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| * APPROVED OMB NO. 3160-0104 EXPIRES: 9/31196 LICENSEE EVENT REPORT (LERI FACILITY NAME 111 DOCKET NUMBER 121 PAGE 131 Palisades Plant 01s101010121s1s 1 I OF 01 5 TITLE 141 PRESSURIZER PENETRATION SAFE END CRACK RESULTS IN PCS LEAKAGE I EVENT DATE 161 LER NUMBER 161 REPORT DATE 161 OTHER FACILITIES INVOLVED !Bl SEQUENTIAL REVISION FACILITY NAMES MONTH DAY YEAR YEAR NUMBER NUMBER MONTH* DAY YEAR N/A 0161010101 I --01 9 i I 9 9 3 3 01 o I 9 o I o 11 0 i I s 3 N/A 0161010101 I THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR I: !Ch.ck OM or more of tM following/ | | * APPROVED OMB NO. 3160-0104 EXPIRES: 9/31196 LICENSEE EVENT REPORT (LERI FACILITY NAME 111 DOCKET NUMBER 121 PAGE 131 Palisades Plant 01s101010121s1s 1 I OF 01 5 TITLE 141 PRESSURIZER PENETRATION SAFE END CRACK RESULTS IN PCS LEAKAGE I EVENT DATE 161 LER NUMBER 161 REPORT DATE 161 OTHER FACILITIES INVOLVED !Bl SEQUENTIAL REVISION FACILITY NAMES MONTH DAY YEAR YEAR NUMBER NUMBER MONTH* DAY YEAR N/A 0161010101 I --01 9 i I 9 9 3 3 01 o I 9 o I o 11 0 i I s 3 N/A 0161010101 I THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR I: !Ch.ck OM or more of tM following/ |
| 1111 OPERATING N MOOE 191 20.4021bl 20.4061cl 60.731a)(211iv) 73.71 (bl *---POWER I 20.406(*111 | | 1111 OPERATING N MOOE 191 20.4021bl 20.4061cl 60.731a)(211iv) 73.71 (bl *---POWER I 20.406(*111 |
| )(ii 60.36icll1 I 60. 7 3(a)(21M 73.71 lei LEVEL I I o --I---1101 20.4061al11 l(iil 60.36(c)(21 | | )(ii 60.36icll1 I 60. 7 3(a)(21M 73.71 lei LEVEL I I o --I---1101 20.4061al11 l(iil 60.36(c)(21 |
| : 60. 73(al12)(vii) | | : 60. 73(al12)(vii) |
| OTHER (Specify in Abatract ---20.406(a)(1 | | OTHER (Specify in Abatract ---20.406(a)(1 |
| )(iiil 60.73(all211il | | )(iiil 60.73(all211il |
| : 60. 7 3 (a)(2) (viii) IA) below end in Text, ---* 20 .406la)(1 | | : 60. 7 3 (a)(2) (viii) IA) below end in Text, ---* 20 .406la)(1 |
| )(iv) x. 60.731all211iil | | )(iv) x. 60.731all211iil |
| : 60. 7 31all211viiillBI NRC Form 366Ai --20.4061all1 IM 60.731all211iiil | | : 60. 7 31all211viiillBI NRC Form 366Ai --20.4061all1 IM 60.731all211iiil |
| : 60. 7 31all211xl LICENSEE CONTACT FOR THIS LER 112) NAME TELEPHONE NUMBER William L. Roberts, Staff Licensing Engin_eer 1 7 1 6 1 4 1 -I a I s I , I 3 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 MAN.UFA.C* | | : 60. 7 31all211xl LICENSEE CONTACT FOR THIS LER 112) NAME TELEPHONE NUMBER William L. Roberts, Staff Licensing Engin_eer 1 7 1 6 1 4 1 -I a I s I , I 3 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 MAN.UFA.C* |
| REPORTABLE MANUFAC* REPORTABLE CAUSE SYSTEM COMPONENT TUR ER TO NPROS . CAUSE SYSTEM COMPONENT TUR ER TO NPROS I I I I I I I I I I I I I I I I I I I I I I I I I I I i SUPPLEMENTAL REP.ORT EXPECTED 1141 MONTH DAY YEAR I EXPECTED I l YES Vf yes, complere EXPECTED_ | | REPORTABLE MANUFAC* REPORTABLE CAUSE SYSTEM COMPONENT TUR ER TO NPROS . CAUSE SYSTEM COMPONENT TUR ER TO NPROS I I I I I I I I I I I I I I I I I I I I I I I I I I I i SUPPLEMENTAL REP.ORT EXPECTED 1141 MONTH DAY YEAR I EXPECTED I l YES Vf yes, complere EXPECTED_ |
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| 0 0 9 -0 0 0 3 o* 0 5 Analysis is ongoing to determine the margin-to-failure for the cracked PORV nozzle safe-end. | | 0 0 9 -0 0 0 3 o* 0 5 Analysis is ongoing to determine the margin-to-failure for the cracked PORV nozzle safe-end. |
| This analysis will provide the conclusion for the severity of the crack growth. SAFETY SIGNIFICANCE These three scenarios are hypothesized to judge the possible safety 6f | | This analysis will provide the conclusion for the severity of the crack growth. SAFETY SIGNIFICANCE These three scenarios are hypothesized to judge the possible safety 6f |
| * event had it occurred while the plant was at power operation. | | * event had it occurred while the plant was at power operation. |
| : 1. A leak of the same size as was experienced during this event could have resulted. | | : 1. A leak of the same size as was experienced during this event could have resulted. |
| The Technical Specifications leakage limit of 1 gpm unidentified leakage may have been approached or exceeded and a normal shutdown would occur. 2. A leak could have started small and gradually progressed in size over time. As the leak increased in size monitoring the increasing leakage into the containment sump would have allowed us to take actions to shut the plant down. Exceeding 1 gpm leakage unidentified would require plant shutdotwn. | | The Technical Specifications leakage limit of 1 gpm unidentified leakage may have been approached or exceeded and a normal shutdown would occur. 2. A leak could have started small and gradually progressed in size over time. As the leak increased in size monitoring the increasing leakage into the containment sump would have allowed us to take actions to shut the plant down. Exceeding 1 gpm leakage unidentified would require plant shutdotwn. |
| : 3. The cracking could have been initially more severe such that a much larger leak developed. | | : 3. The cracking could have been initially more severe such that a much larger leak developed. |
| In the case of the PORV piping, the limiting size of the leak is the cross sectional area of the pressurizer relief valve nozzle. Analysis has been completed for small break LOCAs for up to a one square foot break size * (CENPD-137 Supplement 1-P, "Small Break Model Calculative Methods for the CE Small Break LOCA Evaluation Model," January 1977). Since the PORV nozzle is a three inch nozzle, the area available to leak would be 0.05 square feet. Analysis indicates that the maximum fuel cladding temperature predicted for a small break LOCA of this size is 660°F. The maximum thickness of cladding oxidation is predicted to be 0.002% of the cladding wall thickness. | | In the case of the PORV piping, the limiting size of the leak is the cross sectional area of the pressurizer relief valve nozzle. Analysis has been completed for small break LOCAs for up to a one square foot break size * (CENPD-137 Supplement 1-P, "Small Break Model Calculative Methods for the CE Small Break LOCA Evaluation Model," January 1977). Since the PORV nozzle is a three inch nozzle, the area available to leak would be 0.05 square feet. Analysis indicates that the maximum fuel cladding temperature predicted for a small break LOCA of this size is 660°F. The maximum thickness of cladding oxidation is predicted to be 0.002% of the cladding wall thickness. |
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| YEAA NUMBER REVISION NUMBER Palisades Plant O 5 0 O 0 2 5 5 9 3 - | | YEAA NUMBER REVISION NUMBER Palisades Plant O 5 0 O 0 2 5 5 9 3 - |
| 0 0 9 -0 0 0 4 o* 0 5 or erm 1. An engineering evaluation of the failure has been conducted. | | 0 0 9 -0 0 0 4 o* 0 5 or erm 1. An engineering evaluation of the failure has been conducted. |
| The specific elements of this engineering analysis included the following: | | The specific elements of this engineering analysis included the following: |
| : a. Metallurgical analysis of the failed safe end to identify the cause of the crack. b. Analysis of factors contributing to PWSCC in the pressurizer nozzle safe end. This includes evaluation of material properties and stresses that may have contributed to the failure. Piping stresses and weld residual stresses are being evaluated and will be reviewed by an independent third party. . c. Evaluation of other nozzles safe ends in the primary coolant system, based on the engineering evaluation of the failure, to identify other locations which may be susceptible to the same failure cause. This evaluation includes both nozzles with Inconel 600 safe ends and other safe end materials. | | : a. Metallurgical analysis of the failed safe end to identify the cause of the crack. b. Analysis of factors contributing to PWSCC in the pressurizer nozzle safe end. This includes evaluation of material properties and stresses that may have contributed to the failure. Piping stresses and weld residual stresses are being evaluated and will be reviewed by an independent third party. . c. Evaluation of other nozzles safe ends in the primary coolant system, based on the engineering evaluation of the failure, to identify other locations which may be susceptible to the same failure cause. This evaluation includes both nozzles with Inconel 600 safe ends and other safe end materials. |
| Contributing factors to PWSCC will also be evaluated for the safe ends that are identified as being susceptible to the same failure cause .. This will include evaluation of material properties and stresses. | | Contributing factors to PWSCC will also be evaluated for the safe ends that are identified as being susceptible to the same failure cause .. This will include evaluation of material properties and stresses. |
| : d. Evaluation of appropriate non-destructive examination techniques to identify similar flaws in other susceptible safe ends. 2. Corrective actions for the specific safe end that failed have been identified. | | : d. Evaluation of appropriate non-destructive examination techniques to identify similar flaws in other susceptible safe ends. 2. Corrective actions for the specific safe end that failed have been identified. |
| An engineering evaluation of the repair to the pressurizer safe based* on the root cause analysis of the failure, has shown that the lifetime of the repaired safe end well exceeds the length of the next operating cycle. | | An engineering evaluation of the repair to the pressurizer safe based* on the root cause analysis of the failure, has shown that the lifetime of the repaired safe end well exceeds the length of the next operating cycle. |
| * 3. Corrective actions for other safe ends that may be susceptible to the same failure have peen identified. | | * 3. Corrective actions for other safe ends that may be susceptible to the same failure have peen identified. |
| Other safe ends that may be susceptible to the same failure have been inspected for flaws using appropriate non-destructive examination techniques. | | Other safe ends that may be susceptible to the same failure have been inspected for flaws using appropriate non-destructive examination techniques. |
| : 4. Necessary corrective actions to ensure safe operation of Palisades during the next . operating cycle prior to returning the plant to service will be completed. | | : 4. Necessary corrective actions to ensure safe operation of Palisades during the next . operating cycle prior to returning the plant to service will be completed. |
| : a. Repair of the failed pressurizer safe end. b. Non-destructive examinations of other safe ends potentially susceptible to the same failure cause. Results of the short term corrective actions were transmitted to the NRC in a report dated October 7, 1993. | | : a. Repair of the failed pressurizer safe end. b. Non-destructive examinations of other safe ends potentially susceptible to the same failure cause. Results of the short term corrective actions were transmitted to the NRC in a report dated October 7, 1993. |
| *RC FOfm JeeA f9-8JI . FACILITY NAME 11 I LICENSEE EVENT REPORT !LERI TEXT CONTINUATION OOCIC:E"T NUMBER 121 LER NUMBEl'I 131 SEQUENTIAL. | | *RC FOfm JeeA f9-8JI . FACILITY NAME 11 I LICENSEE EVENT REPORT !LERI TEXT CONTINUATION OOCIC:E"T NUMBER 121 LER NUMBEl'I 131 SEQUENTIAL. |
| YEAR NUMBER u:s. NUClEAA REGUUITORY C0"'"''5SlC>< | | YEAR NUMBER u:s. NUClEAA REGUUITORY C0"'"''5SlC>< |
| APl"IOVEO OMB '<0. J'60-01C* | | APl"IOVEO OMB '<0. J'60-01C* |
| EXPIRES: 8/31 i86 RE'\11SION NUMBER PAGE 141 Pal.isades Plant 0500025593 -oo 9 -0 0 0 5 o* O 5 Long Term 5. Corrective actions necessary to ensure long term safe operation of Palisades will be identified. | | EXPIRES: 8/31 i86 RE'\11SION NUMBER PAGE 141 Pal.isades Plant 0500025593 -oo 9 -0 0 0 5 o* O 5 Long Term 5. Corrective actions necessary to ensure long term safe operation of Palisades will be identified. |
| : a. Engineering of additional repairs which may be necessary for long term operation of the pressurizer safe ends will be performed and additional . repairs and | | : a. Engineering of additional repairs which may be necessary for long term operation of the pressurizer safe ends will be performed and additional . repairs and |
| *actions, if required, will be by the end of the next refueling shutdown. | | *actions, if required, will be by the end of the next refueling shutdown. |
|
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18065B1151997-12-0909 December 1997 LER 97-013-00:on 971110,failure to Closure Test Two Check Valves Resulted in Violation of TS 6.5.7 Occurred.Caused by Close Function for Check Valves.Check Valves Tested to Confirm Proper Closure Capability ML18067A7751997-11-11011 November 1997 LER 97-011-00:on 971012,primary Coolant Pump Was Started W/Sg Temperatures Greater than Cold Leg Temperature.Caused by Inadequate Procedures & Operator Decision Making.Critique of Event Conducted W/Operators Involved ML18067A7581997-10-30030 October 1997 LER 97-010-00:on 970930,determined That Inadequacy in App R Analysis Resulted in Condition Outside Design Basis of Plant.Caused by Missing Cable in Circuit & Raceway Schedule. Developed New Evaluation Re ASD Valves Validation ML18067A7461997-10-23023 October 1997 LER 97-009-00:on 970923,discovered Procedure Weakness Re Implementation of App R Shutdown Methodology.Caused by Human Error.Revised Off-Normal Procedure ONP-25.2, Alternate Safe Shutdown Procedure. ML18067A7191997-10-10010 October 1997 LER 97-008-00:on 970912,spurious Valve Operation Could Result in Loss of Shutdown Capabilities Per 10CFR50,App R, Section Iii.L,Was Discovered.Caused by Failure to Validate Info from App R.Design Bases for SW Backup Reviewed ML18067A6951997-09-24024 September 1997 LER 97-007-00:on 970826,discovered Inadequate Testing of DG Sequencer Control Relay Contacts.Caused by Oversight on Part of Personnel Involved in Installation of Facility Change FC-800.Tested 106D-1/XL & 106D-2/XL Relay Contacts ML18067A5651997-06-0303 June 1997 LER 96-013-01:on 961115,DC Breaker Failed During Testing for as-found Trip Setting.Failure Caused by Oversight within Preventive Maint Program.Breaker Was Replaced & Tested ML18067A5461997-05-12012 May 1997 LER 97-006-00:on 970412,overtime Limits Were Exceeded for Radiation Protection Technicians.Caused by Inadequate Design,Review & Proper Verifications of Overtime Work Schedule.Communicate Overtime Limitation Responsibilities ML18067A4431997-03-24024 March 1997 LER 97-004-00:on 970221,trip of High Pressure Safety Injection Pump Occurred While Filling Safety Injection Tank Resulting in TS Violation.Caused by Particle Lodged Between Surface of Indication disk.Y-phase Relay Was OOS ML18067A4391997-03-21021 March 1997 LER 97-005-00:on 961220,operation of Plant Outside Design Basis Occurred Due to an Unacceptable Repair on Main Steam Isolation Valves.Pipe Plugs Permanently Repaired ML18067A4401997-03-21021 March 1997 LER 97-003-00:on 961101,four Piping Lines Were Determined to Be Potentially Susceptible to Pressurization Due to Containment Temperature Increase During an Accident.Cac Discharge Piping Will Be verified.W/970321 Ltr ML18066A8931997-02-21021 February 1997 LER 97-002-00:on 970123,failure to Meet TSs 4.5.2d(1)(b) for Testing of Emergency Escape Airlock Occurred.Caused by Missed Surveillance.Emergency Escape Air Lock Testing Was Completed & Declared operable.W/970221 Ltr ML18066A8751997-02-0505 February 1997 LER 97-001-00:on 970106,TAVE Temp Dropped Below Minimum Temp for Criticality.Caused by Control Rod Withdrawal Rate to Increase Power Not Sufficient to Match Increase in Steam. Turbine Bypass Valve Actuator repaired.W/970205 Ltr ML18066A8041996-12-23023 December 1996 LER 96-014-00:on 961124,class 1E Raychem Cable Splices Were Installed Incorrectly.Caused by Incorrectly Made Electrical Splices.Total of 270 Splices Have Been Replaced within Containment ML18066A7831996-12-16016 December 1996 LER 96-013-00:on 961115,DC Breaker Failure During Testing for as-found Trip Setting Occurred.Cause Under Investigation.All molded-case Circuit Breakers in DC Distribution Panels Were Replaced ML18065A9951996-10-0404 October 1996 LER 96-002-01:on 960116,initiated TS Required Shutdown Due to Safeguards Cable Fault.Both Sets (Six Cables) of Cables Were Replaced & Installed Through Turbine Generator Bldg ML18065A9171996-09-0909 September 1996 LER 95-012-00:on 960809,TS Violation Occurred,Due to No Senior Reactor Operator in Cr.Caused by Extensive Remodeling.Cr Remodeling completed.W/960909 Ltr ML18065A8961996-08-29029 August 1996 LER 96-011-00:on 960730,CR Continuous Air Monitor Alarm Setpoint Improperly Established.Caused by Failure to Utilize Mod Process in 1988 Leading to Failure to Properly Select & Calibrate Instruments ML18065A8811996-08-20020 August 1996 LER 96-005-01:on 960207,determined Fuse on Main Supply to Two Safety Related DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Lack of Thorough Associated Circuits Analysis.Supply Fuse to Panels Replaced ML18065A8741996-08-16016 August 1996 LER 96-010-00:on 960717,high Pressure Safety Injection Pump Tripped While Filling Safety Injection Tank.Caused by Faulty 150/151Y-207 Time Overcurrent Relay.All Similar Relays in Time Overcurrent Application Have Been Inspected ML18065A8651996-08-12012 August 1996 LER 96-009-00:on 960712,identified Penetration Seal Deficiency on Fire Barriers Caused by Failure to Perform & Document Comprehensive Fire Barrier Evaluation.Developed Basis document.W/960812 Ltr ML18065A8601996-08-0202 August 1996 LER 96-006-01 on 960207,discovered Limits of Design Analysis Could Have Been Violated.Subsequent Tests & Analyses Facility Did Not Exceed Basis.Operating Procedures Have Been Revised to Treat 2530 Megawatts Limit as Absolute Limit ML18065A8321996-08-0101 August 1996 LER 96-003-01:on 960115,alternate Shutdown Panel Inverter Resulted in Unavailability of Panel.Replaced Defective Inverter Alarm Logic Board ML18065A7691996-06-12012 June 1996 LER 96-008-00:on 960513,fire Door Not Maintained Open in Accordance W/Design Basis.Cause Under Investigation. Engineering Evaluation Performed & Revised Documents, Surveillance & Test procedures.W/960612 Ltr ML18065A6901996-05-0101 May 1996 LER 95-001-01:on 950302,malfunction of Left Channel DBA Sequencer Resulted in Inadvertent Actuation of Left Channel Safeguards Equipment.Replaced microprocessor.W/960501 Ltr ML18065A6681996-04-22022 April 1996 LER 96-007-00:on 960321,inadequate Emergency Lighting & Ventilation in post-fire Safe Shutdown Areas.Caused by App R Program Documentation Insufficient to Demonstrate Regulatory Compliance.Lighting modified.W/960422 Ltr ML18065A5721996-03-11011 March 1996 LER 96-006-00:on 960207,average Reactor Power Level Exceeded License Limit Due to Insufficient Procedural Guidance. GOP-12 Revised to Treat 2,530 Mwt Limit as Absolute Limit Requiring Immediate Corrective Action If Exceeded ML18065A5261996-03-0101 March 1996 LER 96-005-00:on 960202,fuse on Main Supply to Two SR DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Inadequate Electrical/App R Design Review.Implemented Hourly Fire tours.W/960301 Ltr ML18065A5111996-02-19019 February 1996 LER 94-012-02:on 940427,determined That Internal Ground in Thermal Margin Monitor Causes Nonconformance W/Rps Design Basis.Incorporated RPS Failure Modes & Effects Analysis in Plant DBD.W/960219 Ltr ML18065A5061996-02-19019 February 1996 LER 96-004-00:on 960118,SIS Disabled W/Primary Coolant Sys Greater than 300 F.Caused by Personnel Error.Permanent Maint Procedure to Disable/Enable SIS Actuation on Low Pressurizer Pressure Will Be Revised to Align W/Ts ML18065A5021996-02-15015 February 1996 LER 96-003-00:on 960115,technicians Found Low Voltage cut- Off for Alternate Shutdown Panel Inverter Set That Resulted in Unavailability of Panel.Caused by Inadequate Post Mod. Readjusted Set Point to Minimum setting.W/960215 Ltr ML18065A4581996-01-31031 January 1996 LER 96-001-00:on 960103,failed to Test Duplicate Equipment. Caused by STS No Longer Containing Requirement for cross- Train Testing of Duplicate Components.Will Submit Request to Delete Subj Requirements from TS.W/960131 Ltr ML18065A4421996-01-19019 January 1996 LER 95-016-00:on 951226,did Not Analyze Primary Coolant Samples within 72 H.Caused by Belief Acceptability to Save Pcs Samples for Choride Analysis Past 72 H.Counseled Chemistry Supervision.W/960119 Ltr ML18065A4041996-01-15015 January 1996 LER 95-014-00:on 950119,PCP Oil Collection Deficiencies Created by FC-860 Piping Mod.Caused by Inadequate DBD for Sys & Lack of Review by Experienced Fire Protection Personnel.Updated Design Basis documentation.W/960115 Ltr ML18065A3291995-12-0404 December 1995 LER 95-013-00:on 951103,circuit Fuse Coordination Deficiency Which Affects App R Safe Shutdown Equipment Noted.Design of Fuse Coordination in Potential Transformer Circuits Will Be Evaluated & Modified as required.W/951204 Ltr ML18065A2361995-11-0202 November 1995 LER 95-012-00:on 950701,discovered Unqualified Electrical Connection in Containment SW Outlet Valve Controller.Caused by Failure of Assigned Engineers to Available Info.Replaced Wire Nuts W/Inline Butt connections.W/951102 Ltr ML18065A2051995-10-20020 October 1995 LER 95-008-01:on 950728,discovered That None of Four Containment High Pressure Channels Would Initiate Reactor Trip Due to Programmatic Deficiencies.Administrative Procedure (AP) 9.44,AP 9.45 & AP 10.44 Will Be Revised ML18065A0841995-09-18018 September 1995 LER 95-011-00:on 950817,CR 40 Withdrawal Occurred When Given Insertion Signal Due to skill-based Error in Crimping & Removing Foreign Matl from CRDM Motor Connection Box.Crd Package replaced.W/950918 Ltr ML18065A0681995-09-14014 September 1995 LER 95-010-00:on 950815,ESFA Resulted in Manual Rt Following Isolation of Pcs.Replaced Failed Instrument Line ML18065A0651995-09-0808 September 1995 LER 95-009-00:on 950728,discovered Lack of Procedural Guidance for Pump Repair Following Fire.Proposed Use of Power Supply Breaker Did Not Adequately Address Effect of Loss of Control Power.Performed Independent Assessment ML18064A8781995-08-28028 August 1995 LER 95-008-00:on 950728,discovered During Design Change Testing That None of Four Containment High Pressure Channels Would Initiate Rt.Caused by Programmatic Deficiencies. Reviewed Selected Tests & Mods from Recent Refueling Outage ML18064A8831995-08-21021 August 1995 LER 95-007-00:on 950720,discovered That 12 Instrument Loops Had V-bolted Type Qualified Cable Splices Connected to Wires W/Exposed Kapton Insulation.Caused by Human Error.All V- Bolted Splices Replaced w/in-line design.W/950821 Ltr 1999-09-02
[Table view] Category:RO)
MONTHYEARML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18065B1151997-12-0909 December 1997 LER 97-013-00:on 971110,failure to Closure Test Two Check Valves Resulted in Violation of TS 6.5.7 Occurred.Caused by Close Function for Check Valves.Check Valves Tested to Confirm Proper Closure Capability ML18067A7751997-11-11011 November 1997 LER 97-011-00:on 971012,primary Coolant Pump Was Started W/Sg Temperatures Greater than Cold Leg Temperature.Caused by Inadequate Procedures & Operator Decision Making.Critique of Event Conducted W/Operators Involved ML18067A7581997-10-30030 October 1997 LER 97-010-00:on 970930,determined That Inadequacy in App R Analysis Resulted in Condition Outside Design Basis of Plant.Caused by Missing Cable in Circuit & Raceway Schedule. Developed New Evaluation Re ASD Valves Validation ML18067A7461997-10-23023 October 1997 LER 97-009-00:on 970923,discovered Procedure Weakness Re Implementation of App R Shutdown Methodology.Caused by Human Error.Revised Off-Normal Procedure ONP-25.2, Alternate Safe Shutdown Procedure. ML18067A7191997-10-10010 October 1997 LER 97-008-00:on 970912,spurious Valve Operation Could Result in Loss of Shutdown Capabilities Per 10CFR50,App R, Section Iii.L,Was Discovered.Caused by Failure to Validate Info from App R.Design Bases for SW Backup Reviewed ML18067A6951997-09-24024 September 1997 LER 97-007-00:on 970826,discovered Inadequate Testing of DG Sequencer Control Relay Contacts.Caused by Oversight on Part of Personnel Involved in Installation of Facility Change FC-800.Tested 106D-1/XL & 106D-2/XL Relay Contacts ML18067A5651997-06-0303 June 1997 LER 96-013-01:on 961115,DC Breaker Failed During Testing for as-found Trip Setting.Failure Caused by Oversight within Preventive Maint Program.Breaker Was Replaced & Tested ML18067A5461997-05-12012 May 1997 LER 97-006-00:on 970412,overtime Limits Were Exceeded for Radiation Protection Technicians.Caused by Inadequate Design,Review & Proper Verifications of Overtime Work Schedule.Communicate Overtime Limitation Responsibilities ML18067A4431997-03-24024 March 1997 LER 97-004-00:on 970221,trip of High Pressure Safety Injection Pump Occurred While Filling Safety Injection Tank Resulting in TS Violation.Caused by Particle Lodged Between Surface of Indication disk.Y-phase Relay Was OOS ML18067A4391997-03-21021 March 1997 LER 97-005-00:on 961220,operation of Plant Outside Design Basis Occurred Due to an Unacceptable Repair on Main Steam Isolation Valves.Pipe Plugs Permanently Repaired ML18067A4401997-03-21021 March 1997 LER 97-003-00:on 961101,four Piping Lines Were Determined to Be Potentially Susceptible to Pressurization Due to Containment Temperature Increase During an Accident.Cac Discharge Piping Will Be verified.W/970321 Ltr ML18066A8931997-02-21021 February 1997 LER 97-002-00:on 970123,failure to Meet TSs 4.5.2d(1)(b) for Testing of Emergency Escape Airlock Occurred.Caused by Missed Surveillance.Emergency Escape Air Lock Testing Was Completed & Declared operable.W/970221 Ltr ML18066A8751997-02-0505 February 1997 LER 97-001-00:on 970106,TAVE Temp Dropped Below Minimum Temp for Criticality.Caused by Control Rod Withdrawal Rate to Increase Power Not Sufficient to Match Increase in Steam. Turbine Bypass Valve Actuator repaired.W/970205 Ltr ML18066A8041996-12-23023 December 1996 LER 96-014-00:on 961124,class 1E Raychem Cable Splices Were Installed Incorrectly.Caused by Incorrectly Made Electrical Splices.Total of 270 Splices Have Been Replaced within Containment ML18066A7831996-12-16016 December 1996 LER 96-013-00:on 961115,DC Breaker Failure During Testing for as-found Trip Setting Occurred.Cause Under Investigation.All molded-case Circuit Breakers in DC Distribution Panels Were Replaced ML18065A9951996-10-0404 October 1996 LER 96-002-01:on 960116,initiated TS Required Shutdown Due to Safeguards Cable Fault.Both Sets (Six Cables) of Cables Were Replaced & Installed Through Turbine Generator Bldg ML18065A9171996-09-0909 September 1996 LER 95-012-00:on 960809,TS Violation Occurred,Due to No Senior Reactor Operator in Cr.Caused by Extensive Remodeling.Cr Remodeling completed.W/960909 Ltr ML18065A8961996-08-29029 August 1996 LER 96-011-00:on 960730,CR Continuous Air Monitor Alarm Setpoint Improperly Established.Caused by Failure to Utilize Mod Process in 1988 Leading to Failure to Properly Select & Calibrate Instruments ML18065A8811996-08-20020 August 1996 LER 96-005-01:on 960207,determined Fuse on Main Supply to Two Safety Related DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Lack of Thorough Associated Circuits Analysis.Supply Fuse to Panels Replaced ML18065A8741996-08-16016 August 1996 LER 96-010-00:on 960717,high Pressure Safety Injection Pump Tripped While Filling Safety Injection Tank.Caused by Faulty 150/151Y-207 Time Overcurrent Relay.All Similar Relays in Time Overcurrent Application Have Been Inspected ML18065A8651996-08-12012 August 1996 LER 96-009-00:on 960712,identified Penetration Seal Deficiency on Fire Barriers Caused by Failure to Perform & Document Comprehensive Fire Barrier Evaluation.Developed Basis document.W/960812 Ltr ML18065A8601996-08-0202 August 1996 LER 96-006-01 on 960207,discovered Limits of Design Analysis Could Have Been Violated.Subsequent Tests & Analyses Facility Did Not Exceed Basis.Operating Procedures Have Been Revised to Treat 2530 Megawatts Limit as Absolute Limit ML18065A8321996-08-0101 August 1996 LER 96-003-01:on 960115,alternate Shutdown Panel Inverter Resulted in Unavailability of Panel.Replaced Defective Inverter Alarm Logic Board ML18065A7691996-06-12012 June 1996 LER 96-008-00:on 960513,fire Door Not Maintained Open in Accordance W/Design Basis.Cause Under Investigation. Engineering Evaluation Performed & Revised Documents, Surveillance & Test procedures.W/960612 Ltr ML18065A6901996-05-0101 May 1996 LER 95-001-01:on 950302,malfunction of Left Channel DBA Sequencer Resulted in Inadvertent Actuation of Left Channel Safeguards Equipment.Replaced microprocessor.W/960501 Ltr ML18065A6681996-04-22022 April 1996 LER 96-007-00:on 960321,inadequate Emergency Lighting & Ventilation in post-fire Safe Shutdown Areas.Caused by App R Program Documentation Insufficient to Demonstrate Regulatory Compliance.Lighting modified.W/960422 Ltr ML18065A5721996-03-11011 March 1996 LER 96-006-00:on 960207,average Reactor Power Level Exceeded License Limit Due to Insufficient Procedural Guidance. GOP-12 Revised to Treat 2,530 Mwt Limit as Absolute Limit Requiring Immediate Corrective Action If Exceeded ML18065A5261996-03-0101 March 1996 LER 96-005-00:on 960202,fuse on Main Supply to Two SR DC Panels & Panel Branch Circuit Breakers Not Properly Coordinated.Caused by Inadequate Electrical/App R Design Review.Implemented Hourly Fire tours.W/960301 Ltr ML18065A5111996-02-19019 February 1996 LER 94-012-02:on 940427,determined That Internal Ground in Thermal Margin Monitor Causes Nonconformance W/Rps Design Basis.Incorporated RPS Failure Modes & Effects Analysis in Plant DBD.W/960219 Ltr ML18065A5061996-02-19019 February 1996 LER 96-004-00:on 960118,SIS Disabled W/Primary Coolant Sys Greater than 300 F.Caused by Personnel Error.Permanent Maint Procedure to Disable/Enable SIS Actuation on Low Pressurizer Pressure Will Be Revised to Align W/Ts ML18065A5021996-02-15015 February 1996 LER 96-003-00:on 960115,technicians Found Low Voltage cut- Off for Alternate Shutdown Panel Inverter Set That Resulted in Unavailability of Panel.Caused by Inadequate Post Mod. Readjusted Set Point to Minimum setting.W/960215 Ltr ML18065A4581996-01-31031 January 1996 LER 96-001-00:on 960103,failed to Test Duplicate Equipment. Caused by STS No Longer Containing Requirement for cross- Train Testing of Duplicate Components.Will Submit Request to Delete Subj Requirements from TS.W/960131 Ltr ML18065A4421996-01-19019 January 1996 LER 95-016-00:on 951226,did Not Analyze Primary Coolant Samples within 72 H.Caused by Belief Acceptability to Save Pcs Samples for Choride Analysis Past 72 H.Counseled Chemistry Supervision.W/960119 Ltr ML18065A4041996-01-15015 January 1996 LER 95-014-00:on 950119,PCP Oil Collection Deficiencies Created by FC-860 Piping Mod.Caused by Inadequate DBD for Sys & Lack of Review by Experienced Fire Protection Personnel.Updated Design Basis documentation.W/960115 Ltr ML18065A3291995-12-0404 December 1995 LER 95-013-00:on 951103,circuit Fuse Coordination Deficiency Which Affects App R Safe Shutdown Equipment Noted.Design of Fuse Coordination in Potential Transformer Circuits Will Be Evaluated & Modified as required.W/951204 Ltr ML18065A2361995-11-0202 November 1995 LER 95-012-00:on 950701,discovered Unqualified Electrical Connection in Containment SW Outlet Valve Controller.Caused by Failure of Assigned Engineers to Available Info.Replaced Wire Nuts W/Inline Butt connections.W/951102 Ltr ML18065A2051995-10-20020 October 1995 LER 95-008-01:on 950728,discovered That None of Four Containment High Pressure Channels Would Initiate Reactor Trip Due to Programmatic Deficiencies.Administrative Procedure (AP) 9.44,AP 9.45 & AP 10.44 Will Be Revised ML18065A0841995-09-18018 September 1995 LER 95-011-00:on 950817,CR 40 Withdrawal Occurred When Given Insertion Signal Due to skill-based Error in Crimping & Removing Foreign Matl from CRDM Motor Connection Box.Crd Package replaced.W/950918 Ltr ML18065A0681995-09-14014 September 1995 LER 95-010-00:on 950815,ESFA Resulted in Manual Rt Following Isolation of Pcs.Replaced Failed Instrument Line ML18065A0651995-09-0808 September 1995 LER 95-009-00:on 950728,discovered Lack of Procedural Guidance for Pump Repair Following Fire.Proposed Use of Power Supply Breaker Did Not Adequately Address Effect of Loss of Control Power.Performed Independent Assessment ML18064A8781995-08-28028 August 1995 LER 95-008-00:on 950728,discovered During Design Change Testing That None of Four Containment High Pressure Channels Would Initiate Rt.Caused by Programmatic Deficiencies. Reviewed Selected Tests & Mods from Recent Refueling Outage ML18064A8831995-08-21021 August 1995 LER 95-007-00:on 950720,discovered That 12 Instrument Loops Had V-bolted Type Qualified Cable Splices Connected to Wires W/Exposed Kapton Insulation.Caused by Human Error.All V- Bolted Splices Replaced w/in-line design.W/950821 Ltr 1999-09-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18066A6901999-11-0101 November 1999 Rev 5 to Palisades Nuclear Plant Colr. ML18066A6761999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Palisades Nuclear Plant ML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6351999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Palisades Nuclear Plant ML18066A6771999-08-31031 August 1999 Operating Data Rept Page of MOR for Aug 1999 for Palisades Nuclear Plant ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A6061999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Palisades Nuclear Plant.With 990803 Ltr ML18066A5201999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Palisades Nuclear Plant.With 990702 Ltr ML18066A4841999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Palisades Nuclear Plant.With 990603 Ltr ML18066A6371999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant ML18068A5941999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant.With 990503 Ltr ML18066A4161999-04-0101 April 1999 Rev 4 to COLR, for Palisades Nuclear Plant ML18066A4501999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Palisades Nuclear Plant.With 990402 Ltr ML18066A4671999-03-31031 March 1999 Rev 0 to SIR-99-032, Flaw Tolerance & Leakage Evaluation Spent Fuel Pool Heat Exchanger E-53B Nozzle Palisades Nuclear Plant. ML18068A5351999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Palisades Nuclear Plant.With 990302 Ltr ML18066A3931999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Palisades Nuclear Plant.With 990202 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML20206F6131998-12-31031 December 1998 1998 Consumers Energy Co Annual Rept. with ML18066A3651998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Palisades Nuclear Plant.With 990105 Ltr ML18066A3421998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Palisades Nuclear Plant.With 981202 Ltr ML18066A3301998-11-11011 November 1998 Part 21 Rept Re Potential Safety Hazard Associated with Wrist Pin Assemblies for FM-Alco 251 Engines at Palisades Nuclear Power Plant.Caused by Insufficient Friction Fit Between Pin & Sleeve.Supplier of Pin Will No Longer Be Used ML18068A4921998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Palisades Nuclear Plant.With 981103 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A3181998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Palisades Nuclear Plant ML18066A2901998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Palisades Nuclear Power Plant.With 980903 Ltr ML18066A3191998-08-31031 August 1998 Revised Monthly Operating Rept Data for Aug 1998 for Palisades Nuclear Plant ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237E0301998-07-31031 July 1998 ISI Rept 3-3 ML18066A2701998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Palisades Nuclear Plant.W/980803 Ltr ML18066A2311998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Palisades Nuclear Plant ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A3061998-06-18018 June 1998 SG Tube Inservice Insp. ML20249C4951998-06-17017 June 1998 Rev 1 to EA-GEJ-98-01, Palisades Cycle 14 Disposition of Events Review ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18066A1711998-06-0101 June 1998 Part 21 Rept Re Impact of RELAP4 Excessive Variability on Palisades Large Break LOCA ECCS Results.Change in PCT Between Cycle 13 & Cycle 14 Does Not Constitute Significant Change Per 10CFR50.46 ML18066A1741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Palisades Nuclear Plant.W/980601 Ltr ML18066A2321998-05-31031 May 1998 Revised MOR for May 1998 for Palisades Nuclear Plant ML18068A4701998-05-31031 May 1998 Annual Rept of Changes in ECCS Models Per 10CFR50.46. ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18066A2331998-04-30030 April 1998 Revised MOR for Apr 1998 for Palisades Nuclear Plant ML18068A3461998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Palisades Nuclear Plant.W/980501 Ltr ML18066A3411998-04-22022 April 1998 Rev 0 to EMF-98-013, Palisades Cycle 14:Disposition & Analysis of SRP Chapter 15 Events. ML18065B2071998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Palisades Nuclear Plant.W/980403 Ltr ML20217C2741998-03-31031 March 1998 Independent Review - Is Consumers Energy Method (W Method) of Determining Palisades Nuclear Plant Best Estimate Fluence by Combining Transport Calculation & Dosimetry Measurements Technically Sound & Does It Meet Intent of Pts ML18066A2341998-03-31031 March 1998 Revised MOR for Mar 1998 for Palisades Nuclear Plant ML18068A3041998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Palisades Nuclear Plant.W/980302 Ltr ML18066A2351998-02-28028 February 1998 Revised MOR for Feb 1998 for Palisades Nuclear Plant ML18065B1641998-02-0505 February 1998 Rev 0 to Regression Analysis for Containment Prestressing Sys at 25th Year Surveillance. ML18067A8211998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Palisades Nuclear Plant.W/980203 Ltr 1999-09-30
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- consumers Power POWERIN& MICHl&AN'S PRD&RESS Palisades Nuclear Plant: 27780 Blue Star Memorial Highway, Coven, Ml 49043 October 15, 1993 Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
- GB Slade General Manager DOCKET 50-255 -LICENSE DPR-20 -PALISADES PLANT -LICENSEE EVENT REPORT 93-009, PRESSURIZER PENETRATION SAFE END CRACK RESULTS IN PCS LEAKAGE Litensee Event Report (LER) is attached.
This is reportable in accordance with 10 CFR 50.73(a)(2)(ii).
Gerald B Slade General Manager CC Administrator, Region Ill, USNRC NRC Resident Inspector
-Palisades Attachment 9310220185 931015. -r:*** PDR ADOCK 05000255 f.. S . PDR * !!,. r A CMS ENERGY COMPAN)'°
- APPROVED OMB NO. 3160-0104 EXPIRES: 9/31196 LICENSEE EVENT REPORT (LERI FACILITY NAME 111 DOCKET NUMBER 121 PAGE 131 Palisades Plant 01s101010121s1s 1 I OF 01 5 TITLE 141 PRESSURIZER PENETRATION SAFE END CRACK RESULTS IN PCS LEAKAGE I EVENT DATE 161 LER NUMBER 161 REPORT DATE 161 OTHER FACILITIES INVOLVED !Bl SEQUENTIAL REVISION FACILITY NAMES MONTH DAY YEAR YEAR NUMBER NUMBER MONTH* DAY YEAR N/A 0161010101 I --01 9 i I 9 9 3 3 01 o I 9 o I o 11 0 i I s 3 N/A 0161010101 I THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR I: !Ch.ck OM or more of tM following/
1111 OPERATING N MOOE 191 20.4021bl 20.4061cl 60.731a)(211iv) 73.71 (bl *---POWER I 20.406(*111
)(ii 60.36icll1 I 60. 7 3(a)(21M 73.71 lei LEVEL I I o --I---1101 20.4061al11 l(iil 60.36(c)(21
- 60. 73(al12)(vii)
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- 60. 7 3 (a)(2) (viii) IA) below end in Text, ---* 20 .406la)(1
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- 60. 7 31all211viiillBI NRC Form 366Ai --20.4061all1 IM 60.731all211iiil
- 60. 7 31all211xl LICENSEE CONTACT FOR THIS LER 112) NAME TELEPHONE NUMBER William L. Roberts, Staff Licensing Engin_eer 1 7 1 6 1 4 1 -I a I s I , I 3 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 MAN.UFA.C*
REPORTABLE MANUFAC* REPORTABLE CAUSE SYSTEM COMPONENT TUR ER TO NPROS . CAUSE SYSTEM COMPONENT TUR ER TO NPROS I I I I I I I I I I I I I I I I I I I I I I I I I I I i SUPPLEMENTAL REP.ORT EXPECTED 1141 MONTH DAY YEAR I EXPECTED I l YES Vf yes, complere EXPECTED_
SUBMISSION DATE! lxl NO SUBMISSION I I I DATE 1161 ABSTRACT {Limit to 1400 spaces. i.e .* *pproximat*iv fiftHl'I ling/trsp<<*
typewrimm lin!al 11 si On September 19, 1993, at approximately 1900 hours0.022 days <br />0.528 hours <br />0.00314 weeks <br />7.2295e-4 months <br />, the plant was in the process of heating up following a refueling outage. The plant's primary coolant system (PCS) was in a hot shutdown condition (532°F and 2060 psia) when plant operations personnel identified a ieak in the power operated relief valve (PORV) line near the nozzle connection to the pressurizer.
The plant was returned to cold shutdown.
The crack tnitiated due primary water stress corrosion cracking (PWSCC) in the heat affected zone (HAZ) of the power operated relief valve (PORV) Inconel 600 safe end. Corrective actions include removing a portion of the safe end containing the crack for evaluation, examining the remaining safe end to.establish its condition for future use, rewelding the PORV pipe to the examined safe end to replace the piping that was removed, and examining and evaluating the remaining pressurizer nozzles and other primary coolant system nozzles to provide assurance of operability prior to returning the plant to service. I \
><RC F"'m 388A U.S. NUCLEAA llEGUL-" TORY COM ... ISSICI< AP9'10VEO OMB NO: 3 160-01 C* EXPIRES: 8131.'86 19-831 FACILITY NAME 11 I LICENSEE EVENT REPORT !LERI TEXT CONTINl)ATION OOCl(ET NUMBER 121 LEll NUMBER 131 SEQUENTIAi.
YEAA NUMBER REVISION NUMBER Palisades Plant Q 5 . Q Q Q 2 5 5 9 3 -
Q
- Q 9 -Q Q Q 2 OF Q 5 EVENT DESCRIPTION On September 19, 1993, at approximately 1900 hours0.022 days <br />0.528 hours <br />0.00314 weeks <br />7.2295e-4 months <br />, the plant was in the process of heating up following a refueling outage. The plant's primary coolant system (PCS) was in a hot shutdown condition (532°F and 2060 psia) when plant operations personnel . identified an increasing trend in containment sump level indication, indicating a leak in the PCS. A few minutes later, an auxiliary operator conducting rounds in the containment reported a steam leak near the pressurizer.
Closer inspection found an isolatable leak in the power operated relief valve (PORV) line near the pressurizer relief valve nozzle. The plant was returned to cold shutdown.
While cooling down, a second visual examination of the leak was performed with primary system pressure about 200 psig. This visual inspection characterized the leak to be a partial circumferencial crack, in or very near to/the Inconel 600 safe-end on the pressurizer On September 17, 1993 the plant achieved cold shutdown and direct visual and NOE examination of the crack area was performed.
The leak area found the circumferencial crack to be approximately 3-inches in length (about 30 percent of the circumference) in the Inconel safe-end to pipe weld. Review of containment sump level information during the event indicates the steam leak was on the order of 0.2 gpm equivalent water. -This event is reportable in accordance with 10 CFR 50.73(a)(2)(ii) as an event that resulted in one of the nuclear power plants principal safety barriers being seriously degraded.
CAUSE OF THE EVENT The crack initiated due to primary water stress corrosion cracking (PWSCC) in the heat affected zone (HAZ) of the PORV line to pressurizer nozzle safe end weld. The cracking mode was intergranular from the inside diameter pipe surface with the final 5 to 10% of crack growth being transgranualar.
- During the inservice inspection of th1s weld earlier this refueling outage, the cap on this weld was ground down to facilitate resolution during volumetric NOE of a recordable indication.
The earlier presence of the weld cap may be why the crack did not open up sooner. ANALYSIS OF THE EVENT At the time of the event the was in the process of heating up from a refueling outage. Plant conditions were such that the PCS was nearly at temperature and pressure and all associated safeguards equipment supporting this stage of plant operation was operable.
The was returned to a cold shutdown condition.
Transition to cold shutdown required no abnormal operations or any safeguards equipment performing a design basis function.
- 'l l<RC FOfm 388A 19*831 Palisades Plant LICENSEE EVENT REPORT (LERI TEXT CONTINUATION DOCKET NUMBER 121 YE.AA LER NUMBEI'\ Ill
- SEQUENTIAL NUMBER U.S. NUCLE.AA qEGULl<TORY APP'IOVEO OMB 1<0. 3'60-0'C4 EXP!RES: 1131/86 RE'\llSlON NUMBER 0 5 0 0 0 2 5 5 9 3 -
0 0 9 -0 0 0 3 o* 0 5 Analysis is ongoing to determine the margin-to-failure for the cracked PORV nozzle safe-end.
This analysis will provide the conclusion for the severity of the crack growth. SAFETY SIGNIFICANCE These three scenarios are hypothesized to judge the possible safety 6f
- event had it occurred while the plant was at power operation.
- 1. A leak of the same size as was experienced during this event could have resulted.
The Technical Specifications leakage limit of 1 gpm unidentified leakage may have been approached or exceeded and a normal shutdown would occur. 2. A leak could have started small and gradually progressed in size over time. As the leak increased in size monitoring the increasing leakage into the containment sump would have allowed us to take actions to shut the plant down. Exceeding 1 gpm leakage unidentified would require plant shutdotwn.
- 3. The cracking could have been initially more severe such that a much larger leak developed.
In the case of the PORV piping, the limiting size of the leak is the cross sectional area of the pressurizer relief valve nozzle. Analysis has been completed for small break LOCAs for up to a one square foot break size * (CENPD-137 Supplement 1-P, "Small Break Model Calculative Methods for the CE Small Break LOCA Evaluation Model," January 1977). Since the PORV nozzle is a three inch nozzle, the area available to leak would be 0.05 square feet. Analysis indicates that the maximum fuel cladding temperature predicted for a small break LOCA of this size is 660°F. The maximum thickness of cladding oxidation is predicted to be 0.002% of the cladding wall thickness.
These values are much less than the 10 CFR 50.46 acceptance criteria of a peak cladding temperature of 2200°F and maximum cladding oxidation of 17%. These analysis are also predicted based on assuming the breaks are located on the bottom of the PCS cold legs. Breaks on the top of the pressurizer are much less limiting due to a predicted lower mass ejection rate. CORRECTIVE ACTION The specific actions that have been or are being taken to address the pressurizer relief valve nozzle safe end crack are summarized below. Initial results of the action plan investigations were reported to the NRC in a dated October .7, 1993. Specific plan actiqns are listed below and have been divided into short term and long term actions. Short term actions will be completed prior to start up from the present refueling outage.
F"'m J99A U.S. NUCLEAA 'IEGUL.UORY APl'llOVED OMS 1<0. J' 60-C' C* . E)(P,RES:
Bil 1 .116 19*8JI LICENSEE EVENT REPORT (LERI TEXT CONTINUATION FACILITY NAME 111 OOCltEi NUMBER 121 LER NUMBER 131 PAGE 141 SEQUENTIAi.
YEAA NUMBER REVISION NUMBER Palisades Plant O 5 0 O 0 2 5 5 9 3 -
0 0 9 -0 0 0 4 o* 0 5 or erm 1. An engineering evaluation of the failure has been conducted.
The specific elements of this engineering analysis included the following:
- a. Metallurgical analysis of the failed safe end to identify the cause of the crack. b. Analysis of factors contributing to PWSCC in the pressurizer nozzle safe end. This includes evaluation of material properties and stresses that may have contributed to the failure. Piping stresses and weld residual stresses are being evaluated and will be reviewed by an independent third party. . c. Evaluation of other nozzles safe ends in the primary coolant system, based on the engineering evaluation of the failure, to identify other locations which may be susceptible to the same failure cause. This evaluation includes both nozzles with Inconel 600 safe ends and other safe end materials.
Contributing factors to PWSCC will also be evaluated for the safe ends that are identified as being susceptible to the same failure cause .. This will include evaluation of material properties and stresses.
- d. Evaluation of appropriate non-destructive examination techniques to identify similar flaws in other susceptible safe ends. 2. Corrective actions for the specific safe end that failed have been identified.
An engineering evaluation of the repair to the pressurizer safe based* on the root cause analysis of the failure, has shown that the lifetime of the repaired safe end well exceeds the length of the next operating cycle.
- 3. Corrective actions for other safe ends that may be susceptible to the same failure have peen identified.
Other safe ends that may be susceptible to the same failure have been inspected for flaws using appropriate non-destructive examination techniques.
- 4. Necessary corrective actions to ensure safe operation of Palisades during the next . operating cycle prior to returning the plant to service will be completed.
- a. Repair of the failed pressurizer safe end. b. Non-destructive examinations of other safe ends potentially susceptible to the same failure cause. Results of the short term corrective actions were transmitted to the NRC in a report dated October 7, 1993.
- RC FOfm JeeA f9-8JI . FACILITY NAME 11 I LICENSEE EVENT REPORT !LERI TEXT CONTINUATION OOCIC:E"T NUMBER 121 LER NUMBEl'I 131 SEQUENTIAL.
YEAR NUMBER u:s. NUClEAA REGUUITORY C0"'"5SlC><
APl"IOVEO OMB '<0. J'60-01C*
EXPIRES: 8/31 i86 RE'\11SION NUMBER PAGE 141 Pal.isades Plant 0500025593 -oo 9 -0 0 0 5 o* O 5 Long Term 5. Corrective actions necessary to ensure long term safe operation of Palisades will be identified.
- a. Engineering of additional repairs which may be necessary for long term operation of the pressurizer safe ends will be performed and additional . repairs and
- actions, if required, will be by the end of the next refueling shutdown.
-* -* b. Further evaluation of non-destructive examination techniques in light of the pressurizer safe end crack will be coriducted.
Enhanced ultrasonic techniques will be. emplbyed in an augmented ,inspection program* for safe ends beginning in next refueling shutdown.
- The NRC has requested additional information on the subject in two letters dated October 7, 1993. Additional information concerning this occurrence and our follow-up actions will be contained in follow-up correspondence to the NRC. ADDITIONAL INFORMATION
- Consumers Company submitted to the NRC information concerning this event in. letters dated September 29, 1993, October 1, 1993, October 4, 1993, and October 7, 1993. NRC correspondence on this issue included a Confirmatory Action Letter dated October l,* 1993 and two requests for additional information concerning the safe .end crack dated. October 8, 1993. '