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| {{#Wiki_filter:REGUL INFORMATION DISTRIBUTI YSTEM (RIDS)ACCESSION NBR: 8710080068 DOC.DATE: 87/10/01 NOTARIZED: | | {{#Wiki_filter:REGUL INFORMATION DISTRIBUTI YSTEM (RIDS) |
| NO'OCKET 5 FACIL: STN-50-528 Palo Verde Nuclear Stations Unit 1~Arizona Publi 05000528 AUTH.NAME AUTHOR AFFILIATION BRADISHi T.R.Arizona Nuclear Power Prospect (formerly Arizona Public Serv HAYNES'.G.Arizona Nuclear Poeer Prospect (formerlg Arizona Public Serv RECIP.NAME RECIPIENT AFFILIATION | | ACCESSION NBR: 8710080068 DOC. DATE: 87/10/01 NOTARIZED: NO 'OCKET 5 FACIL: STN-50-528 Palo Verde Nuclear Stations Unit 1 Arizona Publi 05000528 |
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| | AUTH. NAME AUTHOR AFFILIATION BRADISHi T. R. Arizona Nuclear Power Prospect (formerly Arizona Public Serv HAYNES'. G. Arizona Nuclear Poeer Prospect (formerlg Arizona Public Serv RECIP. NAME RECIPIENT AFFILIATION |
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER 87-024-00: | | LER 87-024-00: on 870902'wo DMA interface cards providing input to core operating limit supervisory sos found incorrectly installed. Caused bg cognitive personnel error Comp uter technic ian counsel ed. W/871001 l tr. |
| on 870902'wo DMA interface cards providing input to core operating limit supervisory sos found incorrectly installed. | | DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR ENCL SIZE: |
| Caused bg cognitive personnel error Comp uter technic ian counsel ed.W/871001 l tr.DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR ENCL SIZE: TITLE: 50.73 Licensee Event Report (LER)i In'cident Rpt>etc.NOTES: Standardi zed plant.05000528 REC IP IENT ID CODE/NAME PD5 LA LICITRAi E COPIES LTTR ENCL 1 1 1 1 RECIPIENT ID CODE/NAME PD5 PD DAVIS>M COPIES LTTR ENCL 1 1 1 INTERNAL: ACRS MICHELSON*EOD/DOA AEOD/DSP/ROAB DEDRO NRR/DEST/CEB NRR/DEST/I CSB NRR/DEST/MTB NRR/DEST/RSB NRR/DLPQ/HFB NRR/DOEA/EAB NRR/DREP/RPB NRR/PMAS/ILRB RES DEPY GI RES/DE/EIB EXTERNAL: EGGG GROH>M LPDR NSI C HARR ISe J NOTES: 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 5 5 1 1 1 1 ACRS MOELLER AEOD/DSP/NAS AEOD/DSP/TPAB NRR/DEST/ADS NRR/DEST/ELB NRR/DEST/MEB NRR/DEST/PSB NRR/DEST/SGB NRR/DLPQ/QAB NRR/DREP/RAB NR D S/SIB REG FILE 02 RES TELFORD.J RGN5 FILE 01 H ST LOBBY WARD NRC PDR.NSIC MAYST G 2 2 1 1 1 1 0 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 TOTAL NUMBER OF COPIES REQUIRED: LTTR 46 ENCL 45 I I 1 t I l NRC Form 355 (933 I LICENSEE EVENT REPORT{LER)US, NUCLEAR REOULATORY COMMISSION APPROVED OMB NO.3)500104 EXPIRES;5/31/SB FACILITY NAME (I)nit 1 DOCKET NUMBER (2)0 5 0 0 0 PA 3 1 OF 4 Core Operating Limit Supervisory System Rendered Inoperable Due to Reversed Circuit Cards EVENT DATE ISI MONTH OAY YEAR YEAR:cscyh SERVE NTIAL NUMBER LER NUMBER (SI IIEvsstors NUMSESI REPORT DATE (7)MONTH DAY YEAR OTHER FACILI1IES INVOLVED (SI FACILITY NAMES DOCKET NUMBER(S)0 5 0 0 0 N/A 0 902 8787 0 2 4 0 1001 8 7 N A 0 5 0 0 0 OPERATINO MODE (~)POWER LEYEL 2 0 20.402(el 20.405 (~)(I I (il 20.405(el(1)(ii) 20.405(~I (11(oil 20.405(~II1)(ir)20.405(~I(1)(v)20.405(c)50.35(el(1(50.35(c)(2)50.73(e)(2)(i)50.734)(2)(E)50.7 34)(2)I IE I LICENSEE CONTACT FOR THIS LER (12)50.734((2(l iv)50.734)(2)4)50.73(e)(2l(rQI 50.734)(2)(r(EI(AI 50.7 3(e I (2)(riii I I 5 I 50.73(e)(21(al THIS REPORT IS SUBMITTED PURSUAN'1 T 0 THE REOUIREMENTS OF 10 CFR (): (Check one or mori of thi follow/no/ | | TITLE: 50. 73 Licensee Event Report (LER) i In'cident Rpt> etc. |
| (11 73.71 (II)73.71(c)OTHER ISpec/fy In Ahstrect below era//n Teat, HIIC Form 3$SAI NAME Thomas R.Bradish, Compliance Su ervisor TELEPHONE NUMBER AREA CODE 602 393-353 1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRI~EO IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFAQ TURER CAUSE SYSTEM COMPONENT MANUFAC.TURER:4 Bl)NA))".c(p-saic.
| | NOTES: Standardi zed plant. 05000528 REC IP IENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 1 PD5 PD 1 1 LICITRAiE 1 1 DAVIS> M 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 |
| IGC PU 2 6 N X IGC PU 2 6 N SUPPLEMENTAL REPORT EXPECTED (14)X NO YES Ilf yeL COmpleie EXPECTED St/Sht/SSIOSI DATE/AssTRAGT ILimlt to te00 spaces, I 4, epproaimetely fifteen ssnpre speci typewri Hen IinNI (15)MONTH DAY YEAR EXPECTED SUBMISSION DATE (15)On September 2, 1987 at 0815 MST, with Unit 1 in Mode 1 (POWER OPERATION) operating at approximately 59 percent power, it was identified that two DMA Interface Cards providing input to the Core Operating Limit Supervisory System (COLSS)had been incorrectly installed.
| | *EOD/DOA 1 1 AEOD/DSP/NAS 1 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TPAB 1 1 DEDRO 1 1 NRR/DEST/ADS 0 NRR/DEST/CEB 1 1 NRR/DEST/ELB 1 1 NRR/DEST/I CSB 1 1 NRR/DEST/MEB 1 1 NRR/DEST/MTB 1 1 NRR/DEST/PSB 1 NRR/DEST/RSB 1 1 NRR/DEST/SGB 1 NRR/DLPQ/HFB 1 1 NRR/DLPQ/QAB 1 NRR/DOEA/EAB 1 1 NRR/DREP/RAB 1 1 NRR/DREP/RPB 2 2 NR D S/SIB 1 NRR/PMAS/ ILRB 1 1 REG FILE 02 1 1 RES DEPY GI 1 1 RES TELFORD. J 1 1 RES/DE/EIB 1 RGN5 FILE 01 1 EXTERNAL: EGGG GROH> M 5 5 H ST LOBBY WARD 1 LPDR 1 1 NRC PDR. 1 1 NSI C HARR ISe J 1 1 NSIC MAYST G 1 NOTES: |
| This rendered the COLSS inoperable.
| | TOTAL NUMBER OF COPIES REQUIRED: LTTR 46 ENCL 45 |
| Technical Specifications 4.2.1.2 and 4.2.4.2 which require monitoring of certain reactor core operating characteristics every 2 hours when COLSS is inoperable above 20 percent rated thermal power were not met beginning at 0106 through 0815 on September 2, 1987.The root cause of the event has been determined to be a cognitive personnel error by a computer technician who inadvertently reversed the two cards during troubleshooting under approved work order documents.
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| The technician did not obtain independent verification of the serial numbers and addresses for the cards which were being changed during the troubleshooting efforts.This is contrary to an approved procedure (work order).As immediate corrective action, the cards were returned locations and COLSS was restored to an operable status.recurrence, the computer technician has been counselled accuracy of his work as well as when it is necessary to verifications conducted.
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| to their correct In order to prevent on the importance of the have independent There have been no previous similar events reported.NRC Perm 345 8710080068 871001 PDR ADOCK 05000528 S PDR
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| NRC Form 455A 19451 LICENSEE EVENT REPORT (LER)TEXT CONTINUATION US.NUCLEAR REOULATORY COMM)55)ON APPROYEO OMS NO 5)EO~ICe EKPIRES;4)S)lSS FACILITY NAME III OOCKET NUEISER LT)YEAR LER NUMSEII I~)5E QV 5 NTI*L NVM ER r)5 v l5 Io rr RVM ER~AOE LT)Palo Verde Unit 1 TEKT llf mare eaece)I reaaeerE eee~H)IC Farm JSSA'5))IT)0 5 0 0 0 5 2 8 8 7 024 0 0 2 oF 0 On September 2, 1987 at 0815 MST, with Unit 1 in Mode 1 (POWER OPERATION) operating at approximately 59 percent power, it was identified that two DMA Interface Cards (CPU)had been incorrectly installed in Remote Input Subsystems (RIS)"B" and"D".This resulted in the Core Operating Limit Supervisory System (COLSS)(IG) receiving reversed incore detector (DET)signals for detectors processed through RIS's"B" and"D", thereby rendering COLSS inoperable.
| | I I |
| With COLSS inoperable, Technical Specification Surveillance Requirements (TSSR)4.2.1.2 and 4.2.4.2 require monitoring of the reactor core (AC)operating characteristics Linear Heat Rate (LHR)and Departure from Nucleate Boiling Ratio (DNBR)margin every 2 hours when the unit is operated at greater than 20 percent rated thermal power.Unit 1 increased power above 20 percent at approximately 0106 on September 2, 1987.Therefore, for approximately 7 hours COLSS was inoperable and the TSSRs were not met.In addition, the ACTION Statement for Technical Specification 3.3.3.2 was exceeded since approximately 50 percent of the incore detectors were rendered inoperable due to the reversed cards.While conducting routine monitoring of plant status during startup of Unit 1 on September 1, 1987, Operations identified that portions of the COLSS data being obtained were not as expected, but were still within the Technical Specification'imits.
| | 1 t |
| Following discussions with-Reactor Engineering, Unit 1 continued power ascension beyond 20 percent.On the morning of September 2, 1987, Reactor Engineering was comparing the results of the previous surveillance tests for incore detectors (72ST-9RX08) with data obtained at approximately 8 percent power and identified a potential discrepancy.
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| Incore detectors which were known to be out of service were now operating and detectors which had been operating were now out of service.The Operations Computer Department investigated the problem and discovered that two DMA Interface Cards were reversed.This resulted in the computer (CPU)system considering RIS"B" incore detectors to be in the"D" quadrant of the reactor core and RIS"D" detectors in the"B" quadrant.The discovery of the improperly installed cards resulted in the COLSS being declared inoperable at 0815.The root cause of the event has been determined to be a cognitive personnel'error by a computer technician (utility non-licensed) who inadvertently reversed the cards while troubleshooting under approved work order documents.
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| The troubleshooting consisted of changing cards between different RISs to determine which, if any, card(s)were not functioning properly.The technician did not obtain independent verification of the serial numbers and addresses for the cards which were being changed during the troubleshooting efforts.This is contrary to an approved procedure (work order).The cards which were identified as not functioning properly (Honeywell, Inc., Model Nos.51302564 and 51302567)will be evaluated/reworked under the existing work control program."rRC rORM 555k 19 45r jl I NAC Porrrr 3CCA 19S)31 FACILITY NAME III LICENSEE EVENT REPORT ILER)TEXT CONTINUATION OOCKET NUMCEA 13)U.d, NUCLEAR AEOULATOA T COMM)SCION APPAOVEO OMd NO 3IEO~ICS EXP)RES)3/3)IIX)LER NUMEEA Id)PACE)3)Palo Verde Unit 1 TEXT III mort soon is ttlrttsL t>>ostsooo)PIAC forrII 3CC)A'I)I 17)YEAR o s o o o 528 87 CCOVCN'IIAL NVM CA 024:Ir)<OCVICION NVM CA-0 0.03oFO 4 As immediate corrective action, the required surveillance test (72ST-9RX03) was initiated at 0820 to meet the applicable Technical Specification ACTION Statements for the inoperable COLSS.Concurrently, the computer technician reinstalled the two cards in their correct locations and obtained independent verification of this action.Independent verification was also performed on those cards which had been removed/reinstalled during the troubleshooting work orders to ensure they were in their correct locations.
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| The incore detector surveillance test (72ST-9RX08) was successfully completed and COLSS was declared operable at 1256 on September 2, 1987.As corrective action to prevent recurrence, the technician has been counselled on the importance of the accuracy of his work as well as when it is necessary to have independent verifications conducted.
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| As a prudent measure, the work order forms utilized for removal/reinstallation of components will be evaluated for adequacy.Upon completion of this evaluation, computer technicians who perform similar types of work will be briefed on the event, the requirements for independent verification of their work, and planned changes to the removal/reinstallation forms, if any.The COLSS provides the plant operators a means of directly monitoring the reactor core status (LHR and DNBR)in order to ensure that the Technical Specification Limiting Conditions for Operation are maintained.
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| However, it is the Core Protection Calculators (CPC)(JC)which utilize the incore detectors (DET)and initiate the automatic protective function (reactor trip)when the predetermined values for Local Power Density (same as Linear Heat Rate)and DNBR are exceeded.Although the values for LHR and DNBR margin could not be correctly monitored from 0106 through 0815 using COLSS, the CPCs were unaffected by the mispositioned cards and available during the event to provide the automatic protective function.CPC Channel"D" (which represents approximately one quadrant of the reactor core)was monitored during the event by the Control Room Operators every 2 hours for Local Power Density (LPD)and DNBR margin as required by Operating Department Guideline No.46.These values were within the Technical Specification values.The shiftly surveillance test (41ST-1ZZ33) which was performed at 2325 on September 1, 1987 prior to the event and at 1235 on September 2, 1987 after the event verified that the maximum deviation between the four channels of LPD and DNBR margin were within the limits specified in the surveillance test.A review of the maximum deviation values and CPC Channel"D" monitoring results indicate that the values for LPD and DNBR for the other three CPC channels would have been within the limits specified in the Technical Specifications.
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| Also, the values which were obtained for LHR and DNBR margin during the performance of surveillance test 72ST-9RX03 following the discovery of the reversed cards were found to be within the acceptance criteria for all four CPC channels.Therefore, this event posed no threat to the health and safety of the public or to the safe operation of the plant, NIIC I OIIM 555k 19 CTI II r'l t NAC form 344A (9 83)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR AEQULATORY COMMISSION APPAOVED OMS NO.3150MIOS EXPIRES: 8/81/88 FACILITY NAME III DOCKET NUMSER)QI YEAR LER NUMSER)4)SEQUENT/AL NUM tr))yet NEVIS/ON:~O NI/M PACE C))Palo Verde Unit 1 TEXT///moro sof Io/I tot/irod.rrw~H/IC form 8//SAT/l)1)0 5 0 0 0 5 2 8 8 7 024 000 4 oF 0 There were no structures, components, or systems that were inoperable at the start of the event, other than those previously described, that contributed to the event.There were no unusual characteristic's of the work location which contributed to the event.There were no automatic or manually initiated safety system responses.
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| Should other concerns or information pertinent to this event be discovered, a supplement to this report will be issued.There have been no previous similar events reported.4oc roAM ssso 19 8)I
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| Arizona Nuclear Power Project P.O.BOX 52034~PHOENIX, ARIZONA 85072-2034 192-00284-JGH/TRB/TJB October 1, 1987 Document Control Desk U.S.Nuclear Regulatory Commission
| | NRC Form 355 US, NUCLEAR REOULATORY COMMISSION (933 I APPROVED OMB NO. 3)500104 LICENSEE EVENT REPORT {LER) EXPIRES; 5/31/SB FACILITY NAME (I) DOCKET NUMBER (2) PA 3 nit 1 0 5 0 0 0 1 OF 4 Core Operating Limit Supervisory System Rendered Inoperable Due to Reversed Circuit Cards EVENT DATE ISI LER NUMBER (SI REPORT DATE (7) OTHER FACILI1IES INVOLVED (SI MONTH OAY YEAR YEAR SERVE NTIAL IIEvsstors DAY FACILITYNAMES DOCKET NUMBER(S) |
| 'ashington, D.C.20555
| | :cscyh NUMBER NUMSESI MONTH YEAR N/A 0 5 0 0 0 0 902 8787 0 2 4 0 1001 8 7 N A 0 5 0 0 0 THIS REPORT IS SUBMITTED PURSUAN'1 T 0 THE REOUIREMENTS OF 10 CFR (): (Check one or mori of thi follow/no/ (11 OPERATINO MODE ( ~ ) 20.402(el 20.405(c) 50.734((2( l iv) 73.71 (II) |
| | POWER 20.405 (~ ) (I I (il 50.35(el(1( 50.734) (2) 4) 73.71(c) |
| | LEYEL 2 0 20.405(el(1)(ii) 50.35(c) (2) 50.73(e)(2l(rQI OTHER ISpec/fy In Ahstrect below era/ /n Teat, HIIC Form 20.405( ~ I (11(oil 50.73(e) (2)(i) 50.734) (2)(r(EI(AI 3$ SAI 20.405( ~ II1)(ir) 50.734) (2)(E) 50.7 3(e I (2)(riiiI I 5 I 20.405( ~ I(1)(v) 50.7 34)(2) I IE I 50.73(e)(21(al LICENSEE CONTACT FOR THIS LER (12) |
| | NAME TELEPHONE NUMBER AREA CODE Thomas R. Bradish, Compliance Su ervisor 602 393- 353 1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRI ~ EO IN THIS REPORT (13) |
| | CAUSE SYSTEM COMPONENT MANUFAQ MANUFAC. |
| | TURER CAUSE SYSTEM COMPONENT TURER |
| | :4 Bl)NA))".c(p-saic. |
| | IGC PU 2 6 N X IGC PU 2 6 N SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED SUBMISSION DATE (15) |
| | YES Ilf yeL COmpleie EXPECTED St/Sht/SSIOSI DATE/ |
| | X NO AssTRAGT ILimlt to te00 spaces, I 4, epproaimetely fifteen ssnpre speci typewri Hen IinNI (15) |
| | On September 2, 1987 at 0815 MST, with Unit 1 in Mode 1 (POWER OPERATION) operating at approximately 59 percent power, it was identified that two DMA Interface Cards providing input to the Core Operating Limit Supervisory System (COLSS) had been incorrectly installed. This rendered the COLSS inoperable. |
| | Technical Specifications 4.2.1.2 and 4.2.4.2 which require monitoring of certain reactor core operating characteristics every 2 hours when COLSS is inoperable above 20 percent rated thermal power were not met beginning at 0106 through 0815 on September 2, 1987. |
| | The root cause of the event has been determined to be a cognitive personnel error by a computer technician who inadvertently reversed the two cards during troubleshooting under approved work order documents. The technician did not obtain independent verification of the serial numbers and addresses for the cards which were being changed during the troubleshooting efforts. This is contrary to an approved procedure (work order). |
| | As immediate corrective action, the cards were returned to their correct locations and COLSS was restored to an operable status. In order to prevent recurrence, the computer technician has been counselled on the importance of the accuracy of his work as well as when it is necessary to have independent verifications conducted. |
| | There have been no previous similar events reported. |
| | 8710080068 871001 PDR ADOCK 05000528 NRC Perm 345 S PDR |
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| ==Dear Sirs:== | | NRC Form 455A 19451 US. NUCLEAR REOULATORY COMM)55)ON LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROYEO OMS NO 5)EO~ICe EKPIRES; 4)S) lSS FACILITY NAME III OOCKET NUEISER LT) |
| | LER NUMSEII I ~ ) ~ AOE LT) |
| | YEAR 5E QV 5 NTI*L r) 5 v l5 Io rr NVM ER RVM ER Palo Verde Unit TEKT llfmare eaece )I reaaeerE eee ~ 1 H)IC Farm JSSA'5) ) IT) 0 5 0 0 0 5 2 8 8 7 024 0 0 2 oF 0 On September 2, 1987 at 0815 MST, with Unit 1 in Mode 1 (POWER OPERATION) operating at approximately 59 percent power, Interface Cards (CPU) had been incorrectly installed in Remote Input Subsystems it was identified that two DMA (RIS) "B" and "D". This resulted in the Core Operating Limit Supervisory System (COLSS)(IG) receiving reversed incore detector (DET) signals for detectors processed through RIS's "B" and "D", thereby rendering COLSS inoperable. With COLSS inoperable, Technical Specification Surveillance Requirements (TSSR) 4.2.1.2 and 4.2.4.2 require monitoring of the reactor core (AC) operating characteristics Linear Heat Rate (LHR) and Departure from Nucleate Boiling Ratio (DNBR) margin every 2 hours when the unit is operated at greater than 20 percent rated thermal power. Unit 1 increased power above 20 percent at approximately 0106 on September 2, 1987. Therefore, for approximately 7 hours COLSS was inoperable and the TSSRs were not met. In addition, the ACTION Statement for Technical Specification 3.3.3.2 was exceeded since approximately 50 percent of the incore detectors were rendered inoperable due to the reversed cards. |
| | While conducting routine monitoring of plant status during startup of Unit 1 on September 1, 1987, Operations identified that portions of the COLSS data being obtained were not as expected, but were still within the Technical Following discussions with -Reactor Engineering, Unit 1 continued power Specification'imits. |
| | ascension beyond 20 percent. On the morning of September 2, 1987, Reactor Engineering was comparing the results of the previous surveillance tests for incore detectors (72ST-9RX08) with data obtained at approximately 8 percent power and identified a potential discrepancy. Incore detectors which were known to be out of service were now operating and detectors which had been operating were now out of service. The Operations Computer Department investigated the problem and discovered that two DMA Interface Cards were reversed. This resulted in the computer (CPU) system considering RIS "B" incore detectors to be in the "D" quadrant of the reactor core and RIS "D" detectors in the "B" quadrant. The discovery of the improperly installed cards resulted in the COLSS being declared inoperable at 0815. |
| | The root cause of the event has been determined to be a cognitive personnel |
| | 'error by a computer technician (utility non-licensed) who inadvertently reversed the cards while troubleshooting under approved work order documents. The troubleshooting consisted of changing cards between different RISs to determine which, if any, card(s) were not functioning properly. The technician did not obtain independent verification of the serial numbers and addresses for the cards which were being changed during the troubleshooting efforts. This is contrary to an approved procedure (work order). The cards which were identified as not functioning properly (Honeywell, Inc., Model Nos. 51302564 and 51302567) will be evaluated/reworked under the existing work control program. |
| | "rRC rORM 555k 19 45r |
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| | jl I |
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| | NAC Porrrr 3CCA 19S) 31 U.d, NUCLEAR AEOULATOAT COMM)SCION LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPAOVEO OMd NO 3IEO~ICS EXP)RES) 3/3) IIX) |
| | FACILITY NAME III OOCKET NUMCEA 13) |
| | LER NUMEEA Id) PACE )3) |
| | YEAR CCOVCN'IIAL :Ir)< OCVICION NVM CA NVM CA Palo Verde Unit TEXT IIImort soon is ttlrttsL t>> ostsooo) 1 PIAC forrII 3CC)A'I) I 17) o s o o o 528 87 024 0 0. 03oFO 4 As immediate corrective action, the required surveillance test (72ST-9RX03) was initiated at 0820 to meet the applicable Technical Specification ACTION Statements for the inoperable COLSS. Concurrently, the computer technician reinstalled the two cards in their correct locations and obtained independent verification of this action. Independent verification was also performed on those cards which had been removed/reinstalled during the troubleshooting work orders to ensure they were in their correct locations. The incore detector surveillance test (72ST-9RX08) was successfully completed and COLSS was declared operable at 1256 on September 2, 1987. |
| | As corrective action to prevent recurrence, the technician has been counselled on the importance of the accuracy of his work as well as when it is necessary to have independent verifications conducted. As a prudent measure, the work order forms utilized for removal/reinstallation of components will be evaluated for adequacy. Upon completion of this evaluation, computer technicians who perform similar types of work will be briefed on the event, the requirements for independent verification of their work, and planned changes to the removal/reinstallation forms, if any. |
| | The COLSS provides the plant operators a means of directly monitoring the reactor core status (LHR and DNBR) in order to ensure that the Technical Specification Limiting Conditions for Operation are maintained. However, it is the Core Protection Calculators (CPC)(JC) which utilize the incore detectors (DET) and initiate the automatic protective function (reactor trip) when the predetermined values for Local Power Density (same as Linear Heat Rate) and DNBR are exceeded. Although the values for LHR and DNBR margin could not be correctly monitored from 0106 through 0815 using COLSS, the CPCs were unaffected by the mispositioned cards and available during the event to provide the automatic protective function. |
| | CPC Channel "D" (which represents approximately one quadrant of the reactor core) was monitored during the event by the Control Room Operators every 2 hours for Local Power Density (LPD) and DNBR margin as required by Operating Department Guideline No. 46. These values were within the Technical Specification values. The shiftly surveillance test (41ST-1ZZ33) which was performed at 2325 on September 1, 1987 prior to the event and at 1235 on September 2, 1987 after the event verified that the maximum deviation between the four channels of LPD and DNBR margin were within the limits specified in the surveillance test. A review of the maximum deviation values and CPC Channel "D" monitoring results indicate that the values for LPD and DNBR for the other three CPC channels would have been within the limits specified in the Technical Specifications. Also, the values which were obtained for LHR and DNBR margin during the performance of surveillance test 72ST-9RX03 following the discovery of the reversed cards were found to be within the acceptance criteria for all four CPC channels. Therefore, this event posed no threat to the health and safety of the public or to the safe operation of the plant, NIIC I OIIM 555k 19 CTI |
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| | r'l II t |
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| | NAC form 344A U.S. NUCLEAR AEQULATORY COMMISSION (9 83) |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPAOVED OMS NO. 3150MIOS EXPIRES: 8/81/88 FACILITY NAME III DOCKET NUMSER )QI LER NUMSER )4) PACE C)) |
| | YEAR SEQUENT/AL )yet NEVIS/ON NUM tr) :~O NI/M Palo Verde Unit TEXT /// moro sof Io /I tot/irod. rrw ~ 1 H/IC form 8//SAT/ l)1) 0 5 0 0 0 5 2 8 8 7 024 components, or systems that were inoperable at the 000 4 oF 0 There were no structures, start of the event, other than those previously described, that contributed to the event. There were no unusual characteristic's of the work location which contributed to the event. There were no automatic or manually initiated safety system responses. Should other concerns or information pertinent to this event be discovered, a supplement to this report will be issued. |
| | There have been no previous similar events reported. |
| | 4oc roAM ssso 19 8) I |
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| | Arizona Nuclear Power Project P.O. BOX 52034 ~ PHOENIX, ARIZONA 85072-2034 192-00284-JGH/TRB/TJB October 1, 1987 Document Control Desk U.S. Nuclear Regulatory Commission D.C. 20555 'ashington, |
| | |
| | ==Dear Sirs:== |
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| ==Subject:== | | ==Subject:== |
| Palo Verde Nuclear Generating Station (PVNGS)Unit 1 Docket No.50-528 Licensee Event Report 1-87-024-00 File: 87-020-404 Attached please find Licensee Event Report (LER)No.1-87-024-00 prepared and submitted pursuant to 10CFR 50.73.In accordance with 10CFR 50.73(d), we are herewith forwarding a copy of the LER to the Regional Administrator of the Region V Office.If you have any questions, please contact T.R.Bradish, Compliance Supervisor at (602)393-3531.Very tr ly yours, UA uy~~-J.G.Haynes Vice President Nuclear Production JGH/TJB/cld Attachment cc: 0.M.DeMichele E.E.Van Brunt, Jr.J.B.Martin R.C.Sorenson E.A.Licitra A.C.Gehr INPO Records Center (all w/a)}} | | Palo Verde Nuclear Generating Station (PVNGS) |
| | Unit 1 Docket No. 50-528 Licensee Event Report 1-87-024-00 File: 87-020-404 Attached please find Licensee Event Report (LER) No. 1-87-024-00 prepared and submitted pursuant to 10CFR 50.73. In accordance with 10CFR 50.73(d), we are herewith forwarding a copy of the LER to the Regional Administrator of the Region V Office. |
| | If you have any questions, please contact T. R. Bradish, Compliance Supervisor at (602) 393-3531. |
| | Very tr ly yours, UA uy~~ |
| | J. G. Haynes Vice President Nuclear Production JGH/TJB/cld Attachment cc: 0. M. DeMichele (all w/a) |
| | E. E. Van Brunt, Jr. |
| | J. B. Martin R. C. Sorenson E. A. Licitra A. C. Gehr INPO Records Center}} |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
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REGUL INFORMATION DISTRIBUTI YSTEM (RIDS)
ACCESSION NBR: 8710080068 DOC. DATE: 87/10/01 NOTARIZED: NO 'OCKET 5 FACIL: STN-50-528 Palo Verde Nuclear Stations Unit 1 Arizona Publi 05000528
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AUTH. NAME AUTHOR AFFILIATION BRADISHi T. R. Arizona Nuclear Power Prospect (formerly Arizona Public Serv HAYNES'. G. Arizona Nuclear Poeer Prospect (formerlg Arizona Public Serv RECIP. NAME RECIPIENT AFFILIATION
SUBJECT:
LER 87-024-00: on 870902'wo DMA interface cards providing input to core operating limit supervisory sos found incorrectly installed. Caused bg cognitive personnel error Comp uter technic ian counsel ed. W/871001 l tr.
DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR ENCL SIZE:
TITLE: 50. 73 Licensee Event Report (LER) i In'cident Rpt> etc.
NOTES: Standardi zed plant. 05000528 REC IP IENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 1 PD5 PD 1 1 LICITRAiE 1 1 DAVIS> M 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2
- EOD/DOA 1 1 AEOD/DSP/NAS 1 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TPAB 1 1 DEDRO 1 1 NRR/DEST/ADS 0 NRR/DEST/CEB 1 1 NRR/DEST/ELB 1 1 NRR/DEST/I CSB 1 1 NRR/DEST/MEB 1 1 NRR/DEST/MTB 1 1 NRR/DEST/PSB 1 NRR/DEST/RSB 1 1 NRR/DEST/SGB 1 NRR/DLPQ/HFB 1 1 NRR/DLPQ/QAB 1 NRR/DOEA/EAB 1 1 NRR/DREP/RAB 1 1 NRR/DREP/RPB 2 2 NR D S/SIB 1 NRR/PMAS/ ILRB 1 1 REG FILE 02 1 1 RES DEPY GI 1 1 RES TELFORD. J 1 1 RES/DE/EIB 1 RGN5 FILE 01 1 EXTERNAL: EGGG GROH> M 5 5 H ST LOBBY WARD 1 LPDR 1 1 NRC PDR. 1 1 NSI C HARR ISe J 1 1 NSIC MAYST G 1 NOTES:
TOTAL NUMBER OF COPIES REQUIRED: LTTR 46 ENCL 45
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NRC Form 355 US, NUCLEAR REOULATORY COMMISSION (933 I APPROVED OMB NO. 3)500104 LICENSEE EVENT REPORT {LER) EXPIRES; 5/31/SB FACILITY NAME (I) DOCKET NUMBER (2) PA 3 nit 1 0 5 0 0 0 1 OF 4 Core Operating Limit Supervisory System Rendered Inoperable Due to Reversed Circuit Cards EVENT DATE ISI LER NUMBER (SI REPORT DATE (7) OTHER FACILI1IES INVOLVED (SI MONTH OAY YEAR YEAR SERVE NTIAL IIEvsstors DAY FACILITYNAMES DOCKET NUMBER(S)
- cscyh NUMBER NUMSESI MONTH YEAR N/A 0 5 0 0 0 0 902 8787 0 2 4 0 1001 8 7 N A 0 5 0 0 0 THIS REPORT IS SUBMITTED PURSUAN'1 T 0 THE REOUIREMENTS OF 10 CFR (): (Check one or mori of thi follow/no/ (11 OPERATINO MODE ( ~ ) 20.402(el 20.405(c) 50.734((2( l iv) 73.71 (II)
POWER 20.405 (~ ) (I I (il 50.35(el(1( 50.734) (2) 4) 73.71(c)
LEYEL 2 0 20.405(el(1)(ii) 50.35(c) (2) 50.73(e)(2l(rQI OTHER ISpec/fy In Ahstrect below era/ /n Teat, HIIC Form 20.405( ~ I (11(oil 50.73(e) (2)(i) 50.734) (2)(r(EI(AI 3$ SAI 20.405( ~ II1)(ir) 50.734) (2)(E) 50.7 3(e I (2)(riiiI I 5 I 20.405( ~ I(1)(v) 50.7 34)(2) I IE I 50.73(e)(21(al LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE Thomas R. Bradish, Compliance Su ervisor 602 393- 353 1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRI ~ EO IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAQ MANUFAC.
TURER CAUSE SYSTEM COMPONENT TURER
- 4 Bl)NA))".c(p-saic.
IGC PU 2 6 N X IGC PU 2 6 N SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED SUBMISSION DATE (15)
YES Ilf yeL COmpleie EXPECTED St/Sht/SSIOSI DATE/
X NO AssTRAGT ILimlt to te00 spaces, I 4, epproaimetely fifteen ssnpre speci typewri Hen IinNI (15)
On September 2, 1987 at 0815 MST, with Unit 1 in Mode 1 (POWER OPERATION) operating at approximately 59 percent power, it was identified that two DMA Interface Cards providing input to the Core Operating Limit Supervisory System (COLSS) had been incorrectly installed. This rendered the COLSS inoperable.
Technical Specifications 4.2.1.2 and 4.2.4.2 which require monitoring of certain reactor core operating characteristics every 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> when COLSS is inoperable above 20 percent rated thermal power were not met beginning at 0106 through 0815 on September 2, 1987.
The root cause of the event has been determined to be a cognitive personnel error by a computer technician who inadvertently reversed the two cards during troubleshooting under approved work order documents. The technician did not obtain independent verification of the serial numbers and addresses for the cards which were being changed during the troubleshooting efforts. This is contrary to an approved procedure (work order).
As immediate corrective action, the cards were returned to their correct locations and COLSS was restored to an operable status. In order to prevent recurrence, the computer technician has been counselled on the importance of the accuracy of his work as well as when it is necessary to have independent verifications conducted.
There have been no previous similar events reported.
8710080068 871001 PDR ADOCK 05000528 NRC Perm 345 S PDR
NRC Form 455A 19451 US. NUCLEAR REOULATORY COMM)55)ON LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROYEO OMS NO 5)EO~ICe EKPIRES; 4)S) lSS FACILITY NAME III OOCKET NUEISER LT)
LER NUMSEII I ~ ) ~ AOE LT)
YEAR 5E QV 5 NTI*L r) 5 v l5 Io rr NVM ER RVM ER Palo Verde Unit TEKT llfmare eaece )I reaaeerE eee ~ 1 H)IC Farm JSSA'5) ) IT) 0 5 0 0 0 5 2 8 8 7 024 0 0 2 oF 0 On September 2, 1987 at 0815 MST, with Unit 1 in Mode 1 (POWER OPERATION) operating at approximately 59 percent power, Interface Cards (CPU) had been incorrectly installed in Remote Input Subsystems it was identified that two DMA (RIS) "B" and "D". This resulted in the Core Operating Limit Supervisory System (COLSS)(IG) receiving reversed incore detector (DET) signals for detectors processed through RIS's "B" and "D", thereby rendering COLSS inoperable. With COLSS inoperable, Technical Specification Surveillance Requirements (TSSR) 4.2.1.2 and 4.2.4.2 require monitoring of the reactor core (AC) operating characteristics Linear Heat Rate (LHR) and Departure from Nucleate Boiling Ratio (DNBR) margin every 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> when the unit is operated at greater than 20 percent rated thermal power. Unit 1 increased power above 20 percent at approximately 0106 on September 2, 1987. Therefore, for approximately 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> COLSS was inoperable and the TSSRs were not met. In addition, the ACTION Statement for Technical Specification 3.3.3.2 was exceeded since approximately 50 percent of the incore detectors were rendered inoperable due to the reversed cards.
While conducting routine monitoring of plant status during startup of Unit 1 on September 1, 1987, Operations identified that portions of the COLSS data being obtained were not as expected, but were still within the Technical Following discussions with -Reactor Engineering, Unit 1 continued power Specification'imits.
ascension beyond 20 percent. On the morning of September 2, 1987, Reactor Engineering was comparing the results of the previous surveillance tests for incore detectors (72ST-9RX08) with data obtained at approximately 8 percent power and identified a potential discrepancy. Incore detectors which were known to be out of service were now operating and detectors which had been operating were now out of service. The Operations Computer Department investigated the problem and discovered that two DMA Interface Cards were reversed. This resulted in the computer (CPU) system considering RIS "B" incore detectors to be in the "D" quadrant of the reactor core and RIS "D" detectors in the "B" quadrant. The discovery of the improperly installed cards resulted in the COLSS being declared inoperable at 0815.
The root cause of the event has been determined to be a cognitive personnel
'error by a computer technician (utility non-licensed) who inadvertently reversed the cards while troubleshooting under approved work order documents. The troubleshooting consisted of changing cards between different RISs to determine which, if any, card(s) were not functioning properly. The technician did not obtain independent verification of the serial numbers and addresses for the cards which were being changed during the troubleshooting efforts. This is contrary to an approved procedure (work order). The cards which were identified as not functioning properly (Honeywell, Inc., Model Nos. 51302564 and 51302567) will be evaluated/reworked under the existing work control program.
"rRC rORM 555k 19 45r
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NAC Porrrr 3CCA 19S) 31 U.d, NUCLEAR AEOULATOAT COMM)SCION LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPAOVEO OMd NO 3IEO~ICS EXP)RES) 3/3) IIX)
FACILITY NAME III OOCKET NUMCEA 13)
LER NUMEEA Id) PACE )3)
YEAR CCOVCN'IIAL :Ir)< OCVICION NVM CA NVM CA Palo Verde Unit TEXT IIImort soon is ttlrttsL t>> ostsooo) 1 PIAC forrII 3CC)A'I) I 17) o s o o o 528 87 024 0 0. 03oFO 4 As immediate corrective action, the required surveillance test (72ST-9RX03) was initiated at 0820 to meet the applicable Technical Specification ACTION Statements for the inoperable COLSS. Concurrently, the computer technician reinstalled the two cards in their correct locations and obtained independent verification of this action. Independent verification was also performed on those cards which had been removed/reinstalled during the troubleshooting work orders to ensure they were in their correct locations. The incore detector surveillance test (72ST-9RX08) was successfully completed and COLSS was declared operable at 1256 on September 2, 1987.
As corrective action to prevent recurrence, the technician has been counselled on the importance of the accuracy of his work as well as when it is necessary to have independent verifications conducted. As a prudent measure, the work order forms utilized for removal/reinstallation of components will be evaluated for adequacy. Upon completion of this evaluation, computer technicians who perform similar types of work will be briefed on the event, the requirements for independent verification of their work, and planned changes to the removal/reinstallation forms, if any.
The COLSS provides the plant operators a means of directly monitoring the reactor core status (LHR and DNBR) in order to ensure that the Technical Specification Limiting Conditions for Operation are maintained. However, it is the Core Protection Calculators (CPC)(JC) which utilize the incore detectors (DET) and initiate the automatic protective function (reactor trip) when the predetermined values for Local Power Density (same as Linear Heat Rate) and DNBR are exceeded. Although the values for LHR and DNBR margin could not be correctly monitored from 0106 through 0815 using COLSS, the CPCs were unaffected by the mispositioned cards and available during the event to provide the automatic protective function.
CPC Channel "D" (which represents approximately one quadrant of the reactor core) was monitored during the event by the Control Room Operators every 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for Local Power Density (LPD) and DNBR margin as required by Operating Department Guideline No. 46. These values were within the Technical Specification values. The shiftly surveillance test (41ST-1ZZ33) which was performed at 2325 on September 1, 1987 prior to the event and at 1235 on September 2, 1987 after the event verified that the maximum deviation between the four channels of LPD and DNBR margin were within the limits specified in the surveillance test. A review of the maximum deviation values and CPC Channel "D" monitoring results indicate that the values for LPD and DNBR for the other three CPC channels would have been within the limits specified in the Technical Specifications. Also, the values which were obtained for LHR and DNBR margin during the performance of surveillance test 72ST-9RX03 following the discovery of the reversed cards were found to be within the acceptance criteria for all four CPC channels. Therefore, this event posed no threat to the health and safety of the public or to the safe operation of the plant, NIIC I OIIM 555k 19 CTI
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NAC form 344A U.S. NUCLEAR AEQULATORY COMMISSION (9 83)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPAOVED OMS NO. 3150MIOS EXPIRES: 8/81/88 FACILITY NAME III DOCKET NUMSER )QI LER NUMSER )4) PACE C))
YEAR SEQUENT/AL )yet NEVIS/ON NUM tr) :~O NI/M Palo Verde Unit TEXT /// moro sof Io /I tot/irod. rrw ~ 1 H/IC form 8//SAT/ l)1) 0 5 0 0 0 5 2 8 8 7 024 components, or systems that were inoperable at the 000 4 oF 0 There were no structures, start of the event, other than those previously described, that contributed to the event. There were no unusual characteristic's of the work location which contributed to the event. There were no automatic or manually initiated safety system responses. Should other concerns or information pertinent to this event be discovered, a supplement to this report will be issued.
There have been no previous similar events reported.
4oc roAM ssso 19 8) I
Arizona Nuclear Power Project P.O. BOX 52034 ~ PHOENIX, ARIZONA 85072-2034 192-00284-JGH/TRB/TJB October 1, 1987 Document Control Desk U.S. Nuclear Regulatory Commission D.C. 20555 'ashington,
Dear Sirs:
Subject:
Palo Verde Nuclear Generating Station (PVNGS)
Unit 1 Docket No. 50-528 Licensee Event Report 1-87-024-00 File: 87-020-404 Attached please find Licensee Event Report (LER) No. 1-87-024-00 prepared and submitted pursuant to 10CFR 50.73. In accordance with 10CFR 50.73(d), we are herewith forwarding a copy of the LER to the Regional Administrator of the Region V Office.
If you have any questions, please contact T. R. Bradish, Compliance Supervisor at (602) 393-3531.
Very tr ly yours, UA uy~~
J. G. Haynes Vice President Nuclear Production JGH/TJB/cld Attachment cc: 0. M. DeMichele (all w/a)
E. E. Van Brunt, Jr.
J. B. Martin R. C. Sorenson E. A. Licitra A. C. Gehr INPO Records Center