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| NRC FORM 366a U.S. NUCLEAR REGULATORY COMMISSION 4195 LICENSEE EVENT REPORT {LER) | | NRC FORM 366a U.S. NUCLEAR REGULATORY COMMISSION 4195 LICENSEE EVENT REPORT {LER) |
| TEXT CONTINUATION FACILITY NAME 111 DOCKET12l LER NUMBER 51 PAGE | | TEXT CONTINUATION FACILITY NAME 111 DOCKET12l LER NUMBER 51 PAGE |
| _CONSUMERS ENERGY COMPANY PALISADES NUCLEAR PLANT 05000255 YEAR I SEQUENTIAL NUMBER REVISION NUMBER 2 OF 5 97 - 00 9 - 00 | | _CONSUMERS ENERGY COMPANY PALISADES NUCLEAR PLANT 05000255 YEAR I SEQUENTIAL NUMBER REVISION NUMBER 2 OF 5 97 - 00 9 - 00 TEXT (If more space 1s required, use add1t1onal copies of NRC Form 366A) (17) |
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| TEXT (If more space 1s required, use add1t1onal copies of NRC Form 366A) (17) | |
| EVENT DESCRIPTION On September 23, 1997, at 1105 hours with the plant at approximately 100% power, it was recognized that an operator action to support an Appendix R program analysis had not been implemented in the appropriate Off-Normal Procedure (ONP). Specifically, ONP 25.2, "Alternate Safe Shutdown Procedure" did not include the action to trip all four primary coolant pumps if the control room had to be evacuated. Instead, the procedure directed the control room operators to | | EVENT DESCRIPTION On September 23, 1997, at 1105 hours with the plant at approximately 100% power, it was recognized that an operator action to support an Appendix R program analysis had not been implemented in the appropriate Off-Normal Procedure (ONP). Specifically, ONP 25.2, "Alternate Safe Shutdown Procedure" did not include the action to trip all four primary coolant pumps if the control room had to be evacuated. Instead, the procedure directed the control room operators to |
| "... trip two primary coolant pumps and leave two operating ... ". | | "... trip two primary coolant pumps and leave two operating ... ". |
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| ~I 4195 LICENSEE EVENT REPORT (LER) | | ~I 4195 LICENSEE EVENT REPORT (LER) |
| TEXT CONTINUATION r;J FACILITY NAME 11 l DOCKETl2l LER NUMBER 6l CONSUMERS ENERGY COMPANY PALISADES NUCLEAR PLANT 05000255 YEAR I SEQUENTIAL NUMBER REVISION NUMBER 5 | | TEXT CONTINUATION r;J FACILITY NAME 11 l DOCKETl2l LER NUMBER 6l CONSUMERS ENERGY COMPANY PALISADES NUCLEAR PLANT 05000255 YEAR I SEQUENTIAL NUMBER REVISION NUMBER 5 |
| 97 - 00 9 - 00 | | 97 - 00 9 - 00 TEXT (If more space 1s required, use add1t1onal copies of NRC Form 366A) (17) |
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| TEXT (If more space 1s required, use add1t1onal copies of NRC Form 366A) (17) | |
| CAUSE OF THE EVENT The cause of the event is a human error. The engineer identifying and transmitting requested changes to the procedure sponsor failed to properly communicate the requirement for tripping all four primary coolant pumps prior to evacuation of the control room. | | CAUSE OF THE EVENT The cause of the event is a human error. The engineer identifying and transmitting requested changes to the procedure sponsor failed to properly communicate the requirement for tripping all four primary coolant pumps prior to evacuation of the control room. |
| A contributing cause for this event is that the process for compiling information from the Appendix R analyses does not require a formal. technical review prior to the information being sent to the procedure sponsor. | | A contributing cause for this event is that the process for compiling information from the Appendix R analyses does not require a formal. technical review prior to the information being sent to the procedure sponsor. |
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| NRC FORM 366a U.S. NUCLEAR REGULATORY COMMISSION 4195 LICENSEE EVENT REPORT (LER) g | | NRC FORM 366a U.S. NUCLEAR REGULATORY COMMISSION 4195 LICENSEE EVENT REPORT (LER) g |
| - TEXT CONTINUATION I | | - TEXT CONTINUATION I |
| FACILITY NAME 11 l DOCKETl2l LER NUMBER *61 YEAR SEQUENTIAL REVISION CONSUMERS ENERGY COMPANY NUMBER NUMBER 05000255 5 PALISADES NUCLEAR PLANT 97 - 00 9 - 00 | | FACILITY NAME 11 l DOCKETl2l LER NUMBER *61 YEAR SEQUENTIAL REVISION CONSUMERS ENERGY COMPANY NUMBER NUMBER 05000255 5 PALISADES NUCLEAR PLANT 97 - 00 9 - 00 TEXT (If more space 1s required, use additional copies of NRC Form 366A) (17) |
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| TEXT (If more space 1s required, use additional copies of NRC Form 366A) (17) | |
| "A method will be developed or enhanced to screen Palisades changes, both physical and procedural, whereby areas potentially affected by the change can be identified so that appropriate Appendix R reviews are performed. Change types to be screened include the following: modifications, Operating Procedure changes, Surveillance Procedure changes, Engineering Analyses which change design basis inputs, and FSAR changes." | | "A method will be developed or enhanced to screen Palisades changes, both physical and procedural, whereby areas potentially affected by the change can be identified so that appropriate Appendix R reviews are performed. Change types to be screened include the following: modifications, Operating Procedure changes, Surveillance Procedure changes, Engineering Analyses which change design basis inputs, and FSAR changes." |
| ADDITIONAL INFORMATION A similar condition was reported under LER 97-008.}} | | ADDITIONAL INFORMATION A similar condition was reported under LER 97-008.}} |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18065B1151997-12-0909 December 1997 LER 97-013-00:on 971110,failure to Closure Test Two Check Valves Resulted in Violation of TS 6.5.7 Occurred.Caused by Close Function for Check Valves.Check Valves Tested to Confirm Proper Closure Capability ML18067A7751997-11-11011 November 1997 LER 97-011-00:on 971012,primary Coolant Pump Was Started W/Sg Temperatures Greater than Cold Leg Temperature.Caused by Inadequate Procedures & Operator Decision Making.Critique of Event Conducted W/Operators Involved ML18067A7581997-10-30030 October 1997 LER 97-010-00:on 970930,determined That Inadequacy in App R Analysis Resulted in Condition Outside Design Basis of Plant.Caused by Missing Cable in Circuit & Raceway Schedule. Developed New Evaluation Re ASD Valves Validation ML18067A7461997-10-23023 October 1997 LER 97-009-00:on 970923,discovered Procedure Weakness Re Implementation of App R Shutdown Methodology.Caused by Human Error.Revised Off-Normal Procedure ONP-25.2, Alternate Safe Shutdown Procedure. ML18067A7191997-10-10010 October 1997 LER 97-008-00:on 970912,spurious Valve Operation Could Result in Loss of Shutdown Capabilities Per 10CFR50,App R, Section Iii.L,Was Discovered.Caused by Failure to Validate Info from App R.Design Bases for SW Backup Reviewed ML18067A6951997-09-24024 September 1997 LER 97-007-00:on 970826,discovered Inadequate Testing of DG Sequencer Control Relay Contacts.Caused by Oversight on Part of Personnel Involved in Installation of Facility Change FC-800.Tested 106D-1/XL & 106D-2/XL Relay Contacts ML18067A5651997-06-0303 June 1997 LER 96-013-01:on 961115,DC Breaker Failed During Testing for as-found Trip Setting.Failure Caused by Oversight within Preventive Maint Program.Breaker Was Replaced & Tested ML18067A5461997-05-12012 May 1997 LER 97-006-00:on 970412,overtime Limits Were Exceeded for Radiation Protection Technicians.Caused by Inadequate Design,Review & Proper Verifications of Overtime Work Schedule.Communicate Overtime Limitation Responsibilities ML18067A4431997-03-24024 March 1997 LER 97-004-00:on 970221,trip of High Pressure Safety Injection Pump Occurred While Filling Safety Injection Tank Resulting in TS Violation.Caused by Particle Lodged Between Surface of Indication disk.Y-phase Relay Was OOS ML18067A4391997-03-21021 March 1997 LER 97-005-00:on 961220,operation of Plant Outside Design Basis Occurred Due to an Unacceptable Repair on Main Steam Isolation Valves.Pipe Plugs Permanently Repaired ML18067A4401997-03-21021 March 1997 LER 97-003-00:on 961101,four Piping Lines Were Determined to Be Potentially Susceptible to Pressurization Due to Containment Temperature Increase During an Accident.Cac Discharge Piping Will Be verified.W/970321 Ltr ML18066A8931997-02-21021 February 1997 LER 97-002-00:on 970123,failure to Meet TSs 4.5.2d(1)(b) for Testing of Emergency Escape Airlock Occurred.Caused by Missed Surveillance.Emergency Escape Air Lock Testing Was Completed & Declared operable.W/970221 Ltr ML18066A8751997-02-0505 February 1997 LER 97-001-00:on 970106,TAVE Temp Dropped Below Minimum Temp for Criticality.Caused by Control Rod Withdrawal Rate to Increase Power Not Sufficient to Match Increase in Steam. Turbine Bypass Valve Actuator repaired.W/970205 Ltr ML18066A8041996-12-23023 December 1996 LER 96-014-00:on 961124,class 1E Raychem Cable Splices Were Installed Incorrectly.Caused by Incorrectly Made Electrical Splices.Total of 270 Splices Have Been Replaced within Containment ML18066A7831996-12-16016 December 1996 LER 96-013-00:on 961115,DC Breaker Failure During Testing for as-found Trip Setting Occurred.Cause Under Investigation.All molded-case Circuit Breakers in DC Distribution Panels Were Replaced ML18065A9951996-10-0404 October 1996 LER 96-002-01:on 960116,initiated TS Required Shutdown Due to Safeguards Cable Fault.Both Sets (Six Cables) of Cables Were Replaced & Installed Through Turbine Generator Bldg ML18065A9171996-09-0909 September 1996 LER 95-012-00:on 960809,TS Violation Occurred,Due to No Senior Reactor Operator in Cr.Caused by Extensive Remodeling.Cr Remodeling completed.W/960909 Ltr ML18065A8961996-08-29029 August 1996 LER 96-011-00:on 960730,CR Continuous Air Monitor Alarm Setpoint Improperly Established.Caused by Failure to Utilize Mod Process in 1988 Leading to Failure to Properly Select & Calibrate Instruments ML18065A8811996-08-20020 August 1996 LER 96-005-01:on 960207,determined Fuse on Main Supply to Two Safety Related DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Lack of Thorough Associated Circuits Analysis.Supply Fuse to Panels Replaced ML18065A8741996-08-16016 August 1996 LER 96-010-00:on 960717,high Pressure Safety Injection Pump Tripped While Filling Safety Injection Tank.Caused by Faulty 150/151Y-207 Time Overcurrent Relay.All Similar Relays in Time Overcurrent Application Have Been Inspected ML18065A8651996-08-12012 August 1996 LER 96-009-00:on 960712,identified Penetration Seal Deficiency on Fire Barriers Caused by Failure to Perform & Document Comprehensive Fire Barrier Evaluation.Developed Basis document.W/960812 Ltr ML18065A8601996-08-0202 August 1996 LER 96-006-01 on 960207,discovered Limits of Design Analysis Could Have Been Violated.Subsequent Tests & Analyses Facility Did Not Exceed Basis.Operating Procedures Have Been Revised to Treat 2530 Megawatts Limit as Absolute Limit ML18065A8321996-08-0101 August 1996 LER 96-003-01:on 960115,alternate Shutdown Panel Inverter Resulted in Unavailability of Panel.Replaced Defective Inverter Alarm Logic Board ML18065A7691996-06-12012 June 1996 LER 96-008-00:on 960513,fire Door Not Maintained Open in Accordance W/Design Basis.Cause Under Investigation. Engineering Evaluation Performed & Revised Documents, Surveillance & Test procedures.W/960612 Ltr ML18065A6901996-05-0101 May 1996 LER 95-001-01:on 950302,malfunction of Left Channel DBA Sequencer Resulted in Inadvertent Actuation of Left Channel Safeguards Equipment.Replaced microprocessor.W/960501 Ltr ML18065A6681996-04-22022 April 1996 LER 96-007-00:on 960321,inadequate Emergency Lighting & Ventilation in post-fire Safe Shutdown Areas.Caused by App R Program Documentation Insufficient to Demonstrate Regulatory Compliance.Lighting modified.W/960422 Ltr ML18065A5721996-03-11011 March 1996 LER 96-006-00:on 960207,average Reactor Power Level Exceeded License Limit Due to Insufficient Procedural Guidance. GOP-12 Revised to Treat 2,530 Mwt Limit as Absolute Limit Requiring Immediate Corrective Action If Exceeded ML18065A5261996-03-0101 March 1996 LER 96-005-00:on 960202,fuse on Main Supply to Two SR DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Inadequate Electrical/App R Design Review.Implemented Hourly Fire tours.W/960301 Ltr ML18065A5111996-02-19019 February 1996 LER 94-012-02:on 940427,determined That Internal Ground in Thermal Margin Monitor Causes Nonconformance W/Rps Design Basis.Incorporated RPS Failure Modes & Effects Analysis in Plant DBD.W/960219 Ltr ML18065A5061996-02-19019 February 1996 LER 96-004-00:on 960118,SIS Disabled W/Primary Coolant Sys Greater than 300 F.Caused by Personnel Error.Permanent Maint Procedure to Disable/Enable SIS Actuation on Low Pressurizer Pressure Will Be Revised to Align W/Ts ML18065A5021996-02-15015 February 1996 LER 96-003-00:on 960115,technicians Found Low Voltage cut- Off for Alternate Shutdown Panel Inverter Set That Resulted in Unavailability of Panel.Caused by Inadequate Post Mod. Readjusted Set Point to Minimum setting.W/960215 Ltr ML18065A4581996-01-31031 January 1996 LER 96-001-00:on 960103,failed to Test Duplicate Equipment. Caused by STS No Longer Containing Requirement for cross- Train Testing of Duplicate Components.Will Submit Request to Delete Subj Requirements from TS.W/960131 Ltr ML18065A4421996-01-19019 January 1996 LER 95-016-00:on 951226,did Not Analyze Primary Coolant Samples within 72 H.Caused by Belief Acceptability to Save Pcs Samples for Choride Analysis Past 72 H.Counseled Chemistry Supervision.W/960119 Ltr ML18065A4041996-01-15015 January 1996 LER 95-014-00:on 950119,PCP Oil Collection Deficiencies Created by FC-860 Piping Mod.Caused by Inadequate DBD for Sys & Lack of Review by Experienced Fire Protection Personnel.Updated Design Basis documentation.W/960115 Ltr ML18065A3291995-12-0404 December 1995 LER 95-013-00:on 951103,circuit Fuse Coordination Deficiency Which Affects App R Safe Shutdown Equipment Noted.Design of Fuse Coordination in Potential Transformer Circuits Will Be Evaluated & Modified as required.W/951204 Ltr ML18065A2361995-11-0202 November 1995 LER 95-012-00:on 950701,discovered Unqualified Electrical Connection in Containment SW Outlet Valve Controller.Caused by Failure of Assigned Engineers to Available Info.Replaced Wire Nuts W/Inline Butt connections.W/951102 Ltr ML18065A2051995-10-20020 October 1995 LER 95-008-01:on 950728,discovered That None of Four Containment High Pressure Channels Would Initiate Reactor Trip Due to Programmatic Deficiencies.Administrative Procedure (AP) 9.44,AP 9.45 & AP 10.44 Will Be Revised ML18065A0841995-09-18018 September 1995 LER 95-011-00:on 950817,CR 40 Withdrawal Occurred When Given Insertion Signal Due to skill-based Error in Crimping & Removing Foreign Matl from CRDM Motor Connection Box.Crd Package replaced.W/950918 Ltr ML18065A0681995-09-14014 September 1995 LER 95-010-00:on 950815,ESFA Resulted in Manual Rt Following Isolation of Pcs.Replaced Failed Instrument Line ML18065A0651995-09-0808 September 1995 LER 95-009-00:on 950728,discovered Lack of Procedural Guidance for Pump Repair Following Fire.Proposed Use of Power Supply Breaker Did Not Adequately Address Effect of Loss of Control Power.Performed Independent Assessment ML18064A8781995-08-28028 August 1995 LER 95-008-00:on 950728,discovered During Design Change Testing That None of Four Containment High Pressure Channels Would Initiate Rt.Caused by Programmatic Deficiencies. Reviewed Selected Tests & Mods from Recent Refueling Outage ML18064A8831995-08-21021 August 1995 LER 95-007-00:on 950720,discovered That 12 Instrument Loops Had V-bolted Type Qualified Cable Splices Connected to Wires W/Exposed Kapton Insulation.Caused by Human Error.All V- Bolted Splices Replaced w/in-line design.W/950821 Ltr 1999-09-02
[Table view] Category:RO)
MONTHYEARML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18065B1151997-12-0909 December 1997 LER 97-013-00:on 971110,failure to Closure Test Two Check Valves Resulted in Violation of TS 6.5.7 Occurred.Caused by Close Function for Check Valves.Check Valves Tested to Confirm Proper Closure Capability ML18067A7751997-11-11011 November 1997 LER 97-011-00:on 971012,primary Coolant Pump Was Started W/Sg Temperatures Greater than Cold Leg Temperature.Caused by Inadequate Procedures & Operator Decision Making.Critique of Event Conducted W/Operators Involved ML18067A7581997-10-30030 October 1997 LER 97-010-00:on 970930,determined That Inadequacy in App R Analysis Resulted in Condition Outside Design Basis of Plant.Caused by Missing Cable in Circuit & Raceway Schedule. Developed New Evaluation Re ASD Valves Validation ML18067A7461997-10-23023 October 1997 LER 97-009-00:on 970923,discovered Procedure Weakness Re Implementation of App R Shutdown Methodology.Caused by Human Error.Revised Off-Normal Procedure ONP-25.2, Alternate Safe Shutdown Procedure. ML18067A7191997-10-10010 October 1997 LER 97-008-00:on 970912,spurious Valve Operation Could Result in Loss of Shutdown Capabilities Per 10CFR50,App R, Section Iii.L,Was Discovered.Caused by Failure to Validate Info from App R.Design Bases for SW Backup Reviewed ML18067A6951997-09-24024 September 1997 LER 97-007-00:on 970826,discovered Inadequate Testing of DG Sequencer Control Relay Contacts.Caused by Oversight on Part of Personnel Involved in Installation of Facility Change FC-800.Tested 106D-1/XL & 106D-2/XL Relay Contacts ML18067A5651997-06-0303 June 1997 LER 96-013-01:on 961115,DC Breaker Failed During Testing for as-found Trip Setting.Failure Caused by Oversight within Preventive Maint Program.Breaker Was Replaced & Tested ML18067A5461997-05-12012 May 1997 LER 97-006-00:on 970412,overtime Limits Were Exceeded for Radiation Protection Technicians.Caused by Inadequate Design,Review & Proper Verifications of Overtime Work Schedule.Communicate Overtime Limitation Responsibilities ML18067A4431997-03-24024 March 1997 LER 97-004-00:on 970221,trip of High Pressure Safety Injection Pump Occurred While Filling Safety Injection Tank Resulting in TS Violation.Caused by Particle Lodged Between Surface of Indication disk.Y-phase Relay Was OOS ML18067A4391997-03-21021 March 1997 LER 97-005-00:on 961220,operation of Plant Outside Design Basis Occurred Due to an Unacceptable Repair on Main Steam Isolation Valves.Pipe Plugs Permanently Repaired ML18067A4401997-03-21021 March 1997 LER 97-003-00:on 961101,four Piping Lines Were Determined to Be Potentially Susceptible to Pressurization Due to Containment Temperature Increase During an Accident.Cac Discharge Piping Will Be verified.W/970321 Ltr ML18066A8931997-02-21021 February 1997 LER 97-002-00:on 970123,failure to Meet TSs 4.5.2d(1)(b) for Testing of Emergency Escape Airlock Occurred.Caused by Missed Surveillance.Emergency Escape Air Lock Testing Was Completed & Declared operable.W/970221 Ltr ML18066A8751997-02-0505 February 1997 LER 97-001-00:on 970106,TAVE Temp Dropped Below Minimum Temp for Criticality.Caused by Control Rod Withdrawal Rate to Increase Power Not Sufficient to Match Increase in Steam. Turbine Bypass Valve Actuator repaired.W/970205 Ltr ML18066A8041996-12-23023 December 1996 LER 96-014-00:on 961124,class 1E Raychem Cable Splices Were Installed Incorrectly.Caused by Incorrectly Made Electrical Splices.Total of 270 Splices Have Been Replaced within Containment ML18066A7831996-12-16016 December 1996 LER 96-013-00:on 961115,DC Breaker Failure During Testing for as-found Trip Setting Occurred.Cause Under Investigation.All molded-case Circuit Breakers in DC Distribution Panels Were Replaced ML18065A9951996-10-0404 October 1996 LER 96-002-01:on 960116,initiated TS Required Shutdown Due to Safeguards Cable Fault.Both Sets (Six Cables) of Cables Were Replaced & Installed Through Turbine Generator Bldg ML18065A9171996-09-0909 September 1996 LER 95-012-00:on 960809,TS Violation Occurred,Due to No Senior Reactor Operator in Cr.Caused by Extensive Remodeling.Cr Remodeling completed.W/960909 Ltr ML18065A8961996-08-29029 August 1996 LER 96-011-00:on 960730,CR Continuous Air Monitor Alarm Setpoint Improperly Established.Caused by Failure to Utilize Mod Process in 1988 Leading to Failure to Properly Select & Calibrate Instruments ML18065A8811996-08-20020 August 1996 LER 96-005-01:on 960207,determined Fuse on Main Supply to Two Safety Related DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Lack of Thorough Associated Circuits Analysis.Supply Fuse to Panels Replaced ML18065A8741996-08-16016 August 1996 LER 96-010-00:on 960717,high Pressure Safety Injection Pump Tripped While Filling Safety Injection Tank.Caused by Faulty 150/151Y-207 Time Overcurrent Relay.All Similar Relays in Time Overcurrent Application Have Been Inspected ML18065A8651996-08-12012 August 1996 LER 96-009-00:on 960712,identified Penetration Seal Deficiency on Fire Barriers Caused by Failure to Perform & Document Comprehensive Fire Barrier Evaluation.Developed Basis document.W/960812 Ltr ML18065A8601996-08-0202 August 1996 LER 96-006-01 on 960207,discovered Limits of Design Analysis Could Have Been Violated.Subsequent Tests & Analyses Facility Did Not Exceed Basis.Operating Procedures Have Been Revised to Treat 2530 Megawatts Limit as Absolute Limit ML18065A8321996-08-0101 August 1996 LER 96-003-01:on 960115,alternate Shutdown Panel Inverter Resulted in Unavailability of Panel.Replaced Defective Inverter Alarm Logic Board ML18065A7691996-06-12012 June 1996 LER 96-008-00:on 960513,fire Door Not Maintained Open in Accordance W/Design Basis.Cause Under Investigation. Engineering Evaluation Performed & Revised Documents, Surveillance & Test procedures.W/960612 Ltr ML18065A6901996-05-0101 May 1996 LER 95-001-01:on 950302,malfunction of Left Channel DBA Sequencer Resulted in Inadvertent Actuation of Left Channel Safeguards Equipment.Replaced microprocessor.W/960501 Ltr ML18065A6681996-04-22022 April 1996 LER 96-007-00:on 960321,inadequate Emergency Lighting & Ventilation in post-fire Safe Shutdown Areas.Caused by App R Program Documentation Insufficient to Demonstrate Regulatory Compliance.Lighting modified.W/960422 Ltr ML18065A5721996-03-11011 March 1996 LER 96-006-00:on 960207,average Reactor Power Level Exceeded License Limit Due to Insufficient Procedural Guidance. GOP-12 Revised to Treat 2,530 Mwt Limit as Absolute Limit Requiring Immediate Corrective Action If Exceeded ML18065A5261996-03-0101 March 1996 LER 96-005-00:on 960202,fuse on Main Supply to Two SR DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Inadequate Electrical/App R Design Review.Implemented Hourly Fire tours.W/960301 Ltr ML18065A5111996-02-19019 February 1996 LER 94-012-02:on 940427,determined That Internal Ground in Thermal Margin Monitor Causes Nonconformance W/Rps Design Basis.Incorporated RPS Failure Modes & Effects Analysis in Plant DBD.W/960219 Ltr ML18065A5061996-02-19019 February 1996 LER 96-004-00:on 960118,SIS Disabled W/Primary Coolant Sys Greater than 300 F.Caused by Personnel Error.Permanent Maint Procedure to Disable/Enable SIS Actuation on Low Pressurizer Pressure Will Be Revised to Align W/Ts ML18065A5021996-02-15015 February 1996 LER 96-003-00:on 960115,technicians Found Low Voltage cut- Off for Alternate Shutdown Panel Inverter Set That Resulted in Unavailability of Panel.Caused by Inadequate Post Mod. Readjusted Set Point to Minimum setting.W/960215 Ltr ML18065A4581996-01-31031 January 1996 LER 96-001-00:on 960103,failed to Test Duplicate Equipment. Caused by STS No Longer Containing Requirement for cross- Train Testing of Duplicate Components.Will Submit Request to Delete Subj Requirements from TS.W/960131 Ltr ML18065A4421996-01-19019 January 1996 LER 95-016-00:on 951226,did Not Analyze Primary Coolant Samples within 72 H.Caused by Belief Acceptability to Save Pcs Samples for Choride Analysis Past 72 H.Counseled Chemistry Supervision.W/960119 Ltr ML18065A4041996-01-15015 January 1996 LER 95-014-00:on 950119,PCP Oil Collection Deficiencies Created by FC-860 Piping Mod.Caused by Inadequate DBD for Sys & Lack of Review by Experienced Fire Protection Personnel.Updated Design Basis documentation.W/960115 Ltr ML18065A3291995-12-0404 December 1995 LER 95-013-00:on 951103,circuit Fuse Coordination Deficiency Which Affects App R Safe Shutdown Equipment Noted.Design of Fuse Coordination in Potential Transformer Circuits Will Be Evaluated & Modified as required.W/951204 Ltr ML18065A2361995-11-0202 November 1995 LER 95-012-00:on 950701,discovered Unqualified Electrical Connection in Containment SW Outlet Valve Controller.Caused by Failure of Assigned Engineers to Available Info.Replaced Wire Nuts W/Inline Butt connections.W/951102 Ltr ML18065A2051995-10-20020 October 1995 LER 95-008-01:on 950728,discovered That None of Four Containment High Pressure Channels Would Initiate Reactor Trip Due to Programmatic Deficiencies.Administrative Procedure (AP) 9.44,AP 9.45 & AP 10.44 Will Be Revised ML18065A0841995-09-18018 September 1995 LER 95-011-00:on 950817,CR 40 Withdrawal Occurred When Given Insertion Signal Due to skill-based Error in Crimping & Removing Foreign Matl from CRDM Motor Connection Box.Crd Package replaced.W/950918 Ltr ML18065A0681995-09-14014 September 1995 LER 95-010-00:on 950815,ESFA Resulted in Manual Rt Following Isolation of Pcs.Replaced Failed Instrument Line ML18065A0651995-09-0808 September 1995 LER 95-009-00:on 950728,discovered Lack of Procedural Guidance for Pump Repair Following Fire.Proposed Use of Power Supply Breaker Did Not Adequately Address Effect of Loss of Control Power.Performed Independent Assessment ML18064A8781995-08-28028 August 1995 LER 95-008-00:on 950728,discovered During Design Change Testing That None of Four Containment High Pressure Channels Would Initiate Rt.Caused by Programmatic Deficiencies. Reviewed Selected Tests & Mods from Recent Refueling Outage ML18064A8831995-08-21021 August 1995 LER 95-007-00:on 950720,discovered That 12 Instrument Loops Had V-bolted Type Qualified Cable Splices Connected to Wires W/Exposed Kapton Insulation.Caused by Human Error.All V- Bolted Splices Replaced w/in-line design.W/950821 Ltr 1999-09-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18066A6901999-11-0101 November 1999 Rev 5 to Palisades Nuclear Plant Colr. ML18066A6761999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Palisades Nuclear Plant ML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6351999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Palisades Nuclear Plant ML18066A6771999-08-31031 August 1999 Operating Data Rept Page of MOR for Aug 1999 for Palisades Nuclear Plant ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A6061999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Palisades Nuclear Plant.With 990803 Ltr ML18066A5201999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Palisades Nuclear Plant.With 990702 Ltr ML18066A4841999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Palisades Nuclear Plant.With 990603 Ltr ML18066A6371999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant ML18068A5941999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant.With 990503 Ltr ML18066A4161999-04-0101 April 1999 Rev 4 to COLR, for Palisades Nuclear Plant ML18066A4501999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Palisades Nuclear Plant.With 990402 Ltr ML18066A4671999-03-31031 March 1999 Rev 0 to SIR-99-032, Flaw Tolerance & Leakage Evaluation Spent Fuel Pool Heat Exchanger E-53B Nozzle Palisades Nuclear Plant. ML18068A5351999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Palisades Nuclear Plant.With 990302 Ltr ML18066A3931999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Palisades Nuclear Plant.With 990202 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML20206F6131998-12-31031 December 1998 1998 Consumers Energy Co Annual Rept. with ML18066A3651998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Palisades Nuclear Plant.With 990105 Ltr ML18066A3421998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Palisades Nuclear Plant.With 981202 Ltr ML18066A3301998-11-11011 November 1998 Part 21 Rept Re Potential Safety Hazard Associated with Wrist Pin Assemblies for FM-Alco 251 Engines at Palisades Nuclear Power Plant.Caused by Insufficient Friction Fit Between Pin & Sleeve.Supplier of Pin Will No Longer Be Used ML18068A4921998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Palisades Nuclear Plant.With 981103 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A3181998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Palisades Nuclear Plant ML18066A2901998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Palisades Nuclear Power Plant.With 980903 Ltr ML18066A3191998-08-31031 August 1998 Revised Monthly Operating Rept Data for Aug 1998 for Palisades Nuclear Plant ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237E0301998-07-31031 July 1998 ISI Rept 3-3 ML18066A2701998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Palisades Nuclear Plant.W/980803 Ltr ML18066A2311998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Palisades Nuclear Plant ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A3061998-06-18018 June 1998 SG Tube Inservice Insp. ML20249C4951998-06-17017 June 1998 Rev 1 to EA-GEJ-98-01, Palisades Cycle 14 Disposition of Events Review ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18066A1711998-06-0101 June 1998 Part 21 Rept Re Impact of RELAP4 Excessive Variability on Palisades Large Break LOCA ECCS Results.Change in PCT Between Cycle 13 & Cycle 14 Does Not Constitute Significant Change Per 10CFR50.46 ML18066A1741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Palisades Nuclear Plant.W/980601 Ltr ML18066A2321998-05-31031 May 1998 Revised MOR for May 1998 for Palisades Nuclear Plant ML18068A4701998-05-31031 May 1998 Annual Rept of Changes in ECCS Models Per 10CFR50.46. ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18066A2331998-04-30030 April 1998 Revised MOR for Apr 1998 for Palisades Nuclear Plant ML18068A3461998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Palisades Nuclear Plant.W/980501 Ltr ML18066A3411998-04-22022 April 1998 Rev 0 to EMF-98-013, Palisades Cycle 14:Disposition & Analysis of SRP Chapter 15 Events. ML18065B2071998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Palisades Nuclear Plant.W/980403 Ltr ML20217C2741998-03-31031 March 1998 Independent Review - Is Consumers Energy Method (W Method) of Determining Palisades Nuclear Plant Best Estimate Fluence by Combining Transport Calculation & Dosimetry Measurements Technically Sound & Does It Meet Intent of Pts ML18066A2341998-03-31031 March 1998 Revised MOR for Mar 1998 for Palisades Nuclear Plant ML18068A3041998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Palisades Nuclear Plant.W/980302 Ltr ML18066A2351998-02-28028 February 1998 Revised MOR for Feb 1998 for Palisades Nuclear Plant ML18065B1641998-02-0505 February 1998 Rev 0 to Regression Analysis for Containment Prestressing Sys at 25th Year Surveillance. ML18067A8211998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Palisades Nuclear Plant.W/980203 Ltr 1999-09-30
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NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150..0104 (4195) EXPIRES 4130/98 ESTIMATED BlJIOO< PER RESPONSE TO COMPLY WllH THIS MANDATORY INFORMATION COLLECTION REQUEST: SO.O HRS. REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT LICENSEE EVENT REPORT (LER) BRANCH (T-8 FJJ), U.S. MJCLEAR REGULATORY COMMISSION, WASHINGTON, DC 2055S-0001, AND TO THE PAPERWORK REDUCTION PROJECT (31~11M, OFFICE OF' MANAGEMENT AND BUDGET, WASHINGTON, DC 20503 (See reverse for required number of digits/characters for each block)
DOCKET NUMBER (2) Page (3)
FACILITY NAME (1) CONSUMERS ENERGY COMPANY PALISADES NUCLEAR PLANT 05000255 1 of 5 TITLE (4) LICENSEE EVENT REPORT 97-009- PROCEDURE WEAKNESS IN IMPLEMENTING APPENDIX R SHUTDOWN METHODOLOGY EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR I* SEQUENTIAL NUMBER REVISION NUMBER MONTH DAY YEAR FACILITY NAME DOCKET NUMBER 05000 FACILITY NAME DOCKET NUMBER 09 23 97 97 - 009 - 00 10 23 97 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS *oF 10 CFR§: (Check one or more) (11)
MODE (9) N 20.2201(b) 20.2203(a)(2)(v) 50. 73(a)(2)(i) , 50. 73(a)(2)(iii)
POWER 20.2203(a)(1) 20.2203(a)(3)(i) x 50.73(a)(2)(ii) 50. 73(a)(2)(x)
LEVEL (10) 100 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50. 73(a)(2)(iii) 73.71 I',::r ..
I 20.2203(a)(2)(ii) 20.2203(a)(2)(iii) 20.2203(a)(2)(ivl 20.2203(a)(4) 50.36(c)(1) 50.36(c)(2) 50.73(a)(2)(iv)
- 50. 73(a)(2)(v) 50.73(a)(2)(viil OTHER Specify in Abstract below or in NRC Form 366A LICENSEE CONTACT FOR THIS LER (12)
NAME William L. Roberts, Licensing Engineer TELEPHONE NUMBER (Include Area Code)
(616) 764,.2976 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS TONPRDS D
SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR I YES If ves COMPLETE EXPECTED COMPLETION DATE x I NO EXPECTED SUBMISSION DATE 115)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On September 23, 1997, at 1105 hours0.0128 days <br />0.307 hours <br />0.00183 weeks <br />4.204525e-4 months <br /> with the plant at approximately 100% power, it was
- recognized that an operator action to support an Appendix R program analysis had not been implemented in the appropriate Off-Normal Procedure (ONP). Specifieally ONP 25.2, "Alternate Safe Shutdown.Procedure" did not include the action to trip all four primary coolant pumps if the control room had to be evacuated. Instead, the procedure directed the control room operators to
"... trip two primary coolant pumps and leave two operating ... ". Once the control room is evacuated, no instrumentation is identified to provide the operational status of the primary coolant pumps or the status of the component cooling water to the primary coolant pump motor and seals.
It has been identified that a fire-initiated hot short could cause one of the component cooling water containment isolation valves to spuriously close, isolating cooling flow to the primary coolant pumps. Palisad~s' J?rifl1ary coolant pump operat_ion_ has_ not been analyzecj for operati_on without - .
seal or motor bearing cooling. The manufacturer indicates that no damage to the seal or pump motor will occur if operated without cooling for no more than ten minutes. ONP 25.2 has been revised to require tripping of all four primary coolant pumps when evacuating of the control room.
Having not implemented the action to support the analysis is contrary to 10 CFR 50 Appendix R direction that during post fire shutdown, ... the fission product barrier shall not be affected, i.e ... there shall be no ... rupture of primary coolant boundary. This is reported as a condition outside of the plant's design basis.
9710300112 971023 5 PDR ADOCK 0500025 s PDR
NRC FORM 366a U.S. NUCLEAR REGULATORY COMMISSION 4195 LICENSEE EVENT REPORT {LER)
TEXT CONTINUATION FACILITY NAME 111 DOCKET12l LER NUMBER 51 PAGE
_CONSUMERS ENERGY COMPANY PALISADES NUCLEAR PLANT 05000255 YEAR I SEQUENTIAL NUMBER REVISION NUMBER 2 OF 5 97 - 00 9 - 00 TEXT (If more space 1s required, use add1t1onal copies of NRC Form 366A) (17)
EVENT DESCRIPTION On September 23, 1997, at 1105 hours0.0128 days <br />0.307 hours <br />0.00183 weeks <br />4.204525e-4 months <br /> with the plant at approximately 100% power, it was recognized that an operator action to support an Appendix R program analysis had not been implemented in the appropriate Off-Normal Procedure (ONP). Specifically, ONP 25.2, "Alternate Safe Shutdown Procedure" did not include the action to trip all four primary coolant pumps if the control room had to be evacuated. Instead, the procedure directed the control room operators to
"... trip two primary coolant pumps and leave two operating ... ".
There is no instrumentation external to the control room identified or analyzed to provide the operational status of the primary coolant pumps or the status of the component cooling water to the primary coolant pump motors and seals. It has been identified that a fire-initiated hot short could cause one of the component cooling water contai.nment isolation valves to close, isolating cooling flow to the primary coolant pumps. Palisades primary coolant pump operation has not .
been analyzed for operation without seal or motor bearing cooling beyond the ten-minute period cited by the manufacturer. A revision to ONP 25.2 was initiated and the procedure change reflecting the tripping of all four primary coolant pumps was issued the next day.
- ANALYSIS OF EVENT The Palisades Plant is a pressurized water reactor with two steam generators and four primary coolant pumps. Water from the component cooling water (CCW) system flows into the containment and provides cooling for each primary coolant pump seal and motor bearing oil.
Beginning in 1994, an Appendix R Enhancement Plan was established to reconstitute the Appendix R analyses and correct identified problems. Rather than recreating or revising existing Appendix R documents, the Enhancement Plan created new analyses to assess and document compliance with requirements.
New analyses were performed based on the assumptions that loss of offsite power may not be the most limiting event. These analyses recognized that if offsite power was not lost, the potential existed for the primary coolant pumps to rerr~in operating. If two of the four primary coolant
. pumpswere-allowed--to remain inoperation following a fire, then component cooling water: pump.
power, control circuitry, and system flow instrumentation would also have to be reviewed to determine what affect the fire had on their operation. These functions would need to be verified as operating once the control room was evacuated to support the continued operation of the primary coolant pumps or the two operating pumps would have to be tripped.
It was decided that if evacuation of the control room was required, then the appropriate action for Palisades would be to trip all four primary coolant pumps rather than trip two and leave two running. Without the pumps operating, a natural circulation cool down is achievable for the
NRC FORM 366a U.S. NUCLEAR REGULATORY COMMISSION J
4195
. LICENSEE EVENT REPORT (LER) g TEXT CONTINUATION FACILITY NAME 11 l DOCKET12l LER NUMBER 16l CONSUMERS ENERGY COMPANY PALISADES NUCLEAR PLANT 05000255 YEAR I SEQUENTIAL NUMBER REVISION NUMBER 5
97 - 00 9 - 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) postulated event.
Tripping all four primary coolant pumps and other conclusions reached as a result of the Appendix R Enhancement Plan reviews were documented in a number of new analyses. It was recognized
.that revisions would be needed to Off Normal Procedure (ONP) 25.2, " Alternate Safe Shutdown Procedure" as a result of these conclusions. These revisions were identified and presented to the ONP 25.2 procedure sponsor in the form of a marked-up version of the procedure. Review of ~~e proposed revision containing the recommended changes to ONP 25.2 determined that the guidance to trip all four prima*ry coolant pumps when evacuating the control room, as prescribed by analysis, was not included. It was also determined that an independent technical review of the proposed revision was not completed; thus, it was never verified that all of the required revisions were included in the document submitted to the procedure sponsor.
Subsequently, Revision 8 to ONP 25.2, a comprehensive revision intended to incorporate the results of the Appendix R Enhancement Plan analyses, was issued in March of 1996. This revision maintained its original direction to trip two and leave two primary coolant pumps running when evacuating the control room. Without indication of the status of CCW flow to the containment being required by procedure, it could be assumed that following evacuation of the control room a hot short could cause one of the three CCW containment isolation valves to close, t~ereby isolating cooling flow to the primary coolant pump seals and motor bearings without operator knowledge.
SAFETY SIGNIFICANCE Without cooling flow, it is assumed that the pump seal would eventually fail in such a way as to create a primary coolant system leak in the area of the pump shaft and seal. This is contrary to the 10 CFR Part 50 Appendix R direction that during post fire shutdown, ... the fission product barrier shall not be affected, i.e .... there shall be no ... rupture of the primary coolant boundary.
For this event to occur, a fire would have to (a) result in evacuation of the control room, (b) result in a hot short that would cause closure of one of the component cooling water valves to the
__containment, (c).notresultin a loss-of offsite power-and (d) not result in a manual or automatic trip of the primary coolant pumps. Our reviews have determined that this event is highly unlikely to occur. The overall impact on plantrisk, resultant from the absence of specific direction to "trip all four primary coolant pumps when evacuating the control room" is, therefore, considered minimal.
NRC FORM 366a U.S. NUCLEAR REGULATORY COMMISSION
~I 4195 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION r;J FACILITY NAME 11 l DOCKETl2l LER NUMBER 6l CONSUMERS ENERGY COMPANY PALISADES NUCLEAR PLANT 05000255 YEAR I SEQUENTIAL NUMBER REVISION NUMBER 5
97 - 00 9 - 00 TEXT (If more space 1s required, use add1t1onal copies of NRC Form 366A) (17)
CAUSE OF THE EVENT The cause of the event is a human error. The engineer identifying and transmitting requested changes to the procedure sponsor failed to properly communicate the requirement for tripping all four primary coolant pumps prior to evacuation of the control room.
A contributing cause for this event is that the process for compiling information from the Appendix R analyses does not require a formal. technical review prior to the information being sent to the procedure sponsor.
CORRECTIVE ACTION ACTIONS COMPLETED:
Remedial
- 1. Off Normal Procedure ONP-25.2, "Alternate Safe Shutdown Procedure" was revised to provide guidance for tripping all four primary coolant. pumps.
PROPOSED CORRECTIVE ACTIONS:
Prevent Recurrence
- 1. All Appendix R engineering analyses will be finalized and a review of the engineering*
analyses'will be completed to ensure consistency in their assumptions and conclusions. It will also be verified that the appropriate procedure changes recommended by the analyses have been made.
- 2. The engineering analysis process will be enhanced to require appropriate technical reviews of transmittal documents utilized for procedure development or revisions.
RELATED CORRECTIVE ACTIONS:
LER 97-008 entitled "Spurious Valve Operation Could Result In Loss of Shutdown Capabilities Per 10 CFR 50, Appendix R, Section 111.L" was transmitted to the NRC in a letter dated October 10, 1997. One of the corrective actions committed in response to that event is applicable to preventing recurrence of the condition described in this event report and is restated here as follows.
NRC FORM 366a U.S. NUCLEAR REGULATORY COMMISSION 4195 LICENSEE EVENT REPORT (LER) g
- TEXT CONTINUATION I
FACILITY NAME 11 l DOCKETl2l LER NUMBER *61 YEAR SEQUENTIAL REVISION CONSUMERS ENERGY COMPANY NUMBER NUMBER 05000255 5 PALISADES NUCLEAR PLANT 97 - 00 9 - 00 TEXT (If more space 1s required, use additional copies of NRC Form 366A) (17)
"A method will be developed or enhanced to screen Palisades changes, both physical and procedural, whereby areas potentially affected by the change can be identified so that appropriate Appendix R reviews are performed. Change types to be screened include the following: modifications, Operating Procedure changes, Surveillance Procedure changes, Engineering Analyses which change design basis inputs, and FSAR changes."
ADDITIONAL INFORMATION A similar condition was reported under LER 97-008.