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| {{#Wiki_filter:REQULAT INFORMATION DISTRIBUTION | | {{#Wiki_filter:REQULAT INFORMATION DISTRIBUTION ~TEM (RIDS) |
| ~TEM (RIDS)ACCESSION NBR: 8705120244 DOC.DATE: 87/05/06 NOTARIZED: | | ACCESSION NBR: 8705120244 DOC. DATE: 87/05/06 NOTARIZED: NO DOCKET ¹ FACIL: STN-50-528 Palo Verde Nuclear Station> Uni t 1> Ari zona Pub li 05000528 AUTH. NAME AUTHOR AFFILIATION BRADISH> T. R. Arizona Nuclear'o!.'er Prospect ( formerlM Ari zona Public Serv HAYNES> J. Q. AT izona Nuclear Pouer Prospect (formerly Ari zona Public Serv REC IP. NAME RECIPIENT AFFILIATION BUB JECT: LER 87-013-00: on 870408> Limiting Condition for Operation |
| NO DOCKET¹FACIL: STN-50-528 Palo Verde Nuclear Station>Uni t 1>Ari zona Pub li 05000528 AUTH.NAME AUTHOR AFFILIATION BRADISH>T.R.Arizona Nuclear'o!.'er Prospect (formerlM Ari zona Public Serv HAYNES>J.Q.AT izona Nuclear Pouer Prospect (formerly Ari zona Public Serv REC IP.NAME RECIPIENT AFFILIATION BUB JECT: LER 87-013-00: | | . 3 0 3 entered due to inoperability of ESF pump room air exhaust sos. Caused bM cognitive personnel error Memo sen+ to~ |
| on 870408>Limiting Condition for Operation.3 0 3 entered due to inoperability of ESF pump room air exhaust sos.Caused bM cognitive personnel error~Memo sen+to onsite managers reminding of responsibilities. | | onsite managers reminding of responsibilities. W/870506 I+r. |
| W/870506 I+r.DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR l ENCL l SIZE: TITLE: 50.73 Licensee Event Report (LER)>Incident Rpt>etc.NOTES: Standardi zed plant.M.Davis>NRR: iCg.05000528 RECIPIENT ID CODE/NAME PD5 LA LICITRA E INTERNAL: ACRS MI CHELBON AEOD/DOA AEOD/DSP/TPAB NRR/DEBT/ADE NRR/DEST/CEB NRR/DEST/ICBB NRR/DEBT/MTB NRR/DEST/RSB NRR/DLPG/HFB NRR/DOEA/EAB NRR/DREP/RAB NR A LRB EQ FIL 02 QN FILE 01 EXTERNAL: EQ8cG QROH>M LPDR NBIC HARRIS>J NOTES: COPIES LTTR ENCL 1 1 1 1 1 0 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 5 5 1 1 1 1 REC IP I ENT ID CODE/NAME PD5 PD DAVIS>M*CRS MOELLER AEOD/DSP/ROAB DEQRO NRR/DEST/ADS NRR/DEST/ELB NRR/DEBT/MEB NRR/DEST/PSB h!RR/DEST/SGB NRR/DLPG/GAB NRR/DREP/EPB NRR/DREP/RPB h!RR/PMAS/PTSB RES SPEIS>T H ST LOBBY WARD NRC PDR NBIC MAYS>G COP IEB LTTR Er,'CL 1 1 1 1 1 1 2 2 1 1 1 0 1 1.1 1 1 1 1 1 1 1 1 2'1 1 1 1 1 1 1 1 TOTAL, NUMBER OF COPIES REQUIRED: LT1R 44 ENCL 42 I | | DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR l ENCL l SIZE: |
| NAC Form Sdd (D.BS)LICENSEE EVENT REPORT (LER)VS.NUCLEAR REOULATOAY COMMISSION APPAOVED OMB NO.2)500)04 EXPIAES:~/21/DS FACILITY NAME (I)Palo Verde Unit 1 TITLE lcl DOCKET NUMBER (2)0 5 0 0 052 PA 2 or-0 3 REPORT DATE (7)LER NUMBER (5)EVEN'1 DATE ISI OTHEA FACILITIES INVOLVED (5)DOCKET NUMBER(5)0 5 0 0 0 FAC/LITY NAMES REVS'ONTH NUMBER SEQUENT/AL NUMDDtl oy DAY YEAR YEAR"os(: DAY YEAR MONTH N A Entry Into Technical Specification LCO 3.0.3 Due to Personnel Error 0 4 088 787 013 00 05 06 7 N A 0 5 0 0 0 OPERATINO MODE (DI POWER LEYEL 1 0 0 50.72(cl(2)(lrl 50,72(~)(2)(rl 50,72(~)12)(rS)50 72(402)(rill)(Al 50.72(c)(2l(rill)IS)50.72(cl(2)(cl 20.405(c)20,402(dl 20.405(~)(1)(l)20.405(~)(I)IQ)20.405(~I()l(iill 20,4N(c)(I)I lv I 20.405(~l(1)(v)50.25Ic)(II 50.2dlc)(2) 50.72(cl(2I(l) 50.72(c)(2)
| | TITLE: 50. 73 Licensee Event Report (LER)> Incident Rpt> etc. |
| IDI 50.7 2 Ic I (2 I (ill)LICENSEE CONTACT FOA THIS LER 112I THIS REPORT IS SUBMITTED PURSUANT TO THE REOUIREMENTS OF 10 CFR ()t IChcch onc or morc of thc folforrind/(Ill 72.71(III 72.71(c)OTHER/Specify/n AO/rrcct hclow cnt/ln ycct, HIIC form d//SAI NAME T.R.Bradish, Compliance Supervisor (Ext.6936)TELEPHONE NUMBER AREA CODE 602 932-5 300 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPOR'7 (12)CAUSE SYSTEM COMPONENT MANUFAC.TVRER EPORTABLE TO NPRDS:";rgb'P()rtg,'c VLE sYsTE COMPONENT MANUFAC.TVRER Ay'j,acr Yn 4 y>>y-'O NPRDS'r.A(tj)S 1!kP~'j%i5i SUPPLEMENTAL REPOR'T EXPECTED 114)YES Ilf ycr, comp/crt E/IPECTED St/dc//SSIOH DATE/ABSTRACT ILrmlt to f400 cpcccr.I.c..cpprocimctcry fiftccn rind/c g>>cc rypcrrrlt>>n
| | NOTES: Standardi zed plant. M. Davis> NRR: iCg. 05000528 RECIPIENT COPIES REC IP I ENT COP IEB ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR Er,'CL PD5 LA 1 PD5 PD 1 1 LICITRA E 1 DAVIS> M 1 1 INTERNAL: ACRS MICHELBON 1 1 *CRS MOELLER 1 1 AEOD/DOA AEOD/DSP/ROAB 2 2 AEOD/DSP/TPAB DEQRO 1 1 NRR/DEBT/ADE 1 0 NRR/DEST/ADS 1 0 NRR/DEST/CEB 1 1 NRR/DEST/ELB 1 1. |
| /mod lid)HO iox IW+k:.>>>CNioo MONTH OAY YEAR EXPECTED SUBMISSION DATE (15)At approximately 1351 MST on April 8, 1987, Palo Verde Unit 1 was in Mode 1 (POt)tER OPERATION) at 100 percent power when Technical Specification (T.S.)Limiting Condition for Operation (LCO)3.0.3 was en'tered due to the inoperability of the Engineered Safety Features (ESF)pump room air exhaust systems.T.S.LCO 3.0.3 was exited at approximately 1541 on April 8, 1987 following the successful completion of Surveillance Test 73ST-9HF01 (Fuel Building AFU Airflow Capacity and Pressurization Test).This event was discovered by a System Engineer (utility non-licensed) during a review of 73ST-9HFOl for future revisions.
| | NRR/DEST/ICBB 1 1 NRR/DEBT/MEB 1 1 NRR/DEBT/MTB NRR/DEST/PSB 1 NRR/DEST/RSB h!RR/DEST/SGB 1 1 NRR/DLPG/HFB 1 1 NRR/DLPG/GAB 1 1 NRR/DOEA/EAB 1 1 NRR/DREP/EPB 1 |
| The root cause of this event was a cognitive personnel error by a system engineer (contractor non-licensed) in that he did not properly complete the"Surveillance Test Package Review Sheet".The responsible system engineer is no longer employed by Arizona Nuclear Power Project.As corrective action, a memo has been sent to onsite Managers to remind them it is the responsibility of each performance group to track their own Conditional ST's and any portion of a scheduled ST that could'ot be performed in its entirety to ensure their status is maintained current.No similar events have been reported where improper documentation of*a partial surveillance test has resulted in exceeding a surveillance requirement.
| | ' |
| 8705120244 87050b PDR ADOCK 05000528 8 PDR HRC corm Sdd
| | 1 NRR/DREP/RAB 1 1 NRR/DREP/RPB 2 NR A LRB 1 1 h!RR/PMAS/PTSB 1 EQ FIL 02 1 RES SPEIS> T 1 1 QN FILE 01 1 1 EXTERNAL: EQ8cG QROH> M 5 5 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 NBIC HARRIS> J 1 1 NBIC MAYS> G 1 1 NOTES: |
| | TOTAL, NUMBER OF COPIES REQUIRED: LT1R 44 ENCL 42 |
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| NRC Fosw 355A 1903 I e LICENSEE EVENT REPORT ILERI TEXT CONTINUATION U 3 NUCLEAR REOULATORY COMMISSION APPROVED OMS NO 3150 0104 EXPIRES: S/31/SS FACILITY NAME ITI DOCKET NUMSER l21 LER NUMSER I~I YEAR'~i.5EOUENTSAL PRI iEYOIOSS MUM TA i<i NQMQTA~AOE (3I Palo Verde Unit 1 TEXT Ill ssssss ssssss is FSss'st.ws oddeewl HJIC Fspnn~'sl IIT)0 5 0 0 0 5 2 8 8 7 013-00 0 2 OF 0 3 At approximately 1351 MST on April 8, 1987, Palo Verde Unit 1 was in Mode 1 (POWER OPERATION) at 100 percent power when Technical Specification (T.S.)Limiting Condition for Operation (LCO)3.0.3 was entered due to the inoperability of the Engineered Safety Features (ESF)(JE)pump room air exhaust systems (AHU).In accordance with T.S.LCO 3.0.3, actions were initiated to place the unit in a Mode in which the ESF pump room air exhaust cleanup systems are not required to be operable.T.S.LCO 3.0.3 was exited, at approximately 1541 on April 8, 1987 following the successful completion of surveillance test 73ST-9HF01 (Fuel Building AFU Airflow Capacity and Pressurization Test).The duration of this event was 1 hour and 50 minutes.On April 8, 1987, a system engineer (utility non-licensed) was reviewing the January 31, 1986 performance of surveillance test (ST)73ST-9HF01 for future revisions when he discovered that the ESF pump room air exhaust cleanup systems had not been surveillance tested as was indicated on the"Surveillance Test Package Review Sheet"..The system engineer discovered an entry in the surveillance test log that stated that the ESF pump room air exhaust cleanup systems were due to be surveillance tested in October 1986.In accordance with T.S.4.7.8.b.l, b.3, d.l and d.2, the ESF pump room air exhaust cleanup systems must be demonstrated operable once every 18 months.The previous test had been completed satisfactorily in April, 1985.The surveillance test interval, including the maximum allowable extension of 25 percent, was exceeded in March 1987.Upon notification of the finding, the Unit 1 Shift Supervisor (utility licensed)declared the ESF pump room air exhaust cleanup systems inoperable and entered the unit into T.S.LCO 3.0.3.The ESF pump room air exhaust cleanup system was declared operable and T.S.LCO 3.0.3 exited at approximately 1541 following successful completion of the surveillance testing.The root cause of this event was a cognitive personnel error by the system engineer (contractor non-licensed) in that he did not properly complete the"Surveillance Test Package Review Sheet".The responsible system engineer is no longer employed by Arizona Nuclear Power Project.The improper completion of the Surveillance Test Package Review Sheet" resulted in the Surveillance Program Control Group scheduling the next performance of 73ST-9HF01 for June 10, 1987.As a result, the surveillance interval for the ESF pump room air exhaust cleanup system was exceeded.Improper completion of the"Surveillance Test Package Review Sheet" is contrary to approved procedural controls.As corrective action, a memo has been sent to all onsite Managers to remind them it is the responsibility of each performance group to track their own Conditional ST's and any portion of a scheduled ST that could not be performed in its entirety to ensure their status is maintained current.'sRC s ORM 355A I953s
| | I NAC Form Sdd VS. NUCLEAR REOULATOAY COMMISSION (D.BS) |
| | APPAOVED OMB NO. 2)500)04 LICENSEE EVENT REPORT (LER) EXPIAES: ~ /21/DS FACILITY NAME (I) DOCKET NUMBER (2) PA 2 TITLE lcl Palo Verde Unit 1 0 5 0 0 052 or- 0 3 Entry Into Technical Specification LCO 3.0.3 Due to Personnel Error EVEN'1 DATE ISI LER NUMBER (5) REPORT DATE (7) OTHEA FACILITIES INVOLVED (5) |
| | MONTH DAY YEAR YEAR "os(: |
| | SEQUENT/AL oy REVS'ONTH DAY YEAR FAC/LITY NAMES DOCKET NUMBER(5) |
| | NUMDDtl NUMBER N A 0 5 0 0 0 0 4 088 787 013 00 05 06 7 N A 0 5 0 0 0 OPERATINO THIS REPORT IS SUBMITTED PURSUANT TO THE REOUIREMENTS OF 10 CFR ()t IChcch onc or morc of thc folforrind/ (Ill MODE (DI 20,402(dl 20.405(c) 50.72(cl(2)(lrl 72.71(III POWER 20.405( ~ ) (1)(l) 50.25Ic)(II (ill) 50,72( ~ )(2)(rl 72.71(c) |
| | LEYEL 1 0 0 20.405( ~ )(I)IQ) 50.2dlc)(2) 50,72( ~ )12)(rS) OTHER /Specify /n AO/rrcct hclow cnt/ ln ycct, HIIC form 20.405( ~ I() l(iill 50.72(cl(2I(l) 50 72(402)(rill) (Al d//SAI 20,4N(c) (I ) I lv I 50.72(c)(2) IDI 50.72(c) (2l(rill)IS) 20.405( ~ l(1)(v) 50.7 2 Ic I (2 I 50.72(cl(2)(cl LICENSEE CONTACT FOA THIS LER 112I NAME TELEPHONE NUMBER AREA CODE T. R. Bradish, Compliance Supervisor (Ext. 6936) 602 932 5 300 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPOR'7 (12) |
| | :";rgb'P()rtg,'c MANUFAC. EPORTABLE Ay'j,acr Yn 4 y>> |
| | CAUSE SYSTEM COMPONENT VLE sYsTE COMPONENT MANUFAC. y-'O TVRER TO NPRDS TVRER NPRDS 'r.A(tj)S 1!kP~'j%i5i iox IW+k:. >>>CNioo SUPPLEMENTAL REPOR'T EXPECTED 114) MONTH OAY YEAR EXPECTED SUBMISSION DATE (15) |
| | YES Ilfycr, comp/crt E/IPECTED St/dc//SSIOH DATE/ HO ABSTRACT ILrmlt to f400 cpcccr. I.c.. cpprocimctcry fiftccn rind/c g>>cc rypcrrrlt>>n /mod lid) |
| | At approximately 1351 MST on April 8, 1987, Palo Verde Unit 1 was in Mode 1 (POt)tER OPERATION) at 100 percent power when Technical Specification (T.S.) Limiting Condition for Operation (LCO) 3.0.3 was en'tered due to the inoperability of the Engineered Safety Features (ESF) pump room air exhaust systems. T.S. LCO 3.0.3 was exited at approximately 1541 on April 8, 1987 following the successful completion of Surveillance Test 73ST-9HF01 (Fuel Building AFU Airflow Capacity and Pressurization Test). This event was discovered by a System Engineer (utility non-licensed) during a review of 73ST-9HFOl for future revisions. |
| | The root cause of this event was a cognitive personnel error by a system engineer (contractor non-licensed) in that he did not properly complete the "Surveillance Test Package Review Sheet". The responsible system engineer is no longer employed by Arizona Nuclear Power Project. As corrective action, a memo has been sent to onsite Managers to remind them it is the responsibility of each performance group to track their own Conditional ST's and any portion of a scheduled ST that be performed in its entirety to ensure their status is maintained current. |
| | could'ot No similar events have been reported where improper documentation of *a partial surveillance test has resulted in exceeding a surveillance requirement. |
| | 8705120244 87050b PDR ADOCK 05000528 8 PDR HRC corm Sdd |
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| NRC'FoIm 344A 18 83I LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REOUI.ATONY COMMISSION APPROVED OM8 NO 3150 OIOS EXPIRES: 8/31/88 FACILITY NAME 111 Palo Verde Unit 1 TEXT////INvo s/Mco/I/POw'NL vso PROOo'one/P/RC FomI 38//AS/IITI DOCKET NUMEER 111 YEAR o s o o o 528 87 LER NUMEER IEI yes SSOUSNTIAL NUM SR 013 II 4 V IS IO 4 NUM 4 II-0 0~AOE 13)03oF 0 3 The successful completion of 73ST-9HF01 demonstrated the operability of the ESF pump room air exhaust cleanup system.Since the ESF pump room air exhaust cleanup system operated as designed, this event did not affect the safe operation of the plant or the health and safety of the public.There were no structures, components, or systems that were inoperable at the start of the event, other than those described above, that contributed to the event.There were no unusual characteristics of the work location which contributed to the event.There were no automatic or manually initiated safety system responses. | | NRC Fosw 355A 1903 I e U 3 NUCLEAR REOULATORY COMMISSION LICENSEE EVENT REPORT ILERI TEXT CONTINUATION APPROVED OMS NO 3150 0104 EXPIRES: S/31/SS FACILITY NAME ITI DOCKET NUMSER l21 LER NUMSER I ~ I ~ AOE (3I YEAR '~i. 5EOUENTSAL PRI iEYOIOSS i<i MUM TA NQMQTA Palo Verde Unit TEXT Illssssss ssssss is FSss'st. |
| There were no operator actions which contributed to this event.No similar events have been reported where improper documentation of a partial surveillance test has resulted in exceeding a surveillance requirement. | | 1 ws oddeewl HJIC Fspnn ~'sl IIT) 0 5 0 0 0 5 2 8 8 7 013 00 0 2 OF 0 3 At approximately 1351 MST on April 8, 1987, Palo Verde Unit 1 was in Mode 1 (POWER OPERATION) at 100 percent power when Technical Specification (T.S.) Limiting Condition for Operation (LCO) 3.0.3 was entered due to the inoperability of the Engineered Safety Features (ESF)(JE) pump room air exhaust systems (AHU). In accordance with T.S. LCO 3.0.3, actions were initiated to place the unit in a Mode in which the ESF pump room air exhaust cleanup systems are not required to be operable. T.S. LCO 3.0.3 was exited, at approximately 1541 on April 8, 1987 following the successful completion of surveillance test 73ST-9HF01 (Fuel Building AFU Airflow Capacity and Pressurization Test). The duration of this event was 1 hour and 50 minutes. |
| 4/IC I OIIM 344A 188)I I jl l l Arizona Nuclear Power Project P.o, BOX 52034~PHOENIX, ARIZONA 85072-2034 192-00203-JGH/TRB/MJC May 6, 1987 U.S.Nuclear Regulatory Commission Document Control Desk Washington, D.C.20555 | | On April 8, 1987, a system engineer (utility non-licensed) was reviewing the January 31, 1986 performance of surveillance test (ST) 73ST-9HF01 for future revisions when he discovered that the ESF pump room air exhaust cleanup systems had not been surveillance tested as was indicated on the "Surveillance Test Package Review Sheet".. The system engineer discovered an entry in the surveillance test log that stated that the ESF pump room air exhaust cleanup systems were due to be surveillance tested in October 1986. |
| | In accordance with T.S. 4.7.8.b.l, b.3, d.l and d.2, the ESF pump room air exhaust cleanup systems must be demonstrated operable once every 18 months. The previous test had been completed satisfactorily in April, 1985. The surveillance test interval, including the maximum allowable extension of 25 percent, was exceeded in March 1987. |
| | Upon notification of the finding, the Unit 1 Shift Supervisor (utility licensed) declared the ESF pump room air exhaust cleanup systems inoperable and entered the unit into T.S. LCO 3.0.3. The ESF pump room air exhaust cleanup system was declared operable and T.S. LCO 3.0.3 exited at approximately 1541 following successful completion of the surveillance testing. |
| | The root cause of this event was a cognitive personnel error by the system engineer (contractor non-licensed) in that he did not properly complete the "Surveillance Test Package Review Sheet". The responsible system engineer is no longer employed by Arizona Nuclear Power Project. The improper completion of the Surveillance Test Package Review Sheet" resulted in the Surveillance Program Control Group scheduling the next performance of 73ST-9HF01 for June 10, 1987. As a result, the surveillance interval for the ESF pump room air exhaust cleanup system was exceeded. Improper completion of the "Surveillance Test Package Review Sheet" is contrary to approved procedural controls. |
| | As corrective action, a memo has been sent to all onsite Managers to remind them it is ST's the responsibility of each performance group to track their own Conditional and any portion of a scheduled ST that could not be performed in its entirety to ensure their status is maintained current. |
| | 'sRC s ORM 355A I953s |
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| | NRC'FoIm 344A U.S. NUCLEAR REOUI.ATONY COMMISSION 18 83I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVED OM8 NO 3150 OIOS EXPIRES: 8/31/88 FACILITY NAME 111 DOCKET NUMEER 111 LER NUMEER IEI ~ AOE 13) |
| | YEAR yes SSOUSNTIAL II4 V IS IO 4 NUM SR NUM 4 II Palo Verde Unit 1 o s o o o 528 87 013 0 0 03oF 0 3 TEXT ////INvo s/Mco /I /POw'NL vso PROOo'one/P/RC FomI 38//AS/ IITI The successful completion of 73ST-9HF01 demonstrated the operability of the ESF pump room air exhaust cleanup system. Since the ESF pump room air exhaust cleanup system operated as designed, this event did not affect the safe operation of the plant or the health and safety of the public. |
| | There were no structures, components, or systems that were inoperable at the start of the event, other than those described above, that contributed to the event. |
| | There were no unusual characteristics of the work location which contributed to the event. There were no automatic or manually initiated safety system responses. |
| | There were no operator actions which contributed to this event. |
| | No similar events have been reported where improper documentation of a partial surveillance test has resulted in exceeding a surveillance requirement. |
| | 4/IC I OIIM 344A 188)I |
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| | Arizona Nuclear Power Project P.o, BOX 52034 ~ PHOENIX, ARIZONA85072-2034 192-00203-JGH/TRB/MJC May 6, 1987 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 |
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| ==Subject:== | | ==Subject:== |
| Palo Verde Nuclear Generating Station (PVNGS)Unit 1 Docket No.STN 50-528 Licensee Event Report 87-013-00 File: 87-020-404 | | Palo Verde Nuclear Generating Station (PVNGS) |
| | Unit 1 Docket No. STN 50-528 Licensee Event Report 87-013-00 File: 87-020-404 |
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| | ==Dear Sirs:== |
| | |
| | Attached please find Licensee Event Report (LER) No. 87-013-00 prepared and submitted pursuant to 10 CFR 50.73. In accordance with 10 CFR 50,.73(d), we are herewith forwarding a copy of the LER to the Regional Administrator of the Region V Office. |
| | If you have any questions, please contact T. R. Bradish, Compliance Supervisor at (602) 932-5300 Ext. 6936. |
| | Very tru y yours, l/6 J. |
| | yr~ |
| | G. Haynes Vice President Nuclear Production JGH/MJC/cld Attachment CCI 0. M. DeMichele (all w/a) |
| | E. E. Van Brunt, Jr. |
| | J. B. Martin R. P. Zimmerman R. C. Sorensen E. A. Licitra A. C. Gehr INPO Records Center |
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| ==Dear Sirs:==
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| Attached please find Licensee Event Report (LER)No.87-013-00 prepared and submitted pursuant to 10 CFR 50.73.In accordance with 10 CFR 50,.73(d), we are herewith forwarding a copy of the LER to the Regional Administrator of the Region V Office.If you have any questions, please contact T.R.Bradish, Compliance Supervisor at (602)932-5300 Ext.6936.Very tru y yours, l/6 yr~J.G.Haynes Vice President Nuclear Production JGH/MJC/cld Attachment CCI 0.M.E.E.J.B.R.P.R.C.E.A.A.C.INPO DeMichele Van Brunt, Jr.Martin Zimmerman Sorensen Licitra Gehr Records Center (all w/a)
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
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Text
REQULAT INFORMATION DISTRIBUTION ~TEM (RIDS)
ACCESSION NBR: 8705120244 DOC. DATE: 87/05/06 NOTARIZED: NO DOCKET ¹ FACIL: STN-50-528 Palo Verde Nuclear Station> Uni t 1> Ari zona Pub li 05000528 AUTH. NAME AUTHOR AFFILIATION BRADISH> T. R. Arizona Nuclear'o!.'er Prospect ( formerlM Ari zona Public Serv HAYNES> J. Q. AT izona Nuclear Pouer Prospect (formerly Ari zona Public Serv REC IP. NAME RECIPIENT AFFILIATION BUB JECT: LER 87-013-00: on 870408> Limiting Condition for Operation
. 3 0 3 entered due to inoperability of ESF pump room air exhaust sos. Caused bM cognitive personnel error Memo sen+ to~
onsite managers reminding of responsibilities. W/870506 I+r.
DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR l ENCL l SIZE:
TITLE: 50. 73 Licensee Event Report (LER)> Incident Rpt> etc.
NOTES: Standardi zed plant. M. Davis> NRR: iCg. 05000528 RECIPIENT COPIES REC IP I ENT COP IEB ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR Er,'CL PD5 LA 1 PD5 PD 1 1 LICITRA E 1 DAVIS> M 1 1 INTERNAL: ACRS MICHELBON 1 1 *CRS MOELLER 1 1 AEOD/DOA AEOD/DSP/ROAB 2 2 AEOD/DSP/TPAB DEQRO 1 1 NRR/DEBT/ADE 1 0 NRR/DEST/ADS 1 0 NRR/DEST/CEB 1 1 NRR/DEST/ELB 1 1.
NRR/DEST/ICBB 1 1 NRR/DEBT/MEB 1 1 NRR/DEBT/MTB NRR/DEST/PSB 1 NRR/DEST/RSB h!RR/DEST/SGB 1 1 NRR/DLPG/HFB 1 1 NRR/DLPG/GAB 1 1 NRR/DOEA/EAB 1 1 NRR/DREP/EPB 1
'
1 NRR/DREP/RAB 1 1 NRR/DREP/RPB 2 NR A LRB 1 1 h!RR/PMAS/PTSB 1 EQ FIL 02 1 RES SPEIS> T 1 1 QN FILE 01 1 1 EXTERNAL: EQ8cG QROH> M 5 5 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 NBIC HARRIS> J 1 1 NBIC MAYS> G 1 1 NOTES:
TOTAL, NUMBER OF COPIES REQUIRED: LT1R 44 ENCL 42
I NAC Form Sdd VS. NUCLEAR REOULATOAY COMMISSION (D.BS)
APPAOVED OMB NO. 2)500)04 LICENSEE EVENT REPORT (LER) EXPIAES: ~ /21/DS FACILITY NAME (I) DOCKET NUMBER (2) PA 2 TITLE lcl Palo Verde Unit 1 0 5 0 0 052 or- 0 3 Entry Into Technical Specification LCO 3.0.3 Due to Personnel Error EVEN'1 DATE ISI LER NUMBER (5) REPORT DATE (7) OTHEA FACILITIES INVOLVED (5)
MONTH DAY YEAR YEAR "os(:
SEQUENT/AL oy REVS'ONTH DAY YEAR FAC/LITY NAMES DOCKET NUMBER(5)
NUMDDtl NUMBER N A 0 5 0 0 0 0 4 088 787 013 00 05 06 7 N A 0 5 0 0 0 OPERATINO THIS REPORT IS SUBMITTED PURSUANT TO THE REOUIREMENTS OF 10 CFR ()t IChcch onc or morc of thc folforrind/ (Ill MODE (DI 20,402(dl 20.405(c) 50.72(cl(2)(lrl 72.71(III POWER 20.405( ~ ) (1)(l) 50.25Ic)(II (ill) 50,72( ~ )(2)(rl 72.71(c)
LEYEL 1 0 0 20.405( ~ )(I)IQ) 50.2dlc)(2) 50,72( ~ )12)(rS) OTHER /Specify /n AO/rrcct hclow cnt/ ln ycct, HIIC form 20.405( ~ I() l(iill 50.72(cl(2I(l) 50 72(402)(rill) (Al d//SAI 20,4N(c) (I ) I lv I 50.72(c)(2) IDI 50.72(c) (2l(rill)IS) 20.405( ~ l(1)(v) 50.7 2 Ic I (2 I 50.72(cl(2)(cl LICENSEE CONTACT FOA THIS LER 112I NAME TELEPHONE NUMBER AREA CODE T. R. Bradish, Compliance Supervisor (Ext. 6936) 602 932 5 300 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPOR'7 (12)
- ";rgb'P()rtg,'c MANUFAC. EPORTABLE Ay'j,acr Yn 4 y>>
CAUSE SYSTEM COMPONENT VLE sYsTE COMPONENT MANUFAC. y-'O TVRER TO NPRDS TVRER NPRDS 'r.A(tj)S 1!kP~'j%i5i iox IW+k:. >>>CNioo SUPPLEMENTAL REPOR'T EXPECTED 114) MONTH OAY YEAR EXPECTED SUBMISSION DATE (15)
YES Ilfycr, comp/crt E/IPECTED St/dc//SSIOH DATE/ HO ABSTRACT ILrmlt to f400 cpcccr. I.c.. cpprocimctcry fiftccn rind/c g>>cc rypcrrrlt>>n /mod lid)
At approximately 1351 MST on April 8, 1987, Palo Verde Unit 1 was in Mode 1 (POt)tER OPERATION) at 100 percent power when Technical Specification (T.S.) Limiting Condition for Operation (LCO) 3.0.3 was en'tered due to the inoperability of the Engineered Safety Features (ESF) pump room air exhaust systems. T.S. LCO 3.0.3 was exited at approximately 1541 on April 8, 1987 following the successful completion of Surveillance Test 73ST-9HF01 (Fuel Building AFU Airflow Capacity and Pressurization Test). This event was discovered by a System Engineer (utility non-licensed) during a review of 73ST-9HFOl for future revisions.
The root cause of this event was a cognitive personnel error by a system engineer (contractor non-licensed) in that he did not properly complete the "Surveillance Test Package Review Sheet". The responsible system engineer is no longer employed by Arizona Nuclear Power Project. As corrective action, a memo has been sent to onsite Managers to remind them it is the responsibility of each performance group to track their own Conditional ST's and any portion of a scheduled ST that be performed in its entirety to ensure their status is maintained current.
could'ot No similar events have been reported where improper documentation of *a partial surveillance test has resulted in exceeding a surveillance requirement.
8705120244 87050b PDR ADOCK 05000528 8 PDR HRC corm Sdd
NRC Fosw 355A 1903 I e U 3 NUCLEAR REOULATORY COMMISSION LICENSEE EVENT REPORT ILERI TEXT CONTINUATION APPROVED OMS NO 3150 0104 EXPIRES: S/31/SS FACILITY NAME ITI DOCKET NUMSER l21 LER NUMSER I ~ I ~ AOE (3I YEAR '~i. 5EOUENTSAL PRI iEYOIOSS i<i MUM TA NQMQTA Palo Verde Unit TEXT Illssssss ssssss is FSss'st.
1 ws oddeewl HJIC Fspnn ~'sl IIT) 0 5 0 0 0 5 2 8 8 7 013 00 0 2 OF 0 3 At approximately 1351 MST on April 8, 1987, Palo Verde Unit 1 was in Mode 1 (POWER OPERATION) at 100 percent power when Technical Specification (T.S.) Limiting Condition for Operation (LCO) 3.0.3 was entered due to the inoperability of the Engineered Safety Features (ESF)(JE) pump room air exhaust systems (AHU). In accordance with T.S. LCO 3.0.3, actions were initiated to place the unit in a Mode in which the ESF pump room air exhaust cleanup systems are not required to be operable. T.S. LCO 3.0.3 was exited, at approximately 1541 on April 8, 1987 following the successful completion of surveillance test 73ST-9HF01 (Fuel Building AFU Airflow Capacity and Pressurization Test). The duration of this event was 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 50 minutes.
On April 8, 1987, a system engineer (utility non-licensed) was reviewing the January 31, 1986 performance of surveillance test (ST) 73ST-9HF01 for future revisions when he discovered that the ESF pump room air exhaust cleanup systems had not been surveillance tested as was indicated on the "Surveillance Test Package Review Sheet".. The system engineer discovered an entry in the surveillance test log that stated that the ESF pump room air exhaust cleanup systems were due to be surveillance tested in October 1986.
In accordance with T.S. 4.7.8.b.l, b.3, d.l and d.2, the ESF pump room air exhaust cleanup systems must be demonstrated operable once every 18 months. The previous test had been completed satisfactorily in April, 1985. The surveillance test interval, including the maximum allowable extension of 25 percent, was exceeded in March 1987.
Upon notification of the finding, the Unit 1 Shift Supervisor (utility licensed) declared the ESF pump room air exhaust cleanup systems inoperable and entered the unit into T.S. LCO 3.0.3. The ESF pump room air exhaust cleanup system was declared operable and T.S. LCO 3.0.3 exited at approximately 1541 following successful completion of the surveillance testing.
The root cause of this event was a cognitive personnel error by the system engineer (contractor non-licensed) in that he did not properly complete the "Surveillance Test Package Review Sheet". The responsible system engineer is no longer employed by Arizona Nuclear Power Project. The improper completion of the Surveillance Test Package Review Sheet" resulted in the Surveillance Program Control Group scheduling the next performance of 73ST-9HF01 for June 10, 1987. As a result, the surveillance interval for the ESF pump room air exhaust cleanup system was exceeded. Improper completion of the "Surveillance Test Package Review Sheet" is contrary to approved procedural controls.
As corrective action, a memo has been sent to all onsite Managers to remind them it is ST's the responsibility of each performance group to track their own Conditional and any portion of a scheduled ST that could not be performed in its entirety to ensure their status is maintained current.
'sRC s ORM 355A I953s
NRC'FoIm 344A U.S. NUCLEAR REOUI.ATONY COMMISSION 18 83I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVED OM8 NO 3150 OIOS EXPIRES: 8/31/88 FACILITY NAME 111 DOCKET NUMEER 111 LER NUMEER IEI ~ AOE 13)
YEAR yes SSOUSNTIAL II4 V IS IO 4 NUM SR NUM 4 II Palo Verde Unit 1 o s o o o 528 87 013 0 0 03oF 0 3 TEXT ////INvo s/Mco /I /POw'NL vso PROOo'one/P/RC FomI 38//AS/ IITI The successful completion of 73ST-9HF01 demonstrated the operability of the ESF pump room air exhaust cleanup system. Since the ESF pump room air exhaust cleanup system operated as designed, this event did not affect the safe operation of the plant or the health and safety of the public.
There were no structures, components, or systems that were inoperable at the start of the event, other than those described above, that contributed to the event.
There were no unusual characteristics of the work location which contributed to the event. There were no automatic or manually initiated safety system responses.
There were no operator actions which contributed to this event.
No similar events have been reported where improper documentation of a partial surveillance test has resulted in exceeding a surveillance requirement.
4/IC I OIIM 344A 188)I
I jl l
l
Arizona Nuclear Power Project P.o, BOX 52034 ~ PHOENIX, ARIZONA85072-2034 192-00203-JGH/TRB/MJC May 6, 1987 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555
Subject:
Palo Verde Nuclear Generating Station (PVNGS)
Unit 1 Docket No. STN 50-528 Licensee Event Report 87-013-00 File: 87-020-404
Dear Sirs:
Attached please find Licensee Event Report (LER) No. 87-013-00 prepared and submitted pursuant to 10 CFR 50.73. In accordance with 10 CFR 50,.73(d), we are herewith forwarding a copy of the LER to the Regional Administrator of the Region V Office.
If you have any questions, please contact T. R. Bradish, Compliance Supervisor at (602) 932-5300 Ext. 6936.
Very tru y yours, l/6 J.
yr~
G. Haynes Vice President Nuclear Production JGH/MJC/cld Attachment CCI 0. M. DeMichele (all w/a)
E. E. Van Brunt, Jr.
J. B. Martin R. P. Zimmerman R. C. Sorensen E. A. Licitra A. C. Gehr INPO Records Center
II t