ML17326A377: Difference between revisions

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{{#Wiki_filter:U.S.NUCLEAR REGULATORY COMMISSION ENSEE EVENT REPORT LICENSE TYPE 30 57 CAT 58 hlRC F(PM 366 i i77)'f-.--ŽCONTROL BLOCK: Q1{PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
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I 6~o1 M I D C C 2 Q2 0 0 0 0 0 0 0 0 0 0 0 0 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 CON'T~o]RF-o~L~B 0 5 0 0 0 3 6 Q7 1 o 1 QS o 3 7 9 SOURCE 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES
&10 WHILE XN MODE 6,WITH.ONE.DXE EG GENERATOR (DG)OUT OF SERVXCE~Os CONTRACTOR PERSONNEL MISTAKENLY BEGAN TO DETERMINATE THE OPERABLE DG'S STARTING BUS FEED CABLE, BLOWING A FUSE XN THE 1KV INVERTER.THIS RENDERED THE DG INOPERABLE UNTX'L THE DG INVERTER WAS SWITCHED~06 TO AN ALTERNATE SUPPLY, A PERlOD OF 45 MINUTES.THIS EVENT IS NON-CONSERVATIVE IN RESPECT TO T.S.3.8.1.2.b.
~os 80 7 8 7 8 SYSTEM CAUSE CAUSE COMP VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE Q11~7E 072~F Q13 z z z z z z 04~z 076~z 016 9 10 11 12 13 18 19 20 SEOUENTIAL OCCURRENCE REPORT REVISION LERiRP EVENT YEAR REPORT NO.CODE TYPE NO.Q17 REPQRT~O~~Q4 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDP PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER IJLIQ18~Q19~iQ20~i027.o o o o~~023~024 Lg026 z 9 9'" 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 o INVESTXGATION REVEALED THAT CONTRACTOR PERSONNEL WHO WERE INSTALLING A DESIGN CHANGE ON THE INOPERABLE DGi HAD MISTAKENLY STARTED DETERMXNATXNG THE OPERABLE DG1S STARTING BUS FEED CABLE THE LOOSE CABLE CAME XN CONTACT WITH AN ADJACENT TERMINAL BLOCK CAUSING A 80 80 45 80 80 80 7)(zgoo ra~80 NRC USE ONLY o 80 o 0 NAME OF PREPARER PHONE: SHORT CXRCUXT AND BLOWXNG A FUSE XN THE 1KV XNVERTER'7 8, 9 FACILITY~3P METHOD OF STATUS%POWER OTHERSTATUS
~DISCOVERY DISCOVERY DESCRIPTION Q32~A037 7 8 9 10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q LOCATION OF RELEASE Q36~76~Z 033~Z034 NA NA 7 8 9 10 11 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION 7~o0o o o0 Q3 7 z Q3 8 NET 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTION 41 8~OO O Q46 NA 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43'TYPE DESCRIPTION e Z Q42 NA 7 8 9 10 PUBLICITY ISSUED DESCRIPTION
~20~N Q44 NA 7 8 9 10 68 69 SUPPLEMENT TO LER 0 79-042/03L-0 SUPPLEMENT TO CAUSE DESCRIPTION THE INVERTER WAS SWXTCHED TO AN ALTERNATE POWER SUPPLY UNTXL THE FUSE WAS REPLACED.THE INVERTER WAS THEN SWITCHED BACK TO ITS NORMAL POWER SUPPLY.TO PREVENT RECURRENCE g THE CONTRACTOR PERSONNEL WERE G IVEN ADD ITIONA'L TRAINING ON NOVEMBER 08@1979 WHICH REVIEWED THE REQUIREMENTS FOR WORKXNG IN CRITICAL AREAS ON SAFETY RELATED EQUIPMENT.
PARTICULARLY REQUIRE-MENTS.FOR CABLE REMOVAL AND WORK AUTHORIZATIONS.}}

Revision as of 10:47, 23 October 2019

LER 79-042/03L-0:on 791101,while in Mode 6,w/one Diesel Generator Out of svc,1kV Inverter Blew Fuse.Caused by Loose Bus Feed Cable Short Circuiting Inverter While Contractor Personnel Worked on Inoperable Generator
ML17326A377
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 12/03/1979
From:
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17326A376 List:
References
LER-79-042-03L-01, LER-79-42-3L-1, NUDOCS 7912100286
Download: ML17326A377 (2)


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