ML13323A521: Difference between revisions

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{{#Wiki_filter:Entergy Nuclear Operations, Inc.600 Rocky Hill RoadPlymouth, MA 02360Pilgrim Nuclear Power StationNovember 12, 2013U.S. Nuclear Regulatory Commission Attn: Document Control DeskWashington, D.C. 20555
==SUBJECT:==
Entergy Nuclear Operations, Inc.Pilgrim Nuclear Power StationDocket No.: 50-293License No.: DPR-35Revised Submittal Schedule for Supplement to the LER 2013-002-00, SRV-3B Safety Relief Valve Declared Inoperable Due to Leakage andSetpoint Drift
==REFERENCE:==
: 1. LER 2013-002-00, "SRV-3B Safety Relief valve Declared Inoperable Due to Leakage and Setpoint Drift", dated March 31, 20132. 10 CFR Part 21 Report, "Notification of a Defect, Bellows Failure",
Curtis Wright Flow Control Company (Target Rock) Letter NID #13307, dated June 17, 2013LETTER NUMBER: 2.13.089
==Dear Sir or Madam:==
Licensee Event Report (LER).2013-002-00, "SRV-3B Safety Relief Valve Declared Inoperable Due to Leakage and Setpoint Drift" was submitted on March 31, 2013 (Reference 1), with atarget schedule of September 30, 2013 to submit a Supplement to the LER, after completing the root cause analysis.
Since then the vendor (Target Rock) has issued a 10 CFR Part 21 Notification, (Reference 2)confirming defects in safety relief valve bellows.
Entergy is incorporating the information related to the reported defect into the root cause analysis.
Due to the recent refueling outage,emergent plant events, and vendor 10 CFR, Part 21 Notification, Pilgrim resources werediverted to address the emergent work activities.
As such, the review and approval of theSRV-3B root cause incorporating the vendor Part 21 Notification and the lessons learned fromthe events is taking longer time than expected.
Accordingly, the LER Supplement is expectedto be submitted by February 14, 2014.The revised submittal schedule was discussed with the NRC/NRR Project Manager.This letter contains no commitments.
PNPS Letter 2.13.089Page 2 of 2Please do not hesitate to contact me at (508) 830-8403, if there are any questions.
Sincerely, Joseph R. Lynch,Manager, Pilgrim Licensing cc:Mr. William M. DeanRegional Administrator, Region 1U.S. Nuclear Regulatory Commission 2100 Renaissance Blvd., Suite 100King of Prussia, PA 19406-2713 INPO Records700 Galleria ParkwayAtlanta, GA 30399-5957 Ms. Nadiyah Morgan, Project ManagerDivision of Operating Reactor Licensing Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission One White Flint NorthMail Stop O-8-C2A11555 Rockville PikeRockville, MD. 20852-2738 USNRC Senior Resident Inspector Pilgrim Nuclear Power Station}}

Revision as of 14:25, 3 July 2018

LER 13-002-00 for Pilgrim Nuclear Power Station Regarding Revised Schedule SRV-3B Safety Relief Valve Declared Inoperable Due to Leakage and Setpoint Drift
ML13323A521
Person / Time
Site: Pilgrim
Issue date: 11/12/2013
From: Lynch J R
Entergy Nuclear Operations
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LER 13-002-00
Download: ML13323A521 (2)


Text

Entergy Nuclear Operations, Inc.600 Rocky Hill RoadPlymouth, MA 02360Pilgrim Nuclear Power StationNovember 12, 2013U.S. Nuclear Regulatory Commission Attn: Document Control DeskWashington, D.C. 20555

SUBJECT:

Entergy Nuclear Operations, Inc.Pilgrim Nuclear Power StationDocket No.: 50-293License No.: DPR-35Revised Submittal Schedule for Supplement to the LER 2013-002-00, SRV-3B Safety Relief Valve Declared Inoperable Due to Leakage andSetpoint Drift

REFERENCE:

1. LER 2013-002-00, "SRV-3B Safety Relief valve Declared Inoperable Due to Leakage and Setpoint Drift", dated March 31, 20132. 10 CFR Part 21 Report, "Notification of a Defect, Bellows Failure",

Curtis Wright Flow Control Company (Target Rock) Letter NID #13307, dated June 17, 2013LETTER NUMBER: 2.13.089

Dear Sir or Madam:

Licensee Event Report (LER).2013-002-00, "SRV-3B Safety Relief Valve Declared Inoperable Due to Leakage and Setpoint Drift" was submitted on March 31, 2013 (Reference 1), with atarget schedule of September 30, 2013 to submit a Supplement to the LER, after completing the root cause analysis.

Since then the vendor (Target Rock) has issued a 10 CFR Part 21 Notification, (Reference 2)confirming defects in safety relief valve bellows.

Entergy is incorporating the information related to the reported defect into the root cause analysis.

Due to the recent refueling outage,emergent plant events, and vendor 10 CFR, Part 21 Notification, Pilgrim resources werediverted to address the emergent work activities.

As such, the review and approval of theSRV-3B root cause incorporating the vendor Part 21 Notification and the lessons learned fromthe events is taking longer time than expected.

Accordingly, the LER Supplement is expectedto be submitted by February 14, 2014.The revised submittal schedule was discussed with the NRC/NRR Project Manager.This letter contains no commitments.

PNPS Letter 2.13.089Page 2 of 2Please do not hesitate to contact me at (508) 830-8403, if there are any questions.

Sincerely, Joseph R. Lynch,Manager, Pilgrim Licensing cc:Mr. William M. DeanRegional Administrator, Region 1U.S. Nuclear Regulatory Commission 2100 Renaissance Blvd., Suite 100King of Prussia, PA 19406-2713 INPO Records700 Galleria ParkwayAtlanta, GA 30399-5957 Ms. Nadiyah Morgan, Project ManagerDivision of Operating Reactor Licensing Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission One White Flint NorthMail Stop O-8-C2A11555 Rockville PikeRockville, MD. 20852-2738 USNRC Senior Resident Inspector Pilgrim Nuclear Power Station