator would dominate the HEP. The performance-shaping factors
for stress and procedures were adjusted in the HEP calculation. The procedures for
using the SBO DG were considered to be incomplete because the Dresden fire safe
shutdown procedures do not address the use of the SBO diesel generator and operators
would be required to use separate procedures for non-fire scenarios to line-up the SBO
DG. Also, the stress of the fire-induced LOOP with failure of the 2/3 EDG was assumed
to be high. The risk contribution from control room fire scenarios was estimated to be
approximately 4.0E-7/yr. The total delta CDF from internal and external scenarios was
estimated to be approximately 8.0E-7/yr. The risk estimate is conservative because it
does not account for any successful run time of the diesel generators and provides only
limited credit for the use of SBO diesel generators in fire scenarios.
The risk contribution from large early release frequency (LERF) was also evaluated.
IMC 0609, Appendix H, Containment Integrity Significance Determination Process
assigns a screening LERF factor of 1.0 to station blackout core damage sequences for
BWRs with Mark I containments. This would result in a delta LERF estimate of
8.0E-7/yr, which represents low to moderate significance. However, based on a
previous Dresden phase 3 SDP evaluation and other SDP evaluations of plants with
Mark 1 containments, a much lower LERF factor of 0.1 is judged to be appropriate for
this SDP phase 3 evaluation. As a result, the risk significance of the finding is estimated
to be less than 1.0E-6/yr delta CDF and less than 1.0E-7/yr delta LERF, which
represents a finding of very low safety significance (Green).
In addition, the failure of plant maintenance personnel to identify and remove the plastic
foreign material exclusion plug prior to equipment return to service was a significant
contributor to the finding. Step 4.2.5.3.B of MA-AA-716-008, Foreign Material Exclusion
Program, states, in part, New parts/components/equipment to be installed in the plant
should be carefully inspected to ensure that no foreign material (e.g., packaging
material, shipping plugs, desiccants, and lubricant/preservatives used for shipping or
storage) are present to prevent introduction to the system. Failure of plant personnel to
question the plastic shipping plug before the equipment was installed and returned to
service was not in compliance with the procedure and, therefore, inspectors determined
that this event was cross-cutting in Human Performance, Work Practices, Procedural
Compliance for failure to follow of personnel to follow the procedure. H.4(b)
Enforcement: 10 CFR Part 50, Appendix B, Criterion IV, Procurement Document
Control, requires, in part, that measures shall be established to assure that applicable
regulatory requirements, design bases, and other requirements which are necessary to
assure adequate quality are suitably included or referenced in the documents for
40 Enclosure
procurement of material, equipment, and services, whether purchased by the applicant
or by its contractors or subcontractors.
Contrary to the above, from December 2007 until June 2009, the licensee did not include
a requirement which was necessary to assure adequate quality in the document for
procurement of the 2/3 EDG Turbo Lube Oil Y Strainer, CAT ID 38412-1. Specifically,
the purchase order did not specify what type of plug was required to be supplied and
installed in the strainer cap prior to installation. The strainer was supplied with a plug
installed that was neither designed nor constructed sufficiently to prevent a leak that
resulted in the inoperability of the 2/3 EDG for greater than 30 days. Immediate
corrective action to correct the leak included installation of a qualified plug in the strainer,
post-maintenance testing of the 2/3 EDG, and inspection of all other diesel generators to
ensure the same condition did not exist on another machine. The catalogue ID was
revised to include a pressure retaining pipe plug with approved material and a
requirement was added for a quality inspection to be performed to inspect the strainer
for metallic pipe plug in blow down port. Individual procedure compliance issues were
addressed through the stations performance improvement initiatives. Because this
violation was of very low safety significance and it was entered into the licensees
corrective action program as IR 926605, this violation is being treated as an NCV,
consistent with Section VI.A.1 of the NRC Enforcement Policy.
(NCV 05000237/2009005-09; 05000249/2009005-09)
.4 Electro-Hydraulic Control (EHC) Fluid Leaking From Stop Valve 3-5699-MSV4-FA
Resulting in Forced Outage D3F49
a. Inspection Scope
The inspectors reviewed the plants response to an EHC leak on Dresden Unit 3 that
caused the unit to come offline. Documents reviewed in this inspection are listed in the
Attachment to this report.
This event follow-up review constituted one sample as defined in IP 71153-05.
b. Findings
Introduction: The inspectors identified an unresolved item regarding the regulatory
requirements associated with the circumstances surrounding the Unit 3 turbine trip on
November 6, 2009.
Description: On November 5, 2009, at 8:53 p.m., Unit 3 Control Room received the
following alarm: 903-7 B-6, EHC [electro-hydraulic control] RESERVOIR LVL HI/LO
(reference IR 989641) indicating a rate of change in the EHC reservoir at 1.3" in 100 hrs
or greater. A non-licensed operator (NLO) was dispatched to stage a barrel of EHC fluid
for addition. Preparations were made for a heater bay entry to look for leaks.
A Unit 3 heater bay entry was made and it was determined that the Unit 3 Main Turbine
Stop Valve (MSV) # 4 had an EHC leak from the fast-acting solenoid valve
(3-5699-MSV4-FA). The leak was determined to be approximately 4-5 gallons of fluid
per hour. A report from the field was that reservoir level had dropped about 1.1" in the
last 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Between 12:50 a.m. and 3:43 a.m. on November 6, 2009, the licensee
added two barrels of EHC fluid to the EHC reservoir.
41 Enclosure
On November 6, 2009, between 9:00 a.m. and 2:00 p.m., licensee management
conducted meetings regarding the repair of the leak on MSV #4. The plan called for
starting to down power Unit 3 to 650 Mwe for a planned 3:00 p.m. entry into the heater
bay to repair the valve. The decision to go to 650 Mwe was to reduce the dose rate in
the area and extend stay time for the repair.
At approximately 3:00 p.m., while staging for entry to repair the leak, Operations
personnel informed the NLO, staged to isolate the oil supply to the leaking valve, that
level in the EHC reservoir was dropping quickly, and requested the NLO to enter the
pipeway as soon as possible.
At approximately 3:05 p.m., the NLO observed oil spraying profusely from the bottom
area of #4 Main Stop Valve and the area of the solenoid that was going to be changed
out. The NLO immediately contacted the control room to report what was observed and
a decision was made to take the turbine offline. At 3:32 p.m., the Unit 3 Turbine was
tripped.
The licensee had not completed their root cause investigation by the end of the
inspection period. The inspectors planned to review the root cause investigation to
determine if there were any violations of NRC requirements and that appropriate
corrective actions were applied. (URI 05000249/2009005-10)
4OA5 Other Activities
.1 Quarterly Resident Inspector Observations of Security Personnel and Activities
a. Inspection Scope
During the inspection period, the inspectors conducted observations of security force
personnel and activities to ensure that the activities were consistent with licensee
security procedures and regulatory requirements relating to nuclear plant security.
These observations took place during both normal and off-normal plant working hours.
These quarterly resident inspector observations of security force personnel and activities
did not constitute any additional inspection samples. Rather, they were considered an
integral part of the inspectors' normal plant status review and inspection activities.
b. Findings
No findings of significance were identified.
.2 Institute of Nuclear Power Operations (INPO) Plant Assessment Report Review
a. Inspection Scope
The inspectors reviewed the interim report for the INPO plant assessment of Dresden
Station conducted in September 2009. The inspectors reviewed the report to ensure
that issues identified were consistent with the NRC perspectives of licensee
performance and to verify if any significant safety issues were identified that required
further NRC follow-up.
42 Enclosure
b. Findings
No findings of significance were identified.
.3 Open) NRC TI 2515/177, Managing Gas Accumulation in Emergency Core Cooling,
Decay Heat Removal and Containment Spray Systems (NRC Generic Letter 2008-01)
a. Inspection Scope
On November 10, 2008, the inspectors conducted a walkdown of the Unit 2 High
Pressure Coolant Injection (HPCI) discharge piping inside the Unit 2 X-Area in sufficient
detail to reasonably assure the acceptability of the licensees walkdowns (TI 2515/177,
Section 04.02.d). The inspectors also verified that the information obtained during the
licensees walkdown was consistent with the items identified during the inspectors
independent walkdown (TI 2515/177, Section 04.02.c.3).
The inspectors verified that Piping and Instrumentation Diagrams (P&IDs) accurately
described the subject system, that the P&IDs were up-to-date with respect to recent
hardware changes, and any discrepancies between as-built configurations and the
P&IDs were documented and entered into the CAP for resolution (TI 2515/177, Section
04.02.b).
In addition, the inspectors reviewed the licensees isometric drawings that describe the
HPCI system configurations to verify that the licensee had acceptably confirmed the
accuracy of the drawings (TI 2515/177, Section 04.02.a). The inspectors considered the
following related to the isometric drawings:
- High point vents were identified.
- High points that do not have vents were acceptably recognizable.
- Other areas where gas can accumulate and potentially impact subject system
operability, such as at orifices in horizontal pipes, isolated branch lines, heat
exchangers, improperly sloped piping, and under closed valves, were acceptably
described in the drawings or in referenced documentation.
- Horizontal pipe centerline elevation deviations and pipe slopes in nominally
horizontal lines that exceed specified criteria were identified.
- All pipes and fittings were clearly shown.
- The drawings were up-to-date with respect to recent hardware changes and that
any discrepancies between as-built configurations and the drawings were
documented and entered into the CAP for resolution.
The licensee indicated that even though they possess isometric drawings of the HPCI
system, they do not rely upon any isometric drawings for gas management in that
system. Therefore, the inspectors were unable to verify the above considerations.
In their review, the inspectors did identify discrepancies in the available isometric
drawings between what was shown on the drawing and the as-built condition of the
system. The discrepancies identified were in drawings M-1151C-2 and ISI-510 Sheet 2
and were associated with the 2-23126-3/4-L vent line. The licensee determined that
drawing M-1151C-2 does not need to be updated because it was created to support a
seismic analysis done before the 2-23126-3/4-L vent line was installed and was not
intended to be updated. They determined that drawing ISI-510 Sheet 2 does not need to
43 Enclosure
be updated because it is a system pressure testing walkdown isometric drawing,
therefore, the discrepancy does not impact the purpose and use of the drawing. These
conclusions were documented in AR 1014280.
Documents reviewed are listed in the Attachment to this report.
This inspection effort counts towards the completion of TI 2515/177, which will be closed
in a later Inspection Report.
b. Findings
No findings of significance were identified.
4OA6 Management Meetings
.1 Exit Meeting Summary
On January 14, 2010, the inspectors presented the inspection results to Mr. T. Hanley,
and other members of the licensee staff. The licensee acknowledged the issues
presented. The inspectors confirmed that none of the potential report input discussed
was considered proprietary.
.2 Interim Exit Meeting
Interim exits were conducted for:
- The results of the inservice inspection with Site Vice-President T. Hanley on
November 13, 2009.
- The results of the As-Low-As-Reasonably-Achievable Planning and Controls
inspection with the Site Vice President, Mr. T. Hanley, on November 17, 2009.
- The annual review of Emergency Action Level and Emergency Plan changes
with the licensee's Emergency Preparedness Manager, Mr. P. Quealy, via
telephone on December 21, 2009.
The inspectors confirmed that none of the potential report input discussed was
considered proprietary.
4OA7 Licensee-Identified Violations
The following violation of very low safety significance (Green) was identified by the
licensee and is a violation of NRC requirements which meets the criteria of Section
VI.A.1 of the NRC Enforcement Policy, for being dispositioned as an NCV.
- Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Criterion XVI,
Corrective Action, states, in part, Measures shall be established to assure that
conditions adverse to quality, such as failures, malfunctions, deficiencies,
deviations, defective material and equipment, and non-conformances are
promptly identified and corrected. In the case of significant conditions adverse to
quality, the measures shall assure that the cause of the condition is determined
and corrective action taken to preclude repetition. A significant condition
adverse to quality for both Unit 2 and Unit 3 containment cooling service water
44 Enclosure
(CCSW) systems was identified by the licensee in RCR 776598-08,
Dresden 3-1503-B, 3B Low Pressure Coolant Injection (LPCI) / Containment
Cooling Heat Exchanger (HX) Failure to Meet Design Basis Heat Removal
Capability Due to Inadequate Programmatic Control of Macrofoulants,
Revision 1, on January 9, 2009. Procedure LS-AA-125, Corrective Action
Program (CAP) Procedure, revision 13, defines significant condition adverse to
quality (SCAQ), in part, as A condition which, if left uncorrected, could have a
serious effect on safety or reliability. In addition, recurring deficiencies or errors
that cannot be dispositioned or brought into conformance by established
corrective action systems," are considered SCAQs. The inspectors determined
that the conditions described in RCR 776598-08, met the licensee's definition of
a significant condition adverse to quality. Contrary to the above requirements,
from January through September 2009, the licensee failed to take measures to
assure that the cause of the condition (blockage of the LPCI heat exchangers)
was determined and corrective action taken to preclude the repetition for a
significant condition adverse to quality on both Unit 2 and Unit 3 CCSW systems.
Specifically, the licensee failed to prevent the recurrence of Asiatic clam
blockage in the 2A LPCI Hx tubes which resulted in the degraded thermal
performance of the Hx. Licensee planned corrective actions included installation
of a temporary modification to provide temporary keepfill that was expected to
provide better chemical treatment of the CCSW piping upstream of the LPCI Hxs,
and a permanent injection skid for biocide to provide for long term assurance of
effective chemical treatment. This violation was determined to be of very low
safety significance because even though the 2A LPCI Hx was degraded it was
able to perform the required design safety function.
ATTACHMENT: SUPPLEMENTAL INFORMATION
45 Enclosure
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
T. Hanley, Site Vice President
S. Marik, Station Plant Manager
H. Bush, Radiation Protection Manager
B. Casey, Engineering Programs (Braidwood)
H. Do, Exelon Corporate ISI
B. Finley, Security Manager
D. Glick, Shipping Specialist
T. Green, Nondestructive Examination Services
J. Griffin, Regulatory Assurance - NRC Coordinator
D. Gronek, Operations Director
J. Hansen, Corporate Licensing
L. Jordan, Training Director
R. Kalb, Chemistry
P. Karaba, Maintenance Director
J. Kish, Engineering Programs
M. Kluge, Design Engineer
D. Leggett, Nuclear Oversight Manager
R. Laburn, Radiation Protection
M. Marchionda, Regulatory Assurance Manager
J. Miller, Nondestructive Examination Services
P. OConnor, Licensed Operator Requalification Training Lead
M. Overstreet, Lead Radiation Protection Supervisor
C. Podczerwinski, Maintenance Rule Coordinator
P. Quealy, Emergency Preparedness Manager
E. Rowley, Chemistry
R. Rybak, Regulatory Assurance
J. Sipek, Engineering Director
N. Starcevich, Radiation Protection Instrumentation Coordinator
J. Strmec, Chemistry Manager
S. Vercelli, Work Management Director
NRC
M. Ring, Chief, Division of Reactor Projects, Branch 1
R. Zuffa, Illinois Emergency Management Agency
R. Schulz, Illinois Emergency Management Agency
1 Attachment
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened:
05000237/2009005-01 NCV Operating Personnel Incorrectly Placed Clearance Tags
(Section 1R04)05000237/2009009-02 NCV NRC Inspector-Identified Control Room Alarm Isolation
Valve Out-of-Position (Section 1R15)05000237/2009005-03 NCV Preconditioning the Unit 2 Emergency Diesel Generator
Prior to Performing TS Surveillance Requirements
(Section 1R19)05000237/2009005-04 URI 2/3 Emergency Diesel Generator (EDG) Overvoltage
05000249/2009005-04 During Division I Undervoltage Surveillance (1R19)05000237/2005009-05 NCV Failure to Follow the Master Refueling Procedure During
Movement of Fuel Assembly JLU569 (Section 1R20)05000249/2009005-06 NCV Mispositioning of a Unit 3 Control Rod at Power
(Section 1R22)05000237/2009005-07 URI Changes to EAL HU6 Potentially Decreased the
Effectiveness of the Plans without Prior NRC Approval
(1EP4)05000249/2009005-08 NCV Procedural Deficiency Causing a Pressure Pulse
Resulting in a Reactor Water Level Low-Low Group 1
Isolation Signal and Unit 3 Reactor Scram
(Section 4OA3.2)05000237/2009005-09 NCV Failure to Ensure a Safety-Related Plug was Ordered and
05000249/2009005-09 Installed in the 2/3 Emergency Diesel Generator
Turbo Lube Oil Y Strainer (Section 4OA3.3)05000249/2009005-10 URI Electro-Hydraulic Control (EHC) Fluid Leaking From Stop
Valve 3-5699-MSV4-FA Resulting in Forced Outage
D3F49 (Section 4OA3.4)
Temporary Instruction 2515/177 Managing Gas Accumulation in Emergency Core Cooling,
Decay Heat Removal and Containment Spray Systems
(NRC Generic Letter 2008-01) (Section 4OA5.3)
2 Attachment
Closed:
05000237/2009005-01 NCV Operating Personnel Incorrectly Placed Clearance Tags
(Section 1R04)05000237/2009009-02 NCV NRC Inspector-Identified Control Room Alarm Isolation
Valve Out-of-Position (Section 1R15)05000237/2009005-03 NCV Preconditioning the Unit 2 Emergency Diesel Generator
Prior to Performing TS Surveillance Requirements
(Section 1R19)05000237/2005009-05 NCV Failure to Follow the Master Refueling Procedure During
Movement of Fuel Assembly JLU569 (Section 1R20)05000249/2009005-06 NCV Mispositioning of a Unit 3 Control Rod at Power
(Section 1R22)05000249/2009005-08 NCV Procedural Deficiency Causing a Pressure Pulse
Resulting in a Reactor Water Level Low-Low Group 1
Isolation Signal and Unit 3 Reactor Scram
(Section 4OA3.2)05000237/2009005-09 NCV Failure to Ensure a Safety-Related Plug was Ordered and
05000249/2009005-09 Installed in the 2/3 Emergency Diesel Generator
Turbo Lube Oil Y Strainer (Section 4OA3.3)05000237/2009004-04 URI Inspector Identified Control Room Alarm Isolation Valve
05000249/2009004-04 Out-of-Position (1R15)05000237/2009003-01 URI Failure of 2/3 Emergency Diesel Generator (EDG) Due to
05000249/2009003-01 Lube Oil Leak On Y-Strainer (4OA3.3)
05000237/2009-001-00 LER Common Mode Failure of Reactor Building Isolation
05000249/2009-001-00 Dampers (4OA3.1)
05000249/2009-001-00 LER Unit 3 Group 1 Isolation and Automatic Reactor Scram
(4OA3.2)
05000237/2009-003-00 LER Emergency Diesel Generator Oil Leak (4OA3.3)
05000249/2009-003-00
Discussed:
Inspection Report 05000237/2008005; 05000249/2008005, Section 1R15 (4OA2.4)05000237/2009002-04 NCV Failure to Take Corrective Actions to Replace a Degraded
Valve in a Timely Manner (4OA3.1)
3 Attachment
LIST OF DOCUMENTS REVIEWED
The following is a partial list of documents reviewed during the inspection. Inclusion on this list
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that
selected sections or portions of the documents were evaluated as part of the overall inspection
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
any part of it, unless this is stated in the body of the inspection report.
1R04 Equipment Alignment (71111.04)
- WO 1079566-01, Perform 250V Station Battery Service Test
- C/O 76319, (ASSY) Battery 250V U2
- DOP 7500-M1/E1, Unit 2/3 Standby Gas Treatment, Revision 6
1R05 Fire Protection (71111.05)
- IR 976782, NRC Observations from U3 Rx Bldg. 570 Pre-Plan Review
1R08 Inservice Inspection Activities (71111.08G)
- IR 00992912; Material Certification of Recirc Piping Could not be Found; November 13, 2009
- IR 00911408;Section XI Class 2 Boundary; April 28, 2009
- IR 00889729; LPCI Heat Exchanger Recordable Indications; March 6, 2009
- IR 00782956; Corrosion Pipe Elbow B CST Tank; June 6, 2008
- IR 00755744; 2/3 EDG Leak on Engine Block; March 28, 2008
- IR 00711323; 2/3 DGCW Pump Suction Pipe Corrosion; December 14, 2007
- IR 00705912; Unit 2 CCSW System Corrosion; December 2, 2007
- IR 00705639; DGCW Pipe Corrosion; December 2, 2007
- IR 00695137; Unit 2 Reactor Head Flange MT Indication; November 8, 2007
- IR 00691069; Loose Anchor Bolt on CS Line; October 31, 2007
- IR 00681657; PT Rejectable Indication; October 22, 2007
- ASME Section XI Repair/Replacement Plan 2-1505A-12-0; April 1, 2009
- Certified Mill Test Report (Consolidated Power Supply); 12 Safety-Related 90 Elbow;
September 15, 2009
- EC 368360; Evaluation of Leakage at Bolted Connections and other Recordable Indications;
Revision 0
- Examination Summary Sheet; D2R21-028 UT of PS2/201-1; November 7, 2009
- Examination Summary Sheet; D2R21-029 UT of PS2-Tee/202-4B; November 7, 2009
- NDE Report No.09-294; VT-3 Visual Examination; November 13, 2009
- NDE Certification; Scott R. Erickson; UT Level III; October 6, 2009
- Procedure GE-PDI-UT-2; PDI Generic Procedure for the Ultrasonic Examination of Austenitic
Pipe Welds; Revision 4
- Procedure GE-PDI-UT-3, PDI Generic Procedure for the Ultrasonic Thru Wall Sizing in Piping
Welds, Revision 2
- Procedure ER-AA-335-018, Detailed General VT-1, VT-1C, VT-3 and VT-3C Visual
Examination of ASME Class MC and CC Containment Surfaces and Components; Revision 5
- Procedure ER-AA-335-1008; Code Acceptance and Recording Criteria for Nondestructive
Surface Examination; Revision 1
- Procedure Qualification Record; A-001; October 19, 1998
- Procedure Qualification Record; A-002; March 9, 1997
- Procedure Qualification Record; 1-50C; January 3, 1984
4 Attachment
- Report No. D2R20-037; Four Indications on the Reactor Head Flange Weld (2RPV UPP
HD/2-THD-FLG); November 11, 2007
- Weld Procedure Specification; 1-1-GTSM-PWHT; Revision 1
- Welder Qualification Record; W2677; October 5, 2009
- Work Order 01189798; Replace Degraded Elbow on 2A CCSW Pump; October 22, 2009
1R12 Maintenance Effectiveness (71111.12)
- Z03, "Control Rod Drive Maintenance Rule Performance Criteria"
- IR 845878, "Scram Dump Valve Leaking", 11/17/2008
- IR 763023, "Review Maintenance Rule Functions Perform review described in In-Progress
Notes", 5/30/2008
- IR 842585, "Handwheel Spins with no Valve Movement", 11/09/2008
- IR 842587, "Valve Handwheel Broken", 11/09/2008
- IR 843592, "HCU P6 Scram Valve Packing Leak", 11/11/2008
- IR 700134, "Relief Valve Continuously Lifted", 11/16/2007
- IR 976292, "CRD Exercising and Condenser Vacuum Scram Impact U3 Restart", 10/05/2009
- WO 1186809, "Scram Dump Valve Leaking", 11/17/2008
- M-34, "Diagram of Control Rod Drive Hydraulic Piping", Revision W
- TS 3.1.3, Control Rod Operability
- TS 3.1.4, Control Rod Scram Times
- TS 3.1.5, Control Rod Scram Accumulators
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
- IR 1009039, 345 kv Line 8014 trip
1R15 Operability Evaluations (71111.15)
- Operability Evaluation No.09-007, 2A LPCI Heat Exchanger (2-1503-A)
- EC 372200, Perform Evaluation of Thermal Performance Test Data of 2A LPCI Hx
- EC 377036, 2A LPCI Heat Exchanger September 18, 2009 Thermal Performance Test
- IR 978203, GL 89-13 Program Health Color Change
- IR 989609, D2R21 Inspection Results for 2A LPCI Heat Exchanger
- IR 990189, 2A LPCI Heat Exchanger Tubesheet Corrosion
- IR 990209, 2A LPCI Hx Top Coverplate Coating Bubbled
- IR 996991, A LPCI HT Exchanger Shell Side RV Lifting
- CY-DR-110-220, LPCI Service Water (CCSW) and Torus Water Sampling, Revision 3
- CY-DR0120-413, Cooling and Service Water Chemical Injection System, Revision 8
- Root Cause Report 967008-03, Dresden 2-1503-A, 2A Low Pressure Coolant Injection
(LPCI)/Containment Cooling Heat Exchanger (Hx) Failure to Meet Design Basis Heat Removal
Capability due to Asiatic Clam Macrofouling Resulting from 2-1501-3A Valve Leakage and
Subsequent Untreated Service Water Make-Up via the CCSW Keepfill Diluting the Biocide
Treatment below the Asiatic Clam Lethal Concentration
- Focus Area Assessment, Dresden Station, CCSW System Asiatic Clam Fouling. Performed
by Water Technology Consultants, Inc.
- EC Evaluation 373443, Evaluation of Leakage From Cylinder Head Covers on 2A SBLC
Pump
- WO1001541-76, 3B SBLC System Pump Test for Operability Verification
5 Attachment
1R19 Post-Maintenance Testing (71111.19)
- IR 1003797, TSC HVAC Surveillances Failed
- WO 1294151, D1/2/3 SAN PM Operability Surv for the TSC AFUs
- DOS 5750-05, Semi-Annual Technical Support Center (TSC) Air Filtration Unit (AFU)
Operability Test, Revision 15
- IR 348426, FIC-2/3-5748-93 Airflow Indication Not Actual Airflow
- WO 826129, FIC-2/3-5748-93 Airflow Indication Not Actual Airflow
- IR 1005336, TSC Flow Controller Range Issue
- EP-AA-1000, Standardized Radiological Emergency Plan, Revision 19
- EP-AA-112-200-F-01, Station Emergency Director Checklist, Revision F
- NUREG-0696, Functional Criteria for Emergency Response Facilities, February 1981
- NUREG-0737, Clarification of TMI Action Plan Requirements, Supplement No. 1,
January 1983.
- M-3006, Technical Support Center HVAC & Plumbing Layout, Revision F
- DOS 6600-01, Diesel Generator Governor Oil Change and Compensating Adjustment,
Revision 23
- IR 992803, U2 EDG Largest Load Reject (TSR 3.8.1.10)
- IR 994101, 2/3 EDG Voltage Transient
- DOS 6600-06, Bus Undervoltage and ECCS Integrated Functional Test for Unit 2/3 Diesel
Generator to Unit 2, Revision 46
- IR 997244, Recirc Pump Instruments not Functioning Reqd for Hydro
- IR 997142, CCP: MCR Panel 923-5 Lost Ventilation Equip Indications
- EC 378040, 2/3 EDG Overvoltage during Division I Undervoltage Surveillance, Revision 0
- IR 1005291, Inaccurate Information Included in IR 994101
- IR 1006989, Control Room Indicators Deenergized
- EACE 994101-07, 2/3 Emergency Diesel Generator (EDG) Voltage Transient
- IR 987850, D2R21 As Found LLRT on 2-0203-2C Exceeded Leakage Limit
- DOS 0250-02, Full Closure Timing and Exercising of Main Steam Isolation Valves, Rev 26
- DOS 0250-03, Main Steam Isolation Valve Fail-Safe Closure Test, Rev 21
- IR 1001725, Higher than Expected Vibrations on 2B Cond Pp.
- IR 1002609, FME: Found in 2B Condensate Pump Suction Piping
- ER-AA-2006, Lost Parts Evaluations, Revision 6
- WO 1098975, 2B Condensate Booster Motor Alignment
- DOP 3300-02, Condensate System Startup, Revision 50
- M-15, Diagram of Condensate Piping, Revision J
- MA-AA-716-012, Post-Maintenance Testing, Revision 11
- MA-AA-716-230-1002, Vibration Analysis/Acceptance Guideline, Revision 2
1R20 Outage (71111.20)
- DGP 01-01, Unit Startup, Revision 153
- IR 975280, 3B CRD FCV Failed to Operate Remotely
- IR 975813, D3F48LL: DEHC Alarms During U3 Chest Warming
- IR 975830, D3F48LL: DEHC Issues During Turbine Roll
- IR 976410, CIV #1 Indicates 57% Open. LVDT Position Indication Failure
6 Attachment
1R22 Surveillance Testing (71111.22)
- IR 984934, DOS 6620-07 SBO Surveillance Need Revision
- IR 745855, "Unable to Close SBO Diesel Onto Bus"
- IR 984179, "Unit 2 SBO Preparation for Standby Readiness Deficiency"
- DOS 6620-07, "SBO 2(3) Diesel Generator Surveillance Tests, Revision 28
- DOP 6620-20, "SBO D/G 2(3) Prelubrication and Barring for Normal Start", Revision 06
- DOA 6500-11, "4 KV Bus Overvoltage," Revision 05
- WO 1257282, "Perform DOS 6620-07, D2 SBO Surveillance," 10/26/2009
- WO 1079209-01, D2 30M/RFL TS LLRT MSIV 203-1B & 203-2B Dry Test
- WO 1077724-01, D2 30M/RFL TS LLRT MSIV 203-1C & 203-2C Dry Test
- WO 1077725-01, D2 30M/RFL TS LLRT MSIV 203-1D & 203-2D Dry Test
- WO 1081285-01, D2 20M/RFL TS LLRT MSIV 203-2A Wet Test
- WO 1079266-01, D2 30M/RFL TS LLRT MSIV 203-2B Wet Test
- WO 1081288-01, D2 30M/RFL TS LLRT MSIV 203-2C Wet Test
- WO 1081313-01, D2 30M/RFL TS LLRT MSIV 203-2D Wet Test
- DOS 7000-01, Local Leak Rate Testing of Main Steam Isolation Valves (Dry Tests), Rev 5
- DOS 7000-02, Local Leak Rate Testing of Main Steam Isolation Valves (Wet Test), Rev 2
- IR 987850, D2R21 As Found LLRT on 2-0203-2C Exceeded Leakage Limit
- IR 987852, D2R21 As Found LLRT on 2-0203-1D Exceeded Leakage Limit
- DIS 1500-01, Reactor Low Pressure (350 PSIG) ECCS Permissive, Revision 27
- IR 944688, Test Valves Not Installed on CST Level Switches (HPCI Logic)
1EP4 Emergency Action Level and Emergency Plan Changes
- Dresden Station Radiological Emergency Plan Annex; Revisions 23, 24, and 25
2OS1 Access Control to Radiologically Significant Areas (71121.01)
- AR 987949987949 Operator PCE in Clean Area above Drywell Bullpen; November 3, 2009
- AR 993194993194 Responding to Guardhouse Portal Monitor Alarm; November 13, 2009
- RP-AA-203-1001; Personnel Exposure Investigation, Revision 6
- RP-AA-210; Dosimetry Issue, Usage and Control; Revision 15
- RP-AA-220; Intake Investigation, Revision 5
- RP-AA-350-1001; Response to Guardhouse Portal Monitor Alarms, Revision 0
- Underwater Construction Corporation Safe Practices Manual, Attachment A: Safety Hazard
Analysis/Dive Plan; November 3, 2009
2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)
- RWP 10010408; D2R21 Drywell Nuclear Instrumentation System Maintenance; Revision 0
- RWP 10010420; D2R21 Drywell Control Rod Drive System Maintenance; Revision 0
- RWP 10010421; D2R21 Drywell Control Rod Drive System Support; Revision 0
- RWP 10010426; D2R21 Drywell In-Service Inspection; Revision 0
- RWP 10010437; D2R21 Torus Diving Activities; Revision 1
- RWP 10010452; D2R21 Reactor Disassembly/Reassembly and Related Activities; Revision 1
- AR 870602-03; Focused Area Self-Assessment: ALARA Planning for Outage Readiness and
Preparation; August 27, 2009
- AR 988447988447 Unit 2 Refuel Floor and Reactor Building Low Level Contamination;
November 3, 2009
7 Attachment
- AR 990061990061 Under Vessel General Electric Worker Receives Small Ingestion;
November 5, 2009
- AR 993319993319 Shaw Laborer Wiping Down cords on RB 613 300K Particle on Scrubs;
November 11, 1009
- RWP-WIP-10010388; D2 R21 Scaffold Installation/Removal Activities (Excluding Drywell);
November 7, 2009
- RP-AA-461; Radiological Controls for Contaminated Water Diving Operations; Revision 2
- RWP-WIP-10010403; D2 R21 Drywell Radiation Protection Department Activities;
November 6, 2009
- RWP-WIP-10010403; D2 R21 Drywell Radiation Protection Department Activities;
November 10, 2009
- RWP-WIP-10010437; D2 R21 Torus Diving Activities; November 10, 2009
- RWP-WIP-10010453; D2 R21 Refuel Floor IVVI Activities; November 7, 2009
4OA1 Performance Indicator (PI) Verification (71151)
- LS-AA-2140; Monthly Data Elements for NRC Occupational Exposure Control Effectiveness;
Revision 4
4OA2 Identification and Resolution of Problems (71152)
- RCR 776598-08, Dresden 3-1503-B, 3B Low Pressure Coolant Injection (LPCI) / Containment
Cooling Heat Exchanger (HX) Failure to Meet Design Basis Heat Removal Capability Due to
Inadequate Programmatic Control of Macrofoulants, Revision 0
- IR 868703, 2A and 2B LPCI Heat Exchanger Samples Tested 0 PPM Biocide
- IR 871271, Biocide Injection Unavailable for CCSW System PMT Run
- IR 877889, Biocide Injection Not Available During U3 CCSW Run
- IR 880708, CCSW Biocide/Clam-Trol Chemical Injection Result Low
- IR 881043, CCSW Biocide/Clamtrol Chemical Injection Result Low
- IR 883155, 3A and 3B LPCI Fail Clam-Trol Test
- IR 884613, 2B LPCI Failed Clam-Trol Test
- IR 887406, Inadequate Biocide Retention
- IR 888462, 0 PPM Biocide Results for 2/3 EDG
- IR 889598, No Biocide Found in Unit 2B LPCI CCSW Hx Lay-up Sample
- IR 891286, No Biocide Found in 2B LPCI CCSW Hx Lay-up Sample
- IR 892241, Procedure change and Eval of Biocide Injection to DGCWPs
- IR 905027, 2B LPCI No Clamtrol Present
- IR 905224, No Biocide Detected in 2/3 DGCSW
- IR 908886, 2A LPCI Biocide Results Less than 8 PPM
- IR 914398, Revision to RCR 776598-08, 3B LPCI Hx Macrofouling Required
- IR 915033, 2A LPCI SW Biocide 24 hr. Sample < 8PPM
- IR 917133, 2B LPCI Failed Clam-Trol Test
- IR 920498, 2A and 2B LPCI SW Biocide <8PPM (24hr Sample)
- IR 923788, Clam-Trol Analysis Failed on 3DGCSW
- IR 999766, 2B LPCI Failed for Biocide
- IR 1000791, 2B LPCI Heat Exchanger Failed Clam-Trol Analysis
- IR 1006553, No Biocide Detected in CCSW from 3B LPCI Hx
- IR 1007918, Unit 2 A and B LPCI Heat Exchangers Fail 18-24 hr Biocide
8 Attachment
4OA3 Follow-Up of Events (71153)
- Licensee Event Report 237/2009-003-00, Emergency Diesel Generator Oil Leak, Revision 00
- IR 926605, Oil Leak on the 2/3 DG Turbo Lube Oil Y-strainer
- MA-AA-716-008, Foreign Material Exclusion Program, Revision 4
- Licensee Event Report 237/2009-001-00, Common Mode Failure of Reactor Building Isolation
Dampers, Revision 00
- IR 877591, Potential 10CFR50 Part 21 Notification of Versa Air Solenoid
- IR 838034, RBV Damper 2-5742-A Slow to Close
- IR 842305, 3-5742-B Damper 90 Seconds to Close
- IR 888338, RBV Isolation Damper Solenoid Valve Incorrect Component Classification
- IR 975779, Post Transient/Scram Walkdown Observation by NRC
- IR 975076, U2/3 EDG Started on Rx Trip when Aux Power Transferred
- IR 974426, U3 Group 1 Isolation and Reactor Scram
- IR 973968, 3A RWCU Pump Tripped and DOA Entry
- IR 973144, RWCU Isolate on High Temperature
- IR 973104, 3A RWCU Tripped
- Root Cause Report 974426-04, U3 Reactor SCRAM and Group 1 Isolation Resulting in
Forced Outage D3F48 Due to DOP 1200-03, titled RWCU System Operation with the Reactor
at Pressure Latent Procedural Deficiency
- LER 249/2009-001-00, Unit 3 Group 1 Isolation and Automatic Reactor Scram
- IR 990113, U3 from 650 MWe to 0 and a Turbine Trip
- IR 990160, 2/3 EDG Auto Started when U3 Main Generator was Tripped
- IR 990112, Need WO Rolled for Repair to U3 EHC Filter Pump Bkr
- IR 990110, U3 EHC Filter Pmp Trip
- IR 990661, MSV #4 Did Not Open During Initial Turbine Roll
4OA5 Other Activities (TI 2515/177)
- IR 994774, Procedures for Venting ECCS/SDC Systems Should Be Revised
- IR 999625, Air Found in HPCI Discharge Piping During UT
- IR 999762, Air Found in Second Location in HPCI Discharge Piping
- IR 1014280, Question from NRC Inspector on ISI Drawing
- EC 371153, Rev 2, NRC GL 2008-01 HPCI System Evaluation
- DOP 2300-01, HPCI Standby Operation, Rev 41
- M-51, Diagram of High Pressure Coolant Injection Piping, Rev CL
- ISI-504, System Pressure Test Walkdown Isometric MSIV Room - X Area, Rev B
- ISI-510, System Pressure Test Walkdown Isometric H.P. Coolant Injection Piping, Sheet 2,
Rev D
- M-1151C-2, Computer Math Model High Pressure Coolant Injection System, Sheet 1, Rev 2
- M-4455, HPCI High Point Vent Line, Sheet 3, Rev A
9 Attachment
LIST OF ACRONYMS USED
ADAMS Agencywide Document Access Management System
AEER Auxiliary Electric Equipment Room
ALARA As-Low-As-Reasonably-Achievable
ASME American Society of Mechanical Engineers
BWR Boiling Water Reactor
CAP Corrective Action Program
CCSW Containment Cooling Service Water
CDF Core Damage Frequency
CFR Code of Federal Regulations
CO Clearance Order
CRD Control Rod Drive
D2 Dresden Unit 2
DRP Division of Reactor Projects
EACE Equipment Apparent Cause Evaluation
EAL Emergency Action Level
EC Engineering Change
EDG Emergency Diesel Generator
ESI Engine Systems Incorporated
FME Foreign Material Exclusion
HEP Human Error Probability
HEPA High Efficiency Particulate Air
HPCI High Pressure Coolant Injection
HCU Hydraulic Control Unit
Hx Heat Exchanger
IPEEE Individual Plant Examination for External Events
IMC Inspection Manual Chapter
INPO Institute of Nuclear Power Operations
IP Inspection Procedure
IR Issue Report
ISI Inservice Inspection
IST In-service Test
LER Licensee Event Report
LERF Large Early Release Frequency
LOCA Loss of Coolant Accident
LOOP Loss of OffSite Power
LPCI Low Pressure Coolant Injection
MOV Motor Operated Valves
MSV Main Stop Valve
NCV Non-Cited Violation
NEI Nuclear Energy Institute
NLO Non-Licensed Operator
NRC Nuclear Regulatory Commission
NRR Office of Nuclear Reactor Regulation
NSO Nuclear Station Operator
OSF Outage Safety Plan
PARS Publicly Available Records
PCIS Primary Containment Isolation Signal
PI Performance Indicator
10 Attachment
P&ID Piping and Instrumentation Diagrams
PM Planned or Preventative Maintenance, or Post-Maintenance
PO Purchase Order
RCR Root Cause Report
RFO Refueling Outage
SBO Station Blackout
SCAQ Significant Condition Adverse to Quality
SDP Significance Determination Process
SPAR Standardized Plant Analysis Risk
SR Surveillance Requirements
SRO Senior Reactor Operator
SSC Structures, Systems and Components
TS Technical Specification
U2 Unit 2
U3 Unit 3
UFSAR Updated Final Safety Analysis Report
URI Unresolved Item
UT Ultrasonic Examination
WO Work Order 11 Attachment
C. Pardee -2-
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its
enclosure, and your response (if any) will be made available electronically for public inspection
in the NRC Public Document Room or from the Publicly Available Records (PARS) component
of NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Mark A. Ring, Chief
Branch 1
Division of Reactor Projects
Docket Nos. 50-237; 50-249
Enclosure: Inspection Report 05000237/2009-005; 05000249/2009-005
w/Attachment: Supplemental Information
cc w/encl: Distribution via ListServ
DOCUMENT NAME: G:\1-SECY\1-WORK IN PROGRESS\DRE 2009 005.DOC
G Publicly Available G Non-Publicly Available G Sensitive G Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl
"E" = Copy with attach/encl "N" = No copy
OFFICE RIII RIII RIII RIII
NAME MRing:cms
DATE 02/10/2010
OFFICIAL RECORD COPY
Letter to C. Pardee from M. Ring dated February 10, 2010
SUBJECT: DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3
INTEGRATED INSPECTION REPORT 05000237/2009-005;
DISTRIBUTION:
Susan Bagley
RidsNrrDorlLpl3-2
RidsNrrPMDresden Resource
RidsNrrDirsIrib Resource
Cynthia Pederson
DRPIII
DRSIII
Patricia Buckley
ROPreports Resource