LER-2078-007, For St. Lucie Unit 1, Technical Specification 4.3.1.1.3 RTD Response Time |
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| 3352078007R00 - NRC Website |
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VQ REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS >
DISTRIBUTION FOR INCOMING MATERIAL 50-335 REC:
OREILLY J P
NRC ORG:
SCHMIDT A D DOCDATE: 02/17/78 FL PWR 5 LIGHT DATE RCVD: 02/27/78 DOCTYPE:
LETTER NOTARIZED:
NO COPIES RECEIVED
SUBJECT:
LTR 1
ENCL 1
LICENSEE EVENT REPT (RO 50-335/78-7>
ON 02/03/78 CONCERNING TECH SPEC TABI E 3. 3. 2 DOES NOT INCLUDE ALLOWANCE FOR RESISTANCE TEMP DETECTOR-(RTD>
RESPONSE
TIMEi THEREBY PREVENTING FULL COMPLIANCE FULL COMPLIANCE WITH TECH SPEC
- 4. 3. i. l. 3
<RESPONSE TIME TEST PLANT NAME: ST LUCIE Ci REVIEWER INITIAL:
XJM DISTRIBUTOR INITIAL:
+4++4++4~HF44t++++4t DISTRIBUTION OF 'THIS MATERIAL IS AS FOLLOWS INCIDENT REPORTS (DISTRIBUTION CODE A002>
FOR ACTION:
INTERNAL:
EXTERNAL:
BR CHIEF
/4 ENCL EI 5 E+4W/2 ENCL SCHROEDER/IF'POL ITO~~+W/ENCL NOVAK/CHECK44W/ENCL KNIGHT++W/ENCL HANAUER~~~W/ENCL EISENHUT++W/ENCL SHAO+4W/ENCL KREGER/J.
COLLINS++W/ENCL K SEYFR IT/IE++W/ENCL LPDR S FT PIERCF FL++W/ENCL TIC++W/ENCL NSIC++W/ENCL ACRS CAT B44W/16 ENCL NRC PDR4~+W/ENCL MIPC4+W/3,ENCL HOUSTON4H~W/ENCL GR IMES+~~ll/ENCL BUTLER~H~W/ENCL TEDESCO4+W/ENCL BAER++W/ENCL VOLLMER/BUNCH++W/ENCL ROSA++W/ENCL COPIES NOT SUB~fITTED PER REGULATORY GUIDE 10.1 I
DISTRIBUT1ON:
LTR 45 ENCL 45 SIZE:
iP+iP+iP THE END CONTROL NBR 780590035
%%%%%%%WH$ %8l+%%%%%%%%%%%%%%%.
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FLORIDA POPOVER & LIGHTCOMPANY February 17, 1978 PRN-LI-78-48 Mr. James P. 0'eilly, Director, Region Ig Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree
- Street, N. W., Suite 1217 Atlanta, Georgia 30303
Dear Mr. O'Reilly:
qlsvapron REPORTABLE OCCURRENCE 335-78-7 ST.
LUCIE UNIT 1 DATE OF OCCURRENCE:
FEBRUARY 3, 197 Oi~'iisil TECHNICAL SPECIFICATION 4.3.1.1.3 RTD RESPONSE TIME The attached Licensee Event Report is being submitted in accordance. with Technical Specification 6.9 to provide prompt notification of the subject occurrence..
Very truly yours,.
A. D. Schmidt Vice President Power Resources MAS/bab Attachment CC Robert Lowenstein, Esquire Director, Office of Inspection and Enforcement (40)
Director, Office of Management Information and.
Program Control (3) 78O590035 o 9 PEOPLE... SERVING PEOPLE
LICENSEE EVENT coNvooL oLoox:
REPORTS (PLAGE PRIa~JT ALLREQUIRED INFGRMAT!GN)
LCENSEE NAME o'
L S
L S
7 -89 1
6 LICENSE NUMSER 0
0 0l0 0
0 0
14 15 UCENSE TYPE EVENT TYPE 25 26 30 31 32 o
o I
I. I> II.
x
~o
- REPORT, REPORT CATEGORY TYPE SOURCE COCKET NUMSER
~o~ corn'
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~i, ol 5 0 0
13 7
8 57 58 59 60 61 3
5 0
Se S9 EVEN OATS REPORT CATE 2 0I3 7
8 OI2 1 7I7 8
74 75 eo EVEIVT OESCRIPTION
~ol2 T chnical Specification Table 3.3-2(Reactor Protective Instrumentation
Response
Times) 7 8 9 eo Q03 does not include allowance for resistance temperature detector (RTD) response t'me, 7
89 60
~0 <
therebv preventing full compliance with Technical Specification 4.3.1.1.3 (response time 7
8 9 oo Qg testin
.. In addition the RTD res onse times of selected channels are apparently greatef 7
8 9 60 tOD~]
than the 5-second value initiall used b
the NSSS vendor in the applicable setpoint t
7 8 9 SYSTEM
CAUSE
COQE CQOE COMPONENT CQOE
~67 ~IIA
~B I
N o
1 R
U 7
8 9 10 11 12 17 C" USE OESCRIPTION [Oa~j The RTDs are mounted in instrument MME cQMpc'Ie4T SUPPUER N
COMPONENT MAhUF~i R
3 7[0 47 N
48 wells.
Apparently, changes in the parameters 7
8 9 60 toD9J governing the response of an RTD in an instrument well affect.the overall response time.
7 8 9 60
~1 0 In addition, St. Lucie Unit 1 and other similar plants have had difficultyverifying the OTHER STATUS NA PZOBA8LZ coNSECUENcees NA 89 FACTORY STATUS.
dd POWER=
~E
~o 7
8 9
10 12 13 FORM OF ACTiY CQATENT RELeeSEO OF R=LEASE AMOUNT OF ACTIVITY
~z NA 7
8" 9
10 11 PERSONNEL EXPOSURES NUMBER TYPE OESCRIPTICN I11j LIMNI L~J NA 7
8 9 11 12 13 PERSONNEL INJURIES NUMBER CESCRIPTION
~4 ~001 0
NA 7
89 11 12 METHOO" OF QISCOVERY a5 as 44 45 OISCOVERY OESCRIPTIQN NA
~ LOCATICN QF RELEASE NA 80 60 80 60 7'9 LOSS OR OAMAGE TO FACIUTY TYPE OESC IPOQN
~1IS 7
89 10 PUSLICITY 7
8 9 NA NA 80 eo AOOITIONAL FACTORS QQ a
e two for continuation of Event Description and Cause Description.
7 8 9 80 7
99 NAME:
A.
Sc PHONE:
60 C>0 dd'I 44T
Reportable Occurrence 335-78-7 Licensee Event Report Page Twoanalysis.
his is based on measurements made by a consultant in mid-January, 1978.
The consultant reported the results on February 3, 1978.
Although the measured response times are greater than 5 seconds, they are less than t.he revised value of 8 seconds contained in a proposed Technical Specification amendment which has been submitted to.the 'NRC (see "Cause De-scription").
This is the first occurrence of this type at St. Lucie Unit l.
(335-78-7)
==Cause==5-second response time assumed in the NSSS setpoint analysis.
As a result of the parametric uncertainties and the measure-ment difficulties, the NSSS vendor had been requested in 1977 to re-evaluate the appropriate setpoints using' response time greater than 5 seconds.
In December, 1977 the NSSS vendor responded with an evaluation that supported response times of up to 8 seconds.
A proposal to incorporate the 8-second value in Table 3 3-2 was forwarded to the NRC by letter L-78-39 dated, February 2,
1978..
All RTDs tested'ad response times less than 8 seconds, so no further action beyond the Technical Specification change proposal, is planned at this time.
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| 05000335/LER-2078-007, For St. Lucie Unit 1, Technical Specification 4.3.1.1.3 RTD Response Time | For St. Lucie Unit 1, Technical Specification 4.3.1.1.3 RTD Response Time | | | 05000335/LER-2078-008, For St. Lucie Unit 1, Due to an Administrative Error During a Procedure Revision Instructions for Documenting Surveillance of Volume in Diesel Generator Engine Mounted Fuel Tanks Were Omitted | For St. Lucie Unit 1, Due to an Administrative Error During a Procedure Revision Instructions for Documenting Surveillance of Volume in Diesel Generator Engine Mounted Fuel Tanks Were Omitted | | | 05000335/LER-2078-009, For St. Lucie Unit 1, During PWR Operation Digital Data Processing System Malfunctioned. Apparent Momentary Memory Failure Caused Ddps to Halt | For St. Lucie Unit 1, During PWR Operation Digital Data Processing System Malfunctioned. 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Inadvertently Missed During One Surveillance Interval Encompassing Short Maintenance Outage & Subsequent Startup | |
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