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{{#Wiki_filter:r f FLORIDA POWER & LIGHT ST. LUCIE UNIT 2 STEAM GENERATOR INSPECTION PLANNING FOR SL2-16, APRIL 2006 St Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 AGENDA.Purpose of Meeting.Background  
{{#Wiki_filter:r f
& S/G Condition* SL2-16 Inspection Scope.Projected Tube Plugging* Operating Experience
FLORIDA POWER & LIGHT ST. LUCIE UNIT 2 STEAM GENERATOR INSPECTION PLANNING FOR SL2-16, APRIL 2006 St Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 AGENDA
* Contingency Planning* Generic Letter 2006-01.Summary & Closing 2 FPL 1 V St. Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Purpose of Meeting* Review SL2 S/G Condition* Review SL2-15 Inspection Planning* Address Staff Concerns St. Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Background  
          . Purpose of Meeting
& S/G Condition* SIG Design* cEModel 3410* 84l1 Tubes I SG* -19.3 EFPY @ SL2-16* A-600 HTMA Tubing* CS Lattice Support System (eggcrates)
          . Background & S/G Condition
* Tubesheet Joint -Explosive* Total Tubes Plugged-SG A -1469 (17.5%)-SG B -1709 (20.3%)* T-Hot -600OF FPL ./2 r St Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Background  
* SL2-16 Inspection Scope
& S/G Condition FPL Steam Generator Program* Committed to Safe Operation* Full Implementation of NEI 97-06, S/G Program Guidelines
          . Projected Tube Plugging
' Inspection
* Operating Experience
' Chemistry Leak Monitoring
* Contingency Planning
* Generic Letter 2006-01
          . Summary & Closing 2
FPL 1
 
V St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Purpose of Meeting
* Review SL2 S/G Condition
* Review SL2-15 Inspection Planning
* Address Staff Concerns St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & S/G Condition
* SIG Design
* cEModel 3410
* 84l1 Tubes I SG
                                * -19.3 EFPY @ SL2-16
* A-600 HTMA Tubing
* CS Lattice Support System (eggcrates)
* Tubesheet Joint - Explosive
* Total Tubes Plugged
                                  - SG A - 1469 (17.5%)
                                  - SG B - 1709 (20.3%)
* T-Hot -600OF FPL                                 ./
2
 
r St Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & S/G Condition FPL Steam Generator Program
* Committed to Safe Operation
* Full Implementation of NEI 97-06, S/G Program Guidelines
          ' Inspection
          ' Chemistry Leak Monitoring
* Incorporate Industry Experience
* Incorporate Industry Experience
* Extensive Examination History at Unit 2 X Conservative Approach& In Situ Pressure Test at Last 6 Inspections  
* Extensive Examination History at Unit 2 XConservative  Approach
,,- --FP 5 FPLop St. Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Background  
          &In Situ Pressure Test at Last 6 Inspections ,,-   - -
& S/G Condition* Last Inspection  
FP                 5 FPLop St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & S/G Condition
-SL2-15 in January 2005 a Results Discussed with NRR During Outage' Damage Mechanisms Generally as Expected 1 Tube Ding with ODSCC Limited PWSCC in Tubesheet (3 in Upper 2", 1 at Tack Roll)'Increase in Axial ODSCC at Eggcrate Supports'RCL Indications Detected During Pull Out Scans'Addressed in OA Model'Tested with Qualified Technique if > .35 Volts'No Tube Integrity Issues A .FPL 3 V St. Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Indication Count Summary for SL2-15 Mechanism Axial ODSCC at Eggcrate Supports Axial ODSCC at Diagonal Supports Axial ODSCC at Tube Dings Axial ODSCC in Freespans Axial ODSCC at Top of HL Tubesheet Axial IDSCC Below Top of HL Tubesheet Circ. ODSCC at Top of HL Tubesheet Circ. IDSCC at Top of HL Tubesheet Circ. IDSCC at HL Tube End Wear Due to Foreign Objects Wear at Diagonal & Vertical Supports Wear at Eggcrate Tube Supports FPL SIG A SIG B Total 1184 1266 2450 1 8 9 0 1 1 0 1 1 14 2 16 1 1 2 7 10 17 0 1 1 0 1 1 1 1 2 672 443 1115 67 73 140 St. Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Background
* Last Inspection - SL2-15 in January 2005 a Results Discussed with NRR During Outage
& S/G Condition TUBE PLUGGING HISTORY Damaae Mechanism (1)OD Cracks at Tube Supports Mech. Wear at Tube Supports OD Cracks at Tubesheet Preservice, FO, Preventative Circ. OD Cracks at Tubesheet OD Volumetric  
      ' Damage Mechanisms Generally as Expected 1Tube Ding with ODSCC Limited PWSCC in Tubesheet (3in Upper 2", 1 at Tack Roll)
-Various ID Cracks in Tubesheet OD Cracks at Dings OD Cracks in Freespan 4100 14 18 17 5 11101 259 11 20 51 13 2 4103 482 27 6 10 1105 1592 1 20 2 15 4 3 5 1_ 1 1 54 361 530 1635 Cumulative Plugging Cumulative Percent'I (1) Axial unless noted otherwise FPL 652 1013 1543 3178 , 3.9% 6.0% 9.2% -1B.9%:..a_ ot- '8 4 V St Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Background  
      'Increase in Axial ODSCC at Eggcrate Supports
& SIG Condition Benchmark of Predicted (best estimate) vs. Observed Indications Mechanism Case Predicted Observed Axial ODSCC at Eggcrates Worst SG 928 1217 Axial ODSCC at Tube Dings All SGs 2 1 Axial ODSCC at Transition All SGs 43 16 Axial IDSCC below Transition All SGs 15 2 Circ. ODSCC at Transition All SGs 25 17 FPL St. Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Background  
      'RCL Indications Detected During Pull Out Scans
& SIG Condition Probability of Burst (POB)Mechanism SG A SIG B ODSCC' at E c029crats 0.0777 ODSCC at D)ings 0.00(Y O)SCC at Topofa-Tubcshect  
            'Addressed in OA Model
-0 Cumulatisv P0I3 0.0356* Significant Axial Degradation Mechanisms
            'Tested with Qualified Technique if > .35 Volts
* Cycle 15 Length for 10% POB Criterion  
      'No Tube Integrity Issues.            A FPL 3
-17.4 EFPM* Cycle 15 Length for 5% POB Criterion  
 
-16.2 EFPM _ o* Planned Cycle 15 Length is -14.5 EFPM , FPLI S  
V St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Indication Count Summary for SL2-15 Mechanism                       SIG A    SIG B    Total Axial ODSCC at Eggcrate Supports         1184      1266      2450 Axial ODSCC at Diagonal Supports             1        8        9 Axial ODSCC at Tube Dings                     0          1        1 Axial ODSCC in Freespans                     0          1        1 Axial ODSCC at Top of HL Tubesheet           14        2        16 Axial IDSCC Below Top of HL Tubesheet         1          1        2 Circ. ODSCC at Top of HL Tubesheet           7      10        17 Circ. IDSCC at Top of HL Tubesheet           0          1        1 Circ. IDSCC at HL Tube End                   0          1        1 Wear Due to Foreign Objects                   1          1        2 Wear at Diagonal & Vertical Supports       672      443      1115 Wear at Eggcrate Tube Supports             67        73      140 FPL St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & S/G Condition TUBE PLUGGING HISTORY Damaae Mechanism (1)                4100 11101    4103      1105 OD Cracks at Tube Supports            14  259      482      1592 Mech. Wear at Tube Supports            18  11                    1 OD Cracks at Tubesheet                17   20        27        20 Preservice, FO, Preventative                51        6          2 Circ. OD Cracks at Tubesheet           5    13        10        15 OD Volumetric - Various                     2 ID Cracks in Tubesheet                                 4          3 OD Cracks at Dings                           5                    1 OD Cracks in Freespan                 _              1          1 54   361       530       1635 Cumulative Plugging       652 1013       1543     3178   ,
-i St. Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Background  
Cumulative Percent        3.9% 6.0%     9.2% -1B.9%:..
& S/G Condition In Situ Pressure Testing SL2-9 Through SL2-15* 73 Total Indications (19 at SL2-15)* Mechanisms Include Axial ODSCC at Eggcrates Axial ODSCC at Dings'LAxial ODSCC at TTS' Axial IDSCC below TTS Circ ODSCC at TTS' Circ IDSCC at TTS OD Volumetric TTS FPL* No Leakage or Burst* 11.- -Bl y 5 .". ..St. Lucie Unit 2- Steam Generator Inspection Planning for SL2-16 SL2-16 Inspection Scope* Visual Examination of All Tube Plugs* Bobbin Probe All Active Tubes Screen Dings <5 Volts in Straight Sections' Full Length Row 3-140, Straight Length Row 1-2* Plus Point Probe 100% Hot Leg Top of Tubesheet
  'I      (1) Axial unless noted otherwise a_      '8 ot-FPL 4
(+3" /-13")Cold Leg Periphery Tubes (+3"/-2")20% Row 1-2 U-bends (A-23, B-25)20% Wear at Vertical Straps (A-86, B-58)' .00% Wear at Eggcrates, HL & CL Diagonals (A-274,;B-202)
 
Full Tubesheet if No Tube Expansion (A-21,-B-1) 1-FPL 6 I St Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 SL2-16 Inspection Scope (con't)* Plus Point Probe for Dings SGA SGB' All Dings Hot Leg Tubesheet to 1st Support 68 78' All Dings >5 volts 1st Support to HL Bend 57 80 All Dings in HL & CL Square Bends Row 19-140 90 68' All Dings >5 volts in Horizontal Run Row 19-140 71 102' All Dings in Rows 1-18 U-Bends 113 89' 20% Dings >5 volts CL Tubesheet to CL Bend 17 23 416 440* In Situ Testing Based on Industry Screening Guidance FPL -13 St. Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Projected Tube Plugging Pr~dictd cNumbir PrchictedNurnm.r of Indliations at of Tub.. R*paired EO :i5 atE FOC IS Mochanismitocation SIG A SIG B SIG A SIC B Axial ODS('C at ls '.cratr Sulqxirts ILtwer 5t 21_00 2178 145S 1257 BLkt Estinlatc 2561 2331 1556 1345 tUppcr954%
V St Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & SIG Condition Benchmark of Predicted (best estimate) vs. Observed Indications Mechanism                     Case     Predicted       Observed Axial ODSCC at Eggcrates             Worst SG     928           1217 Axial ODSCC at Tube Dings           All SGs         2               1 Axial ODSCC at Transition           All SGs       43               16 Axial IDSCC below Transition         All SGs       15               2 Circ. ODSCC at Transition           All SGs       25               17 FPL St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & SIG Condition Probability of Burst (POB)
2722 2485 165.1 1434 Aexial ODSCC Near TTS 30 I0 30 10 ircuinfermntial ODSCC2at 171S I 20 15 20 ANial I DSCC fICAow TriS 5 , S 5 C.irunircrcntiiil iScc .tcibw rrs s 5 S 5 Axi&#xb6;,l Oi )SCC at Dings S 5 5 Best Estimate Cumulative Repairs -3050 -3075 Current Tube Plugging Limit 2520 .;252 : FPL 14 7 I St. Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Tube Sleeving Plans Westinghouse Alloy 800 Leak Limiting Sleeve* 60-70% of Repairable Tubes are Candidates
Mechanism                 SG A         SIG B ODSCC' at E       c029crats                       0.0777 ODSCC at D)ings                             0.00(Y O)SCC at Topofa-Tubcshect                     -0 Cumulatisv P0I3                             0.0356
* Sleeve Tubes that Require Only 1 Sleeve* Maintain 30% Effective Tube Plugging Margin* Contingency for 42% Tube Plugging> Required Repairs Exceed Expectations
* Significant Axial Degradation Mechanisms
' Sleeving Field Effort Difficulties
* Cycle 15 Length for 10% POB Criterion - 17.4 EFPM
-' 15 FPL St. Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Operating Experience
* Cycle 15 Length for 5% POB Criterion - 16.2 EFPM               _   o
* Continue Emphasis on Dings/Dents  
* Planned Cycle 15 Length is -14.5 EFPM                           ,
&Anomalous Indications
FPLI S
* Foreign Object Damage* Batwing Support Condition (Waterford)
 
* Fabrication Issues (Byron & Davis Besse)* Tube to Tube Wear (Tube Sever)' Susceptible Locations to be Reviewed by Lead Analysts.-16 FPL 8 St. Lucie Unit 2 -Si Inspection Plannin, Contingenc Issue or Inspection Item Leaking Plug Crack in Row 1&2 U-bend team Generator g for SL2-16 Crack in U-bend Wear Scar Crack in Cold Leg Ding Foreign Object Wear CL Expansion Transition Cracking Freespan Cracking RCL Indications on Pull Out Scan FPL y Planning ContinQency Action Replace as Necessary Test 100% Affected Rows& 20% Row 3, etc.Test All (A-430, B-290)Test All (A-85, B-1 15)Bound FO Wear Test 100% in Affected SG Validate Bobbin POD Retest if >.35 Volts ,,,&#xa2; <tws-7 17 St. Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Generic Letter 2006-01 Submit LAR to Adopt TSTF-449 By May 31, 2006> Replacement SG Program> Original SG Program* Include Sleeving Repair Method* Include Tubesheet Inspection Provisions (C*)* Administrative Controls-Limit Pri-Sec Leakage to 108 gpd/SG-Address Leakage Predictions for 1 7 Tubesheet
-i St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & S/G Condition In Situ Pressure Testing SL2-9 Through SL2-15
& Sleeves 18 FPL ,es 9 I St. Lucie Unit 2 -Steam Generator Inspection Planning for SL2-16 Summary & Closing* FPL Program Meets Industry Guidance.Comprehensive Inspection Program* Reasonable Assurance of Tube Integrity* Compliance with Tech Specs & NRC Positions* Amend License for TSTF-449* Identify & Address Staff Concerns FPL 19 10}}
* 73 Total Indications (19 at SL2-15)
* Mechanisms Include Axial ODSCC at Eggcrates Axial ODSCC at Dings
                  'LAxial ODSCC at TTS
                  ' Axial IDSCC below TTS Circ ODSCC at TTS
                  ' Circ IDSCC at TTS OD Volumetric TTS
* No Leakage or Burst 5    .- - Bl y . ". . .
* 11 FPL St. Lucie Unit 2- Steam Generator Inspection Planning for SL2-16 SL2-16 Inspection Scope
* Visual Examination of All Tube Plugs
* Bobbin Probe All Active Tubes Screen Dings <5 Volts in Straight Sections
        ' Full Length Row 3-140, Straight Length Row 1-2
* Plus Point Probe 100% Hot Leg Top of Tubesheet (+3" /-13")
Cold Leg Periphery Tubes (+3"/-2")
20% Row 1-2 U-bends (A-23, B-25) 20% Wear at Vertical Straps (A-86, B-58)
        ' .00% Wear at Eggcrates, HL & CL Diagonals (A-274,;B-202)
Full Tubesheet if No Tube Expansion (A-21,-B-1)               1-FPL 6
 
I St Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 SL2-16 Inspection Scope (con't)
* Plus Point Probe for Dings SGA       SGB
      '   All Dings Hot Leg Tubesheet to 1st Support                     68       78
      '   All Dings >5 volts 1st Support to HL Bend                       57       80 All Dings in HL & CL Square Bends Row 19-140 90                           68
      '   All Dings >5 volts in Horizontal Run Row 19-140 71                       102
      '   All Dings in Rows 1-18 U-Bends                                 113       89
      '   20% Dings >5 volts CL Tubesheet to CL Bend                       17       23 416       440
* In Situ Testing Based on Industry Screening Guidance FPL                                                                       -         13 St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Projected Tube Plugging Pr~dictdcNumbir    PrchictedNurnm.r of Indliations at of Tub.. R*paired EO :i5             atE FOCIS Mochanismitocation           SIG A       SIG B SIG A       SIC B Axial ODS('C at ls   '.cratr Sulqxirts ILtwer 5t                       21_00       2178   145S         1257 BLkt Estinlatc                 2561       2331   1556         1345 tUppcr954%                       2722       2485   165.1       1434 Aexial ODSCC Near TTS                   30           I0     30           10 ircuinfermntial ODSCC2at 171S         I         20     15           20 ANial I DSCC fICAow TriS                   5         ,       S           5 C.irunircrcntiiil iScc. tcibw rrs         s         5       S           5 Axi&#xb6;,l Oi)SCC at Dings                     5 S                             5 Best Estimate Cumulative Repairs -3050           -3075 Current Tube Plugging Limit           2520 .;252           :
FPL                                                                                   14 7
 
I St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Tube Sleeving Plans Westinghouse Alloy 800 Leak Limiting Sleeve
* 60-70% of Repairable Tubes are Candidates
* Sleeve Tubes that Require Only 1 Sleeve
* Maintain 30% Effective Tube Plugging Margin
* Contingency for 42% Tube Plugging
          > Required Repairs Exceed Expectations
          ' Sleeving Field Effort Difficulties
                                                  -       '     15 FPL St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Operating Experience
* Continue Emphasis on Dings/Dents &
Anomalous Indications
* Foreign Object Damage
* Batwing Support Condition (Waterford)
* Fabrication Issues (Byron & Davis Besse)
* Tube to Tube Wear (Tube Sever)
        '   Susceptible Locations to be Reviewed by Lead Analysts
                                                .   -16 FPL 8
 
St. Lucie Unit 2 - Siteam Generator Inspection Plannin,g for SL2-16 Contingenc y Planning Issue or Inspection Item                 ContinQency Action Leaking Plug                             Replace as Necessary Crack in Row 1&2 U-bend                   Test 100% Affected Rows
                                            & 20% Row 3, etc.
Crack in U-bend Wear Scar                 Test All (A-430, B-290)
Crack in Cold Leg Ding                   Test All (A-85, B-1 15)
Foreign Object Wear                      Bound FO Wear CL Expansion Transition Cracking         Test 100% in Affected SG Freespan Cracking                         Validate Bobbin POD RCL Indications on Pull Out Scan         Retest if >.35 Volts  ,,,&#xa2; <tws-7 17 FPL St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Generic Letter 2006-01 Submit LAR to Adopt TSTF-449 By May 31, 2006
        >  Replacement SG Program
        > Original SG Program
* Include Sleeving Repair Method
* Include Tubesheet Inspection Provisions (C*)
            *Administrative Controls
                - Limit Pri-Sec Leakage to 108 gpd/SG
                - Address Leakage Predictions for                          1 7 Tubesheet & Sleeves                                  18 FPL                                ,es 9
 
I St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Summary & Closing
* FPL Program Meets Industry Guidance
    . Comprehensive Inspection Program
* Reasonable Assurance of Tube Integrity
* Compliance with Tech Specs & NRC Positions
* Amend License for TSTF-449
* Identify & Address Staff Concerns FPL                                             19 10}}

Latest revision as of 19:34, 23 November 2019

License Presentation Materials from Meeting with FPL Regarding SG Inspection at St. Lucie
ML061110072
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 04/20/2006
From:
Florida Power & Light Co
To:
Office of Nuclear Reactor Regulation
References
Download: ML061110072 (10)


Text

r f

FLORIDA POWER & LIGHT ST. LUCIE UNIT 2 STEAM GENERATOR INSPECTION PLANNING FOR SL2-16, APRIL 2006 St Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 AGENDA

. Purpose of Meeting

. Background & S/G Condition

  • SL2-16 Inspection Scope

. Projected Tube Plugging

  • Operating Experience
  • Contingency Planning

. Summary & Closing 2

FPL 1

V St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Purpose of Meeting

  • Review SL2 S/G Condition
  • Review SL2-15 Inspection Planning
  • Address Staff Concerns St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & S/G Condition
  • SIG Design
  • cEModel 3410
  • 84l1 Tubes I SG
  • A-600 HTMA Tubing
  • CS Lattice Support System (eggcrates)
  • Tubesheet Joint - Explosive
  • Total Tubes Plugged

- SG A - 1469 (17.5%)

- SG B - 1709 (20.3%)

  • T-Hot -600OF FPL ./

2

r St Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & S/G Condition FPL Steam Generator Program

  • Committed to Safe Operation
  • Full Implementation of NEI 97-06, S/G Program Guidelines

' Inspection

' Chemistry Leak Monitoring

  • Incorporate Industry Experience
  • Extensive Examination History at Unit 2 XConservative Approach

&In Situ Pressure Test at Last 6 Inspections ,,- - -

FP 5 FPLop St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & S/G Condition

  • Last Inspection - SL2-15 in January 2005 a Results Discussed with NRR During Outage

' Damage Mechanisms Generally as Expected 1Tube Ding with ODSCC Limited PWSCC in Tubesheet (3in Upper 2", 1 at Tack Roll)

'Increase in Axial ODSCC at Eggcrate Supports

'RCL Indications Detected During Pull Out Scans

'Addressed in OA Model

'Tested with Qualified Technique if > .35 Volts

'No Tube Integrity Issues. A FPL 3

V St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Indication Count Summary for SL2-15 Mechanism SIG A SIG B Total Axial ODSCC at Eggcrate Supports 1184 1266 2450 Axial ODSCC at Diagonal Supports 1 8 9 Axial ODSCC at Tube Dings 0 1 1 Axial ODSCC in Freespans 0 1 1 Axial ODSCC at Top of HL Tubesheet 14 2 16 Axial IDSCC Below Top of HL Tubesheet 1 1 2 Circ. ODSCC at Top of HL Tubesheet 7 10 17 Circ. IDSCC at Top of HL Tubesheet 0 1 1 Circ. IDSCC at HL Tube End 0 1 1 Wear Due to Foreign Objects 1 1 2 Wear at Diagonal & Vertical Supports 672 443 1115 Wear at Eggcrate Tube Supports 67 73 140 FPL St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & S/G Condition TUBE PLUGGING HISTORY Damaae Mechanism (1) 4100 11101 4103 1105 OD Cracks at Tube Supports 14 259 482 1592 Mech. Wear at Tube Supports 18 11 1 OD Cracks at Tubesheet 17 20 27 20 Preservice, FO, Preventative 51 6 2 Circ. OD Cracks at Tubesheet 5 13 10 15 OD Volumetric - Various 2 ID Cracks in Tubesheet 4 3 OD Cracks at Dings 5 1 OD Cracks in Freespan _ 1 1 54 361 530 1635 Cumulative Plugging 652 1013 1543 3178 ,

Cumulative Percent 3.9% 6.0% 9.2% -1B.9%:..

'I (1) Axial unless noted otherwise a_ '8 ot-FPL 4

V St Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & SIG Condition Benchmark of Predicted (best estimate) vs. Observed Indications Mechanism Case Predicted Observed Axial ODSCC at Eggcrates Worst SG 928 1217 Axial ODSCC at Tube Dings All SGs 2 1 Axial ODSCC at Transition All SGs 43 16 Axial IDSCC below Transition All SGs 15 2 Circ. ODSCC at Transition All SGs 25 17 FPL St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & SIG Condition Probability of Burst (POB)

Mechanism SG A SIG B ODSCC' at E c029crats 0.0777 ODSCC at D)ings 0.00(Y O)SCC at Topofa-Tubcshect -0 Cumulatisv P0I3 0.0356

  • Significant Axial Degradation Mechanisms
  • Cycle 15 Length for 10% POB Criterion - 17.4 EFPM
  • Cycle 15 Length for 5% POB Criterion - 16.2 EFPM _ o
  • Planned Cycle 15 Length is -14.5 EFPM ,

FPLI S

-i St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Background & S/G Condition In Situ Pressure Testing SL2-9 Through SL2-15

  • 73 Total Indications (19 at SL2-15)
  • Mechanisms Include Axial ODSCC at Eggcrates Axial ODSCC at Dings

'LAxial ODSCC at TTS

' Axial IDSCC below TTS Circ ODSCC at TTS

' Circ IDSCC at TTS OD Volumetric TTS

  • No Leakage or Burst 5 .- - Bl y . ". . .
  • 11 FPL St. Lucie Unit 2- Steam Generator Inspection Planning for SL2-16 SL2-16 Inspection Scope
  • Visual Examination of All Tube Plugs
  • Bobbin Probe All Active Tubes Screen Dings <5 Volts in Straight Sections

' Full Length Row 3-140, Straight Length Row 1-2

  • Plus Point Probe 100% Hot Leg Top of Tubesheet (+3" /-13")

Cold Leg Periphery Tubes (+3"/-2")

20% Row 1-2 U-bends (A-23, B-25) 20% Wear at Vertical Straps (A-86, B-58)

' .00% Wear at Eggcrates, HL & CL Diagonals (A-274,;B-202)

Full Tubesheet if No Tube Expansion (A-21,-B-1) 1-FPL 6

I St Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 SL2-16 Inspection Scope (con't)

  • Plus Point Probe for Dings SGA SGB

' All Dings Hot Leg Tubesheet to 1st Support 68 78

' All Dings >5 volts 1st Support to HL Bend 57 80 All Dings in HL & CL Square Bends Row 19-140 90 68

' All Dings >5 volts in Horizontal Run Row 19-140 71 102

' All Dings in Rows 1-18 U-Bends 113 89

' 20% Dings >5 volts CL Tubesheet to CL Bend 17 23 416 440

  • In Situ Testing Based on Industry Screening Guidance FPL - 13 St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Projected Tube Plugging Pr~dictdcNumbir PrchictedNurnm.r of Indliations at of Tub.. R*paired EO :i5 atE FOCIS Mochanismitocation SIG A SIG B SIG A SIC B Axial ODS('C at ls '.cratr Sulqxirts ILtwer 5t 21_00 2178 145S 1257 BLkt Estinlatc 2561 2331 1556 1345 tUppcr954% 2722 2485 165.1 1434 Aexial ODSCC Near TTS 30 I0 30 10 ircuinfermntial ODSCC2at 171S I 20 15 20 ANial I DSCC fICAow TriS 5 , S 5 C.irunircrcntiiil iScc. tcibw rrs s 5 S 5 Axi¶,l Oi)SCC at Dings 5 S 5 Best Estimate Cumulative Repairs -3050 -3075 Current Tube Plugging Limit 2520 .;252  :

FPL 14 7

I St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Tube Sleeving Plans Westinghouse Alloy 800 Leak Limiting Sleeve

  • 60-70% of Repairable Tubes are Candidates
  • Maintain 30% Effective Tube Plugging Margin
  • Contingency for 42% Tube Plugging

> Required Repairs Exceed Expectations

' Sleeving Field Effort Difficulties

- ' 15 FPL St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Operating Experience

  • Continue Emphasis on Dings/Dents &

Anomalous Indications

  • Foreign Object Damage
  • Batwing Support Condition (Waterford)
  • Fabrication Issues (Byron & Davis Besse)
  • Tube to Tube Wear (Tube Sever)

' Susceptible Locations to be Reviewed by Lead Analysts

. -16 FPL 8

St. Lucie Unit 2 - Siteam Generator Inspection Plannin,g for SL2-16 Contingenc y Planning Issue or Inspection Item ContinQency Action Leaking Plug Replace as Necessary Crack in Row 1&2 U-bend Test 100% Affected Rows

& 20% Row 3, etc.

Crack in U-bend Wear Scar Test All (A-430, B-290)

Crack in Cold Leg Ding Test All (A-85, B-1 15)

Foreign Object Wear Bound FO Wear CL Expansion Transition Cracking Test 100% in Affected SG Freespan Cracking Validate Bobbin POD RCL Indications on Pull Out Scan Retest if >.35 Volts ,,,¢ <tws-7 17 FPL St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Generic Letter 2006-01 Submit LAR to Adopt TSTF-449 By May 31, 2006

> Replacement SG Program

> Original SG Program

  • Include Sleeving Repair Method
  • Include Tubesheet Inspection Provisions (C*)
  • Administrative Controls

- Limit Pri-Sec Leakage to 108 gpd/SG

- Address Leakage Predictions for 1 7 Tubesheet & Sleeves 18 FPL ,es 9

I St. Lucie Unit 2 - Steam Generator Inspection Planning for SL2-16 Summary & Closing

  • FPL Program Meets Industry Guidance

. Comprehensive Inspection Program

  • Reasonable Assurance of Tube Integrity
  • Compliance with Tech Specs & NRC Positions
  • Identify & Address Staff Concerns FPL 19 10