IR 05000352/2018001: Difference between revisions

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=Text=
=Text=
{{#Wiki_filter:UNITED STATES May 11, 2018
{{#Wiki_filter:May 11, 2018


==SUBJECT:==
==SUBJECT:==
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Sincerely,
Sincerely,
/RA/
/RA/  
James A. Krafty, Acting Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Numbers: 50-352 and 50-353 License Numbers: NPF-39 and NPF-85
 
James A. Krafty, Acting Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Numbers: 50-352 and 50-353 License Numbers: NPF-39 and NPF-85  


===Enclosure:===
===Enclosure:===
Inspection Report 05000352/2018001 and 05000353/2018001
Inspection Report 05000352/2018001 and 05000353/2018001  


==Inspection Report==
==Inspection Report==
Docket Numbers: 50-352 and 50-353 License Numbers: NPF-39 and NPF-85 Report Numbers: 05000352/2018001 and 05000353/2018001 Enterprise Identifier: I-2018-001-0071 Licensee: Exelon Generation Company, LLC Facility: Limerick Generating Station, Units 1 & 2 Location: Sanatoga, PA 19464 Inspection Dates: January 1, 2018 through March 31, 2018 Inspectors: S. Rutenkroger, PhD, Senior Resident Inspector M. Fannon, Resident Inspector H. Anagnostopoulos, Senior Health Physicist J. Furia, Senior Health Physicist Approved By: J. Krafty, Acting Chief Reactor Projects Branch 4 Division of Reactor Projects Enclosure
Docket Numbers:  
 
50-352 and 50-353  
 
License Numbers:  
 
NPF-39 and NPF-85  
 
Report Numbers:  
 
05000352/2018001 and 05000353/2018001  
 
Enterprise Identifier:
I-2018-001-0071  
 
Licensee:  
 
Exelon Generation Company, LLC  
 
Facility:  
 
Limerick Generating Station, Units 1 & 2  
 
Location:  
 
Sanatoga, PA 19464  
 
Inspection Dates:  
 
January 1, 2018 through March 31, 2018  
 
Inspectors:  
 
S. Rutenkroger, PhD, Senior Resident Inspector  
 
M. Fannon, Resident Inspector  
 
H. Anagnostopoulos, Senior Health Physicist  
 
J. Furia, Senior Health Physicist  
 
Approved By:  
 
J. Krafty, Acting Chief  
 
Reactor Projects Branch 4  
 
Division of Reactor Projects  


=SUMMARY=
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Exelons performance at
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Exelons performance at  


Limerick Generating Station Units 1 and 2 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.
Limerick Generating Station Units 1 and 2 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.
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Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC identified and self-revealed findings, violations, and additional items are summarized in the table below.
Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC identified and self-revealed findings, violations, and additional items are summarized in the table below.


List of Findings and Violations Failure of Emergency Diesel Generator Lube Oil Pipe Nipple Fitting Cornerstone           Significance                               Cross-cutting     Report Aspect            Section Mitigating           Green NCV                                   [P.1] -            71153 Systems              05000353/2018001-01                         Identification Opened/Closed A self-revealed Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI,
===List of Findings and Violations===
Failure of Emergency Diesel Generator Lube Oil Pipe Nipple Fitting Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000353/2018001-01 Opened/Closed  
[P.1] -
Identification 71153 A self-revealed Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI,
Corrective Action, and LGS Unit 2 technical specification (TS) 3.8.1.1 was identified when Exelon failed to correct a degraded lube oil pipe nipple fitting on the D22 emergency diesel generator (EDG) when maintenance was performed to address leakage which caused inoperability of the EDG for greater than its TS allowed outage time.
Corrective Action, and LGS Unit 2 technical specification (TS) 3.8.1.1 was identified when Exelon failed to correct a degraded lube oil pipe nipple fitting on the D22 emergency diesel generator (EDG) when maintenance was performed to address leakage which caused inoperability of the EDG for greater than its TS allowed outage time.


Emergency Diesel Generator Combustion Air Overheating Cornerstone           Significance                               Cross-cutting     Report Aspect            Section Mitigating           Green NCV                                   [P.3] -            71153 Systems              05000352/2018001-02                         Resolution Opened/Closed A self-revealed Green NCV of LGS Unit 1 TS 6.8.1 and TS 3.8.1.1 was identified when Exelon failed to properly maintain an operating procedure to maintain a fail-safe design feature for the EDGs which led to the D12 EDG combustion air overheating and caused the EDG to be inoperable for greater than its TS allowed outage time.
Emergency Diesel Generator Combustion Air Overheating Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000352/2018001-02 Opened/Closed  
[P.3] -
Resolution 71153 A self-revealed Green NCV of LGS Unit 1 TS 6.8.1 and TS 3.8.1.1 was identified when Exelon failed to properly maintain an operating procedure to maintain a fail-safe design feature for the EDGs which led to the D12 EDG combustion air overheating and caused the EDG to be inoperable for greater than its TS allowed outage time.


Additional Tracking Items Type     Issue number               Title                           Report       Status Section LER       05000353/2017-008-00       EDG Inoperable for Greater      71153        Closed 05000353/2017-008-01       Than 30 Days Resulting in a Condition Prohibited by Technical Specifications LER       05000352/2018-001-00       D12 EDG Inoperable for           71153        Closed Greater than 30 Days Resulting in a Condition Prohibited by TS
===Additional Tracking Items===
Type Issue number Title Report Section Status LER 05000353/2017-008-00 05000353/2017-008-01 EDG Inoperable for Greater Than 30 Days Resulting in a Condition Prohibited by Technical Specifications 71153 Closed LER 05000352/2018-001-00 D12 EDG Inoperable for Greater than 30 Days Resulting in a Condition Prohibited by TS 71153 Closed


=PLANT STATUS=
=PLANT STATUS=
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==REACTOR SAFETY==
==REACTOR SAFETY==
 
==71111.01 - Adverse Weather Protection==
==71111.01 - Adverse Weather Protection
 
===Impending Severe Weather (2 samples)===
===Impending Severe Weather (2 samples)===
  ==
: (1) The inspectors evaluated readiness for impending adverse weather conditions for the onset of winter weather, including high winds, on January 5, 2018.
: (1) The inspectors evaluated readiness for impending adverse weather conditions for the onset of winter weather, including high winds, on January 5, 2018.
: (2) The inspectors evaluated readiness for impending adverse weather conditions for the onset of winter weather, including high winds, on March 2, 2018.
: (2) The inspectors evaluated readiness for impending adverse weather conditions for the onset of winter weather, including high winds, on March 2, 2018.


==71111.04 - Equipment Alignment
==71111.04 - Equipment Alignment==
 
===Partial Walkdown (5 samples)===
===Partial Walkdown (5 samples)===
  ==
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
: (1) Unit 2 high pressure coolant injection on January 16 and 17, 2018
: (1) Unit 2 high pressure coolant injection on January 16 and 17, 2018
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: (5) Unit 1 D12 EDG during the division 1 and 3 direct current bus maintenance window on March 28, 2018
: (5) Unit 1 D12 EDG during the division 1 and 3 direct current bus maintenance window on March 28, 2018


==71111.05 - Fire Protection
==71111.05 - Fire Protection==
 
===Quarterly Inspection (5 samples)===
===Quarterly Inspection (5 samples)===
==
The inspectors evaluated fire protection program implementation in the following selected areas:
The inspectors evaluated fire protection program implementation in the following selected areas:
: (1) Fire area 2, Unit common 13.2kV switchgear room, elevation 217, on January 8, 2018
: (1) Fire area 2, Unit common 13.2kV switchgear room, elevation 217, on January 8, 2018
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: (5) Fire area 43, Unit 1 safeguard isolation valve area room 309, elevation 217, on March 28, 2018
: (5) Fire area 43, Unit 1 safeguard isolation valve area room 309, elevation 217, on March 28, 2018


==71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance
==71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance==
==
 
===Operator Requalification (1 sample)===
===Operator Requalification (1 sample)===
The inspectors observed and evaluated licensed operator simulator training scenarios on
The inspectors observed and evaluated licensed operator simulator training scenarios on February 20, 2018.


===February 20, 2018.
===Operator Performance (1 sample)===
Operator Performance (1 sample)===
The inspectors observed the downpower and normal plant shutdown of Unit 1 for a planned refueling outage on March 25 and 26, 2018
The inspectors observed the downpower and normal plant shutdown of Unit 1 for a planned refueling outage on March 25 and 26, 2018


==71111.12 - Maintenance Effectiveness
==71111.12 - Maintenance Effectiveness==
 
===Routine Maintenance Effectiveness (2 samples)===
===Routine Maintenance Effectiveness (2 samples)===
==
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
: (1) Unit 1 reactor manual control system
: (1) Unit 1 reactor manual control system
: (2) Unit 2 reactor manual control system
: (2) Unit 2 reactor manual control system


==71111.13 - Maintenance Risk Assessments and Emergent Work Control (6 samples)
==71111.13 - Maintenance Risk Assessments and Emergent Work Control (6 samples)==
==
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
: (1) Unit 2 reactor core isolation cooling relay replacements on January 16 and 17, 2018
: (1) Unit 2 reactor core isolation cooling relay replacements on January 16 and 17, 2018
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: (6) Unit 1 A emergency core cooling system maintenance during reduced core inventory in the refueling outage on March 27 and 28, 2018
: (6) Unit 1 A emergency core cooling system maintenance during reduced core inventory in the refueling outage on March 27 and 28, 2018


==71111.15 - Operability Determinations and Functionality Assessments (6 samples)
==71111.15 - Operability Determinations and Functionality Assessments (6 samples)==
==
The inspectors evaluated the following operability determinations and functionality assessments:
The inspectors evaluated the following operability determinations and functionality assessments:
: (1) Unit 2, D21 EDG room low temperature alarm on December 31, 2017
: (1) Unit 2, D21 EDG room low temperature alarm on December 31, 2017
Line 136: Line 176:
: (6) Unit common, B control room air supply controller not properly maintaining room temperature on February 4, 2018
: (6) Unit common, B control room air supply controller not properly maintaining room temperature on February 4, 2018


==71111.18 - Plant Modifications (2 samples)
==71111.18 - Plant Modifications (2 samples)==
==
The inspectors evaluated the following temporary or permanent modifications:
The inspectors evaluated the following temporary or permanent modifications:
: (1) Engineering change package 622647 - Inflatable Seal - Secondary Containment
: (1) Engineering change package 622647 - Inflatable Seal - Secondary Containment
: (2) Engineering change request 433952, D23 Repair of the Blower Inspection Cover Bolt Holes Using Stainless Steel Heli-Coil Thread Inserts
: (2) Engineering change request 433952, D23 Repair of the Blower Inspection Cover Bolt Holes Using Stainless Steel Heli-Coil Thread Inserts


==71111.19 - Post Maintenance Testing (6 samples)
==71111.19 - Post Maintenance Testing (6 samples)==
==
The inspectors evaluated post maintenance testing for the following maintenance/repair activities:
The inspectors evaluated post maintenance testing for the following maintenance/repair activities:
: (1) Unit 2 D24 EDG fuse replacement following an intermittent issue in the automatic start logic circuit on December 6, 2017
: (1) Unit 2 D24 EDG fuse replacement following an intermittent issue in the automatic start logic circuit on December 6, 2017
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: (6) Unit 2 D24 EDG heating, ventilation, and cooling fan controller replacement on February 22, 2018
: (6) Unit 2 D24 EDG heating, ventilation, and cooling fan controller replacement on February 22, 2018


==71111.20 - Refueling and Other Outage Activities
==71111.20 - Refueling and Other Outage Activities==
==
The inspectors evaluated the Unit 1 refueling outage 1R17 from March 26, 2018, through the end of the inspection period. The following portions of the inspection procedure were not performed during this period.
The inspectors evaluated the Unit 1 refueling outage 1R17 from March 26, 2018, through the end of the inspection period. The following portions of the inspection procedure were not performed during this period.
: (1) Fatigue Management
: (1) Fatigue Management
: (2) Startup
: (2) Startup


==71111.22 - Surveillance Testing   The inspectors evaluated the following surveillance tests:
==71111.22 - Surveillance Testing==
==
The inspectors evaluated the following surveillance tests:  


===Routine (3 samples)===
===Routine===
{{IP sample|IP=IP 71111.22|count=3}}
: (1) ST-6-092-113-2, D23 EDG 24 hour endurance run on January 18 and 19, 2018
: (1) ST-6-092-113-2, D23 EDG 24 hour endurance run on January 18 and 19, 2018
: (2) RT-6-051-320-1, Unit 1 B residual heat removal remote operation test on February 7, 2018
: (2) RT-6-051-320-1, Unit 1 B residual heat removal remote operation test on February 7, 2018
: (3) ST-2-074-642-1, Unit 1 source range and intermediate range neutron monitors pre-shutdown testing on March 18, 2018
: (3) ST-2-074-642-1, Unit 1 source range and intermediate range neutron monitors pre-shutdown testing on March 18, 2018  


===In-service (2 samples)===
===In-service (2 samples)===
: (1) ST-6-052-231-1, Unit 1 A core spray pump, valve, and flow test on January 4, 2018
: (1) ST-6-052-231-1, Unit 1 A core spray pump, valve, and flow test on January 4, 2018
: (2) ST-6-052-232-1, Unit 1 B core spray pump, valve, and flow test on March 10, 2018
: (2) ST-6-052-232-1, Unit 1 B core spray pump, valve, and flow test on March 10, 2018  


===Containment Isolation Valve (2 samples)===
===Containment Isolation Valve (2 samples)===
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==RADIATION SAFETY==
==RADIATION SAFETY==
 
==71124.02 - Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls==
==71124.02 - Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls
==
 
===Radiological Work Planning (1 sample)===
===Radiological Work Planning (1 sample)===
The inspectors evaluated Exelons radiological work planning by reviewing the following activities:
The inspectors evaluated Exelons radiological work planning by reviewing the following activities:
: (1) ALARA Plan 2017-101
: (1) ALARA Plan 2017-101
: (2) ALARA Plan 2017-050
: (2) ALARA Plan 2017-050
: (3) ALARA Plan 2017-052 Verification of Dose Estimates and Exposure Tracking Systems (1 sample)
: (3) ALARA Plan 2017-052  
 
===Verification of Dose Estimates and Exposure Tracking Systems (1 sample)===
The inspectors evaluated dose estimates and exposure tracking.
The inspectors evaluated dose estimates and exposure tracking.


==71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation
==71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,==
==
and Transportation  
 
===Radioactive Material Storage===
{{IP sample|IP=IP 71124.08|count=1}}


===Radioactive Material Storage (1 sample)===
The inspectors observed radioactive waste container storage areas and verified the postings and controls and that Exelon had established a process for monitoring the impact of long-term storage of the waste.
The inspectors observed radioactive waste container storage areas and verified the postings and controls and that Exelon had established a process for monitoring the impact of long-term storage of the waste.


===Radioactive Waste System Walkdown (1 sample)===
===Radioactive Waste System Walkdown (1 sample)===
The inspectors walked down the following:
The inspectors walked down the following:  
Accessible portions of liquid and solid radioactive waste processing systems to verify current system alignment and material condition Abandoned in place radioactive waste processing equipment to review the controls in place to ensure protection of personnel Changes made to the radioactive waste processing systems since the last inspection Processes for mixing and transferring radioactive waste resin and/or sludge discharges into shipping/disposal containers Current methods and procedures for dewatering waste
 
Accessible portions of liquid and solid radioactive waste processing systems to verify current system alignment and material condition  
 
Abandoned in place radioactive waste processing equipment to review the controls in place to ensure protection of personnel  
 
Changes made to the radioactive waste processing systems since the last inspection  
 
Processes for mixing and transferring radioactive waste resin and/or sludge discharges into shipping/disposal containers  
 
Current methods and procedures for dewatering waste  


===Waste Characterization and Classification (1 sample)===
===Waste Characterization and Classification (1 sample)===
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==OTHER ACTIVITIES - BASELINE==
==OTHER ACTIVITIES - BASELINE==
===71151 - Performance Indicator Verification===
{{IP sample|IP=IP 71151|count=6}}


===71151 - Performance Indicator Verification ===
{{IP sample|IP=IP 71151|count=6}}
The inspectors verified Exelons performance indicator submittals listed below for the period January 1, 2017 through December 31, 2017.
The inspectors verified Exelons performance indicator submittals listed below for the period January 1, 2017 through December 31, 2017.
: (1) Unit 1 and Unit 2 Unplanned Power Changes per 7000 Critical Hours
: (1) Unit 1 and Unit 2 Unplanned Power Changes per 7000 Critical Hours
: (2) Unit 1 and Unit 2 High Pressure Injection Systems
: (2) Unit 1 and Unit 2 High Pressure Injection Systems
: (3) Unit 1 and Unit 2 Heat Removal Systems
: (3) Unit 1 and Unit 2 Heat Removal Systems  


===71153 - Follow-up of Events and Notices of Enforcement Discretion   Licensee Event Reports (LER) ===
===71153 - Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports (LER)===
{{IP sample|IP=IP 71153|count=2}}
{{IP sample|IP=IP 71153|count=2}}
The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:
The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:
: (1) LER 05000353/2017-008-00 and 05000353/2017-008-01, EDG Inoperable for Greater Than 30 Days Resulting in a Condition Prohibited by Technical Specifications, on December 11, 2017, and February 22, 2018. The review for this event is documented in the inspection results section.
: (1) LER 05000353/2017-008-00 and 05000353/2017-008-01, EDG Inoperable for Greater Than 30 Days Resulting in a Condition Prohibited by Technical Specifications, on December 11, 2017, and February 22, 2018. The review for this event is documented in the inspection results section.
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==INSPECTION RESULTS==
==INSPECTION RESULTS==
Failure of Emergency Diesel Generator Lube Oil Pipe Nipple Fitting Cornerstone             Significance                             Cross-cutting       Report Aspect              Section Mitigating               Green                                     [P.1] -            71153 Systems                  NCV                                       Identification 05000353/2018001-01 Opened/Closed A self-revealed Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, and LGS Unit 2 technical specification (TS) 3.8.1.1 was identified when Exelon failed to correct a degraded lube oil pipe nipple fitting on the D22 EDG when maintenance was performed to address leakage which caused inoperability of the EDG for greater than its TS allowed outage time.
Failure of Emergency Diesel Generator Lube Oil Pipe Nipple Fitting Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000353/2018001-01 Opened/Closed  
[P.1] -
Identification 71153 A self-revealed Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, and LGS Unit 2 technical specification (TS) 3.8.1.1 was identified when Exelon failed to correct a degraded lube oil pipe nipple fitting on the D22 EDG when maintenance was performed to address leakage which caused inoperability of the EDG for greater than its TS allowed outage time.


=====Description:=====
=====Description:=====
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Corrective Action(s): Exelon replaced the fitting and restored operability of the EDG on October 15, 2017, revised equipment data to require replacement of a pipe nipple fitting instead of reusing if a future leak is identified, and initiated actions to replace similar fittings for extent of condition.
Corrective Action(s): Exelon replaced the fitting and restored operability of the EDG on October 15, 2017, revised equipment data to require replacement of a pipe nipple fitting instead of reusing if a future leak is identified, and initiated actions to replace similar fittings for extent of condition.


Corrective Action Reference(s): Issue Report (IR) 4070641
Corrective Action Reference(s): Issue Report (IR) 4070641  


=====Performance Assessment:=====
=====Performance Assessment:=====
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The lube oil consumption rate was less than 0.05 gpm. The leak rate was consistent at about 0.03125 gpm. Therefore, at a minimum the lube oil storage tank contained sufficient oil to make up to the D22 EDG oil reservoir for over 40 hours of EDG operation.
The lube oil consumption rate was less than 0.05 gpm. The leak rate was consistent at about 0.03125 gpm. Therefore, at a minimum the lube oil storage tank contained sufficient oil to make up to the D22 EDG oil reservoir for over 40 hours of EDG operation.


Cross-Cutting Aspect: The inspectors determined that this finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Identification, because Exelon personnel did not recognize deviations from standards, training, and skill of the craft when addressing leakage. [P.1]
Cross-Cutting Aspect: The inspectors determined that this finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Identification, because Exelon personnel did not recognize deviations from standards, training, and skill of the craft when addressing leakage. [P.1]  


=====Enforcement:=====
=====Enforcement:=====
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Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy.
Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy.


Emergency Diesel Generator Combustion Air Overheating Cornerstone           Significance                               Cross-cutting       Report Aspect              Section Mitigating System     Green                                     [P.3] -              71153 NCV                                       Resolution 05000352/2018001-02 Opened/Closed A self-revealed Green NCV of LGS Unit 1 TS 6.8.1 and TS 3.8.1.1 was identified when Exelon failed to properly maintain an operating procedure to maintain a fail-safe design feature for the EDGs which led to the D12 EDG combustion air overheating and caused the EDG to be inoperable for greater than its TS allowed outage time.
Emergency Diesel Generator Combustion Air Overheating Cornerstone Significance Cross-cutting Aspect Report Section Mitigating System Green NCV 05000352/2018001-02 Opened/Closed  
[P.3] -
Resolution 71153 A self-revealed Green NCV of LGS Unit 1 TS 6.8.1 and TS 3.8.1.1 was identified when Exelon failed to properly maintain an operating procedure to maintain a fail-safe design feature for the EDGs which led to the D12 EDG combustion air overheating and caused the EDG to be inoperable for greater than its TS allowed outage time.


=====Description:=====
=====Description:=====
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Corrective Action(s): Exelon recalibrated and reinstalled the TIC, revised the operating procedure to ensure EDG functionality is maintained, and replaced the degraded PCV.
Corrective Action(s): Exelon recalibrated and reinstalled the TIC, revised the operating procedure to ensure EDG functionality is maintained, and replaced the degraded PCV.


Corrective Action Reference(s): IR 4081882
Corrective Action Reference(s): IR 4081882  


=====Performance Assessment:=====
=====Performance Assessment:=====
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The dominant core damage sequence involved a weather related loss of offsite power, with failure of the D12 EDG, common cause failure of the remaining Unit 1 EDGs, failure to cross-tie a Unit 2 EDG to a Unit 1 safety bus, failure to depressurize given the eventual loss of direct current (DC) power, and failure to recover either offsite power or an EDG within 5 hours. In accordance with IMC 0609 guidance a review of the external event risk or large early release frequency was not performed given the increase in internal event CDF was below the 1E-7/yr threshold and would not be expected to change the risk estimation.
The dominant core damage sequence involved a weather related loss of offsite power, with failure of the D12 EDG, common cause failure of the remaining Unit 1 EDGs, failure to cross-tie a Unit 2 EDG to a Unit 1 safety bus, failure to depressurize given the eventual loss of direct current (DC) power, and failure to recover either offsite power or an EDG within 5 hours. In accordance with IMC 0609 guidance a review of the external event risk or large early release frequency was not performed given the increase in internal event CDF was below the 1E-7/yr threshold and would not be expected to change the risk estimation.


Cross-Cutting Aspect: The inspectors determined that this finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Resolution, because Exelon did not take effective corrective action when the intermittent low temperature condition caused by the degraded PCV was identified. Specifically, Exelon did not take appropriate interim corrective action to address the operating procedures TIC adjustments in order to mitigate the issue while more fundamental causes were being addressed. [P.3]
Cross-Cutting Aspect: The inspectors determined that this finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Resolution, because Exelon did not take effective corrective action when the intermittent low temperature condition caused by the degraded PCV was identified. Specifically, Exelon did not take appropriate interim corrective action to address the operating procedures TIC adjustments in order to mitigate the issue while more fundamental causes were being addressed. [P.3]  


=====Enforcement:=====
=====Enforcement:=====
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On April 12, 2018, the inspectors presented the quarterly resident inspector inspection results to Rick Libra, Site Vice-President, and other members of the Exelon staff.
On April 12, 2018, the inspectors presented the quarterly resident inspector inspection results to Rick Libra, Site Vice-President, and other members of the Exelon staff.


THIRD PARTY REVIEWS Inspectors reviewed Institute on Nuclear Power Reactor reports that were issued during the inspection period.
THIRD PARTY REVIEWS  
 
Inspectors reviewed Institute on Nuclear Power Reactor reports that were issued during the inspection period.


=DOCUMENTS REVIEWED=
=DOCUMENTS REVIEWED=
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F-R-309, Unit 1, Safeguard Isolation Valve Area Room 309 (El 217), Revision 11
F-R-309, Unit 1, Safeguard Isolation Valve Area Room 309 (El 217), Revision 11
Condition Reports
Condition Reports
20254       4120452
20254
20452
71111.11Q
71111.11Q
Procedures
Procedures
Line 345: Line 401:
71111.12Q
71111.12Q
Condition Reports
Condition Reports
2632557       2655420       2663432       3986074     3988302       3991456
2632557
4003680       4011371       4076445       4106926
2655420
2663432
3986074
3988302
3991456
4003680
4011371
4076445
4106926  
 
Miscellaneous
Miscellaneous
Engage System Health Reports
Engage System Health Reports
Line 355: Line 420:
WC-AA-101-1006, On-Line Risk Management and Assessment, Revision 2
WC-AA-101-1006, On-Line Risk Management and Assessment, Revision 2
Condition Reports
Condition Reports
4102016       4102082
4102016
4102082
Miscellaneous
Miscellaneous
E2 Work Schedule for Week of 2/25/18
E2 Work Schedule for Week of 2/25/18
Line 367: Line 433:
ON-115, Loss of Control Enclosure Cooling, Revision 25
ON-115, Loss of Control Enclosure Cooling, Revision 25
Condition Reports
Condition Reports
4082004       4088765     4089921       4099141     4099223     4100277
4082004
4100294       4100598     4117844
4088765
4089921
4099141
4099223
4100277
4100294
4100598
4117844
Work Order
Work Order
4308130
4308130
Line 380: Line 453:
ST-6-076-310-2, SGTS Reactor Enclosure Secondary Containment Integrity Test, Revision 21
ST-6-076-310-2, SGTS Reactor Enclosure Secondary Containment Integrity Test, Revision 21
Condition Reports
Condition Reports
4085733       4105709     4121117
4085733
4105709
21117
Work Orders
Work Orders
4703263       4727391      4733863       4738484     4750273
4703263
27391
4733863
4738484
4750273  
 
Miscellaneous
Miscellaneous
EC 622647, Inflatable Seal - Secondary Containment, Revision 2
EC 622647, Inflatable Seal - Secondary Containment, Revision 2
Line 394: Line 474:
ST-6-092-312-1, D12 Diesel Generator Slow Start Operability Test Run, Revision 103
ST-6-092-312-1, D12 Diesel Generator Slow Start Operability Test Run, Revision 103
Condition Reports
Condition Reports
0379493       0381794       4081625     4094240       4103817       4104251
0379493
0381794
4081625
4094240
4103817
4104251
Work Orders
Work Orders
1382270       4243506        4255083      4595702       4699475
1382270
243506
255083
4595702
4699475
Miscellaneous
Miscellaneous
CGIFU01, EPRI CGI Joint Utility Task Group Commercial Grade Item Evaluation for UL 198E
CGIFU01, EPRI CGI Joint Utility Task Group Commercial Grade Item Evaluation for UL 198E
Line 418: Line 507:
Procedures
Procedures
ST-4-LLR-031-1, Main Steam Line A, Revision 13
ST-4-LLR-031-1, Main Steam Line A, Revision 13
ST-4-LLR-041-1, Main Steam Line B, Revision 12
ST-4-LLR-041-1, Main Steam Line B, Revision 12  
 
Work Orders
Work Orders
4309668         4310968
4309668
4310968
71124.08
71124.08
Procedures
Procedures
Line 432: Line 523:
Containerized Waste Facility, Revision 13
Containerized Waste Facility, Revision 13
RP-AA-600-1005, Radioactive Material and Non Disposal Site Waste Shipments, Rev 19
RP-AA-600-1005, Radioactive Material and Non Disposal Site Waste Shipments, Rev 19
RP-AA-600-1006, Shipment of Category 1 Quantities of Radioactive Material or Waste
RP-AA-600-1006, Shipment of Category 1 Quantities of Radioactive Material or Waste  
        (Category 1 RAMQC), Revision 11
(Category 1 RAMQC), Revision 11
RP-AA-600-1007, Radioactive Waste Shipments to Energy Solutions Clive Utah Disposal
RP-AA-600-1007, Radioactive Waste Shipments to Energy Solutions Clive Utah Disposal
Facility Bulk Waste Facility (BWF), Revision 8
Facility Bulk Waste Facility (BWF), Revision 8
RP-AA-600-1008, Radioactive Waste Shipments to Waste Control Specialists (WCS) Disposal
RP-AA-600-1008, Radioactive Waste Shipments to Waste Control Specialists (WCS) Disposal
Facility, Revision 5
Facility, Revision 5
RP-AA-600-1009, Shipment of Category 2 Quantities of Radioactive Material or Waste
RP-AA-600-1009, Shipment of Category 2 Quantities of Radioactive Material or Waste  
        (Category 2 RAMQC), Revision 2
(Category 2 RAMQC), Revision 2
RP-AA-600-1010, Use and Operation of WMG Software for Creating Containers, Samples,
RP-AA-600-1010, Use and Operation of WMG Software for Creating Containers, Samples,
Waste Streams and Waste Types, Revision 2
Waste Streams and Waste Types, Revision 2
Line 465: Line 556:
EnergySolutions Internal Audit CORP-16-004, Clive Facility
EnergySolutions Internal Audit CORP-16-004, Clive Facility
NUPIC 24365, EnergySolutions
NUPIC 24365, EnergySolutions
NUPIC 24515, Waste Control Specialists, LLC
NUPIC 24515, Waste Control Specialists, LLC  
 
CFR Part 61 Scaling Factors
CFR Part 61 Scaling Factors
Waste Sludge Tank; Deep Bed; Dry Active Waste; Fuel Floor; Reactor Water Clean-Up
Waste Sludge Tank; Deep Bed; Dry Active Waste; Fuel Floor; Reactor Water Clean-Up
Line 508: Line 600:
ST-6-092-316-1, D12 Diesel Generator Fast Start Operability Test Run, Revision 54
ST-6-092-316-1, D12 Diesel Generator Fast Start Operability Test Run, Revision 54
ST-6-092-362-2, D22 Diesel Generator Operability Verification, Revision 40
ST-6-092-362-2, D22 Diesel Generator Operability Verification, Revision 40
ST-6-092-362-2, D22 Diesel Generator Operability Verification, Revision 40
ST-6-092-362-2, D22 Diesel Generator Operability Verification, Revision 40  
 
Condition Reports
Condition Reports
1108417       1422131      2924515        4021268      4049989       4062096
1108417
4069001       4070641       4073004       4081882       4082219
22131
24515
21268
4049989
4062096
4069001
4070641
4073004
4081882
4082219
Work Orders
Work Orders
2075815       2079589       4292476        4318057       4642785       4650838
2075815
4650858       4652385       4652410       4652412       4663824       4672813
2079589
4686262       4697246
292476
4318057
4642785
4650838
4650858
4652385
4652410
4652412
4663824
4672813
4686262
4697246
Miscellaneous
Miscellaneous
ANSI/ASME B1.20.1, Pipe Threads, General Purpose (Inch), 1983
ANSI/ASME B1.20.1, Pipe Threads, General Purpose (Inch), 1983
Line 521: Line 634:
L-S-07, Diesel Generator and Auxiliary Systems, Revision 15
L-S-07, Diesel Generator and Auxiliary Systems, Revision 15
L-S-07, Diesel Generator and Auxiliary Systems, Revision 15
L-S-07, Diesel Generator and Auxiliary Systems, Revision 15
PES-S-006, Code Reconciliation, Revision 6
PES-S-006, Code Reconciliation, Revision 6  
 
UNITED STATES
UNITED STATES
NUCLEAR REGULATORY COMMISSION
NUCLEAR REGULATORY COMMISSION
REGION I
REGION I
2100 RENAISSANCE BOULEVARD, SUITE 100
2100 RENAISSANCE BOULEVARD, SUITE 100
KING OF PRUSSIA, PA 19406-2713
KING OF PRUSSIA, PA 19406-2713  
 
May 11, 2018
May 11, 2018
Mr. Bryan C. Hanson
Mr. Bryan C. Hanson
Line 533: Line 648:
4300 Winfield Road
4300 Winfield Road
Warrenville, IL 60555
Warrenville, IL 60555
SUBJECT:         LIMERICK GENERATING STATION - INTEGRATED INSPECTION REPORT
SUBJECT:
LIMERICK GENERATING STATION - INTEGRATED INSPECTION REPORT
05000352/2018001 AND 05000353/2018001
05000352/2018001 AND 05000353/2018001
Dear Mr. Hanson:
Dear Mr. Hanson:
Line 553: Line 669:
: [[contact::U. S. Nuclear Regulatory Commission]], ATTN: Document Control
: [[contact::U. S. Nuclear Regulatory Commission]], ATTN: Document Control
Desk, Washington, DC, 20555-0001; with copies to the Regional Administrator, Region I, and
Desk, Washington, DC, 20555-0001; with copies to the Regional Administrator, Region I, and
the NRC Resident Inspector at LG
the NRC Resident Inspector at LGS.
: [[contact::S.
This letter, its enclosure, and your response (if any) will be made available for public inspection
This letter]], its enclosure, and your response (if any) will be made available for public inspection
and copying at http://www.nrc.gov/reading-rm/adams.html and the NRCs Public Document
and copying at http://www.nrc.gov/reading-rm/adams.html and the NRCs Public Document
Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390,
Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390,
Public Inspections, Exemptions, Requests for Withholding.
Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
Sincerely,  
                                                /RA/
 
/RA/  
 
James  
James  
: [[contact::A. Krafty]], Acting Chief
: [[contact::A. Krafty]], Acting Chief
Reactor Projects Branch 4
Reactor Projects Branch 4
Division of Reactor Projects
Division of Reactor Projects
B. Hanson                         2
B. Hanson  
 
Docket Numbers: 50-352 and 50-353
Docket Numbers: 50-352 and 50-353
License Numbers: NPF-39 and NPF-85
License Numbers: NPF-39 and NPF-85
Line 572: Line 690:
and 05000353/2018001
and 05000353/2018001
cc w/encl:
cc w/encl:
Distribution via ListServ
Distribution via ListServ  
 
ML18131A015
ML18131A015
SUNSI Review                 Non-Sensitive                   Publicly Available
SUNSI Review  
Sensitive                        Non-Publicly Available
 
OFFICE         RI/DRP               RI/DRP             RI/DRP
Non-Sensitive
NAME           S. Rutenkroger       S. Barber/jk for   J. Krafty
Sensitive
DATE           05/10/18             5/10/18           5/11/18
 
Publicly Available
Non-Publicly Available
OFFICE
RI/DRP
RI/DRP
RI/DRP  
 
NAME
S. Rutenkroger
S. Barber/jk for
J. Krafty  
 
DATE
05/10/18
5/10/18
5/11/18  


U.S. NUCLEAR REGULATORY COMMISSION
U.S. NUCLEAR REGULATORY COMMISSION
Inspection Report
Inspection Report  
Docket Numbers:             50-352 and 50-353
 
License Numbers:           NPF-39 and NPF-85
Docket Numbers:
Report Numbers:             05000352/2018001 and 05000353/2018001
50-352 and 50-353  
Enterprise Identifier:     I-2018-001-0071
 
Licensee:                   Exelon Generation Company, LLC
License Numbers:
Facility:                   Limerick Generating Station, Units 1 & 2
NPF-39 and NPF-85  
Location:                   Sanatoga, PA 19464
 
Inspection Dates:           January 1, 2018 through March 31, 2018
Report Numbers:
Inspectors:                
05000352/2018001 and 05000353/2018001  
: [[contact::S. Rutenkroger]], PhD, Senior Resident Inspector
 
: [[contact::M. Fannon]], Resident Inspector
Enterprise Identifier:
: [[contact::H. Anagnostopoulos]], Senior Health Physicist
I-2018-001-0071  
: [[contact::J. Furia]], Senior Health Physicist
 
Approved By:              
Licensee:
: [[contact::J. Krafty]], Acting Chief
Exelon Generation Company, LLC  
Reactor Projects Branch 4
 
Division of Reactor Projects
Facility:
Limerick Generating Station, Units 1 & 2  
 
Location:
Sanatoga, PA 19464  
 
Inspection Dates:
January 1, 2018 through March 31, 2018  
 
Inspectors:  
: [[contact::S. Rutenkroger]], PhD, Senior Resident Inspector  
: [[contact::M. Fannon]], Resident Inspector  
: [[contact::H. Anagnostopoulos]], Senior Health Physicist  
: [[contact::J. Furia]], Senior Health Physicist  
 
Approved By:  
: [[contact::J. Krafty]], Acting Chief  
 
Reactor Projects Branch 4  
 
Division of Reactor Projects  


SUMMARY
SUMMARY
Line 610: Line 765:
List of Findings and Violations
List of Findings and Violations
Failure of Emergency Diesel Generator Lube Oil Pipe Nipple Fitting
Failure of Emergency Diesel Generator Lube Oil Pipe Nipple Fitting
Cornerstone           Significance                               Cross-cutting     Report
Cornerstone
Aspect            Section
Significance
Mitigating           Green NCV                                   [P.1] -            71153
Cross-cutting
Systems              05000353/2018001-01                         Identification
Aspect
Opened/Closed
Report
Section
Mitigating
Systems
Green NCV
05000353/2018001-01
Opened/Closed  
[P.1] -
Identification
71153
A self-revealed Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI,
A self-revealed Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI,
Corrective Action, and LGS Unit 2 technical specification (TS) 3.8.1.1 was identified when
Corrective Action, and LGS Unit 2 technical specification (TS) 3.8.1.1 was identified when
Line 621: Line 785:
inoperability of the EDG for greater than its TS allowed outage time.
inoperability of the EDG for greater than its TS allowed outage time.
Emergency Diesel Generator Combustion Air Overheating
Emergency Diesel Generator Combustion Air Overheating
Cornerstone           Significance                               Cross-cutting     Report
Cornerstone
Aspect            Section
Significance
Mitigating           Green NCV                                   [P.3] -            71153
Cross-cutting
Systems              05000352/2018001-02                         Resolution
Aspect
Opened/Closed
Report
Section
Mitigating
Systems
Green NCV
05000352/2018001-02
Opened/Closed  
[P.3] -
Resolution
71153
A self-revealed Green NCV of LGS Unit 1 TS 6.8.1 and TS 3.8.1.1 was identified when Exelon
A self-revealed Green NCV of LGS Unit 1 TS 6.8.1 and TS 3.8.1.1 was identified when Exelon
failed to properly maintain an operating procedure to maintain a fail-safe design feature for the
failed to properly maintain an operating procedure to maintain a fail-safe design feature for the
Line 631: Line 804:
inoperable for greater than its TS allowed outage time.
inoperable for greater than its TS allowed outage time.
Additional Tracking Items
Additional Tracking Items
Type     Issue number               Title                           Report       Status
Type
Issue number
Title
Report
Section
Section
LER       05000353/2017-008-00       EDG Inoperable for Greater      71153        Closed
Status
05000353/2017-008-01       Than 30 Days Resulting in a
LER
05000353/2017-008-00
05000353/2017-008-01
EDG Inoperable for Greater
Than 30 Days Resulting in a
Condition Prohibited by
Condition Prohibited by
Technical Specifications
Technical Specifications
LER       05000352/2018-001-00       D12 EDG Inoperable for           71153        Closed
71153
Closed
LER
05000352/2018-001-00
D12 EDG Inoperable for
Greater than 30 Days
Greater than 30 Days
Resulting in a Condition
Resulting in a Condition
Prohibited by TS
Prohibited by TS
71153
Closed
PLANT STATUS
PLANT STATUS
Unit 1 began the inspection period at rated thermal power. On March 25 to 26, 2018, the unit
Unit 1 began the inspection period at rated thermal power. On March 25 to 26, 2018, the unit
Line 663: Line 850:
REACTOR SAFETY
REACTOR SAFETY
71111.01 - Adverse Weather Protection
71111.01 - Adverse Weather Protection
Impending Severe Weather (2 samples)
Impending Severe Weather (2 samples)  
    (1) The inspectors evaluated readiness for impending adverse weather conditions for the
(1) The inspectors evaluated readiness for impending adverse weather conditions for the
onset of winter weather, including high winds, on January 5, 2018.
onset of winter weather, including high winds, on January 5, 2018.  
    (2) The inspectors evaluated readiness for impending adverse weather conditions for the
(2) The inspectors evaluated readiness for impending adverse weather conditions for the
onset of winter weather, including high winds, on March 2, 2018.
onset of winter weather, including high winds, on March 2, 2018.
71111.04 - Equipment Alignment
71111.04 - Equipment Alignment
Partial Walkdown (5 samples)
Partial Walkdown (5 samples)
The inspectors evaluated system configurations during partial walkdowns of the following
The inspectors evaluated system configurations during partial walkdowns of the following
systems/trains:
systems/trains:  
    (1) Unit 2 high pressure coolant injection on January 16 and 17, 2018
(1) Unit 2 high pressure coolant injection on January 16 and 17, 2018  
    (2) Unit 1 D11 and D13 emergency diesel generators (EDGs) on February 5, 2018
(2) Unit 1 D11 and D13 emergency diesel generators (EDGs) on February 5, 2018  
    (3) Unit 2 2A batteries and chargers during 2BD101 battery planned maintenance on
(3) Unit 2 2A batteries and chargers during 2BD101 battery planned maintenance on
February 5 through 9, 2018
February 5 through 9, 2018  
    (4) Unit 1 B residual heat removal subsystem in shutdown cooling during the A emergency
(4) Unit 1 B residual heat removal subsystem in shutdown cooling during the A emergency
core cooling subsystem maintenance window on March 27, 2018
core cooling subsystem maintenance window on March 27, 2018  
    (5) Unit 1 D12 EDG during the division 1 and 3 direct current bus maintenance window on
(5) Unit 1 D12 EDG during the division 1 and 3 direct current bus maintenance window on
March 28, 2018
March 28, 2018  
 
71111.05 - Fire Protection
71111.05 - Fire Protection
Quarterly Inspection (5 samples)
Quarterly Inspection (5 samples)
The inspectors evaluated fire protection program implementation in the following selected
The inspectors evaluated fire protection program implementation in the following selected
areas:
areas:  
  (1) Fire area 2, Unit common 13.2kV switchgear room, elevation 217, on January 8, 2018
(1) Fire area 2, Unit common 13.2kV switchgear room, elevation 217, on January 8, 2018  
  (2) Fire area 8, Unit 1 class 1E battery room, elevation 239, on January 23, 2018
(2) Fire area 8, Unit 1 class 1E battery room, elevation 239, on January 23, 2018  
  (3) Fire area 10, Unit 2 class 1E battery rooms, elevation 239, on February 5, 2018
(3) Fire area 10, Unit 2 class 1E battery rooms, elevation 239, on February 5, 2018  
  (4) Fire area 28, Unit common standby gas treatment area rooms, elevation 332, on
(4) Fire area 28, Unit common standby gas treatment area rooms, elevation 332, on
February 27, 201
February 27, 201  
  (5) Fire area 43, Unit 1 safeguard isolation valve area room 309, elevation 217, on
(5) Fire area 43, Unit 1 safeguard isolation valve area room 309, elevation 217, on
March 28, 2018
March 28, 2018
71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance
71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance
Line 701: Line 889:
Routine Maintenance Effectiveness (2 samples)
Routine Maintenance Effectiveness (2 samples)
The inspectors evaluated the effectiveness of routine maintenance activities associated
The inspectors evaluated the effectiveness of routine maintenance activities associated
with the following equipment and/or safety significant functions:
with the following equipment and/or safety significant functions:  
  (1) Unit 1 reactor manual control system
(1) Unit 1 reactor manual control system  
  (2) Unit 2 reactor manual control system
(2) Unit 2 reactor manual control system
71111.13 - Maintenance Risk Assessments and Emergent Work Control (6 samples)
71111.13 - Maintenance Risk Assessments and Emergent Work Control (6 samples)
The inspectors evaluated the risk assessments for the following planned and emergent
The inspectors evaluated the risk assessments for the following planned and emergent
work activities:
work activities:  
  (1) Unit 2 reactor core isolation cooling relay replacements on January 16 and 17, 2018
(1) Unit 2 reactor core isolation cooling relay replacements on January 16 and 17, 2018  
  (2) Unit common B control room emergency fresh air system testing on February 7, 2018
(2) Unit common B control room emergency fresh air system testing on February 7, 2018  
  (3) Unit 2 A residual heat removal maintenance on February 26 and 27, 2018
(3) Unit 2 A residual heat removal maintenance on February 26 and 27, 2018  
  (4) Unit common A standby gas treatment system maintenance on February 27, 2018
(4) Unit common A standby gas treatment system maintenance on February 27, 2018  
  (5) Unit common A emergency service water, A standby gas treatment system, and
(5) Unit common A emergency service water, A standby gas treatment system, and
Unit 2 A reactor enclosure recirculation system maintenance on March 1, 2018
Unit 2 A reactor enclosure recirculation system maintenance on March 1, 2018  
  (6) Unit 1 A emergency core cooling system maintenance during reduced core inventory
(6) Unit 1 A emergency core cooling system maintenance during reduced core inventory
in the refueling outage on March 27 and 28, 2018
in the refueling outage on March 27 and 28, 2018  
 
71111.15 - Operability Determinations and Functionality Assessments (6 samples)
71111.15 - Operability Determinations and Functionality Assessments (6 samples)
The inspectors evaluated the following operability determinations and functionality
The inspectors evaluated the following operability determinations and functionality
assessments:
assessments:  
  (1) Unit 2, D21 EDG room low temperature alarm on December 31, 2017
(1) Unit 2, D21 EDG room low temperature alarm on December 31, 2017  
  (2) Unit 2 high pressure coolant injection condensate pump discharge check valve failure on
(2) Unit 2 high pressure coolant injection condensate pump discharge check valve failure on
January 25, 2018
January 25, 2018  
  (3) Unit 2 high pressure coolant injection vacuum breaker check valve oversized disc on
(3) Unit 2 high pressure coolant injection vacuum breaker check valve oversized disc on
January 31, 2018
January 31, 2018  
  (4) Unit common A emergency service water pump motor step voltage test leakage current
(4) Unit common A emergency service water pump motor step voltage test leakage current
on January 31, 2018
on January 31, 2018  
  (5) Unit 2 D21 EDG multiple battery ground alarms while raising speed during the slow
(5) Unit 2 D21 EDG multiple battery ground alarms while raising speed during the slow
start surveillance test on February 2, 2018
start surveillance test on February 2, 2018  
  (6) Unit common, B control room air supply controller not properly maintaining room
(6) Unit common, B control room air supply controller not properly maintaining room
temperature on February 4, 2018
temperature on February 4, 2018
71111.18 - Plant Modifications (2 samples)
71111.18 - Plant Modifications (2 samples)
The inspectors evaluated the following temporary or permanent modifications:
The inspectors evaluated the following temporary or permanent modifications:  
  (1) Engineering change package 622647 - Inflatable Seal - Secondary Containment
(1) Engineering change package 622647 - Inflatable Seal - Secondary Containment  
  (2) Engineering change request 433952, D23 Repair of the Blower Inspection Cover Bolt
(2) Engineering change request 433952, D23 Repair of the Blower Inspection Cover Bolt
Holes Using Stainless Steel Heli-Coil Thread Inserts
Holes Using Stainless Steel Heli-Coil Thread Inserts
71111.19 - Post Maintenance Testing (6 samples)
71111.19 - Post Maintenance Testing (6 samples)
The inspectors evaluated post maintenance testing for the following maintenance/repair
The inspectors evaluated post maintenance testing for the following maintenance/repair
activities:
activities:  
  (1) Unit 2 D24 EDG fuse replacement following an intermittent issue in the automatic start
(1) Unit 2 D24 EDG fuse replacement following an intermittent issue in the automatic start
logic circuit on December 6, 2017
logic circuit on December 6, 2017  
  (2) Unit 2 reactor core isolation cooling relay replacements on January 16 and 17, 2018
(2) Unit 2 reactor core isolation cooling relay replacements on January 16 and 17, 2018  
  (3) Unit 1 D12 EDG air cooler temperature indicator controller pressure control valve (PCV)
(3) Unit 1 D12 EDG air cooler temperature indicator controller pressure control valve (PCV)
replacement on February 5, 2018
replacement on February 5, 2018  
  (4) Unit 2 B2 battery cell replacements on February 5 and 6, 2018
(4) Unit 2 B2 battery cell replacements on February 5 and 6, 2018  
  (5) Unit 2 B2 battery charger current adjustment on February 15, 2018
(5) Unit 2 B2 battery charger current adjustment on February 15, 2018  
  (6) Unit 2 D24 EDG heating, ventilation, and cooling fan controller replacement on
(6) Unit 2 D24 EDG heating, ventilation, and cooling fan controller replacement on
February 22, 2018
February 22, 2018
71111.20 - Refueling and Other Outage Activities
71111.20 - Refueling and Other Outage Activities
The inspectors evaluated the Unit 1 refueling outage 1R17 from March 26, 2018, through
The inspectors evaluated the Unit 1 refueling outage 1R17 from March 26, 2018, through
the end of the inspection period. The following portions of the inspection procedure were
the end of the inspection period. The following portions of the inspection procedure were
not performed during this period.
not performed during this period.  
  (1) Fatigue Management
(1) Fatigue Management  
  (2) Startup
(2) Startup  
 
71111.22 - Surveillance Testing
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
The inspectors evaluated the following surveillance tests:
Routine (3 samples)
Routine (3 samples)  
  (1) ST-6-092-113-2, D23 EDG 24 hour endurance run on January 18 and 19, 2018
(1) ST-6-092-113-2, D23 EDG 24 hour endurance run on January 18 and 19, 2018  
  (2) RT-6-051-320-1, Unit 1 B residual heat removal remote operation test on
(2) RT-6-051-320-1, Unit 1 B residual heat removal remote operation test on
February 7, 2018
February 7, 2018  
  (3) ST-2-074-642-1, Unit 1 source range and intermediate range neutron monitors pre-
(3) ST-2-074-642-1, Unit 1 source range and intermediate range neutron monitors pre-
shutdown testing on March 18, 2018
shutdown testing on March 18, 2018
In-service (2 samples)
In-service (2 samples)  
  (1) ST-6-052-231-1, Unit 1 A core spray pump, valve, and flow test on January 4, 2018
(1) ST-6-052-231-1, Unit 1 A core spray pump, valve, and flow test on January 4, 2018  
  (2) ST-6-052-232-1, Unit 1 B core spray pump, valve, and flow test on March 10, 2018
(2) ST-6-052-232-1, Unit 1 B core spray pump, valve, and flow test on March 10, 2018
Containment Isolation Valve (2 samples)
Containment Isolation Valve (2 samples)  
  (1) ST-4-LLR-031-1, Unit 1 main steam line A inboard and outboard isolation valves
(1) ST-4-LLR-031-1, Unit 1 main steam line A inboard and outboard isolation valves
leakage rate testing on March 29, 2018
leakage rate testing on March 29, 2018  
  (2) ST-4-LLR-041-1, Unit 1 main steam line B inboard and outboard isolation valves
(2) ST-4-LLR-041-1, Unit 1 main steam line B inboard and outboard isolation valves
leakage rate testing on March 29, 2018
leakage rate testing on March 29, 2018
RADIATION SAFETY
RADIATION SAFETY
Line 772: Line 962:
Radiological Work Planning (1 sample)
Radiological Work Planning (1 sample)
The inspectors evaluated Exelons radiological work planning by reviewing the following
The inspectors evaluated Exelons radiological work planning by reviewing the following
activities:
activities:  
  (1) ALARA Plan 2017-101
(1) ALARA Plan 2017-101  
  (2) ALARA Plan 2017-050
(2) ALARA Plan 2017-050  
  (3) ALARA Plan 2017-052
(3) ALARA Plan 2017-052
Verification of Dose Estimates and Exposure Tracking Systems (1 sample)
Verification of Dose Estimates and Exposure Tracking Systems (1 sample)
The inspectors evaluated dose estimates and exposure tracking.
The inspectors evaluated dose estimates and exposure tracking.
Line 783: Line 973:
The inspectors observed radioactive waste container storage areas and verified the postings
The inspectors observed radioactive waste container storage areas and verified the postings
and controls and that Exelon had established a process for monitoring the impact of long-
and controls and that Exelon had established a process for monitoring the impact of long-
term storage of the waste.
term storage of the waste.  
 
Radioactive Waste System Walkdown (1 sample)
Radioactive Waste System Walkdown (1 sample)
The inspectors walked down the following:
The inspectors walked down the following:  
 
Accessible portions of liquid and solid radioactive waste processing systems to verify
Accessible portions of liquid and solid radioactive waste processing systems to verify
current system alignment and material condition
current system alignment and material condition
Line 807: Line 999:
71151 - Performance Indicator Verification (6 samples)
71151 - Performance Indicator Verification (6 samples)
The inspectors verified Exelons performance indicator submittals listed below for the
The inspectors verified Exelons performance indicator submittals listed below for the
period January 1, 2017 through December 31, 2017.
period January 1, 2017 through December 31, 2017.  
  (1) Unit 1 and Unit 2 Unplanned Power Changes per 7000 Critical Hours
(1) Unit 1 and Unit 2 Unplanned Power Changes per 7000 Critical Hours  
  (2) Unit 1 and Unit 2 High Pressure Injection Systems
(2) Unit 1 and Unit 2 High Pressure Injection Systems  
  (3) Unit 1 and Unit 2 Heat Removal Systems
(3) Unit 1 and Unit 2 Heat Removal Systems
71153 - Follow-up of Events and Notices of Enforcement Discretion
71153 - Follow-up of Events and Notices of Enforcement Discretion
Licensee Event Reports (LER) (2 samples)
Licensee Event Reports (LER) (2 samples)
The inspectors evaluated the following licensee event reports which can be accessed at
The inspectors evaluated the following licensee event reports which can be accessed at
https://lersearch.inl.gov/LERSearchCriteria.aspx:
https://lersearch.inl.gov/LERSearchCriteria.aspx:  
  (1) LER 05000353/2017-008-00 and 05000353/2017-008-01, EDG Inoperable for Greater
(1) LER 05000353/2017-008-00 and 05000353/2017-008-01, EDG Inoperable for Greater
Than 30 Days Resulting in a Condition Prohibited by Technical Specifications, on
Than 30 Days Resulting in a Condition Prohibited by Technical Specifications, on
December 11, 2017, and February 22, 2018. The review for this event is documented in
December 11, 2017, and February 22, 2018. The review for this event is documented in
the inspection results section.
the inspection results section.  
  (2) LER 05000352/2018-001-00, D12 EDG Inoperable for Greater than 30 Days Resulting in
(2) LER 05000352/2018-001-00, D12 EDG Inoperable for Greater than 30 Days Resulting in  
 
a Condition Prohibited by TS, on February 5, 2018. The review for this event is
a Condition Prohibited by TS, on February 5, 2018. The review for this event is
documented in the inspection results section.
documented in the inspection results section.
INSPECTION RESULTS
INSPECTION RESULTS
Failure of Emergency Diesel Generator Lube Oil Pipe Nipple Fitting
Failure of Emergency Diesel Generator Lube Oil Pipe Nipple Fitting
Cornerstone             Significance                             Cross-cutting       Report
Cornerstone
Aspect              Section
Significance
Mitigating               Green                                     [P.1] -            71153
Cross-cutting
Systems                  NCV                                       Identification
Aspect
Report
Section
Mitigating
Systems
Green
NCV
05000353/2018001-01
05000353/2018001-01
Opened/Closed
Opened/Closed  
[P.1] -
Identification
71153
A self-revealed Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI,
A self-revealed Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI,
Corrective Action, and LGS Unit 2 technical specification (TS) 3.8.1.1 was identified when
Corrective Action, and LGS Unit 2 technical specification (TS) 3.8.1.1 was identified when
Line 867: Line 1,069:
fittings condition indicated additional tightening of at least two additional threads beyond
fittings condition indicated additional tightening of at least two additional threads beyond
original installation which is outside the tolerances of ASME B1.20.1, Pipe Threads, General
original installation which is outside the tolerances of ASME B1.20.1, Pipe Threads, General
Purpose (Inch). Based on these conditions, the inspectors determined that Exelon had a
Purpose (Inch). Based on these conditions, the inspectors determined that Exelon had a  
 
reasonable opportunity to foresee and correct the degraded fitting as required by Exelon
reasonable opportunity to foresee and correct the degraded fitting as required by Exelon
procedure PI-AA-125, Corrective Action Program (CAP) Procedure, when the second repair
procedure PI-AA-125, Corrective Action Program (CAP) Procedure, when the second repair
Line 896: Line 1,099:
to be inoperable from September 7 to October 15, 2017.
to be inoperable from September 7 to October 15, 2017.
Significance: The inspectors assessed the significance of the finding using IMC 0609,
Significance: The inspectors assessed the significance of the finding using IMC 0609,
Appendix A, Exhibit 2, and determined that this finding was of very low safety significance
Appendix A, Exhibit 2, and determined that this finding was of very low safety significance  
(Green). Specifically, the inspectors, in consultation with a Region I senior reactor analyst
(Green). Specifically, the inspectors, in consultation with a Region I senior reactor analyst  
(SRA), determined that the condition did not represent an actual loss of the D22 EDG
(SRA), determined that the condition did not represent an actual loss of the D22 EDG
probabilistic risk assessment safety function, i.e. the capability to provide power for up to 24
probabilistic risk assessment safety function, i.e. the capability to provide power for up to 24
Line 911: Line 1,114:
Violation: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that
Violation: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that
measures shall be established to assure that conditions adverse to quality, such as
measures shall be established to assure that conditions adverse to quality, such as
deficiencies, defective material, and non-conformances are promptly identified and corrected.
deficiencies, defective material, and non-conformances are promptly identified and corrected.  
 
LGS Unit 2 TS 3.8.1.1 requires that an inoperable diesel generator be restored to an operable
LGS Unit 2 TS 3.8.1.1 requires that an inoperable diesel generator be restored to an operable
status within 30 days or the unit be in at least hot shutdown within the next 12 hours and in
status within 30 days or the unit be in at least hot shutdown within the next 12 hours and in
Line 924: Line 1,128:
Enforcement Policy.
Enforcement Policy.
Emergency Diesel Generator Combustion Air Overheating
Emergency Diesel Generator Combustion Air Overheating
Cornerstone           Significance                               Cross-cutting       Report
Cornerstone
Aspect              Section
Significance
Mitigating System     Green                                     [P.3] -              71153
Cross-cutting
NCV                                       Resolution
Aspect
Report
Section
Mitigating System
Green
NCV
05000352/2018001-02
05000352/2018001-02
Opened/Closed
Opened/Closed  
[P.3] -
Resolution
71153
A self-revealed Green NCV of LGS Unit 1 TS 6.8.1 and TS 3.8.1.1 was identified when
A self-revealed Green NCV of LGS Unit 1 TS 6.8.1 and TS 3.8.1.1 was identified when
Exelon failed to properly maintain an operating procedure to maintain a fail-safe design
Exelon failed to properly maintain an operating procedure to maintain a fail-safe design
Line 961: Line 1,173:
setpoint, in accordance with operating procedure S92.9.N, Routine Inspection of the Diesel
setpoint, in accordance with operating procedure S92.9.N, Routine Inspection of the Diesel
Generators. However, Exelon determined that an intermittent malfunction of the PCV in the
Generators. However, Exelon determined that an intermittent malfunction of the PCV in the
supply air to the temperature controller caused the TIC setpoint to be lower and fail to
supply air to the temperature controller caused the TIC setpoint to be lower and fail to  
 
respond. During the next engine run on December 7, 2017, the PCV delivered proper air
respond. During the next engine run on December 7, 2017, the PCV delivered proper air
pressure after three hours of runtime which resulted in the TIC setpoint being at 200 °F based
pressure after three hours of runtime which resulted in the TIC setpoint being at 200 °F based
Line 990: Line 1,203:
resulted in the D12 EDG being inoperable from November 6 to December 12, 2017.
resulted in the D12 EDG being inoperable from November 6 to December 12, 2017.
Significance: The inspectors screened the significance of the finding using IMC 0609,
Significance: The inspectors screened the significance of the finding using IMC 0609,
Appendix A, Exhibit 2, and determined that this finding required a detailed risk evaluation
Appendix A, Exhibit 2, and determined that this finding required a detailed risk evaluation  
(DRE) since the inoperability exceeded the TS allowed outage time of 30 days.
(DRE) since the inoperability exceeded the TS allowed outage time of 30 days.
A Region I SRA completed the DRE and estimated the increase in core damage frequency
A Region I SRA completed the DRE and estimated the increase in core damage frequency  
(CDF) associated with this performance deficiency to be 8.8E-8/yr, or of very low safety
(CDF) associated with this performance deficiency to be 8.8E-8/yr, or of very low safety
significance (Green). To perform the DRE, the SRA used the Systems Analysis Programs for
significance (Green). To perform the DRE, the SRA used the Systems Analysis Programs for
Line 1,004: Line 1,217:
intercooler air outlet temperatures. As noted in Exelons review of the issue, the concern with
intercooler air outlet temperatures. As noted in Exelons review of the issue, the concern with
these higher temperatures was related to blower degradation and engine degradation which
these higher temperatures was related to blower degradation and engine degradation which
was determined to challenge the operability of the ED
was determined to challenge the operability of the EDG.
: [[contact::G.
The SRA reviewed procedures E-1, Loss of All AC Power, and E-10/20, Loss of Offsite
The SRA reviewed procedures E-1]], Loss of All AC Power, and E-10/20, Loss of Offsite
Power, and determined that a best estimate value for the ability to cross-tie power from  
Power, and determined that a best estimate value for the ability to cross-tie power from
 
Unit 2 safety busses to Unit 1 safety busses was 6E-2. This failure probability to take cross-
Unit 2 safety busses to Unit 1 safety busses was 6E-2. This failure probability to take cross-
tie actions was calculated through the use of a SPAR-H calculation conservatively assuming
tie actions was calculated through the use of a SPAR-H calculation conservatively assuming
Line 1,049: Line 1,262:
Enforcement Policy.
Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
The inspectors verified no proprietary information was retained or documented in this report.  
 
On April 12, 2018, the inspectors presented the quarterly resident inspector inspection
On April 12, 2018, the inspectors presented the quarterly resident inspector inspection
results to Rick Libra, Site Vice-President, and other members of the Exelon staff.
results to Rick Libra, Site Vice-President, and other members of the Exelon staff.  
 
THIRD PARTY REVIEWS
THIRD PARTY REVIEWS
Inspectors reviewed Institute on Nuclear Power Reactor reports that were issued during the
Inspectors reviewed Institute on Nuclear Power Reactor reports that were issued during the
inspection period.
inspection period.  
 
DOCUMENTS REVIEWED
DOCUMENTS REVIEWED
71111.01
71111.01
Line 1,085: Line 1,301:
F-R-309, Unit 1, Safeguard Isolation Valve Area Room 309 (El 217), Revision 11
F-R-309, Unit 1, Safeguard Isolation Valve Area Room 309 (El 217), Revision 11
Condition Reports
Condition Reports
20254       4120452
20254
20452
71111.11Q
71111.11Q
Procedures
Procedures
Line 1,092: Line 1,309:
71111.12Q
71111.12Q
Condition Reports
Condition Reports
2632557       2655420       2663432       3986074     3988302       3991456
2632557
4003680       4011371       4076445       4106926
2655420
2663432
3986074
3988302
3991456
4003680
4011371
4076445
4106926  
 
Miscellaneous
Miscellaneous
Engage System Health Reports
Engage System Health Reports
Line 1,102: Line 1,328:
WC-AA-101-1006, On-Line Risk Management and Assessment, Revision 2
WC-AA-101-1006, On-Line Risk Management and Assessment, Revision 2
Condition Reports
Condition Reports
4102016       4102082
4102016
4102082
Miscellaneous
Miscellaneous
E2 Work Schedule for Week of 2/25/18
E2 Work Schedule for Week of 2/25/18
Line 1,114: Line 1,341:
ON-115, Loss of Control Enclosure Cooling, Revision 25
ON-115, Loss of Control Enclosure Cooling, Revision 25
Condition Reports
Condition Reports
4082004       4088765     4089921       4099141     4099223     4100277
4082004
4100294       4100598     4117844
4088765
4089921
4099141
4099223
4100277
4100294
4100598
4117844
Work Order
Work Order
4308130
4308130
Line 1,127: Line 1,361:
ST-6-076-310-2, SGTS Reactor Enclosure Secondary Containment Integrity Test, Revision 21
ST-6-076-310-2, SGTS Reactor Enclosure Secondary Containment Integrity Test, Revision 21
Condition Reports
Condition Reports
4085733       4105709     4121117
4085733
4105709
21117
Work Orders
Work Orders
4703263       4727391      4733863       4738484     4750273
4703263
27391
4733863
4738484
4750273  
 
Miscellaneous
Miscellaneous
EC 622647, Inflatable Seal - Secondary Containment, Revision 2
EC 622647, Inflatable Seal - Secondary Containment, Revision 2
Line 1,141: Line 1,382:
ST-6-092-312-1, D12 Diesel Generator Slow Start Operability Test Run, Revision 103
ST-6-092-312-1, D12 Diesel Generator Slow Start Operability Test Run, Revision 103
Condition Reports
Condition Reports
0379493       0381794       4081625     4094240       4103817       4104251
0379493
0381794
4081625
4094240
4103817
4104251
Work Orders
Work Orders
1382270       4243506        4255083      4595702       4699475
1382270
243506
255083
4595702
4699475
Miscellaneous
Miscellaneous
CGIFU01, EPRI CGI Joint Utility Task Group Commercial Grade Item Evaluation for UL 198E
CGIFU01, EPRI CGI Joint Utility Task Group Commercial Grade Item Evaluation for UL 198E
Line 1,165: Line 1,415:
Procedures
Procedures
ST-4-LLR-031-1, Main Steam Line A, Revision 13
ST-4-LLR-031-1, Main Steam Line A, Revision 13
ST-4-LLR-041-1, Main Steam Line B, Revision 12
ST-4-LLR-041-1, Main Steam Line B, Revision 12  
 
Work Orders
Work Orders
4309668         4310968
4309668
4310968
71124.08
71124.08
Procedures
Procedures
Line 1,179: Line 1,431:
Containerized Waste Facility, Revision 13
Containerized Waste Facility, Revision 13
RP-AA-600-1005, Radioactive Material and Non Disposal Site Waste Shipments, Rev 19
RP-AA-600-1005, Radioactive Material and Non Disposal Site Waste Shipments, Rev 19
RP-AA-600-1006, Shipment of Category 1 Quantities of Radioactive Material or Waste
RP-AA-600-1006, Shipment of Category 1 Quantities of Radioactive Material or Waste  
        (Category 1 RAMQC), Revision 11
(Category 1 RAMQC), Revision 11
RP-AA-600-1007, Radioactive Waste Shipments to Energy Solutions Clive Utah Disposal
RP-AA-600-1007, Radioactive Waste Shipments to Energy Solutions Clive Utah Disposal
Facility Bulk Waste Facility (BWF), Revision 8
Facility Bulk Waste Facility (BWF), Revision 8
RP-AA-600-1008, Radioactive Waste Shipments to Waste Control Specialists (WCS) Disposal
RP-AA-600-1008, Radioactive Waste Shipments to Waste Control Specialists (WCS) Disposal
Facility, Revision 5
Facility, Revision 5
RP-AA-600-1009, Shipment of Category 2 Quantities of Radioactive Material or Waste
RP-AA-600-1009, Shipment of Category 2 Quantities of Radioactive Material or Waste  
        (Category 2 RAMQC), Revision 2
(Category 2 RAMQC), Revision 2
RP-AA-600-1010, Use and Operation of WMG Software for Creating Containers, Samples,
RP-AA-600-1010, Use and Operation of WMG Software for Creating Containers, Samples,
Waste Streams and Waste Types, Revision 2
Waste Streams and Waste Types, Revision 2
Line 1,212: Line 1,464:
EnergySolutions Internal Audit CORP-16-004, Clive Facility
EnergySolutions Internal Audit CORP-16-004, Clive Facility
NUPIC 24365, EnergySolutions
NUPIC 24365, EnergySolutions
NUPIC 24515, Waste Control Specialists, LLC
NUPIC 24515, Waste Control Specialists, LLC  
 
CFR Part 61 Scaling Factors
CFR Part 61 Scaling Factors
Waste Sludge Tank; Deep Bed; Dry Active Waste; Fuel Floor; Reactor Water Clean-Up
Waste Sludge Tank; Deep Bed; Dry Active Waste; Fuel Floor; Reactor Water Clean-Up
Line 1,255: Line 1,508:
ST-6-092-316-1, D12 Diesel Generator Fast Start Operability Test Run, Revision 54
ST-6-092-316-1, D12 Diesel Generator Fast Start Operability Test Run, Revision 54
ST-6-092-362-2, D22 Diesel Generator Operability Verification, Revision 40
ST-6-092-362-2, D22 Diesel Generator Operability Verification, Revision 40
ST-6-092-362-2, D22 Diesel Generator Operability Verification, Revision 40
ST-6-092-362-2, D22 Diesel Generator Operability Verification, Revision 40  
 
Condition Reports
Condition Reports
1108417       1422131      2924515        4021268      4049989       4062096
1108417
4069001       4070641       4073004       4081882       4082219
22131
24515
21268
4049989
4062096
4069001
4070641
4073004
4081882
4082219
Work Orders
Work Orders
2075815       2079589       4292476        4318057       4642785       4650838
2075815
4650858       4652385       4652410       4652412       4663824       4672813
2079589
4686262       4697246
292476
4318057
4642785
4650838
4650858
4652385
4652410
4652412
4663824
4672813
4686262
4697246
Miscellaneous
Miscellaneous
ANSI/ASME B1.20.1, Pipe Threads, General Purpose (Inch), 1983
ANSI/ASME B1.20.1, Pipe Threads, General Purpose (Inch), 1983

Latest revision as of 22:05, 5 January 2025

Integrated Inspection Reports 05000352/2018001 and 05000353/2018001
ML18131A015
Person / Time
Site: Limerick  Constellation icon.png
Issue date: 05/11/2018
From: James Krafty
Reactor Projects Region 1 Branch 4
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
References
IR 2018001
Download: ML18131A015 (22)


Text

May 11, 2018

SUBJECT:

LIMERICK GENERATING STATION - INTEGRATED INSPECTION REPORT 05000352/2018001 AND 05000353/2018001

Dear Mr. Hanson:

On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Limerick Generating Station (LGS), Units 1 and 2. On April 12, 2018, the NRC inspectors discussed the results of this inspection with Rick Libra, Site Vice-President, and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented two findings of very low safety significance (Green) in this report.

These findings involved violations of NRC requirements. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at LGS. In addition, if you disagree with a cross-cutting aspect assignment, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC, 20555-0001; with copies to the Regional Administrator, Region I, and the NRC Resident Inspector at LGS.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRCs Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

James A. Krafty, Acting Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Numbers: 50-352 and 50-353 License Numbers: NPF-39 and NPF-85

Enclosure:

Inspection Report 05000352/2018001 and 05000353/2018001

Inspection Report

Docket Numbers:

50-352 and 50-353

License Numbers:

NPF-39 and NPF-85

Report Numbers:

05000352/2018001 and 05000353/2018001

Enterprise Identifier:

I-2018-001-0071

Licensee:

Exelon Generation Company, LLC

Facility:

Limerick Generating Station, Units 1 & 2

Location:

Sanatoga, PA 19464

Inspection Dates:

January 1, 2018 through March 31, 2018

Inspectors:

S. Rutenkroger, PhD, Senior Resident Inspector

M. Fannon, Resident Inspector

H. Anagnostopoulos, Senior Health Physicist

J. Furia, Senior Health Physicist

Approved By:

J. Krafty, Acting Chief

Reactor Projects Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Exelons performance at

Limerick Generating Station Units 1 and 2 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.

Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC identified and self-revealed findings, violations, and additional items are summarized in the table below.

List of Findings and Violations

Failure of Emergency Diesel Generator Lube Oil Pipe Nipple Fitting Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000353/2018001-01 Opened/Closed

[P.1] -

Identification 71153 A self-revealed Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action, and LGS Unit 2 technical specification (TS) 3.8.1.1 was identified when Exelon failed to correct a degraded lube oil pipe nipple fitting on the D22 emergency diesel generator (EDG) when maintenance was performed to address leakage which caused inoperability of the EDG for greater than its TS allowed outage time.

Emergency Diesel Generator Combustion Air Overheating Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000352/2018001-02 Opened/Closed

[P.3] -

Resolution 71153 A self-revealed Green NCV of LGS Unit 1 TS 6.8.1 and TS 3.8.1.1 was identified when Exelon failed to properly maintain an operating procedure to maintain a fail-safe design feature for the EDGs which led to the D12 EDG combustion air overheating and caused the EDG to be inoperable for greater than its TS allowed outage time.

Additional Tracking Items

Type Issue number Title Report Section Status LER 05000353/2017-008-00 05000353/2017-008-01 EDG Inoperable for Greater Than 30 Days Resulting in a Condition Prohibited by Technical Specifications 71153 Closed LER 05000352/2018-001-00 D12 EDG Inoperable for Greater than 30 Days Resulting in a Condition Prohibited by TS 71153 Closed

PLANT STATUS

Unit 1 began the inspection period at rated thermal power. On March 25 to 26, 2018, the unit was down powered and shutdown for a planned refueling outage. The unit remained shutdown for the refueling outage for the remainder of the inspection period.

Unit 2 began the inspection period at rated thermal power. On March 17, 2018, the unit was down powered to 64 percent to repair a main condenser tube leak. The unit was returned to rated thermal power the same day and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess Exelons performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather (2 samples)

(1) The inspectors evaluated readiness for impending adverse weather conditions for the onset of winter weather, including high winds, on January 5, 2018.
(2) The inspectors evaluated readiness for impending adverse weather conditions for the onset of winter weather, including high winds, on March 2, 2018.

71111.04 - Equipment Alignment

Partial Walkdown (5 samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 2 high pressure coolant injection on January 16 and 17, 2018
(2) Unit 1 D11 and D13 emergency diesel generators (EDGs) on February 5, 2018
(3) Unit 2 2A batteries and chargers during 2BD101 battery planned maintenance on February 5 through 9, 2018
(4) Unit 1 B residual heat removal subsystem in shutdown cooling during the A emergency core cooling subsystem maintenance window on March 27, 2018
(5) Unit 1 D12 EDG during the division 1 and 3 direct current bus maintenance window on March 28, 2018

71111.05 - Fire Protection

Quarterly Inspection (5 samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Fire area 2, Unit common 13.2kV switchgear room, elevation 217, on January 8, 2018
(2) Fire area 8, Unit 1 class 1E battery room, elevation 239, on January 23, 2018
(3) Fire area 10, Unit 2 class 1E battery rooms, elevation 239, on February 5, 2018
(4) Fire area 28, Unit common standby gas treatment area rooms, elevation 332, on February 27, 201
(5) Fire area 43, Unit 1 safeguard isolation valve area room 309, elevation 217, on March 28, 2018

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (1 sample)

The inspectors observed and evaluated licensed operator simulator training scenarios on February 20, 2018.

Operator Performance (1 sample)

The inspectors observed the downpower and normal plant shutdown of Unit 1 for a planned refueling outage on March 25 and 26, 2018

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness (2 samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Unit 1 reactor manual control system
(2) Unit 2 reactor manual control system

71111.13 - Maintenance Risk Assessments and Emergent Work Control (6 samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unit 2 reactor core isolation cooling relay replacements on January 16 and 17, 2018
(2) Unit common B control room emergency fresh air system testing on February 7, 2018
(3) Unit 2 A residual heat removal maintenance on February 26 and 27, 2018
(4) Unit common A standby gas treatment system maintenance on February 27, 2018
(5) Unit common A emergency service water, A standby gas treatment system, and Unit 2 A reactor enclosure recirculation system maintenance on March 1, 2018
(6) Unit 1 A emergency core cooling system maintenance during reduced core inventory in the refueling outage on March 27 and 28, 2018

71111.15 - Operability Determinations and Functionality Assessments (6 samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 2, D21 EDG room low temperature alarm on December 31, 2017
(2) Unit 2 high pressure coolant injection condensate pump discharge check valve failure on January 25, 2018
(3) Unit 2 high pressure coolant injection vacuum breaker check valve oversized disc on January 31, 2018
(4) Unit common A emergency service water pump motor step voltage test leakage current on January 31, 2018
(5) Unit 2 D21 EDG multiple battery ground alarms while raising speed during the slow start surveillance test on February 2, 2018
(6) Unit common, B control room air supply controller not properly maintaining room temperature on February 4, 2018

71111.18 - Plant Modifications (2 samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Engineering change package 622647 - Inflatable Seal - Secondary Containment
(2) Engineering change request 433952, D23 Repair of the Blower Inspection Cover Bolt Holes Using Stainless Steel Heli-Coil Thread Inserts

71111.19 - Post Maintenance Testing (6 samples)

The inspectors evaluated post maintenance testing for the following maintenance/repair activities:

(1) Unit 2 D24 EDG fuse replacement following an intermittent issue in the automatic start logic circuit on December 6, 2017
(2) Unit 2 reactor core isolation cooling relay replacements on January 16 and 17, 2018
(3) Unit 1 D12 EDG air cooler temperature indicator controller pressure control valve (PCV)replacement on February 5, 2018
(4) Unit 2 B2 battery cell replacements on February 5 and 6, 2018
(5) Unit 2 B2 battery charger current adjustment on February 15, 2018
(6) Unit 2 D24 EDG heating, ventilation, and cooling fan controller replacement on February 22, 2018

71111.20 - Refueling and Other Outage Activities

The inspectors evaluated the Unit 1 refueling outage 1R17 from March 26, 2018, through the end of the inspection period. The following portions of the inspection procedure were not performed during this period.

(1) Fatigue Management
(2) Startup

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Routine

(1) ST-6-092-113-2, D23 EDG 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> endurance run on January 18 and 19, 2018
(2) RT-6-051-320-1, Unit 1 B residual heat removal remote operation test on February 7, 2018
(3) ST-2-074-642-1, Unit 1 source range and intermediate range neutron monitors pre-shutdown testing on March 18, 2018

In-service (2 samples)

(1) ST-6-052-231-1, Unit 1 A core spray pump, valve, and flow test on January 4, 2018
(2) ST-6-052-232-1, Unit 1 B core spray pump, valve, and flow test on March 10, 2018

Containment Isolation Valve (2 samples)

(1) ST-4-LLR-031-1, Unit 1 main steam line A inboard and outboard isolation valves leakage rate testing on March 29, 2018
(2) ST-4-LLR-041-1, Unit 1 main steam line B inboard and outboard isolation valves leakage rate testing on March 29,

RADIATION SAFETY

71124.02 - Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls

Radiological Work Planning (1 sample)

The inspectors evaluated Exelons radiological work planning by reviewing the following activities:

(1) ALARA Plan 2017-101
(2) ALARA Plan 2017-050
(3) ALARA Plan 2017-052

Verification of Dose Estimates and Exposure Tracking Systems (1 sample)

The inspectors evaluated dose estimates and exposure tracking.

71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,

and Transportation

Radioactive Material Storage

The inspectors observed radioactive waste container storage areas and verified the postings and controls and that Exelon had established a process for monitoring the impact of long-term storage of the waste.

Radioactive Waste System Walkdown (1 sample)

The inspectors walked down the following:

Accessible portions of liquid and solid radioactive waste processing systems to verify current system alignment and material condition

Abandoned in place radioactive waste processing equipment to review the controls in place to ensure protection of personnel

Changes made to the radioactive waste processing systems since the last inspection

Processes for mixing and transferring radioactive waste resin and/or sludge discharges into shipping/disposal containers

Current methods and procedures for dewatering waste

Waste Characterization and Classification (1 sample)

The inspectors identified radioactive waste streams and reviewed radiochemical sample analysis results to support radioactive waste characterization. The inspectors reviewed the use of scaling factors and calculations to account for difficult-to-measure radionuclides.

Shipment Preparation (1 sample)

The inspectors reviewed the records of shipment packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping papers provided to the driver, and Exelons verification of shipment readiness.

Shipping Records (1 sample)

The inspectors reviewed selected non-excepted package shipment records.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified Exelons performance indicator submittals listed below for the period January 1, 2017 through December 31, 2017.

(1) Unit 1 and Unit 2 Unplanned Power Changes per 7000 Critical Hours
(2) Unit 1 and Unit 2 High Pressure Injection Systems
(3) Unit 1 and Unit 2 Heat Removal Systems

71153 - Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports (LER)

The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) LER 05000353/2017-008-00 and 05000353/2017-008-01, EDG Inoperable for Greater Than 30 Days Resulting in a Condition Prohibited by Technical Specifications, on December 11, 2017, and February 22, 2018. The review for this event is documented in the inspection results section.
(2) LER 05000352/2018-001-00, D12 EDG Inoperable for Greater than 30 Days Resulting in a Condition Prohibited by TS, on February 5, 2018. The review for this event is documented in the inspection results section.

INSPECTION RESULTS

Failure of Emergency Diesel Generator Lube Oil Pipe Nipple Fitting Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000353/2018001-01 Opened/Closed

[P.1] -

Identification 71153 A self-revealed Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, and LGS Unit 2 technical specification (TS) 3.8.1.1 was identified when Exelon failed to correct a degraded lube oil pipe nipple fitting on the D22 EDG when maintenance was performed to address leakage which caused inoperability of the EDG for greater than its TS allowed outage time.

Description:

The EDG systems are safety related standby emergency power systems for LGS Units 1 and 2 consisting of four diesel generator sets per unit. Each EDG has a lube oil system that cools the diesel engine, lubricates the engine wear surfaces (moving parts), and captures friction wear products. On October 11, 2017, during testing of the D22 EDG, Exelon personnel identified a lube oil leak from a 0.5 inch tapered thread pipe nipple fitting between the lube oil filter and the lube oil filter vent valve. The personnel estimated the leak to be approximately 0.03125 gallons per minute (gpm) (about one-half cup per minute), and Exelon declared the EDG inoperable.

Exelon performed an equipment corrective action program evaluation and identified that the same fitting was found to be leaking and/or weeping on August 31, 2010, and October 3, 2012. After identifying leakage on August 31, 2010, Exelon removed, cleaned, visually inspected, and reinstalled the fitting with thread sealant on November 29, 2011. After the second identification of leakage on October 3, 2012, Exelon performed a similar repair for a second time on August 29, 2013. Exelon planned a similar repair when the fitting leaked for a third time on September 7, 2017. The repair was initially planned for October 6, 2017, but was subsequently rescheduled for November 3, 2017. Exelon identified three through-wall cracks and irregular threads in the fitting and concluded the apparent cause of the failure on October 11, 2017, was age related cyclic fatigue induced by diesel engine vibration. Exelon also determined that the repairs made in 2011 and 2013 contributed to the stresses and crack development and propagation rate based on galling of the threads, wrench marks on the exterior of the fitting, and deeper thread engagement.

The inspectors determined that a rework investigation was required by Exelon procedure MA-AA-716-017, Station Rework Reduction Program, when leakage was identified the second time. Exelon was unable to find evidence that a rework investigation was performed or provide a basis for not performing one. The inspectors concluded a rework investigation would have reasonably provided additional focus and oversight on the subsequent maintenance performed on August 29, 2013. The inspectors determined that additional focus would have provided an opportunity to identify the galled threads on the pipe nipple, the high installation torque required to insert the nipple, and the deeper thread engagement of the nipple following the repair (the nipple was essentially fully inserted into the housing). The fittings condition indicated additional tightening of at least two additional threads beyond original installation which is outside the tolerances of ASME B1.20.1, Pipe Threads, General Purpose (Inch). Based on these conditions, the inspectors determined that Exelon had a reasonable opportunity to foresee and correct the degraded fitting as required by Exelon procedure PI-AA-125, Corrective Action Program (CAP) Procedure, when the second repair was performed.

The inspectors also noted that when maintenance personnel fabricated a replacement fitting after the October 11, 2017, failure, the new fitting leaked during post-maintenance testing.

Maintenance personnel responded by tightening the fitting further, and the fitting leaked again during post-maintenance testing. Exelon then removed the fitting, determined the threads of the new fitting were not satisfactory, that personnel had not verified the threads were properly cut, and fabricated a second new fitting. Although the performance deficiency occurred on August 29, 2013, the inspectors considered the above and determined the applicable cross-cutting aspect of not recognizing deviations from ASME standards, training, and skill of the craft when taking action to address leakage was indicative of current performance.

Corrective Action(s): Exelon replaced the fitting and restored operability of the EDG on October 15, 2017, revised equipment data to require replacement of a pipe nipple fitting instead of reusing if a future leak is identified, and initiated actions to replace similar fittings for extent of condition.

Corrective Action Reference(s): Issue Report (IR) 4070641

Performance Assessment:

Performance Deficiency: The inspectors determined that the failure to correct a degraded lube oil pipe nipple fitting on the D22 EDG when maintenance was performed to address leakage was reasonably within Exelons ability to foresee and correct and should have been prevented.

Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the equipment performance attribute of the mitigating systems cornerstone to ensure the availability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). Specifically, the issue caused the D22 EDG to be inoperable from September 7 to October 15, 2017.

Significance: The inspectors assessed the significance of the finding using IMC 0609, Appendix A, Exhibit 2, and determined that this finding was of very low safety significance (Green). Specifically, the inspectors, in consultation with a Region I senior reactor analyst (SRA), determined that the condition did not represent an actual loss of the D22 EDG probabilistic risk assessment safety function, i.e. the capability to provide power for up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The lube oil storage tank contained over 216 gallons during the period.

The lube oil consumption rate was less than 0.05 gpm. The leak rate was consistent at about 0.03125 gpm. Therefore, at a minimum the lube oil storage tank contained sufficient oil to make up to the D22 EDG oil reservoir for over 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of EDG operation.

Cross-Cutting Aspect: The inspectors determined that this finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Identification, because Exelon personnel did not recognize deviations from standards, training, and skill of the craft when addressing leakage. [P.1]

Enforcement:

Violation: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that measures shall be established to assure that conditions adverse to quality, such as deficiencies, defective material, and non-conformances are promptly identified and corrected.

LGS Unit 2 TS 3.8.1.1 requires that an inoperable diesel generator be restored to an operable status within 30 days or the unit be in at least hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in cold shutdown within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Contrary to the above, from August 29, 2013 to October 15, 2017, a condition adverse to quality was not promptly corrected. Specifically, repairs made to the D22 lube oil filter housing to vent valve pipe nipple fitting failed to correct the cracked fitting which caused the leakage. This caused the D22 EDG to be inoperable from September 7, 2017, to October 15, 2017. The action to restore the diesel within 30 days was not met on October 7, 2017, and Unit 2 was not in at least hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in cold shutdown within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy.

Emergency Diesel Generator Combustion Air Overheating Cornerstone Significance Cross-cutting Aspect Report Section Mitigating System Green NCV 05000352/2018001-02 Opened/Closed

[P.3] -

Resolution 71153 A self-revealed Green NCV of LGS Unit 1 TS 6.8.1 and TS 3.8.1.1 was identified when Exelon failed to properly maintain an operating procedure to maintain a fail-safe design feature for the EDGs which led to the D12 EDG combustion air overheating and caused the EDG to be inoperable for greater than its TS allowed outage time.

Description:

The EDG systems are safety related standby emergency power systems for LGS Units 1 and 2. Each EDG has an air cooler coolant heat exchanger that cools the water that cools the combustion air entering the engine. A three-way thermostatic control valve maintains combustion air temperature between 115 degrees Fahrenheit (°F) and 145 °F by controlling how much emergency service water flows through this heat exchanger.

On December 7, 2017, during surveillance testing of the D12 EDG, Exelon personnel recognized that the combustion air temperature was abnormally high at 220 °F, with an expected band of 115 °F to 145 °F. The D12 EDG had run unloaded for about two hours, then fully loaded for about one hour when the condition was recognized. Exelon shutdown and declared the D12 EDG inoperable and entered TS Limiting Condition for Operation 3.8.1.1. As part of troubleshooting, the temperature indicating controller (TIC) was removed, bench tested satisfactorily, re-installed, and recalibrated to a setpoint temperature of 130°F.

Exelon found the cooling water controllers setpoint dial set at 200°F instead of at the required setpoint of 130°F. On December 12, 2017, Exelon restored and declared the D12 EDG operable.

Exelon performed a past operability review and root cause evaluation and determined that the past functionality of the D12 EDG was adversely impacted such that the EDG was inoperable since performance of the 24-hour endurance run that began on November 6, 2017. Specifically, Exelon determined that on November 6, 2017, while performing a routine running check of engine operation, an equipment operator identified that the air cooler temperature controller setpoint was not at 130°F with process temperatures off-scale low.

The low temperatures were previously identified with an existing IR, initiated on June 12, 2017. The operator adjusted the dial in order to adjust the temperature controller setpoint, in accordance with operating procedure S92.9.N, Routine Inspection of the Diesel Generators. However, Exelon determined that an intermittent malfunction of the PCV in the supply air to the temperature controller caused the TIC setpoint to be lower and fail to respond. During the next engine run on December 7, 2017, the PCV delivered proper air pressure after three hours of runtime which resulted in the TIC setpoint being at 200 °F based on the as-left dial position that was established on November 6, 2017.

Exelon determined the root cause of the issue was the intermittent condition of the PCV that caused intermittent combustion air low temperature operation. Exelon further determined the contributing cause of the issue was the operating procedure directing action which introduced a failure mechanism for the cooling system that was otherwise designed to fail safe (i.e. loss of supply air results in maximum cooling with no loss of diesel function). Finally, Exelon determined the most significant organizational contributor to the issue was the organizations failure to take effective corrective action to address the known low temperature condition which was caused by the degraded pressure control valve.

Corrective Action(s): Exelon recalibrated and reinstalled the TIC, revised the operating procedure to ensure EDG functionality is maintained, and replaced the degraded PCV.

Corrective Action Reference(s): IR 4081882

Performance Assessment:

Performance Deficiency: The inspectors determined that the failure to properly maintain an operating procedure for the EDGs to maintain a fail-safe design feature was reasonably within Exelons ability to foresee and correct and should have been prevented. Specifically, there was a reasonable ability to ensure the operating procedure was appropriate to the circumstances given the previously identified intermittent combustion air low temperature operation and the failure of the TIC to respond to the dial adjustment that was directed by the operating procedure.

Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the equipment performance attribute of the mitigating systems cornerstone to ensure the availability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). Specifically, the inadequate procedure resulted in the D12 EDG being inoperable from November 6 to December 12, 2017.

Significance: The inspectors screened the significance of the finding using IMC 0609, Appendix A, Exhibit 2, and determined that this finding required a detailed risk evaluation (DRE) since the inoperability exceeded the TS allowed outage time of 30 days.

A Region I SRA completed the DRE and estimated the increase in core damage frequency (CDF) associated with this performance deficiency to be 8.8E-8/yr, or of very low safety significance (Green). To perform the DRE, the SRA used the Systems Analysis Programs for Hands-On Evaluation (SAPHIRE), Revision 8.1.6, Standardized Plant Analysis Risk (SPAR)

Model, version 8.50 for LGS Unit 1. This model was determined to require an update to appropriately modify logic and power dependencies associated with the low pressure injection motor operated valve logic. These modifications were assessed and performed by an Idaho National Labs (INL) SPAR model contractor. A limited use updated SPAR model version was posted on the INL website and used by the SRA to run the conditional assessment assuming a failure to run for the D12 EDG. The failure was assumed given the unexpected high intercooler air outlet temperatures. As noted in Exelons review of the issue, the concern with these higher temperatures was related to blower degradation and engine degradation which was determined to challenge the operability of the EDG.

The SRA reviewed procedures E-1, Loss of All AC Power, and E-10/20, Loss of Offsite Power, and determined that a best estimate value for the ability to cross-tie power from Unit 2 safety busses to Unit 1 safety busses was 6E-2. This failure probability to take cross-tie actions was calculated through the use of a SPAR-H calculation conservatively assuming barely adequate time exists, high stress, and low experience for the task. Basic event EPS-XHE-XM-DGXT, was therefore changed from TRUE to 6E-2. An exposure time of 36 days was used based on the inoperable time determined for the D12 EDG. Additionally, no recovery credit was given for the high temperature condition. This was considered a conservative assumption by the SRA given that procedure S92.9.N existed and if used during a postulated event may have resulted in observation of the nonconforming condition and subsequent action to dial back the temperature setpoint. The SRA determined this action would have returned temperatures to the normal band.

The dominant core damage sequence involved a weather related loss of offsite power, with failure of the D12 EDG, common cause failure of the remaining Unit 1 EDGs, failure to cross-tie a Unit 2 EDG to a Unit 1 safety bus, failure to depressurize given the eventual loss of direct current (DC) power, and failure to recover either offsite power or an EDG within 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. In accordance with IMC 0609 guidance a review of the external event risk or large early release frequency was not performed given the increase in internal event CDF was below the 1E-7/yr threshold and would not be expected to change the risk estimation.

Cross-Cutting Aspect: The inspectors determined that this finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Resolution, because Exelon did not take effective corrective action when the intermittent low temperature condition caused by the degraded PCV was identified. Specifically, Exelon did not take appropriate interim corrective action to address the operating procedures TIC adjustments in order to mitigate the issue while more fundamental causes were being addressed. [P.3]

Enforcement:

Violation: LGS Unit 1 TS 6.8.1, requires, in part, written procedures to be established, implemented, and maintained covering applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Regulatory Guide 1.33, Revision 2, Appendix A, Section 1, requires procedures with instructions prepared as appropriate for the operation of onsite emergency power sources (e.g. diesel generators). In addition, LGS Unit 1 TS 3.8.1.1 requires that an inoperable diesel generator be restored to an operable status within 30 days or the unit be in at least hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in cold shutdown within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Contrary to the above, Exelon did not properly maintain EDG operating procedure S92.9.N as appropriate for the operation of the EDGs.

This caused the D12 EDG to be inoperable from November 6, 2017, to December 12, 2017.

The action to restore the diesel within 30 days was not met on December 6, 2017, and Unit 1 was not in at least hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in cold shutdown within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 12, 2018, the inspectors presented the quarterly resident inspector inspection results to Rick Libra, Site Vice-President, and other members of the Exelon staff.

THIRD PARTY REVIEWS

Inspectors reviewed Institute on Nuclear Power Reactor reports that were issued during the inspection period.

DOCUMENTS REVIEWED

71111.01

Procedures

GP-7, Cold Weather Preparation and Operation, Revision 53

SE-14, Snow, Revision 21

SE-9, Preparation for Severe Weather, Revision 45

Condition Reports

4088765

71111.04Q

Procedures

1S92.1.N (COL-2), Equipment Alignment for 1B Diesel Generator Operation, Revision 32

2S55.1.A (COL), Equipment Alignment for Automatic Operation of HPCI System, Revision 19

GP-6.2, Shutdown Operations - Shutdown Cooling Tech Spec Actions, Revision 54

S51.6.A, Swapping RHR Pumps in RHR SDC Mode, Revision 18

S51.8.B, Shutdown Cooling/Reactor Coolant Recirculation Operation Start-Up and Shutdown,

Revision 81

S55.1.A, Normal HPCI Line-Up for Automatic Operation, Revision 37

ST-6-095-905-2, Unit 2 Safeguard Battery Weekly Inspection, Revision 23

ST-6-095-911-2, Div I 125/250 Vdc 2A1D101/2A2D101 Safeguard Battery Quarterly Inspection,

Revision 36

ST-6-095-915-2, Div I 125/250 Vdc 2A1D101/2A2D101 Safeguard Battery Monthly Inspection,

Revision 15

71111.05Q

Procedures

F-A-336, Pre-Fire Plan Common, 13.2kV Switchgear Room 336, Revision 15

F-A-425, Pre-Fire Plan Common, Unit 1, Class 1E Battery 5, Revision 13

F-A-426, Pre-Fire Plan Common, Unit 2, Class 1E Battery 426 and 454, Revision 9

F-A-624, Pre-Fire Plan Common, Standby Gas Treatment Area Rooms 624 and 625, Revision 7

F-R-309, Unit 1, Safeguard Isolation Valve Area Room 309 (El 217), Revision 11

Condition Reports

20254

20452

71111.11Q

Procedures

GP-3, Normal Plant Shutdown, Revision 164

S91.6.B, Transferring House Loads to S/U Buses, Revision 19

71111.12Q

Condition Reports

2632557

2655420

2663432

3986074

3988302

3991456

4003680

4011371

4076445

4106926

Miscellaneous

Engage System Health Reports

71111.13

Procedures

ER-AA-600-1042, On-Line Risk Management, Revision 11

OP-LG-108-117-1000, Limerick Protected Equipment Program, Revision 6

WC-AA-101-1006, On-Line Risk Management and Assessment, Revision 2

Condition Reports

4102016

4102082

Miscellaneous

E2 Work Schedule for Week of 2/25/18

Protected Equipment Scheme on 2/27/18

Protected Equipment Scheme on 3/1/18

Protected Equipment Scheme on 3/27/18 and 3/28/18

71111.15

Procedures

OP-AA-102-103, Operator Work-Around Program, Revision 4

OP-AA-102-106, Operator Response Time Program, Revision 4

ON-115, Loss of Control Enclosure Cooling, Revision 25

Condition Reports

4082004

4088765

4089921

4099141

4099223

4100277

4100294

4100598

4117844

Work Order 4308130

Miscellaneous

L-S-29, Chilled Water System, Revision 14

71111.18

Procedures

CC-AA-10, Configuration Control Process, Revision 9

CC-AA-101, Engineering Change Requests, Revision 5

IP-ENG-001, Standard Design Process, Revision 0

ST-6-076-310-2, SGTS Reactor Enclosure Secondary Containment Integrity Test, Revision 21

Condition Reports

4085733

4105709

21117

Work Orders

4703263

27391

4733863

4738484

4750273

Miscellaneous

EC 622647, Inflatable Seal - Secondary Containment, Revision 2

ECR 433952

71111.19

Procedures

M-095-005, Replacement of Station Battery Cells, Revision 10

PES-S-004, Sampling Plan, Revision 2

ST-2-049-100-2, RCIC Logic System Functional: Simulated Automatic Actuation Test, Revision

ST-2-049-101-2, RCIC Logic System Functional: Isolation Logic Test, Revision 16

ST-6-092-312-1, D12 Diesel Generator Slow Start Operability Test Run, Revision 103

Condition Reports

0379493

0381794

4081625

4094240

4103817

4104251

Work Orders

1382270

243506

255083

4595702

4699475

Miscellaneous

CGIFU01, EPRI CGI Joint Utility Task Group Commercial Grade Item Evaluation for UL 198E

Inspection Report 0101903

LIM-72331, Failure Analysis of Fuses, 12/27/17

Listed Fuses, 7/9/91

71111.22

IST

Procedures

ST-6-052-231-1, A Loop Core Spray Pump, Valve, and Flow Test, Revision 83

ST-6-052-232-1, B Loop Core Spray Pump, Valve, and Flow Test, Revision 74

Routine

Procedures

RT-6-051-320-1, B RHR Remote Operability Test, Revision 7

ST-2-074-642-1, Source Range and Intermediate Range Neutron Monitor Pre-Shutdown

Functional Test, Revision 8

ST-6-092-113-2, D23 Diesel Generator 24 Hour Endurance Test, Revision 43

Condition Reports

4116219

Containment Isolation Valve

Procedures

ST-4-LLR-031-1, Main Steam Line A, Revision 13

ST-4-LLR-041-1, Main Steam Line B, Revision 12

Work Orders

4309668

4310968

71124.08

Procedures

RP-AA-600, Radioactive Material/Waste Shipments, Revision 16

RP-AA-600-1001, Exclusive Use and Emergency Response Information, Revision 9

RP-AA-600-1002, Highway Route Controlled Quantity/Advanced Notification for

Radioactive/Waste Shipments, Revision 6

RP-AA-600-1003, Radioactive Waste Shipments to Barnwell and the Defense Consolidation

Facility (DCF), Revision 10

RP-AA-600-1004, Radioactive Waste Shipments to Energy Solutions Clive Utah Disposal Site

Containerized Waste Facility, Revision 13

RP-AA-600-1005, Radioactive Material and Non Disposal Site Waste Shipments, Rev 19

RP-AA-600-1006, Shipment of Category 1 Quantities of Radioactive Material or Waste

(Category 1 RAMQC), Revision 11

RP-AA-600-1007, Radioactive Waste Shipments to Energy Solutions Clive Utah Disposal

Facility Bulk Waste Facility (BWF), Revision 8

RP-AA-600-1008, Radioactive Waste Shipments to Waste Control Specialists (WCS) Disposal

Facility, Revision 5

RP-AA-600-1009, Shipment of Category 2 Quantities of Radioactive Material or Waste

(Category 2 RAMQC), Revision 2

RP-AA-600-1010, Use and Operation of WMG Software for Creating Containers, Samples,

Waste Streams and Waste Types, Revision 2

RP-AA-600-1011, Use and Operation of WMG Software for Gross Gamma Characterization and

Generation of Shipping Paperwork, Revision 4

RP-AA-600-1012, Use and Operation of WMG Software for Direct Sample Characterization and

Generation of Shipping Paperwork, Revision 2

RP-AA-600-1014, Use and Operation of WMG Software Filter Module, Revision 2

RP-AA-600-1015, Use and Operation of WMG Software for Outage Service Module, Revision 3

RP-AA-600-1016, Use and Operation of the WMG Software for Characterization of

Miscellaneous Items, Revision 0

RP-AA-601, Surveying Radioactive Material Shipments, Revision 20

RP-AA-602, Packaging of Radioactive Material Shipments, Revision 20

RP-AA-602-1001, Packaging of Radioactive Material/Waste Shipments, Revision 17

RP-AA-602-1002, Loading Dry Active Waste and Other Waste Forms for Energy Solutions

Waste Acceptance Guide (WAG-501), Revision 0

RP-AA-602-1003, Radioactive Materials/Waste Shipments Transported Via Rail, Revision 1

RP-AA-603, Inspection and Loading of Radioactive Material Shipments, Rev 10

RP-AA-605, 10 CFR 61 Program, Revision 7

RP-AA-607, Radioactive Material Shipped in Accordance With IATA requirements, Revision 5

RW-AA-100, Process Control Program for Radioactive Wastes, Revision 12

RW-AA-605, 10 CFR 61 Program, Revision 7

Quality Assurance

NOSA-LIM-16-04, Chemistry, Radwaste, Effluent and Environmental Monitoring Audit Report

EnergySolutions Internal Audit CORP-16-004, Clive Facility

NUPIC 24365, EnergySolutions

NUPIC 24515, Waste Control Specialists, LLC

CFR Part 61 Scaling Factors

Waste Sludge Tank; Deep Bed; Dry Active Waste; Fuel Floor; Reactor Water Clean-Up

Condition Reports

3955208

28930

4085448

4092536

4092545

4092549

4092556

4092578

Training

RC-102, Use of WMG Programs and Regulatory Interface

RC-300, Transportation of Radioactive Material by Air

Shipments

MW-16-010; MW-16-045; MW-16-059; MW-17-006; MW-17-031

71151

Procedures

LS-AA-2200, Mitigating System Performance Index Data Acquisition and Reporting, Revision 5

NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7

Miscellaneous

MSPI Data

Operation Narrative Logs

Power History Graphs

71153

Procedures

ARC-BOP-1BC514 C1, Lube Oil Temp High, Revision 1

ARC-BOP-2BC514 B2,

J.W. Temp High, Revision 1

E-1, Loss of All AC Power (Station Blackout), Revision 51

E-1, Loss of All AC Power (Station Blackout), Revision 51

E-10/20, Loss of Offsite Power, Revision 56

E-10/20, Loss of Offsite Power, Revision 56

MA-AA-716-017, Station Rework Reduction Program, Revision 7

S92.9.N, Routine Inspection of the Diesel Generators, Revision 73

S92.9.N, Routine Inspection of the Diesel Generators, Revision 74

ST-2-020-401-1, Electrical Power Systems 1BG501 Diesel Generator Critical and Non-Critical

Instruments Calibration / Functional Test, Revision 31

ST-6-092-112-1, D12 Diesel Generator 24 Hour Endurance Test, Revision 39

ST-6-092-312-1, D12 Diesel Generator Slow Start Operability Test Run, Revision 103

ST-6-092-316-1, D12 Diesel Generator Fast Start Operability Test Run, Revision 54

ST-6-092-362-2, D22 Diesel Generator Operability Verification, Revision 40

ST-6-092-362-2, D22 Diesel Generator Operability Verification, Revision 40

Condition Reports

1108417

22131

24515

21268

4049989

4062096

4069001

4070641

4073004

4081882

4082219

Work Orders

2075815

2079589

292476

4318057

4642785

4650838

4650858

4652385

4652410

4652412

4663824

4672813

4686262

4697246

Miscellaneous

ANSI/ASME B1.20.1, Pipe Threads, General Purpose (Inch), 1983

LIM-64785, Failure Analysis of a Threaded Pipe Nipple from Limerick Station, 12/5/2017

L-S-07, Diesel Generator and Auxiliary Systems, Revision 15

L-S-07, Diesel Generator and Auxiliary Systems, Revision 15

PES-S-006, Code Reconciliation, Revision 6

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

2100 RENAISSANCE BOULEVARD, SUITE 100

KING OF PRUSSIA, PA 19406-2713

May 11, 2018

Mr. Bryan C. Hanson

Senior Vice President, Exelon Generation Company, LLC

President and Chief Nuclear Officer, Exelon Nuclear

4300 Winfield Road

Warrenville, IL 60555

SUBJECT:

LIMERICK GENERATING STATION - INTEGRATED INSPECTION REPORT

05000352/2018001 AND 05000353/2018001

Dear Mr. Hanson:

On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at Limerick Generating Station (LGS), Units 1 and 2. On April 12, 2018, the NRC inspectors

discussed the results of this inspection with Rick Libra, Site Vice-President, and other members

of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented two findings of very low safety significance (Green) in this report.

These findings involved violations of NRC requirements. The NRC is treating these violations

as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violations or significance of these NCVs, you should provide a response within

days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with

copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC

Resident Inspector at LG

S. In addition, if you disagree with a cross-cutting aspect assignment,

you should provide a response within 30 days of the date of this inspection report, with the basis

for your disagreement, to the

U. S. Nuclear Regulatory Commission, ATTN: Document Control

Desk, Washington, DC, 20555-0001; with copies to the Regional Administrator, Region I, and

the NRC Resident Inspector at LGS.

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and the NRCs Public Document

Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390,

Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

James

A. Krafty, Acting Chief

Reactor Projects Branch 4

Division of Reactor Projects

B. Hanson

Docket Numbers: 50-352 and 50-353

License Numbers: NPF-39 and NPF-85

Enclosure:

Inspection Report 05000352/2018001

and 05000353/2018001

cc w/encl:

Distribution via ListServ

ML18131A015

SUNSI Review

Non-Sensitive

Sensitive

Publicly Available

Non-Publicly Available

OFFICE

RI/DRP

RI/DRP

RI/DRP

NAME

S. Rutenkroger

S. Barber/jk for

J. Krafty

DATE

05/10/18

5/10/18

5/11/18

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers:

50-352 and 50-353

License Numbers:

NPF-39 and NPF-85

Report Numbers:

05000352/2018001 and 05000353/2018001

Enterprise Identifier:

I-2018-001-0071

Licensee:

Exelon Generation Company, LLC

Facility:

Limerick Generating Station, Units 1 & 2

Location:

Sanatoga, PA 19464

Inspection Dates:

January 1, 2018 through March 31, 2018

Inspectors:

S. Rutenkroger, PhD, Senior Resident Inspector
M. Fannon, Resident Inspector
H. Anagnostopoulos, Senior Health Physicist
J. Furia, Senior Health Physicist

Approved By:

J. Krafty, Acting Chief

Reactor Projects Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Exelons performance at

Limerick Generating Station Units 1 and 2 by conducting the baseline inspections described in

this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process

is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.

Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC

identified and self-revealed findings, violations, and additional items are summarized in the table

below.

List of Findings and Violations

Failure of Emergency Diesel Generator Lube Oil Pipe Nipple Fitting

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Mitigating

Systems

Green NCV 05000353/2018001-01

Opened/Closed

[P.1] -

Identification

71153

A self-revealed Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action, and LGS Unit 2 technical specification (TS) 3.8.1.1 was identified when

Exelon failed to correct a degraded lube oil pipe nipple fitting on the D22 emergency diesel

generator (EDG) when maintenance was performed to address leakage which caused

inoperability of the EDG for greater than its TS allowed outage time.

Emergency Diesel Generator Combustion Air Overheating

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Mitigating

Systems

Green NCV 05000352/2018001-02

Opened/Closed

[P.3] -

Resolution

71153

A self-revealed Green NCV of LGS Unit 1 TS 6.8.1 and TS 3.8.1.1 was identified when Exelon

failed to properly maintain an operating procedure to maintain a fail-safe design feature for the

EDGs which led to the D12 EDG combustion air overheating and caused the EDG to be

inoperable for greater than its TS allowed outage time.

Additional Tracking Items

Type

Issue number

Title

Report

Section

Status

LER 05000353/2017-008-00

05000353/2017-008-01

EDG Inoperable for Greater

Than 30 Days Resulting in a

Condition Prohibited by

Technical Specifications

71153

Closed

LER 05000352/2018-001-00

D12 EDG Inoperable for

Greater than 30 Days

Resulting in a Condition

Prohibited by TS

71153

Closed

PLANT STATUS

Unit 1 began the inspection period at rated thermal power. On March 25 to 26, 2018, the unit

was down powered and shutdown for a planned refueling outage. The unit remained shutdown

for the refueling outage for the remainder of the inspection period.

Unit 2 began the inspection period at rated thermal power. On March 17, 2018, the unit was

down powered to 64 percent to repair a main condenser tube leak. The unit was returned to

rated thermal power the same day and remained at or near rated thermal power for the

remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed plant status activities described in

IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem

Identification and Resolution. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess Exelons performance and compliance

with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather (2 samples)

(1) The inspectors evaluated readiness for impending adverse weather conditions for the

onset of winter weather, including high winds, on January 5, 2018.

(2) The inspectors evaluated readiness for impending adverse weather conditions for the

onset of winter weather, including high winds, on March 2, 2018.

71111.04 - Equipment Alignment

Partial Walkdown (5 samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1) Unit 2 high pressure coolant injection on January 16 and 17, 2018

(2) Unit 1 D11 and D13 emergency diesel generators (EDGs) on February 5, 2018

(3) Unit 2 2A batteries and chargers during 2BD101 battery planned maintenance on

February 5 through 9, 2018

(4) Unit 1 B residual heat removal subsystem in shutdown cooling during the A emergency

core cooling subsystem maintenance window on March 27, 2018

(5) Unit 1 D12 EDG during the division 1 and 3 direct current bus maintenance window on

March 28, 2018

71111.05 - Fire Protection

Quarterly Inspection (5 samples)

The inspectors evaluated fire protection program implementation in the following selected

areas:

(1) Fire area 2, Unit common 13.2kV switchgear room, elevation 217, on January 8, 2018

(2) Fire area 8, Unit 1 class 1E battery room, elevation 239, on January 23, 2018

(3) Fire area 10, Unit 2 class 1E battery rooms, elevation 239, on February 5, 2018

(4) Fire area 28, Unit common standby gas treatment area rooms, elevation 332, on

February 27, 201

(5) Fire area 43, Unit 1 safeguard isolation valve area room 309, elevation 217, on

March 28, 2018

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (1 sample)

The inspectors observed and evaluated licensed operator simulator training scenarios on

February 20, 2018.

Operator Performance (1 sample)

The inspectors observed the downpower and normal plant shutdown of Unit 1 for a planned

refueling outage on March 25 and 26, 2018

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness (2 samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated

with the following equipment and/or safety significant functions:

(1) Unit 1 reactor manual control system

(2) Unit 2 reactor manual control system

71111.13 - Maintenance Risk Assessments and Emergent Work Control (6 samples)

The inspectors evaluated the risk assessments for the following planned and emergent

work activities:

(1) Unit 2 reactor core isolation cooling relay replacements on January 16 and 17, 2018

(2) Unit common B control room emergency fresh air system testing on February 7, 2018

(3) Unit 2 A residual heat removal maintenance on February 26 and 27, 2018

(4) Unit common A standby gas treatment system maintenance on February 27, 2018

(5) Unit common A emergency service water, A standby gas treatment system, and

Unit 2 A reactor enclosure recirculation system maintenance on March 1, 2018

(6) Unit 1 A emergency core cooling system maintenance during reduced core inventory

in the refueling outage on March 27 and 28, 2018

71111.15 - Operability Determinations and Functionality Assessments (6 samples)

The inspectors evaluated the following operability determinations and functionality

assessments:

(1) Unit 2, D21 EDG room low temperature alarm on December 31, 2017

(2) Unit 2 high pressure coolant injection condensate pump discharge check valve failure on

January 25, 2018

(3) Unit 2 high pressure coolant injection vacuum breaker check valve oversized disc on

January 31, 2018

(4) Unit common A emergency service water pump motor step voltage test leakage current

on January 31, 2018

(5) Unit 2 D21 EDG multiple battery ground alarms while raising speed during the slow

start surveillance test on February 2, 2018

(6) Unit common, B control room air supply controller not properly maintaining room

temperature on February 4, 2018

71111.18 - Plant Modifications (2 samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Engineering change package 622647 - Inflatable Seal - Secondary Containment

(2) Engineering change request 433952, D23 Repair of the Blower Inspection Cover Bolt

Holes Using Stainless Steel Heli-Coil Thread Inserts

71111.19 - Post Maintenance Testing (6 samples)

The inspectors evaluated post maintenance testing for the following maintenance/repair

activities:

(1) Unit 2 D24 EDG fuse replacement following an intermittent issue in the automatic start

logic circuit on December 6, 2017

(2) Unit 2 reactor core isolation cooling relay replacements on January 16 and 17, 2018

(3) Unit 1 D12 EDG air cooler temperature indicator controller pressure control valve (PCV)

replacement on February 5, 2018

(4) Unit 2 B2 battery cell replacements on February 5 and 6, 2018

(5) Unit 2 B2 battery charger current adjustment on February 15, 2018

(6) Unit 2 D24 EDG heating, ventilation, and cooling fan controller replacement on

February 22, 2018

71111.20 - Refueling and Other Outage Activities

The inspectors evaluated the Unit 1 refueling outage 1R17 from March 26, 2018, through

the end of the inspection period. The following portions of the inspection procedure were

not performed during this period.

(1) Fatigue Management

(2) Startup

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Routine (3 samples)

(1) ST-6-092-113-2, D23 EDG 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> endurance run on January 18 and 19, 2018

(2) RT-6-051-320-1, Unit 1 B residual heat removal remote operation test on

February 7, 2018

(3) ST-2-074-642-1, Unit 1 source range and intermediate range neutron monitors pre-

shutdown testing on March 18, 2018

In-service (2 samples)

(1) ST-6-052-231-1, Unit 1 A core spray pump, valve, and flow test on January 4, 2018

(2) ST-6-052-232-1, Unit 1 B core spray pump, valve, and flow test on March 10, 2018

Containment Isolation Valve (2 samples)

(1) ST-4-LLR-031-1, Unit 1 main steam line A inboard and outboard isolation valves

leakage rate testing on March 29, 2018

(2) ST-4-LLR-041-1, Unit 1 main steam line B inboard and outboard isolation valves

leakage rate testing on March 29, 2018

RADIATION SAFETY

71124.02 - Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls

Radiological Work Planning (1 sample)

The inspectors evaluated Exelons radiological work planning by reviewing the following

activities:

(1) ALARA Plan 2017-101

(2) ALARA Plan 2017-050

(3) ALARA Plan 2017-052

Verification of Dose Estimates and Exposure Tracking Systems (1 sample)

The inspectors evaluated dose estimates and exposure tracking.

71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,

and Transportation

Radioactive Material Storage (1 sample)

The inspectors observed radioactive waste container storage areas and verified the postings

and controls and that Exelon had established a process for monitoring the impact of long-

term storage of the waste.

Radioactive Waste System Walkdown (1 sample)

The inspectors walked down the following:

Accessible portions of liquid and solid radioactive waste processing systems to verify

current system alignment and material condition

Abandoned in place radioactive waste processing equipment to review the controls

in place to ensure protection of personnel

Changes made to the radioactive waste processing systems since the last inspection

Processes for mixing and transferring radioactive waste resin and/or sludge

discharges into shipping/disposal containers

Current methods and procedures for dewatering waste

Waste Characterization and Classification (1 sample)

The inspectors identified radioactive waste streams and reviewed radiochemical sample

analysis results to support radioactive waste characterization. The inspectors reviewed the

use of scaling factors and calculations to account for difficult-to-measure radionuclides.

Shipment Preparation (1 sample)

The inspectors reviewed the records of shipment packaging, surveying, labeling, marking,

placarding, vehicle checks, emergency instructions, disposal manifest, shipping papers

provided to the driver, and Exelons verification of shipment readiness.

Shipping Records (1 sample)

The inspectors reviewed selected non-excepted package shipment records.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification (6 samples)

The inspectors verified Exelons performance indicator submittals listed below for the

period January 1, 2017 through December 31, 2017.

(1) Unit 1 and Unit 2 Unplanned Power Changes per 7000 Critical Hours

(2) Unit 1 and Unit 2 High Pressure Injection Systems

(3) Unit 1 and Unit 2 Heat Removal Systems

71153 - Follow-up of Events and Notices of Enforcement Discretion

Licensee Event Reports (LER) (2 samples)

The inspectors evaluated the following licensee event reports which can be accessed at

https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) LER 05000353/2017-008-00 and 05000353/2017-008-01, EDG Inoperable for Greater

Than 30 Days Resulting in a Condition Prohibited by Technical Specifications, on

December 11, 2017, and February 22, 2018. The review for this event is documented in

the inspection results section.

(2) LER 05000352/2018-001-00, D12 EDG Inoperable for Greater than 30 Days Resulting in

a Condition Prohibited by TS, on February 5, 2018. The review for this event is

documented in the inspection results section.

INSPECTION RESULTS

Failure of Emergency Diesel Generator Lube Oil Pipe Nipple Fitting

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000353/2018001-01

Opened/Closed

[P.1] -

Identification

71153

A self-revealed Green non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action, and LGS Unit 2 technical specification (TS) 3.8.1.1 was identified when

Exelon failed to correct a degraded lube oil pipe nipple fitting on the D22 EDG when

maintenance was performed to address leakage which caused inoperability of the EDG for

greater than its TS allowed outage time.

Description: The EDG systems are safety related standby emergency power systems for

LGS Units 1 and 2 consisting of four diesel generator sets per unit. Each EDG has a lube oil

system that cools the diesel engine, lubricates the engine wear surfaces (moving parts), and

captures friction wear products. On October 11, 2017, during testing of the D22 EDG,

Exelon personnel identified a lube oil leak from a 0.5 inch tapered thread pipe nipple fitting

between the lube oil filter and the lube oil filter vent valve. The personnel estimated the leak

to be approximately 0.03125 gallons per minute (gpm) (about one-half cup per minute), and

Exelon declared the EDG inoperable.

Exelon performed an equipment corrective action program evaluation and identified that the

same fitting was found to be leaking and/or weeping on August 31, 2010, and October 3,

2012. After identifying leakage on August 31, 2010, Exelon removed, cleaned, visually

inspected, and reinstalled the fitting with thread sealant on November 29, 2011. After the

second identification of leakage on October 3, 2012, Exelon performed a similar repair for a

second time on August 29, 2013. Exelon planned a similar repair when the fitting leaked for a

third time on September 7, 2017. The repair was initially planned for October 6, 2017, but

was subsequently rescheduled for November 3, 2017. Exelon identified three through-wall

cracks and irregular threads in the fitting and concluded the apparent cause of the failure on

October 11, 2017, was age related cyclic fatigue induced by diesel engine vibration. Exelon

also determined that the repairs made in 2011 and 2013 contributed to the stresses and crack

development and propagation rate based on galling of the threads, wrench marks on the

exterior of the fitting, and deeper thread engagement.

The inspectors determined that a rework investigation was required by Exelon procedure MA-

AA-716-017, Station Rework Reduction Program, when leakage was identified the second

time. Exelon was unable to find evidence that a rework investigation was performed or

provide a basis for not performing one. The inspectors concluded a rework investigation

would have reasonably provided additional focus and oversight on the subsequent

maintenance performed on August 29, 2013. The inspectors determined that additional focus

would have provided an opportunity to identify the galled threads on the pipe nipple, the high

installation torque required to insert the nipple, and the deeper thread engagement of the

nipple following the repair (the nipple was essentially fully inserted into the housing). The

fittings condition indicated additional tightening of at least two additional threads beyond

original installation which is outside the tolerances of ASME B1.20.1, Pipe Threads, General

Purpose (Inch). Based on these conditions, the inspectors determined that Exelon had a

reasonable opportunity to foresee and correct the degraded fitting as required by Exelon

procedure PI-AA-125, Corrective Action Program (CAP) Procedure, when the second repair

was performed.

The inspectors also noted that when maintenance personnel fabricated a replacement fitting

after the October 11, 2017, failure, the new fitting leaked during post-maintenance testing.

Maintenance personnel responded by tightening the fitting further, and the fitting leaked again

during post-maintenance testing. Exelon then removed the fitting, determined the threads of

the new fitting were not satisfactory, that personnel had not verified the threads were properly

cut, and fabricated a second new fitting. Although the performance deficiency occurred on

August 29, 2013, the inspectors considered the above and determined the applicable cross-

cutting aspect of not recognizing deviations from ASME standards, training, and skill of the

craft when taking action to address leakage was indicative of current performance.

Corrective Action(s): Exelon replaced the fitting and restored operability of the EDG on

October 15, 2017, revised equipment data to require replacement of a pipe nipple fitting

instead of reusing if a future leak is identified, and initiated actions to replace similar fittings

for extent of condition.

Corrective Action Reference(s): Issue Report (IR) 4070641

Performance Assessment:

Performance Deficiency: The inspectors determined that the failure to correct a degraded

lube oil pipe nipple fitting on the D22 EDG when maintenance was performed to address

leakage was reasonably within Exelons ability to foresee and correct and should have been

prevented.

Screening: The inspectors determined the performance deficiency was more than minor

because it adversely affected the equipment performance attribute of the mitigating systems

cornerstone to ensure the availability of systems that respond to initiating events to prevent

undesirable consequences (i.e. core damage). Specifically, the issue caused the D22 EDG

to be inoperable from September 7 to October 15, 2017.

Significance: The inspectors assessed the significance of the finding using IMC 0609,

Appendix AProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609,</br></br>Appendix A" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Exhibit 2, and determined that this finding was of very low safety significance

(Green). Specifically, the inspectors, in consultation with a Region I senior reactor analyst

(SRA), determined that the condition did not represent an actual loss of the D22 EDG

probabilistic risk assessment safety function, i.e. the capability to provide power for up to 24

hours. The lube oil storage tank contained over 216 gallons during the period.

The lube oil consumption rate was less than 0.05 gpm. The leak rate was consistent at about

0.03125 gpm. Therefore, at a minimum the lube oil storage tank contained sufficient oil to

make up to the D22 EDG oil reservoir for over 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of EDG operation.

Cross-Cutting Aspect: The inspectors determined that this finding has a cross-cutting aspect

in the area of Problem Identification and Resolution, Identification, because Exelon personnel

did not recognize deviations from standards, training, and skill of the craft when addressing

leakage. [P.1]

Enforcement:

Violation: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that

measures shall be established to assure that conditions adverse to quality, such as

deficiencies, defective material, and non-conformances are promptly identified and corrected.

LGS Unit 2 TS 3.8.1.1 requires that an inoperable diesel generator be restored to an operable

status within 30 days or the unit be in at least hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in

cold shutdown within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Contrary to the above, from August 29, 2013 to

October 15, 2017, a condition adverse to quality was not promptly corrected. Specifically,

repairs made to the D22 lube oil filter housing to vent valve pipe nipple fitting failed to correct

the cracked fitting which caused the leakage. This caused the D22 EDG to be inoperable

from September 7, 2017, to October 15, 2017. The action to restore the diesel within 30 days

was not met on October 7, 2017, and Unit 2 was not in at least hot shutdown within the next

hours and in cold shutdown within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the

Enforcement Policy.

Emergency Diesel Generator Combustion Air Overheating

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Mitigating System

Green

NCV 05000352/2018001-02

Opened/Closed

[P.3] -

Resolution

71153

A self-revealed Green NCV of LGS Unit 1 TS 6.8.1 and TS 3.8.1.1 was identified when

Exelon failed to properly maintain an operating procedure to maintain a fail-safe design

feature for the EDGs which led to the D12 EDG combustion air overheating and caused the

EDG to be inoperable for greater than its TS allowed outage time.

Description: The EDG systems are safety related standby emergency power systems for

LGS Units 1 and 2. Each EDG has an air cooler coolant heat exchanger that cools the water

that cools the combustion air entering the engine. A three-way thermostatic control valve

maintains combustion air temperature between 115 degrees Fahrenheit (°F) and 145 °F by

controlling how much emergency service water flows through this heat exchanger.

On December 7, 2017, during surveillance testing of the D12 EDG, Exelon personnel

recognized that the combustion air temperature was abnormally high at 220 °F, with an

expected band of 115 °F to 145 °

F. The D12 EDG had run unloaded for about two hours,

then fully loaded for about one hour when the condition was recognized. Exelon shutdown

and declared the D12 EDG inoperable and entered TS Limiting Condition for Operation

3.8.1.1. As part of troubleshooting, the temperature indicating controller (TIC) was removed,

bench tested satisfactorily, re-installed, and recalibrated to a setpoint temperature of 130°F.

Exelon found the cooling water controllers setpoint dial set at 200°F instead of at the required

setpoint of 130°

F. On December 12, 2017, Exelon restored and declared the D12 EDG

operable.

Exelon performed a past operability review and root cause evaluation and determined that the

past functionality of the D12 EDG was adversely impacted such that the EDG was

inoperable since performance of the 24-hour endurance run that began on November 6,

2017. Specifically, Exelon determined that on November 6, 2017, while performing a routine

running check of engine operation, an equipment operator identified that the air cooler

temperature controller setpoint was not at 130°F with process temperatures off-scale low.

The low temperatures were previously identified with an existing IR, initiated on

June 12, 2017. The operator adjusted the dial in order to adjust the temperature controller

setpoint, in accordance with operating procedure S92.9.N, Routine Inspection of the Diesel

Generators. However, Exelon determined that an intermittent malfunction of the PCV in the

supply air to the temperature controller caused the TIC setpoint to be lower and fail to

respond. During the next engine run on December 7, 2017, the PCV delivered proper air

pressure after three hours of runtime which resulted in the TIC setpoint being at 200 °F based

on the as-left dial position that was established on November 6, 2017.

Exelon determined the root cause of the issue was the intermittent condition of the PCV that

caused intermittent combustion air low temperature operation. Exelon further determined the

contributing cause of the issue was the operating procedure directing action which introduced

a failure mechanism for the cooling system that was otherwise designed to fail safe (i.e. loss

of supply air results in maximum cooling with no loss of diesel function). Finally, Exelon

determined the most significant organizational contributor to the issue was the organizations

failure to take effective corrective action to address the known low temperature condition

which was caused by the degraded pressure control valve.

Corrective Action(s): Exelon recalibrated and reinstalled the TIC, revised the operating

procedure to ensure EDG functionality is maintained, and replaced the degraded PCV.

Corrective Action Reference(s): IR 4081882

Performance Assessment:

Performance Deficiency: The inspectors determined that the failure to properly maintain an

operating procedure for the EDGs to maintain a fail-safe design feature was reasonably within

Exelons ability to foresee and correct and should have been prevented. Specifically, there

was a reasonable ability to ensure the operating procedure was appropriate to the

circumstances given the previously identified intermittent combustion air low temperature

operation and the failure of the TIC to respond to the dial adjustment that was directed by the

operating procedure.

Screening: The inspectors determined the performance deficiency was more than minor

because it adversely affected the equipment performance attribute of the mitigating systems

cornerstone to ensure the availability of systems that respond to initiating events to prevent

undesirable consequences (i.e. core damage). Specifically, the inadequate procedure

resulted in the D12 EDG being inoperable from November 6 to December 12, 2017.

Significance: The inspectors screened the significance of the finding using IMC 0609,

Appendix AProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609,</br></br>Appendix A" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Exhibit 2, and determined that this finding required a detailed risk evaluation

(DRE) since the inoperability exceeded the TS allowed outage time of 30 days.

A Region I SRA completed the DRE and estimated the increase in core damage frequency

(CDF) associated with this performance deficiency to be 8.8E-8/yr, or of very low safety

significance (Green). To perform the DRE, the SRA used the Systems Analysis Programs for

Hands-On Evaluation (SAPHIRE), Revision 8.1.6, Standardized Plant Analysis Risk (SPAR)

Model, version 8.50 for LGS Unit 1. This model was determined to require an update to

appropriately modify logic and power dependencies associated with the low pressure injection

motor operated valve logic. These modifications were assessed and performed by an Idaho

National Labs (INL) SPAR model contractor. A limited use updated SPAR model version was

posted on the INL website and used by the SRA to run the conditional assessment assuming

a failure to run for the D12 EDG. The failure was assumed given the unexpected high

intercooler air outlet temperatures. As noted in Exelons review of the issue, the concern with

these higher temperatures was related to blower degradation and engine degradation which

was determined to challenge the operability of the EDG.

The SRA reviewed procedures E-1, Loss of All AC Power, and E-10/20, Loss of Offsite

Power, and determined that a best estimate value for the ability to cross-tie power from

Unit 2 safety busses to Unit 1 safety busses was 6E-2. This failure probability to take cross-

tie actions was calculated through the use of a SPAR-H calculation conservatively assuming

barely adequate time exists, high stress, and low experience for the task. Basic event

EPS-XHE-XM-DGXT, was therefore changed from TRUE to 6E-2. An exposure time of

days was used based on the inoperable time determined for the D12 ED

G. Additionally,

no recovery credit was given for the high temperature condition. This was considered a

conservative assumption by the SRA given that procedure S92.9.N existed and if used during

a postulated event may have resulted in observation of the nonconforming condition and

subsequent action to dial back the temperature setpoint. The SRA determined this action

would have returned temperatures to the normal band.

The dominant core damage sequence involved a weather related loss of offsite power, with

failure of the D12 EDG, common cause failure of the remaining Unit 1 EDGs, failure to cross-

tie a Unit 2 EDG to a Unit 1 safety bus, failure to depressurize given the eventual loss of

direct current (DC) power, and failure to recover either offsite power or an EDG within

hours. In accordance with IMC 0609 guidance a review of the external event risk or large

early release frequency was not performed given the increase in internal event CDF was

below the 1E-7/yr threshold and would not be expected to change the risk estimation.

Cross-Cutting Aspect: The inspectors determined that this finding has a cross-cutting aspect

in the area of Problem Identification and Resolution, Resolution, because Exelon did not take

effective corrective action when the intermittent low temperature condition caused by the

degraded PCV was identified. Specifically, Exelon did not take appropriate interim corrective

action to address the operating procedures TIC adjustments in order to mitigate the issue

while more fundamental causes were being addressed. [P.3]

Enforcement:

Violation: LGS Unit 1 TS 6.8.1, requires, in part, written procedures to be established,

implemented, and maintained covering applicable procedures recommended in Appendix A of

Regulatory Guide 1.33, Revision 2, February 1978. Regulatory Guide 1.33, Revision 2,

Appendix A, Section 1, requires procedures with instructions prepared as appropriate for the

operation of onsite emergency power sources (e.g. diesel generators). In addition, LGS

Unit 1 TS 3.8.1.1 requires that an inoperable diesel generator be restored to an operable

status within 30 days or the unit be in at least hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in

cold shutdown within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Contrary to the above, Exelon did not properly

maintain EDG operating procedure S92.9.N as appropriate for the operation of the EDGs.

This caused the D12 EDG to be inoperable from November 6, 2017, to December 12, 2017.

The action to restore the diesel within 30 days was not met on December 6, 2017, and Unit 1

was not in at least hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in cold shutdown within the

following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the

Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 12, 2018, the inspectors presented the quarterly resident inspector inspection

results to Rick Libra, Site Vice-President, and other members of the Exelon staff.

THIRD PARTY REVIEWS

Inspectors reviewed Institute on Nuclear Power Reactor reports that were issued during the

inspection period.

DOCUMENTS REVIEWED

71111.01

Procedures

GP-7, Cold Weather Preparation and Operation, Revision 53

SE-14, Snow, Revision 21

SE-9, Preparation for Severe Weather, Revision 45

Condition Reports

4088765

71111.04Q

Procedures

1S92.1.N (COL-2), Equipment Alignment for 1B Diesel Generator Operation, Revision 32

2S55.1.A (COL), Equipment Alignment for Automatic Operation of HPCI System, Revision 19

GP-6.2, Shutdown Operations - Shutdown Cooling Tech Spec Actions, Revision 54

S51.6.A, Swapping RHR Pumps in RHR SDC Mode, Revision 18

S51.8.B, Shutdown Cooling/Reactor Coolant Recirculation Operation Start-Up and Shutdown,

Revision 81

S55.1.A, Normal HPCI Line-Up for Automatic Operation, Revision 37

ST-6-095-905-2, Unit 2 Safeguard Battery Weekly Inspection, Revision 23

ST-6-095-911-2, Div I 125/250 Vdc 2A1D101/2A2D101 Safeguard Battery Quarterly Inspection,

Revision 36

ST-6-095-915-2, Div I 125/250 Vdc 2A1D101/2A2D101 Safeguard Battery Monthly Inspection,

Revision 15

71111.05Q

Procedures

F-A-336, Pre-Fire Plan Common, 13.2kV Switchgear Room 336, Revision 15

F-A-425, Pre-Fire Plan Common, Unit 1, Class 1E Battery 5, Revision 13

F-A-426, Pre-Fire Plan Common, Unit 2, Class 1E Battery 426 and 454, Revision 9

F-A-624, Pre-Fire Plan Common, Standby Gas Treatment Area Rooms 624 and 625, Revision 7

F-R-309, Unit 1, Safeguard Isolation Valve Area Room 309 (El 217), Revision 11

Condition Reports

20254

20452

71111.11Q

Procedures

GP-3, Normal Plant Shutdown, Revision 164

S91.6.B, Transferring House Loads to S/U Buses, Revision 19

71111.12Q

Condition Reports

2632557

2655420

2663432

3986074

3988302

3991456

4003680

4011371

4076445

4106926

Miscellaneous

Engage System Health Reports

71111.13

Procedures

ER-AA-600-1042, On-Line Risk Management, Revision 11

OP-LG-108-117-1000, Limerick Protected Equipment Program, Revision 6

WC-AA-101-1006, On-Line Risk Management and Assessment, Revision 2

Condition Reports

4102016

4102082

Miscellaneous

E2 Work Schedule for Week of 2/25/18

Protected Equipment Scheme on 2/27/18

Protected Equipment Scheme on 3/1/18

Protected Equipment Scheme on 3/27/18 and 3/28/18

71111.15

Procedures

OP-AA-102-103, Operator Work-Around Program, Revision 4

OP-AA-102-106, Operator Response Time Program, Revision 4

ON-115, Loss of Control Enclosure Cooling, Revision 25

Condition Reports

4082004

4088765

4089921

4099141

4099223

4100277

4100294

4100598

4117844

Work Order 4308130

Miscellaneous

L-S-29, Chilled Water System, Revision 14

71111.18

Procedures

CC-AA-10, Configuration Control Process, Revision 9

CC-AA-101, Engineering Change Requests, Revision 5

IP-ENG-001, Standard Design Process, Revision 0

ST-6-076-310-2, SGTS Reactor Enclosure Secondary Containment Integrity Test, Revision 21

Condition Reports

4085733

4105709

21117

Work Orders

4703263

27391

4733863

4738484

4750273

Miscellaneous

EC 622647, Inflatable Seal - Secondary Containment, Revision 2

ECR 433952

71111.19

Procedures

M-095-005, Replacement of Station Battery Cells, Revision 10

PES-S-004, Sampling Plan, Revision 2

ST-2-049-100-2, RCIC Logic System Functional: Simulated Automatic Actuation Test, Revision

ST-2-049-101-2, RCIC Logic System Functional: Isolation Logic Test, Revision 16

ST-6-092-312-1, D12 Diesel Generator Slow Start Operability Test Run, Revision 103

Condition Reports

0379493

0381794

4081625

4094240

4103817

4104251

Work Orders

1382270

243506

255083

4595702

4699475

Miscellaneous

CGIFU01, EPRI CGI Joint Utility Task Group Commercial Grade Item Evaluation for UL 198E

Inspection Report 0101903

LIM-72331, Failure Analysis of Fuses, 12/27/17

Listed Fuses, 7/9/91

71111.22

IST

Procedures

ST-6-052-231-1, A Loop Core Spray Pump, Valve, and Flow Test, Revision 83

ST-6-052-232-1, B Loop Core Spray Pump, Valve, and Flow Test, Revision 74

Routine

Procedures

RT-6-051-320-1, B RHR Remote Operability Test, Revision 7

ST-2-074-642-1, Source Range and Intermediate Range Neutron Monitor Pre-Shutdown

Functional Test, Revision 8

ST-6-092-113-2, D23 Diesel Generator 24 Hour Endurance Test, Revision 43

Condition Reports

4116219

Containment Isolation Valve

Procedures

ST-4-LLR-031-1, Main Steam Line A, Revision 13

ST-4-LLR-041-1, Main Steam Line B, Revision 12

Work Orders

4309668

4310968

71124.08

Procedures

RP-AA-600, Radioactive Material/Waste Shipments, Revision 16

RP-AA-600-1001, Exclusive Use and Emergency Response Information, Revision 9

RP-AA-600-1002, Highway Route Controlled Quantity/Advanced Notification for

Radioactive/Waste Shipments, Revision 6

RP-AA-600-1003, Radioactive Waste Shipments to Barnwell and the Defense Consolidation

Facility (DCF), Revision 10

RP-AA-600-1004, Radioactive Waste Shipments to Energy Solutions Clive Utah Disposal Site

Containerized Waste Facility, Revision 13

RP-AA-600-1005, Radioactive Material and Non Disposal Site Waste Shipments, Rev 19

RP-AA-600-1006, Shipment of Category 1 Quantities of Radioactive Material or Waste

(Category 1 RAMQC), Revision 11

RP-AA-600-1007, Radioactive Waste Shipments to Energy Solutions Clive Utah Disposal

Facility Bulk Waste Facility (BWF), Revision 8

RP-AA-600-1008, Radioactive Waste Shipments to Waste Control Specialists (WCS) Disposal

Facility, Revision 5

RP-AA-600-1009, Shipment of Category 2 Quantities of Radioactive Material or Waste

(Category 2 RAMQC), Revision 2

RP-AA-600-1010, Use and Operation of WMG Software for Creating Containers, Samples,

Waste Streams and Waste Types, Revision 2

RP-AA-600-1011, Use and Operation of WMG Software for Gross Gamma Characterization and

Generation of Shipping Paperwork, Revision 4

RP-AA-600-1012, Use and Operation of WMG Software for Direct Sample Characterization and

Generation of Shipping Paperwork, Revision 2

RP-AA-600-1014, Use and Operation of WMG Software Filter Module, Revision 2

RP-AA-600-1015, Use and Operation of WMG Software for Outage Service Module, Revision 3

RP-AA-600-1016, Use and Operation of the WMG Software for Characterization of

Miscellaneous Items, Revision 0

RP-AA-601, Surveying Radioactive Material Shipments, Revision 20

RP-AA-602, Packaging of Radioactive Material Shipments, Revision 20

RP-AA-602-1001, Packaging of Radioactive Material/Waste Shipments, Revision 17

RP-AA-602-1002, Loading Dry Active Waste and Other Waste Forms for Energy Solutions

Waste Acceptance Guide (WAG-501), Revision 0

RP-AA-602-1003, Radioactive Materials/Waste Shipments Transported Via Rail, Revision 1

RP-AA-603, Inspection and Loading of Radioactive Material Shipments, Rev 10

RP-AA-605, 10 CFR 61 Program, Revision 7

RP-AA-607, Radioactive Material Shipped in Accordance With IATA requirements, Revision 5

RW-AA-100, Process Control Program for Radioactive Wastes, Revision 12

RW-AA-605, 10 CFR 61 Program, Revision 7

Quality Assurance

NOSA-LIM-16-04, Chemistry, Radwaste, Effluent and Environmental Monitoring Audit Report

EnergySolutions Internal Audit CORP-16-004, Clive Facility

NUPIC 24365, EnergySolutions

NUPIC 24515, Waste Control Specialists, LLC

CFR Part 61 Scaling Factors

Waste Sludge Tank; Deep Bed; Dry Active Waste; Fuel Floor; Reactor Water Clean-Up

Condition Reports

3955208

28930

4085448

4092536

4092545

4092549

4092556

4092578

Training

RC-102, Use of WMG Programs and Regulatory Interface

RC-300, Transportation of Radioactive Material by Air

Shipments

MW-16-010; MW-16-045; MW-16-059; MW-17-006; MW-17-031

71151

Procedures

LS-AA-2200, Mitigating System Performance Index Data Acquisition and Reporting, Revision 5

NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7

Miscellaneous

MSPI Data

Operation Narrative Logs

Power History Graphs

71153

Procedures

ARC-BOP-1BC514 C1, Lube Oil Temp High, Revision 1

ARC-BOP-2BC514 B2,

J.W. Temp High, Revision 1

E-1, Loss of All AC Power (Station Blackout), Revision 51

E-1, Loss of All AC Power (Station Blackout), Revision 51

E-10/20, Loss of Offsite Power, Revision 56

E-10/20, Loss of Offsite Power, Revision 56

MA-AA-716-017, Station Rework Reduction Program, Revision 7

S92.9.N, Routine Inspection of the Diesel Generators, Revision 73

S92.9.N, Routine Inspection of the Diesel Generators, Revision 74

ST-2-020-401-1, Electrical Power Systems 1BG501 Diesel Generator Critical and Non-Critical

Instruments Calibration / Functional Test, Revision 31

ST-6-092-112-1, D12 Diesel Generator 24 Hour Endurance Test, Revision 39

ST-6-092-312-1, D12 Diesel Generator Slow Start Operability Test Run, Revision 103

ST-6-092-316-1, D12 Diesel Generator Fast Start Operability Test Run, Revision 54

ST-6-092-362-2, D22 Diesel Generator Operability Verification, Revision 40

ST-6-092-362-2, D22 Diesel Generator Operability Verification, Revision 40

Condition Reports

1108417

22131

24515

21268

4049989

4062096

4069001

4070641

4073004

4081882

4082219

Work Orders

2075815

2079589

292476

4318057

4642785

4650838

4650858

4652385

4652410

4652412

4663824

4672813

4686262

4697246

Miscellaneous

ANSI/ASME B1.20.1, Pipe Threads, General Purpose (Inch), 1983

LIM-64785, Failure Analysis of a Threaded Pipe Nipple from Limerick Station, 12/5/2017

L-S-07, Diesel Generator and Auxiliary Systems, Revision 15

L-S-07, Diesel Generator and Auxiliary Systems, Revision 15

PES-S-006, Code Reconciliation, Revision 6