ML17326A063: Difference between revisions

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{{#Wiki_filter:4A,I'K(iuRY g*REGULATORY INFORMATZON DISTRIBUTION SYSTEM(RIDS)ACCESSION NBR:9907280074 DOC.DATE:
{{#Wiki_filter:4 A,I'K(iuRY g*REGULATORY INFORMATZON DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9907280074 DOC.DATE: 99/07/22 NOTARIZED:
99/07/22NOTARIZED:
NO DOCKET FACIL:50-315 Donald C.Cook Nuclear Power'lant, Unit 1, Indiana M 05000315 AUTH.NAME AUTHOR AFFILIATION RENCHECK,M.W.
NODOCKETFACIL:50-315 DonaldC.CookNuclearPower'lant, Unit1,IndianaM05000315AUTH.NAMEAUTHORAFFILIATION RENCHECK,M.W.
Indiana Michigan Power Co.RECIP.NAME RECIPIENT AFFILIATION Records Management Branch (Document Control Desk)
IndianaMichiganPowerCo.RECIP.NAME RECIPIENT AFFILIATION RecordsManagement Branch(Document ControlDesk)


==SUBJECT:==
==SUBJECT:==
ForwardsLER98-014-03,
Forwards LER 98-014-03,"'Response to High-High Containment Pressure'rocedure Not Consistent With Analysis of Record." Revised info marked by sidebars in right hand margin.l7 Commitments made by util, listed.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR t ENCL 1 SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES: RECIPIENT ID CODE/NAME LPD3-1 PD INTERNAL ILE CE E NRR/DRIP/REXB RES/DET/ERAB RGN3 FILE 01 COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME STANG, J NRR/DIPM/IOLB NRR/DSSA/SPLB RES/DRAA/OERAB COPIES LTTR ENCL 1 1 1 1 1.1 1 1 EXTERNAL: L ST LOBBY WARD NOAC POORE,W.NRC PDR 1 1 1 1 1 1 LMITCO MARSHALL NOAC QUEENER,DS NUDOCS FULL TXT 1 1 1 1 1 1 NOTE TO ALL ERIDS" RECIPIENTS:
"'Response toHigh-High Containment Pressure'rocedure NotConsistent WithAnalysisofRecord."Revisedinfomarkedbysidebarsinrighthandmargin.l7 Commitments madebyutil,listed.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:LTR tENCL1SIZE:TITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:RECIPIENT IDCODE/NAME LPD3-1PDINTERNALILECEENRR/DRIP/REXB RES/DET/ERAB RGN3FILE01COPIESLTTRENCL1111111111RECIPIENT IDCODE/NAME STANG,JNRR/DIPM/IOLB NRR/DSSA/SPLB RES/DRAA/OERAB COPIESLTTRENCL11111.111EXTERNAL:
PLEASE HELP US TO REDUCE WASTE.TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LIS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATIONS CONTACT THE DOCUMENT CONTR DESK (DCD)ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 15 ENCL 15 Indiana'hlichiga~
LSTLOBBYWARDNOACPOORE,W.NRCPDR111111LMITCOMARSHALLNOACQUEENER,DS NUDOCSFULLTXT111111NOTETOALLERIDS"RECIPIENTS:
Power Company~Cook Hudew Raor Onecook Rart Mgnarl ha 49106 6i 6 465 5901 Z INDIANA NICHIGAN PWER July 22, 1999 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Operating License DPR-58 Docket No.50-315 Document Control Manager: In accordance with the criteria established by 10 CFR 50.73 entitled Licensee Event''P LER 315/98-014-03,"Response to High-High Containment Pressure" Procedure Not Consistent with Analysis of Record.This revision to the LER provides the safety significance of the identified condition, corrects a flow value in the Analysis section, and clarifies commitments as identified below.This information is marked by sidebars in the right hand margin.The commitments identified in this LER are as follows:~The containment integrity analysis will be used to determine a conservative time for actuation of RHR spray.This task will be completed by August 31, 1999.~Functional Restoration Procedure FRZ-1,"Response to High-High Containment Pressure", will be revised to be consistent with the new analysis.As Unit 2 will be returned to service first, the Unit 2 procedure will be revised and approved by December 1, 1999, with the procedure for Unit 1 scheduled for revision and approval by January 30, 2000.~A program will be developed to identify, document and control the key accident analyses assumptions used in accident analysis.Implementation of the program will be complete by August 31, 1999.Sincerely, M.W.encheck Vice President-Nuclear Engineering 9'ai07280074 990722 PDR ADQCK 050003i5 S PDR
PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATION REMOVEDFROMDISTRIBUTION LISORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATIONS CONTACTTHEDOCUMENTCONTRDESK(DCD)ONEXTENSION 415-2083FULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:
/mbd Attachment J.E.Dyer, Region III R.P.Powers J.Streeter G.P.Arent R., Whale D.Hahn Records Center, INPO NRC Resident Inspector}}
LTTR15ENCL15 Indiana'hlichiga~
PowerCompany~CookHudewRaorOnecookRartMgnarlha491066i64655901ZINDIANANICHIGANPWERJuly22,1999UnitedStatesNuclearRegulatory Commission DocumentControlDeskWashington, DC20555Operating LicenseDPR-58DocketNo.50-315DocumentControlManager:Inaccordance withthecriteriaestablished by10CFR50.73entitledLicenseeEvent''PLER315/98-014-03, "Response toHigh-High Containment Pressure" Procedure NotConsistent withAnalysisofRecord.ThisrevisiontotheLERprovidesthesafetysignificance oftheidentified condition, correctsaflowvalueintheAnalysissection,andclarifies commitments asidentified below.Thisinformation ismarkedbysidebarsintherighthandmargin.Thecommitments identified inthisLERareasfollows:~Thecontainment integrity analysiswillbeusedtodetermine aconservative timeforactuation ofRHRspray.Thistaskwillbecompleted byAugust31,1999.~Functional Restoration Procedure FRZ-1,"Response toHigh-High Containment Pressure",
willberevisedtobeconsistent withthenewanalysis.
AsUnit2willbereturnedtoservicefirst,theUnit2procedure willberevisedandapprovedbyDecember1,1999,withtheprocedure forUnit1scheduled forrevisionandapprovalbyJanuary30,2000.~Aprogramwillbedeveloped toidentify, documentandcontrolthekeyaccidentanalysesassumptions usedinaccidentanalysis.
Implementation oftheprogramwillbecompletebyAugust31,1999.Sincerely, M.W.encheckVicePresident-NuclearEngineering 9'ai07280074 990722PDRADQCK050003i5SPDR
/mbdAttachment J.E.Dyer,RegionIIIR.P.PowersJ.StreeterG.P.ArentR.,WhaleD.HahnRecordsCenter,INPONRCResidentInspector}}

Revision as of 09:19, 6 July 2018

Forwards LER 98-014-03, Response to High-High Containment Pressure Procedure Not Consistent with Analysis of Record. Revised Info Marked by Sidebars in Right Hand Margin. Commitments Made by Util,Listed
ML17326A063
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 07/22/1999
From: RENCHECK M W
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML17326A064 List:
References
NUDOCS 9907280074
Download: ML17326A063 (3)


Text

4 A,I'K(iuRY g*REGULATORY INFORMATZON DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9907280074 DOC.DATE: 99/07/22 NOTARIZED:

NO DOCKET FACIL:50-315 Donald C.Cook Nuclear Power'lant, Unit 1, Indiana M 05000315 AUTH.NAME AUTHOR AFFILIATION RENCHECK,M.W.

Indiana Michigan Power Co.RECIP.NAME RECIPIENT AFFILIATION Records Management Branch (Document Control Desk)

SUBJECT:

Forwards LER 98-014-03,"'Response to High-High Containment Pressure'rocedure Not Consistent With Analysis of Record." Revised info marked by sidebars in right hand margin.l7 Commitments made by util, listed.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR t ENCL 1 SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES: RECIPIENT ID CODE/NAME LPD3-1 PD INTERNAL ILE CE E NRR/DRIP/REXB RES/DET/ERAB RGN3 FILE 01 COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME STANG, J NRR/DIPM/IOLB NRR/DSSA/SPLB RES/DRAA/OERAB COPIES LTTR ENCL 1 1 1 1 1.1 1 1 EXTERNAL: L ST LOBBY WARD NOAC POORE,W.NRC PDR 1 1 1 1 1 1 LMITCO MARSHALL NOAC QUEENER,DS NUDOCS FULL TXT 1 1 1 1 1 1 NOTE TO ALL ERIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE.TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LIS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATIONS CONTACT THE DOCUMENT CONTR DESK (DCD)ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 15 ENCL 15 Indiana'hlichiga~

Power Company~Cook Hudew Raor Onecook Rart Mgnarl ha 49106 6i 6 465 5901 Z INDIANA NICHIGAN PWER July 22, 1999 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Operating License DPR-58 Docket No.50-315 Document Control Manager: In accordance with the criteria established by 10 CFR 50.73 entitled Licensee EventP LER 315/98-014-03,"Response to High-High Containment Pressure" Procedure Not Consistent with Analysis of Record.This revision to the LER provides the safety significance of the identified condition, corrects a flow value in the Analysis section, and clarifies commitments as identified below.This information is marked by sidebars in the right hand margin.The commitments identified in this LER are as follows:~The containment integrity analysis will be used to determine a conservative time for actuation of RHR spray.This task will be completed by August 31, 1999.~Functional Restoration Procedure FRZ-1,"Response to High-High Containment Pressure", will be revised to be consistent with the new analysis.As Unit 2 will be returned to service first, the Unit 2 procedure will be revised and approved by December 1, 1999, with the procedure for Unit 1 scheduled for revision and approval by January 30, 2000.~A program will be developed to identify, document and control the key accident analyses assumptions used in accident analysis.Implementation of the program will be complete by August 31, 1999.Sincerely, M.W.encheck Vice President-Nuclear Engineering 9'ai07280074 990722 PDR ADQCK 050003i5 S PDR

/mbd Attachment J.E.Dyer, Region III R.P.Powers J.Streeter G.P.Arent R., Whale D.Hahn Records Center, INPO NRC Resident Inspector