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| issue date = 03/06/1992
| issue date = 03/06/1992
| title = LER 92-009-00:on 920213,control Room Ventilation Sys Inadvertently Switched to Emergency Mode.Caused by Combination of Inadequate Job Planning & Personnel Error. Job Planning Requirements reviewed.W/920306 Ltr
| title = LER 92-009-00:on 920213,control Room Ventilation Sys Inadvertently Switched to Emergency Mode.Caused by Combination of Inadequate Job Planning & Personnel Error. Job Planning Requirements reviewed.W/920306 Ltr
| author name = HILLMAN C T, SLADE G B
| author name = Hillman C, Slade G
| author affiliation = CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.),
| author affiliation = CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.),
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:.
{{#Wiki_filter:.*                                                                                        e.
* 1l . consumers Power POWERINli MICHlliAN'S PROliRESS Palisades Nuclear Plant:
                                . consumers 1l Power                                                     GB Slade General Manager POWERINli MICHlliAN'S PROliRESS Palisades Nuclear Plant:     ~7780 Blue Star Memorial Highway. Coven. Ml 49043
Blue Star Memorial Highway. Coven. Ml 49043
* March 6, 1992 Nuclear Regulatory Commission Document Control Desk
* March 6, 1992 Nuclear Regulatory Commission Document Control Desk
* Washington, DC 20555 DOCKET 50-255 -LICENSE DPR-20 -PALISADES PLANT -e . GB Slade General Manager LICENSEt EVENT REPORT ACTUATION OF THE CONTROL ROOM HVAC SYSTEM DUE TO DAMAGED ELECTRICAL CABLE Report (LER) 92-009 is attached:
* Washington, DC 20555 DOCKET 50-255 - LICENSE DPR PALISADES PLANT -
This event is to the NRC perlOCFR50.73(a)(2)(iv) as an event that resulted in the automatic . actuation of an Engineered Safety Feature, the Control Room HVAC.
LICENSEt EVENT REPORT 92~009~INADVERTENT ACTUATION OF THE CONTROL ROOM HVAC SYSTEM DUE TO DAMAGED ELECTRICAL CABLE Lic~nse~ E~ent Report (LER) 92-009 is attached: This event is re~ortable to the NRC perlOCFR50.73(a)(2)(iv) as an event that resulted in the automatic
J / -. , ______ _ /0.// *. Gerald B Slade General Manager CC Administrator, Region Ill, USNRC NRC.Resident Inspector  
        . actuation of an Engineered Safety Feature, the Control Room HVAC.
-Palisades Attachment r r .... ... ' .. : :> 9203110250 920306 PDR ACOCK 05000255 PDR
                  ~ ~4-~ *. J / -. ,_______
-l"'"C l'ot,.; -U.l. llUCLIAll lllOULATOfl"'
              /0.//
CC *ION -OVID 0111 lltO. J11D...01CM LICENSEE EVENT REPORT (LERI IXPlllU: 1/3111& fACILITY NAME 11 I JDOCKIT lllUllalll IJI I r--& l:sl Palisades Plant o-1s1010101 21515 , loFlo L3 -TITLE l*I INADVERTENT ACTUATION OF THE CONTROL ROOM HVAC SYSTEM DUE TO DAMAGED ELECTRICAL CABLE IVINT DATI Ill LIA 1111.MeEll Ill llll'OllT DATE 17i OTHlll PACILITIU IWVOWID Ill ..-ONTM OAY YEAR YEAR* kt SIQUINTIAL Ft M-MONTM DAY YEAR. FACILITY NAMU DOCKET lolUMHR.111 NUMIEll NUMllllll N/A 01&1010101 I I n I ? ,I al ? -d* olg ol o d 016 91 a ? 3 2 NIA. 01610.10101 I I . 'Of'lllATING THll llll'OilT 11 IUIMITTEO l'UlllUANT TO TMl lllOUllllMIHTI OF 10 Cfll &sect;: !Cltcl< -or __ of"'-"11--.,J 1111 llllOOI Ill N I0.41121111 20.40lllcl x I0.711allllllwl n.11i..1 * -..........  
Gerald B Slade General Manager CC Administrator, Region Ill, USNRC NRC.Resident Inspector - Palisades Attachment r r.... ,~ ... ' .. : :>
...... l'OWlll 20 .... 1.1111111 I0.*1*1111 I0.71WllJIM 71.711*1 LIVIL 0 010 ..___ --...... 1101 ao .... c.11111w1 I0.*101121 I0.711111211  
9203110250 920306 PDR ACOCK 05000255 s                                PDR
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:-:.; IO .... lal1111Hll IO.JJC.1121111 I0.714-ICllhrlllllAI  
                                                                                                                                                                                                                                                                                                    *ION IXPlllU: 1/3111&
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LICENSEE EVENT REPORT (LERI I~      fACILITY NAME 11 I                                                                                                                                                                                             JDOCKIT lllUllalll IJI                           I               r--&             l:sl Palisades Plant                                                                                                                                                                                       o-1s1010101 21515                                   , loFlo                         L3
:;:;::;:;:  
    - TITLE l*I INADVERTENT ACTUATION OF THE CONTROL ROOM HVAC SYSTEM DUE TO DAMAGED ELECTRICAL CABLE IVINT DATI Ill                                                       LIA 1111.MeEll Ill                               llll'OllT DATE 17i                                                 OTHlll PACILITIU IWVOWID Ill
} ) ---1:-: ;:;::;.;:;:;:;:;:;  
          ..-ONTM                 OAY                   YEAR             YEAR*     kt   SIQUINTIAL NUMIEll      Ft     M-NUMllllll MONTM                     DAY                 YEAR.                     FACILITY NAMU                       DOCKET lolUMHR.111 N/A                                               01&1010101                                           I         I n I ? ,I                         ~        a        ?        al ? - d* olg                           ol o d 3                          016                     91   2       NIA.                                             01610.10101                                         I         I THll llll'OilT 11 IUIMITTEO l'UlllUANT TO TMl lllOUllllMIHTI OF 10 Cfll                                           &sect;: !Cltcl< -     or __ of"'- "11--.,J 1111
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;:;: 20.tOllalllll*I I0.7JlallJlllUI I0.711811211*1 LICINIH CONTACT FOR TMll LIA 11ZI N.t.ME ** AAEA CODE Cris T. Hillman, *Staff Licensing Engineer 6 11 ti 7 16 (+ , I -18 I 91l13 COMPLETE ONE LINE F II ILU II II I I MANUFAC-!REPORTABLE I :::!!!!!11!:  
                                                                                                                                                                                                                                            ...... 71.711*1 0 010                             ao ....c.11111w1                                                                                                     I0.711111211 .. 1                                 OTMlll IS#J<<"r I* ~
:":::  
1101                                                                                                            I0.*101121 i--                                                                                                                             -     *"'1 I* r .. r. NllC , _
' C.t.USE* SYSTEM COMPONENT CAUSE SYSTEM COMPONENT MANUFAC*
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                                              -;-;;:;:; ;:;:;;:;:; ;:;:         20.tOllalllll*I                                   I0.7JlallJlllUI LICINIH CONTACT FOR TMll LIA 11ZI I0.711811211*1 N.t.ME                                                                                                                                                                                                                                     **
:;:;:;:;:;:;:;:;:;:;:;.
AAEA CODE Cris T. Hillman, *Staff Licensing Engineer                                                                                                                                                                       6 11     ti     7 16 (+ , I - 18 I 91l13 COMPLETE ONE LINE F                                               II               ILU II     II     I                       I C.t.USE* SYSTEM                                COMPONENT                    MANUFAC-TUR ER
v*,::-*:--
                                                                                                            !REPORTABLE TO NPRDS      I   :::!!!!!11!: :":::                           CAUSE SYSTEM           COMPONENT             MANUFAC*
I I I I I r I i-:-::;:;:;:;:;:;:;:;::::::  
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.;.;.;:;:;:;:;:;:;:;:;
                                                                                                                                                                                                                                                ~ll'ORTAILI TO Nl'AOS       l: : :1*-:.:.*:*: -:~:1: ' ,j:'*: .,: : : : :i:!:j: '
u::;: I I I I .1 I I ,;.;:;:;:;:;:;:;::::::::::::  
I                        I       I     I           I     I     I J:/                >
;.;:;.;:;:;:;:;;:*:;:;
I              I    I      I        I  I    I
llEPORT EXPECTED 11*1 ..-ONTM 0.t.Y Y'JA EKPECTED ' n YES Ill,._, -EX".ECTED SVlllllSSION DA
                                                                                                                                                                                                                                                                  * :::1-::::::::'-:.::::,.:::1:.:.:::/:-;_*::w::_:'j
* IUIMISSION
                                                                                                                                      ;:;::;:;::-:-;:-:;:;:;:;:                                                                                                     1;:::;:;:;:;:;:;:;:;::::::: :;:;:;:;:;:;:;:;:;:;:;.
.. o DATE 1151 . I I I fLimlr ro 140IJ.f!>>CW, I.* .. .,,,,roaimareJr fl,,..,, linfl*41>>n ry,c>>wrimn 1;,,.,1 (111 .. On February 13, 1992, at 1920 hours; the control room ventilation system inadvertently switched to the emergency mode. At the time of occurrence, the plant was in cold shutdown and .the primary . coolant system was depressurized.
v*,::-*:--                 ::; :                                                                                            i-:-::;:;:;:;:;:;:;:;:::::: .;.;.;:;:;:;:;:;:;:;:;
The control room operators immediately verified that there was riot a valid. containment high pressure (CHP) or a containment high radiation (CHR) signal* .present.
I                        I        I    I          I    r    I                      u::;:                                                       I             I   I     I       .1   I     I                           ,;.;:;:;:;:;:;:;:::::::::::: ;.;:;.;:;:;:;:;;:*:;:;
It was subsequently determined that Electrical Maintenance was replacing damaged fl ex conduit on the CHR relay SR-6 circuit. When the wire on relay SR-6, point 16, was disconnected, the electrical circuit schem*e SlOl . de-energized causing the "A" train of Control Room HVAC to automatically switch to the emergency mode. This event was caused by a combination of -inadequate job planning and personnel error. Corrective action for this event includes (1) in-plant training for electricians, I&C staff and I&C technicians on the importance of job plan and schematics reviews prior . to i nit i at i ng work and (2) a review of job planning-requirements the importance of post-maintenance testing with the job planners.
                                                                                              ~LIMENTAL llEPORT EXPECTED 11*1                                                                                                                             ..-ONTM               0.t.Y                 Y'JA EKPECTED '
NRC For"' .. Ill-SJ; LICENSE-ENT REPORT (LERI TEXT CONTINU ON OOCIUT """9111 121 ...... "'I ..
n                                                                                                                                     ~
*ICf...i...&r::>*  
IUIMISSION YES Ill,._, -                                     EX".ECTED SVlllllSSION DA         ~El *                                               .. o DATE 1151
.... :::a11111au:::.
                                                                                                                                                                                                                                                              .I                       I                     I
A"'9*0VEO .... '<0 ;* !IO...<J*O-. (IO*llts 1.11 U. ... ".90" .. ...... *&OI *21 Palisades Plant 0 1 s I 0 I 0 Io I 2 1 1 5 9 I 2 -o Io 19 -o 10 o 12 oF o 1 3 T'IXTt*--*._..
        ~RACT                      fLimlr         ro     140IJ.f!>>CW, I.* .. .,,,,roaimareJr       fl,,..,, linfl*41>>n ry,c>>wrimn 1;,,.,1 (111 On February 13, 1992, at 1920 hours; the control room ventilation system inadvertently switched to the emergency mode. At the time of occurrence, the plant was in cold shutdown and .the primary .coolant system was depressurized.
__ /fl/IC .........  
The control room operators immediately verified that there was riot a valid.
'1Jtl71 EVENT DESCRIPTION On February 13, 1992, at 1920 hours, the control room ventilation system [VI] inadvertently switched to the emergency mode. At the time of occurrence, the plant was in cold shutdown and the primary coolant system was depressurized.
containment high pressure (CHP) or a containment high radiation (CHR) signal*
The control room operators immediately verified that there was not a valid containment high (CHP) or a containment high radiation (CHR) signal present. It was subsequently determined that Electrical Mairitenance was .replacing damaged flex conduit [IK;CND] on the CHR relay 5R;6 [IK;RLY]
                          .present. It was subsequently determined that Electrical Maintenance was replacing damaged fl ex conduit on the CHR relay SR-6 circuit. When the wire on relay SR-6, point 16, was disconnected, the electrical circuit schem*e SlOl
When the wire on relay point 16, was disconnected, the electrical circuit scheme SlOl de-energized causing the "A" train of Ctintrol Room HVAC to automatically switch to the @mergency mode .. The Electrical Supervisor was notified.of the actuation.
                        . de-energized causing the "A" train of Control Room HVAC to automatically switch to the emergency mode.
The work described under the work order was completed and circuit was re-terminated.
This event was caused by a combination of -inadequate job planning and personnel error.
This event is reportable to the NRC per 10CFR50,J3(a)(2)(iv) as an event that resulted in the automatic actuation of an Engineered Safety Feature, the Room HVAC. CAUSE OF THE EVENT De-energization of emergency HVAC activation relays by lifting wire in the . control room emergency HVAC system activation sc.heme (SlOl) was caused by a combination of inadequate job planning and personnel
Corrective action for this event includes (1) in-plant training for electricians, I&C staff and I&C technicians on the importance of job plan and schematics reviews prior .to i nit i at i ng work and (2) a review of job planning-requirements .~nd the importance of post-maintenance testing with the job planners.
* This event did not involve the failure of equipment to $afety. ANALYSIS OF THE EVENT The.job plan for the work order called for.the on relay SR-6, point 16, to be lifted in order to remove it from a crushed flex conduit. Following removal from the flex conduit the wire was to be inspected for damage. When the wire was lifted, the.continuity of the circuit was broken causing the circuit to thereby activating the .relay to automatically switch* .the control room HVAC to the emergency mode; Although the job plan was incorr.ect in that it did not identify the electrical scheme as a "de-energize to actuate''
NRC For"' . .
scheme; it did the electricians to the correct electrical prints (E-271, Sh. 8) whi.ch clearly shows the electrical scheme to be a to actuate''
Ill-SJ;
scheme. Normal electrical maintenance prattice would be to review drawings and check for electrical potential before lifting wires. This normal practice should have caught the incorrect job plan. Since the qrawings were not reviewed, the error in the job plan went undetected.
 
** LICENSEE-NT.
                                                                                        "'I .. "'C~l.&*. *ICf...i...&r::>* ....:::a11111au:::.
REPORT ILERl TEXT CONTINUA N "'a  
LICENSE-ENT REPORT (LERI TEXT CONTINU                    ON                A"'9*0VEO   ~ .... '<0 ;* !IO...<J*O- .
*1wwi.:.ar:i*." :=--t1a10-
(IO*llts 1.11 U .
*"*ov10 ., .. , ;,o E "'*IS t'."li 15 OOClllT lfUM911'1 121 ..... '" *&QI iJl .... ... Palisades Plant 0 5 0 0 0 2 5 5 9 2 -0 0 9 _ .,._ 0 0 . 0 3 OF 0 3 TUT,. --* .__ --/IC_ ...... .-.a*,, 1111 An additional weakness was noted in the job plan in that post maintenance testing was inadequate  
OOCIUT """9111 121
.. A continuity check of wire was performed, however, more thorough post mai.ntenance testing would be expected following the removal and re-termination of a wire from a safety-related relay. CORRECTIVE ACTION . . The f611owing corrective actjons have been completed:  
                                                                                                    .. ".90"
: 1. Restate expectation that electricians review job plan and prints thoroughly before ariy physical Also, point out requirement for check of potential from both a safety and proper work practice standpoint  
                                                                                                                          *&OI *21 Palisades Plant T'IXTt*--*._.. __ /fl/IC ......... '1Jtl71 0
.. Review both actions with the I&C staff and I&C and document on in-plant training form.
1s I 0 I 0 Io I 21~ 15 9 I 2 -    o Io 19    -      o 10        o 12        oF      o 13 EVENT DESCRIPTION On February 13, 1992, at 1920 hours, the control room ventilation system [VI]
inadvertently switched to the emergency mode. At the time of occurrence, the plant was in cold shutdown and the primary coolant system was depressurized.
The control room operators immediately verified that there was not a valid containment high pr~ssure (CHP) or a containment high radiation (CHR) signal present. It was subsequently determined that Electrical Mairitenance was
      .replacing damaged flex conduit [IK;CND] on the CHR relay 5R;6 [IK;RLY]
    *circuit~    When the wire on relay 5R~6, point 16, was disconnected, the electrical circuit scheme SlOl de-energized causing the "A" train of Ctintrol Room HVAC to automatically switch to the @mergency mode ..
The Electrical Supervisor was notified.of the actuation. The work described under the work order was completed and circuit was re-terminated.
This event is reportable to the NRC per 10CFR50,J3(a)(2)(iv) as an event that resulted in the automatic actuation of an Engineered Safety Feature, the Cont~ol Room HVAC.
CAUSE OF THE EVENT De-energization of emergency HVAC activation relays by lifting wire in the
    . control room emergency HVAC system activation sc.heme (SlOl) was caused by a combination of inadequate job planning and personnel er~or.~
* This event did not involve the failure of           ~ny  equipment     im~ortant    to $afety.
ANALYSIS OF THE EVENT The.job plan for the work order called for.the wi~e on relay SR-6, point 16, to be lifted in order to remove it from a crushed flex conduit. Following removal from the flex conduit the wire was to be inspected for damage. When the wire was lifted, the.continuity of the circuit was broken causing the circuit to de~energize, thereby activating the .relay to automatically switch*
      .the control room HVAC to the emergency mode; Although the job plan was incorr.ect in that it did not identify the electrical scheme as a "de-energize to actuate'' scheme; it did ~efer the electricians to the correct electrical prints (E-271, Sh. 8) whi.ch clearly shows the electrical scheme to be a "de-energiz~ to actuate'' scheme.       Normal electrical maintenance prattice would be to review drawings and check for electrical potential before lifting ~ny wires. This normal practice should have caught the incorrect job plan. Since the qrawings were not reviewed, the error in the job plan went undetected.
 
                                                                                                          "'a *uC:~l** *1wwi.:.ar:i*." :=--t1a10-LICENSEE-NT. REPORT ILERl TEXT CONTINUA                          N                *"*ov10 ., .., ;,o   i*~-010.
E"'*IS t'."li 15 OOClllT lfUM911'1 121
                                                                                    .... ...   ~ ..... ~"  '"                      *&QI iJl Palisades Plant                               0   5     0   0   0 2 5 5 9 2 -           0 0 9 _.,._ 0 0 . 0 3             OF   0   3 TUT,. - -   * .__ -   -     /IC_ ...... .-.a*,, 1111 An additional weakness was noted in the job plan in that post maintenance testing was inadequate .. A continuity check of th~ wire was performed, however, more thorough post mai.ntenance testing would be expected following the removal and re-termination of a wire from a safety-related relay.
CORRECTIVE ACTION The f611owing corrective actjons have been completed:
: 1. Restate expectation that electricians review job plan and prints thoroughly before ariy physical ~ork begin~. Also, point out requirement for check of potential from both a safety and proper work practice standpoint .. Review both actions with the el~ctricians, I&C staff and I&C tec~nicians and document on in-plant training form.
* 2 .. Review proper job planning requirements with planners to emphasize a review of all prints and the importance of proper post maintenance testing in accordance .with Administrative Procedure 5.19; ADDITIONAL INFORMATION Norie}}
* 2 .. Review proper job planning requirements with planners to emphasize a review of all prints and the importance of proper post maintenance testing in accordance .with Administrative Procedure 5.19; ADDITIONAL INFORMATION Norie}}

Latest revision as of 16:03, 23 February 2020

LER 92-009-00:on 920213,control Room Ventilation Sys Inadvertently Switched to Emergency Mode.Caused by Combination of Inadequate Job Planning & Personnel Error. Job Planning Requirements reviewed.W/920306 Ltr
ML18058A266
Person / Time
Site: Palisades Entergy icon.png
Issue date: 03/06/1992
From: Hillman C, Slade G
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-92-009, LER-92-9, NUDOCS 9203110250
Download: ML18058A266 (4)


Text

.* e.

. consumers 1l Power GB Slade General Manager POWERINli MICHlliAN'S PROliRESS Palisades Nuclear Plant: ~7780 Blue Star Memorial Highway. Coven. Ml 49043

  • March 6, 1992 Nuclear Regulatory Commission Document Control Desk

LICENSEt EVENT REPORT 92~009~INADVERTENT ACTUATION OF THE CONTROL ROOM HVAC SYSTEM DUE TO DAMAGED ELECTRICAL CABLE Lic~nse~ E~ent Report (LER)92-009 is attached: This event is re~ortable to the NRC perlOCFR50.73(a)(2)(iv) as an event that resulted in the automatic

. actuation of an Engineered Safety Feature, the Control Room HVAC.

~ ~4-~ *. J / -. ,_______

/0.//

Gerald B Slade General Manager CC Administrator, Region Ill, USNRC NRC.Resident Inspector - Palisades Attachment r r.... ,~ ... ' .. : :>

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LICENSEE EVENT REPORT (LERI I~ fACILITY NAME 11 I JDOCKIT lllUllalll IJI I r--& l:sl Palisades Plant o-1s1010101 21515 , loFlo L3

- TITLE l*I INADVERTENT ACTUATION OF THE CONTROL ROOM HVAC SYSTEM DUE TO DAMAGED ELECTRICAL CABLE IVINT DATI Ill LIA 1111.MeEll Ill llll'OllT DATE 17i OTHlll PACILITIU IWVOWID Ill

..-ONTM OAY YEAR YEAR* kt SIQUINTIAL NUMIEll Ft M-NUMllllll MONTM DAY YEAR. FACILITY NAMU DOCKET lolUMHR.111 N/A 01&1010101 I I n I ? ,I ~ a  ? al ? - d* olg ol o d 3 016 91 2 NIA. 01610.10101 I I THll llll'OilT 11 IUIMITTEO l'UlllUANT TO TMl lllOUllllMIHTI OF 10 Cfll §: !Cltcl< - or __ of"'- "11--.,J 1111

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AAEA CODE Cris T. Hillman, *Staff Licensing Engineer 6 11 ti 7 16 (+ , I - 18 I 91l13 COMPLETE ONE LINE F II ILU II II I I C.t.USE* SYSTEM COMPONENT MANUFAC-TUR ER

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~LIMENTAL llEPORT EXPECTED 11*1 ..-ONTM 0.t.Y Y'JA EKPECTED '

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~RACT fLimlr ro 140IJ.f!>>CW, I.* .. .,,,,roaimareJr fl,,..,, linfl*41>>n ry,c>>wrimn 1;,,.,1 (111 On February 13, 1992, at 1920 hours0.0222 days <br />0.533 hours <br />0.00317 weeks <br />7.3056e-4 months <br />; the control room ventilation system inadvertently switched to the emergency mode. At the time of occurrence, the plant was in cold shutdown and .the primary .coolant system was depressurized.

The control room operators immediately verified that there was riot a valid.

containment high pressure (CHP) or a containment high radiation (CHR) signal*

.present. It was subsequently determined that Electrical Maintenance was replacing damaged fl ex conduit on the CHR relay SR-6 circuit. When the wire on relay SR-6, point 16, was disconnected, the electrical circuit schem*e SlOl

. de-energized causing the "A" train of Control Room HVAC to automatically switch to the emergency mode.

This event was caused by a combination of -inadequate job planning and personnel error.

Corrective action for this event includes (1) in-plant training for electricians, I&C staff and I&C technicians on the importance of job plan and schematics reviews prior .to i nit i at i ng work and (2) a review of job planning-requirements .~nd the importance of post-maintenance testing with the job planners.

NRC For"' . .

Ill-SJ;

"'I .. "'C~l.&*. *ICf...i...&r::>* ....:::a11111au:::.

LICENSE-ENT REPORT (LERI TEXT CONTINU ON A"'9*0VEO ~ .... '<0 ;* !IO...<J*O- .

(IO*llts 1.11 U .

OOCIUT """9111 121

.. ".90"

  • &OI *21 Palisades Plant T'IXTt*--*._.. __ /fl/IC ......... '1Jtl71 0

1s I 0 I 0 Io I 21~ 15 9 I 2 - o Io 19 - o 10 o 12 oF o 13 EVENT DESCRIPTION On February 13, 1992, at 1920 hours0.0222 days <br />0.533 hours <br />0.00317 weeks <br />7.3056e-4 months <br />, the control room ventilation system [VI]

inadvertently switched to the emergency mode. At the time of occurrence, the plant was in cold shutdown and the primary coolant system was depressurized.

The control room operators immediately verified that there was not a valid containment high pr~ssure (CHP) or a containment high radiation (CHR) signal present. It was subsequently determined that Electrical Mairitenance was

.replacing damaged flex conduit [IK;CND] on the CHR relay 5R;6 [IK;RLY]

  • circuit~ When the wire on relay 5R~6, point 16, was disconnected, the electrical circuit scheme SlOl de-energized causing the "A" train of Ctintrol Room HVAC to automatically switch to the @mergency mode ..

The Electrical Supervisor was notified.of the actuation. The work described under the work order was completed and circuit was re-terminated.

This event is reportable to the NRC per 10CFR50,J3(a)(2)(iv) as an event that resulted in the automatic actuation of an Engineered Safety Feature, the Cont~ol Room HVAC.

CAUSE OF THE EVENT De-energization of emergency HVAC activation relays by lifting wire in the

. control room emergency HVAC system activation sc.heme (SlOl) was caused by a combination of inadequate job planning and personnel er~or.~

  • This event did not involve the failure of ~ny equipment im~ortant to $afety.

ANALYSIS OF THE EVENT The.job plan for the work order called for.the wi~e on relay SR-6, point 16, to be lifted in order to remove it from a crushed flex conduit. Following removal from the flex conduit the wire was to be inspected for damage. When the wire was lifted, the.continuity of the circuit was broken causing the circuit to de~energize, thereby activating the .relay to automatically switch*

.the control room HVAC to the emergency mode; Although the job plan was incorr.ect in that it did not identify the electrical scheme as a "de-energize to actuate scheme; it did ~efer the electricians to the correct electrical prints (E-271, Sh. 8) whi.ch clearly shows the electrical scheme to be a "de-energiz~ to actuate scheme. Normal electrical maintenance prattice would be to review drawings and check for electrical potential before lifting ~ny wires. This normal practice should have caught the incorrect job plan. Since the qrawings were not reviewed, the error in the job plan went undetected.

"'a *uC:~l** *1wwi.:.ar:i*." :=--t1a10-LICENSEE-NT. REPORT ILERl TEXT CONTINUA N *"*ov10 ., .., ;,o i*~-010.

E"'*IS t'."li 15 OOClllT lfUM911'1 121

.... ... ~ ..... ~" '" *&QI iJl Palisades Plant 0 5 0 0 0 2 5 5 9 2 - 0 0 9 _.,._ 0 0 . 0 3 OF 0 3 TUT,. - - * .__ - - /IC_ ...... .-.a*,, 1111 An additional weakness was noted in the job plan in that post maintenance testing was inadequate .. A continuity check of th~ wire was performed, however, more thorough post mai.ntenance testing would be expected following the removal and re-termination of a wire from a safety-related relay.

CORRECTIVE ACTION The f611owing corrective actjons have been completed:

1. Restate expectation that electricians review job plan and prints thoroughly before ariy physical ~ork begin~. Also, point out requirement for check of potential from both a safety and proper work practice standpoint .. Review both actions with the el~ctricians, I&C staff and I&C tec~nicians and document on in-plant training form.
  • 2 .. Review proper job planning requirements with planners to emphasize a review of all prints and the importance of proper post maintenance testing in accordance .with Administrative Procedure 5.19; ADDITIONAL INFORMATION Norie