ML17266A210: Difference between revisions

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=Text=
=Text=
{{#Wiki_filter:NBC POR941 Ssa                                                                                                                                      U. S NUCLEAR REGULATORY CC44MISSION IT  nI LECENSEE EVENT REPORT
{{#Wiki_filter:NBC POR941 Ssa                                                                                                                                      U. S NUCLEAR REGULATORY CC44MISSION IT  nI LECENSEE EVENT REPORT CQNTROI SLCCXI                            E    E                  IQI                        IPLP~S PRINT CR TYPc ALI. REQUIRED INPORAIATIONI I                                      5 1            3    4 FEL    I  SI LYCSNSSS COOS LES        I  I 14 Q      01      1-101 I
                                                                                    '
CQNTROI SLCCXI                            E    E                  IQI                        IPLP~S PRINT CR TYPc ALI. REQUIRED INPORAIATIONI I                                      5 1            3    4 FEL    I  SI LYCSNSSS COOS LES        I  I 14 Q      01      1-101 I
1901 010 i
1901 010 i
I I 2 4 5 9,4 si4M 4 B I
I I 2 4 5 9,4 si4M 4 B I
                                                                                                                                   . I      10
                                                                                                                                   . I      10
                                                                                                                                                   ~5 Qi      3 11
                                                                                                                                                   ~5 Qi      3 11 I  I I 4922, fPP I  I  IQA~IQ 40    52    ~4 53 CCN 0  E
                                                                                                                                                                    '
I  I I 4922, fPP I  I  IQA~IQ 40    52    ~4 53 CCN 0  E
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4
4
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LZJQ 2$
LZJQ 2$
LOO~O 21 4l  40 LYJQ 41 ZNJQ              i 42 ZIQ          JA              31 CAUSE DESCRIPTION ANO CORRECTIVE ACTIQNS Q27 0          In accordance with NSSS recommendation                                                                        r crease the minimum shutdown mar in from lA ho to                                                                              2X h            ensures          20 min.
LOO~O 21 4l  40 LYJQ 41 ZNJQ              i 42 ZIQ          JA              31 CAUSE DESCRIPTION ANO CORRECTIVE ACTIQNS Q27 0          In accordance with NSSS recommendation                                                                        r crease the minimum shutdown mar in from lA ho to                                                                              2X h            ensures          20 min.
time la se to                        criticalit                      and          to reclude ooerati n wi char ina umps with a artiall drained RCS in M00 5                                                                                                  hi
time la se to                        criticalit                      and          to reclude ooerati n wi char ina umps with a artiall drained RCS in M00 5                                                                                                  hi iQQ>>>>Q 7
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a 3
a 3

Latest revision as of 10:03, 4 February 2020

LER 80-027/09T-0:on 800514,during Shutdown for Maint,Nsss Notified Util That Partial Draining of RCS While in Mode 5 Is Condition That Has Not Been Analyzed for Boron Dilution Event.Procedures Revised to Increase Min Shutdown Margin
ML17266A210
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 05/21/1980
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17208A673 List:
References
REF-PT21-80-220-001 LER-80-027-09T, LER-80-27-9T, NUDOCS 8006030449
Download: ML17266A210 (2)


Text

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=VEi4T'DESCRIPTION 9 NO PROS*EL.E CONSEQUENCES QIO 0 '"- ) Durin shutdown for maintenance the NSSS notified FP th t oartial drain-in of the RCS while in Node 5 is a condition that has not been anal zed for the boron dilution event. Reduced'RCS"volume would result in

~35 a redi cted t ilme to cri tical i t 1 ess than the assumed time eri od for o er ator action assumin the T.S. minimum shutdown mar in of lA ho existed at the onset of the event . This is reportable under T.S. 6.9.1.8 because a partiall drained RCS is less conservative than anal zed in the. FSAR .

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LOO~O 21 4l 40 LYJQ 41 ZNJQ i 42 ZIQ JA 31 CAUSE DESCRIPTION ANO CORRECTIVE ACTIQNS Q27 0 In accordance with NSSS recommendation r crease the minimum shutdown mar in from lA ho to 2X h ensures 20 min.

time la se to criticalit and to reclude ooerati n wi char ina umps with a artiall drained RCS in M00 5 hi iQQ>>>>Q 7

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3 9

PACILITY.

STATUS ACTIVITY CON TCNT RKLILASSO CP BSL~PS

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event of this t e. It is also re ortable under 10 CFR 1 12 AMOUNTOP OTNSBSTATUS Q20 A~iVITYQSS JA MST44CO OP clscQVSBv

~QSI 1 NA

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CISCCVSBV CSSCBIPTIC94 LCCATICN OP BSLSASS QSE 2

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0 11

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12 NA PSBSQNHSI INJUBI%2 I

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0 II Qaa 12 NA 30 I CSS QP Cail OAMAC2 9 0 PACI LITY CSSCBIPTICN QAS

~19 ~ZQ2 2 3 3 '0 pvsLIcrv NA I'IRC I'SE CNI.Y 30 0 i4 IQ~ :0' NA 3 Ss 59 50 NAME OB PRcPARER EE. A. Scho man p94QNc. 305 552 3802 8 OG603O

Reportable Occurrence 335-80-27 Licensee Event Report Pa e Two Additional Information

l. The applicability of this occurrence to. St. Luci.e Unit 2 and Turkey Point Units 3 8 4 is under consideration.
2. A Technical Specification change is being prepared to address operation in Mode 5 with a partially drained RCS
3. Entry into Mode 5 is from Nodes requiring higher shutdown margins.

Deliberate dilution would be re'quired ta a'chieve the minimum shutdown margin specified in Technical Specifications for Node 5.

The higher shutdown margins in Mode 4 and 6 and the need for deliberate dilution to achieve the minimum Node 5 shutdown margin makes this event unlikely.