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| issue date = 04/06/1977
| issue date = 04/06/1977
| title = LER 77-017-00 for Saint Lucie Unit 1 Regarding Dropped or Misaligned CEA 20 and CEA 23
| title = LER 77-017-00 for Saint Lucie Unit 1 Regarding Dropped or Misaligned CEA 20 and CEA 23
| author name = Schmidt A D
| author name = Schmidt A
| author affiliation = Florida Power & Light Co
| author affiliation = Florida Power & Light Co
| addressee name = Moseley N C
| addressee name = Moseley N
| addressee affiliation = NRC/RGN-II
| addressee affiliation = NRC/RGN-II
| docket = 05000335
| docket = 05000335
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:NRC FoAM 196 U.S.NUCLEAR AEGUL*TOA V COMMISSION DOCKET NUMOE A I2.70)'BC DISTRIBUTION FoR f,.T 50 DOCKET MATERIAL FILE NUMOEA INCIDENT REPORT TO:~~Mr.Norman C.Moseley FROM;Florida Power&Light Companyt Miami, Florida A.D.Schmidt DATE OF DOCUMENT 4/6/77 DATE RECEIVED 4 21 77 QLETTEA Q OA IG INAL Qcopv DESCRIPTION
{{#Wiki_filter:NRC FoAM 196                                           U.S. NUCLEAR AEGUL*TOAV COMMISSION       DOCKET NUMOE A I2.70)
\Q NOTOR IZE D QUNCLASSIFIED INPUT FOAM ENCLOSURE NUMBER OF COPIES RECEIVED I at~8~I Ltre trans the following:
                  'BC DISTRIBUTION FoR f,.       T 50 DOCKET MATERIAL FILE NUMOEA INCIDENT REPORT TO:         ~                                 FROM;                                            DATE OF DOCUMENT
, (Ig((5, PLANT NAME:~vG,$t,.Lncie Uni.t Nc.1 QgQ gJL I (1-P)Licensee Event Report (RO 50-335/77-17) on 3/7/77 concerning CEA 20 not withdrawing'ecause the Upper Electrical
          ~
'Limit reed switch had failed closed, thus prohibiting
Florida  Power &  Light  Companyt                                          4/6/77 Mr. Norman C. Moseley                   Miami, Florida                                 DATE RECEIVED A. D. Schmidt                                                                 4 21 77 QLETTEA                   Q NOTOR IZE D                               INPUT FOAM               NUMBER OF COPIES RECEIVED Q OA IG INAL Qcopv DESCRIPTION QUNCLASSIFIED ENCLOSURE I at~8~
('outward CEA.mo ti one~~~(RO 50-335/76-46) on 3/11/77 concernirig the containment escape lock inner door failing e tech spec surveillance
\
~~.~-.(4-p).,'OTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS BRANCH CHIEF: W 3 CYS FOR ACTION LICo ASST,:>I CXS ACRS (CXS 149b&%HC S NT FOR ACTION/I NFO RiVIAT ION G FILE INTERNAL D IST RI OUT ON I&E(2 MIPC SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIIKS CASE HANAUER TEDESCO/FIACCARY EISENHUT SHAO VOLLMER/BUNCH KREGER/J~COLLINS LPDR:~1e ee.TIC: N~C.EXTERNAL DISTRIOUTION CONTROL NUMOER 7>ll 4 0/94 NRC FOAM 196{2 70) 0~4~4 tt P.O.BOX 013100, MIAMI, FL 33101 Qlyyz FLORIDA POWER&LIGHT COMPANY April 6, 1977 Mr.Norman C.Moseley, Director, Region II Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 1217 Atlanta, Georgia 30303
I   Ltre trans the following:                                   Licensee Event Report (RO 50-335/77-17) on 3/7/77 concerning CEA 20 not the Upper Electrical 'Limit reed withdrawing'ecause switch had failed       closed, thus prohibiting
                                    , (Ig((5,                                            ti
('
outward CEA .mo one ~ ~ ~
(RO 50-335/76-46) on 3/11/77 concernirig the containment escape lock inner door failing
                                                                                                          ~ -.
e PLANT NAME:                    ~
vG,                      tech spec surveillance         ~ ~ .
    $  t,. Lncie Uni.t Nc. 1 QgQ gJL                                                  (1-P)      (4-p)   .,
I                            IF 'OTE:
PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS FOR ACTION/INFO RiVIATION BRANCH CHIEF:
W 3 CYS FOR ACTION LICo ASST,:
        >I       CXS ACRS       (   CXS 149b&%HC S NT INTERNAL D IST RI OUT ON G  FILE I&E(2 MIPC SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIIKS CASE HANAUER TEDESCO/FIACCARY EISENHUT SHAO VOLLMER/BUNCH KREGER/J     ~ COLLINS EXTERNAL DISTRIOUTION                                                CONTROL NUMOER LPDR:
TIC:
                  ~     1e ee.                                                                         7>ll 4 0/94 N~C.
NRC FOAM 196 {2 70)


==Dear Mr.Moseley:==
0
.PRN-LI-77-99 Aegulatory EQLCfg q REPORTABLE OCCURRENCE 335-77-17~cj~ST.LUCIE UNIT 1 DATE OF OCCURRENCE:
~ 4 ~ 4 tt
MARCH 7, 1977 CEA 20 6 CEA 23 The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.
 
Very truly yours, D.Schmidt Vice President Power Resources'e MAS/ms Attachment CC Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement (30)Director, Office of Management Information and Program Control (3)r7 jld"b/8 9 PEOPLE...SERVING PEOPLE 1'QI IE ,~  
P. O. BOX 013100, MIAMI, FL 33101 Qlyyz FLORIDA POWER & LIGHT COMPANY April      6, 1977
~CONTROL BLOCK: LICENSEE EVENT REPORT fPL~SE PRiNT ALL RECIUIRED INFOAMAT!ON)
                                                    . PRN-LI-77-99 Aegulatory           EQLCfg q
LCENSEE BYNAME F L S L S 1 0 0 7 89 14 15 REPORT REPORT CATEGORY TYPE SOURCE I001I coN'T~~L~L 0 7 8 57 58 59 60 61 LICENSE NUMBER 0 0 0 0 0-0 0 UCENSE TYPE EVENT TYPE 411 1 1 I z~03 25 26 30 OOCKET NUMBER EVENT OATE REPORT OATE 5 0-0 3 3 5 0 3 0 7 7 7 0 3 1 5 7 7 68 69 74 75 60 EVENT DESCRIPTION QO 2 Durin surveillance testin , CEA 20 would not withdraw with the rest of Group 2, so 7 89 80[QQ4]Shutdown margin was veri f ied, power was reduced to 70 percent, and while the rest of 7 8 9 80 Qp 5 the group was being aligned to CEA 20, CEA 23 dropped.CEA 23 was recovered in 34 60 The o erabilit 7 8 9 QOQ minu tes thereb sa t is f in ac tion a m I I I I f 7 8 9 BO I action was taken in accordance with action statement"d" of Specification 3.1.3.1.89 SYSTEM CAUSE COOE COOE COtiIPONENT COOE~0>~RB~B 0 K T B R K 7 8 9 10 11 12 17 CAUSE DESCRIPTION tOOBj CEA 20 would not withdraw because PAVE COMPO I I ENT SUPPLER COMPO BJ ENT MANUF~i'FER C 4 9 0 N 47 48 the Upper Electrical Limit (UEL)reed switch had 80 7 8 9 80 Q~I failed closed, thus prohibiting outward CEA motion.The failed reed switch was taken 7 8 9 60 of the circuit and the s are UEL reed switches were verified to be in service.OTHER STATUS NA 7 8 9 LOSS OR DAMAGE TO FACILITY TYPE OESCRIPTION l91 LzJ 7 89 10 PUBLICITY 7 89 7 89 , FACILIIY STATUS'%OWER@~~]~B~OB 0 7 8 9 10 12 13 FORM OF AcnVITY COATENT RELEASED OF RELEASE AMOUNT OF ACnVITY KIH NA 7 8 9 10 11 PERSONNEL EXPOSURES NUMSER TYPE OESCRIPTION
Mr. Norman C. Moseley, Director, Region    II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 1217 Atlanta, Georgia    30303
~io~oo o'~z 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER CESCRIPTIOtJ PP+0 0 7 8 9 11 12 PROBABLE CONSEQUENCES Qg METHOO OF OISCOVERY 44 45 44 45 NA NA NA NA 80 OISCOVERY OESCRIPTION NA cO LOCATION OF RELEASE NA 60 80 ao 80 60.BO ADDITIONAL FACTORS Qg See a e two for continuation of Event Description and Cause Description.
 
7 89 7 89 M: A.Scho man PHONEI 305 552-3802 COO 65 I~II 0T 4~V~M ,'7i Reportable Occurrence 335-77-17 Licensee Event Report Pa e Two Event Descri tion (continued) of CEA 20 was then restored and power was increased to 100 percent.CEA 20 had been declared inoperable for 43.minutes.This was the fourth occurrence of dropped or misaligned CEA's (335-76-25, 335-76-37, and 335-77-6)but was unrelated to the previous occurrences.
==Dear Mr. Moseley:==
 
REPORTABLE OCCURRENCE 335-77-17     ~cj~
ST. LUCIE UNIT 1 DATE OF OCCURRENCE:   MARCH 7, 1977 CEA 20 6 CEA 23 The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.
Very truly yours, D. Schmidt Vice President e
Power Resources MAS/ms Attachment CC   Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement             (30)
Director, Office of Management Information and Program Control (3) r7 jld"b/89 PEOPLE... SERVING PEOPLE
 
1' QI IE
        , ~
 
LICENSEE EVENT REPORT
                    ~     CONTROL BLOCK:                                                                         fPL~SE PRiNT ALL RECIUIRED INFOAMAT!ON)
BYNAME LCENSEE                                                                                         UCENSE                EVENT LICENSE NUMBER                                        TYPE                  TYPE F   L   S   L   S     1         0   0         0   0   0   0     0   0           0         411     1     1   I z     ~03
                    ~
7    89                              14      15                                                      25       26                     30 REPORT    REPORT CATEGORY      TYPE    SOURCE                  OOCKET NUMBER                                 EVENT OATE                     REPORT OATE I001I coN'T                    ~L        ~L          0    5   0   0         3   3     5         0   3     0 7   7     7       0   3   1   5     7     7 7    8          57      58      59        60      61                                    68     69                           74     75                           60 I
EVENT DESCRIPTION QO 2     Durin surveillance testin                       , CEA 20       would not withdraw with the                       rest of       Group 2, so 7     8 9                                                                                                                                                              BO action        was taken        in    accordance        with action statement "d" of Specification 3.1.3.1.
7    89                                                                                                                                                               80
[QQ4]     Shutdown margin was                 veri fied,       power was reduced to 70 percent,                         and     while the rest of 7     8 9                                                                                                                                                               80 Qp 5       the group was being               aligned to         CEA   20,   CEA 23       dropped.           CEA 23 was         recovered     in   34 7 8 9                                                                                                                                                                   60 QOQ       minu tes thereb sa                 t is f in       ac tion       a   m II  II f                                         The o    erabilit 89                                                                     PAVE                                                                                      80 SYSTEM COOE CAUSE COOE             COtiIPONENT COOE COMPO IIENT SUPPLER COMPO BJ ENT MANUF~i'FER
  ~0>     ~RB             ~B           0     K   T   B     R   K                             C      4    9    0            N 7 8 9 10                   11       12                             17                                               47        48 CAUSE DESCRIPTION tOOBj     CEA 20       would not withdraw because                     the Upper Electrical Limit (UEL) reed switch had 7     8 9 7
Q~ I8 9 failed closed, thus prohibiting outward                               CEA   motion.           The     failed reed switch           was taken 80 60 of the circuit           and   the   s   are   UEL   reed switches were                 verified to         be   in service.
7     89       FACILIIY 80
            ,                                                                       METHOO OF STATUS           '%OWER                     OTHER STATUS            OISCOVERY                            OISCOVERY OESCRIPTION
@~~
7
      ]8        9
                ~B             ~OB         0                     NA                                                                NA 10             12   13                             44      45                                                                            cO FORM OF AcnVITY       COATENT RELEASED     OF RELEASE           AMOUNT OF ACnVITY                                                       LOCATION OF RELEASE KIH                                                     NA                                                                        NA 7     8       9               10     11                                       44        45                                                                          60 PERSONNEL EXPOSURES NUMSER         TYPE     OESCRIPTION
~io       ~oo           o   '~z 7     8 9                 11     12     13                                                                                                                               80 PERSONNEL INJURIES NUMBER           CESCRIPTIOtJ PP+               0     0                                                                           NA 7     8 9                 11   12                                                                                                                                       ao PROBABLE CONSEQUENCES Qg8                                                                                                  NA 7        9                                                                                                                                                            80 LOSS OR DAMAGE TO FACILITY TYPE        OESCRIPTION l91 LzJ 7 89 NA 10                                                                                                                                                  60 PUBLICITY NA 7    89                                                                                                                                                              .BO ADDITIONAL FACTORS Qg           See       a e two       for continuation of               Event Description and Cause Description.
7     89 7     89 M: A. Scho           man                                                             305 552-3802 PHONEI COO   65 I ~ II 0T
 
4 ~
V
~ M
,'7i
 
Reportable Occurrence 335-77-17 Licensee Event Report Pa e Two Event Descri   tion (continued) of CEA 20 was then restored and power was increased to 100 percent.
CEA 20 had been declared inoperable for 43. minutes. This was the fourth occurrence of dropped or misaligned CEA's (335-76-25, 335-76-37, and 335-77-6) but was unrelated to the previous occurrences.
(335-77-17)
(335-77-17)
Cause Descri tion continued CEA 23 dropped due to a 240 VAC circuit breaker tripping.The system was determined not to have any other problems.The circuit breaker was closed and CEA 23 operated correctly.  
Cause Descri tion continued CEA 23 dropped due to a 240 VAC circuit breaker tripping. The system was determined not to have any other problems. The circuit breaker was closed and CEA 23 operated correctly.
~r"x l<
 
FLORIDA POWER&LIGHT COMPANY April 8, 1977 PRN-LI-77-102 Mr.Norman C.Moseley, Director, Region II Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 1217 Atlanta, Georgia 30303  
  ~ r "x
l<
 
FLORIDA POWER & LIGHT COMPANY April   8, 1977 PRN-LI-77-102 Mr. Norman C. Moseley, Director, Region     II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 1217 Atlanta, Georgia     30303
 
==Dear Mr. Moseley:==
 
REPORTABLE OCCURRENCE  335-77-18 ST. LUCIE UNIT 1 DATE OF OCCURRENCE:  March ll, 1977 CONTAXNMENT AIR  LOCK The  attached Licensee Event Report is being submitted in accordance with Technical Specification 6..9 to provide 30-day notification of the subject occurrence.
Very  truly yours, A. D. Schmidt Vice President.
Power Resources MAS/slh Attachment cc:  Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement        (30)
Director, Office of Management, Xnformation and Program Control (3)
PEOPLE... SERVING PEOPLE
 
II
    ~      ~
C
        'I 1
 
    ~,
LICENSEE EVENT REPORT co~TRo~ BLocx:                                                              ,  (PLEASE PRINT ALL REQUIRED INFORMATION/)
1                        6
                      'CENSEE                                                                                  UCENSE                  EVENT NAME                                    UCENSE NUMBER                                  TYPE                    TYPE o1        FL        S    L    S 1            0  0    0      0 0    0 0          0    0          4 1    1      1    1      ~03 7      89                              14    15                                              25    26                      30    31    32 REPORT      REPOAT CATEGORY        TYPE      SOURCE              OOCKET NUMBEA                          EVENT OATE                      REPORT OATE
  ~a~ corn'                      ~L                      0 5    0        0 3      3  5        0    3    1 1    7      7    -
0 3      1  4  7    7 7 8              57      58      59        60      61                                68    69 74    75                      80 EVENT DESCRIPTION                                                          t
[oat              in          er o          ation the containment              escape    lock inner door failed Technical 7      8 9                                                                                                                                                60 mtediate corrective action was to maintain 7      89                                                                                                                                                  80 k closed.        This was the        third  occurrence          of  an. in-7      8 9                                                                                                                                                80 Qg8        o      able airlock door (335-76-14 and 335-76-46) but was unrelated to the previous 7        9                                                                                                                                                80 joag        occurrences.            (335-77-18) .
7      8 9                                                                PRME                                                                            80 SYSTEM      CAUSE                                          COMPONENT            COMPONENT COOE        COOE              COMPONENT COOS              SUFPUER            MA%4%ACTUAEA
[OD~]~A                  ~E            XX      X X      XX                          C    3    1 0                N 7      8 9 10              11        12                          17                                                    48 CAUSE DESCRIPTION Qg8          Seals on the inner door failed due to hardening of the rubber. ()he seals were over                                                      4 7        9                                                                                                                                                eo Qg            ears old).          The      seals were replaced and tested satisfactorily.
7 8      9 QOj 7      89    FACILITY
                                                                                                                      '                                    eo METHOO OF tlI 7      8      9
                ~
STATUS FOAM OF 5
                              ~z.
10 POWER o    o 12 13 OTHER STATUS N A 44 OISCOVERY 45      46 OISCOVEAY OESCRIPTION N/A 60 ACTIVITY      CONTENT RELEASEO      OF RELEASE              AMOUNT OF ACTIVITY                                            LOCATION OF AELEASE
                ~z            ~z                            NA                                                          N/A 7      8      0                10      11                                                                                                                60 PERSONNEL EXPOSURES 7
Q)j 89
          ~i~ NUMBER 11 TYPE Iz J 12      13 OESCAIPTION N/A 60 PERSONNEL INJURIFS NUMBER          CESCAIPTION
          ~00          0                                  N/A 7      8 9              11  12                                                                                                                          eo P+03ABLE CONSEQUENCES
~15                                                      N/A 7      89                                                                                                                                                  60 LOSS OR DAMAGE TO FACILITY TYPE      OESCAIPTION 7    89          10 Z~r reduced              to  1      cent    for re lacenent of seals.
60 PUBLICITY N/A 7    89 ADDITIONAL FACTORS N/A 7    89 7    89                                                                                                                                                  60 NAME:        M. A. Scho                                                            PHONE305/ 552-3779 CPO ddt e ddT


==Dear Mr.Moseley:==
k
REPORTABLE OCCURRENCE 335-77-18 ST.LUCIE UNIT 1 DATE OF OCCURRENCE:
  ~ r 'o P(}}
March ll, 1977 CONTAXNMENT AIR LOCK The attached Licensee Event Report is being submitted in accordance with Technical Specification 6..9 to provide 30-day notification of the subject occurrence.
Very truly yours, A.D.Schmidt Vice President.
Power Resources MAS/slh Attachment cc: Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement (30)Director, Office of Management, Xnformation and Program Control (3)PEOPLE...SERVING PEOPLE II~'~C'I 1
~, o1 FL 7 89 co~TRo~BLocx: 1 6 UCENSE NUMBER 0 0-0 0 0 0 0'CENSEE NAME S L S 1 UCENSE TYPE EVENT TYPE 0 0 4 1 1 1 1~03 25 26 30 31 32 14 15 LICENSEE EVENT REPORT , (PLEASE PRINT ALL REQUIRED INFORMATION/)
REPORT CATEGORY TYPE~a~corn'~L 7 8 57 58 59 REPOAT SOURCE 60 OOCKET NUMBEA EVENT OATE REPORT OATE 0 5 0-0 3 3 5 0 3 1 1 7 7-0 3 1 4 7 7 61 68 69'74 75 80 EVENT DESCRIPTION
[oat in er o 7 8 9 7 89 t ation the containment escape lock inner door failed Technical 60 mtediate corrective action was to maintain 80 k closed.This was the third occurrence of an.in-7 8 9 joag occurrences.
(335-77-18)
.7 8 9 SYSTEM CAUSE COOE COOE COMPONENT COOS[OD~]~A~E XX X X XX 7 8 9 10 11 12 17 CAUSE DESCRIPTION Qg Seals on the inner door failed due PRME COMPONENT SUFPUER COMPONENT MA%4%ACTUAEA C 3 1 0 N 48 to hardening of the rubber.()he seals were over 4 7 8 9 Qg ears old).The seals were replaced and tested satisfactorily.
7 8 9 Qg o able airlock door (335-76-14 and 335-76-46) but was unrelated to the previous 80 80 80 eo 7 8 9 QOj OTHER STATUS N A AMOUNT OF ACTIVITY NA N/A 7 89 FACILITY STATUS 5 POWER tlI~~z.o o 7 8 9 10 12 13 FOAM OF ACTIVITY CONTENT RELEASEO OF RELEASE~z~z 7 8 0 10 11 PERSONNEL EXPOSURES NUMBER TYPE OESCAIPTION Q)j~i~Iz J 7 89 11 12 13 PERSONNEL IN JURIFS NUMBER CESCAIPTION
~00 0 7 8 9 11 12 METHOO OF OISCOVERY 44 45 46 N/A'OISCOVEAY OESCRIPTION N/A LOCATION OF AELEASE N/A eo 60 60 60 eo P+03ABLE CONSEQUENCES
~15 7 89 LOSS OR DAMAGE TO FACILITY TYPE OESCAIPTION Z~r reduced to 1 7 89 10 PUBLICITY 7 89 ADDITIONAL FACTORS 7 89 N/A cent for re lacenent of seals.N/A N/A 60 60 7 89 NAME: M.A.Scho PHONE305/552-3779 60 CPO ddt e ddT k~r'o P(}}

Latest revision as of 04:30, 3 February 2020

LER 77-017-00 for Saint Lucie Unit 1 Regarding Dropped or Misaligned CEA 20 and CEA 23
ML18110A890
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 04/06/1977
From: Schmidt A
Florida Power & Light Co
To: Moseley N
NRC/RGN-II
References
PRN-LI-77-99 LER 77-017-00
Download: ML18110A890 (12)


Text

NRC FoAM 196 U.S. NUCLEAR AEGUL*TOAV COMMISSION DOCKET NUMOE A I2.70)

'BC DISTRIBUTION FoR f,. T 50 DOCKET MATERIAL FILE NUMOEA INCIDENT REPORT TO: ~ FROM; DATE OF DOCUMENT

~

Florida Power & Light Companyt 4/6/77 Mr. Norman C. Moseley Miami, Florida DATE RECEIVED A. D. Schmidt 4 21 77 QLETTEA Q NOTOR IZE D INPUT FOAM NUMBER OF COPIES RECEIVED Q OA IG INAL Qcopv DESCRIPTION QUNCLASSIFIED ENCLOSURE I at~8~

\

I Ltre trans the following: Licensee Event Report (RO 50-335/77-17) on 3/7/77 concerning CEA 20 not the Upper Electrical 'Limit reed withdrawing'ecause switch had failed closed, thus prohibiting

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outward CEA .mo one ~ ~ ~

(RO 50-335/76-46) on 3/11/77 concernirig the containment escape lock inner door failing

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e PLANT NAME: ~

vG, tech spec surveillance ~ ~ .

$ t,. Lncie Uni.t Nc. 1 QgQ gJL (1-P) (4-p) .,

I IF 'OTE:

PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS FOR ACTION/INFO RiVIATION BRANCH CHIEF:

W 3 CYS FOR ACTION LICo ASST,:

>I CXS ACRS ( CXS 149b&%HC S NT INTERNAL D IST RI OUT ON G FILE I&E(2 MIPC SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIIKS CASE HANAUER TEDESCO/FIACCARY EISENHUT SHAO VOLLMER/BUNCH KREGER/J ~ COLLINS EXTERNAL DISTRIOUTION CONTROL NUMOER LPDR:

TIC:

~ 1e ee. 7>ll 4 0/94 N~C.

NRC FOAM 196 {2 70)

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P. O. BOX 013100, MIAMI, FL 33101 Qlyyz FLORIDA POWER & LIGHT COMPANY April 6, 1977

. PRN-LI-77-99 Aegulatory EQLCfg q

Mr. Norman C. Moseley, Director, Region II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 1217 Atlanta, Georgia 30303

Dear Mr. Moseley:

REPORTABLE OCCURRENCE 335-77-17 ~cj~

ST. LUCIE UNIT 1 DATE OF OCCURRENCE: MARCH 7, 1977 CEA 20 6 CEA 23 The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.

Very truly yours, D. Schmidt Vice President e

Power Resources MAS/ms Attachment CC Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement (30)

Director, Office of Management Information and Program Control (3) r7 jld"b/89 PEOPLE... SERVING PEOPLE

1' QI IE

, ~

LICENSEE EVENT REPORT

~ CONTROL BLOCK: fPL~SE PRiNT ALL RECIUIRED INFOAMAT!ON)

BYNAME LCENSEE UCENSE EVENT LICENSE NUMBER TYPE TYPE F L S L S 1 0 0 0 0 0 0 0 0 0 411 1 1 I z ~03

~

7 89 14 15 25 26 30 REPORT REPORT CATEGORY TYPE SOURCE OOCKET NUMBER EVENT OATE REPORT OATE I001I coN'T ~L ~L 0 5 0 0 3 3 5 0 3 0 7 7 7 0 3 1 5 7 7 7 8 57 58 59 60 61 68 69 74 75 60 I

EVENT DESCRIPTION QO 2 Durin surveillance testin , CEA 20 would not withdraw with the rest of Group 2, so 7 8 9 BO action was taken in accordance with action statement "d" of Specification 3.1.3.1.

7 89 80

[QQ4] Shutdown margin was veri fied, power was reduced to 70 percent, and while the rest of 7 8 9 80 Qp 5 the group was being aligned to CEA 20, CEA 23 dropped. CEA 23 was recovered in 34 7 8 9 60 QOQ minu tes thereb sa t is f in ac tion a m II II f The o erabilit 89 PAVE 80 SYSTEM COOE CAUSE COOE COtiIPONENT COOE COMPO IIENT SUPPLER COMPO BJ ENT MANUF~i'FER

~0> ~RB ~B 0 K T B R K C 4 9 0 N 7 8 9 10 11 12 17 47 48 CAUSE DESCRIPTION tOOBj CEA 20 would not withdraw because the Upper Electrical Limit (UEL) reed switch had 7 8 9 7

Q~ I8 9 failed closed, thus prohibiting outward CEA motion. The failed reed switch was taken 80 60 of the circuit and the s are UEL reed switches were verified to be in service.

7 89 FACILIIY 80

, METHOO OF STATUS '%OWER OTHER STATUS OISCOVERY OISCOVERY OESCRIPTION

@~~

7

]8 9

~B ~OB 0 NA NA 10 12 13 44 45 cO FORM OF AcnVITY COATENT RELEASED OF RELEASE AMOUNT OF ACnVITY LOCATION OF RELEASE KIH NA NA 7 8 9 10 11 44 45 60 PERSONNEL EXPOSURES NUMSER TYPE OESCRIPTION

~io ~oo o '~z 7 8 9 11 12 13 80 PERSONNEL INJURIES NUMBER CESCRIPTIOtJ PP+ 0 0 NA 7 8 9 11 12 ao PROBABLE CONSEQUENCES Qg8 NA 7 9 80 LOSS OR DAMAGE TO FACILITY TYPE OESCRIPTION l91 LzJ 7 89 NA 10 60 PUBLICITY NA 7 89 .BO ADDITIONAL FACTORS Qg See a e two for continuation of Event Description and Cause Description.

7 89 7 89 M: A. Scho man 305 552-3802 PHONEI COO 65 I ~ II 0T

4 ~

V

~ M

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Reportable Occurrence 335-77-17 Licensee Event Report Pa e Two Event Descri tion (continued) of CEA 20 was then restored and power was increased to 100 percent.

CEA 20 had been declared inoperable for 43. minutes. This was the fourth occurrence of dropped or misaligned CEA's (335-76-25, 335-76-37, and 335-77-6) but was unrelated to the previous occurrences.

(335-77-17)

Cause Descri tion continued CEA 23 dropped due to a 240 VAC circuit breaker tripping. The system was determined not to have any other problems. The circuit breaker was closed and CEA 23 operated correctly.

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FLORIDA POWER & LIGHT COMPANY April 8, 1977 PRN-LI-77-102 Mr. Norman C. Moseley, Director, Region II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 1217 Atlanta, Georgia 30303

Dear Mr. Moseley:

REPORTABLE OCCURRENCE 335-77-18 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: March ll, 1977 CONTAXNMENT AIR LOCK The attached Licensee Event Report is being submitted in accordance with Technical Specification 6..9 to provide 30-day notification of the subject occurrence.

Very truly yours, A. D. Schmidt Vice President.

Power Resources MAS/slh Attachment cc: Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement (30)

Director, Office of Management, Xnformation and Program Control (3)

PEOPLE... SERVING PEOPLE

II

~ ~

C

'I 1

~,

LICENSEE EVENT REPORT co~TRo~ BLocx: , (PLEASE PRINT ALL REQUIRED INFORMATION/)

1 6

'CENSEE UCENSE EVENT NAME UCENSE NUMBER TYPE TYPE o1 FL S L S 1 0 0 0 0 0 0 0 0 0 4 1 1 1 1 ~03 7 89 14 15 25 26 30 31 32 REPORT REPOAT CATEGORY TYPE SOURCE OOCKET NUMBEA EVENT OATE REPORT OATE

~a~ corn' ~L 0 5 0 0 3 3 5 0 3 1 1 7 7 -

0 3 1 4 7 7 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTION t

[oat in er o ation the containment escape lock inner door failed Technical 7 8 9 60 mtediate corrective action was to maintain 7 89 80 k closed. This was the third occurrence of an. in-7 8 9 80 Qg8 o able airlock door (335-76-14 and 335-76-46) but was unrelated to the previous 7 9 80 joag occurrences. (335-77-18) .

7 8 9 PRME 80 SYSTEM CAUSE COMPONENT COMPONENT COOE COOE COMPONENT COOS SUFPUER MA%4%ACTUAEA

[OD~]~A ~E XX X X XX C 3 1 0 N 7 8 9 10 11 12 17 48 CAUSE DESCRIPTION Qg8 Seals on the inner door failed due to hardening of the rubber. ()he seals were over 4 7 9 eo Qg ears old). The seals were replaced and tested satisfactorily.

7 8 9 QOj 7 89 FACILITY

' eo METHOO OF tlI 7 8 9

~

STATUS FOAM OF 5

~z.

10 POWER o o 12 13 OTHER STATUS N A 44 OISCOVERY 45 46 OISCOVEAY OESCRIPTION N/A 60 ACTIVITY CONTENT RELEASEO OF RELEASE AMOUNT OF ACTIVITY LOCATION OF AELEASE

~z ~z NA N/A 7 8 0 10 11 60 PERSONNEL EXPOSURES 7

Q)j 89

~i~ NUMBER 11 TYPE Iz J 12 13 OESCAIPTION N/A 60 PERSONNEL INJURIFS NUMBER CESCAIPTION

~00 0 N/A 7 8 9 11 12 eo P+03ABLE CONSEQUENCES

~15 N/A 7 89 60 LOSS OR DAMAGE TO FACILITY TYPE OESCAIPTION 7 89 10 Z~r reduced to 1 cent for re lacenent of seals.

60 PUBLICITY N/A 7 89 ADDITIONAL FACTORS N/A 7 89 7 89 60 NAME: M. A. Scho PHONE305/ 552-3779 CPO ddt e ddT

k

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