ML18127A660

From kanterella
Jump to navigation Jump to search
LER 1978-019-00 for St. Lucie Unit 1, on 05/30/78 Concerning During Special Low Pier Feedwater Control System Test a 15% Feedwater Bypass Control Valve Inadvertently Opened Fully Causing Excessive Cooling of 1A Steam Generator
ML18127A660
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 06/28/1978
From: Schmidt A
Florida Power & Light Co
To: O'Reilly J
NRC/RGN-II, NRC/IE
References
PRN-LI-78-173 LER 1978-019-00
Download: ML18127A660 (5)


Text

REGULATORY INFORMATION DISTRIBUTION SYSTEI'I < R IDS)

DISTRIBUTION FOR INCOMING MATERIAL 50-335 REC: V. eR-C.t~'4 8P ORG: SCHMIDT A D DQCDATE: 06/28/78 NRC FL PIJR 5 LIGHT DATE RCVD: 07/07/78 DOCTYPE: LETTFR NOTARIZED: NO COPIES RECEIVED

SUBJECT:

LTR 1 ENCL 1

, FORWARDING LICENSEE FVENT REPT < RO 50-335/78-019) ON 05f30/78 CONCFRNING DURING SPFCIAL LOLA PIER FEEDWATER CONTROL SYSTEM TEST A 15/ FEEDWATER BYPASS l CONTROL VALVE INADVERTFNTLY OPENED FUI LY CAUSING EXCESSIVE COOLING OF iA STEAM GENERATOR.

PLANT NAME: ST LUCIE )I:1

+<<->t<<~H~<<+<<4'<<<<<<<<<<<<DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS REVIEI JER INITIAL: X JM DISTRIBUTOR INITIAL: ~

INCIDENT REPORTS

<DISTRIBUTION CODE A002)

FQR ACTION: ~ ~~<<W/4 ENCL INTERNAL: NRC PDR+<<W/ENCL z2 ENCL MIPC+<<Il/3 ENCL I 8( C SYSTEMS BR<<4~W/ENCL EMERGENCY Pl AN BR<<+IJ/ENCL NOVAK/CHECK4H~W/ENCL EEB<<<<W/ENCL AD FOR ENG<<<<W/ENCI Pl ANT SYSTFMS BR<<<W/ENCL HANAUER<<<<W/ENCL AD FOR PLANT SYSTEMS<<<<W/ENCL AD FOR SYS 0 PROJ<<<<W/ENCL REACTOR SAFETY BR<<W/ENCL ENGINEERING BR~~<<W/ENCL VOI LMER/BUNCH<<>W/ENCL KREGER/ J. CQI LINS<<<<.l Jf ENCL POWER SYS BR<<4tW/ENCL K SEYFR IT/IE<<<<W/ENCL EXTERNAL: LPDR S Fl PIFRCE Fl <<<<W/ENCL T I C~~<<W/ENCL NS I C<<<<l Jf ENCL g)0 ACRS CAT B<<<<W/16 FNCL DISTRIBUTION: LTR 45 ENCL 45 CONTROL NBR: 781880119 SI ZE: 1 P+iP

<sw<<<<<<<<<<<<<<<<esp<<<<cs<<ss<<e<<<<<<ss<<<<n<><sn<<is<<<<<<<<THE ENl3 <<<<<<<<<<<<<<<<%<<<<<<<<<<<<<<<<<<%4k%%<<%<<<<%

0 .r 4

'I

'1 r

FLORIDA POWER 8I LIGHT COMPANY June 28, 1978, PRN-L I-78+? 3 rn Mr. James P. O'Reilly, Director, Region II CU4= f>l Office of Inspection and Enforcement C/l E"s ~

U. S. Nuclear Regulatory Commission ~V)

V 0 mal 230 Peachtree Street, N. 11., Suite 1217 MORI

~UJ Atlanta, Georgia 30303 n =I Pl CO n

Dear Mr. O'Reilly:

REPORTABLE OCCURRENCE 335-78-19 ST.LUCIE UNIT 1 DATE OF OCCURRENCE: MAY 30 1978 TECHNICAL SPECIFICATION 3.1.1.5 RCS AVERAGE TEMPERATURE The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence. I 4

Very truly yours,

. Schmidt Vice President Power Resources MAS/pa Attachment cc: Harold F. Reis, Esquire Director, Office of Inspection and Enforcement (30)

Director, Office of Management Information and Program Control (3) 781880119 PEOPLE... SERVING PEOPLE

NRC FORM SEB U S NUCLEAR REOULATORY COMMISSION IT TTI LICENSEE EVcHT REPORT CONTROL Sl CCKI I I I I I QI lPLBASB PRINT OR TYP AI.L, REQUIRED INFORMATIONI I

~O O.l 01 CI 01- 0 0 z 411 1 ll Q4~IQs I 3 UCSNSKK'OOK LICKiss s K iV UM0 KA 2,0., LICailSK TYPs 40 Si <<*i

~

~O CON'T ILiCS So s

6I il i i i i i OOCXKT NUMSKA 5'Czcsssz Sa aa i I SCS~D6 KVKNTQATK l4 IS lz 18~17 AKPQATOATK ii 30 SS EVENT DESCRIPTION ANO PROBABL" CONSBCU NCSS QIO Durin a s ecial low ower about 3X feedwater control s stem test, a 15 feedwater b ass control valve inadvertently opened fully causing excessiv cooling of 1A Steam Generator. Reactor coolant system average temperatur dropped slightly below 515F (about*1F) requiring ACTION in accordance.wi h SPecification 3.1.1.5. The reactor was tripped manually'hen this occurre .

This was the first occurrence of this type at St. Lucie...

~oa 7 a 9 30 SYSTEM CAUSE CAUSE COMP. VALVE COOK COOK SUSCOOK COMPONENT COOK SUB QK 3 'OOK

~ss ~Ra Qii ~K Qzz ~X Qiz II S T R 0IQis ~Y Qis 0~ Qs 7 a 9 Io 12 la 1$ l9 20 SKQUKNTIAL OCCUAAKACK APPQAT AKVISIONi 22 24 as 2l 29 29 , ao ACTION PUTUAK= KPP KC SHUTQQWN ' Al ACIIMKNT SIPAOP 'QMPONKNT

~<~'"

PAIMECOMP.

~isis "cls 'is

~

a4 CAUSE DESCRIPTION ANO CORRBCTIVB AEONS Zszs as SI Q22 40 i

>>z.s 4I As 42,

'i's i'cs 42

~ssz 44 41 o A vendor ro osed modification of the 15% Feedwater Control System was tem-poraril installed on the A loop for feasibility testing (to.improve stabil it . of the automatic mode). Gain settings based on analytical'results roved to be unrealistic and caused the bypass valve to open. The settings were chan ed to allow corn letion of the test.

s~>>'"

2 QZG 2 a P4CILITV STATUS LJs ACTIVITY CQNTKsIT

~i' IO A POWZA I2 I2 OTIIEA STATUS 44 MKTHOO CP CISCQVEAV

~AQOI

'S 4E Operator Observation OISCOVKAV O KSCAzpTION Q42 slKLKASKO OP AKLMsSZ AMOUNTOP ACTIVITYQSS LQCATIQ'IQP A jl.KASK QS EK LZJ Q>>

I a 9 MQS Io II 44 45 N A so PSASONNKL KXPOSUA KS NUMSKA TVPS OKSCPIPTION Q+

~iz ~00' 'Qzi Z Qa N/A

~ ~~8 II I'2 I2 4 KASCNNZL IN4UAIKS N A I.CSS QP Csl O4M*O- 0 P4CILITV ao VPK QKSCAIPTION Q4>

CZ a LZJQ2 9 'o PUSLICI.Y N A NRC USB ONLY 30 I.SSUco QKSCAIPT:CN Q<<S s) a Q

2:0 IQ44 N/A NAMBOF PREPARER M. A. Scho man (305) 552-3802