ML17266A226: Difference between revisions

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| issue date = 06/30/1980
| issue date = 06/30/1980
| title = LER 80-028/03L-0:on 800531,during Normal Operations,Channel a of 1A Steam Generator Low Pressure Trip Failed.Caused by Failure of Power Supply Associated W/Channel A.Vendor Contacted & New Power Supply Installed & Tested
| title = LER 80-028/03L-0:on 800531,during Normal Operations,Channel a of 1A Steam Generator Low Pressure Trip Failed.Caused by Failure of Power Supply Associated W/Channel A.Vendor Contacted & New Power Supply Installed & Tested
| author name = SCHOPPMAN M A
| author name = Schoppman M
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  

Revision as of 02:50, 19 June 2019

LER 80-028/03L-0:on 800531,during Normal Operations,Channel a of 1A Steam Generator Low Pressure Trip Failed.Caused by Failure of Power Supply Associated W/Channel A.Vendor Contacted & New Power Supply Installed & Tested
ML17266A226
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 06/30/1980
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17208A808 List:
References
LER-80-028-03L, LER-80-28-3L, NUDOCS 8007140372
Download: ML17266A226 (2)


Text

NRC PQRIElQ44 P 77l LICENSEE EVENT REPORT UE*E4UCI.fAR RSCULATORY C~~IEIISSIQN

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