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| issue date = 12/27/1979
| issue date = 12/27/1979
| title = LER 79-063/03L-0:on 791127,in Mode 1,both Boric Acid Transfer Pumps Were Made Inoperable.Caused Intentionally to Unplug Branch Line That Had Solidified
| title = LER 79-063/03L-0:on 791127,in Mode 1,both Boric Acid Transfer Pumps Were Made Inoperable.Caused Intentionally to Unplug Branch Line That Had Solidified
| author name = LEASE R S
| author name = Lease R
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:NRC FORM 366 ,{7-77)r r'~3'ONTROL BLOCK: U.S.NUCLEAR REGULATORY COMMISSION tCENSEE EVENT REPORT Q 1 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 6 tOOi]7 8 CON'T~O 7 8 M I D Q2 9 LICENSEE CODE 14 15 LICENSE NUMBER soUROE LIJO 0 5 0 0 0 3 1 5 Q 1 60 61 DOCKET NUMBER 68 69 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 WHILE OPERATING IN MODE 1 BOTH B 3 Q"~QR 25 26 LICENSE TYPE 30 57 CAT 58 Q 1 2 7 7 9 QB>2 2 7 7 9 QB EVENT DATE'4 75 REPORT DATE 80~03 FOR A PERIOD OF 4'HOURS AND 40 MINUTES.THIS WAS CON R 0 H~o4 THE ALTERNATE FLOW PATH FROM THE REFUELING WATER T A~O6~O7~OB 7 8 9 80 7 8 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT'CODE SUBCODE SUBCODE~RB Q11 X Q12~2Q13 Z Z Z Z Z Z Q4~ZQ18~2 Q'8 9 10 11 12 13 18 19 20 SEQUENTIAl OCCURRENCE REPORT REVISION LERIRO EVENT YEAR REPORT NO.CODE TYPE NO..Q17 RRRRR7~79+~06 3+W~03+L+QO 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER
{{#Wiki_filter:NRC FORM 366                                                                                                                         U. S. NUCLEAR REGULATORY COMMISSION
~ZP18~ZQ79~ZQRP~ZQ27 0 0 0 0 N P>>~NQ24~ZP>>2 0 0 0 P28 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o THE BORIC ACID TRANSFER PUMPS WERE INTENTIONALL M DE I'ERA E T U BRANCH LINE THAT HAD SOLIDIFIED.
,{7-77) r r'~                                                                   tCENSEE EVENT REPORT 7
TIMING WAS SELECTED ANTICIPATED.
3'ONTROL BLOCK:
3 4 7 8 9 FACILITY~30 METHOD OF STATUS BB POWER OTHER STATUS Q DISCOVERY 8 E Q28~l0 0 Q29 NA~BQ31 7 8 9 10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF RElEASE AMOUNT OF ACTIVITY~~~[LL6]~Z Q33~ZQ NA 7 8 9 10 11 44 45 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39 7 L0 0 0 0~0~IQ3 7 Z Q3 8 NA 7 8 9 11 12 13 PERSONNEL INJURIES DISCOVERY DESCRIPTION OPERATOR OBSERVATION LOCATION OF RELEASE~80 80 80 80 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43 TYPE DESCRIPTION g Z Q42 NA 8 9 10 PUBLICITY ISSUED DESCRIPTION
tOOi]
~2O~NQ4 NA 7 8 9 10 NAME OF PREPARER LEASE 80 NRC USE ONLY 3 68 69 804 g (616)465-5901 X-313 0 0 a+i ,I}}
CON'T 8     9 M     I   D LICENSEE CODE             14 Q2 15 6
Q1 LICENSE NUMBER (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 25 Q 3 26        LICENSE TYPE        30 Q"  ~
57 CAT 58 QR
  ~O 7          8 soUROE     LIJO 60            61 0     5     0   0   0 DOCKET NUMBER 3   1   5 68 Q 69 1     1   2 EVENT 7 7 9 QB>
DATE'4                    75 2     2 REPORT DATE 7   7     9 80 QB EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                              Q10 WHILE OPERATING IN MODE                          1      BOTH B
~03                     FOR A PERIOD OF                   4 'HOURS AND 40 MINUTES .                       THIS     WAS CON R                     0         H
  ~o4                   THE ALTERNATE FLOW PATH FROM THE REFUELING WATER                                                   T     A
  ~O6
~O7
  ~OB 7         8 9                                                                                                                                                                           80 SYSTEM               CAUSE           CAUSE                                                         COMP.           VALVE CODE               CODE       SUBCODE                   COMPONENT'CODE                       SUBCODE           SUBCODE
                                    ~RB             Q11       X   Q12     ~2Q13             Z   Z     Z   Z     Z     Z Q4         ~ZQ18             ~2     Q'8 7          8                      9           10           11             12             13                               18           19               20 SEQUENTIAl                           OCCURRENCE             REPORT                         REVISION
              . Q17 LERIRO RRRRR7 ACTION FUTURE EVENT YEAR
                                      ~79 21        22 EFFECT
                                                              +
23 SHUTDOWN
                                                                              ~06 24 REPORT NO.
3 26
                                                                                                      +W 27
                                                                                                                      ~03 28 ATTACHMENT CODE 29 NPRDQ TYPE
                                                                                                                                              +L 30 PRIME COMP.
                                                                                                                                                              +
31 NO.
QO 32 COMPONENT TAKEN ACTION                 ON PLANT           METHOD                   HOURS Q22           SUBMITTED         FORM SUB.         SUPPLIER             MANUFACTURER
                  ~ZP18 ~ZQ79                   ~ZQRP             ~ZQ27               0     0   0     0           N   P>>       ~NQ24               ~ZP>>               2     0   0 0   P28 33         34                 35                 36             37                     40     41               42                 43               44               47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o               THE BORIC ACID TRANSFER PUMPS WERE INTENTIONALL                                                   M DE     I'       ERA       E T     U BRANCH         LINE THAT           HAD     SOLIDIFIED.             TIMING       WAS SELECTED ANTICIPATED.
3 4
7         8     9                                                                                                                                                                       80 FACILITY STATUS               POWER                       OTHER STATUS       Q
                                                                                      ~30      METHOD OF DISCOVERY                               DISCOVERY DESCRIPTION
                              ~l0 BB 8           E   Q28                     0   Q29               NA                         ~BQ31                                   OPERATOR OBSERVATION 7         8   9             10               12       13                             44     45         46                                                                         80 ACTIVITY CONTENT
                                                                                                                                                                    ~
0 RELEASED OF RElEASE                         AMOUNT OF ACTIVITY~~~                                                         LOCATION OF RELEASE
[LL6] ~Z 7        8    9 Q33   ~ZQ 10           11 NA 44           45                                                                               80 PERSONNEL EXPOSURES 7       L0 0   ~0~
NUMBER 0         IQ3 7 TYPE Z   Q3 8 DESCRIPTION Q39 NA 7         8   9               11       12         13                                                                                                                                 80 PERSONNEL INJURIES 7         8   9               11       12                                                                                                                                             80 LOSS OF OR DAMAGE TO FACILITY TYPE       DESCRIPTION                   Q43 g           Z   Q42                     NA 8   9           10 PUBLICITY DESCRIPTION NRC USE ONLY ISSUED
~2O             ~NQ4                           NA                                                                                                                                           3 7       8     9           10                                                                                                                       68    69                            804  g NAME OF PREPARER                                   LEASE                                                               (616) 465-5901 X-313
 
0 0 a+i
        ,I}}

Latest revision as of 05:27, 29 October 2019

LER 79-063/03L-0:on 791127,in Mode 1,both Boric Acid Transfer Pumps Were Made Inoperable.Caused Intentionally to Unplug Branch Line That Had Solidified
ML17326A432
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 12/27/1979
From: Lease R
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17318A528 List:
References
LER-79-063-03L, LER-79-63-3L, NUDOCS 8001020406
Download: ML17326A432 (2)


Text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION

,{7-77) r r'~ tCENSEE EVENT REPORT 7

3'ONTROL BLOCK:

tOOi]

CON'T 8 9 M I D LICENSEE CODE 14 Q2 15 6

Q1 LICENSE NUMBER (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 25 Q 3 26 LICENSE TYPE 30 Q" ~

57 CAT 58 QR

~O 7 8 soUROE LIJO 60 61 0 5 0 0 0 DOCKET NUMBER 3 1 5 68 Q 69 1 1 2 EVENT 7 7 9 QB>

DATE'4 75 2 2 REPORT DATE 7 7 9 80 QB EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 WHILE OPERATING IN MODE 1 BOTH B

~03 FOR A PERIOD OF 4 'HOURS AND 40 MINUTES . THIS WAS CON R 0 H

~o4 THE ALTERNATE FLOW PATH FROM THE REFUELING WATER T A

~O6

~O7

~OB 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT'CODE SUBCODE SUBCODE

~RB Q11 X Q12 ~2Q13 Z Z Z Z Z Z Q4 ~ZQ18 ~2 Q'8 7 8 9 10 11 12 13 18 19 20 SEQUENTIAl OCCURRENCE REPORT REVISION

. Q17 LERIRO RRRRR7 ACTION FUTURE EVENT YEAR

~79 21 22 EFFECT

+

23 SHUTDOWN

~06 24 REPORT NO.

3 26

+W 27

~03 28 ATTACHMENT CODE 29 NPRDQ TYPE

+L 30 PRIME COMP.

+

31 NO.

QO 32 COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER

~ZP18 ~ZQ79 ~ZQRP ~ZQ27 0 0 0 0 N P>> ~NQ24 ~ZP>> 2 0 0 0 P28 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o THE BORIC ACID TRANSFER PUMPS WERE INTENTIONALL M DE I' ERA E T U BRANCH LINE THAT HAD SOLIDIFIED. TIMING WAS SELECTED ANTICIPATED.

3 4

7 8 9 80 FACILITY STATUS POWER OTHER STATUS Q

~30 METHOD OF DISCOVERY DISCOVERY DESCRIPTION

~l0 BB 8 E Q28 0 Q29 NA ~BQ31 OPERATOR OBSERVATION 7 8 9 10 12 13 44 45 46 80 ACTIVITY CONTENT

~

0 RELEASED OF RElEASE AMOUNT OF ACTIVITY~~~ LOCATION OF RELEASE

[LL6] ~Z 7 8 9 Q33 ~ZQ 10 11 NA 44 45 80 PERSONNEL EXPOSURES 7 L0 0 ~0~

NUMBER 0 IQ3 7 TYPE Z Q3 8 DESCRIPTION Q39 NA 7 8 9 11 12 13 80 PERSONNEL INJURIES 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Q43 g Z Q42 NA 8 9 10 PUBLICITY DESCRIPTION NRC USE ONLY ISSUED

~2O ~NQ4 NA 3 7 8 9 10 68 69 804 g NAME OF PREPARER LEASE (616) 465-5901 X-313

0 0 a+i

,I