ML17266A410: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:HRCPORMSEE lZ 77l LICENSEE EVENT REPORT U S NUCLEAR RECULATORY COMMISSION 1 CON'T~O 1 CONTROL E I.CCIEI I I I'Qi IPSE PAINT OR TYPE ALI REOUIREO INPORMATIONl I Fl I S LIS 1Qz>HI-0 ttlIH Iil 9-9 9 QZ4 9 UCE.'l$4$CQQE 14'5 UCSNS4 NUM 4f B 1$I l I IQ<<~Qi 1104NSE TYS'E 40 Si<<AT 5$8''i<<iii 8 i$0$1 OCTET NVMEEA'$4$EVENT QAT$14 15 EVENT OESCRIPTION ANO>ROSAELE CONSECUENCES QIO During 100/power o eration the DDPS corn uter droo e 2I21 61 8 1 Q9 Af rOAT CATE 10 resulted in a loss of the CEA pulse countin backu osition indicati n.Action was taken in accordance with T.S.1.3.3.d.
{{#Wiki_filter:HRCPORMSEE                                                                                                                                       U S NUCLEAR RECULATORY COMMISSION lZ 77l LICENSEE EVENT REPORT CONTROL         E I.CCIEI                   I     I           I       'Qi                     IPSE PAINT OR TYPE ALI REOUIREO INPORMATIONl I
The DDPS was line and backup CEA position indication restored in 30 minutes which is well within limits., This is the 22nd event for loss of DDPS and backup.position indication for the CEA's.5Y5TEM CAVSE CAU5$CCMBI YALYE Coot CQQE 5USCQOE CCMSONEHT CQOE 5VSCQOSSUECQOS RLJS 4IS LJS~G i48 L'JS a 9 10 11 II la 1919~0 SEQUENTIAL OCCJABENCE BEPOAT IIEVISION~LEBIBO EVENTY8~4>
Fl                   LIS                               HI-                         Iil     9 9 9 QZ4                           I l I IQ<<
llfrOATNO COO E 1Y8E~No, Q'-~>>m~i~~m~uLIW.I I II 15 I~1~11<<5<<9<<0~)II ACTlON J AVTVAE tr SEC 514UTQOWN ATTACIiMENT'l)llO<<4 41IIMEC<<JMW CQMSONENT TAKEN Ai.TIQN CN PLANT'tTNOQ NOVAS ZZ SVSMITTSO rOAM>U$.SvrrUEB MANVPACTUAEB 44ihJS HIS 4iS i'LJ8 LJS i-'8~8 IO 54-A 14 51~40 41 45 44, 41 CAUSP.OESCRIPTION ANO CORREC IVE ACTIONS QZT 5 The loss of DDPS is sof tware re lated.Inves t i gat ion of the sof tware rob-lem is currently in progress by the vendor and FP&L.1 a 9$4CIUTY STA11is'.ro84EB.OTNEBSTAIVS QZO i8i L'JS~i'S~9 10 II II 44 ACTIVITY CQNTENT IIELEASEO OP O'EI fASt'MQVNl'QP ACIIVITY QZS~~QO.NA 1 5 9 10 Il 44 rSA'SQNNE L tlCAOSUBES
                                                                                                      'i<<iii I S                          1Qz      >                    0      ttlIH                                                                                ~
'NUMSEB TYSE OESCPIrnON Q~~r~F999'O~~O" 8A 1 5)l I lI II SSBSCNN EL INIU RIES~ia~SP 9 Q<<i" NA ufTNQO Ol'ISCQVf BY 4$4$45 olscovEBY olscBISTIQN Qsz 0 erator Observation LOCATION OP RELEASE QE NA 50 10 10 1 I 9 I'I I'I 1 a a NAAIE OP PREPARER I.c55 op cll 5AM*et o AAQIUTY Q4$.YSS OESCBISTIQN MOZ 1'0 SVSUC'>>Issvzo ofscBln..oN 9 I~'Q44'1'.0'A P.L.Pace 10 NRC USE OHI.Y 4$$9 IO rNONEI 305 552-3801'8103>60 7~8.
Qi 1            9         UCE.'l$ 4$ CQQE                 14'5                             UCSNS4     NUM 4f B                         1$             1104NSE TYS'E     40   Si <<AT 5$
r~j}}
      ~O 1
CON'T
                                        $0 8      $1           OCTET
                                                                                        '
NVMEEA'$ 4$ EVENT QAT$
8i 14     15 2I21    61 AfrOAT CATE 8    1 10 Q9 EVENT OESCRIPTION ANO >ROSAELE CONSECUENCES QIO During 100/ power o eration the DDPS corn uter droo e resulted in a loss of the CEA pulse countin backu                                                                                     osition indicati n.
Action was taken in accordance with T.S.1.3.3.d. The DDPS was line and backup CEA position indication restored in 30 minutes which is well within limits., This is the 22nd event for loss of DDPS and backup.
position indication for the CEA's.
a Q '- ~>>
9 5Y5TEM Coot RLJS 4IS LJS 10 CAVSE CQQE 11 CAU5$
5USCQOE II SEQUENTIAL llfrOATNO
                                                                                                          ~G la CCMSONEHT CQOE OCCJABENCE CCMBI 5VSCQOSSUECQOS 1919i48 L'JS BEPOAT YALYE
                                                                                                                                                                            ~0 IIEVISION ~
                                                                                                                                                                                      ~8 EVENTY8~4>                                                                                     COO E             1Y8E   ~                   No, LEBIBO I I        II m ~i~~
15               I ~               1~
m~
11 uLIW.
                                                                                                                                          <<5       <<9         <<0             ~)
II ACTlONJ AVTVAE                       tr SEC           514UTQOWN                                               ATTACIiMENT'l)llO<<4               41IIMEC<<JMW           CQMSONENT CN PLANT'tTNOQ TAKEN Ai.TIQN 44ihJS HIS IO           54-                     A 4iS 14               51 i  '
NOVAS
                                                                                                              ~
ZZ 40 SVSMITTSO LJ8 LJS 41 rOAM>U$.
45 i'8 SvrrUEB          MANVPACTUAEB 44,           41 CAUSP. OESCRIPTION ANO CORREC                             IVE ACTIONS is sof tware re lated . Inves t igat ion of the sof tware rob-QZT 5          The      loss of                  DDPS lem     is currently in progress by the vendor and FP&L.
1     a i8i L'JS 9
9
                    $ 4CIUTY STA11is ACTIVITY IIELEASEO OP O'EI
                                      ~i'
                                '.ro84EB.
10 CQNTENT fASt II S~  II
                                                          'MQVNl'QP ACIIVITY OTNEBSTAIVS          QZO QZS 44 ufTNQO 4$
BY Ol'ISCQVf 4$
0 olscovEBY olscBISTIQN Qsz erator Observation LOCATION OP RELEASE QE 50
                                      'A
                                      ~~QO.                   NA                                                                          NA 1     5     9               10               Il                                               44           45                                                                            10 rSA'SQNNE L tlCAOSUBES
        ~r 1      5    )
                          'NUMSEB
                      ~F999 'O~~O" lI TYSE lI OESCPIrnON Q~
II 8A 10 SSBSCNN EL       INIU RIES
        ~ia ~SP                       9     Q<<i
                                                                              "
NA 1     I     9                 I 'I       I 'I I.c55 op   cll 5AM*et o AAQIUTYQ4$
                        .YSS       OESCBISTIQN 1      a MOZ 1       '0 SVSUC'>>                                                                                                                                               NRC USE OHI.Y 10 Issvzo       ofscBln..oN 9
                          ~'Q44 I
a      '1         '.0                                                                                                                                 4$  $9                        IO NAAIE OP PREPARER                                    P. L. Pace                                                     rNONEI         305       552-3801' 8103 >60 7~8.
 
r~
j}}

Revision as of 16:25, 29 October 2019

LER 81-008/03L-0:on 810202,digital Data Processing Sys Dropped Off Line Resulting in Loss of Control Element Assembly Pulse Counting Backup Position Indication.Caused by software-related Problems.Investigation Continuing
ML17266A410
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 02/26/1981
From: Pace P
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17209A814 List:
References
LER-81-008-03L, LER-81-8-3L, NUDOCS 8103160758
Download: ML17266A410 (2)


Text

HRCPORMSEE U S NUCLEAR RECULATORY COMMISSION lZ 77l LICENSEE EVENT REPORT CONTROL E I.CCIEI I I I 'Qi IPSE PAINT OR TYPE ALI REOUIREO INPORMATIONl I

Fl LIS HI- Iil 9 9 9 QZ4 I l I IQ<<

'i<<iii I S 1Qz > 0 ttlIH ~

Qi 1 9 UCE.'l$ 4$ CQQE 14'5 UCSNS4 NUM 4f B 1$ 1104NSE TYS'E 40 Si <<AT 5$

~O 1

CON'T

$0 8 $1 OCTET

'

NVMEEA'$ 4$ EVENT QAT$

8i 14 15 2I21 61 AfrOAT CATE 8 1 10 Q9 EVENT OESCRIPTION ANO >ROSAELE CONSECUENCES QIO During 100/ power o eration the DDPS corn uter droo e resulted in a loss of the CEA pulse countin backu osition indicati n.

Action was taken in accordance with T.S.1.3.3.d. The DDPS was line and backup CEA position indication restored in 30 minutes which is well within limits., This is the 22nd event for loss of DDPS and backup.

position indication for the CEA's.

a Q '- ~>>

9 5Y5TEM Coot RLJS 4IS LJS 10 CAVSE CQQE 11 CAU5$

5USCQOE II SEQUENTIAL llfrOATNO

~G la CCMSONEHT CQOE OCCJABENCE CCMBI 5VSCQOSSUECQOS 1919i48 L'JS BEPOAT YALYE

~0 IIEVISION ~

~8 EVENTY8~4> COO E 1Y8E ~ No, LEBIBO I I II m ~i~~

15 I ~ 1~

m~

11 uLIW.

<<5 <<9 <<0 ~)

II ACTlONJ AVTVAE tr SEC 514UTQOWN ATTACIiMENT'l)llO<<4 41IIMEC<<JMW CQMSONENT CN PLANT'tTNOQ TAKEN Ai.TIQN 44ihJS HIS IO 54- A 4iS 14 51 i '

NOVAS

~

ZZ 40 SVSMITTSO LJ8 LJS 41 rOAM>U$.

45 i'8 SvrrUEB MANVPACTUAEB 44, 41 CAUSP. OESCRIPTION ANO CORREC IVE ACTIONS is sof tware re lated . Inves t igat ion of the sof tware rob-QZT 5 The loss of DDPS lem is currently in progress by the vendor and FP&L.

1 a i8i L'JS 9

9

$ 4CIUTY STA11is ACTIVITY IIELEASEO OP O'EI

~i'

'.ro84EB.

10 CQNTENT fASt II S~ II

'MQVNl'QP ACIIVITY OTNEBSTAIVS QZO QZS 44 ufTNQO 4$

BY Ol'ISCQVf 4$

0 olscovEBY olscBISTIQN Qsz erator Observation LOCATION OP RELEASE QE 50

'A

~~QO. NA NA 1 5 9 10 Il 44 45 10 rSA'SQNNE L tlCAOSUBES

~r 1 5 )

'NUMSEB

~F999 'O~~O" lI TYSE lI OESCPIrnON Q~

II 8A 10 SSBSCNN EL INIU RIES

~ia ~SP 9 Q<> NRC USE OHI.Y 10 Issvzo ofscBln..oN 9

~'Q44 I

a '1 '.0 4$ $9 IO NAAIE OP PREPARER P. L. Pace rNONEI 305 552-3801' 8103 >60 7~8.

r~

j