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{{#Wiki_filter:~CA.TEGORYREGULATORYINFORMATIONDISTRIBUTIONSYSTEM(RZDS)ACCESSIONNBR:9812140132DOC.DATE:98/12/08NOTARIZED:NOFACIL:50-315DonaldC.CookNuclearPowerPlant,Unit1,IndianaMAUTH.NAMEAUTHORAFFILIATIONWEBER,L.IndianaMichiganPowerCo.SAMPSON,'J.R.IndianaMichiganPowerCo.RECIP.NAMERECIPIENTAFFILIATIONDOCKET05000315
{{#Wiki_filter:~CA.TEGORYREGULATORY INFORMATION DISTRIBUTION SYSTEM(RZDS)ACCESSION NBR:9812140132 DOC.DATE:
98/12/08NOTARIZED:
NOFACIL:50-315 DonaldC.CookNuclearPowerPlant,Unit1,IndianaMAUTH.NAMEAUTHORAFFILIATION WEBER,L.IndianaMichiganPowerCo.SAMPSON,'J.R.
IndianaMichiganPowerCo.RECIP.NAME RECIPIENT AFFILIATION DOCKET05000315


==SUBJECT:==
==SUBJECT:==
LER98-039-01reEOPstepconflictswithsmallbreakLOCAanalysis.LER98-039-00hasbeencanceled.With981208ltr.DISTRIBUTIONCODE:IE22TCOPIESRECEIVED:LTRIENCLJSIZE:TITLE:50.73/50.9LicenseeEventReport(LER),IncidentRpt,etc.NOTES:RECIPIENTIDCODE/NAMEPD3-3PDINTERNAL:AEODDRABFILECENRRDEEELBNRR/DRCH/HICBNRR/DRCH/HQMBNRR/DSSA/SPLBRGN3FILE01COPIESLTTRENCL112'1111.11111111RECIPIENTIDCODE/NAMESTANG,JAEOD/SPD/RRABNRR/DE/ECGBNRR/DE/EMEBNRR/DRCH/HOHBNRR/DRPM/PECBRES/DET/EIBCOPIESLTTRENCL11111111111111EXTERNAL:LSTLOBBYWARDNOACPOORE,W.NRCPDR111111LITCOBRYCE,JHNOACQUEENER,DSNUDOCSFULLTXT11'111DNOTETOALL"RIDS"RECIPIENTS:PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATIONREMOVEDFROMDISTRIBUTIONLISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION,CONTACTTHEDOCUMENTCONTROZDESK(DCD)ONEXTENSION415-2083FULLTEXTCONVERSIONREQUIREDTOTALNUMBEROFCOPIESREQUIRED:LTTR22ENCL22  
LER98-039-01 reEOPstepconflicts withsmallbreakLOCAanalysis.LER 98-039-00 hasbeencanceled.
With981208ltr.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:LTR IENCLJSIZE:TITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:RECIPIENT IDCODE/NAME PD3-3PDINTERNAL:
AEODDRABFILECENRRDEEELBNRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RGN3FILE01COPIESLTTRENCL112'1111.11111111RECIPIENT IDCODE/NAME STANG,JAEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HOHB NRR/DRPM/PECB RES/DET/EIB COPIESLTTRENCL11111111111111EXTERNAL:
LSTLOBBYWARDNOACPOORE,W.NRCPDR111111LITCOBRYCE,JHNOACQUEENER,DS NUDOCSFULLTXT11'111DNOTETOALL"RIDS"RECIPIENTS:
PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATION REMOVEDFROMDISTRIBUTION LISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION, CONTACTTHEDOCUMENTCONTROZDESK(DCD)ONEXTENSION 415-2083FULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:
LTTR22ENCL22  


IndianaMichiganPowerCompanyCowNuaew~~~Ran~M).ecioa616MN)lZINDIANANICHIGANIaOWKRDecember8,1998UnitedStatesNuclearRegulatoryCommissionDocumentControlDeskWashington,DC20555OperatingLicenseDPR-58DocketNo.50-315DocumentControlManager:Inaccordancewiththecriteriaestablishedby10CFR50.73entitledLicenseeEventLER315/98-039-01,"Retraction-EmergencyOperationProcedureStepConflictswithSmallBreakLOCAAnalysis".Nocommitmentswereidentifiedinthisdocument.Sincerely,J.R.SampsonSiteVicePresidentImbdAttachmentJ.'L.Caldwell(Acting),RegionIIIR.P.PowersP.A.BarrettJ.B.KingseedR.-WhaleD.HahnRecordsCenter,INPONRCResidentInspector9812140132981208PDRADQCK05000315SPDR NRC,Form366U.S.NUCLEARREGULATORYCOMMISSION(6-1998)LICENSEEEVENTREPORT(LER)(See.reverseforrequirednumberofdigits/charactersforeachblock)APPROVEDBYOM8NO.31604104EXPIRES06/30/2001KSTSIATKDBURDENPKRRESPONSETOCOMPLYWITHTIBSMANDATORYINFORMATlONCOLLKCTCNRKOLJKST'.$0.0HRS.REPORTEDLESSONSLEARNEDARENCORPORATKOerTOTHKLJCKNSLNOPROCESSANOFKOBACKTOINOLJSTRY.FCRWAROCOMMENTSRKCAROLNOBLIOKNKSTSIATKTOTHK~ORMATIONANORECORDSIMNACKMKNTBRANCHIT4FS)).U.S.NUCLEARRKGLAATORYCOMMISSION.WASH)NOTCH.DC2055%001,ANOTOTHKP~RKOLJCTNtrPROJECTL5)5001LH).OFFlCKOFIlAWCKMKNTANOBLJOCKT,WAS)eNOTOJLOCFACIUTYNAMEII)TITLE<<)CookNuclearPlantUnit1DOCKETNUMBER(2)05000-315PAGEP)1of2Retraction-EmergencyOperatingProcedureStepConflictswithSmallBreakLOCAAnalysisEVENTDATE(5)LERNUMBER(6)REPORTDATE(7)OTHERFACILITIESINVOLVED(8)MONTHDAY0824YEARYEARSEQUENTIALNUMBERREVISIONNUMBER19981998-039-01MONTH12DAY081998AILINAMCookUnit2AILINUMB05000-316DNUMOPERATINGMODE(9)50.73(a)(2)(viii)5o.73(a)(2)(i)20.2203(a)(2)(v)20.2201(b)THISREPORTISSUBMITTEDPURSUANTTOTHEREQUIREMENTSOF10CFRg:(Checkoneormore)(11)POWERLEVEL(10)00O'P~P~F%"k~'ti45'NE623J('~820.2203(a)(1)20.2203(a)(2)(i)20.2203(a)(2)(ii)20.2203(a)(2)(iii)20.2203(a)(2)(iv)20.2203(a)(3)(i)20.2203(a)(3)(ii)20.2203(a)(4)50.36(c)(1)50.36(c)(2)LICENSEECONTACTFORTHISLER(12)50.73(a)(2)(ii)50.73(a)(2)(iii)50.73(a)(2)(iv)50.73(a)(2)(v)50.73(a)(2)(vii)50.73(a)(2)(x)73.71OTHERSPeoifyhAbelraclbe)orrornNRCForllr368AMr.LarryWeber,OperationsManagerTELEPHONENUMBER(B)etudeAreaCode)616/465-5901X2443COMPLETEONELINEFOREACHCOMPONENTFAILUREDESCRIBEDINTHISREPORT(13)CAUSESYSTEMCOMPONENTMANUFACTURERREPORTABLETOEPIXCAUSESYSTEMCOMPONENTMANUFACTURERREPORTABLETOEPIXSUPPLEMENTALREPORTEXPECTED(14)YES(IfYes,completeEXPECTEDSUBMISSIONDATEXNOEXPECTEDSUBMISSIONDATE15MONTHDAYAbstract(Limitto1400spaces,l.e.,approximately15single-spacedtypewrittenlines)(16)OnAugust24,1998,withbothunitsinColdShutdown,areviewofthecurrentrevisionofEmergencyOperatingProcedure(EOP),"TransfertoColdLegRecirculation,"identifiedastepthatdidnotappeartosatisfyanassumptionintheWestinghouseSmallBreakLossofCoolantAccident(SBLOCA)analysisatthepointintimewhenhighheadsafetyinjection(Sl)pumpflowwouldbedeliveredtothereactorcoolantsystem(RCS).TheEOPsteprequiredtheSlpumpstobeturnedoffifRCSpressureexceeded1250psig(1000psigforadversecontainmentcondition)afterisolationofthepumpminimumflowlinereturningSIpumpflowtotherefuelingwaterstoragetank(RWST).TheSlpumpswouldbeturnedofftopreventpumpdamageduetoinadequatepumpminimumflow.ThiswouldleaveonlythecentrifugalchargingpumpsinjectingtotheRCSduringaSBLOCAwithhighRCSpressure.TheWestinghouseanalysisassumesSIpumpinjectiontotheRCSwheneverRCSpressureislessthan1350psig.WhenRCSpressureinstrumentuncertaintywasapplied,theEOPsteptoterminateSlwasconsideredcapableofplacingtheplantinaconditionoutsideofthesafetyanalysisduringaSBLOCAthatallowedRCSpressuretoremainhighbutlessthan1350psig.AnENSnotificationwasmadeonAugust24,1998,at1705hoursEDTinaccordancewith10CFR50.72(b)(2)(i).AninterimLERwassubmittedonSeptember22,1998,inaccordancewith10CFR50.73(a)(2)(ii).OperationsprovidedWestinghousewithdetailsoftheuseoftheEOPstepandrequestedananalysisofthesignificanceofthecondition.OnNovember4,1998,Westinghouseprovidedanassessmentbasedonitsanalysis.OurreviewoftheassessmentconfirmedthatbyuseoftheEOPstheplantwouldnothavebeenplacedinaconditionwheretheSlpumpterminationcriterionwouldhavebeenreached.Therefore,theplantwaswithinitsanalyzedbasis,andLER315/98-039-00isbeingretracted.NRCFORM366(6-1998)
IndianaMichiganPowerCompanyCowNuaew~~~Ran~M).ecioa616MN)lZINDIANANICHIGANIaOWKRDecember8,1998UnitedStatesNuclearRegulatory Commission DocumentControlDeskWashington, DC20555Operating LicenseDPR-58DocketNo.50-315DocumentControlManager:Inaccordance withthecriteriaestablished by10CFR50.73entitledLicenseeEventLER315/98-039-01, "Retraction
NRCFORM366AU.S.NUCLEARREGULATORYCOMMISSION(6-1998)LICENSEEEVENTREPORT(LER)TEXTCONTINUATIONFACILITYNAME(1)CookNuclearPlantUnit1DOCKETNUMBER(2)05000-315YEAR1998LERNUMBER(6)SEQUENTIALNUMBER039REVISIONNUMBER01PAGE(3)2of2TEXT(lfmorospeceisrequired,useeddiiionalcopiesorNRCForm(366A)(17)OnAugust24,1998,withbothunitsinColdShutdown,areviewofthecurrentrevision,Revision5,ofEmergencyOperatingProcedure(EOP)01/02-OHP4023.ES-1.3,"TransfertoColdLegRecirculation,"identifiedastepthatdidnotappeartosatisfyanassumptionintheWestinghouseSmallBreakLossofCoolantAccident(SBLOCA)analysisatthetimewhenhighheadsafetyinjection(Sl)pumpflowwouldbedeliveredtothereactorcoolantsystem(RCS).TheEOPsteprequiredtheSlpumpstobeturnedoffifRCSpressureexceeded1250poundspersquareinchgage(psig),1000psigforadversecontainmentconditions,afterisolationofthepumpminimumflowlinereturningSlpumpflowtotherefuelingwaterstoragetank(RWST).TheSlpumpswouldbeturnedofftopreventpumpdamageduetoinadequatepumpminimumflow.ThenormalminimumflowpathtotheRWSTcannotbeusedduringaLOCAbecauseitisundesirabletopumpradioactivelycontaminatedwaterfromthecontainmentsumptotheRWST.Therefore,priortoswitchingSIpumpsuctionfromtheRWSTtothecontainmentsump,asdirectedbytheEOP,theSlpumpminimumflowlinestotheRWSTwouldbeisolated.TheSlpumpswouldthenhavetorelyonRCSinjectionflowtosatisfytherequirementforadequatepumpminimumflowofapproximately70gallonsperminute.ThisflowrateisdeterminedbyactualRCSpressureandthephysicalcharacteristicsofthepumps.IndicatedRCSpressurewaschosenastheproceduralcriterionforoperatorstodetermineiftheSlpumpsneededtobestopped.EarlierrevisionsoftheprocedurehaddirectedthepumpstobestoppedatvariousindicatedRCSpressuresbetween1000psigand1630psig.SomerevisionsoftheprocedurealsousedindicatedlowSlflowtodirectstoppingthepumps.Duetoinstrumentuncertaintytheindicatedvaluescouldhaverepresentedhigherorloweractualvalues.DuringaSBLOCA,pressureincontainmentcouldbehighenoughtohaveanadverseeffectonRCSpressureinstruments.Insuchanadversecontainmentcondition,instrumentuncertaintycouldbegreater.TurningoffthehighheadSlpumpswouldleaveonlythecentrifugalchargingpumpsinjectingtotheRCSduringaSBLOCAwithpersistenthighRCSpressure.TheWestinghouseSBLOCAanalysisassumeshighheadSlpumpinjectiontotheRCSwheneverRCSpressureislessthanapproximately1350psigduringaSBLOCA.Wheninstrumentuncertaintywasapplied,theEOPsteptoterminatehighheadSlwasconsideredcapableofplacingtheplantinaconditionoutsideofthesafetyanalysisduringaSBLOCAthatallowedRCSpressuretoremainhigh,butlessthan1350psig.AnENSnotificationwasmadeonAugust24,1998,at1705hoursEDTinaccordancewith10CFR50.72(b)(2)(i).AninterimLERwassubmittedonSeptember22,1998,inaccordancewith10CFR50.73(a)(2)(ii).OperationsprovidedWestinghousewithdetailsontheuseoftheEOPstepandrequestedananalysisofthesignificanceofthecondition.OnNovember4,1998,Westinghouseprovideditsassessmentoftheconditionbasedonitsanalysis.TheWestinghouseassessmentexamineswhetheradesignbasisSBLOCAfortheCookNuclearPlantwouldleadtoconditionsrequiredbythevariousrevisionsoftheprocedureforSltermination.ToassesstheconditionsthatcouldbepresentedbycontrolroomindicationsfollowingapostulatedSBLOCA,designbasissimulationsusingtheMAAP4computercodewereused.Theeffectsofplantspecificuncertaintieswereincludedintheassessment.ArangeofSBLOCAsizes,downtoverysmallbreaksthatwouldresultinRCSrepressurization,wasconsidered.ThepotentialforoperationwithoutSlflow,withRCSpressuresaslowas835poundspersquareinchabsolute,wasconsidered.This.representsthelowestadversecontainmentRCSpressurewheninstrumenterrorisconsidered,withouttheerrorduetoexcessradiationexposure.Excessradiationwasnotanexpectedcondition.TheassessmentconcludesthatnodesignbasisSBLOCA,requiringoneormoreSlpumps,wouldbedeprivedofflowasaresultofaSBLOCA.TheconclusioniscitedasapplicableforallpastoperationandalsoasapplyingtoaproposedfuturerevisionoftheEOPwhichwouldcallforstoppingtheSIpumpswhentheindicatedRCSpressureis1250psig(1200psigforadversecontainment).Therefore,the'plantwaswithinitsanalyzedconditionofoperation,andLER315/98-039-00isbeingretracted.NRCFORM366A(6-1998)}}
-Emergency Operation Procedure StepConflicts withSmallBreakLOCAAnalysis".
Nocommitments wereidentified inthisdocument.
Sincerely, J.R.SampsonSiteVicePresident ImbdAttachment J.'L.Caldwell(Acting),
RegionIIIR.P.PowersP.A.BarrettJ.B.KingseedR.-WhaleD.HahnRecordsCenter,INPONRCResidentInspector 9812140132 981208PDRADQCK05000315SPDR NRC,Form366U.S.NUCLEARREGULATORY COMMISSION (6-1998)LICENSEEEVENTREPORT(LER)(See.reverse forrequirednumberofdigits/characters foreachblock)APPROVEDBYOM8NO.31604104EXPIRES06/30/2001 KSTSIATKD BURDENPKRRESPONSETOCOMPLYWITHTIBSMANDATORY INFORMATlON COLLKCTCN RKOLJKST'.
$0.0HRS.REPORTEDLESSONSLEARNEDARENCORPORATKO erTOTHKLJCKNSLNO PROCESSANOFKOBACKTOINOLJSTRY.
FCRWAROCOMMENTSRKCAROLNO BLIOKNKSTSIATKTOTHK~ORMATION ANORECORDSIMNACKMKNT BRANCHIT4FS)).U.S.NUCLEARRKGLAATORY COMMISSION.
WASH)NOTCH.
DC2055%001, ANOTOTHKP~RKOLJCTNtr PROJECTL5)5001LH).
OFFlCKOFIlAWCKMKNTANOBLJOCKT,WAS)eNOTOJL OCFACIUTYNAMEII)TITLE<<)CookNuclearPlantUnit1DOCKETNUMBER(2)05000-315 PAGEP)1of2Retraction
-Emergency Operating Procedure StepConflicts withSmallBreakLOCAAnalysisEVENTDATE(5)LERNUMBER(6)REPORTDATE(7)OTHERFACILITIES INVOLVED(8)MONTHDAY0824YEARYEARSEQUENTIAL NUMBERREVISIONNUMBER19981998-039-01MONTH12DAY081998AILINAMCookUnit2AILINUMB05000-316 DNUMOPERATING MODE(9)50.73(a)(2)(viii) 5o.73(a)(2)(i) 20.2203(a)(2)(v) 20.2201(b)THISREPORTISSUBMITTED PURSUANTTOTHEREQUIREMENTS OF10CFRg:(Checkoneormore)(11)POWERLEVEL(10)00O'P~P~F%"k~
'ti45'NE623J('~820.2203(a)(1) 20.2203(a)(2)(i) 20.2203(a)(2)(ii) 20.2203(a)(2)(iii) 20.2203(a)(2)(iv) 20.2203(a)(3)(i) 20.2203(a)(3)(ii) 20.2203(a)(4) 50.36(c)(1) 50.36(c)(2)
LICENSEECONTACTFORTHISLER(12)50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii) 50.73(a)(2)(x) 73.71OTHERSPeoifyhAbelraclbe)orrornNRCForllr 368AMr.LarryWeber,Operations ManagerTELEPHONE NUMBER(B)etudeAreaCode)616/465-5901 X2443COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT(13)CAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE TOEPIXCAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE TOEPIXSUPPLEMENTAL REPORTEXPECTED(14)YES(IfYes,completeEXPECTEDSUBMISSION DATEXNOEXPECTEDSUBMISSION DATE15MONTHDAYAbstract(Limitto1400spaces,l.e.,approximately 15single-spaced typewritten lines)(16)OnAugust24,1998,withbothunitsinColdShutdown, areviewofthecurrentrevisionofEmergency Operating Procedure (EOP),"Transfer toColdLegRecirculation,"
identified astepthatdidnotappeartosatisfyanassumption intheWestinghouse SmallBreakLossofCoolantAccident(SBLOCA)analysisatthepointintimewhenhighheadsafetyinjection (Sl)pumpflowwouldbedelivered tothereactorcoolantsystem(RCS).TheEOPsteprequiredtheSlpumpstobeturnedoffifRCSpressureexceeded1250psig(1000psigforadversecontainment condition) afterisolation ofthepumpminimumflowlinereturning SIpumpflowtotherefueling waterstoragetank(RWST).TheSlpumpswouldbeturnedofftopreventpumpdamageduetoinadequate pumpminimumflow.Thiswouldleaveonlythecentrifugal chargingpumpsinjecting totheRCSduringaSBLOCAwithhighRCSpressure.
TheWestinghouse analysisassumesSIpumpinjection totheRCSwheneverRCSpressureislessthan1350psig.WhenRCSpressureinstrument uncertainty wasapplied,theEOPsteptoterminate Slwasconsidered capableofplacingtheplantinacondition outsideofthesafetyanalysisduringaSBLOCAthatallowedRCSpressuretoremainhighbutlessthan1350psig.AnENSnotification wasmadeonAugust24,1998,at1705hoursEDTinaccordance with10CFR50.72(b)(2)(i).
AninterimLERwassubmitted onSeptember 22,1998,inaccordance with10CFR50.73(a)(2)(ii).
Operations providedWestinghouse withdetailsoftheuseoftheEOPstepandrequested ananalysisofthesignificance ofthecondition.
OnNovember4,1998,Westinghouse providedanassessment basedonitsanalysis.
Ourreviewoftheassessment confirmed thatbyuseoftheEOPstheplantwouldnothavebeenplacedinacondition wheretheSlpumptermination criterion wouldhavebeenreached.Therefore, theplantwaswithinitsanalyzedbasis,andLER315/98-039-00isbeingretracted.
NRCFORM366(6-1998)
NRCFORM366AU.S.NUCLEARREGULATORY COMMISSION (6-1998)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION FACILITYNAME(1)CookNuclearPlantUnit1DOCKETNUMBER(2) 05000-315 YEAR1998LERNUMBER(6)SEQUENTIAL NUMBER039REVISIONNUMBER01PAGE(3)2of2TEXT(lfmorospeceisrequired, useeddiiional copiesorNRCForm(366A)(17)OnAugust24,1998,withbothunitsinColdShutdown, areviewofthecurrentrevision, Revision5,ofEmergency Operating Procedure (EOP)01/02-OHP 4023.ES-1.3, "Transfer toColdLegRecirculation,"
identified astepthatdidnotappeartosatisfyanassumption intheWestinghouse SmallBreakLossofCoolantAccident(SBLOCA)analysisatthetimewhenhighheadsafetyinjection (Sl)pumpflowwouldbedelivered tothereactorcoolantsystem(RCS).TheEOPsteprequiredtheSlpumpstobeturnedoffifRCSpressureexceeded1250poundspersquareinchgage(psig),1000psigforadversecontainment conditions, afterisolation ofthepumpminimumflowlinereturning Slpumpflowtotherefueling waterstoragetank(RWST).TheSlpumpswouldbeturnedofftopreventpumpdamageduetoinadequate pumpminimumflow.ThenormalminimumflowpathtotheRWSTcannotbeusedduringaLOCAbecauseitisundesirable topumpradioactively contaminated waterfromthecontainment sumptotheRWST.Therefore, priortoswitching SIpumpsuctionfromtheRWSTtothecontainment sump,asdirectedbytheEOP,theSlpumpminimumflowlinestotheRWSTwouldbeisolated.
TheSlpumpswouldthenhavetorelyonRCSinjection flowtosatisfytherequirement foradequatepumpminimumflowofapproximately 70gallonsperminute.Thisflowrateisdetermined byactualRCSpressureandthephysicalcharacteristics ofthepumps.Indicated RCSpressurewaschosenastheprocedural criterion foroperators todetermine iftheSlpumpsneededtobestopped.Earlierrevisions oftheprocedure haddirectedthepumpstobestoppedatvariousindicated RCSpressures between1000psigand1630psig.Somerevisions oftheprocedure alsousedindicated lowSlflowtodirectstoppingthepumps.Duetoinstrument uncertainty theindicated valuescouldhaverepresented higherorloweractualvalues.DuringaSBLOCA,pressureincontainment couldbehighenoughtohaveanadverseeffectonRCSpressureinstruments.
Insuchanadversecontainment condition, instrument uncertainty couldbegreater.TurningoffthehighheadSlpumpswouldleaveonlythecentrifugal chargingpumpsinjecting totheRCSduringaSBLOCAwithpersistent highRCSpressure.
TheWestinghouse SBLOCAanalysisassumeshighheadSlpumpinjection totheRCSwheneverRCSpressureislessthanapproximately 1350psigduringaSBLOCA.Wheninstrument uncertainty wasapplied,theEOPsteptoterminate highheadSlwasconsidered capableofplacingtheplantinacondition outsideofthesafetyanalysisduringaSBLOCAthatallowedRCSpressuretoremainhigh,butlessthan1350psig.AnENSnotification wasmadeonAugust24,1998,at1705hoursEDTinaccordance with10CFR50.72(b)(2)(i).
AninterimLERwassubmitted onSeptember 22,1998,inaccordance with10CFR50.73 (a)(2)(ii).
Operations providedWestinghouse withdetailsontheuseoftheEOPstepandrequested ananalysisofthesignificance ofthecondition.
OnNovember4,1998,Westinghouse provideditsassessment ofthecondition basedonitsanalysis.
TheWestinghouse assessment examineswhetheradesignbasisSBLOCAfortheCookNuclearPlantwouldleadtoconditions requiredbythevariousrevisions oftheprocedure forSltermination.
Toassesstheconditions thatcouldbepresented bycontrolroomindications following apostulated SBLOCA,designbasissimulations usingtheMAAP4computercodewereused.Theeffectsofplantspecificuncertainties wereincludedintheassessment.
ArangeofSBLOCAsizes,downtoverysmallbreaksthatwouldresultinRCSrepressurization, wasconsidered.
Thepotential foroperation withoutSlflow,withRCSpressures aslowas835poundspersquareinchabsolute, wasconsidered.
This.represents thelowestadversecontainment RCSpressurewheninstrument errorisconsidered, withouttheerrorduetoexcessradiation exposure.
Excessradiation wasnotanexpectedcondition.
Theassessment concludes thatnodesignbasisSBLOCA,requiring oneormoreSlpumps,wouldbedeprivedofflowasaresultofaSBLOCA.Theconclusion iscitedasapplicable forallpastoperation andalsoasapplyingtoaproposedfuturerevisionoftheEOPwhichwouldcallforstoppingtheSIpumpswhentheindicated RCSpressureis1250psig(1200psigforadversecontainment).
Therefore, the'plantwaswithinitsanalyzedcondition ofoperation, andLER315/98-039-00 isbeingretracted.
NRCFORM366A(6-1998)}}

Revision as of 06:07, 29 June 2018

LER 98-039-01 Re EOP Step Conflicts with Small Break LOCA Analysis.Ler 98-039-00 Has Been Canceled.With 981208 Ltr
ML17335A382
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 12/08/1998
From: SAMPSON J R, WEBER L
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-98-039, LER-98-39, NUDOCS 9812140132
Download: ML17335A382 (5)


Text

~CA.TEGORYREGULATORY INFORMATION DISTRIBUTION SYSTEM(RZDS)ACCESSION NBR:9812140132 DOC.DATE:

98/12/08NOTARIZED:

NOFACIL:50-315 DonaldC.CookNuclearPowerPlant,Unit1,IndianaMAUTH.NAMEAUTHORAFFILIATION WEBER,L.IndianaMichiganPowerCo.SAMPSON,'J.R.

IndianaMichiganPowerCo.RECIP.NAME RECIPIENT AFFILIATION DOCKET05000315

SUBJECT:

LER98-039-01 reEOPstepconflicts withsmallbreakLOCAanalysis.LER 98-039-00 hasbeencanceled.

With981208ltr.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:LTR IENCLJSIZE:TITLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.NOTES:RECIPIENT IDCODE/NAME PD3-3PDINTERNAL:

AEODDRABFILECENRRDEEELBNRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RGN3FILE01COPIESLTTRENCL112'1111.11111111RECIPIENT IDCODE/NAME STANG,JAEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HOHB NRR/DRPM/PECB RES/DET/EIB COPIESLTTRENCL11111111111111EXTERNAL:

LSTLOBBYWARDNOACPOORE,W.NRCPDR111111LITCOBRYCE,JHNOACQUEENER,DS NUDOCSFULLTXT11'111DNOTETOALL"RIDS"RECIPIENTS:

PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATION REMOVEDFROMDISTRIBUTION LISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION, CONTACTTHEDOCUMENTCONTROZDESK(DCD)ONEXTENSION 415-2083FULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:

LTTR22ENCL22

IndianaMichiganPowerCompanyCowNuaew~~~Ran~M).ecioa616MN)lZINDIANANICHIGANIaOWKRDecember8,1998UnitedStatesNuclearRegulatory Commission DocumentControlDeskWashington, DC20555Operating LicenseDPR-58DocketNo.50-315DocumentControlManager:Inaccordance withthecriteriaestablished by10CFR50.73entitledLicenseeEventLER315/98-039-01, "Retraction

-Emergency Operation Procedure StepConflicts withSmallBreakLOCAAnalysis".

Nocommitments wereidentified inthisdocument.

Sincerely, J.R.SampsonSiteVicePresident ImbdAttachment J.'L.Caldwell(Acting),

RegionIIIR.P.PowersP.A.BarrettJ.B.KingseedR.-WhaleD.HahnRecordsCenter,INPONRCResidentInspector 9812140132 981208PDRADQCK05000315SPDR NRC,Form366U.S.NUCLEARREGULATORY COMMISSION (6-1998)LICENSEEEVENTREPORT(LER)(See.reverse forrequirednumberofdigits/characters foreachblock)APPROVEDBYOM8NO.31604104EXPIRES06/30/2001 KSTSIATKD BURDENPKRRESPONSETOCOMPLYWITHTIBSMANDATORY INFORMATlON COLLKCTCN RKOLJKST'.

$0.0HRS.REPORTEDLESSONSLEARNEDARENCORPORATKO erTOTHKLJCKNSLNO PROCESSANOFKOBACKTOINOLJSTRY.

FCRWAROCOMMENTSRKCAROLNO BLIOKNKSTSIATKTOTHK~ORMATION ANORECORDSIMNACKMKNT BRANCHIT4FS)).U.S.NUCLEARRKGLAATORY COMMISSION.

WASH)NOTCH.

DC2055%001, ANOTOTHKP~RKOLJCTNtr PROJECTL5)5001LH).

OFFlCKOFIlAWCKMKNTANOBLJOCKT,WAS)eNOTOJL OCFACIUTYNAMEII)TITLE<<)CookNuclearPlantUnit1DOCKETNUMBER(2)05000-315 PAGEP)1of2Retraction

-Emergency Operating Procedure StepConflicts withSmallBreakLOCAAnalysisEVENTDATE(5)LERNUMBER(6)REPORTDATE(7)OTHERFACILITIES INVOLVED(8)MONTHDAY0824YEARYEARSEQUENTIAL NUMBERREVISIONNUMBER19981998-039-01MONTH12DAY081998AILINAMCookUnit2AILINUMB05000-316 DNUMOPERATING MODE(9)50.73(a)(2)(viii) 5o.73(a)(2)(i) 20.2203(a)(2)(v) 20.2201(b)THISREPORTISSUBMITTED PURSUANTTOTHEREQUIREMENTS OF10CFRg:(Checkoneormore)(11)POWERLEVEL(10)00O'P~P~F%"k~

'ti45'NE623J('~820.2203(a)(1) 20.2203(a)(2)(i) 20.2203(a)(2)(ii) 20.2203(a)(2)(iii) 20.2203(a)(2)(iv) 20.2203(a)(3)(i) 20.2203(a)(3)(ii) 20.2203(a)(4) 50.36(c)(1) 50.36(c)(2)

LICENSEECONTACTFORTHISLER(12)50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii) 50.73(a)(2)(x) 73.71OTHERSPeoifyhAbelraclbe)orrornNRCForllr 368AMr.LarryWeber,Operations ManagerTELEPHONE NUMBER(B)etudeAreaCode)616/465-5901 X2443COMPLETEONELINEFOREACHCOMPONENT FAILUREDESCRIBED INTHISREPORT(13)CAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE TOEPIXCAUSESYSTEMCOMPONENT MANUFACTURER REPORTABLE TOEPIXSUPPLEMENTAL REPORTEXPECTED(14)YES(IfYes,completeEXPECTEDSUBMISSION DATEXNOEXPECTEDSUBMISSION DATE15MONTHDAYAbstract(Limitto1400spaces,l.e.,approximately 15single-spaced typewritten lines)(16)OnAugust24,1998,withbothunitsinColdShutdown, areviewofthecurrentrevisionofEmergency Operating Procedure (EOP),"Transfer toColdLegRecirculation,"

identified astepthatdidnotappeartosatisfyanassumption intheWestinghouse SmallBreakLossofCoolantAccident(SBLOCA)analysisatthepointintimewhenhighheadsafetyinjection (Sl)pumpflowwouldbedelivered tothereactorcoolantsystem(RCS).TheEOPsteprequiredtheSlpumpstobeturnedoffifRCSpressureexceeded1250psig(1000psigforadversecontainment condition) afterisolation ofthepumpminimumflowlinereturning SIpumpflowtotherefueling waterstoragetank(RWST).TheSlpumpswouldbeturnedofftopreventpumpdamageduetoinadequate pumpminimumflow.Thiswouldleaveonlythecentrifugal chargingpumpsinjecting totheRCSduringaSBLOCAwithhighRCSpressure.

TheWestinghouse analysisassumesSIpumpinjection totheRCSwheneverRCSpressureislessthan1350psig.WhenRCSpressureinstrument uncertainty wasapplied,theEOPsteptoterminate Slwasconsidered capableofplacingtheplantinacondition outsideofthesafetyanalysisduringaSBLOCAthatallowedRCSpressuretoremainhighbutlessthan1350psig.AnENSnotification wasmadeonAugust24,1998,at1705hoursEDTinaccordance with10CFR50.72(b)(2)(i).

AninterimLERwassubmitted onSeptember 22,1998,inaccordance with10CFR50.73(a)(2)(ii).

Operations providedWestinghouse withdetailsoftheuseoftheEOPstepandrequested ananalysisofthesignificance ofthecondition.

OnNovember4,1998,Westinghouse providedanassessment basedonitsanalysis.

Ourreviewoftheassessment confirmed thatbyuseoftheEOPstheplantwouldnothavebeenplacedinacondition wheretheSlpumptermination criterion wouldhavebeenreached.Therefore, theplantwaswithinitsanalyzedbasis,andLER315/98-039-00isbeingretracted.

NRCFORM366(6-1998)

NRCFORM366AU.S.NUCLEARREGULATORY COMMISSION (6-1998)LICENSEEEVENTREPORT(LER)TEXTCONTINUATION FACILITYNAME(1)CookNuclearPlantUnit1DOCKETNUMBER(2) 05000-315 YEAR1998LERNUMBER(6)SEQUENTIAL NUMBER039REVISIONNUMBER01PAGE(3)2of2TEXT(lfmorospeceisrequired, useeddiiional copiesorNRCForm(366A)(17)OnAugust24,1998,withbothunitsinColdShutdown, areviewofthecurrentrevision, Revision5,ofEmergency Operating Procedure (EOP)01/02-OHP 4023.ES-1.3, "Transfer toColdLegRecirculation,"

identified astepthatdidnotappeartosatisfyanassumption intheWestinghouse SmallBreakLossofCoolantAccident(SBLOCA)analysisatthetimewhenhighheadsafetyinjection (Sl)pumpflowwouldbedelivered tothereactorcoolantsystem(RCS).TheEOPsteprequiredtheSlpumpstobeturnedoffifRCSpressureexceeded1250poundspersquareinchgage(psig),1000psigforadversecontainment conditions, afterisolation ofthepumpminimumflowlinereturning Slpumpflowtotherefueling waterstoragetank(RWST).TheSlpumpswouldbeturnedofftopreventpumpdamageduetoinadequate pumpminimumflow.ThenormalminimumflowpathtotheRWSTcannotbeusedduringaLOCAbecauseitisundesirable topumpradioactively contaminated waterfromthecontainment sumptotheRWST.Therefore, priortoswitching SIpumpsuctionfromtheRWSTtothecontainment sump,asdirectedbytheEOP,theSlpumpminimumflowlinestotheRWSTwouldbeisolated.

TheSlpumpswouldthenhavetorelyonRCSinjection flowtosatisfytherequirement foradequatepumpminimumflowofapproximately 70gallonsperminute.Thisflowrateisdetermined byactualRCSpressureandthephysicalcharacteristics ofthepumps.Indicated RCSpressurewaschosenastheprocedural criterion foroperators todetermine iftheSlpumpsneededtobestopped.Earlierrevisions oftheprocedure haddirectedthepumpstobestoppedatvariousindicated RCSpressures between1000psigand1630psig.Somerevisions oftheprocedure alsousedindicated lowSlflowtodirectstoppingthepumps.Duetoinstrument uncertainty theindicated valuescouldhaverepresented higherorloweractualvalues.DuringaSBLOCA,pressureincontainment couldbehighenoughtohaveanadverseeffectonRCSpressureinstruments.

Insuchanadversecontainment condition, instrument uncertainty couldbegreater.TurningoffthehighheadSlpumpswouldleaveonlythecentrifugal chargingpumpsinjecting totheRCSduringaSBLOCAwithpersistent highRCSpressure.

TheWestinghouse SBLOCAanalysisassumeshighheadSlpumpinjection totheRCSwheneverRCSpressureislessthanapproximately 1350psigduringaSBLOCA.Wheninstrument uncertainty wasapplied,theEOPsteptoterminate highheadSlwasconsidered capableofplacingtheplantinacondition outsideofthesafetyanalysisduringaSBLOCAthatallowedRCSpressuretoremainhigh,butlessthan1350psig.AnENSnotification wasmadeonAugust24,1998,at1705hoursEDTinaccordance with10CFR50.72(b)(2)(i).

AninterimLERwassubmitted onSeptember 22,1998,inaccordance with10CFR50.73 (a)(2)(ii).

Operations providedWestinghouse withdetailsontheuseoftheEOPstepandrequested ananalysisofthesignificance ofthecondition.

OnNovember4,1998,Westinghouse provideditsassessment ofthecondition basedonitsanalysis.

TheWestinghouse assessment examineswhetheradesignbasisSBLOCAfortheCookNuclearPlantwouldleadtoconditions requiredbythevariousrevisions oftheprocedure forSltermination.

Toassesstheconditions thatcouldbepresented bycontrolroomindications following apostulated SBLOCA,designbasissimulations usingtheMAAP4computercodewereused.Theeffectsofplantspecificuncertainties wereincludedintheassessment.

ArangeofSBLOCAsizes,downtoverysmallbreaksthatwouldresultinRCSrepressurization, wasconsidered.

Thepotential foroperation withoutSlflow,withRCSpressures aslowas835poundspersquareinchabsolute, wasconsidered.

This.represents thelowestadversecontainment RCSpressurewheninstrument errorisconsidered, withouttheerrorduetoexcessradiation exposure.

Excessradiation wasnotanexpectedcondition.

Theassessment concludes thatnodesignbasisSBLOCA,requiring oneormoreSlpumps,wouldbedeprivedofflowasaresultofaSBLOCA.Theconclusion iscitedasapplicable forallpastoperation andalsoasapplyingtoaproposedfuturerevisionoftheEOPwhichwouldcallforstoppingtheSIpumpswhentheindicated RCSpressureis1250psig(1200psigforadversecontainment).

Therefore, the'plantwaswithinitsanalyzedcondition ofoperation, andLER315/98-039-00 isbeingretracted.

NRCFORM366A(6-1998)