|
|
(3 intermediate revisions by the same user not shown) |
Line 3: |
Line 3: |
| | issue date = 10/07/1999 | | | issue date = 10/07/1999 |
| | title = LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr | | | title = LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr |
| | author name = FREHAFER K W, STALL J A | | | author name = Frehafer K, Stall J |
| | author affiliation = FLORIDA POWER & LIGHT CO. | | | author affiliation = FLORIDA POWER & LIGHT CO. |
| | addressee name = | | | addressee name = |
Line 16: |
Line 16: |
|
| |
|
| =Text= | | =Text= |
| {{#Wiki_filter:MMJ;NVUlCY'~~~~REGULATORY INFORMATION DISTRIBUTION SYSTEM(RIDS)ACCESSION NBR:9910140083 DOC.DATE: | | {{#Wiki_filter:MMJ;NVUlC Y' REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS) |
| 99/10/07NOTARIZED: | | ACCESSION NBR:9910140083 |
| NOFACIL:50-335 St.LuciePlant,Unit1,FloridaPower&LightCo.AUTH.NAME.'AUTHORAFFILIATION FREHAFER,K.W.
| | ~ |
| FloridaPower&LightCo.STALL,J.A.
| | DOC.DATE: 99/10/07 NOTARIZED: NO |
| ,FloridaPower&LightCo.RECIP.NAME RECIPIENT AFFILIATION DOCKET¹05000335 | | ~ |
| | FACIL:50-335 St. Lucie Plant, Unit 1, Florida Power & Light Co. |
| | ~ |
| | DOCKET ¹ |
| | ~ |
| | 05000335 AUTH.NAME . 'AUTHOR AFFILIATION FREHAFER,K.W. Florida Power & Light Co. |
| | STALL,J.A. , Florida Power & Light Co. |
| | RECIP.NAME RECIPIENT AFFILIATION |
|
| |
|
| ==SUBJECT:== | | ==SUBJECT:== |
| LER99-004-00:on 990912,noted thatMSSVsurveillance wasoutsideofTSrequirements.
| | LER 99-004-00:on 990912,noted that MSSV surveillance was outside of TS requirements. Caused by setpoint drift. Subject MSSVs are being refurbished & retested prior to unit startup from SLl-16 refueling outage. With 991007 ltr. |
| Causedbysetpointdrift.SubjectMSSVsarebeingrefurbished
| | DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR I ENCL I SIZE: |
| &retestedpriortounitstartupfromSLl-16refueling outage.With991007ltr.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:LTR IENCLISIZE:TITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:'ECIPXENT IDCODE/NAME LPD2-2INTERNAL: | | TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc. |
| ACRSNRR/DIPM/IOLB NRR/DSSA/SPLB RES/DRY/OERAB COPIESLTTRENCL1111111111RECIPIENT IDCODE/NAME GLEAVES,W NRR/DRXP/REXB RES/DET/ERAB RGN2FILE01'OPIESLTTRENCL1111111111EXTERNAL:
| | NOTES: |
| LSTLOBBYWARDNOACPOORE,W.NRCPDR111111LMXTCOMARSHALLNOACQUEENER,DS NUDOCSFULLTXT111111NOTETOALL"RIDS"RECIPIENTS:
| | 'ECIPXENT COPIES RECIPIENT 'OPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL LPD2-2 1 1 GLEAVES,W 1 1 INTERNAL: ACRS 1 1 1 1 NRR/DIPM/IOLB 1 1 NRR/DRXP/REXB 1 1 NRR/DSSA/SPLB 1 1 RES/DET/ERAB 1 1 RES/DRY/OERAB 1 1 RGN2 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LMXTCO MARSHALL 1 1 NOAC POORE,W. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS: |
| PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATION REMOVEDFROMDISTRIBUTION LISTORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION, CONTACTTHEDOCUMENTDESK(DCD)ONEXTENSION 415-2083TDOCUMENTCONTRCFULLTEXTCONVERSION REQUIREDTOTAL,NUMBEROFCOPIESREQUIRED:
| | PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR REMOVED FROM DISTRIBUTION LIST DESK (DCD) ON EXTENSION 415-2083 ORGANIZATION, CONTACT T THE DOCUMENT CONTRC FULL TEXT CONVERSION REQUIRED TOTAL, NUMBER OF COPIES REQUIRED: LTTR 16 ENCL 16 |
| LTTR16ENCL16 FloridaPowerStLightCompany,6351S.OceanDrive,JensenBeach,FL34957FPLOctober7,1999L-99-21910CFR$50.73U.S.NuclearRegulatory Commission Attn:DocumentControlDeskWashington, D.C.20555Re:St.LucieUnit1DocketNo.50-335Reportable Event:1999-004-00 DateofEvent:September 12,1999MainSteamSafetyValvesSurveillance OutsideTechnical Secification Reuirements TheattachedLicenseeEventReport1999-004isbeingsubmitted pursuanttotherequirements of10CFRf50.73toprovidenotification ofthesubjectevent.Verytrulyyours,J.A.StallVicePresident St.LucieNuclearPlantJAS/EJW/KWF Attachment cc:RegionalAdministrator, USNRC,RegionIISeniorResidentInspector, USNRC,St.LucieNuclearPlant99i0140083 991007PDRADOCK05000335PDRanFPLGroupcompany NRCFORM366I6.1999)U.S.NUCLEARREGULATORY COMMISSION LICENSEEEVENTREPORT(LER)(Seereverseforrequirednumberofdigits/characters foreachblock)APPROVEDBYOMBNO.3160-0104 EXPIRES06/30/2001 Estimated burdenperresponsetocomplywiththismandatory information collection request:50hrs.Reportedlessonsteamedareincorporated intothelicensing processandfedbacktoindustry.
| |
| Forwardcommentsregarding burdenestimatetotheRecord.TAanagement Branch{TWF33),U.S.NuclearRegulatory Commission, Washington, Dc205554001, andtothePapenvork Reduction Project(31504104j, OfficeofManagement andBudget,Washington, DC20503.Ifaninformation collection doesnotdisplayacurrently validOMBcontrolnumber,theNRCmaynotconductorsponsor,andapersonisnotrequiredtorespondto,theInformation collection.
| |
| FACILITYNAME(1)St.LucieUnit1DOCKETNUMBER(2)05000335PAGE(3)Page1of5TITLE(4)MainSteamSafetyValvesSurveillance OutsideTechnical Specification'equirements MONTHDAYYEAREVENTDATE(6)LERNUMBER(6)YEARSEQUENTIAL REVISIONNUMBERNUMBERREPORTDATE(7)MONTHDAYFACIUTYNAMEOTHERFACILITIES INVOLVED(8)DOCKETNUMBER091219991999-004-0010071999FACIUTYNAMEDOCKETNUMBEROPERATING MODE(9)POWERLEVEL{10)07020.2201(b)20.2203(a)
| |
| {1)20.2203(a)(2)
| |
| (i),20.2203(a)(2)(v) 20.2203(a)(3){I)20.2203{a)
| |
| (3)(ii)X50.73(a)(2)(i) 50.73(a)(2)(ii)50.73(a)(2)(iii)THISREPORTISSUBMITTEDPURSUANTTOTHEREQUIREMENTS OF10CFR5:(Chockonoormore)(11)50.73{a)(2)(viii) 50.73(a)(2)(x)73.7120.2203{a)
| |
| (2)(ii)20.2203(a)
| |
| (2)(iii)20.2203(a)
| |
| {2)(iv)20.2203(a)
| |
| (4)50.36(c){1) 50.36(c)(2)50.73(a){2)(iv)50.73(a)(2)
| |
| (v)50.73(a)(2){vii)OTHERSpecifyInAbstractbeloworinNRCForm366ANAMELICENSEECONTACTFORTHISLER{12)TELEPHONE NUMBERunaludaAraaCoda)KennethW.Frehafer, Licensing Engineer(561)467-7748COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT13)CAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE ToEPIXCAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE ToEPIXSUPPLEMENTAL REPORTEXPECTED(14)YES(tfyes,c'omplete EXPECTEDSUBMISSION DATE).XNoEXPECTED,SUBMISSION DATE(16)MONTHDAYABSTRACT/Limitto1400spaces,i.e.,approximately 15singlewpaced typewritten lines/(16)OnSeptember 12,1999,St.LucieUnit1wasinMode1andholdingat.approximately 70percentreactorpowerfortesting'f themainsteamsafetyvalves(MSSVs)inaccordance withproceduze 1-MSP-08.07, "MainSteamSa'fetySetpointSurveillance."
| |
| ThreetrainAandonetrainBMSSVsliftedlow,outsideoftherequiredTechnical Specification pressuresetpointrangeof+/-1percent.Priortotesting,thereactortripsetpoints werereducedtoallowcontinued operation withtwoMSSVspertrainoutofservice.ThesetpressureofoneofthetrainAMSSVswasresettoallowcontinued operation.
| |
| TheapparentcauseoftheMSSVsurveillance failureswassetpointdrift.PerASMEcodeconsiderations, aformalrootcauseisnotrequired.
| |
| Thesafetysignificance ofthelowas-foundMSSVsetpoints wasevaluated andfoundtobeinsignificant.
| |
| ThesubjectMSSVsarebeingrefurbished andretestedpriortounitstartupfromtheSL1-16refueling outage.FPLisconsidering whetherachangetotheSt.LucieTechnical Specifications orTSbasesisappropriate toaddressthedifferences betweenNUREG-1432 andtheSt.~LucieTechnical Specifications concerning as-foundandas-leftsafetyreliefsetpoints.
| |
| NRCFORM3BBIB.1999)
| |
| NRCFORM366A(6-1998)LlCENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)St.LucieUnit1DOCKETNUMBER(2)05000335LERNUMBER(6)SEQUENTIAL REVISIONNUMBERNUMBER1999-004-00PAGE(3)Page2of5TEXT(Ifmorespaceisreriuired, useadditional copiesofIVRCForm366A)(17)Description oftheEventOnSeptember 12,1999,St.LucieUnit1wasinMode1andholdingatapproximately 70percentreactorpowerfortestingofthemainsteamsafetyvalves(MSSVs)(EIIS)SB)RV) duringthedownpowex fortheSL1-16refueling outage.Thefollowing MSSVsliftedoutsideoftheirTechnical Specifications (TS)requiredpressurerange.Additionally V8213liftedoutsideofthe+/-3%ASMEcodeallowedrangeby0.6psiglow.Thissurveillance testingoftheMSSVs'etpoints wasperformed inaccordance withprocedure 1-HSP-08.07, "HainSteamSafetySetpointSurveillance."
| |
| ValveSepointV8201V8202V8211V8213TrainMeasuredLiftPressure(psia)986.9982.91025.51008.7TSLimit1000+/-1%1000+/-1()1040+/-1()1040+/-1'hDeviation FromTSLimit(())1'1-1071-1.45-3013MSSVsV8201,V8211,and,V8213 wereleftinoperable andoutofserviceatthecompletion oftesting.V8202wasrestoredtoOPERABLEstatsbysetpointadjustment withintheactiontimeofTechnical Specification 3.7.1.1.PriortotestingtheMSSVs,thereactortripsetpoints hadbeenreducedtoallowcontinued operation withtwoMSSVspertrainoutofservicepexworkordex(WO)98023939-02.
| |
| Nomorethantwovalvespertrainwereoutofserviceandthereactortripsetpoints wereproperlyadjustedinaccordance withTe'chnical Specification 3.7'.1,therefore therewerenooperability concerns.
| |
| CauseoftheEventTheas-foundsetpressuredeviations wererelatively minorandsimilartothosefoundinpastcycles.Theapparentcauseissetpointdriftand/ortheuseofthenewtestmethods.Asdescribed below,aformalrootcauseisnotrequiredbyASME/ANSI OM-1987,partl.PerASME/ANSI OM-1'tt1.3.3.1(e)(2) andCodeInterpretation 92-8,aClass1pressurereliefvalvewithanas-foundsetpointoutsidetheacceptance rangeofthesetpointontheminussideisnotconsidered afailure.Asaconsequence, additi.onal testingforvalvesfailingoutsidethenegativeacceptance criteriaisnotrequiredbytheASMECode.FPLqualityinstruction (QI)11-PR/PSL-7, "ControlofCodeSafetyandReliefValves,"containsadditional criteriawithin95.5.3thatgenerally requiresadditional testingforvalvesfailingthenegativetolerance criteria.
| |
| TheQIcriteriaarebasedontheadversesystemfunctional issuesresulting fromreliefvalveseatleakageandpremature lift.However,pertheQI,thecriteriaforadditional testingofvalvesfaili.ngthenegativetolerance acceptance criteriamaybewaivedoralteredbasedonanevaluation oftheas-foundtestpressure, valveinspection, systemrequirements andhistori.cal records.Theexpansion oftestingscopeduetothefailureofV8213waswaivedbasedonthesmallamountofdeviation (3.13%vs.3%),theacceptable resultsoftheother'alve testswithrespecttoASMENRCFORM388A18.1898)
| |
|
| |
|
| NRCFORM366AI6-1888)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.NUCLEARREGULATORY COMMISSION FACILITYNAME(1)St.LucieUnit1DOCKETNUMBER(2)05000335LERNUMBER(6)SEQUENTIAL REVISIONNUMBERNUMBER1999-004-00PAGE(3)Page3of5TEXTllfmorespecsisrequired, useadditionelcopiesofNRCForm366A)(17)CauseoftheEvent(cont'd)criteria, theabsenceofrecentproblemswithMSSVseatleakageandpremature lift,andtheinsignificant effectofasmallnegativesetpressuredeviation inahighbankMSSVreliefvalve.TheMSSVsarebeingrefurbished andretested.
| | Florida Power St Light Company, 6351 S. Ocean Drive, Jensen Beach, FL 34957 October 7, 1999 FPL L-99-219 10 CFR $ 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Re: St. Lucie Unit 1 Docket No. 50-335 Reportable Event: 1999-004-00 Date of Event: September 12, 1999 Main Steam Safety Valves Surveillance Outside Technical S ecification Re uirements The attached Licensee Event Report 1999-004 is being submitted pursuant to the requirements of f |
| AnalysisoftheEventThiseventisreportable under10CFR50.72(a)(2)(i)(B)as"anyoperation orcondition prohibited theplant'sTechnical Specifications."
| | 10 CFR 50.73 to provide notification of the subject event. |
| TheSt.LucieUnit1Technical Specifications differfromNUREG-1432r "Standard Technical Specification Combustion Engineering Plants,"inthatanas-foundMSSVsetpointtolerance isnotincludedintheSt.LucieTechnical Specifications.
| | Very truly yours, J. A. Stall Vice President St. Lucie Nuclear Plant JAS/EJW/KWF Attachment cc: Regional Administrator, USNRC, Region II Senior Resident Inspector, USNRC, St. Lucie Nuclear Plant 99i0140083 991007 05000335 PDR ADOCK PDR an FPL Group company |
| FPLisconsidering whetherachangetotheSt.LucieTechnical Specifications ozTSbasesisappropriate toaddressthisTechnical Specification difference.
| |
| AnalysisofSafetySignificance TheMSSVsmustopentoprovideoverpressure protection forthesteamgenerators andreliefcapacitytoremovedecayheat.TheMSSVsareclassified asSafety-Related, QualityGroupBcomponents.
| |
| PerTStable3.7-1themaximumallowable powerlevelhightripsetpointwithtwoinoperable steamlinesafetyvalvesoneitheroperating steamgenerator is79.8%EffectonSafetAnalsesValvesV8201,V8202,V8211andV8213liftedoutsidetheTSliftsettingtolerance limitof+/-1percent.However,theseliftsettingfailuresweregreaterthanthe-1percentlimit.ValvesV8205andV8216liftedwithinthetolerance limitspecified intheTS.Itwillbeassumedforthepurposeofthisevaluation*
| |
| thatalltheremaining valveswouldhaveliftedwithintheirtolerance limits.TheonlyFSARanalyzedeventsthatcouldpotentially beaffectedbythedeviations intheMSSVsetpoints arethelossofexterhalload(LOEL)andthesmallbreak,LOCA(SBLOCA).
| |
| Theloss.ofexternalloadevent,including thecaseofinoperable MSSVs,reliesontheMSSVstoreleasethesystemenergysoastopreventtheprimaryandthesecondary sidepressures fromexceeding theoverpzessurization criteria.
| |
| Theanalysisofthiseventassumesconservatively thattheMSSVsbegintoopenattheTSallowedmaximumliftpressurecorresponding toatolerance of+1percent.Openingofthevalvesatapressurelowerthanthatassumedinthesafetyanalysiswouldbebeneficial forthistransient andtheresultswouldremainboundedbytheFSARresults.IntheanalysisofthesmallbreakLOCAevent,itis-assumedthattheMSSVsbegintoopenataliftpressurecorresponding toatolerance of+3percent.Theas-foundsetpressures therefore would,nothaveanyadverse'impactonthesmallbreakLOCAanalysisresults,aspresented intheFSAR.OtherFSAReventsincluding thesteamgenerator tuberupture(SGTR)eventarenotimpactedbythevariations intheMSSVliftpressure.
| |
| TheSGTReventanalyzedintheFSARconservatively assumestheopeningoftheatmospheric dumpvalves(ADVs)toNRCFORM3BBA(6-1888)
| |
|
| |
|
| NRCFORM366AIs-1998)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S.I'IUCLEAR REGULATORY COMMISSION FACILITYNAME(1)St.LucieUnit1DOCKETNUMBER(2)05000335LERNUMBER(6)SEQUENTIAL REVISIONNUMBERNUMBER1999-004-00PAGE(3)Page4of5TEXT(Ifmorespeceisrequired, useedditionelcopiesofNRCForm366AJ(17)AnalysisofSafetySignificance (cont'd)releasethesteamfromtherupturedsteamgenerators.
| | NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3160-0104 EXPIRES 06/30/2001 I6.1999) |
| Theidentified MSSVs'etpoint pressuredeviations thuswouldnotimpacttheFSARconclusions forthisevent.'heopeningofMSSVsatpressures lowerthantheliftpressurecorzesponding to-1percenttolerance isthusdetermined to'havenoadverseimpactonthesafetyanalysis, including deviations outside-3.percent.
| | Estimated burden per response to comply with this mandatory information collection request: 50 hrs. Reported lessons teamed are incorporated into the licensing process and fed back to industry. Forward comments regarding LICENSEE EVENT REPORT (LER) burden estimate to the Record. TAanagement Branch {TW F33), U.S. Nuclear Regulatory Commission, Washington, Dc 205554001, and to the Papenvork Reduction Project (31504104j, Office of Management and Budget, (See reverse for required number of Washington, DC 20503. If an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, digits/characters for each block) and a person is not required to respond to, the Information collection. |
| Amuchlowernegativevalve'tolerance limit,althoughacceptable fromsafetyanalysisconsiderations, mayhaveoperational impactasthemargintooperating pressuregetsreduced.TheMSSVs's-found setpressurevalues(specified above)wereoutsidethetolerance limitsspecified intheSt.LucieUnit1Technical Specification 3.7.1.1.Thisdegradedcondition howeverdidnotcompromise plantsafety.Theevaluation performed usingtheas-foundsetpoints concludes that,Cycle15operation hadremainedwithinthedesignbasisoftheplantforallanalyzedFSARevents.Nosafetycriteriawouldhavebeenviolatedduetotheidentified condition oftheMSSVs.SeointDriftConsiderations ThebelowchartshowstheMSSVtestsinthelast3cyclesforunit1.Not'allofthevalvesweretestedduringthesecycles.TheAs-Found()Failurecolumnisshownforthecyclesthatwereevaluated.
| | FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3) |
| Theyrepresent thepercentage fromnameplate setpointthatthevalvewasoutoftolerance.
| | St. Lucie Unit 1 05000335 Page 1 of 5 TITLE (4) |
| Thenoneinthecolumnmeans,thatthetestwassatisfactory.
| | Main Steam Safety Valves Surveillance Outside Technical Specification'equirements EVENT DATE (6) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) |
| ThepercentDriftbetweenCycles.columnisthepercentage changethatthevalveexperienced overonecycletakenfromthe2"eas-leftsetpointtestandthenextas-foundtestofthevalve.IValveS/NUnit1N55128-00-0001 N55128-00-0002 N55128-00-0003 N55128-00-0004 N55128-00-0005 N55128-00-0006 N55128-00-0007 N55128-00-0008 N55128-00-0009 N55128-00-0010 N55128-00-0011 N55128-00-0011 N55128-00-0012 N55128-00-0013 N55128-00-0014 N55128-00-0015 N55128-00-0016 Date19961996199619961996199619961996-199619961995199919961996199619961996As-Pound%'ailurenonenone1.4none-1.52~1.831.932.54nonenonenone-1.45none1.951.271.17noneDate1999199919971999199719971997199619971999199719971999As-Pound%Pailure-1.71-1.31-1.03none1.62nonenone1.37none-3.13nonenonenone%Driftbetweencles-1.62-1.93-1.12-0.201.52-.50-.191.17-2.13-~68-3.50-1.35.10-0.87 NRCFORM366A(8-1998)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION U.S:NUCLEARREGULATORY COMMISSION FACILITYNAME{1)St.LucieUnit1DOCKETNUMBERI205000335LERNUMBERI6)SEQUENTIAL REVISIONNUMBERNUMBER1999-004-00PAGEI3)Page5of5TEXT(Ifmorespaceisrequired, useadditional copiesofNRCForm3MAJ(17)AnalysisofSafetySignificance (cont'd)ThesedataarefromtheReliefValveDatabase.
| | SEQUENTIAL REVISION FACIUTYNAME DOCKET NUMBER MONTH DAY YEAR YEAR MONTH DAY NUMBER NUMBER FACIUTYNAME DOCKET NUMBER 09 12 1999 1999 - 004 - 00 10 07 1999 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQ UIREMENTS OF 10 CFR 5: (Chock ono or more) (11) |
| Thisevaluation doesnottakeintoaccounttheinstrument inaccuracies orthedifference inreadingsbetween'the 1"and2""testsdonetoacceptthevalves.Thetestmethodology waschangedforUnit1forthe1999testing.Theplantstartedusingcomputeroperatedtestmachinevs.thepreviousmanualtestmethod.Bothtesttechniques usealiftingdevicebutthenewersystem'sramprateandsetpointinterpretation arelesssubjective andoperatordependent whichprovideformoreconsistent andaccuratereadings.
| | MODE (9) 20.2201 (b) , 20.2203(a)(2)(v) X 50.73(a)(2)(i) 50.73{a) (2)(viii) |
| FPLconcluded thatthereliefvalvessetpointdriftismostlyscattered datawithnodominanttrendingsetpointdriftforanyvalveoverthecyclesanalyzed.
| | POWER 20.2203(a) {1) 20.2203 (a) (3) {I) 50.73(a) (2)(ii) 50.73(a) (2)(x) |
| Therefore, thereisnoconcernpertaining tothedownwarddriftoftheMSSVsetpoints. | | LEVEL {10) 070 20.2203(a)(2) (i) 20.2203{a) (3)(ii) 50.73(a) (2)(iii) 73.71 20.2203{a) (2) (ii) 20.2203(a) (4) 50.73(a) {2)(iv) OTHER 20.2203(a) (2)(iii) 50.36(c){1) 50.73(a)(2) (v) Specify In Abstract below or 20.2203(a) {2)(iv) 50.36(c) (2) 50.73(a) (2) {vii) in NRC Form 366A LICENSEE CONTACT FOR THIS LER {12) |
| Basedontheabove,thiseventhadnoimpactonthehealthandsafetyofthepublic,Corrective Actions1.ThesubjectMSSVsarebeingrefurbished byWyleLabsviaWO98018487.
| | NAME TELEPHONE NUMBER unaluda Araa Coda) |
| 2.ThesubjectMSSVswillbereworkedandretestedperWO98018488. | | Kenneth W. Frehafer, Licensing Engineer (561) 467 7748 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13) |
| 3.FPLisconsidering achangetotheSt.LucieTechnical Specifications toaddressthedifferences betweenNUREG-1432 andtheSt.LucieTechnical Specifications concerning as-foundandas-leftsafetyreliefvalvesetpoints. | | CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE REPORTABLE To EPIX CAUSE SYSTEM COMPONENT MANUFACTURER To EPIX SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY EXPECTED YES SUBMISSION (tf yes, c'omplete EXPECTED SUBMISSION DATE). X No , |
| Additional Information FailedComonentsIdentified BasedonASMEcodeconsiderations, therewerenoMSSVtestfailures. | | DATE (16) |
| SimilarEventsLER50-389/1999-004-00 and50-389/1999-004-01, "AsFoundCycle10Pressurizer SafetyValveSetpoints OutsideTechnical Specification Limits,"wasissuedforUnit2pressurizer codesafetysurveillance failures.
| | ABSTRACT /Limit to 1400 spaces, i.e., approximately 15 singlewpaced typewritten lines/ (16) |
| NRCFORM3BBAIB.1898) r~}}
| | On September 12, 1999, St. Lucie Unit 1 was in Mode 1 and holding at. approximately 70 percent reactor power for testing'f the main steam safety valves (MSSVs) in accordance with proceduze 1-MSP-08.07, "Main Steam Sa'fety Setpoint Surveillance." |
| | Three train A and one train B MSSVs lifted low, outside of the required Technical Specification pressure setpoint range of +/- 1 percent. Prior to testing, the reactor trip setpoints were reduced to allow continued operation with two MSSVs per train out of service. The set pressure of one of the train A MSSVs was reset to allow continued operation. |
| | The apparent cause of the MSSV surveillance failures was setpoint drift. Per ASME code considerations, a formal root cause is not required. The safety significance of the low as-found MSSV setpoints was evaluated and found to be insignificant. |
| | The subject MSSVs are being refurbished and retested prior to unit startup from the SL1-16 refueling outage. FPL is considering whether a change to the St. Lucie Technical Specifications or TS bases is appropriate to address the differences between NUREG-1432 and the St. Lucie Technical Specifications concerning as-found and as-left |
| | ~ |
| | safety relief setpoints. |
| | NRC FORM 3BB IB.1999) |
| | |
| | NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6-1998) |
| | LlCENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION DOCKET PAGE (3) |
| | FACILITY NAME (1) LER NUMBER (6) |
| | NUMBER (2) |
| | SEQUENTIAL REVISION NUMBER NUMBER St. Lucie Unit 1 05000335 004 - Page 2 of 5 1999 00 TEXT (Ifmore space is reriuired, use additional copies of IVRC Form 366A) (17) |
| | Description of the Event On September 12, 1999, St. Lucie Unit 1 was in Mode 1 and holding at approximately 70 percent reactor power for testing of the main steam safety valves (MSSVs) |
| | (EIIS)SB)RV) during the downpowex for the SL1-16 refueling outage. The following MSSVs lifted outside of their Technical Specifications (TS) required pressure range. |
| | Additionally V8213 lifted outside of the +/- 3% ASME code allowed range by 0.6 psig low. This surveillance testing of the MSSVs'etpoints was performed in accordance with procedure 1-HSP-08.07, "Hain Steam Safety Setpoint Surveillance." |
| | Measured Deviation Valve Train Lift TS Limit From TS Sepoint Pressure Limit (() ) |
| | (psia) |
| | V8201 986.9 1000 +/- 1% 1 '1 V8202 982. 9 1000 +/- 1() -1071 V8211 1025.5 1040 +/- 1() -1.45 V8213 1008.7 1040 +/- 1'h -3013 MSSVs V8201, V8211, and,V8213 were left inoperable and out of service at the completion of testing. V8202 was restored to OPERABLE stats by setpoint adjustment within the action time of Technical Specification 3.7.1.1. Prior to testing the MSSVs, the reactor trip setpoints had been reduced to allow continued operation with two MSSVs per train out of service pex work ordex (WO) 98023939-02. No more than two valves per train were out of service and the reactor trip setpoints were properly adjusted in accordance with Te'chnical Specification 3.7 '.1, therefore there were no operability concerns. |
| | Cause of the Event The as-found set pressure deviations were relatively minor and similar to those found in past cycles. The apparent cause is setpoint drift and/or the use of the new test methods. As described below, a formal root cause is not required by ASME/ANSI OM-1987, part l. |
| | Per ASME/ANSI OM-1 'tt1.3.3.1(e)(2) and Code Interpretation 92-8, a Class 1 pressure relief valve with an as-found setpoint outside the acceptance range of the setpoint on the minus side is not considered a failure. As a consequence, additi.onal testing for valves failing outside the negative acceptance criteria is not required by the ASME Code. FPL quality instruction (QI) 11-PR/PSL-7, "Control of Code Safety and Relief Valves," contains additional criteria within 95.5.3 that generally requires additional testing for valves failing the negative tolerance criteria. The QI criteria are based on the adverse system functional issues resulting from relief valve seat leakage and premature lift. However, per the QI, the criteria for additional testing of valves faili.ng the negative tolerance acceptance criteria may be waived or altered based on an evaluation of the as-found test pressure, valve inspection, system requirements and histori.cal records. The expansion of testing scope due to the failure of V8213 was waived based on the small amount of deviation (3.13% vs. 3%), the acceptable results of the other'alve tests with respect to ASME NRC FORM 388A 18.1898) |
| | |
| | NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION I 6-1 888) |
| | LICENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION DOCKET PAGE (3) |
| | FACILITY NAME (1) NUMBER (2) |
| | LER NUMBER (6) |
| | SEQUENTIAL REVISION NUMBER NUMBER St. Lucie Unit 1 05000335 Page 3 of 5 1999 004 00 TEXT llfmore specs is required, use addi tionel copies of NRC Form 366A ) (17) |
| | Cause of the Event (cont'd) criteria, the absence of recent problems with MSSV seat leakage and premature lift, and the insignificant effect of a small negative set pressure deviation in a high bank MSSV relief valve. The MSSVs are being refurbished and retested. |
| | Analysis of the Event This event is reportable under 10 CFR 50.72 (a) (2) (i) (B) as "any operation or condition prohibited the plant's Technical Specifications." The St. Lucie Unit 1 Technical Specifications differ from NUREG-1432r "Standard Technical Specification Combustion Engineering Plants," in that an as-found MSSV setpoint tolerance is not included in the St. Lucie Technical Specifications. |
| | FPL is considering whether a change to the St. Lucie Technical Specifications oz TS bases is appropriate to address this Technical Specification difference. |
| | Analysis of Safety Significance The MSSVs must open to provide overpressure protection for the steam generators and relief capacity to remove decay heat. The MSSVs are classified as Safety-Related, Quality Group B components. |
| | Per TS table 3.7-1 the maximum allowable power level high trip setpoint with two inoperable steam line safety valves on either operating steam generator is 79.8% |
| | Effect on Safet Anal ses Valves V8201, V8202, V8211 and V8213 lifted outside the TS limit of +/- 1 percent. However, these lift lift setting tolerance setting failures were greater than the |
| | -1 percent limit. Valves V8205 and V8216 lifted within the tolerance limit specified in the TS. It will be assumed for the purpose of this evaluation* that all the remaining valves would have lifted within their tolerance limits. |
| | The only FSAR analyzed events that could potentially be affected by the deviations in the MSSV setpoints are the loss of exterhal load (LOEL) and the small break, LOCA (SBLOCA). |
| | The loss. of external load event, including the case of inoperable MSSVs, relies on the MSSVs to release the system energy so as to prevent the primary and the secondary side pressures from exceeding the overpzessurization criteria. The analysis of this event assumes conservatively that the MSSVs begin to open at the TS allowed maximum lift pressure corresponding to a tolerance of + 1 percent. Opening of the valves at a pressure lower than that assumed in the safety analysis would be beneficial for this transient and the results would remain bounded by the FSAR results. |
| | In the analysis of the small break LOCA event, open at a lift it is- assumed that the MSSVs begin to pressure corresponding to a tolerance of + 3 percent. The as-found set pressures therefore would, not have any adverse 'impact on the small break LOCA analysis results, as presented in the FSAR. |
| | Other FSAR events including the steam generator tube rupture (SGTR) event are not impacted by the variations in the MSSV lift pressure. |
| | FSAR conservatively assumes the opening of the atmospheric dump valves (ADVs) to The SGTR event analyzed in the NRC FORM 3BBA (6-1888) |
| | |
| | NRC FORM 366A U.S. I'IUCLEAR REGULATORY COMMISSION Is-1998) |
| | LICENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) |
| | SEQUENTIAL REVISION NUMBER NUMBER St. Lucie Unit 1 05000335 Page 4 of 5 1999 004 00 TEXT (If more speceis required, use eddi tionel copies of NRC Form 366AJ (17) |
| | Analysis of Safety Significance (cont'd) release the steam from the ruptured steam generators. The identified MSSVs'etpoint pressure deviations thus would not impact the FSAR conclusions for this event. |
| | 'he opening of MSSVs at pressures lower than the lift pressure corzesponding to -1 percent tolerance is thus determined to'have no adverse impact on the safety analysis, including deviations outside -3.percent. A much lower negative valve |
| | 'tolerance limit, although acceptable from safety analysis considerations, may have operational impact as the margin to operating pressure gets reduced. |
| | The MSSVs's-found set pressure values (specified above) were outside the tolerance limits specified in the St. Lucie Unit 1 Technical Specification 3.7.1.1. This degraded condition however did not compromise plant safety. The evaluation performed using the as-found setpoints concludes that, Cycle 15 operation had remained within the design basis of the plant for all analyzed FSAR events. No safety criteria would have been violated due to the identified condition of the MSSVs. |
| | Se oint Drift Considerations The below chart shows the MSSV tests in the last 3 cycles for unit 1. Not'all of the valves were tested during these cycles. The As-Found () Failure column is shown for the cycles that were evaluated. They represent the percentage from nameplate setpoint that the valve was out of tolerance. The none in the column means, that the test was satisfactory. The percent Drift between Cycles .column is the percentage change that the valve experienced over one cycle taken from the 2"e as-left setpoint test and the next as-found test of the valve. I Valve S/N Unit Date As-Pound % |
| | Date As-Pound % % Drift between 1 |
| | 'ailure Pailure cles N55128-00-0001 1996 none 1999 -1.71 -1.62 N55128-00-0002 1996 none 1999 -1.31 -1.93 N55128-00-0003 1996 1.4 1997 -1.03 -1. 12 N55128-00-0004 1996 none N55128-00-0005 1996 -1.52 1999 none -0.20 N55128-00-0006 1996 ~ |
| | 1.83 1997 1.62 1.52 N55128-00-0007 1996 1.93 N55128-00-0008 1996- 2.54 N55128-00-0009 1996 none 1997 none -.50 N55128-00-0010 1996 none 1997 none -.19 N55128-00-0011 1995 none 1996 1.37 1. 17 N55128-00-0011 1999 -1.45 -2. 13 N55128-00-0012 1996 none 1997 none - 68 |
| | ~ |
| | N55128-00-0013 1996 1.95 1999 -3.13 -3.50 N55128-00-0014 1996 1.27 1997 none -1.35 N55128-00-0015 1996 1.17 1997 none .10 N55128-00-0016 1996 none 1999 none -0.87 |
| | |
| | NRC FORM 366A U.S: NUCLEAR REGULATORY COMMISSION (8-1998) |
| | LICENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION FACILITY NAME {1) DOCKET NUMBER I2 LER NUMBER I6) PAGE I3) |
| | SEQUENTIAL REVISION NUMBER NUMBER St. Lucie Unit 1 05000335 Page 5 of 5 1999 004 00 TEXT (Ifmore spaceis required, use additional copies of NRC Form 3MAJ (17) |
| | Analysis of Safety Significance (cont'd) |
| | These data are from the Relief Valve Database. This evaluation does not take into account the instrument inaccuracies or the difference in readings between'the 1" and 2"" tests done to accept the valves. |
| | The test methodology was changed for Unit 1 for the 1999 testing. The plant started using computer operated test machine vs. the previous manual test method. Both test techniques use a lifting device but the newer system's ramp rate and setpoint interpretation are less subjective and operator dependent which provide for more consistent and accurate readings. |
| | FPL concluded that the relief valves setpoint drift is mostly scattered data with no dominant trending setpoint drift for any valve over the cycles analyzed. Therefore, there is no concern pertaining to the downward drift of the MSSV setpoints. |
| | Based on the above, this event had no impact on the health and safety of the public, Corrective Actions |
| | : 1. The subject MSSVs are being refurbished by Wyle Labs via WO 98018487. |
| | : 2. The subject MSSVs will be reworked and retested per WO 98018488. |
| | : 3. FPL is considering a change to the St. Lucie Technical Specifications to address the differences between NUREG-1432 and the St. Lucie Technical Specifications concerning as-found and as-left safety relief valve setpoints. |
| | Additional Information Failed Com onents Identified Based on ASME code considerations, there were no MSSV test failures. |
| | Similar Events LER 50-389/1999-004-00 and 50-389/1999-004-01, "As Found Cycle 10 Pressurizer Safety Valve Setpoints Outside Technical Specification Limits, " was issued for Unit 2 pressurizer code safety surveillance failures. |
| | NRC FORM 3BBA IB.1898) |
| | |
| | r |
| | ~}} |
|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17241A4891999-10-0707 October 1999 LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr ML17241A4111999-07-16016 July 1999 LER 99-007-00:on 990610,unplanned Cooldown Transient Occurred Due to Personnel Error.Trained & Briefed Personnel & Revised Procedures.With 990716 Ltr ML17241A4031999-07-0606 July 1999 LER 99-006-00:on 990605,sub-critical Reactor Trip Occurred Due to Inadvertent MSIV Opening.Caused by Personnel Error. Provided Operation Supervision Instruction to Operating Crews,Stand Down Meetings & Operator Aids.With 990706 Ltr ML17241A4041999-07-0606 July 1999 LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr ML17241A3941999-06-30030 June 1999 LER 99-004-01:on 990415,as Found Cycle 10 Psv Setpoints Were Outside TS Limits.Caused by Manufacturing Process Defect. All Three Psvs Were Replaced with pre-tested Valves During Cycle 11 Refueling Outage.With 990630 Ltr ML17241A3551999-06-0404 June 1999 LER 99-002-00:on 990505,both Trains of Safety Injection Actuation Were Blocked During Surveillance.Caused by Procedure Error.Procedure Revised.With 990604 Ltr ML17241A3321999-05-17017 May 1999 LER 99-004-00:on 990415,determined That as Found Cycle 10 Psv Setpoints Outside TS Limits.Root Cause Under Investigation.Psvs Replaced with pe-tested Valves During Cycle 11 ML17241A3271999-05-0606 May 1999 LER 99-003-00:on 990406,ECCS Suction Header Leak Resulted in Both ECCS Trains Being Inoperable & Entry Into TS 3.0.3. Caused by Chloride Induced OD Stress Corrosion Cracking of Piping.Made Code Repairs & Coated Piping.With 990506 Ltr ML17229B0791999-04-0707 April 1999 LER 99-001-00:on 990309,discovered Inadequate Design & IST SRs for Iodine Removal Sys (Irs).Caused by Original Design Inadequacies & Personnel Error.Naoh Tank Vent Valve V07233 Was Tagged Open.With 990407 Ltr ML17229B0801999-04-0707 April 1999 LER 99-002-00:on 990311,SG ECT Error Caused Operation with Condition Prohibited by Ts.Caused by Deficiencies in Data Analysis Guideline Instructions.Licensee Will Change Data Analysis Guidelines for Lead Analysts.With 990407 Ltr ML17229B0541999-03-10010 March 1999 LER 99-001-00:on 990211,inadequate TS SRs for SIT & SDC Isolation Valves Were Noted.Caused by Failure to Correctly Implement TS Srs.Submitted LAR to Align Required TS SR with Design Bases Requirements Being Verified.With 990310 Ltr ML17229A9901999-01-20020 January 1999 LER 98-009-00:on 981223,noted That Facility Operated Outside of Design Basis.Caused by non-conservative MSLB Analysis Inputs.Will Review SR Component Differences Between Units & Will re-baseline LTOP Analysis.With 990120 Ltr ML17229A9821999-01-0404 January 1999 LER 98-010-00:on 981207,RCS Boron Sample Frequency Required by Ts,Was Exceeded by Twelve Minutes.Caused by Personnel Error.Equipment Clearance Order Was Lifted to Draw Required Sample & Operations Procedure Was Changed.With 990104 Ltr ML17229A9611998-12-22022 December 1998 LER 97-002-01:on 981204,containment Sump Debris Screen Was Not IAW Design.Caused by Inadequate C/As for Sump Screen Anamolies.All Identified Sump Screen Deficiencies Were Dispositioned &/Or Repaired.With 981222 Ltr ML17229A9561998-12-15015 December 1998 LER 98-008-00:on 981118,missed TS SG U Tube Insp.Caused by Encoding Errors While Using Remote Positioning Fixtures.All SG Tube Surveyed.With 981215 Ltr ML17229A9301998-11-25025 November 1998 LER 98-005-01:on 980807,discovered That New MOV Methodology Caused Past PORV Block Valve Operability Problem.Caused by Inadequacies in Original Vendor MOV Methodology.Planned Valve Mods Will Be Implemented During Cycle 11 1998 Outage ML17229A9021998-11-0404 November 1998 LER 98-008-00:on 981008,inadequate Reactor Protection Sys Trip Bypass TS Was Noted.Caused by Poorly Worded Ts. Submitted LAR to Clarify Power Requirements for High Rate of Power Trips.With 981104 Ltr ML17229A8771998-10-14014 October 1998 LER 98-006-00:on 980918,inadvertent Afas Actuation Was Noted.Caused by Degradation of Multiple Afas Power Supplies. Replaced Afas Power Supplies & Revised Procedures.With 981014 Ltr ML17229A8761998-10-14014 October 1998 LER 98-007-00:on 980918,identified Discrepancies Between Fire Protection Design Requirements & Field Conditions. Caused by Inadequate Translation & Implementation of Fire Protection Requirements.Procedures Revised.With 981014 Ltr ML17229A8511998-09-0202 September 1998 LER 98-005-00:on 980807,discovered That PORV Margins Were Insufficient to Accommodate Addl Conservatism.Caused by Inadequacies in Original Vendor MOV Methodology.Will Implement Planned Valve Actuator mods.W/980902 Ltr ML17229A8201998-07-29029 July 1998 LER 98-007-00:on 980630,inadequate Procedure May Have Resulted in SBO Recovery Complications.Caused by Inadequate Procedures.Attached Caution Tags to Appropriate Control switches.W/980729 Ltr ML17229A7411998-05-28028 May 1998 LER 98-004-00:on 980430,discovered Waste Gas Decay Tank Operation W/O Available Oxygen Analyzers,Which Is Prohibited by Ts.Caused by Inadequate Licensee Review of License Amend. Oxygen Analyzer recalibrated.W/980528 Ltr ML17229A7381998-05-21021 May 1998 LER 98-006-00:on 980421,missed EDG Fuel Oil Sample Surveillance Was Noted.Caused by Personnel Error.Revised Fuel Oil Sampling Service Purchase Order & Revised Site procedure.W/980521 Ltr ML17229A7011998-04-27027 April 1998 LER 98-003-00:on 980326,discovered Containment Pressure Instrumentation Design Single Failure Vulnerability.Caused by Inadequate Design by Personnel Error.Removed RPS & ESFAS Containment Pressure Bypass Keys immediately.W/980427 Ltr ML17229A6761998-04-0202 April 1998 LER 98-005-00:on 980305,identified Two Conditions That Were Outside App R Design Bases.Caused by Design Oversight During Development of Original App R Safe SD Design.Established 30 Minute Roving Fire Watches & Provided training.W/980402 Ltr ML17229A6731998-03-26026 March 1998 LER 98-002-00:on 980224,radiation Monitor Surveillance Inadequacies Led to Operating of Facility Prohibited by Tss. Caused by Congnitive Personnel Error.Permanent Procedure Changes Were implemented.W/980326 Ltr ML17229A6551998-03-0505 March 1998 LER 98-001-00:on 980206,high/low Pressure Shutdown Cooling Interface Was Noted Outside App R Design Bases.Caused by Personnel Error.Addl Guidance Was Provided to Engineering Dept personnel.W/980305 Ltr ML17229A6281998-02-19019 February 1998 LER 98-004-00:on 980121,emergency Lighting Outside App R Design Bases Occurred.Caused by Congnitive Personnel Error During Translation of App R Section Iii.Procedures Onop 1 & 2 ONP-100.01 Were Issued for Use on 980206.W/980219 Ltr ML17229A6211998-02-0909 February 1998 LER 98-003-00:on 980110,manual Rt Due to DEH Leak at Turbine Test Block Was Noted.Caused by o-ring Extrusion.Shortened Bolts by About 0.125 & Reinstalled at Correct Torque values.W/980209 Ltr ML17229A6191998-02-0404 February 1998 LER 98-002-00:on 980105,CIS Bistable in Bypass Resulted in Condition Prohibited by Tss.Caused by Personnel Error. Radiation Monitor Was Restored to service.W/980204 Ltr ML17229A6161998-02-0303 February 1998 LER 98-001-00:on 980104,inadvertent RPS Actuation Occurred Due to Personnel Error.Caused by Procedural Inadequacies & Inadequate self-checking by Licensed Utility Personnel. Placards Have Been Placed in CRs.W/980203 Ltr ML17229A6051998-01-27027 January 1998 LER 97-010-01:on 971027,inadvertent Core Alteration Prohibited by TSs Were Noted Due to Stuck Cea.Caused by Personnel Error.Cea #24 Was Dislodged & Transferred to Spent Pool for insp.W/980127 Ltr ML17229A5501997-12-0505 December 1997 LER 97-008-00:on 971107,inadequate CR Ventilation Surveillance Resulted in Condition Prohibited by Ts.Caused by non-cognitive Personnel Error.Operating Procedure 2-1900050 Was revised.W/971205 Ltr ML17309A9091997-12-0202 December 1997 LER 97-011-00:on 971102,non-conservative RAS Set Point Resulted in Operation Prohibited by Ts.Caused by Inadequate Set Point & Instrument Loop Scaling Process.Revised ESFAS Functional Tp W/Proper Set point.W/971202 Ltr ML17229A5391997-11-26026 November 1997 LER 97-010-00:on 971027,inadvertant Core Alteration Prohibited by TS Occurred.Caused by CEA Failure to Detach from Ugs.Safety Evaluation Was Performed & Procedural Rev Made to Continue Upper Guide Structure move.W/971126 Ltr ML17229A5151997-11-0707 November 1997 LER 97-007-00:on 971008,inoperable Containment Cooling Fan Resulted in Operation of Facility Outside Design Basis. Caused by non-cognitive Personnel Error.Ccs Operation Was Revised & Issued on 971013.W/971107 Ltr ML17229A4991997-10-17017 October 1997 LER 97-009-00:on 970917,inoperable PORV Block Valve Resulted in Operation Prohibited by Tech Specs Occurred.Caused by Plant GL 89-10 Program Plan to Review Plant Manager Action Item Sys.Porv Block Valve V-1403 restored.W/971017 Ltr ML17309A9011997-08-27027 August 1997 LER 97-008-00:on 970728,mechanical Fire Penetrations Were Inoperable & Outside App R Design Bases.Caused by Seal Mfg Not Providing Formal Documentation for Installed Seals. Modified Inoperable Fire penetrations.W/970827 Ltr ML17229A4311997-07-29029 July 1997 LER 97-006-00:on 970630,discovered Inadequate Testing of Engineered Safety Features Subgroup Relays.Caused by Inadequacy in Implementing TS Requirements in Surveillance Procedures.Revised Surveillance procedures.W/970729 Ltr ML17229A4241997-07-25025 July 1997 LER 97-005-00:on 970625,discovered That Hot Shutdown Control Panel Shutdown Cooling Flow indicator,FI-3306 Inoperable. Caused by Weakness in Work Order & Procedure Used to Repair FI-3306.Section Meeting W/I&C Planners held.W/970725 Ltr ML17229A3971997-07-11011 July 1997 LER 97-004-00:on 970611,discovered Incorrect Original Cable Tray Fire Stop Assembly Installation Was Outside App R Design Basis.Caused by Personnel Error.Hourly Fire Watch Patrols Will Be posted.W/970711 Ltr ML17229A3871997-06-19019 June 1997 LER 97-003-00:on 970521,determined Required Post Maint Open Stroke Test for Valve V3245,2B2 SIT Discharge Check Valve, Had Not Been Performed.Caused by Personnel Error.Procedure revised.W/970619 Ltr ML17229A3841997-06-17017 June 1997 LER 97-002-00:on 970518,containment Sump Debris Screen Was Not IAW Design Due to Gaps in Screen Encl.Performed SER to Document Containment Sump Design requirements.W/970617 Ltr ML17229A3751997-06-0202 June 1997 LER 97-006-00:on 970501,operation Was Prohibited by TS Due to Inadequately Tested Degraded Voltage Sys.Revised Unit 1 ESFAS Surveillance Test procedure.W/970602 Ltr ML17229A3611997-05-29029 May 1997 LER 97-007-00:on 970502,reactor Coolant Pump Oil Collection Sys Was Outside App R Design Bases.Identified Leak Sites Were Repaired & Mods to RCP Oil Collection Sys to Capture Any Future Leakage from areas.W/970529 Ltr ML17229A3491997-05-21021 May 1997 LER 97-001-00:on 970423,containment Isolation Actuation Occurred.Caused by Increased Radiation Levels During Removal of Upper Guide Structure.Proper Actuation of Containment Isolation Components Was verified.W/970521 Ltr ML17229A3441997-05-13013 May 1997 LER 97-005-00:on 970419,reactor Was Shutdown Due to Reactor Coolant Pressure Boundary Leakage.Hot Cracking Was Caused by Weld Contamination.Repairs to RCPB Were Completed & 1A SDC Train Was Restored to Svc ML17229A3141997-04-30030 April 1997 LER 97-004-00:on 970402,refueling Machine Was Operating in Manner Prohibited by TS Due to Original Design of Refueling Machine Bypass Feature Conflicting W/Ts Requirements. Eliminated Overload Cut Off Limit bypass.W/970430 Ltr ML17229A2951997-03-31031 March 1997 LER 97-003-00:on 970304,automatic Rt Resulted from Loss of Electrical Power to 1A2 Rc Pump.Rcp Breaker Was Replaced & Pump Was Returned to svc.W/970331 Ltr ML17229A2721997-03-21021 March 1997 LER 97-002-00:on 970221,operation in Excess of Max Rated Thermal Power Occurred Due to Digital Data Processing Sys (Ddps) Calorimetric Error.Verified Acceptable Performance of Ddps Functions & Reviewed Software mods.W/970321 Ltr 1999-07-06
[Table view] Category:RO)
MONTHYEARML17241A4891999-10-0707 October 1999 LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr ML17241A4111999-07-16016 July 1999 LER 99-007-00:on 990610,unplanned Cooldown Transient Occurred Due to Personnel Error.Trained & Briefed Personnel & Revised Procedures.With 990716 Ltr ML17241A4031999-07-0606 July 1999 LER 99-006-00:on 990605,sub-critical Reactor Trip Occurred Due to Inadvertent MSIV Opening.Caused by Personnel Error. Provided Operation Supervision Instruction to Operating Crews,Stand Down Meetings & Operator Aids.With 990706 Ltr ML17241A4041999-07-0606 July 1999 LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr ML17241A3941999-06-30030 June 1999 LER 99-004-01:on 990415,as Found Cycle 10 Psv Setpoints Were Outside TS Limits.Caused by Manufacturing Process Defect. All Three Psvs Were Replaced with pre-tested Valves During Cycle 11 Refueling Outage.With 990630 Ltr ML17241A3551999-06-0404 June 1999 LER 99-002-00:on 990505,both Trains of Safety Injection Actuation Were Blocked During Surveillance.Caused by Procedure Error.Procedure Revised.With 990604 Ltr ML17241A3321999-05-17017 May 1999 LER 99-004-00:on 990415,determined That as Found Cycle 10 Psv Setpoints Outside TS Limits.Root Cause Under Investigation.Psvs Replaced with pe-tested Valves During Cycle 11 ML17241A3271999-05-0606 May 1999 LER 99-003-00:on 990406,ECCS Suction Header Leak Resulted in Both ECCS Trains Being Inoperable & Entry Into TS 3.0.3. Caused by Chloride Induced OD Stress Corrosion Cracking of Piping.Made Code Repairs & Coated Piping.With 990506 Ltr ML17229B0791999-04-0707 April 1999 LER 99-001-00:on 990309,discovered Inadequate Design & IST SRs for Iodine Removal Sys (Irs).Caused by Original Design Inadequacies & Personnel Error.Naoh Tank Vent Valve V07233 Was Tagged Open.With 990407 Ltr ML17229B0801999-04-0707 April 1999 LER 99-002-00:on 990311,SG ECT Error Caused Operation with Condition Prohibited by Ts.Caused by Deficiencies in Data Analysis Guideline Instructions.Licensee Will Change Data Analysis Guidelines for Lead Analysts.With 990407 Ltr ML17229B0541999-03-10010 March 1999 LER 99-001-00:on 990211,inadequate TS SRs for SIT & SDC Isolation Valves Were Noted.Caused by Failure to Correctly Implement TS Srs.Submitted LAR to Align Required TS SR with Design Bases Requirements Being Verified.With 990310 Ltr ML17229A9901999-01-20020 January 1999 LER 98-009-00:on 981223,noted That Facility Operated Outside of Design Basis.Caused by non-conservative MSLB Analysis Inputs.Will Review SR Component Differences Between Units & Will re-baseline LTOP Analysis.With 990120 Ltr ML17229A9821999-01-0404 January 1999 LER 98-010-00:on 981207,RCS Boron Sample Frequency Required by Ts,Was Exceeded by Twelve Minutes.Caused by Personnel Error.Equipment Clearance Order Was Lifted to Draw Required Sample & Operations Procedure Was Changed.With 990104 Ltr ML17229A9611998-12-22022 December 1998 LER 97-002-01:on 981204,containment Sump Debris Screen Was Not IAW Design.Caused by Inadequate C/As for Sump Screen Anamolies.All Identified Sump Screen Deficiencies Were Dispositioned &/Or Repaired.With 981222 Ltr ML17229A9561998-12-15015 December 1998 LER 98-008-00:on 981118,missed TS SG U Tube Insp.Caused by Encoding Errors While Using Remote Positioning Fixtures.All SG Tube Surveyed.With 981215 Ltr ML17229A9301998-11-25025 November 1998 LER 98-005-01:on 980807,discovered That New MOV Methodology Caused Past PORV Block Valve Operability Problem.Caused by Inadequacies in Original Vendor MOV Methodology.Planned Valve Mods Will Be Implemented During Cycle 11 1998 Outage ML17229A9021998-11-0404 November 1998 LER 98-008-00:on 981008,inadequate Reactor Protection Sys Trip Bypass TS Was Noted.Caused by Poorly Worded Ts. Submitted LAR to Clarify Power Requirements for High Rate of Power Trips.With 981104 Ltr ML17229A8771998-10-14014 October 1998 LER 98-006-00:on 980918,inadvertent Afas Actuation Was Noted.Caused by Degradation of Multiple Afas Power Supplies. Replaced Afas Power Supplies & Revised Procedures.With 981014 Ltr ML17229A8761998-10-14014 October 1998 LER 98-007-00:on 980918,identified Discrepancies Between Fire Protection Design Requirements & Field Conditions. Caused by Inadequate Translation & Implementation of Fire Protection Requirements.Procedures Revised.With 981014 Ltr ML17229A8511998-09-0202 September 1998 LER 98-005-00:on 980807,discovered That PORV Margins Were Insufficient to Accommodate Addl Conservatism.Caused by Inadequacies in Original Vendor MOV Methodology.Will Implement Planned Valve Actuator mods.W/980902 Ltr ML17229A8201998-07-29029 July 1998 LER 98-007-00:on 980630,inadequate Procedure May Have Resulted in SBO Recovery Complications.Caused by Inadequate Procedures.Attached Caution Tags to Appropriate Control switches.W/980729 Ltr ML17229A7411998-05-28028 May 1998 LER 98-004-00:on 980430,discovered Waste Gas Decay Tank Operation W/O Available Oxygen Analyzers,Which Is Prohibited by Ts.Caused by Inadequate Licensee Review of License Amend. Oxygen Analyzer recalibrated.W/980528 Ltr ML17229A7381998-05-21021 May 1998 LER 98-006-00:on 980421,missed EDG Fuel Oil Sample Surveillance Was Noted.Caused by Personnel Error.Revised Fuel Oil Sampling Service Purchase Order & Revised Site procedure.W/980521 Ltr ML17229A7011998-04-27027 April 1998 LER 98-003-00:on 980326,discovered Containment Pressure Instrumentation Design Single Failure Vulnerability.Caused by Inadequate Design by Personnel Error.Removed RPS & ESFAS Containment Pressure Bypass Keys immediately.W/980427 Ltr ML17229A6761998-04-0202 April 1998 LER 98-005-00:on 980305,identified Two Conditions That Were Outside App R Design Bases.Caused by Design Oversight During Development of Original App R Safe SD Design.Established 30 Minute Roving Fire Watches & Provided training.W/980402 Ltr ML17229A6731998-03-26026 March 1998 LER 98-002-00:on 980224,radiation Monitor Surveillance Inadequacies Led to Operating of Facility Prohibited by Tss. Caused by Congnitive Personnel Error.Permanent Procedure Changes Were implemented.W/980326 Ltr ML17229A6551998-03-0505 March 1998 LER 98-001-00:on 980206,high/low Pressure Shutdown Cooling Interface Was Noted Outside App R Design Bases.Caused by Personnel Error.Addl Guidance Was Provided to Engineering Dept personnel.W/980305 Ltr ML17229A6281998-02-19019 February 1998 LER 98-004-00:on 980121,emergency Lighting Outside App R Design Bases Occurred.Caused by Congnitive Personnel Error During Translation of App R Section Iii.Procedures Onop 1 & 2 ONP-100.01 Were Issued for Use on 980206.W/980219 Ltr ML17229A6211998-02-0909 February 1998 LER 98-003-00:on 980110,manual Rt Due to DEH Leak at Turbine Test Block Was Noted.Caused by o-ring Extrusion.Shortened Bolts by About 0.125 & Reinstalled at Correct Torque values.W/980209 Ltr ML17229A6191998-02-0404 February 1998 LER 98-002-00:on 980105,CIS Bistable in Bypass Resulted in Condition Prohibited by Tss.Caused by Personnel Error. Radiation Monitor Was Restored to service.W/980204 Ltr ML17229A6161998-02-0303 February 1998 LER 98-001-00:on 980104,inadvertent RPS Actuation Occurred Due to Personnel Error.Caused by Procedural Inadequacies & Inadequate self-checking by Licensed Utility Personnel. Placards Have Been Placed in CRs.W/980203 Ltr ML17229A6051998-01-27027 January 1998 LER 97-010-01:on 971027,inadvertent Core Alteration Prohibited by TSs Were Noted Due to Stuck Cea.Caused by Personnel Error.Cea #24 Was Dislodged & Transferred to Spent Pool for insp.W/980127 Ltr ML17229A5501997-12-0505 December 1997 LER 97-008-00:on 971107,inadequate CR Ventilation Surveillance Resulted in Condition Prohibited by Ts.Caused by non-cognitive Personnel Error.Operating Procedure 2-1900050 Was revised.W/971205 Ltr ML17309A9091997-12-0202 December 1997 LER 97-011-00:on 971102,non-conservative RAS Set Point Resulted in Operation Prohibited by Ts.Caused by Inadequate Set Point & Instrument Loop Scaling Process.Revised ESFAS Functional Tp W/Proper Set point.W/971202 Ltr ML17229A5391997-11-26026 November 1997 LER 97-010-00:on 971027,inadvertant Core Alteration Prohibited by TS Occurred.Caused by CEA Failure to Detach from Ugs.Safety Evaluation Was Performed & Procedural Rev Made to Continue Upper Guide Structure move.W/971126 Ltr ML17229A5151997-11-0707 November 1997 LER 97-007-00:on 971008,inoperable Containment Cooling Fan Resulted in Operation of Facility Outside Design Basis. Caused by non-cognitive Personnel Error.Ccs Operation Was Revised & Issued on 971013.W/971107 Ltr ML17229A4991997-10-17017 October 1997 LER 97-009-00:on 970917,inoperable PORV Block Valve Resulted in Operation Prohibited by Tech Specs Occurred.Caused by Plant GL 89-10 Program Plan to Review Plant Manager Action Item Sys.Porv Block Valve V-1403 restored.W/971017 Ltr ML17309A9011997-08-27027 August 1997 LER 97-008-00:on 970728,mechanical Fire Penetrations Were Inoperable & Outside App R Design Bases.Caused by Seal Mfg Not Providing Formal Documentation for Installed Seals. Modified Inoperable Fire penetrations.W/970827 Ltr ML17229A4311997-07-29029 July 1997 LER 97-006-00:on 970630,discovered Inadequate Testing of Engineered Safety Features Subgroup Relays.Caused by Inadequacy in Implementing TS Requirements in Surveillance Procedures.Revised Surveillance procedures.W/970729 Ltr ML17229A4241997-07-25025 July 1997 LER 97-005-00:on 970625,discovered That Hot Shutdown Control Panel Shutdown Cooling Flow indicator,FI-3306 Inoperable. Caused by Weakness in Work Order & Procedure Used to Repair FI-3306.Section Meeting W/I&C Planners held.W/970725 Ltr ML17229A3971997-07-11011 July 1997 LER 97-004-00:on 970611,discovered Incorrect Original Cable Tray Fire Stop Assembly Installation Was Outside App R Design Basis.Caused by Personnel Error.Hourly Fire Watch Patrols Will Be posted.W/970711 Ltr ML17229A3871997-06-19019 June 1997 LER 97-003-00:on 970521,determined Required Post Maint Open Stroke Test for Valve V3245,2B2 SIT Discharge Check Valve, Had Not Been Performed.Caused by Personnel Error.Procedure revised.W/970619 Ltr ML17229A3841997-06-17017 June 1997 LER 97-002-00:on 970518,containment Sump Debris Screen Was Not IAW Design Due to Gaps in Screen Encl.Performed SER to Document Containment Sump Design requirements.W/970617 Ltr ML17229A3751997-06-0202 June 1997 LER 97-006-00:on 970501,operation Was Prohibited by TS Due to Inadequately Tested Degraded Voltage Sys.Revised Unit 1 ESFAS Surveillance Test procedure.W/970602 Ltr ML17229A3611997-05-29029 May 1997 LER 97-007-00:on 970502,reactor Coolant Pump Oil Collection Sys Was Outside App R Design Bases.Identified Leak Sites Were Repaired & Mods to RCP Oil Collection Sys to Capture Any Future Leakage from areas.W/970529 Ltr ML17229A3491997-05-21021 May 1997 LER 97-001-00:on 970423,containment Isolation Actuation Occurred.Caused by Increased Radiation Levels During Removal of Upper Guide Structure.Proper Actuation of Containment Isolation Components Was verified.W/970521 Ltr ML17229A3441997-05-13013 May 1997 LER 97-005-00:on 970419,reactor Was Shutdown Due to Reactor Coolant Pressure Boundary Leakage.Hot Cracking Was Caused by Weld Contamination.Repairs to RCPB Were Completed & 1A SDC Train Was Restored to Svc ML17229A3141997-04-30030 April 1997 LER 97-004-00:on 970402,refueling Machine Was Operating in Manner Prohibited by TS Due to Original Design of Refueling Machine Bypass Feature Conflicting W/Ts Requirements. Eliminated Overload Cut Off Limit bypass.W/970430 Ltr ML17229A2951997-03-31031 March 1997 LER 97-003-00:on 970304,automatic Rt Resulted from Loss of Electrical Power to 1A2 Rc Pump.Rcp Breaker Was Replaced & Pump Was Returned to svc.W/970331 Ltr ML17229A2721997-03-21021 March 1997 LER 97-002-00:on 970221,operation in Excess of Max Rated Thermal Power Occurred Due to Digital Data Processing Sys (Ddps) Calorimetric Error.Verified Acceptable Performance of Ddps Functions & Reviewed Software mods.W/970321 Ltr 1999-07-06
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17241A4891999-10-0707 October 1999 LER 99-004-00:on 990912,noted That MSSV Surveillance Was Outside of TS Requirements.Caused by Setpoint Drift.Subject MSSVs Are Being Refurbished & Retested Prior to Unit Startup from SL1-16 Refueling Outage.With 991007 Ltr ML17241A4951999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for St Lucie,Units 1 & 2.With 991014 Ltr ML17241A4741999-08-31031 August 1999 Rev 1 to PCM 99016, St Lucie Unit 1,Cycle 16 Colr. ML17241A4591999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for St Lucie,Units 1 & 2.With 990913 Ltr ML17241A4301999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for St Lucie Units 1 & 2.With 990805 Ltr ML17241A4111999-07-16016 July 1999 LER 99-007-00:on 990610,unplanned Cooldown Transient Occurred Due to Personnel Error.Trained & Briefed Personnel & Revised Procedures.With 990716 Ltr ML17241A4031999-07-0606 July 1999 LER 99-006-00:on 990605,sub-critical Reactor Trip Occurred Due to Inadvertent MSIV Opening.Caused by Personnel Error. Provided Operation Supervision Instruction to Operating Crews,Stand Down Meetings & Operator Aids.With 990706 Ltr ML17241A4041999-07-0606 July 1999 LER 99-005-00:on 990604,CEA Drop Resulted in Manual Reactor Trip.Caused by Procedural Inadequacies.Procedure Changes Are Planned to Correct Lack of Procedural Guidance for CEA Subgroup Power Switch Replacement.With 990706 Ltr ML17241A4091999-06-30030 June 1999 Monthly Operating Repts for June 1999 for St Lucie,Units 1 & 2.With 990712 Ltr ML17241A3941999-06-30030 June 1999 LER 99-004-01:on 990415,as Found Cycle 10 Psv Setpoints Were Outside TS Limits.Caused by Manufacturing Process Defect. All Three Psvs Were Replaced with pre-tested Valves During Cycle 11 Refueling Outage.With 990630 Ltr ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17241A3551999-06-0404 June 1999 LER 99-002-00:on 990505,both Trains of Safety Injection Actuation Were Blocked During Surveillance.Caused by Procedure Error.Procedure Revised.With 990604 Ltr ML17241A3631999-05-31031 May 1999 Monthly Operating Repts for May 1999 for St Lucie Units 1 & 2.With 990610 Ltr ML17241A3321999-05-17017 May 1999 LER 99-004-00:on 990415,determined That as Found Cycle 10 Psv Setpoints Outside TS Limits.Root Cause Under Investigation.Psvs Replaced with pe-tested Valves During Cycle 11 ML17241A3271999-05-0606 May 1999 LER 99-003-00:on 990406,ECCS Suction Header Leak Resulted in Both ECCS Trains Being Inoperable & Entry Into TS 3.0.3. Caused by Chloride Induced OD Stress Corrosion Cracking of Piping.Made Code Repairs & Coated Piping.With 990506 Ltr ML17241A3331999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for St Lucie,Units 1 & 2.With 990517 Ltr ML17229B0801999-04-0707 April 1999 LER 99-002-00:on 990311,SG ECT Error Caused Operation with Condition Prohibited by Ts.Caused by Deficiencies in Data Analysis Guideline Instructions.Licensee Will Change Data Analysis Guidelines for Lead Analysts.With 990407 Ltr ML17229B0841999-04-0707 April 1999 Rev 2 to PSL-ENG-SEMS-98-102, Engineering Evaluation of ECCS Suction Lines. ML17229B0791999-04-0707 April 1999 LER 99-001-00:on 990309,discovered Inadequate Design & IST SRs for Iodine Removal Sys (Irs).Caused by Original Design Inadequacies & Personnel Error.Naoh Tank Vent Valve V07233 Was Tagged Open.With 990407 Ltr ML17229B0961999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for St Lucie,Units 1 & 2.With 990408 Ltr ML17229B0541999-03-10010 March 1999 LER 99-001-00:on 990211,inadequate TS SRs for SIT & SDC Isolation Valves Were Noted.Caused by Failure to Correctly Implement TS Srs.Submitted LAR to Align Required TS SR with Design Bases Requirements Being Verified.With 990310 Ltr ML17229B0461999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for St Lucie,Units 1 & 2.With 990310 Ltr ML17229B0051999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for St Lucie,Units 1 & 2.With 990211 Ltr ML17229A9901999-01-20020 January 1999 LER 98-009-00:on 981223,noted That Facility Operated Outside of Design Basis.Caused by non-conservative MSLB Analysis Inputs.Will Review SR Component Differences Between Units & Will re-baseline LTOP Analysis.With 990120 Ltr ML17229A9961999-01-14014 January 1999 SG Tube Inservice Insp Special Rept. ML17229A9821999-01-0404 January 1999 LER 98-010-00:on 981207,RCS Boron Sample Frequency Required by Ts,Was Exceeded by Twelve Minutes.Caused by Personnel Error.Equipment Clearance Order Was Lifted to Draw Required Sample & Operations Procedure Was Changed.With 990104 Ltr ML17229A9831998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for St Lucie,Units 1 & 2.With 990111 Ltr ML17229A9611998-12-22022 December 1998 LER 97-002-01:on 981204,containment Sump Debris Screen Was Not IAW Design.Caused by Inadequate C/As for Sump Screen Anamolies.All Identified Sump Screen Deficiencies Were Dispositioned &/Or Repaired.With 981222 Ltr ML17229A9561998-12-15015 December 1998 LER 98-008-00:on 981118,missed TS SG U Tube Insp.Caused by Encoding Errors While Using Remote Positioning Fixtures.All SG Tube Surveyed.With 981215 Ltr ML17241A3581998-12-0909 December 1998 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period of 970526-981209. ML17229A9421998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for St Lucie,Units 1 & 2.With 981215 Ltr ML17229A9301998-11-25025 November 1998 LER 98-005-01:on 980807,discovered That New MOV Methodology Caused Past PORV Block Valve Operability Problem.Caused by Inadequacies in Original Vendor MOV Methodology.Planned Valve Mods Will Be Implemented During Cycle 11 1998 Outage ML17229A9021998-11-0404 November 1998 LER 98-008-00:on 981008,inadequate Reactor Protection Sys Trip Bypass TS Was Noted.Caused by Poorly Worded Ts. Submitted LAR to Clarify Power Requirements for High Rate of Power Trips.With 981104 Ltr ML17241A4931998-11-0101 November 1998 Statement of Account for Period of 981101-990930 for Suntrust Bank,As Trustee for Florida Municipal Power Agency Nuclear Decommissioning Trust (St Lucie Project). ML17229A9051998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for St Lucie,Units 1 & 2.With 981110 Ltr ML17229A8871998-10-19019 October 1998 Part 21 Rept Re Potential Defect in Swagelok Stainless Steel Front Ferrule,Part Number SS-503-1 Which Was Machined with Improper Length.C/A Includes Insp Equipment That Will 100% Identify Short Length ML17229A8781998-10-19019 October 1998 Part 21 Rept Re Potential Defect in Swagelok Stainless Steel Front Ferrule,Part Number SS-503-1,which Was Machined with Improper Length.Insp Equipment That Will 100% Identify Short Length ML17229A8771998-10-14014 October 1998 LER 98-006-00:on 980918,inadvertent Afas Actuation Was Noted.Caused by Degradation of Multiple Afas Power Supplies. Replaced Afas Power Supplies & Revised Procedures.With 981014 Ltr ML17229A8761998-10-14014 October 1998 LER 98-007-00:on 980918,identified Discrepancies Between Fire Protection Design Requirements & Field Conditions. Caused by Inadequate Translation & Implementation of Fire Protection Requirements.Procedures Revised.With 981014 Ltr ML17229A8721998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for St Lucie Units 1 & 2.With 981009 Ltr ML17229A8511998-09-0202 September 1998 LER 98-005-00:on 980807,discovered That PORV Margins Were Insufficient to Accommodate Addl Conservatism.Caused by Inadequacies in Original Vendor MOV Methodology.Will Implement Planned Valve Actuator mods.W/980902 Ltr ML17229A8611998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for St Lucie,Units 1 & 2.With 980911 Ltr ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17229A8481998-08-0707 August 1998 Rev 1 to PSL-ENG-SEFJ-98-013, St Lucie Unit 2,Cycle 10 Colr. ML17229A9461998-08-0707 August 1998 Rev 0 to PCM 98016, St Lucie Unit 2,Cycle 11 Colr. ML17229A8301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for St Lucie,Units 1 & 2.W/980814 Ltr ML17229A8201998-07-29029 July 1998 LER 98-007-00:on 980630,inadequate Procedure May Have Resulted in SBO Recovery Complications.Caused by Inadequate Procedures.Attached Caution Tags to Appropriate Control switches.W/980729 Ltr ML17229A7981998-06-30030 June 1998 Monthly Operating Repts for June 1998 for St Lucie,Units 1 & 2.W/980713 Ltr ML17229A7701998-05-31031 May 1998 Monthly Operating Repts for May 1998 for St Lucie,Units 1 & 2.W/980612 Ltr ML17229A7411998-05-28028 May 1998 LER 98-004-00:on 980430,discovered Waste Gas Decay Tank Operation W/O Available Oxygen Analyzers,Which Is Prohibited by Ts.Caused by Inadequate Licensee Review of License Amend. Oxygen Analyzer recalibrated.W/980528 Ltr 1999-09-30
[Table view] |
Text
MMJ;NVUlC Y' REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9910140083
~
DOC.DATE: 99/10/07 NOTARIZED: NO
~
FACIL:50-335 St. Lucie Plant, Unit 1, Florida Power & Light Co.
~
DOCKET ¹
~
05000335 AUTH.NAME . 'AUTHOR AFFILIATION FREHAFER,K.W. Florida Power & Light Co.
STALL,J.A. , Florida Power & Light Co.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 99-004-00:on 990912,noted that MSSV surveillance was outside of TS requirements. Caused by setpoint drift. Subject MSSVs are being refurbished & retested prior to unit startup from SLl-16 refueling outage. With 991007 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR I ENCL I SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
'ECIPXENT COPIES RECIPIENT 'OPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL LPD2-2 1 1 GLEAVES,W 1 1 INTERNAL: ACRS 1 1 1 1 NRR/DIPM/IOLB 1 1 NRR/DRXP/REXB 1 1 NRR/DSSA/SPLB 1 1 RES/DET/ERAB 1 1 RES/DRY/OERAB 1 1 RGN2 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LMXTCO MARSHALL 1 1 NOAC POORE,W. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR REMOVED FROM DISTRIBUTION LIST DESK (DCD) ON EXTENSION 415-2083 ORGANIZATION, CONTACT T THE DOCUMENT CONTRC FULL TEXT CONVERSION REQUIRED TOTAL, NUMBER OF COPIES REQUIRED: LTTR 16 ENCL 16
Florida Power St Light Company, 6351 S. Ocean Drive, Jensen Beach, FL 34957 October 7, 1999 FPL L-99-219 10 CFR $ 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Re: St. Lucie Unit 1 Docket No. 50-335 Reportable Event: 1999-004-00 Date of Event: September 12, 1999 Main Steam Safety Valves Surveillance Outside Technical S ecification Re uirements The attached Licensee Event Report 1999-004 is being submitted pursuant to the requirements of f
10 CFR 50.73 to provide notification of the subject event.
Very truly yours, J. A. Stall Vice President St. Lucie Nuclear Plant JAS/EJW/KWF Attachment cc: Regional Administrator, USNRC, Region II Senior Resident Inspector, USNRC, St. Lucie Nuclear Plant 99i0140083 991007 05000335 PDR ADOCK PDR an FPL Group company
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3160-0104 EXPIRES 06/30/2001 I6.1999)
Estimated burden per response to comply with this mandatory information collection request: 50 hrs. Reported lessons teamed are incorporated into the licensing process and fed back to industry. Forward comments regarding LICENSEE EVENT REPORT (LER) burden estimate to the Record. TAanagement Branch {TW F33), U.S. Nuclear Regulatory Commission, Washington, Dc 205554001, and to the Papenvork Reduction Project (31504104j, Office of Management and Budget, (See reverse for required number of Washington, DC 20503. If an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, digits/characters for each block) and a person is not required to respond to, the Information collection.
FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3)
St. Lucie Unit 1 05000335 Page 1 of 5 TITLE (4)
Main Steam Safety Valves Surveillance Outside Technical Specification'equirements EVENT DATE (6) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
SEQUENTIAL REVISION FACIUTYNAME DOCKET NUMBER MONTH DAY YEAR YEAR MONTH DAY NUMBER NUMBER FACIUTYNAME DOCKET NUMBER 09 12 1999 1999 - 004 - 00 10 07 1999 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQ UIREMENTS OF 10 CFR 5: (Chock ono or more) (11)
MODE (9) 20.2201 (b) , 20.2203(a)(2)(v) X 50.73(a)(2)(i) 50.73{a) (2)(viii)
POWER 20.2203(a) {1) 20.2203 (a) (3) {I) 50.73(a) (2)(ii) 50.73(a) (2)(x)
LEVEL {10) 070 20.2203(a)(2) (i) 20.2203{a) (3)(ii) 50.73(a) (2)(iii) 73.71 20.2203{a) (2) (ii) 20.2203(a) (4) 50.73(a) {2)(iv) OTHER 20.2203(a) (2)(iii) 50.36(c){1) 50.73(a)(2) (v) Specify In Abstract below or 20.2203(a) {2)(iv) 50.36(c) (2) 50.73(a) (2) {vii) in NRC Form 366A LICENSEE CONTACT FOR THIS LER {12)
NAME TELEPHONE NUMBER unaluda Araa Coda)
Kenneth W. Frehafer, Licensing Engineer (561) 467 7748 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13)
CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE REPORTABLE To EPIX CAUSE SYSTEM COMPONENT MANUFACTURER To EPIX SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY EXPECTED YES SUBMISSION (tf yes, c'omplete EXPECTED SUBMISSION DATE). X No ,
DATE (16)
ABSTRACT /Limit to 1400 spaces, i.e., approximately 15 singlewpaced typewritten lines/ (16)
On September 12, 1999, St. Lucie Unit 1 was in Mode 1 and holding at. approximately 70 percent reactor power for testing'f the main steam safety valves (MSSVs) in accordance with proceduze 1-MSP-08.07, "Main Steam Sa'fety Setpoint Surveillance."
Three train A and one train B MSSVs lifted low, outside of the required Technical Specification pressure setpoint range of +/- 1 percent. Prior to testing, the reactor trip setpoints were reduced to allow continued operation with two MSSVs per train out of service. The set pressure of one of the train A MSSVs was reset to allow continued operation.
The apparent cause of the MSSV surveillance failures was setpoint drift. Per ASME code considerations, a formal root cause is not required. The safety significance of the low as-found MSSV setpoints was evaluated and found to be insignificant.
The subject MSSVs are being refurbished and retested prior to unit startup from the SL1-16 refueling outage. FPL is considering whether a change to the St. Lucie Technical Specifications or TS bases is appropriate to address the differences between NUREG-1432 and the St. Lucie Technical Specifications concerning as-found and as-left
~
safety relief setpoints.
NRC FORM 3BB IB.1999)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6-1998)
LlCENSEE EVENT REPORT (LER)
TEXT CONTINUATION DOCKET PAGE (3)
FACILITY NAME (1) LER NUMBER (6)
NUMBER (2)
SEQUENTIAL REVISION NUMBER NUMBER St. Lucie Unit 1 05000335 004 - Page 2 of 5 1999 00 TEXT (Ifmore space is reriuired, use additional copies of IVRC Form 366A) (17)
Description of the Event On September 12, 1999, St. Lucie Unit 1 was in Mode 1 and holding at approximately 70 percent reactor power for testing of the main steam safety valves (MSSVs)
(EIIS)SB)RV) during the downpowex for the SL1-16 refueling outage. The following MSSVs lifted outside of their Technical Specifications (TS) required pressure range.
Additionally V8213 lifted outside of the +/- 3% ASME code allowed range by 0.6 psig low. This surveillance testing of the MSSVs'etpoints was performed in accordance with procedure 1-HSP-08.07, "Hain Steam Safety Setpoint Surveillance."
Measured Deviation Valve Train Lift TS Limit From TS Sepoint Pressure Limit (() )
(psia)
V8201 986.9 1000 +/- 1% 1 '1 V8202 982. 9 1000 +/- 1() -1071 V8211 1025.5 1040 +/- 1() -1.45 V8213 1008.7 1040 +/- 1'h -3013 MSSVs V8201, V8211, and,V8213 were left inoperable and out of service at the completion of testing. V8202 was restored to OPERABLE stats by setpoint adjustment within the action time of Technical Specification 3.7.1.1. Prior to testing the MSSVs, the reactor trip setpoints had been reduced to allow continued operation with two MSSVs per train out of service pex work ordex (WO) 98023939-02. No more than two valves per train were out of service and the reactor trip setpoints were properly adjusted in accordance with Te'chnical Specification 3.7 '.1, therefore there were no operability concerns.
Cause of the Event The as-found set pressure deviations were relatively minor and similar to those found in past cycles. The apparent cause is setpoint drift and/or the use of the new test methods. As described below, a formal root cause is not required by ASME/ANSI OM-1987, part l.
Per ASME/ANSI OM-1 'tt1.3.3.1(e)(2) and Code Interpretation 92-8, a Class 1 pressure relief valve with an as-found setpoint outside the acceptance range of the setpoint on the minus side is not considered a failure. As a consequence, additi.onal testing for valves failing outside the negative acceptance criteria is not required by the ASME Code. FPL quality instruction (QI) 11-PR/PSL-7, "Control of Code Safety and Relief Valves," contains additional criteria within 95.5.3 that generally requires additional testing for valves failing the negative tolerance criteria. The QI criteria are based on the adverse system functional issues resulting from relief valve seat leakage and premature lift. However, per the QI, the criteria for additional testing of valves faili.ng the negative tolerance acceptance criteria may be waived or altered based on an evaluation of the as-found test pressure, valve inspection, system requirements and histori.cal records. The expansion of testing scope due to the failure of V8213 was waived based on the small amount of deviation (3.13% vs. 3%), the acceptable results of the other'alve tests with respect to ASME NRC FORM 388A 18.1898)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION I 6-1 888)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION DOCKET PAGE (3)
FACILITY NAME (1) NUMBER (2)
LER NUMBER (6)
SEQUENTIAL REVISION NUMBER NUMBER St. Lucie Unit 1 05000335 Page 3 of 5 1999 004 00 TEXT llfmore specs is required, use addi tionel copies of NRC Form 366A ) (17)
Cause of the Event (cont'd) criteria, the absence of recent problems with MSSV seat leakage and premature lift, and the insignificant effect of a small negative set pressure deviation in a high bank MSSV relief valve. The MSSVs are being refurbished and retested.
Analysis of the Event This event is reportable under 10 CFR 50.72 (a) (2) (i) (B) as "any operation or condition prohibited the plant's Technical Specifications." The St. Lucie Unit 1 Technical Specifications differ from NUREG-1432r "Standard Technical Specification Combustion Engineering Plants," in that an as-found MSSV setpoint tolerance is not included in the St. Lucie Technical Specifications.
FPL is considering whether a change to the St. Lucie Technical Specifications oz TS bases is appropriate to address this Technical Specification difference.
Analysis of Safety Significance The MSSVs must open to provide overpressure protection for the steam generators and relief capacity to remove decay heat. The MSSVs are classified as Safety-Related, Quality Group B components.
Per TS table 3.7-1 the maximum allowable power level high trip setpoint with two inoperable steam line safety valves on either operating steam generator is 79.8%
Effect on Safet Anal ses Valves V8201, V8202, V8211 and V8213 lifted outside the TS limit of +/- 1 percent. However, these lift lift setting tolerance setting failures were greater than the
-1 percent limit. Valves V8205 and V8216 lifted within the tolerance limit specified in the TS. It will be assumed for the purpose of this evaluation* that all the remaining valves would have lifted within their tolerance limits.
The only FSAR analyzed events that could potentially be affected by the deviations in the MSSV setpoints are the loss of exterhal load (LOEL) and the small break, LOCA (SBLOCA).
The loss. of external load event, including the case of inoperable MSSVs, relies on the MSSVs to release the system energy so as to prevent the primary and the secondary side pressures from exceeding the overpzessurization criteria. The analysis of this event assumes conservatively that the MSSVs begin to open at the TS allowed maximum lift pressure corresponding to a tolerance of + 1 percent. Opening of the valves at a pressure lower than that assumed in the safety analysis would be beneficial for this transient and the results would remain bounded by the FSAR results.
In the analysis of the small break LOCA event, open at a lift it is- assumed that the MSSVs begin to pressure corresponding to a tolerance of + 3 percent. The as-found set pressures therefore would, not have any adverse 'impact on the small break LOCA analysis results, as presented in the FSAR.
Other FSAR events including the steam generator tube rupture (SGTR) event are not impacted by the variations in the MSSV lift pressure.
FSAR conservatively assumes the opening of the atmospheric dump valves (ADVs) to The SGTR event analyzed in the NRC FORM 3BBA (6-1888)
NRC FORM 366A U.S. I'IUCLEAR REGULATORY COMMISSION Is-1998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
SEQUENTIAL REVISION NUMBER NUMBER St. Lucie Unit 1 05000335 Page 4 of 5 1999 004 00 TEXT (If more speceis required, use eddi tionel copies of NRC Form 366AJ (17)
Analysis of Safety Significance (cont'd) release the steam from the ruptured steam generators. The identified MSSVs'etpoint pressure deviations thus would not impact the FSAR conclusions for this event.
'he opening of MSSVs at pressures lower than the lift pressure corzesponding to -1 percent tolerance is thus determined to'have no adverse impact on the safety analysis, including deviations outside -3.percent. A much lower negative valve
'tolerance limit, although acceptable from safety analysis considerations, may have operational impact as the margin to operating pressure gets reduced.
The MSSVs's-found set pressure values (specified above) were outside the tolerance limits specified in the St. Lucie Unit 1 Technical Specification 3.7.1.1. This degraded condition however did not compromise plant safety. The evaluation performed using the as-found setpoints concludes that, Cycle 15 operation had remained within the design basis of the plant for all analyzed FSAR events. No safety criteria would have been violated due to the identified condition of the MSSVs.
Se oint Drift Considerations The below chart shows the MSSV tests in the last 3 cycles for unit 1. Not'all of the valves were tested during these cycles. The As-Found () Failure column is shown for the cycles that were evaluated. They represent the percentage from nameplate setpoint that the valve was out of tolerance. The none in the column means, that the test was satisfactory. The percent Drift between Cycles .column is the percentage change that the valve experienced over one cycle taken from the 2"e as-left setpoint test and the next as-found test of the valve. I Valve S/N Unit Date As-Pound %
Date As-Pound % % Drift between 1
'ailure Pailure cles N55128-00-0001 1996 none 1999 -1.71 -1.62 N55128-00-0002 1996 none 1999 -1.31 -1.93 N55128-00-0003 1996 1.4 1997 -1.03 -1. 12 N55128-00-0004 1996 none N55128-00-0005 1996 -1.52 1999 none -0.20 N55128-00-0006 1996 ~
1.83 1997 1.62 1.52 N55128-00-0007 1996 1.93 N55128-00-0008 1996- 2.54 N55128-00-0009 1996 none 1997 none -.50 N55128-00-0010 1996 none 1997 none -.19 N55128-00-0011 1995 none 1996 1.37 1. 17 N55128-00-0011 1999 -1.45 -2. 13 N55128-00-0012 1996 none 1997 none - 68
~
N55128-00-0013 1996 1.95 1999 -3.13 -3.50 N55128-00-0014 1996 1.27 1997 none -1.35 N55128-00-0015 1996 1.17 1997 none .10 N55128-00-0016 1996 none 1999 none -0.87
NRC FORM 366A U.S: NUCLEAR REGULATORY COMMISSION (8-1998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME {1) DOCKET NUMBER I2 LER NUMBER I6) PAGE I3)
SEQUENTIAL REVISION NUMBER NUMBER St. Lucie Unit 1 05000335 Page 5 of 5 1999 004 00 TEXT (Ifmore spaceis required, use additional copies of NRC Form 3MAJ (17)
Analysis of Safety Significance (cont'd)
These data are from the Relief Valve Database. This evaluation does not take into account the instrument inaccuracies or the difference in readings between'the 1" and 2"" tests done to accept the valves.
The test methodology was changed for Unit 1 for the 1999 testing. The plant started using computer operated test machine vs. the previous manual test method. Both test techniques use a lifting device but the newer system's ramp rate and setpoint interpretation are less subjective and operator dependent which provide for more consistent and accurate readings.
FPL concluded that the relief valves setpoint drift is mostly scattered data with no dominant trending setpoint drift for any valve over the cycles analyzed. Therefore, there is no concern pertaining to the downward drift of the MSSV setpoints.
Based on the above, this event had no impact on the health and safety of the public, Corrective Actions
- 1. The subject MSSVs are being refurbished by Wyle Labs via WO 98018487.
- 2. The subject MSSVs will be reworked and retested per WO 98018488.
- 3. FPL is considering a change to the St. Lucie Technical Specifications to address the differences between NUREG-1432 and the St. Lucie Technical Specifications concerning as-found and as-left safety relief valve setpoints.
Additional Information Failed Com onents Identified Based on ASME code considerations, there were no MSSV test failures.
Similar Events LER 50-389/1999-004-00 and 50-389/1999-004-01, "As Found Cycle 10 Pressurizer Safety Valve Setpoints Outside Technical Specification Limits, " was issued for Unit 2 pressurizer code safety surveillance failures.
NRC FORM 3BBA IB.1898)
r
~