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=Text=
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{{#Wiki_filter:-,: .... ,
{{#Wiki_filter:',".
consumers
consumers
* Power POWERlNli lllllCHlliAN-S PROlillESS . ',". *Palisades Nuclear Plant:
* Power                                                                                                     *
* 27780 .Blue Star Highway. Covert. Ml 49043 April 27, 1992 **,. .-Nuclear. Regulatory Commission*
* o. G B* Slade
'Document Control Desk WashiDgton, .DC
                                                                                                                                                                        . General Manager POWERlNli lllllCHlliAN-S PROlillESS .
* *. r. *--;. " * .... ,. *.' *
                      *Palisades Nuclear Plant:
* o. G B* Slade . General Manager * .... :*. DOC.KET .50-255 LICENSE *DPR"'20 "'_.  
* 27780 .Blue Star Meinc>ria~. Highway.         Covert.       Ml 49043
* . * * ,. **:.' ,* .. *' . L.ICENSEE EVENT REPORT 92'-024 INADVERTENT' OPENING OF* THE STATiON POWER* .. *BREAKER.
                                                                                                                                                *....
RESULTING IN AN ESF ACTUATION .AND iNT_ERRUPTION OF SHUTDOWN COOLING *. **.:. -* f.* *. *--.:::-,.* ,-*, * ... L Event Report. ( LER) 92--024 is. attached.<*  
April 27, 1992
.. .Thi's event* is* rep.ortabl e *i rf..-. *. *. * .. ... * .* *. -accordanc.e w*ith lOCFR50. 73 ( a)(2H iv)' as an* eveh(that in ari 'automa't i c *. * .
                                                                        **,.
an engineered-safety *feature.  
                                                                                                                                                                                                **:.'
*: * * * * * * . ...-, . . . -' . . . :-*g* .* .. :. . . ' . ; ' .'. . . '*' .. ... ''fa* * .. c. . * * . *;.*-n . .
: r.     *-
B Slad* . * :* General_*
                                  .-                                                                        - ;. "
Manager -. 'I * . :** .\ '
                                                                                                                                                                                                                              *-  -    .:::-,.*
* cc
                                                                                                                            *.... ,.                                                             ,* .. *'
*Ill, USNRC NRC: Res'ident Inspector
Nuclear. Regulatory Commission*
*Pali sades* Attachment" . .... * . ,.. \, -,:** * ,_+ * . ... . . :' . ... ,, . '<. . , .. -* *-" 9205'010265 920427 PDR ADOCK 05000255 S PDR . A CM5 ENERGY COMPANY ICtlC ...... U.S. llUCLIAll lllGULATOllY c..831. .. .*I * .. "'"'&deg;YID OMI lllO. JI  
            - ,:
'* LICENSEE EVENT (LEA) IX"llll' 1/31 II& -'AclLITY N.t.1111 111 IOOCll" ...... 121 r--tlll Palisades Plant 0111010101 15 IS 1 loF 016 TITLI l'I INADVERTENT OPENING OF-THE STATION POWER BREAKER RESULTING IN AN ESF ACTUA 'lON -ANU T N'T'F.R t>Tlt>'T' T rn ()H' cam'T'DOWN COOLING ( UMalll Ill lll'OllT OATI 171 OTMI ,. **n I YEAR 191QUIHTIAL.
                        'Document Control Desk                                                    *.                                                                                 :*.
1::;:::;::
WashiDgton, .DC 20~55 *                                                               *.'
N\llllOH MONTH DAY -YEAR 'ACIL.ITY NAMU OOCltlT 'IUMUlllll HUM81R HUMHR -N/A 0 I IO IO Io I I .I 01 3 7 9 91 2 -* 01 214 OJO q 4 fp 91 2 N/A 0 1S10 IO I 01 I I OPlllATlllO 11 lllPOllT II IU9MITTIO l'UlllUANT TO THI lllOUllllMINTI
LICENSE *DPR"'20 "'_. Oi>A~rsADEs !>.LANT*~ *
&deg;' 10 C'll &sect;: -&deg;' -of* '&deg;'-.J 1111 ..,.,. Ill 211.41121111 ID.4Dllol x IO.nlallllli.1 71.711111 I --*""'-"&deg;"'" 211 ... 111111111 ID*Colltl . ID.71191111M  
                                                                                                                                                                                                                    ,-*,
' 1U11ol LIVIL -----1101 nl nln 211.-181111111 ID*l*llZI ID,nlalllllwll OTMlll fS-Wtt ltt .--W, lll4ti* ---....,._ ,,, T**t, NllC ,_ -211 .... 11111111111 ID.71111121111 I0.711911111fll111AI .aAJ --211.*c.11111i.1 I0.7JlalllliMI 1D.nca11111w111ca1
                                                                                                                                                                                                                  *...
---211 ... C.111 llwl I0.71111111UUI ID.nlalllHai LICINIH CONTACT 'Oii TMll .I ( 131 NAMI Tl . ii u If" ARIA CODI Cris T. Hillman. Staff Licensing Engineer I 116 7 16 I 41"' I 8f 9'1 l 13 'L 'I II L ii 0 " c.. 'II: lllt ii Oii :1 -REPORTABLE 1::::::::
DOC.KET .50-255                                                                                                                              .                 * * ,.
:*:::.;::::*:*:*
                        . L.ICENSEE EVENT REPORT 92'-024 ~-- INADVERTENT' OPENING OF* THE STATiON POWER* ..
::::::::::::::
                      *BREAKER. RESULTING IN AN ESF ACTUATION .AND iNT_ERRUPTION OF SHUTDOWN COOLING *.          **.:.  -
:::::::::::  
* f.*                      *.
.. :*:::::::*:::.
Li,~en'see Event Report. ( LER) 92--024 is. attached.<*...Thi's event* is* rep.ortabl e *i rf..-. *. *. *. :~...* .*
:* CAUll sviTIM COMPONENT MANU,AC. :::: ::::.*:-:  
                    *. -accordanc.e w*ith lOCFR50. 73 ( a)(2H iv)' as an* eveh(that -res~lted, in ari 'automa't i c *. * .
.. ;.: :-:**:-: ... : ::::::: CAUSE IYSTIM
                          ~ctuation'*of an engineered- safety *feature. *: *                                                                  *              *  * * *
* MANU,AC. lliilPORTAILI TUAIR TO NPRCS *:-: :::::::::
                      *g* .* . :.
:::::::.:-:*  
                                .        ...-,     .               .       .         -'         .                   .           .     :-
.;.:::: TUlllll TO N""DI * ::::::: ::::::::::: . . :::::::: :::::::::::  
                                                                                  -. 'I    *
'.*': :::: I I I I I I I :::::;:: ::::*:*::*:*.
                                      *~*
.:-:::::::
                                .'*' ..*~
I I I I I I ,, *:-:* :::::::::
                                              .                   . '
::::::::::
                                            .   ;     '             .'.
::::::-:,
                                  ~                                                              . :**                                                                                                          ~~*
I :::::*:* *:*:::::::
                                                  ~.*;.*-n      . ''fa*
:*:: ....... ,.::;:: .I I I I I* I :::;*:-:::*:-:
                                                                                                                                                                                                          -,:**          * ,_+ *
:::::::: .:-:::-::<::::  
                                                            .
.. I I I I I I I IUPPLIMINTAL llll'OllT IXl'ICTID 11" IXPICTID MC)NTH DAY YJAA . n Yll ,;, ""* _.;,. IX'*C'TEO IV6111$SION. IUIMIAION NO DATI llSI. :1 I I AaTllACT (Uttt/r "'. 1"10 -*I.e.. --tr fl'-11,,,,._ ,,,,,.w,;rr.tt Ii-1111 ,. On March 1992, at 2226 with the plant in cold shutdown, cooling flow interrupted 'C' bus power to operating
                                                                                                                          ....* .
*shutdown cooling pump was de-energized as a resu t of reaker testing on the station powet breaker.
                                                                                                      .\
on the bus resulted in both diesel generators starting.
                                                                                                                    .~:                                  ...
The interruption of shutdown coolinJ lasted for .. _ .
                          * ..      c.
four minutes.
                                      .
the shtitdown cooling luw ihterr&#xb5;ption, t e core exit temperature increase approximately stx degrees fahrenheit.  
                                                .   *     *   .
*1wo root causes for this event f:!X*ist. . The Shift Supervisor allowed work to proceed on the 'C' bus despite the provided.
                                                                .
to him b{ the Operations Scheduler, and contrary to information provided in the operating procedures.
                                                                                                                                                        .
In addition, *work proteeded beyond that was .authorized by the* Shi ft Sup.ervi sor. , * ** . * * . . . Corrective action for this event included-immediate action to discuss the event with all and operations work shifts emphasizing the problems associated with deviating from procedures and approved work scope. Further corrective action includes evaluating the use of a more formal communications policy within the maintenance departments, training electrical repairman and supervisors on the breaker testing requirements .stated in administrative defining expectations for responsibility of operating
                                                                                                                                                                                                                ..    :'
* . reakers, relocating the taution placards to a more visible location within the breaker cubicle, evaluate the start-up and station breakers to prevent operation in the -" est 11 pas it ion, and modifying t e .
                                                                                                                              ,..
* general operating prqcedure as necessary. . ' .. llCF--'.
                          ~er~ld          B Slad* .                                                                                                                                                                             . ...     ,,
-LICENSEE -NT AEP()AT ILIA> TEXT CONTINUA-N Palisades Plant T1llT ,. _ .... _._. ____ ltl/C ,,..,.._ .... " 1111 ** EVENT DESCRIPTION On March.27, 1992, at 2226 hours, with the plant in cold shutdown cooling was temporari.ly interrupted when the 'C' bus power to the -0perating shutdown cooling pump was de-energized as a result breaker testing on the station power breaker [FK;BKR].
.... ,             * :* General_* Manager
Undervoltage on the *1 c 1 bus resulted in both diesel-generators starting.
                                                                                                                                                      .'<.
The interruption of shutdown*
        .~'.
lasted for approximately four minutes. During the of shutdown.
                  '
tooling, the pr.iniary coolant system (PCS) [AB] temperature increased.
* cc Adnrinistrator:~"-Region *Ill,                                      USNRC                                            . ,..
S&deg;F; based on one exit thermocouple, 7&deg;F, based.on ariothet core exit thermocouple, and 1 &deg; F based on the s*hutdown cooling heat exchanger in let temperature  
NRC: Res'ident Inspector                          *Pali sades*                                  \,
.. The .initial PCS temperature approximately 82&deg;F. This event is reportable to the NRC in with as an that resulted *in an automatic actuation of an engineered safety . feature (diesel generators).
Attachment"
CAUSE OF THE EVENT Two root causes for th{s event Shift Supervisor.allowed work to proceed on the 'C' bus despite the guidance provided to *him by the Operations
    -*
            *-"
9205'010265 920427 PDR ADOCK 05000255 S                                         PDR .                           A CM5 ENERGY COMPANY
 
ICtlC . . . . . .                                                                                                                                                                                       U.S. llUCLIAll lllGULATOllY                     ~ION c..831.
                              ..                                                                                                                                                         .*I                 * .. "'"'&deg;YID OMI lllO. JI ID~ICM IX"llll' 1/31 II&
              '*                                                                  LICENSEE EVENT R~PORT (LEA)
                                                                                                                                                                                                                                      -
'AclLITY N.t.1111 111                                                                                                                                                                     IOOCll" ......           121                                     r--             tlll Palisades Plant                                                                                                                                                                         0111010101 15 IS 1 loF 016 TITLI l'I INADVERTENT OPENING OF- THE STATION POWER BREAKER                                                                                                     RESULTING                 IN AN ESF ACTUA 'lON -ANU T N'T'F.R t>Tlt>'T' T rn             cam'T'DOWN COOLING
(
()H' UMalll Ill                                     lll'OllT OATI 171                                                       OTMI                 ,.             **n     I 191QUIHTIAL.                                                                                                                                                     OOCltlT 'IUMUlllll
                                              )~~~~~= HUM81R YEAR                            1::;:::;:: N\llllOH MONTH                           DAY                 -YEAR                       'ACIL.ITY NAMU HUMHR N/A
                                                                                                                                                                                                          -          0 I IO IO Io I                                   I .I 01 3         ~ 7 9             91 2     -*       01 214                   OJO           q 4 fp                                       91 2                     N/A                                         0 1S10 IO I 01                                   I I
                                                                                                                                                  &deg;' 10 C'll &sect;: (~ -
                                                                                    ---                                                                          ----
OPlllATlllO 11 lllPOllT II IU9MITTIO l'UlllUANT TO THI lllOUllllMINTI                                                                                  &deg;' -       of*     '&deg;'-.J     1111
          ..,.,. Ill x                                                        71.711111
                                                                                                                                                                                                                    --
211.41121111                                           ID.4Dllol                                                                 IO.nlallllli.1
                                  --
                                                                                                                                                                                                                  *""'-
I                    211. . .111111111                                     ID*Colltl .                                                               ID.71191111M                                     '  1U11ol
      "&deg;"'"
LIVIL OTMlll fS-Wtt ltt .--W, lll4ti*--
1101         nl nln           211.-181111111                                         ID*l*llZI                                                                 ID,nlalllllwll
                                                                                                                                                                                                                              ....,._ ,,, T**t, NllC , _
211 ....11111111111 211.*c.11111i.1 211. . .C.111 llwl
                                                                                  --         ID.71111121111 I0.7JlalllliMI I0.71111111UUI                                                       -
I0.711911111fll111AI 1D.nca11111w111ca1 ID.nlalllHai
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I                :1                      I On March 27~ 1992, at 2226 ho~rs, with the plant in cold shutdown, s~utdo~n cooling flow ~as interrupted ~hen ~he 'C' bus ~u,plyirig power to t~e operating
              *shutdown cooling pump was de-energized as a resu t of reaker testing on the station powet breaker. Und~rvoltage on the 'C~ bus resulted in both diesel generators starting. The interruption of shutdown coolinJ lasted for .. _ .
a~proximately four minutes. Durin~ the shtitdown cooling luw ihterr&#xb5;ption, t e core exit temperature increase approximately stx degrees fahrenheit.
              *1wo root causes for this event f:!X*ist. . The Shift Supervisor allowed work to proceed on the 'C' bus despite the ~ufdance provided. to him b{ the Operations Scheduler, and contrary to information provided in the ~enera operating procedures. In addition, *work proteeded beyond that whic~ was .authorized by the* Shi ft Sup.ervi sor. , * .                                                               * .                                     **                                  .
                                                                                                                                                                                              .
Corrective action for this event included-immediate action to discuss the event with all mainten~nce and operations work shifts emphasizing the problems associated with deviating from procedures and approved work scope. Further corrective action includes evaluating the use of a more formal communications policy within the maintenance departments, training electrical repairman and supervisors on the breaker testing requirements .stated in administrative grocedures~ defining expectations for th~ responsibility of operating *                                                                                                                                                              .
reakers, relocating the taution placards to a more visible location within the breaker cubicle, evaluate modifyin~ the start-up and station safe~uards breakers to prevent operation in the -" est pas it ion, and modifying t e .
* 11 general
                      .
operating prqcedure                          '
as necessary.
.. l l C F - -
              '.
 
                              - LICENSEE -NT AEP()AT ILIA> TEXT CONTINUA-N Palisades Plant T1llT ,. _    . . . ._._. __ _ _ltl/C ,,..,.._ ...." 1111
* EVENT DESCRIPTION On March.27, 1992, at 2226 hours, with the plant in cold ~hutdown, shutdown cooling was temporari.ly interrupted when the 'C' bus su~plying power to the
              -0perating shutdown cooling pump [B~;P] was de-energized as a result ~f breaker testing on the station power breaker [FK;BKR]. Undervoltage on the
* c bus 1 1 resulted in both diesel- generators starting. The interruption of shutdown*
              ~ooling lasted for approximately four minutes.     During the interrupti~n of shutdown. tooling, the pr.iniary coolant system (PCS) [AB] temperature increased.
S&deg;F; based on one ~ore exit thermocouple, 7&deg;F, based.on ariothet core exit thermocouple, and 1&deg;F based on the s*hutdown cooling heat exchanger in let temperature t~ermocouple .. The .initial PCS temperature wa~ approximately 82&deg;F.
This event is reportable to the NRC in a~co~dance with 10CFR50~73la)(~)(iv) as an ~vent that resulted *in an automatic actuation of an engineered safety .
feature (diesel generators).
CAUSE OF THE EVENT Two root causes for th{s event ~xist~:The Shift Supervisor.allowed work to proceed on the 'C' bus despite the guidance provided to *him by the Operations
* Scheduler, and contrary to information provided in the general' operating.
* Scheduler, and contrary to information provided in the general' operating.
procedures..
procedures.. In aqdition*, work pro~eeded beyond that which was authorized by the Shift Supervisor.*.                                     *       *
In aqdition*, work beyond that which was authorized by the Shift Supervisor.*.  
* This event does not involve the failure of any equi pm~nt i_mportant to safety.
* *
ANALYSIS OF THE EVENT The P~lisades ~afety related Electr~cal Distribution System consist~ of two 2400V electrical buses which supply power to numerous loads in the plant, including the low pressure safety injection (LPSI) pumps which ~erve as the .
* This event does not involve the failure of any equi i_mportant to safety. ANALYSIS OF THE EVENT The related Distribution System of two 2400V electrical buses which supply power to numerous loads in the plant, including the low pressure safety injection (LPSI) pumps which as the . . Shutdown Cooling pumps. Each of these buses are normally powered by one of the following incciming breakers:*
            . Shutdown Cooling pumps. Each of these buses are normally powered by one of the following incciming breakers:*                             _:
_:
* Start~up Power.
* Power.
* Station Safeguards Power
* Station Safeguards Power
* Diesel.Power These breakers have three possible positions wfthin their
* Diesel.Power These breakers have three possible positions wfthin their cubicles~ 1.
: 1. **Disconnect position -is the position in which the control power is from the breaker, the interlocks are not connected, and the .breaker cannot be connected to a load. 2. Test position -in: this position .control power* is to the breaker, the interlocks are connected, and the breaker cannot be connected to i load. 3. Connect position -in which the control power is connected to the breaker, the interlocks are connected, and the breaker can be connected to a load.
          **Disconnect position - is the position in which the control power is disconnect~d from the breaker, the interlocks are not connected, and the
UCENSEE .T AIPOAT ILIA> TIXT
            .breaker cannot be connected to a load. 2. Test position - in: this position
*o1 I "" 11 C*&.A* *1c;..,, .. *-o .. 10 :>w1 "o*  
            .control power* is conn~cted to the breaker, the interlocks are connected, and the breaker cannot be connected to i load. 3. Connect position - in which the control power is connected to the breaker, the interlocks are connected, and the breaker can be connected to a load.
..... ., ,,,," OOCI IT "'*II* Ill .. i11 **01 JI **** . '* 01s1010101 21 SIS 91 2 -01214 -0 o I 3 Palisades Plant . . . .. --. . .. Taft*--*.-
 
__ ... ,... ... .It .is normal plant policy during shutdown cooling operations to maintain two independent power sources available to each of the two safety related buses, 'C' and 'D'. This is controlled via the operating Also, the Operations Scheduling Supervisor communicates these requirements to the operating crews via the following:
CONTINUA~
* A Shutdown Cooling Ava*lability list, and
                                                                                      *o1 I ""11 C*&.A* *1c;..,, .. .a;~** ::..1a1e-UCENSEE . T AIPOAT ILIA> TIXT OOCI IT "'*II* Ill
* A Shutdown Cooling Risk Assessment list which augments th*  
                                                                                                ......, ,,,,"
*availability list.* * *This is tontained in general operating procedure (GOP) 14, "Shutdown Cooling Operations;" Step 6.5.a and band is the used to control equipment status with respect to Shutdown Risk Management Earlier in the 1992 Refueling Outage, the station safeguards supply breaker charging motor failed to stop when requ.ired.
                                                                                                *-o.. 10 :>w1 "o*          l'lO...J*~
A spare breaker was placed in the breaker cubicle on the 'C.' bus and maintenance was performed on the normal *breaker.
                                                                            ~** .. ~.      i11                           **01 JI
On the shift of March 1992, the spare breaker was.replaced with the.normal breaker and subsequent testing indicated that the problem still existed with the normal breaker. As a result, the normal breaker was oir again .removed from the cubicle and the spare was put back in the 'C' bus. .
                                                      . '*
* This work was performed with all loads, including the operating shutdown cooling pump P-67A, from 'D' bus. At. the end of the "day" shift on* . March 27, 1992,. the safety related electrical distribution system was aligned with 'C' bus supplying all loads .. At that time, *'C' bus'. was powered from the. itation safeguards power supply breaker;_
                                                                      ****   IH~~~:*:~
The 'D'. was not supplying loads because* testing on the 'D' bus was scheduled for *the _foll owing day. Early "afternoon" shift of March 27, electrical
                                                                                                    ~*~~=
* finished work on the normai station safeguards breaker charging*motor.
Palisades Plant Taft*--*.- __ ... ,... ...         *~1111  .
The *
01s1010101 21 SIS
* breaker was successfully tested five times outside of the.cubicle.
                                                . .     ..
Based on the of the tests, the electrical repairman in charge that the spare be removed from the cubicle and the normal breaker installed.
91 2 -    01214
The *shift Supervisor discussed the request with 'the Shift and that the work could risk. The Shift Supervisor and Shift Engineer discussed two options to complete the
                                                                                  -- .     ... -      ~  0      oI      3 oir 0 16
* job: * * .*
                                                                                                                                              ..
        .It .is normal plant policy during shutdown cooling operations to maintain two independent power sources available to each of the two safety related buses,
        'C' and 'D'. This is controlled via the operating proced~res. Also, the Operations Scheduling Supervisor communicates these requirements to the operating crews via the following:
* A Shutdown Cooling ~quipment Ava*lability list, and
* A Shutdown Cooling Risk Assessment list which augments th*                 equi~ment
              *availability list.*                 *
      *This infor~atiori is tontained in general operating procedure (GOP) 14, "Shutdown Cooling Operations;" Step 6.5.a and band is the ~ethod used to control equipment status with respect to Shutdown Risk Management iss~es.
Earlier in the 1992 Refueling Outage, the station safeguards supply breaker charging motor failed to stop when requ.ired. A spare breaker was placed in the breaker cubicle on the 'C.' bus and maintenance was performed on the normal
      *breaker. On the "day~ shift of March 27~ 1992, the spare breaker was.replaced with the.normal breaker and subsequent testing indicated that the problem still existed with the normal breaker. As a result, the normal breaker was again .removed from the cubicle and the spare was put back in the 'C' bus. .
* This work was performed with all loads, including the operating shutdown cooling pump P-67A, po~er~d from 'D' bus. At. the end of the "day" shift on* .
March 27, 1992,. the safety related electrical distribution system was aligned with 'C' bus supplying all loads .. At that time, *'C' bus'. was powered from the.
itation safeguards power supply breaker;_ The 'D'. bu~ was not supplying loads because* testing on the 'D' bus was scheduled for *the _foll owing day.
Early ~n t~e "afternoon" shift of March 27, 199~, electrical mai~tenance
* finished work on the normai station safeguards breaker charging*motor. The
*
* breaker was successfully tested five times outside of the.cubicle. Based on the result~ of the succe~sf~l tests, the electrical repairman in charge
        ~equested that the spare ~reaker be removed from the cubicle and the normal breaker installed. The *shift Supervisor discussed the request with 'the Shift
      *Enginee~ and dete~mined that the work could b~ compl~ted ~ith mini~um risk.
The Shift Supervisor and Shift Engineer discussed two options to complete the
* job:                     *                                                                     *             .*
                                                                                                                                        .  '
* Transfer all loads to*'D' bus, or;
* Transfer all loads to*'D' bus, or;
* Trarisfer. bus supply power from the station safeguards breaker to the start-up breaker (the alternate power supply). . . . The Shift Superv*isor elected to swap the 'C' bus supply from the station . safeguards breaker to the start-up supply breaker. This transfer successfully crimpleted.
* Trarisfer. 'C~ bus supply power from the station safeguards breaker to the start-up breaker (the alternate power supply).
However, the electrical configuration did not comply with* the Shutdown Cooling Equipment Availability sheets provided to the Control Room by the Operations Scheduling Supervisor per General Operating Procedures (GOP) 14; "Shutdown Cooling Operations." 0 16 .. . ' . ' ' . i
                            . .     .
.... LICENSEE -NT AIPORT ILIAI TIXT CONTINUA *. * """I 'IWC:..a .. a' *IC\,,o\i  
The Shift Superv*isor elected to swap the 'C' bus supply from the station
.. ... ==--**10..
      . safeguards ~upply breaker to the start-up supply breaker. This transfer ~as successfully crimpleted. However, the electrical configuration did not comply                                                       ~  .
a-oveo
with* the Shutdown Cooling Equipment Availability sheets provided to the                                                           ''
.. o
Control Room by the Operations Scheduling Supervisor per General Operating Procedures (GOP) 14; "Shutdown Cooling Operations."
..... ., .. ,." OOCKIT ""'91* lat .. .._. ..... . **o* JI Palisades Plant
                                                                                                                                          .i
 
                                                                                          """I 'IWC:..a .. a' *IC\,,o\i .. ,~ ... ==--**10..
LICENSEE -NT AIPORT ILIAI TIXT CONTINUA* .*
                                                                                                ......, ..,."
a-oveo ~"'' ..o l''&deg;""'~
OOCKIT ""'91* lat
                                                                              ~** ...._......                             . **o* JI
....
....
The Shift Supervisor directed an Auxiliary Operator (AO).remove the 'spare' station safeguards supply.breaker from 'C' bus and replace it with the*normal breaker as the electrical repair-worker had requested; The Shift Supervisor directed the AO to leave.the normal breaker in the "conned" position with the chargirig.motor fuses installed.
Palisades Plant T'DT_1*~-*    .... -~~_,..,.J!lllll'.~1171 The Shift Supervisor directed an Auxiliary Operator (AO).remove the 'spare' station safeguards supply.breaker from 'C' bus and replace it with the*normal breaker as the electrical repair-worker had requested; The Shift Supervisor directed the AO to leave.the normal breaker in the "conned" position with the chargirig.motor fuses installed. The control power fuses were not installed.
The control power fuses were not installed.
This would ~llow racking in the breaker but not allow breaker operation. The Shift Supervisor did not give permission to either the AO or the. electrical
This would racking in the breaker but not allow breaker operation.
            .repair-worker*to do anything else with the breaker in the cubicle other than leave* it in the. "connect" position with charging motor fuses installed. The
The Shift Supervisor did not give permission to either the AO or the. electrical .repair-worker*to do anything else with the breaker in the cubicle other than leave* it in the. "connect" position with charging motor fuses installed.
              *AO completed the work as di.rected by the Shift Supervisor .. During this time P-67A, _the operating shutdown ~o~ling pump, was powered from the 'C' bus,* ,
The *AO completed the work as di.rected by the Shift Supervisor  
which in turn was supplied from the start-up power supply breaker.
.. During this time P-67A, _the operating shutdown pump, was powered from the 'C' bus,* , which in turn was supplied from the start-up power supply breaker. *.
          *. Th~ Electri~al Mai~tenance      Supervisor requested the electrical repair-worker and the AO to place the brea~er in the "test" position and to close the .
Supervisor requested the electrical repair-worker and the AO to place the in the "test" position and to close the .
* breaker to test the charging motor. The Electrical Maintenance Supervisor
* breaker to test the charging motor. The Electrical Maintenance Supervisor  
            *wanted to ensure the charg,ing motor functioned properly and, therefore,. felt
*wanted to ensure the charg,ing motor functioned properly and, therefore,.
            *this action was w~rranted~
felt *this action was
* Neither the AO or the electriccil repair-worker questioned the req~est based on their understanding of the approved ~ork scope.: .Caution signs* existed fn twtr areas. One on. the inside .of the start-:UP and stati oii safeguards breaker cu bi cl es to warri operators not to close the *
* Neither the AO or the electriccil repair-worker questioned the based on their understanding of the approved scope.: .Caution signs* existed fn twtr areas. One on. the inside .of the start-:UP and stati oii safeguards breaker cu bi cl es to warri operators not to close the * . breakers whjle the was in the "test"* position.
            . breakers whjle the b~e~ker was in the "test"* position. These signs ara*poorly * *'
These signs ara*poorly  
Jocated and are not rea~ily visib_le .. A second_ tautior:i sign js.on the outside .                                   **,.*
* *' Jocated and are not visib_le .. A second_ tautior:i sign js.on the outside .. of the breaker panel stating testing shall be done per Administrative Procedure 4w02. Wheri breaker .closed while in the "test" position, start-up power supply breaker opened and 'C' bus de-energized.
of the breaker panel stating testing shall be done per Administrative Procedure 4w02. Wheri ~he breaker ~as .closed while in the "test" position, th~,
The relay logic the start-up breakers and the Station* safeguards breakers on 'C' and 'D' bus is such that the.-bus.
start-up power supply breaker opened and 'C' bus de-energized. The relay logic fo~ the start-up breakers and the Station* safeguards breakers on 'C' and
cannot be supplied from two power sources ... Since the operating cooling pump was supplied from 'C' bus,* shutdown cooling was iriterrupted.  
              'D' bus is such that the.-bus. cannot be supplied from two power sources... Since the operating ~hutdown cooling pump was supplied from 'C' bus,* shutdown cooling was iriterrupted. *         *       .
* * . RESPONSE_
RESPONSE_ TO EVENT
TO EVENT . . . Both di eselS gene.raters started* as a result of 1 ow voltage on 'C' ,bus. The 1-1 diesel generator  
                              .       .     .
*did not synchronize to 'C' bus because the control power. fuses were r:ibt installed iri the station safeguards breaker. This allowed the *diesel generator logic to respond as. if.the station safeguards breaker was c.losed .to the bus. The .'D' bus was already powered from station* safeguards, the 1-2 diesel did not synchronize to the The operator's responded using the Off-Normal*
Both di eselS gene.raters started* as a result of 1ow voltage on 'C' ,bus. The 1-1 diesel generator *did not synchronize to 'C' bus because the control power.
Operating Procedure (ONP} 17, "Loss *of Shutdown*
fuses were r:ibt installed iri the station safeguards breaker. This allowed the
Cooling," and.manually latched the synchroniiing relay, allowing the. 1-1 diesel generator to synchronize to 'C' bus. The automatic load *
            *diesel generator logic to respond as. if.the station safeguards breaker was c.losed .to the bus. The .'D' bus was already powered from station* safeguards, the~efore, the 1-2 diesel generate~ did not synchronize to the bus~                    The operator's responded using the Off-Normal* Operating Procedure (ONP} 17, "Loss
* sequencers then placed loads -0n 'C' bus. -LPSI pump P-678 was started after throttling closed.the injection.valves and shutdown cooling was restored less that 4 minutes after the bus initially de-energized.
              *of Shutdown* Cooling," and.manually latched the synchroniiing relay, allowing the. 1-1 diesel generator to synchronize to 'C' bus. The automatic load *
PCS temperature increased approximately seven fahrenheit. . **,.*
* sequencers then placed loads -0n 'C' bus. -LPSI pump P-678 was started after throttling closed.the injection.valves and shutdown cooling was restored less that 4 minutes after the ~C' bus initially de-energized. PCS temperature increased approximately seven d~grees fahrenheit. .
* LJCENSEE .T AIPOAT ILIAI TIXT CONTINUA.  
 
'-'I A-OvlO ... "0 1*
                                                                                                    '-'I  111
...... ., .. .,." OOClllT ""'91 a Ill .. IAel. '" **o* ,, ...... Palisades Plant .TDT '"--* ._.. _,. _ ,_ ,._ _. . ., ,,,, On Monday, March 30, 1992, a Management .Review Board (MRB) was he_ld to review the Loss of 'C' and interruption of Shutdown Cooling incident which occurred on Friday, March 27, 1992. MRB was convened and clarified the following facts presented in the "Plant Personnel  
                                                                                                              ~C~&** llCti,,\,,atr~** :~***O LJCENSEE . T AIPOAT ILIAI TIXT CONTINUA.
*statements" contained in the *.Post-Trip Review Report.
OOClllT ""'91 a Ill
* The Shift Supervisor the to repair-worker to test the breaker charging .motor in the position while the breaker was in the cubitle.
                                                                                                            ...... ., ...,."
* The Shift Supervisor directed the AD.tQ refuove the (spare) breaker from the station start-up power breaker cubicle and to install the repaired breaker in the cubicle, irr,the "connect" position and with the charging motor fuses installed. (The.
A-OvlO ~ ... "0 1* !I0-4*~
* control power fuses were not installed.)  
                                                                                        ~**                                        **o* ,,
... -:
                                                                              ......       .. IAel. '"
* The discussions with the. AO and the electrical repair:..worker were independent af each The AO was .unaware of the scope cif work for *.which-the electrical repair-worker was approved. .
* Palisades Plant
* The Ele.ctrical Maintenance Supervisor was not .involved in* either.of the conversations with the.Shift Supervisor and was, therefore, unaware of the approved scope of work. *. * * *
  .TDT ' " - - * ._.. _,. _   ,_ ,._ _. .., ,,,,
* When the normal breaker was in the cubicle, only the motor . fuses were installed.
On Monday, March 30, 1992, a Management .Review Board (MRB) was he_ld to review the Loss of 'C' b~s. and interruption of Shutdown Cooling incident which occurred on Friday, March 27, 1992. Th~ MRB was convened and clarified the following facts presented in the "Plant Personnel *statements" contained in the
The contra 1 power fuses were not i nsta 11
          *.Post-Trip Review Report.
* Wheh Electrital  
* The Shift Supervisor releas~d the ~ork to         th~ electric~1            repair-worker to test the breaker charging .motor in the       11
*Maintenance Supervisor.
                                                                          ~onnect 11 position while the breaker was in the cubitle.
requested the electrical repair-worker and AO to place the breaker in "test" position and close breaker, neither the electrical or AO questioned the request based on their understanding of the approved work scope.
* The Shift Supervisor directed the AD.tQ refuove the e~isting (spare) breaker from the station start-up power breaker cubicle and to install the repaired (nor~al) breaker in the cubicle, leavin~ the.break~~ irr,the "connect" position and with the charging motor fuses installed. (The. *                                  :
* The electrical repair-work.er racked the breaker from the "connect" *position to the "test" position and closed the breakei.
control power fuses were not installed.)
operation of equipment is the responsibility of the Operations Department.)
                                                                                                                        ...
* The Shift Supervisor did not feel the work he authorfzed (transferring  
    -
'C' bus power from the station safeguards supply breaker to the start-up supply breaker and replacing the station start-up breaker while lEaving the breaker in the "connect" position to test the tharging motor) was a *risk to shutdown safety. *
* The discussions with the. AO and the electrical repair:..worker were independent af each other~** The AO was .unaware of the scope cif work for
* signs inside the cubicles, which had been placed* in the.cubicles as a tesult -0f similar events, were not clearly visible to the workers.
                  *.which-the electrical repair-worker was approved.                                             .
* The caution* signs on the. front of the breaker cubicles, which state that breaket shall be performed in with the requirements of Administrative Protedure 4.02, "Control of Equipment Status," did not stop the event. .1 ' .' 
* The Ele.ctrical Maintenance Supervisor was not .involved in* either.of the conversations with the.Shift Supervisor and was, therefore, unaware of the approved scope of work.         *.                               * *
* *.* *-*. * * ...... _.. . .;...;.....*-:--
                *
..  
* When the normal breaker was i~stalled in the cubicle, only the chargin~
* --* * '.
motor .fuses were installed. The contra 1 power fuses were not i nsta 11 ed~.
**-*-*
* Wheh ~he Electrital *Maintenance Supervisor. requested the electrical repair-worker and AO to place the breaker in ~he "test" position and close th~ breaker, neither the electrical ~epair-worker or AO questioned the request based on their understanding of the approved work scope.
IOllC*w*-. LICENSEE &r.REPORT TEXT CONTINUA.
* The electrical repair-work.er racked the breaker from the "connect"
""' .. ._,C:.&*a
                    *position to the "test" position and closed the breakei. '(Th~ operation of equipment is the responsibility of the Operations Department.)
:I* .. ::a..1a10-
* The Shift Supervisor did not feel the work he authorfzed (transferring
&-0vlO "0
                      'C' bus power from the station safeguards supply breaker to the start-up                                               .1 supply breaker and replacing the station start-up breaker while lEaving the breaker in the "connect" position to test the tharging motor) was a
..... ., .. ,. " .. ;* -! ooca n ""'91
                    *risk to shutdown safety.                                                           *
* 111 lllAllSlll
* T~e-taution    signs inside the br~aker cubicles, which had been placed* in the.cubicles as a tesult -0f ~revious similar events, were not clearly visible to the workers.
*ti *. -..... io .. ... ., .. *&OI JI Plant o 1 s Io Io I 21 515 9 I 2 _ o 12 14 _ 01 o o I 6 o I 6 ..
                                                                                                                                                ' ~.
* The* El ectri cal Mai ntehanc;e Super.visor
* The caution* signs on the. front of the breaker cubicles, which state that                                                 .'
*and e lectri cal . repair-worker were .. * -... not aware of previous problems w'ith t-esting these breakers while in the position.
breaket t~sting shall be performed in a~cordance with the requirements of Administrative Protedure 4.02, "Control of Equipment Status," did not stop the event.
The AO had trair:iing*on the problems but did not recall the testing problems .. -. -
 
ACtibN The correitive actions were developed as a result of the* investigation of
                                    * *.* *- * . ~, *     * ...... _....;...;.....*-:-- *~-J.. ~-**'-*** * - -* * '.     ***-----~~ * * - * - **~--------'-*-----
* , * *_ Immediate ac-t ion .taken by Operat fons*
ILi~> TEXT CONTINUA.
was. to meet with ::a 11 shifts to event and for* shutdown risk management.
IOllC*w*-
_ :
1~1          .                                                                                                                                                                           ""' ~  .. ._,C:.&*a          *le;~~*' :I* .. ::a..1a10-LICENSEE &r.REPORT ooca n
* _ .. , _ *,
                                                                                                                                                                                                    ......, ..,. "
* incident was .als9 djscussed with all maintenahte.
                                                                                                                                                                                                    &-0vlO ~"' "0 1*~~*).e
shifts emphasiz'ing
                                                                                                                                                                                                                          ..
*the with from.the . .* . . ' .' . ' .. . . . . . . ... --. . ' . . . . . ... .
                                                                                                                                ""'91
* and evaJuate the use of :a 'more formal. communicatfons.policy.: . within the maintenanc'e*departmentS.
* 111
*Consider-the existing operatjons*."-. ,po}icy-in thi*S
                                                                                                                                                                          ~**    lllAllSlll *ti                                      *&OI JI
'.for.tonsistency.
                                                                                                                                                                                                          ...*.- ......,io ..
p.ur.poses.  
Pali~ades            Plant o 1s Io Io I~ I 21 515 9 I 2 _~.                               o 12    14        ~ _ 01                o oI        6 o~    o I 6 ..
* * * ... , ** _1;. : ' . Trafn electrical rep.air-worker and :superv*i so rs . on* the breaker testing* ... requirements stated in Administrative Procedure 4.02: Specifically, ,. __ ** ** address* the problems with testing* incoming breakers racked in to t.he *,
* The* El ectri cal Mai ntehanc;e Super.visor *and e lectri cal . repair-worker were .. *
expectations for breaker operations . ** by in this .. traini_ng: . .. .. .. -,
                - ... not aware of previous problems w'ith t-esting these breakers while in the "tes~" position. The AO had trair:iing*on the previou_s~ problems but did not recall the testing problems .. -                                                                                                                              .                         -
* Define expectations for _breaker operations.
          .*toRRECTI~E ACtibN The follow~ng correitive actions were developed as a result of the*
Siiec i nca 11 y, . define account ab le depar.tments
investigation of thi~*incident:                                                                                      * ,                                                     *
'*for breaker**  
                  *_ Immediate ac-t ion .taken by Operat fons* Management~ was. to meet with ::a 11 shifts to dis~us~~the event and ex~ectations for* shutdown risk management. _                                    :
<>per at ions in the "connect."; "test", and
* _                  ..                           ,                             _
.. * -:. ... * ; '. : e' Pla-ce cauti,on placard.s which are:locatedjnside the breaker a more* vi s_i ble '.locati ori within .. the.
                                                      *,
c*ubj cl e. ,, _ ***
* T~e incident was .als9 djscussed with all maintenahte. shifts emphasiz'ing
of: a to the start-up ,and. stafio_p-safeguards
                          *the  probl~ms-associated                                                with            d~viating                      from.the    .a~pro~ed.w6rk~scope.
** breakers to. preven.t 'operation*
                                  .          .* .       . '
in the "test" position.  
                                                                ...                                     .. ~-'    ' ..
* . . . _ .* *' * 'Eyaluate GOP 14, Step 6.5 and Attachment 3 with respect to this event. -* This ensure Operations Management's are .'clearly defi.ned *to thE? shift SROs via this procedure.  
                                                                                                                        ~-
*Modify' the * **proce.dure-as necessary.:
                                                                                                                                  .
as a result of this evaluation-_.'
                                                                                                                                    . . .                   .   .       . ... - -      .. '        . .            ..          .
.. ** ADDITIONAL INFORMATION None}}
                  * 'lnvestig~te and evaJuate the use of :a 'more formal. communicatfons.policy.: .
within the maintenanc'e*departmentS. *Consider- the existing operatjons*."-.
                          ,po}icy-in thi*S ev~l.uatio.n '.for.tonsistency. p.ur.poses.                                                                                              * *                                                *
                                                                                                                        ... ,            **  _1;.                                                 :  '
                  *~ . Trafn electrical rep.air-worker and :superv*i so rs .on* the breaker testing*                                                                                                                                         ...
requirements stated in Administrative Procedure 4.02: Specifically,                                                                                                                                          ,. __ **
* address* the problems with testing* incoming breakers racked in to t.he *,
                            "test~ positi4~.                                Incl~de expectations for breaker operations develop~d                                                                                                              . **
by .op_eration~ in this .. traini_ng:                                                                                    .    .. ..       .                                             -                       ,
* Define expectations for _breaker operations. Siiec i nca 11 y, . define account ab le depar.tments '*for breaker** <>per at ions in the "connect."; "test",
and "~i~C:onnect".positions..                                                                  ..                              * -:.                                                                ... *
                    -~                                                                                                                                                                                  :
e'
                  ;
                                                                                                                                                                                      '.
Pla-ce cauti,on placard.s which are:locatedjnside the breaker &#xa2;ubi~les-in*
..; * -!
a more* vi s_i ble '.locati ori within ..the. br~aker c*ubj cl e. ,,                                                                                                                            _
                *** Evalu~t.ion. of: a .inodificati.~n to the start-up ,and. stafio_p- safeguards
* breakers to. preven.t 'operation* in the "test" position. * . . . _.*
                ~,    *'
                  * 'Eyaluate GOP 14, Step 6.5 and Attachment 3 with respect to this event. -
* This evaluatiort:shoul~ ensure Operations Management's e~pectations are
                          .'clearly defi.ned *to thE? shift SROs via this procedure. *Modify' the *
                          **proce.dure-as necessary.: as a result of this evaluation-_.'                                                                                                                                       ..
          ** ADDITIONAL INFORMATION None}}

Revision as of 18:17, 21 October 2019

LER 92-024-00:on 920327,inadvertent Opening of Station Power Breaker Resulting in ESF Actuation & Interruption of Shutdown Cooling.Caused by Supervisor Allowing Work to Proceed on C Bus.Event Discussed w/maint.W/920427 Ltr
ML18058A381
Person / Time
Site: Palisades Entergy icon.png
Issue date: 04/27/1992
From: Hillman C, Slade G
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-92-024, LER-92-24, NUDOCS 9205010265
Download: ML18058A381 (7)


Text

',".

consumers

  • Power *
  • o. G B* Slade

. General Manager POWERlNli lllllCHlliAN-S PROlillESS .

  • Palisades Nuclear Plant:
  • 27780 .Blue Star Meinc>ria~. Highway. Covert. Ml 49043
  • ....

April 27, 1992

    • ,.
    • .'
r. *-

.- - ~  ;. "

  • - - .:::-,.*
  • .... ,. ,* .. *'

Nuclear. Regulatory Commission*

- ,:

'Document Control Desk *.  :*.

WashiDgton, .DC 20~55 * *.'

LICENSE *DPR"'20 "'_. Oi>A~rsADEs !>.LANT*~ *

,-*,

  • ...

DOC.KET .50-255 . * * ,.

. L.ICENSEE EVENT REPORT 92'-024 ~-- INADVERTENT' OPENING OF* THE STATiON POWER* ..

  • f.* *.

Li,~en'see Event Report. ( LER) 92--024 is. attached.<*...Thi's event* is* rep.ortabl e *i rf..-. *. *. *. :~...* .*

  • . -accordanc.e w*ith lOCFR50. 73 ( a)(2H iv)' as an* eveh(that -res~lted, in ari 'automa't i c *. * .

~ctuation'*of an engineered- safety *feature. *: * * * * * *

  • g* .* . :.

. ...-, . . . -' . . .  :-

-. 'I *

  • ~*

.'*' ..*~

. . '

.  ; ' .'.

~ . :** ~~*

~.*;.*-n . fa*

-,:** * ,_+ *

.

....* .

.\

.~: ...

  • .. c.

.

. * * .

.

.

..  :'

,..

~er~ld B Slad* . . ... ,,

.... , * :* General_* Manager

.'<.

.~'.

'

  • cc Adnrinistrator:~"-Region *Ill, USNRC . ,..

NRC: Res'ident Inspector *Pali sades* \,

Attachment"

-*

  • -"

9205'010265 920427 PDR ADOCK 05000255 S PDR . A CM5 ENERGY COMPANY

ICtlC . . . . . . U.S. llUCLIAll lllGULATOllY ~ION c..831.

.. .*I * .. "'"'°YID OMI lllO. JI ID~ICM IX"llll' 1/31 II&

'* LICENSEE EVENT R~PORT (LEA)

-

'AclLITY N.t.1111 111 IOOCll" ...... 121 r-- tlll Palisades Plant 0111010101 15 IS 1 loF 016 TITLI l'I INADVERTENT OPENING OF- THE STATION POWER BREAKER RESULTING IN AN ESF ACTUA 'lON -ANU T N'T'F.R t>Tlt>'T' T rn cam'T'DOWN COOLING

(

()H' UMalll Ill lll'OllT OATI 171 OTMI ,. **n I 191QUIHTIAL. OOCltlT 'IUMUlllll

)~~~~~= HUM81R YEAR 1::;:::;:: N\llllOH MONTH DAY -YEAR 'ACIL.ITY NAMU HUMHR N/A

- 0 I IO IO Io I I .I 01 3 ~ 7 9 91 2 -* 01 214 OJO q 4 fp 91 2 N/A 0 1S10 IO I 01 I I

°' 10 C'll §: (~ -

--- ----

OPlllATlllO 11 lllPOllT II IU9MITTIO l'UlllUANT TO THI lllOUllllMINTI °' - of* '°'-.J 1111

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.aAJ NAMI LICINIH CONTACT 'Oii TMll .I ( 131 ARIA CODI Tl . ii u If" Cris T. Hillman. Staff Licensing Engineer I 116 7 16 I 41"' I 8f 9'1 l 13

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.I I I I I I* I I I I I I I I IUPPLIMINTAL llll'OllT IXl'ICTID 11" MC)NTH DAY YJAA

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I :1 I On March 27~ 1992, at 2226 ho~rs, with the plant in cold shutdown, s~utdo~n cooling flow ~as interrupted ~hen ~he 'C' bus ~u,plyirig power to t~e operating

  • shutdown cooling pump was de-energized as a resu t of reaker testing on the station powet breaker. Und~rvoltage on the 'C~ bus resulted in both diesel generators starting. The interruption of shutdown coolinJ lasted for .. _ .

a~proximately four minutes. Durin~ the shtitdown cooling luw ihterrµption, t e core exit temperature increase approximately stx degrees fahrenheit.

  • 1wo root causes for this event f:!X*ist. . The Shift Supervisor allowed work to proceed on the 'C' bus despite the ~ufdance provided. to him b{ the Operations Scheduler, and contrary to information provided in the ~enera operating procedures. In addition, *work proteeded beyond that whic~ was .authorized by the* Shi ft Sup.ervi sor. , * . * . ** .

.

Corrective action for this event included-immediate action to discuss the event with all mainten~nce and operations work shifts emphasizing the problems associated with deviating from procedures and approved work scope. Further corrective action includes evaluating the use of a more formal communications policy within the maintenance departments, training electrical repairman and supervisors on the breaker testing requirements .stated in administrative grocedures~ defining expectations for th~ responsibility of operating * .

reakers, relocating the taution placards to a more visible location within the breaker cubicle, evaluate modifyin~ the start-up and station safe~uards breakers to prevent operation in the -" est pas it ion, and modifying t e .

  • 11 general

.

operating prqcedure '

as necessary.

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- LICENSEE -NT AEP()AT ILIA> TEXT CONTINUA-N Palisades Plant T1llT ,. _ . . . ._._. __ _ _ltl/C ,,..,.._ ...." 1111

  • EVENT DESCRIPTION On March.27, 1992, at 2226 hours0.0258 days <br />0.618 hours <br />0.00368 weeks <br />8.46993e-4 months <br />, with the plant in cold ~hutdown, shutdown cooling was temporari.ly interrupted when the 'C' bus su~plying power to the

-0perating shutdown cooling pump [B~;P] was de-energized as a result ~f breaker testing on the station power breaker [FK;BKR]. Undervoltage on the

  • c bus 1 1 resulted in both diesel- generators starting. The interruption of shutdown*

~ooling lasted for approximately four minutes. During the interrupti~n of shutdown. tooling, the pr.iniary coolant system (PCS) [AB] temperature increased.

S°F; based on one ~ore exit thermocouple, 7°F, based.on ariothet core exit thermocouple, and 1°F based on the s*hutdown cooling heat exchanger in let temperature t~ermocouple .. The .initial PCS temperature wa~ approximately 82°F.

This event is reportable to the NRC in a~co~dance with 10CFR50~73la)(~)(iv) as an ~vent that resulted *in an automatic actuation of an engineered safety .

feature (diesel generators).

CAUSE OF THE EVENT Two root causes for th{s event ~xist~:The Shift Supervisor.allowed work to proceed on the 'C' bus despite the guidance provided to *him by the Operations

  • Scheduler, and contrary to information provided in the general' operating.

procedures.. In aqdition*, work pro~eeded beyond that which was authorized by the Shift Supervisor.*. * *

  • This event does not involve the failure of any equi pm~nt i_mportant to safety.

ANALYSIS OF THE EVENT The P~lisades ~afety related Electr~cal Distribution System consist~ of two 2400V electrical buses which supply power to numerous loads in the plant, including the low pressure safety injection (LPSI) pumps which ~erve as the .

. Shutdown Cooling pumps. Each of these buses are normally powered by one of the following incciming breakers:* _:

  • Start~up Power.
  • Station Safeguards Power
  • Diesel.Power These breakers have three possible positions wfthin their cubicles~ 1.
    • Disconnect position - is the position in which the control power is disconnect~d from the breaker, the interlocks are not connected, and the

.breaker cannot be connected to a load. 2. Test position - in: this position

.control power* is conn~cted to the breaker, the interlocks are connected, and the breaker cannot be connected to i load. 3. Connect position - in which the control power is connected to the breaker, the interlocks are connected, and the breaker can be connected to a load.

CONTINUA~

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.It .is normal plant policy during shutdown cooling operations to maintain two independent power sources available to each of the two safety related buses,

'C' and 'D'. This is controlled via the operating proced~res. Also, the Operations Scheduling Supervisor communicates these requirements to the operating crews via the following:

  • availability list.* *
  • This infor~atiori is tontained in general operating procedure (GOP) 14, "Shutdown Cooling Operations;" Step 6.5.a and band is the ~ethod used to control equipment status with respect to Shutdown Risk Management iss~es.

Earlier in the 1992 Refueling Outage, the station safeguards supply breaker charging motor failed to stop when requ.ired. A spare breaker was placed in the breaker cubicle on the 'C.' bus and maintenance was performed on the normal

  • breaker. On the "day~ shift of March 27~ 1992, the spare breaker was.replaced with the.normal breaker and subsequent testing indicated that the problem still existed with the normal breaker. As a result, the normal breaker was again .removed from the cubicle and the spare was put back in the 'C' bus. .
  • This work was performed with all loads, including the operating shutdown cooling pump P-67A, po~er~d from 'D' bus. At. the end of the "day" shift on* .

March 27, 1992,. the safety related electrical distribution system was aligned with 'C' bus supplying all loads .. At that time, *'C' bus'. was powered from the.

itation safeguards power supply breaker;_ The 'D'. bu~ was not supplying loads because* testing on the 'D' bus was scheduled for *the _foll owing day.

Early ~n t~e "afternoon" shift of March 27, 199~, electrical mai~tenance

  • finished work on the normai station safeguards breaker charging*motor. The
  • breaker was successfully tested five times outside of the.cubicle. Based on the result~ of the succe~sf~l tests, the electrical repairman in charge

~equested that the spare ~reaker be removed from the cubicle and the normal breaker installed. The *shift Supervisor discussed the request with 'the Shift

  • Enginee~ and dete~mined that the work could b~ compl~ted ~ith mini~um risk.

The Shift Supervisor and Shift Engineer discussed two options to complete the

  • job: * * .*

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  • Transfer all loads to*'D' bus, or;
  • Trarisfer. 'C~ bus supply power from the station safeguards breaker to the start-up breaker (the alternate power supply).

. . .

The Shift Superv*isor elected to swap the 'C' bus supply from the station

. safeguards ~upply breaker to the start-up supply breaker. This transfer ~as successfully crimpleted. However, the electrical configuration did not comply ~ .

with* the Shutdown Cooling Equipment Availability sheets provided to the

Control Room by the Operations Scheduling Supervisor per General Operating Procedures (GOP) 14; "Shutdown Cooling Operations."

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Palisades Plant T'DT_1*~-* .... -~~_,..,.J!lllll'.~1171 The Shift Supervisor directed an Auxiliary Operator (AO).remove the 'spare' station safeguards supply.breaker from 'C' bus and replace it with the*normal breaker as the electrical repair-worker had requested; The Shift Supervisor directed the AO to leave.the normal breaker in the "conned" position with the chargirig.motor fuses installed. The control power fuses were not installed.

This would ~llow racking in the breaker but not allow breaker operation. The Shift Supervisor did not give permission to either the AO or the. electrical

.repair-worker*to do anything else with the breaker in the cubicle other than leave* it in the. "connect" position with charging motor fuses installed. The

  • AO completed the work as di.rected by the Shift Supervisor .. During this time P-67A, _the operating shutdown ~o~ling pump, was powered from the 'C' bus,* ,

which in turn was supplied from the start-up power supply breaker.

  • . Th~ Electri~al Mai~tenance Supervisor requested the electrical repair-worker and the AO to place the brea~er in the "test" position and to close the .
  • breaker to test the charging motor. The Electrical Maintenance Supervisor
  • wanted to ensure the charg,ing motor functioned properly and, therefore,. felt
  • this action was w~rranted~
  • Neither the AO or the electriccil repair-worker questioned the req~est based on their understanding of the approved ~ork scope.: .Caution signs* existed fn twtr areas. One on. the inside .of the start-:UP and stati oii safeguards breaker cu bi cl es to warri operators not to close the *

. breakers whjle the b~e~ker was in the "test"* position. These signs ara*poorly * *'

Jocated and are not rea~ily visib_le .. A second_ tautior:i sign js.on the outside . **,.*

of the breaker panel stating testing shall be done per Administrative Procedure 4w02. Wheri ~he breaker ~as .closed while in the "test" position, th~,

start-up power supply breaker opened and 'C' bus de-energized. The relay logic fo~ the start-up breakers and the Station* safeguards breakers on 'C' and

'D' bus is such that the.-bus. cannot be supplied from two power sources... Since the operating ~hutdown cooling pump was supplied from 'C' bus,* shutdown cooling was iriterrupted. * * .

RESPONSE_ TO EVENT

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Both di eselS gene.raters started* as a result of 1ow voltage on 'C' ,bus. The 1-1 diesel generator *did not synchronize to 'C' bus because the control power.

fuses were r:ibt installed iri the station safeguards breaker. This allowed the

  • diesel generator logic to respond as. if.the station safeguards breaker was c.losed .to the bus. The .'D' bus was already powered from station* safeguards, the~efore, the 1-2 diesel generate~ did not synchronize to the bus~ The operator's responded using the Off-Normal* Operating Procedure (ONP} 17, "Loss
  • of Shutdown* Cooling," and.manually latched the synchroniiing relay, allowing the. 1-1 diesel generator to synchronize to 'C' bus. The automatic load *
  • sequencers then placed loads -0n 'C' bus. -LPSI pump P-678 was started after throttling closed.the injection.valves and shutdown cooling was restored less that 4 minutes after the ~C' bus initially de-energized. PCS temperature increased approximately seven d~grees fahrenheit. .

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  • Palisades Plant

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On Monday, March 30, 1992, a Management .Review Board (MRB) was he_ld to review the Loss of 'C' b~s. and interruption of Shutdown Cooling incident which occurred on Friday, March 27, 1992. Th~ MRB was convened and clarified the following facts presented in the "Plant Personnel *statements" contained in the

  • .Post-Trip Review Report.
  • The Shift Supervisor releas~d the ~ork to th~ electric~1 repair-worker to test the breaker charging .motor in the 11

~onnect 11 position while the breaker was in the cubitle.

  • The Shift Supervisor directed the AD.tQ refuove the e~isting (spare) breaker from the station start-up power breaker cubicle and to install the repaired (nor~al) breaker in the cubicle, leavin~ the.break~~ irr,the "connect" position and with the charging motor fuses installed. (The. *  :

control power fuses were not installed.)

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  • The discussions with the. AO and the electrical repair:..worker were independent af each other~** The AO was .unaware of the scope cif work for
  • .which-the electrical repair-worker was approved. .
  • The Ele.ctrical Maintenance Supervisor was not .involved in* either.of the conversations with the.Shift Supervisor and was, therefore, unaware of the approved scope of work. *. * *
  • When the normal breaker was i~stalled in the cubicle, only the chargin~

motor .fuses were installed. The contra 1 power fuses were not i nsta 11 ed~.

  • Wheh ~he Electrital *Maintenance Supervisor. requested the electrical repair-worker and AO to place the breaker in ~he "test" position and close th~ breaker, neither the electrical ~epair-worker or AO questioned the request based on their understanding of the approved work scope.
  • The electrical repair-work.er racked the breaker from the "connect"
  • position to the "test" position and closed the breakei. '(Th~ operation of equipment is the responsibility of the Operations Department.)
  • The Shift Supervisor did not feel the work he authorfzed (transferring

'C' bus power from the station safeguards supply breaker to the start-up .1 supply breaker and replacing the station start-up breaker while lEaving the breaker in the "connect" position to test the tharging motor) was a

  • risk to shutdown safety. *
  • T~e-taution signs inside the br~aker cubicles, which had been placed* in the.cubicles as a tesult -0f ~revious similar events, were not clearly visible to the workers.

' ~.

  • The caution* signs on the. front of the breaker cubicles, which state that .'

breaket t~sting shall be performed in a~cordance with the requirements of Administrative Protedure 4.02, "Control of Equipment Status," did not stop the event.

  • *.* *- * . ~, * * ...... _....;...;.....*-:-- *~-J.. ~-**'-*** * - -* * '. ***-----~~ * * - * - **~--------'-*-----

ILi~> TEXT CONTINUA.

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  • The* El ectri cal Mai ntehanc;e Super.visor *and e lectri cal . repair-worker were .. *

- ... not aware of previous problems w'ith t-esting these breakers while in the "tes~" position. The AO had trair:iing*on the previou_s~ problems but did not recall the testing problems .. - . -

.*toRRECTI~E ACtibN The follow~ng correitive actions were developed as a result of the*

investigation of thi~*incident: * , *

  • _ Immediate ac-t ion .taken by Operat fons* Management~ was. to meet with ::a 11 shifts to dis~us~~the event and ex~ectations for* shutdown risk management. _  :
  • _ .. , _
  • ,
  • T~e incident was .als9 djscussed with all maintenahte. shifts emphasiz'ing
  • the probl~ms-associated with d~viating from.the .a~pro~ed.w6rk~scope.

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  • 'lnvestig~te and evaJuate the use of :a 'more formal. communicatfons.policy.: .

within the maintenanc'e*departmentS. *Consider- the existing operatjons*."-.

,po}icy-in thi*S ev~l.uatio.n '.for.tonsistency. p.ur.poses. * * *

... , ** _1;.  : '

  • ~ . Trafn electrical rep.air-worker and :superv*i so rs .on* the breaker testing* ...

requirements stated in Administrative Procedure 4.02: Specifically, ,. __ **

  • address* the problems with testing* incoming breakers racked in to t.he *,

"test~ positi4~. Incl~de expectations for breaker operations develop~d . **

by .op_eration~ in this .. traini_ng: . .. .. . - ,

  • Define expectations for _breaker operations. Siiec i nca 11 y, . define account ab le depar.tments '*for breaker** <>per at ions in the "connect."; "test",

and "~i~C:onnect".positions.. .. * -:. ... *

-~  :

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Pla-ce cauti,on placard.s which are:locatedjnside the breaker ¢ubi~les-in*

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a more* vi s_i ble '.locati ori within ..the. br~aker c*ubj cl e. ,, _

      • Evalu~t.ion. of: a .inodificati.~n to the start-up ,and. stafio_p- safeguards
  • breakers to. preven.t 'operation* in the "test" position. * . . . _.*

~, *'

  • 'Eyaluate GOP 14, Step 6.5 and Attachment 3 with respect to this event. -
  • This evaluatiort:shoul~ ensure Operations Management's e~pectations are

.'clearly defi.ned *to thE? shift SROs via this procedure. *Modify' the *

    • proce.dure-as necessary.: as a result of this evaluation-_.' ..
    • ADDITIONAL INFORMATION None