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  ...                          _
  '*
                                                  U. S. NUCLEAR REGULATORY COMMISSION
                                                                    ~ REGION I
                                                                                                                                                    e
.                              License' Nos.                  DPR 66,' NPF-73
                              Report Nos.                    50-334/97-08, 50-412/97-08'
                              Docket Nos.                    50-334, 50-412
                              Licensee:                      Duquesne Light Company-(DLC)_                                                        ,
                                                              Post Office Box 4                                                                    :
                                                              Shippingport, PA 15077
.
                                                                                                                                                    '
i-                            Facility: -  _
                                                              Beaver Valley Power Station, Units 1 and 2
                              Inspection Period:              October 5,1997 through November 15,1997
                                                                                                                                                    ,
                            ' inspectors:                    D. Kern, Senior Resident inspector -
                                                              F. Lyon, Resident inspector
                                                              G. Dentel, Resident inspector
<
                                                              J. Furia, Senior Radiation Specialist, DRS
                                                              L. Eckert, Radiation Specialist, DRS
                                                              S. Chaudhary, Senior Reactor Engineer, DRS
                              Approved by:                    P. Eselgroth, Chief
                                                              Reactor Projects Branch 7
          9712160278 971126
*
          PDR- ADOCK 05000334
          R                                  PDR
,
      -.  , . . _ . - - -.          , - -      - , , . , -    ,,n, - --      -                  , , - - - , - - , - , . , , - - . .    .-,m-~.,
 
    _ _ - _ _ _ _ _ _ __ _                    ___                                                                                                                    .
                                                            .. .            .      . .                ..                                                .
                                                                                                                                                              .. . . .
                                                                                                                                                                        .
  .
!  .
                                                                  EXECUTIVE SUMMARY
                                                                                                                                                                          4
                                                        Beaver Valley Power Station, Units 1 & 2
                                                    NRC Inspection Report 50-334/97-08 & 50 412/97-08
                            This integrated inspection included aspects of licensee operations, engineering,
                            maintenance, and plant support. The report covers a 6-week period of resident inspection;
                            in addition, it includes the results of announced inspections by regional inspectors in the
                            areas of radiation protection, rt riioactive effluent control, and inservice inspection.
                            Operations
                            *      Rod cluster control assembly (RCCA) R-19 was mispositioned during insert change-
                                    outs due to inadecuate position verification by contractor personnel and inadequate
                                    supervisory oversight of the evolution by DLC staff, inspectors assessed that the
                                    licensee root cause analysis for the RCCA mispositioning was thorough and that
                                    DLC took reasonable corrective actions to prevent recurrence. (Section 01.2)
                            *      Tagging the Unit 1 containment iodine fans and the steam generator blowdown tank
                                    out-of-service, even though the equipment was required in some emergency
                                    response procedures, was an isolated instance due to inadequate review and
                                    implementation of the Retired Equipment Program. (Section O3.1)
                            *      Operators demonstrated a strong questioning attitude in identifying a longstanding
                                    discrepancy in the auxiliary feedwater surveillance test. (Section 04.1)
                            *        Operators' failure to question the acceptability of charging pump gas accumulation-
                                    data and lack of system engineering guidance was a weakness. (Section 04.1)
                              *      Operator response to a fuel filter leak during emergency diesel generator (EDG)
                                      testing was conservative, and operator response in the control room to the loss of
                                      the EDG was appropriate, inspectors noted good control of event response by
                                      control room supervisors. (Section M1.3)
                              Maintenance
                              *        Poor work practices resulted in a fuel filter leak during EDG testing and a thrust
                                      bearing failure during post maintenance testing on an auxiliary feedwater pump.
                                      The licensee appropriately dispositioned the failures in accordance with the
                                      Maintenance Rule. (Sections M1.2 and M1.3)
                              Enaineerina
                              e      The licensee's review and corrective actions adequately addressed the inadvertent
                                      actuation of the Control Room Emergency Breathing Air Pressurization System
                                      (CREBAPS) on October 6,1996. The CREBAPS Focused Design Review conducted
                                      in response to the event was a thorough evaluation of the system and provided
                                      good recommendations for resolving the longstanding problems. However, the
                                                                                ii
                                                                                                                                                                            I
                                                                                                  . _ _ _ __ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
 
    _ _ _ _ _ - _ _ _ _ _ - -
  .
l
l  .
                                                    long-term action to eliminate the spurious activation of this engineered safety
                                                    features system has not been implemented yet, showing a slow response on the
                                                    licensee's part to resolve the longstanding operator work-around. (Section 08.1)
                                            e      Engineers determined that under certain con % ions the voltage supplied to the
                                                    Unit 1 nuclear instrumentation system power supplies could potentially adversely
                                                    affect the reactor trip system protective action functions. Engineers' performance
                                                    during assessment of this issue and extent of condition reviews was conservative
                                                    and demonstrated a strong questioning attitude. Corrective actions, including
                                                    design change implementation, were timely and technically sound. (Section E1.1)
                                            *      The licensee's team evaluating the gas binding events for the Unit 2 High Head
                                                    Safety injection (HHSI) pumps uncovered weaknesses in the original engineering
                                                    analysis performed to establish venting frequencies. Strong questioning by licensee
                                                    management and team members led to these findings. The venting frequency
                                                    established in 1988 to ensure minimal gas accumulation in the suction lines was
                                                    inadequate to prevent gas binding of the Unit 2 HHSI pumps. The inadequate
                                                    corrective actions to preclude gas binding of the pumps were addressed in NRC
                                                    Inspection Report 50 334 and 412/97-07. Further, the inspectors determined,
                                                    venting of the HHSI pump suction lines immediately prior to TS surveillances may
                                                    be a violation of NRC requirements pertaining to test validity and is unresolved.
                                                      (Section E2.1)
                                              e      The licensee's inservice inspection program plan for Unit 1, with relief requests,
                                                      was satisfactorily maintained and implemented. The non-destructive examination
                                                      personnel were properly qualified and certified, examination procedures were
                                                      adequate to assure valid examinations, and deficiencies were appropriately
                                                      evaluated and resolved. The new data management software appeared to be
                                                      effective. (Section E8)
                                              Plant Sucoort
                                              *      The program for control of radiological work during the Unit 1 refueling outage was
                                                      generally effective; however, one violati< of NRC requirements was identified
                                                      regarding radiation worker knowledge of radiation levels in their work and transit
                                                      areas. (Section R1)
                                              *      Overall, the radioactive liquid and gaseous effluent control programs were good.
                                                      The Radiation Monitoring System (RMS) reliability was adequate; however, a
                                                      violation pertaining to RMS calibration practice was noted. (Section R2.1)
                                              *      The ventilation system surveillance program for radioactive effluent control was
                                                      well implemented. (Section R2.2)
                                              e      Good quality control and quality assurance programs were established for
                                                      radi active effluent control. (Section R7)
                                                                                                                                                                                  iii
        _ - _ _ _ _ _ _ _ _ _ - - - _ _ _ _              _ _ - _ _ _ _ _ _ - _ - _ - _ _ _ - - _ _ _ _ _ _ - _ - _ _ _ _ - _ - - _ - _ _- - - _ - - _ _ - - _ _ - - - - _ _ . _
 
                _ _ - _ _ - _ _ _ _ _ _ _ _ - _ - _ .                                                                                                                .
                                                                                                                                                                                                                    .. .                                ._
  .
l
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                                                                                                                                                                              TABLE OF CONTENTS
      EX EC U TIV E S U M M A RY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii
      TAB LE O F C O NT E NT S . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv
        1. Operations                                    ....................................................                                                                                                                                                                  1
                          O1                            Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
                                                        01.1 General Comments (71707) . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
                                                          ....................................................                                                                                                                                                                  1
                          02                            Operational Status of Facilities and Equipment . . . . . . . . . . . . . . . . . . . 3
                                                        02.1 Engineered Safety Feature System Walkdowns (71707) . . . . . . . 3
                          03                          Operations Procedures and Documentation (92901) . . . . . . . . . . . . . . . 3
                                                        03.1 (Closed) Unresolved item 50-334 and 412/97-07-01 .........                                                                                                                                                          3
                          04                          Operator Knowledge and Performance . . . . . . . . . . . . . . . . . . . . . . . . . 4
                                                        04.1 Questioning Attitude of Operators . . . . . . . . . . . . . . . . . . . . . . . 4
                          08                          - Miscellaneous Operations issues . .                                                                                                                                                ..........................          5
                                                      -08.1 (Closed) Licensee Event Report (LER) 50-334/96-012 . . . . . . . . . 5
                                                        08.2 (Closed) LER 50-334/97 004-01 (92901) . . . . . . . . . . . . . . . . . . 7
                                                        08.3 (Closed) LER 50-334/97-032 (92901) . . . . . . . . . . . . . . . . . . . . 7
          11. M a i nt e n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
                            M1                          Conduct of Maintenance ..................................                                                                                                                                                              7
                                                        M 1.1 Routine Maintenance Observations (62707) . . . . . . . . . . . . . . . . 7
                                                        M1.2 Routino Surveillance Observations (61726) ................                                                                                                                                                          8
                                                        M1.3 Leak on Unit 1 EDG Fuel Oil Filter (71707, 92902) . . . . . . . . . . . 9
          111. E ng i n e e ri n g . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
                              El                        Conduct of Engineering ...................................                                                                                                                                                              9
                                                        E1.1 Vital Bus Voltage Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
                              E2                        Engineering Support of Facilities and Equipment . . . . . . . . . . . . . . . . . 11
                                                        E2.1 (Closed) Unresolved item (URI) 50-334 and 412/97-07 04 ....                                                                                                                                                      11
                              E8                        Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . . . . . . 14
                                                        E8.1 Inservice Inspection . . . . . . . . . . . . . . . . . . . . . . . . . . .....                                                                                                                                    14
                                                        E8.2 (Closed) VIO 50-334/96-05-02 (92903) . . . . . . . . . . . . . . . . . . 18
          IV . Pl a n t S u p p o rt . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19
                              R1                        Radiological Protection and Chemistry (RP&C) Controls . . . . . . . . . . . . 19
                                R2                        Status of RP&C Facilities and Equipment . . . . . . . . . . . . . . . . . . . . . . 21
                                                          R2.1 Calibration of Effluent / Process / Area / Accident Radiation
                                                                                                Monitoring Systems (RMS) . . . . . . . . . . . . . . . . . . . . . . . . . . . 21
                                                          R2.2 Air Cleaning Systems ..............................                                                                                                                                                              24
                                R5                        Staff Training and Qualification in RP&C . . . . . . . . . . . . . . . . . . . . . . 24
                                R7                        Quality Assurance (QA) in RP&C Activities .                                                                                                                                                      ................... 25
                                L1                        Review of FS AR Commitments . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25
                                                                                                                                                                                                                                          iv
                                                                                                                                                                                                                                                                                    l
                                                                                                                                                                                                                                                                                    l
    . _ _                                      _ _ .      . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ - _ _ _ - . - _ - _ _ .
 
    .
    .
      Table of Contents
      V. Ma nag em e nt Meeting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26
              X1    Exit M e eting Summ ary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26
              X2    Pre-Decisional Enforcement Conference . . . . . . . . . . . . . . . . ......                                      26
      PARTI AL LIST OF PERSONS CONTACTED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
      INSP?.CTIO N PROCEDURES U SED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28
      ITEMS OPENED, CLOSED AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . _ 29
      LI ST O F A C R O N Y M S U S E D . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30
.
..
                                                          V
                                                                                                                                              l
                                                                                                                                              !
                                                                      _ - _ . . _ _ . _ . _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _    ..
 
    _____ _ ____ _ __
                                                    .
                                                        .. ..                          .
                                                                                                                      _
  ,
  -
t
                                                                Report Details
                      Summary of Plant Status
                      Unit 1 began this inspection period in Mode 6 (refueling) for the 12th refueling outage. On
                      October 10, the reactor vessel was defueled. On October 20, fuel reloading commenced
                      and the unit re-entered Mode 6. On October 29, the reactor vessel head was tensioned
                      and the unit entered Mode 5 (cold shutdown).
                      Unit 2 operated at 100% power this inspection period.
                                                                l. Operations
                      01      Conduct of Operations
                      01.1 General Comments (71707)'
                                Using Inspection Procedure 71707, the inspectors conducted frequent reviews of
                                ongoing plant operations, in general, the conduct of operations was professional
                                and safety-conscious; specific events and noteworthy observations are detailed in
                                the sections below.
                        01.2 ffiscositioned Rod Cluster Control Assembiv (RCCA)
                        a.    insoection Scone (92901)
                                Inspectors reviewed the licensee root cause analysis for the mispositioning of an
                                RCCA in the spent fuel pool. The review included interviews with selected staff -
                                and managers, and review of applicable refueling procedures, Nuclear Power
                                Division Administrative Procedures (NPDAPs) regarding vendor services, work
                                location conditions, and corrective actions,
                          b.    Observations and Findinas
                                During RCCA eddy current testing and insert change-outs on October 12, RCCA R-
                                  19 was incorrectly inserted into spent fuel pool (SFP) rack location M107 instead of
                                  N107 following removal from the eddy current test stand. The RCCA movements
                                  were being performed in accordance with Refueling Procedure Book 111 - 1RP-12R-
                                  3.22, " Insert Changeouts, Reposition Fuel Assemblies, and Assembly Verification in
                                  Spent Fuel Pit."
                                  Movement of the RCCAs was conducted by two contractor personnel, a SFP bridge
                                  operator and a spotter, and a DLC refueling engineer assistant. Shortly after the
                            ' Topical headings such a 01, M8, etc., are used in accordance with the NRC
                        standardized reactor inspection report outline. Individual reports are not expected to
                        address all outline topics.
 
,
.
                                          2
  movement of RCCA R 19 to its post-inspection location in the SFP, the bridge
  operator realized that it had been moved to the wrong location. Contractor
  supervision, the nuclear shift supervisor, and the DLC Refueling Supervisor were
  immediately notified. A fuel assembly handling deviation report was prepared and
  approved in accordance with procedure and R-19 was moved to its proper location.
  if the positioning error had not been recognized by the bridge operator, refueling -
  procedures contained additional checks later in the process which would likely have
  caught the error.
  DLC senior management learned of the mispositioned RCCA two days afterward
  when Condition Report 971817 was reviewed during processing. All assembly,
  insert, and tool movement was halted until an investigation was completed and
  corrective actions were put in place to prevent recurrence. The DLC root cause
  analysis highlighted the following deficiencies:
  1.      Poor self-verificction techniques were used by the contractor personnel.
          Contributing factors were poor lighting on the index rail and the light blue
          color of the lettering.
  2.      The refueling assistant did not perform independent verification of RCCA
          position. The refueling assistant had no formal training and there was no
          pre-evolution briefing.
  Corrective actions for the mispositioning of R-19 included: changes were made to
  enhance the refueling procedures, a formal training program was initiated for
  refueling engineer assistants, the lighting was improved at the index rails, and an
  ISEG review of the event was initiated.
  Inspectors also reviewed the vendor oversight requirements of NPDAP 9.8, Rev.4,
  " Request for Contracted Services," and the current Rev.5, and assessed that the
  mispositioning did not involve a programmatic concern with vendor control. The
  root cause analysis and recommended corrective actions were presented to the
  Nuclear Safety Review Board. The inspectors noted that having the Plant Manager
  present the analysis and recommended corrective actions diminished the
  independence of the NSRB review and subsequent recommendations to the Plant
  Manager. Inspectors assessed that the licensee root cause analysis for the RCCA
  mispositioning was thorough and that DLC took reasonable corrective actions to
  prevent recurrence.
  TS 6.8.1.a requires that, " Written procedures shall be established, implemented,
  and maintained covering...the applicable procedures recommended in Appendix "A"
  of Regulatory Guide 1.33, Revision 2, February 1978." Regulatory Guide 1.33
  includes procedures for refueling. Mispositioning RCCA R-19 was a failure to
  implement refueling procedure 1RP-12R-3.22 and was a violation of TS 6.8.1.a.
  This non-repetitive, licensee identified and corrected violation is being treated as a
  Non-Cited Violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy
  (NCV 50-334/97-08-01).
 
  _ _ _ _ _ _ _ _ - _ _ _ _ _ - _ - _ _ _ _ _ _ _ _ .
                                                                                ..                                    ..                            .
                                                                                                                                                                                    .
                                                                                                                                                                                        . .. .. .. .. . ..
.
.
                                                                                                                                                        3
                                            c.        Conclusion
                                                      RCCA R-19 was mispositioned during insert change-outs due to inadequate position
                                                      verification by contractor personnel and inadequate supervisory oversight of the
                                                      evolution by DLC staff. The misposition was immediately recognized by the
                                                      personnel involved and immediate corrective actions were taken to move the RCCA
                                                      to its correct position, inspectors assessed that the licensee root cause analysis for
                                                      the RCCA mispositioning was thorough and that DLC took reasonable corrective
                                                      actions to prevent recurrence.
                                    O2                Operational Status of Facilities and Equipment
                                      O2.1 Enoineered Safety Feature System Watkdowns (71707)
                                                      The inspectors walked down accessible portions of selected systems to assess
                                                        equipment operability, material condition, and housekeeping. Minor discrepancies
                                                        were brought to DLC staff's attention and corrected. No substantive concerns were
                                                        identified. The following systems were waWed down:
                                                        e      Unit 1 Containment
                                                        *      Unit 1 Residual Heat Removal System
                                        03              Operations Procedures and Documentation (92901)
                                        03.1 (Closed) Unresolved item 50-334 and 412/97-07-01: Retired Equipment Program
                                                        Inspectors reviewed the Retired Equipment Program following the licensee discovery
                                                        that some equipment was tagged as " retired in place" that was required for use in >
                                                        emergency operating procedures. The issue and the licensee's immediate corrective
                                                        actions were documented in NRC Inspection Report 50-334 and 412/97-07,
                                                        Section 03.1.
                                                        The licensee extent of condition review did not identify any additional equipment
                                                        tagged out that was required for use in emergency or abnormal operating
                                                        procedures (EOPs or AOPs). The candidate components and systems identified by
                                                          system engineers and operators for potential retirement were entered into the
                                                          evaluation process per Nuclear Power Division Administrative Procedure 8.33,
                                                          Rev.0, " Retired Equipment Program." Tha Director, System Engineering, expected
                                                          the evaluations to be completed by December 15. No additional concerns were
                                                          noted by the inspectors,
                                                          inspectors concluded that there were no safety consequences to having the
                                                          containment iodine fans and the steam generator blowdown tank (1FW-TK-1)
                                                          t igged out as " retired in place," %cause the equipment was not safety-related,pnd
                                                          was not depended upon in accident analysis. In addition, alternate methods of
                                                          emergency response other than the iodine fans and blowdown tank were
                                                          proceduralized, inspectors assessed that tagging the equipment out-of-service was
                                                                                                                                                                                                          i
                                                                                                                                                                                                          1
                                                                                      . _ _ _ _ . _ __ _ _ _ . . . _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
 
- _ _ _ _ _ _ _
                                                                                                        _-
        .
                                                                                                                                                          4
                                                                                                                an isolated instance due to inadequate review and implementation of the Retired
                                                                                                                Equipment Program.
                                                                                                                TS 6.8.1.a requires that, " Written procedures shall be established, implemented,
                                                                                                                and maintained covering...the applicable procedures recommended in Appendix "A"
                                                                                                                of Regulatory Guide 1.33, Revision 2, February 1978." Regulatory Guide 1.33
                                                                                                                includes p,ocedures for combating emergencies and other significant events.
                                                                                                                Equipment was retired-in-place without recognizing that it was required in certain
                                                                                                                EOPs. Failure to maintain the EOPs current was a violation of TS 6.8.1.a. This
                                                                                                                non-repetitivt licensee-identified and corrected violation is being treated as a Non-
                                                                                                                Cited Violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy
                                                                                                                (NCV 50-334 and 412/97-08-02).
                                                                                  04                            Operator Knowledge and Perlormance
                                                                                  04.1 Questionino Attitude of Ooerators
                                                                                            a.                  insoection Scoce (71707)
                                                                                                                                        "
                                                                                                                During routine control room tours, inspectors observed operator activities and
                                                                                                                response to degraded conditions.
                                                                                              b.                Findinos and Observations
                                                                                                                in general, the inspectois noted that operators wera knowledgeable of plant
                                                                                                                conditions and out-of-service equipment. The inspectors observed two particular
                                                                                                                  instances that reflected on the questioning attitude of the operators.                . , .
                                                                                                                  Operators questioned steps in the surveillance test for the auxiliary feedwater
                                                                                                                  pumps. During performance of auxiliary feedwater (AFW) pump testing, the manual
                                                                                                                  discharge isolation valve is shut to prevent AFW flow to the steam generators. In
                                                                                                                  accordance with Technical Specification (TS) 4.7.1.2.a.4, an operator is stationed
                                                                                                                  at the pump and is in constant communication with the control room. if needed,
                                                                                                                  the operator is expected to open the discharge valve. The operators questioned
                                                                                                                  whether this is physically possible due to the pressure differential across the valve.
                                                                                                                  Engineering calculations show that the operator would not be able to open the
                                                                                                                  valve. The issue and corrective actions are being tracked under Condition Report
                                                                                                                  971892. The inspectors noted that operators displayed an excellent questioning
                                                                                                                  attitude in identifying this longstanding practice of stationing the operator at the
                                                                                                                  pump.
                                                                                                                  Since the beginning of September 1997, Quality Service personnel have performed
                                                                                                                  ultrasonic examinations to determine gas accumulation in the suction lines of the
                                                                                                                  charging pumps (see Section E2.1 and NRC Inspection Report 50-334 and 50-
                                                                                                                  412/97-07). The gas accumulation was reported to the control room operators in
                                                                                                                  units of inches. Based on interviews, the inspectors determined that the operators
                                                                                                                  did not have a clear understanding of what the values meant nor their impact on
                                                                                                                  operability of the charging pumps. After inspectors' questioning and discussions
                                                                                                                                                                                                              i
                                                                                                                                                                                                              1
                                                                                                                                                                                                              1
    _ - _ _ - _ - _ _ _ _ _ _ _ _ - _ _ - _ - _ _ _ _ - _ - - _ _ _ - _ _ _ _ _ - _ _ - - - _ _ - - _ _ _ - _ -                                              _ __ - _- _ - -____ - _ -
 
                  _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ -
            .
                                                                                                                                        ~
I
                                                                                          5
                                          with operations and system engineering management in October, the system
                                          engineering staff provided guidance to the operators on the quality service
                                          examinations results. The inspectors observed that the current practice provided
                                          the operators with a well defined gas volume limit to make an operability
                                          determination. The lack of adequate guidance, prior to the inspectors' questioning
                                            of the issue, resulted from poor questioning from the operators and failure of
                                            system engineers to provide appropriate guidance to the operators,
              c.                          Conclusion
                                            The inspectors had mixed observations with regard to the questioning attitude of
                                            the reactor operators. In one instance, operators using a strong questioning attitude
                                            identified a longstanding discrepancy in an AFW pump test. However, operators'
                                              failure to question the acceptability of charging pump gas accumulation data was a
                                              weakness.
              08                              f11sc611aneous Operations issues
              08.1 (Closed) Licensee Event Report (LER) 50-334/96-012: Entry into Technical
                                              Specification 3.0.3 Due to isolation of Control Room Emergency Breathing Air
                                              Pressurization System,
              a.                              Insoection Scone (71707)
                                                On October 6,1996, Unit 2 control room operators inadvertently actuated the
                                                Control Room Emergency Breathing Air Pressurization System (CREBAPS).
                                                CREBAPS provides pressurized air to the dual unit control room. Unit 1 operators ,
                                                isolated CREBAPS (to mitigate the consequences) and, as a result, entered into        -
                                                Technical Specification (TS) 3.0.3. This event was previously discussed in NRC
                                                Inspection Report 50-334 and 50-412/96-08. The inspectors reviewed LER 50-
                                                  334/96-012 and other licensee documents. The inspectors also interviewed
                                                  licensee personnel to evaluate corrective actions, the effects of the CREBAPS bottle
                                                  isolation operator work-around, and reliability of the system. The following
                                                  documents were reviewed:
                                                    *    "CREBAPS Focused Design Review Report," Rev.1
                                                    *    Problem Report 2-96-610, " Inadvertent CREBAPS Stuation"
                                                    *    Unit 1 Maintenance Rule System Basis Document, " Area Ventilation Systems
                                                          - Control Area, System 44A," Rev. 3
                                                    e    2DBD-44A2, Rev. 3, Design Basis Document for Area Ventilation Systems -
                                                          Control Area
                                                    *    Unit 2 Shift Logs for August 1997
                                                      *  Unit 1 Equipment Out of Service Log, 01/01/97 - 10/31/97
                                                      *  Unit 1 Work Around Log, dated 09/25/97.
  _ _ _ _ _      _ _ _ _                                    _ _ _ _ - _ _ _ - _  _ - _ -  __ _ - _ -___ _ _ _ _
 
    - _________        - - _ .            .    .
                                                                  .  .
                                                                                                      . ..
  .
!
                                                            6
                b. Observations and Findinas
                  There have been 20 LERs written at BVPS 1 and 2 since 1987 due to spurious
                  CREBAPS actuations and entry into TS 3.0.3. Most of the inadvertent actuations
                  were due to radiation monitor noise and electronic sensitivity problems. To prevent        '
                  an inadvertent air bottle discharge during testing of the radiation monitors,
                  surveillance procedures were revised to isolate the CREBAPS bottles, and TS
                  3.7.7.1 (Unit 1) and TS 3.7.7 (Unit 2) were amended to allow isolation of the
                  CREBAPS bottles for up to 8 hours. The licensee identified the isolation of the
                  bottles as an operator work-around in August 1995. There have been 5 spurious
                  actuations of the CREBAPS system this year. There were no discharges of the
                  system because the CREBAPS bottles were isolated through the proceduralized
                  operator work around.
                  Licensee corrective actions listed in LER 50-334/96-012 have been completed and
                  are appropriate to the specifics of this event. As part of the corrective actions, the
                  licensee performed a focused design review of the CREBAPS. The inspectors
                  assessed that the CREBAPS Focused Design Review Report was a very thorough
                  evaluation of the system, and the recommended corrective actions addressed the
                  root causes of the spurious actuations. Many of the recommended corrective
                    actions of the Focused Design Review have been implemented and have been
                    beneficial. The licensee installed Technical Evaluation Report (TER) 10587 in late
                    June for control room area radiation mor :.or RM-218A, and in September for RM-
                    2188. This TER improved grounding in the instrument tack, improved coaxial
                    shielding, installed snubbers and in-line resistor-capacitor filters, and installed a
                    delay modification in the radiation monitors to prevent false alarms upon startup or
                    following a source check. These modifications were positive improvements.                *
                    However, several spurious actuations have occurred since the modifications.
                    System engineering staff concluded that additional corrective action to install a time
                    delay in the radiation monitor actuation circuitry is necessary; however, it has not
                    been scheduled yet. Therefore, the longstanding operator work-around has
                    continued.
                    Through review of the August Unit 2 operating shift togs, the inspectors determined
                    that portions of the CREBAPS system had been isolated 21% of the time.
                    Approximately 3% of the time was 'iue to the testing and surveillance operator
                    work around, 7% for periodic maintenance, and 11% due to unscheduled corrective
                    maintenance. The inspectors interviewed the licensee system engineer, the
                    maintenance rule program coordinator, and PRA engineer to determine the
                    applicability of system unavailability to the Maintenance Rule. The CREBAPS
                    system was considered a non-risk-significant standby system and was tracked
                    through plant level criteria, with a limit on maintenance preventable functional
                    failures (MPFFs) tracked for the standby safety-related functions. The inspectors
                    determined that this level of tracking was in accordance with the Maintenance Rule.
                                            -                          _ _ _ _ _ _ _ _ _ _ _ _ _ _ _      .
 
    _
      __ ____ ___ _ __ - - -__ -                          . .          .  .
                                                                                  .
                                                                                        .        . ..  . _ ..    ..    ..
                                                                                                                            .
  .
l
                                                                            7
                              c.  Conclusions
                                  The licensee's review and cc,rrective actions adequately addressed the inadvertent
                                  actuation of the Control Room Emergency Breathing Air Pressurization System
                                  (CREBAPS) on October 6,1996. The CREBAPS Focused Design Review conducted
                                  in response to the event was a thorough evaluation of the system and provided
                                  good recommendations for resolving the longstanding problems. However, the
                                  long term action to eliminate the spurious activation of this engineered safety
                                  features system has not been implemented yet, showing a slow response on the
                                  licensee's part to resolve the longstanding operator work-around.
                          08.2 (Closed) LER 50-334/97-004-01 (92901): Failure to Test Post DBA Hydrogen
                                  Control System Recombiners in Accordance with Technical Specifications.
                                    The issue was documented in NRC Inspection Report 50-334 and 412/97-02,
                                                                                                                              '
                                    Section M8.2. No new issues were raised in the LER revision. The scheduled
                                    completion dates for corrective actions were revised or updated.
                          08.3 (Closed) LER 50-334/97-032(92901): Emergency Diesel Generator (EDG)
                                    Automatic Start During Bus Transfer from Unit to System Station Transformer.
                                    The issue was documented in NRC Inspection Report 50-334 and 412/97-07,
                                    Section E2.3 No new concerns were raised in the LER. Inspectors noted that the
                                    licensee has submitted a TS arnendment request (Proposed Operating License
                                    Change Request No.243, dated November 4,1997) for Unit 1 to revisc the
                                    emergency bus undervoltage trip setpoint, allowable value and time delay for EDG
                                    start. This is intended to be a permanent corrective action to prevent unnecessary..
                                    EDG starts during fast bus tran.cfers and while starting reactor coolant pump 1 A.
                                    The licensee also intends to review the TS amendment history associated with the
                                    event to determine if the existing T/S amendment process has any adverse impact
                                    and to identify and implement appropriate enhancements, if necessary, by February
                                    27,1998.
                                                                    II Maintenance
                              M1    Conduct of Maintenance
                              M 1.1 Routine Maintenance Observations (62707)
                                    The inspectors observed selected maintenance activities on important systems and
                                    components. The activities observed and reviewod are listed below.
                                      * 1PMP-13RS-P-Leak Test-1 M        Recirculation Spray Pump Leak Test
                                      * DCP 2298                          Additional Small Bore Pipe Supports Upgrade
                                      * DCP 2209                          ARPI Electronics Upgrade
                                                                                                                      .        .
 
    . _ _ _ - _ _ _    ___ _ - _.                                                                                                .
                                                                                                                                  .
                                                                                                                                      .
.
  9
                                                                            8
                                * MWR 061194                              FW P 2 AFW Pump Terry Turbine Overhaul
                                The activities observed and reviewed were performed safely and in accordance with
                                proper procedures, except as noted below. Inspectors noted that an appropriate
                                level n' supervisory attention was given to the work depending on its r iority and.
                                difficulty.
                                  Motor driveri auxiliary feedwater pump FW-P 3A was overhauled during the
                                  refueling outage under MWR 067122. During post-maintenance testing, the inboard
                                  pump bearing was destroyed. Investigation revealed that the balance drum had not
                                  been set correctly by maintenance technicians during pump reassembly. The root
                                  cause was attributed to poor workmanship. The issue was documented on
                                  Condition Report 971956. Following repairs, the pump was tested satisf actorily
                                  and returned to service. The licensee concluded that the issue was not a
                                  maintenance preventable functional failure (MPFF) under the Maintenance Rule
                                  because the pump was out-of service for overhaul and was not required in Mode 5
                                  (cold shutdown), and the failure was discovered during post-maintenance testing.
                                  Inspectors discussed the issue with system engineering staff and agreed that it was
                                  not an MPFF. Corrective actions to prevent recurrence were under evaluation at the
                                  end of the period.
                    M1.2 Routine Surveillance Observations (6172fd
                                  The inspectors observed portions of selected surveillance tests. Operational
                                  surveillance tests (OSTs) reviewed and observed by the inspectors are listed below.
                                    * 10ST-36.1, Rev.17        Diesel Generator No.1 Monthly Test
                                    * 10ST-24.8, Rev.6          Motor Driven AFW Pumps Check Valves and Flow Test
                                    * 10ST 36.4, Rev 9          Diesel Generator No.2 Automatic Test
                                    * 10ST-7.11, Rev.11        CHS and SIS Operability Test
                                    * 10ST-13.11, Rev.4        OS System Operability Test
                                    * 20ST 26.1, Rev.13        Turbine Throttle, Governor, Reheat Stop and Intercept
                                                                Valve Test
                                    * 10ST-47.2, Rev.18        Containment Integrity Verification
                                    The surveillance testing was performed safely and in accordance with proper
                                    procedures. AddiUunal observations regarding surveillance testing are discussed in
                                    the following sections. The inspectors noted that an appropriate level of
                                    supervisory attention was given to the testing, depending on its sensitivity.
                                                __        _      . _ _  _ _ _ _ _ _ _ _ _ _ _ _ _ -_________.__ _ ___-____-_    _
 
  _-_
      .
      .
                                                        9
        M1.3 Leak on Unit 1 EDG Fuel Oil Filter (71707. 92902)
              10ST-30.4 performs an automatic start of emergency diesel generator (EDG) No.2
              by simulating a loss of offsite power to 4kV bus 10. Immediately after the EDG
              start, a Train "B" safety injection signal is actuated to ensure proper sequencer
              operation. Required loads are then verified to trip and then sequence onto
              emergency bus 1DF. Following logic functional testing, EDG trips are disabled and
              a load reject test of greater than 600KW is performed on the EDG.
              During test performance on Novernber 8, the EDG undervoltage start and sequencer
              operation was satisfactory. However, about 30 seconds into the run, operators
              noted fuel oil spraying from engine mounted duplex fuel oil filter 1EE-FL-10B.
              Operators shut the EDG fuel rack to stop the diesel and the leak. Loss of the EDG
              resulted in loss of power to the 4kV bus 1DF, 480V bus 9P, and all "B" train
                120VAC loads Vital buses 2 and 4 remained energized from their respective            .
              batteries. There was minimalimpact on the plant due to the initiallineup for the
              test. Operators restored power to the affected buses in accordance with applicable
              alarm response procedures within 45 minutes, inspectors observed the event from
              the control room and toured the EDG room shortly afterward. The amount of fuel
              oil spilled was small due to quick operator action in securing the EDG. Inspectors
                assessed that operator response at the EDG to the fuelleak was conservative, and
                operator response in the control room to the loss of the EDG was appropriate,
                inspectors noted good control of event response by control room supervisors.
                The fuel oil filter gasket was inspected, reseated, and tested satisf actorily.
                Maintenance technicians concluded that the gasket had not been sufficiently
                compressed during installation, possibly because a new gasket material was being
                used. The issue was documented under Condition Report 972111 for evaluation
                and corrective actions. The surveillance test on the EDG was successfully
                performed on November 10.
p                                                til. Enalneerina
          E1    Conduct of Engineering
          E1.1  Vital Bus Voltaae Evaluation
          a.    Insoection Scooe (37551. r 2700. 92903)
                While reviewing plans to upgrade existing solid state protection system (SSPS)
                relays, engineers identified a concern regarding the adegaacy of voltage supplied to
                the nuclear instrumentation system (NIS) power supplies. The inspectors
                interviewed personnel, reviewed design documents and observed design charge
                implementation activities to evaluate licensee resolution of this issue.
 
    _ _ _ . -
  .
(
  ~
                                                          10
              b. Observations and Findinas
                  On October 8,1997, engineers determined that under certain conditions the voltage
                  supplied to the Unit 1 NIS power supplies could be outside of the vendor's
                  recommended range (11812.5 volts). This condition could potentially adversely
                  affect the reactor trip system (RTS) protective action functions that respond to
                  power level data from the NIS. The inspectors discussed the issue with operations
                  and engineering personnel and noted that the issue was properly reported to the
                  NRC in accordance with 10 CFR 50.72 and 10 CFR 50.73
                                                                                                          1
                  The inspectors observed that engineers were conservative in assessing a cumulative
                  worst case scenario. Engineers applied the maximum allowable variation in the
                  invertor and regulating transformer output voltages combined with the worst case
                  voltage drop from the transformer to the NIS protection rack (due to various vital
                  bus and NIS protection rack loadirg). Engineers also applied the most restrictive
                  available tolerance band to the NIS power supplies. The Unit 2 NIS power supplies
                  have a vendor specified voltage tolerance of 11815% volts. Although the Unit 1
                  and Unit 2 NIS power supplies are very similar, the documented tolerance for Unit 1
                  (found in the vendor troubleshooting manual) is much more restrictive. Even though
                  the Unit i NIS voltages were outside of vendor recommendations, engineers believe
                  power supplies were likely to have functioned properly as installed, because they
                  were similar in design to the Unit 2 power supplies. Notwithstanding, since
                  documentation of acceptable NIS performance outside of the specified voltage, . sand
                  was not available, engineers recommended upgrading the existing Unit 1 NIS pow r
                  supply voltage transformers. Engineers determined that the existing Unit 2 NIS
                    pov'er supply was acceptable, based on design drawings, calculations, and voltage
                    measurements.
                    As an immediate action, operators verified that voltages were within the vendor
                    specified range each operating shift. In addition, maintenance records
                    demonstrated that the voltages were within the specified range when last verified
                    per periodic maintenance. Engineers reviewed Unit 1 operating history documents
                    and did not identify any actual plant conditions during which voltage was outside of
                    the vendor's recommendations. The unit was in cold shutdc ivn at the time of
                    discovery. Engineers closely communicated with the vendor, initiated a design
                    change to upgrade the power conditioning, and reviewed the potential extent of
                    condition for additional vital bus loads for both units. The inspectors determined
                    that initial actions were timely and technically sound.
                    Design change package (DCP) 2296, " Vital Bus Vo'tage Requirements", was written
                    to upgrade the NIS power supply regulating transformers (11811% volts) and
                    improve connections from the vital bus distribution panels. The inspectors reviewed
                    the DCP and observed portions of the field installation and testing. The DCP was
                    properly implemented and closely coordinated with operations personnel to establish
                    prerequisite plant conditions for installation and testing.
                    Calculation Nos. 8700-E-231(232) were initiated to model vital bus component
                    performance for all four vital buses and downstream components. These
                                                                                                            l
                                                                  _ _ _ _ . ._ _ ____-___________ _ _-_ _
 
  . _ _ _ _ - _ _ _ _ _ _ _ _  -
                  .
i
)                    .
                                                                              11
                                    calculations were nearing completion at the end of this report period. No additional
                                    safety related load discrepancies had been identified. Based on the results of the
                                    completed Unit 1 calculations, engineers will determine whether a detailed Unit 2
                                    analysis is needed.
                              c.    Conclusions
                                    Engineers determined that under certain conditions the voltage supplied to the Unit
                                                                                                                                    *
                                    1 NIS power supplies could potentially adversely affect the reactor trip system
                                    protective action functions. Engineers' performance during ascessment of this issue
                                    and extent of condition reviews, was conservative and demonstrated a strong
                                    questioning attitude. Corrective actions, including design change implementation,
                                    were timely and tv.chnically sound.
                                                                                                                                      ~
                              E2    Engineering Support of Facilities and Equipment
                              E 2.1  (Closed) Unresolved item (URI) 50-334 and 412/97-07-04: Adequacy of the High
                                      Head Safety injection Pump Surveillance Tests to Ensure Operability
                                a.    Inspection Scone (37551)
                                      The inspectors reviewed the adequacy of the surveillance procedure to determine
                                      functionality of the high head safety injection (HHSil/ charging pumps. The
                                      inspectors interviewed operators, system engineers, and system engineering
                                      managcment. The inspectors reviewed the following documents:
                                      *      Inservice Testing (IST) data for the Unit 2 HHSl pumps since 1991;
                                      *      Completed surveillance procedures for Unit 2 HHSI pumps for 1996 and
                                              1997;
                                      *      The last five revisions to the surveillance proceduros for the Unit 2 HHSI
                                              pumps;
                                      *      Minimum operating performance curves (located in the Inservice Testing
                                              Program for Pumps and Valves)
                                  b.  Observations and Findinas
                                      The inspectors identified several issues in NRC inspection Report 50-334 and
                                      412/97-07 that were related to the adequacy of the Unit 2 surveillance procedures
                                      20ST-7.4(5)(6), " Centrifugal Charging Pump [2CHS*P21 A(B)(C))," to determine
                                      functionality of the HHSI pumps.
                                      Syryeillance Procedure /IST Acceotability
                                        The surveillance procedures require that at specific flow rates (~ 200 gpm),
                                        operators obtain IST data including pump bearing temperatures, motor bearing
                                                                              _ - _ _ - _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ - _ - _ _
 
    - _ _ _ _ - -
                                      .
                                            .. ..    .. .. ..    .  .
I    .
                                                                12
                    temperatures, pump vibration data, pressures, and flow rates. Af ter recordinq this
                    data, the procedures allow throttling of the flow to meet the Technical Spech tion
                    (TS) required difierential pressure. Based on review of the TS, the minimum
                    operating performance curves, and basis for the differential pressure values, the
                    inspectors determined that the procedure was acceptable to measure end determine
                    whether pum; performance met the TS required differential pressures.
                    The acceptance criteria in the surveillance procedure require that the pumps operate
                    within the limits of the ASME Section XIIST program. The inspectors determined
                    from past IST results and procedure rev;ews, that the data was collected at a
                    constant flow rate which ensured the data would provide meaningful trending
                    information. The ASME acceptance criteria for differential pressure were not clearly
                    linked to the flow reo due to poor procedure human factors; however, the
                    inspecters determined the performtnce data was properly evaluated to correlate to
                    the acceptanco criteria. Based on engineering memorandums and IST program
                    infermation reviewed, the inspectors determined that the licensee had established a
                    nexus between the acceptance criteria and the minimum cperating performance
                    curve. The minimum operating performance curve establishes the required flow for
                    safety analysis. This clases URI 50 334 and 412/97 07 04.
                    Mditional Back4NMDilBiprmation
                      in Ma'ch 1988, Beaver Valley experienced gas binding of the Unit 2 HHSI pump
                      (2CHbP21 A). NRC Information Notice 88 23, " Potential for Gas Binding of High-
                      Pressua Safety injection Pumps During a Loss-of-Coolant Accident," highlighted the
                      indus      ssue. Engineering performed model testing and ultrasonic testing (UT)
                      exami      )ns of piping to <ietermine gas growth rates. Several colutions were    .
                      evalunt      and a manual venting path was established for both units. The venting
                      times were established based on UT measurements of gas accumulation in 1988
                      and an estimated maximum gas accumulation limit (based on prior history).
                      The licensee did not find the Unit 2 UT examination results performed in 1988
                      during tecords reviews in 1997. The conclusions derived lgas accumulation rates)
                      from those results were documented and used to establish the pump venting
                      frequencies. Unit 1 gas accumulation rates were established based on 48 hours of
                      data taken in 1988. Between 1989 and August 1997, the licansee did not conduct
                      UT testing for Unit 1 or Unit 2 to verify gas accumulation rates were valid. Unit 2
                      UT examinations conducted since August 1997 showed that the majority of the gas
                      accumulation occurred during pump shutdown and not during steady stato
                      conditions. However, the overall Unit 2 gas accumulation rate, were bounded by
                      the 1988 conclusions. Auditional UT examinations for Unit 1 were cor' ducted on all
                      three Unit 1 HHSI pump suction lines in early November. The gas accumulation
                      rates are still under investigation.
                        Prior to March 1988, the licensee had experienced 21 safety injection events at
                        Unit 1 without failure of the HHSI pumps. The maximum gas accumulation limit
                        (8.1 cubic feet) was determined using past suavsful HHSI pump operation and
                        engineering analysis in evaluating the void size during those events. Based un this
                                                                                                            ;
  _              _
 
                    -            -_.    _                ._    _    -_          -_    _ _ - .
  .
  e
                                            13
    analysis a maximum gas accumulation limit was established for Unit 1 and Unit 2.
    The use of Unit 1 data to support a Unit 2 rnaximum gas accumulation limit may
    have been inappropriate due to the different piping configurations.
    In October 1997, the licensee team investigating the gas binding events asse:; sed
    that the maximum gas accumulation limit should be reevaluated for Unit 1 and
    Unit 2. Based on preliminary evaluation, system engineers have established a
    maximum gas accumulation limit of 0.5 cubic feet for Unit 2. The limit is based on
    vendor recommendation to minim!ze entrained gas to 5% by volume. Daily UT
    measurements on Unit 2 suction lines have been performed to verify that the limit
    has been met. The Unit 1 preliminary datermination of gas accumulation lirait will
    be completed prior to Mode 4 entry. The final evaluation of ge= eccumulation limit
    is under investigation by the team for Unit 1 and Unit 2. Thti l'.;ensee is
    reevaluating the engineering analysis for the Original values and vo.ndor information
    to determine an appropriate maximum gas accumulation limit. This effort includes
    construction of a model to help address cuestions on gas ccumulation and
    transportation of that gas to the pump.
    In addition, the established vent path was ineffective due to inmfficient driving
    force to move the gas from the charging pump piping to the col 6ction tank.
    Periodic venting did not always aJequately vent the Unit 2 HHSI pump suction lines.
    The Unit 2 "C" HHSI pump experienced gas binding during multiple starts in June
    1993 and during starts in November 1996 and August 1997. The repeated gas
    binding events were the most likely cause for the pumps' degraded performance                ,
    and subsequent replacement in September 1997. The inadequate venting and gas                  !
    binding events were documented in Nf4C Inspection Report 50 334 and 412/97 07.
    Based on the gas binding events that occurred on Unit 2 "C" HHSl pump, the
    inspectors determined that the established vent path and venting frequencies were
    inadequate to ensure proper pump performance. The inadequate venting system
    and the questionable acceptable gas accumulation limits resulted in inadequate
    venting frequencies. From 1988 to August 1997, the licenseo setied on the venting
i    frequencies to maintain acceptable low levels of gas entrainment for operability of
    the HHSI pumps. The failure to take appropriate corrective actions to preclude gas
    binding of the pumps was an apparent violation documented in NRC Inspection
    Report 50 334 and 412/97 07.
    Ventino Prior to Manual Pumo Starts
i
(    During review of the surveillance procedure and discussions with system engineers
    and operations management, the inspectors determined that HHSi pump suction
'
    lines were routinely vented prior to performing manual pump starts, including the
    periodic surveillance test. The procedures allowed venting the HHSI pump prior to
    starting the pump at the nuclear shift supervisor's discretion. Unit 1 and Unit 2
    c,perators typically vented the HHSI pumps prior to performing the quarterly
    surveillances, safeguards protection system testing (GO testing), and 18-month full
    flow testing. The venting prior to pump start was done to eliminate any gas in the
    system to enhance pump long-term reliabili'y.
 
  -. . - -                              . --                                            -.- - - - - - . - - - - - . -.~ - -. - - .-
          .
                                                                                                                                                                                          I
                                                                                                                                                                                            i
                                                                                                                            14
                                              The venting frequency established to ensure minimal as accumulation in the
                                              suction lines was inadequate to prevent gas binding or the Unit 2 HHSI pumps. 'The                                                          ,
                                              inspectors determined that venting the suction lines immediately prior to performing                                                        i
                                                                                                                                                                                          '
                                              the surveillance testing changed the as found condition of the system from that
                                              which would normally be present if the system was automatically called upon to                                                                1
                                              perform its safety function. . Changing the as-found condition of the HHSI pump
                                              suction lines immediately prior to performing periodic surveillance tests may
                                              interfere with the licensee's ability to properly assass the operability of the system.
                                              10 CFR 50, Appendix B, Criterion XI, " Test Control", requires, in part, that "... the
                                              test is performed under suitable environmental conditions." Suitable environmental-
                                          - conditions include conditions representative of the expseted conditions when the
                                              aquipment is required to perform its safety function. The normal practice of venting -                                                      >
                                              prior to surveillance testing may be a violation of NRC requirements pertaining to
                                              the validity of the test results, depending upon the periodic venting program                                                            . ,
                                              implemented between the surveillance tests. This is considered an unresolved item
                                              pending further NRC review. (URI 50 334 and 412/97 08 03).                                                                                  ,
                                                                                                                                                                                          '
                                      c.      Conclusion
                                              The inspectors observed that the licensee's team evaluating the gas binding events
                                              in August 1997 had uncovered weaknesses in the original engineering analysis
                                              perfortned to establish venting frequencies. Strong questioning by licensee
                                              management and team members led to these findings, inspectors identified
                                              weaknesses in the licensee's oversight of gas accumulation in the safety significant
                                              HHSI system from 1988 to 1997, in that the licensee did not verify the original gas
                                              accumulation rate assumptions, and d!d not verify the adequacy of the periodic vent
                                              path used during that time period.
                                              Periodic venting practices established in 1988 to ensure minimal gas accumulation
                                              in the suction lines was inadequate to prevent gas binding of the Unit 2 HHSI
                                              pumps. The frequency of venting should be based on a good venting method, an
                                              established gas accumulation limit, and an established gas accumubtion rate. Since
                                              the venting method was not effective and the established gas accumulation rate and
                                              limits were incorrect, the venting frequency was inadequate. The inadequate
                                              corrective actions to preclude the gas binding of the pumps were addressed in
                                              Inspection Report 50 33t, and 412/97 07. Acceptability of the pre surveillance test
                                              venting that had been in effect is unresolved.
                                  E8        Miscellaneous Engineering Issues
                                  E8.1      Inservice Insoection
                                      a.      Insoection Scone (73753. 92903)                                                                                                            .
                                              An inspection of the inservice inspection (ISI) program was conducted by a regional
                                              inspector from October 20 24,1997. The objective of this inspection was to verify
                                              that the inservice inspection (ISI), repair, and replacement of Class 1,2, and 3
                                              pressure retaining components are performed in accordance with the Technical
4
            , ....me,,. , , , , - . -          -    e..,..,r .. - . . , ~ .- . . .- . . ,,,,-.              _ #              - + ~ , , , ,24,. ... . .,,y -v-o, ,c-,- ,.enww,,.~,.w.
 
      _. .            . - .          - -                            . _ -
.
.
                                                15
      Specifications (TS), the applicable ASME Code, NRC requirements, and industry
      initiatives, including any relief requests granted by the NRC.
                                                                                              i
      The scope of the inspection included the review of the licensee's ISI program plan      i
      for Beaver Valby Unit 1, orocedures, qualification of inspection / examination          l
      personnel, schdule vi planned Isis for the refueling outage IR12, and observation        l
      of ISI work.                                                                            '
  b. Observation and Findinas
      1.      The ISI Prooram Plan
              The ISI program plan for the third 10 year interva! was submitted to the NRC
              on September 17,1997. The plan includes several relief requests and
              alternate inspection methods. Although the plan has not yet been approved
              by the NM, the licensee has implemented the proposed plan with the
              rationale that many of these relief requests and alternate inspection methods
              had been approved by the NRC for the previous plan, thus it would be
              acceptable for the third interval. However, if the NRC does ' it approve nny
              of tM proposed relief requests or alternates, the licensee ha two mea
              scheouled " outages" to modify and implement an approved plan,
      2.      Steam Generator Tube Eddy Current insoection
              Duquesne Light Company (DLC), the licensee for Beaver Valley Unit 1 (BV-
                1), had nearly completed its steam generator (SG) tube eddy current
              inspections for the current refueling outage. BV-1 has three Westinghouse
              Model 51 SGs with carbon steel drilled hole tube support plates and          -
              WEXTEX joints in the tubesheet. DLC performed fulllength bobbin coil eddy
              current inspections of all active tubes in each SG. The licensee also
              performed specialized inspections using the plus point probe of the low row
              U bends, hot and cold leg top of the tubesheet (TTS), most bobbin coil
              indications, and rolled plugs. DLC also conducted a secondary side visual
              inspection of the wrapper supports and found no degradation.
              Through bobbin coil inspections, DLC identified four pluggable (i.e., greater
              than 40% throughwall) wear indications due to cold lag thinning and anti-
              vibration bar (AVB) wear. The licensee also detected tube support plate
              (TSP) cracking through bobbin coilinspection and followed up using the plus
              point probe to confirm about fifteen suc,h indications in the patch plate
              region. The licensee is evaluating how to dispusition the affected tubes.
              DLC inspected 100% of the TTS on the hot leg side and 20% of the TTS on
              the cold leg side in each SG. The axial extent of the tubesheet inspections
              included six inches above the TTS to three inches below the TTS, On the
              hot leg side, the licensee reported 127 repairable indications. Most were
              identified as axially-oriented outside-diameter stress corrosion cracking
              (ODSCC) located above the TTS in the tube " collar" region (area of heavy
 
                                          . - _. . _ -      -  -          _  ___--  _ _ _ _
.
                                        16
      tube deposits not removed through sludge lancing). A few were axial and
      circumferentially-oriented indications located below the WEXTEX expansion
      transition inside the tubesheet. On the cold leg side, the licensee identified
      nine axially-oriented ODSCC indications located above the TTS; for this SG,
      the licensee expanded its inspection scope to include 100% of the TTS
      region. The longest extent for a circumferential crack was about 90' and
      the longest axial crack was reported to be about 0.8 inches long. Eight
      volumetric indications (some pit-like) were found in the TTS region as well.
      DLC inspected 100% of the row 1 and 2 U bends and 20% of the row 3 U-
      bends. The licensee reported 11 row 1 U bend indications and 1 row 2 U-
      bend indication characterized as primary water stress corrosion cracking
      (PWSCC) and located in the bend tangent. DLC's low row U bends have
      been stress relieved.
      The licensee performed a 100% inspection of dents > 5 volts, a 20% sample
      of dents >205 volts, and 100% of all dents and dings (dents located in the
      freespan) >2 volts located between the TTS and the 3rd TSP. No
      indications were reported.
      DLC inspected 100% of its inconel 600(1-600) rolled plugs and 20% of its
      Inconel 690 (1690) rolled plugs. The licensee reported seven 1600 plug
      indications. The licensee intends to replace these with l 690 rolled plugs
      during this outage. No I 690 plug indications were reported.
      For the identified degradation mechanism, the licensee has selected the most
      limiting (based on length, depth and voltage) indications for insitu pressure
      testing. At the time of this inspection, the pressure testing of SG tubes was
      in progress. The inspector witnessed one such test from the remote test
      control location.
  3.  Qualification /Cortification of NDE Personnel
      The inspector reviewed the qualification and certification records of
      approximately seven individuals engaged in non-destructive examination
      (NDE) of the ISI program. The review indicated that the inspectors were
      properly qualified by formal and practical training, and were certified to
      proper levels of inspection / examination responsibility in different examination
      methods; e.g., visual examination (VT), liquid penetrant (PT), magnetic
      particle (MT), or ultrasonic examination (UT).
  4.  Observation of ISI Examinations
      The inspector observed / witnessed several NDEs to assess the adequacy of
      procedures, knowledge and proficiency of test personnel, and the validity of
      the test results. The following tests were observed:
    _  _        -      -    _
 
    _. -.- _ - - -                      _- - - -                _
                                                                        _ - - _ -              - - - - .      - .            . -.-
                                                                                                                                          ,
                                                                                                                                          i
                                                                                                                                          >
                                                                                                                                          t
      '
                                                                                                                                          !
                                                  '                                                                                      '
                                                                    17
                                                                                                                                          '
                          1.          Surface examination by dye penetrant: CH 23 3 5-03, and CH 23 4-
i                                      F 06 inside containment;                                                                          ;
                          2.          Volumetric examination by UT: 1 SA 41 FD24 in the auxiliary
                                        building; and                                                                                      ,
                                                                                                                                          j
                                                                                                                                          '
                          3.          Pressure test of steam generator tube: 5A21 from the remotu
                                        display / control test facility for SG tube examination and tests.                                ,
'
                          The tests / examinations were performed by knowledgeable and qualified                                          i
                          Individuals, using approved proc?dures, materials, and calibrated equipment.
                          The results were properly recoroad.                                                                            7
                                                                                                                                          '
                    5.    Evaluation and Resolution of Deficiency
                                                                                                                                          i
                          The inspector reviewed the evaluation and resolution by Engineering of three
                                                                                                                                          *
                          " unsatisfactory" test results. These deficiencies were documented in
                          Condition Reports 970792,970793 and 970836, and were related to PT
,
                          surface examinations.
>
                          In all cases, the disposition of the indication by grinding and blending the
                          surface profile to established contour was appropriate.                                            '
                    O.    NDE Procedures
                          The inspector reviewed the following NDE procedure to assess the clarity
                          and technical adequacy of established requirements.
                          GP-105                Evaluation of PSl/ISI Flaw Indications, Rev. 6
                          LP-101                Solvent Removable Visible Dye, Rev.15
                          MT-201                Magnetic Particle Examination, Rev.13
                          UT-301                Linearity of Ultrasonic Instruments, Rev. 9
                          UT-303                Ultrasonic Examination of Piping Welds, 2" to 6" Thick and
                                                  Vessels Less than or Equal to 2" Wall Thickness, Rev.12
a                  The inspector determined that the procedures were clearly written, estbblished
                    technically valid requirements and were appropriately maintained, controlled, and ~
                    used by NDE personnel.
                    Additionally, the licensee has implemented a new data management software for
                    tracking and managing ISI program. Th' new system appears comprehensive and
                    has been successfully used at other utilities.
                                                                                                                                          ,
  l-
                                                                                                                                          ,
                                                                                                                                          .
                                . , - .              . .- .                  -,s  -    , - . -          ,-v-n    . . - -,        , -
 
                                                                              _
  .
  .
                                                    18
      c.  ConclutdQnt
          Based on the above observation, review of documentation, and discussions with
          personnel responsible for ISI program, the inspector concluded that the licensee's
          ISI program plan is satisfactorily maintained and implemented. The NDE personnel
          are properly qualified / certified, examination procedures are adequate to assure valid
          examinations, and deficiencies are appropriately evaluated and resolved. The new
          data management software appears effective.
    E8.2 (Closef f) VIO 50 334/96 05-02(92903): Inadequate cap'eration for UT
          examinations
          The above violation pertained to a failure to perform a calibration for UT
          examination using a reflector perpendicular to the cound beam for examinations          ,
                                                                                                  !
          with the sound beam to the weld seem (circumferential examinations) on six ASME
          class 2 pipe weld examinations. Also, for two calibrations (C 96-57 and C 96-46)
          sido drilled holes were not used to construct the distance amplitude correction
          (DAC) curve.
          In response to the Notice of Violation, the licensee initiated entrective actions to
          resolve the deficiency, and to prevent similar occurrences in tue future. The
          licensee's actions included the following:
          1.      Problem Reports 196 487,196-488 and 196 489 were submitted to the
                  Operations Experience Group on May 17,1996. These problem reports
                  identified the scope of incorrect calibrations and provided technical
                  assessments of the deficiencies identified during the exit meeting on
                  May 16,1996.
          2.      An independent review of the problem reports was performed by Materials
                  and Standards Engineering to address poter.tial operability concerns.
          3.      Independent root cause evaluation using the Taproot root cause evaluation
                  method was performed on the problems identified.
          Actions Taken to Prevent Recurrence
          As a result of the recommendations in the root cause evaluations, the following
          corrective actions were being taken:
          1.      UT Procedure UT-303 was revised for clarification and to allow ID notch
                  calibration and was demonstrated to the authorized nuclear inservice
                  inspector (ANil).
          2.      NDE catractor training has been included in procedure OSP 2.5, which
                  provides procedural contrels for onsite training of contracted NDE personnel
                  using DLC. NDE procedures.
!
l
                                                                                    --.    ,
 
                                                                                                  l
  '
                                                                                                  I
                                                                                                  ;
                                                                                                  I
  ,                                                                                                i
                                                                                                  i
                                                  19
        3.      The calibration report forms have been revised to more clearly define
                calibration orientation and calibration reflectors used.
        4.      The dissimilar metal welds examined using only the ID notch for calibration
                were re-examined using a qualified UT technique during 1R12.
        The inspector verified the licensee's corrective actions by review of documentation
        and discussion with cognizant personnel, and found the actions acceptable and
        effective. Based on the above observation, this item is closed.
                                          IV. Plant Support
    R1  Radiological Protection and Chemistry (RP&C) Controls
    a. Insnection Scone (83750)
        The inspectors reviewed the licensee's program for radiation protection during a
        refueling outage (1R12). Areas reviewed included high and locked high radiation
        area controls, radiation worker performance indicators, including maintaining
        occupational exposures as low as is reasonably achievable (ALARA), and radiation
        worker practices. The inspection was accomplished by a review of plant
        dncuments and procedures, interviews with personnel, and walkdowns of the
        related areas,
    b. Observations and Findinas
        The inspectors reviewed the licensee's performance during the Unit 1 refueling
        outage (1R12) which commenced in late September. Outage goals previously
        established included completion of the outage in 40 days (with a challenge goal of
        36 days), an occupational exposure goal of not more than 201 person rem, and a
        personnel contamination event goal of not more than 180. During the period of this
        specialist inspection, outage activities included eddy current testing in all three
        steam generators, reactor head and upper core internals removal, and the first 36
        hours of fuel removal.
        The inspectors reviewed the licensee's control of high ar.d locked high radiation
        areas, especially those located in the containment. All areas reviewed, which
        included the entrances to the steam generator / reactor cociant pump cubicles, were
        determined to be appropriately controlled, barricaded and posted in accordance with
        plant technical specifications. Workers interviewed in the high radiation areas were
        aware of their work area exposure rates and appropriate radiological controls to
        minimize their exposures. Health physics technicians were observed providing
        d3 tailed and extensive briefings to workers and providing appropriate job coverage.
        Of particular note was the licensee's utilization of remote teledosimetry, closed
        circuit cameras and communication fa steam generator eddy current testing. By
i      utilizing this type of control, the licensee was a' ole to significantly reduce total job
i
l
!
l
 
                            . - .        _                      -.
  .
                                                                                          l
                                            20
    exposures, especially for the radiological cor tmis technicians, while providing real  ;
    time exposure rate data so ac to minimize suam generator worker exposures.
    As noted above, the licensee had established an outage ALARA goal of not more
    than 201 person-rem, and through day 12 of the outage the exposures appeared to
    be tracking well, although the licensee does not track exposure against percentage
    of work completed and the outage was estimated to be two days behind schedule.
    The inspector noted that the licensee was focused on personnel contamination
    events (PCEs) and had established an outage goal of not more than 180 PCEs.
    During the specialist inspection, the inspectors noted that workers entering the
    radiologically controlled areas (RCAs) were not checking the posted general area
    survey maps located at the primary plant staff and contractor entry points, as
    specified in the licensee's radiation work permits. Since the licensee did not utilize
    a direct verbal briefing system between workers and the health physics staff prior to
    entries, it appeared to the inspectors that the potential existed for workers to be in
    portions of the RCA without knowing the radiological conditions. On October 7th
    and 8th, the inspectors conducted a random survey of workers located in the
    general areas of the primary auxiliary building, especially the transit path to the
    containment personnel hatch, and inside the containment, in the outer annulus
    regions. None of the ten workers interviewed could identify the radiological
    conditions in the areas they were standing in or had walked through. None of the
    workere could identify their nearest ALARA low dose waiting area. The inspectors
    further noted that workers failed to review the radiological survey maps placed at
    the two main RCA entrances, as required by their RWPs. Further, the inspectors
    noted that a number of the posted survey maps at the RCA access points were
    outdated and did not accurately reflect current plant conditions. Failure of workers
    to follow instructions contained in their RWPs is a violation of TS 6.8.1.a, which
    requires that written procedures and instructions be established, implemented and
    maintained regarding radiation protection procedures. (VIO 50 334/97-08-04).
    On two separate occasions, the inspectors observed workers in the containment
    who appeared to be unaware of their surroundings. One worker was observed lying
    on the floor on the 692' elevation next to a desk and chair at the health physics
    control point for that level, while another was outside the "C" steam generator
    cubicle on the 718' elevation. Neither location was a designated low dose waiting
    area. Both workers had their eyes closed, and did not open them cr notice the
    inspector until just as the inspector passed them. The inspector notified plant
    supervisors of his observations, and his concern that personnel, not actively
    engaged in work in the RCA, should be outside the RCA or in posted ALARA low
    dose waiting areas. The first example was subsequently documented in a plant
    condition report.
    During tours of the containment, the inspectors noted generally poor radiological
    housekeeping. The same observation was made by the plant Health Physics
    Manager, who stressed the importance of this issue at a morning management
    meeting attended by the inspectors. By the end of the specialist inspection,
l  housekeeping had improved but was still considered poor.
!
!
                                              .
 
  _ . . _ _ _ .    _ _ _            _= _ ..          .___          .      _ ..___. _ _ _          . _ _ . .      _ . _ _ ._
        .
.
          .
                                                                    21
                          The inspectors also reviewed the license's most recent results from the National
                          Voluntary Laboratory Accreditation Program (NVLAP) of its thermoluminescent -
                          dosimetry program. During NRC Inspection Report 50 334 and 412/97-02, the
                          inspectors noted that the licensee had failed test criteria 1, Accideni ' ow Energy
                          Photon. Since that time the licensee has resubmitted 15 test dostw/.ers, five per
                          month for three months, and has received a passing grade from NVLAP.
                  c.      Conclusions
                          Generally effective radiological controls were in place for the refueling outage,
                          especially for the control of work in high and locked high radiation areas. However;
                          radiological housekeeping was poor, some posted survey maps of the RCA were out
                          of date, and two workers were observed in the RCA who were not aware of their
                          surroundings. One violation of NRC requirements was also identified concerning
                          workers failing to follow the RWP requirement to review the applicable survey maps
                          of the RCA prior to entry.
                R2        Status of RP&C Facilities and Equipment
                R2.1      Calibration of Effluent / Process / Area / Accident Radiation Monitorino Svstems (RMS)
                  a.      Insoection Scope (84750)
,
                          The inspector reviewed the most recent radiological and electronic calibration
                          results and calibration procedures for the effluent / process RMS. The inspector also
                          held discussions with Health Physics and instrumentation and Controls staff, and
                          the RMS System Engineer.
                          The inspector utilized the following documents as a basis to determine whether the
                          calibration procedures contained sufficient detail and guidance to verify conversion
                          factors (calibration factors) and monitoring capability for the intended range
                          (linearity):
                          o        Regulatory Guide 1.21, " Measuring, Evaluating, and Reporting Radioactivity
                                    in Solid Wastes and Releases of Radioactive Materials in Liquid and Gaseous
                                    Effluents from Light Water Cooled Nuclear Power Plants, February 1979"
,                        o        Regulatory Guide 4.15, " Quality Assurance for Radiological Monitoring
                                    Programs (Normal Operations)- Effluent Streams r, rid the Environment.
                                    February 1979"
                            e      ANSI N42.18,1980, " Specification and Performance of On-Site
                                    Instrumentation for Continuously Monitoring Radioactivity in Effluents"
                            e      EPRI TR-102644, " Calibration of Radiation Monitors at Nuclear Power r)lants,
                                    March 1994"
                                                            _  -_
                                                                      . - .      -        . -  -              - .-            --
 
  - - - - . ..        .  _- -. - - .                  .          .    . .    . . -  --      .-_  .        . _ . . .-
  4
  .
                                                                    22                                                  .
                                                                                                                        !
                      *-          Victoreen Installation, Operation, and Maintenance Instruction Manual Beta
                                                                                                                        '
                                    Scintillation Detectors Models 843 20,843 20A, and 843 20B            *
                      *            Victoreen Instruction Manual Gamma Scintillation Detector Model 843 30              l
                      The following Unit 1 RMS were reviewed.
                      *            Liquid Waste Effluent
                                                                                                                        '
                      *            Component Cooling Recirculation Spray Heat Exchange
                      *            Process Vent Noble Gas
                      *            Auxiliary. Building Noble Gas
                      *            Supplementary Leak Collection Noble Gas
                      *            Containment Air
.                    *            Containment Purge
                      The following Unit 2 RMS were reviewed.
                      *            Liquid Waste Effluent
                      *            Ventilation System Noble Gas
                      *            Elevated Release Noble Gas
                      *            Decontamination Building Noble Gas
                      *            Waste Gas Storage Vault
                      *            Condensate Polishing Building Noble Gas
'
                      *            Containment Purge Noble Gas
                  b. Observations and Findinas
                      Electronic calibrations were appropriate. Linearity checking was appropriate. Good
                      tracking and trending of the RMS was noted. The inspector noted that despite the
                      age of RMS, reliability has been good. There were few open work orders at the
                      time of the inspection.
                      The inspector did note that the licensee typically used supervisory discretion
                      (permitted by procedure) rather than using the detailed guidance within the Health
                      Physics Department procedure 5.11 for establishing a high voltage setting. Of the
                      22 channels of RMS reviewed, only 3 channels met EPRI guidance for establishing
                      the operating high voltage. The inspector noted that the practice was contrary to
                      existing standards and industry guidance documents.
                      RM-1RM 215A (Unit 1 containment particulate; Victorcen detector type 843-20A)
                      operating voltage was established at 650 volts. Per licensee calibration data, the
4                    percent change over 50 volts at 650 volts on a operating voltage vs. count rate
                      curve was 365% The inspector noted that the vendor instruction manual directed
                      the user to generate a plateau curve and noted that at 1100 volts the count rate
                      should reach the lower end of the plateau. Contrary to the vendor instruction
                      manual and the above noted guidance documents that operating high voltage be set
                      on the plateau, the licensee established operating high voltage by changing high
              . _~-                      -        .        -,
 
    . ..-. . - -- --- - - . .                                        _- . -. . - - ..-.-. - ~ ~ ..                                -
                                                                                                                                  -          .- -    --
    .
,
                                                                                                                                                          I
                                                                                                                                                          4
3
                                                              23
            - voltage to a point at.which actual counts equalled expected counts with a National
              Institute of Standards and Technology (NIST) traceable source.
              RM 1LW-104 (Unit 1 liquid waste effluent; Victoreen detector type 843 30)
              operating voltage was established at 450 volts. Per licensee calibration data, the
              percent change over 50 volts at 450 volts on a operating voltage vs. count rate
              curve was 133% The inspector noted that the vendor instruction manual
              specifications for operating voltage were 500 to 1400 volts. The inspector also
              noted that the vendor manual recommended that the operating high voltage be
              established by generating a signal to noise ratio curve and setting high voltage to
              the peak value on the curve (this method is also described in EPRI TR 102644).
              Contrary to the vendor instruction manual and the above noted guidance
              documents, the licensee established operating high voltage by changing high -
              voltage to a point at which actual counts equalled expected counts with a NIST                                                              !
              traceable source.
              TS 6.8.1.a requires, in part, that written procedures shall be established,
              implemented, and maintained covering the activities recommended in Appendix A of
              Regulatory Guide 1.33 (RG 1.33), Revision 2, February 1978. Appendix A of the
              RG 1.33, " Typical Procedures for Pressurized Water Reactors and Boiling Water
              Reactors," describes typical procedures for the control of radioactivity, including
              procedures involving radiation monitoring systems.
              Contrary to the above, the licensee failed to establish adequate RMS calibration
              instructions in regard to determining RMS operating high voltage. Specifically,
              operating high voltage was not established on a plateau for RM 1RM 215A (Unit 1
              Containment Particulate) and RM 1LW-104 (Unit 1 Liquid Waste Effluent). This was
              contrary to vendor manual "Victoreen Installation,- Operation, and Maintenance, ~
              Instruction Manual Beta Scintillation Detectors Models 843 20, 843-20A, and 843-
              20B" and "Victoreen instructional Manual Gamma Scintillation Detectors Model
              843-30" respectively; and was contrary to RMS calibration standards and industry
              guidance documents. This is a violation of NRC requirements (VIO 50-334/97-08-
              05).
              In reviewing as found and as left high voltages for the above noted RMS calibrations
            - and a synopsis of similar data provided by the RMS Health Physicist, the inspecte."
              noted that typically there was little if any high voltage drift. In one case, a drift of
              30 volts was noted. For this particular RMS, the operating high voltage had been
              set close to the plateau and, as a result, this relatively large drif t in operating high
              voltage had very little impact on the accuracy of RMS output. While the technique
              used to establish operating high voltage was technically deficient, the inspector did
              not identify any case in which high voltage drift had led to error such that the
              validity of data provided in the annual effluent report was questionable. During the
              inspection and at the exit meeting, licensee representatives indicated that prior to a
              planned batra release a sample is taken, thereby providing a check on RMS
              operability.
.
                                                                                                                                                          f
  _                                                                                                                                    ,
                              ,, .,                m..,,,,,,,, ,,1,,            -                  g 9__p 7..
                                                                                                              ,.
                                                                                                                9__,,_. ., ,,9,,.  ,.- , . ,      ,,
 
  .
                                                                                                ]
                                                    24
            The inspector questioned the licensee as to whether they could provide any
            information pertaining to new/ refurbished detector failures. The Health Physics      I
            Marager informed the inspector that if BVPS identified a faulty detector, it was      I
            replaced; but, the f ailure cause may not be documented. This matter will be          l
            reviewed further (IFl 50-334/97 08-06).
      c.  Conclusion
            RMS reliability has generally been good. Electronic alignment and linearity checking
            were good. The inspector noted that the licensee had failed to implement industry
            guidance (EPRI TR 102644 and ANSI N42.18) which specifically direct that the
            operating voltage be set on a plateau and, in two cases, had failed to implement
            vendor manual instructions for establishing operating high voltage. The inspector
            concluded that this was a poor calibration practice which has the potential for      ,
            leading to instrument error. Instrument error could impede or prevent an accurate
            assessment of public exposures and environmental impact in the case of an
            inadvertent release of radioactive materials.
      R2.2 Air Cleanino Systems
      a.  Insoection Scoco (84750)
            The inspectors reviewed the licensee's most recent surveillance test results,
            including visual inspections, in-place High Efficiency Particulate Air (HEPA) leak
            tests, in-place charcoal leek tests, air capacity tests, pressure drop tests, and
            laboratory tests for the iodine collection efficiencies for the Supplementary Leak
            Collection and Release Systems (SLCRS).
      b.  Observations and Findinas
            All test results were within the licensee's acceptance criteria. No procedural
            inadequacies were noted. Unsatisfactory test results were analyzed and corrective
            actions were implemented in a timely manner. The inspectors noted that attention
            given to the air cleaning systems was good. System Engineers monitored and
            trended the performance of the air cleaning systems.
      c.  Conclusions
,
t
!
'
            Those portions of the test program reviewed were wellimplemented with strong
            monitoring and trending of air cleaning system performance parameters.
      R5    Staff Training and Qualification in RP&C
l
      a.  Insoection Scone (83750)
    +
            The inspectors reviewed the qualifications of 23 contractor health physics
            technicians to ensure they were appropriately classified as junior or senior
            technicians. The records were selected by the inspectors at random.
 
        ._ _ _ _ _ _ _ . _ _ _ . . _ _ _
                                      _                                                                                                      _ _ _ _ _ ___.. _ ._.. _ .. _ _
            .
                                                                                                                                                                                                                                              :
                                                                                                                                                                                                                                              t
                                                                                                                                    25                                                                                                        ,
                                                                                                                                                                                                                                              i
  >
                                          b.          Observations                                                                                                                                                                            l
                                                                                                                                                                                                                                              8
                                                      The licensee hired 86 contractor health physics technicians (66 senior and 20
                                                    junior) in ordet to support the Unit 1 refueling outage. The inspectors selected 23                                                                                                      i
                                                      records at random and reviewed the licensee's calculations for technician                                                                                                                !
                                                      experience. All calculations reviewed were determined to be appropriate, and in
                                                      general, the inspectors determined that the licensee was conservative in reviewing
                                                      technician qualifications.                                                                                                                                                              ,
                                        c.          Conclusions
,
                                                    The licens9e appropriately classified contractor health physics technicians with
                                                                                  ~
                                                                                                                                                                                                                                            'l
                                                      regards to previous experience.
                                    . R7              Quality Assurance (QA)in RP&C Activities                                                                                                                                                ,
                                        a.          Inspection Scope (84750)
'
                                                    The inspection consisted of: (1) review of the 1996 Quality Services Unit (OSU)-
                                                      audit of the Site Radiological Effluent and Environmental Monitoring Programs, (2)                                                                                                      '
                                                      QSU surveillances and (3) self assessments.
                                        b.          Observations and Findinas
                                                    Audit team members included a technical specialist from another utility. The depth
>
                                                    of the audit was good. The audit team identified several minor discrepancies and
                                                    matters for enhancing the radioactive liquid and gaseous effluent control programs..
                                                    No items were of regulatory significance.                                                                                                                                                l
!                                                    Surveillances and self assessments were also well-targeted arcl helped to augment
                                                    the audit.~
!
                                        c.          Conclusion
                                                    This program area was wellimplemented.
                                    L1              Review of FSAR Commitments
l
l_                                                  - While performing the inspections discussed in this report, the inspectors leviewed
'
                                          -
                                                    the applicable parts of the UFSAR that related to the areas inspected. The
                                                    inspectors verified that the UFSAR wording was consistent with the observed plant
                                                    practices, procedures and/or parameters.
                                                                                                                                                                                                                                              .
    .,.,_,_w.,_,,._,,._~                    ---,.y.    , , , , _ . , . , , . . ,  _m., . . , , , ,v,.. ...,,,--,....~,_...J.,',,-
                                                                                                                                _
                                                                                                                                    ,,,__,m_,                  ,. , , , , . _ , _ .. ., , , , . . . .,., _. . , .., , , . . . . .___,__ _ _
 
  __ .      _ _ - . - _ _ _. __                ._      _ . _ - . - - _ . _ . _ . - . . _ . - - _ - _ _ . __                      _ _ . _ _ _ . _
      .
                                                                                                    26
                                                                          V. Mananoment Meetinas
                          X1          Exh Meeting Summery
                          The inspectors presented the results of the radiation protection and radioactive effluent                                      ~i
                          control inspections to Mr. R. Vento on October 10,1997. The results of the ISl program
                          inspection were presented to Mr. S. Jain and Mr. R. LeGrand on October 24. The licensee
                            acknowledged the findings presented. After further in office review of information
                          pertaining to the RMS calibration, the inspector concluded that a violation of NRC
                          requirements had occurred.                                                                                                        '
                          The inspectors conducted an interim exit with Mr. S. Jain on November 10,1997, to
                          discuss the apparent violation documented in this report. The inspectors presented the
                          remainder of the inspection results in a meeting with Mr. J. Cross and members of his staff
                          at the conclusion of the inspection on November 21,1997. The licensee acknowledged                                                i
                          the findings presented with one exception,                                                                                        i
                                                        .                                                        -
                                                                                                                                                            ;
                                                                                                                                                            '
                          The licensee disagreed with the NRC's position that venting the HHSl pumps immediately
                          prior to surveillance test preconditioned the pumps. The licensee stated that the purpose                                        ,
                          of venting the suction lines on the HHSl pumps prior to surveillance testing was to ensure
                          long term reliability of the pumps. The venting was not performed to create an enhanced                                          l
                          test environment.~ The licensee stated that venting the pump would not change the                                                <
                          environment such that it could be considered preconditioning.
;                          The inspectors asked the licensee whether any materials examined during the inspection
!
                          should be considered proprietary. No proprietary information was identified.
                          X2        Pre-Decisional Enforcement Conference
                                                                                                                                                            '
                          The pre-decisional enforcement conference referred to in NRC Inspection Report 50-334
                          and 50-412/97 07 has been scheduled for December 10 at the NRC Region i office to                                                3
                          discuss the apparent violation documented in that report and URI 50 334 and 412/97-08-                                            ,
                          03 of this report.
                                                                                                                                                            i
                                                                                                                                                            1
                                                                                                                                                            E
'
                                                                                                                                                          .i
i
:
!
l
        _ .. -_                _ . _ .  -,    _ _ .        - . . - . - . - . _                .          ._  _- ._ .~_-__,_.-      - _ ,._- _ - _ .
 
  .. . . -.          .          .  . .        --  - - - .        - . . - - _ - _ . - - - - - .                  . - -- .
4
-
                                                                                                                                        !
                                                              27                                                                          ,
                                                                                                                                        '
                                      PARTIAL. LIST OF PERSONS CONTACTED
            QLG
            J. Cross, President,' Generation Group                                                                                      ,
            R. LeGrand, Vice President, Nuclear Operations / Plant Manager
            S. Jain, Vice President, Nuclear Services
            M. Pergar, Acting Manager, Quality Services Unit
            B. Tulte, General Manager, Nuclear Operations
            R. Hansen, General Manager, Maintenance Programs Unit
            R. Vento, Manager, Health Physics
            D. Orndorf, Manager, Chemistry
            F. Curl, Manager, Nuclear Construction
            J. Matsko, Manager, Outage Management Department
            T. Lutkehaus, Manager, Maintenance Planning & Administration
          .T. McGhee, Coordinator, Onsite Safety Committee
            Ji Macdonald, Manager, System & Performance Engineering
            K. Beatty, General Manager, Nuclear Support Unit
            J. Arias, Director, Safety & Licensing
            W. Kline, Manager, Nuclear Engineering Department
            R. Brosi, Manager, Management Services
            O. Arredondo, Manager, Nuclear Procurement
            NBC
            D. Kern, SRI
            G. Dentel, Ri
            F. Lyon, RI -
                                                                                                                                        ,
                                          - - ,.  -            -.-.-,.ur              --          , ,w ~, . m -- w,,    y  --~ ~ - ~
 
-. - . - - . . . .-.                        -            _ _= - - - - - ._-_.-- - -.--                                              ._        .-. - - - -_                                        _-_ .
      4
                                                                                                                                                                                                        .
!                                                                                                        28                                                                                            !
                                                                                    INSPECTION PROCEDURES USED
                                                                                                                                                                                                        .
                              IP 37551:                      Onsite Engineering
                              IP 61726:                      Surveillance Observation
                              IP 62707:                      Maintenance Observation                                                                                                                    l
                              lP 71707:                      Plant Operations                                                                                                                            .
                              IP 71750:-                    Plant Support                                                                                                                              !
                                                                                                                                                                                                        !
                              IP 73753:                      Inservice inspection
                              IP 83750:                      Occupational Exposure
                              IP 84750:                      Radioactive Waste Treatment, and Effluent and Environmental
                                                              Monitoring
                              IP 92700:                      Onsite Follow up of Written Reports of Nontoutine Events at Power                                                                          ;
                                                              Reactor Facilities
                              IP 92901:                      Follow up - Operations
                              IP 92902:                      Follow up - Maintenance                                                                                                                    i
                              IP 92903:                      Follow up - Engineering
;
,
t
4
                                                                                                                                                                                                        ,
    ,      . . . . . . - . -,      w..-..,  , - - . - .          _-,..-,.,._,.,r,.  . . , . - + . , - . , , , e. - . . . . . , ,m    ,..,-,    ,yy. , , , ,.i,.r - ,,-,,_,nm,-ry,.m..,pg,.--yy
 
                  .      . _ . _ _ _ _ _ _    _.  _ _ - _ - _ . _ _ _                        _ _ _ _ _ _ . . _ _ _ _ _ _ . _ - - _ _ _ . _ _ _
            .-
            .
                                                                                29                                                                            i
                                                                                                                                                              ~
                                              ITEMS OPENED, CLOSED AND DISCUSSED
>
                    Ooened
                    50 412/97 08-03              URI              Test Control High Head Safsty injection Pumps
                                                                      (Section E2.1)
                                                                                                                                                              !
                    50-334/97-08-04              VIO              Workers were Unaware of Radiological Conditione in                                        i
                                                                    their Work and Transit Areas in the RCA (Section R1)
                    50 334/97 08-05              VIO                Failure to Calibrate RMS in Accordance with Propor
                                                                    Procedures (Section R2.1)
                                                                                                                                                              ,
                    50 334/97 08-06              IFl              Documentation of RMS Detector Failures (Section R2.1)                                    ,
                    Ooened/ Closed
                    50 334/97 08 01              NCV Mispositioning of RCCA in the SFP (Section 01.2)
                    50 334 and 312/97 08 02 NCV implementation of the Retired Equipment Program
                                                                    (Section 03.1)
                    Closed
                    50 334/96-012                LER              Entry into Technical Specification 3.0.3 Due to Isolation
                                                                    of Control Room Emergency Breathing Air Pressurization
                                                                    System (Section 08.1)
                    50 334/97-004-01              LER              Failure to Test Post DBA Hydrogen Control System
                                                                    Recombiners in Accordance With Technical
                                                                    Specifications (Section 08.2)                                                            ,
i
!
                    50 334/97-032                LER              EDG Automatic Start During Bus Transfer from Unit to
                                                                    System Station Transformer (Section 08.3)
                    50 334 and 412/97-07 04 URI                    Adequacy of the High Head Safety injection Pump
!                                                                    Surveillance Tests to Ensure Operability (Section E2.1)
                    50 334/96-05 02              VIO              Inadequate Calibration for UT examinations
,
                                                                    (Section E8.2)
                    50 334 and 412/97-07-01 URI                    implementation of the Retired Equipment Program
                                                                    (Section 03.1)
i
  . _ - . _ _ , _-                _ _ .      _
                                                      . _ _ _ _ . _ . _ .        __ _ _ .. _- _                                  _ _ - - . .    . _. __ _ _
 
                . - -              - -          - . . . -    -    _ . .          _      _ _ . ~ - - -      - - - .                  .. - -
                                                                                                                                                  l
                                                                                                                                                  1
              *
              .
                                                                                      30
                                                                LIST OF ACRONYMS USED
                      1R12                  Unit 112th Refueling Outage
                      AFW                    Auxiliary Feedwater Pump
                      ALARA                  As Low As is Reasonably Achievable
                      ANil                  Authorized Nuclear Inservice inspector
                      AOP                    Abnormal Operating Procedure
                                                                                                                                                l
                      AVB                    Anti Vibration Bar                                                                                  i
                                                                                                                                                  '
                      BVPS                  Bebver Valley Power Station
:                      CR                    Condition Report
                      CREBAPS                Control Room Emergency Breathing Air Pressurization System
                      DCP                    Design Change Package
                      DLC                    Duquesne Light Company
                      EDG                    Emergency Diesel Generator                                                                        ,
                      eel                    Est stated Enforcement issue                                                                      ,
                      EOP                    Emergency Operating Procedure
                      .ESF                    Engineered Safety Feature
                      HEPA                  High efficiency Particulate Air
                      HHSl                  High Head Safety injection
                      l&C                    Instrumentation and Controls
                      ISI                    Inservice Inspection                                                                              '
                      IST                    Inservice Surveillance Test
                      LER                    Licensee Event Report
                      MPFF                  Maintenance Preventable Functional Failures
                      MSP                    Maintenance Surveillance Procedure
                      MT                    Magnetic Particulate
                      NCV                    Non-Cited Violation
                      NDE                    Nondestructive Examination
                      NIS                    Nuclear Instrumentation System
                      NIST                  National Institute of Standards and Technology
                      NPDAPS                Nuclear Power Division Administrative Procedure                                                  ,
                      NVLAP                  Nuclear Voluntary Laboratory Accreditation Program
                      ODCM                  Offsite Dose Calculation Manual
                      ODSCC                  Outside Diameter Stress Corrosion Cracking
                      OST                    Operational Surveillance Test
                      PCE                    Personnel Contamination Event
                      PDR                    Public Document Room
                      PMP                    Preventive Maintenance Procedure
                      PT                    Liquid Penetrant
                      PWSCC                  Primary Water Stress Corrosion Cracking
                      QA                    Cuality Assurance
                      OC                    Quality Control
                      OSU                    Quality Services Unit
                      RCA-                  Radiological Controlled Area
                      RCCA                  Rob Jiuster Control Assembly
                      RMS                    Radiation Monitoring System
                      RP&C                  Radiological Protection and Chemistry
                      RTS                    Reactor Trip System
  . . _ _ _ _ _ _ .      _ _ . _ _    _ _ _.              __            _ _ . _ _      __          .- . . . _
                                                                                                                        . _ _ , _ _ _ _ , _
 
.
.
                                        31
    RWP    Radiological Work Permit
  :SFP    Spent Fuel Pool
    SG    Steam Generator
    SLCRS _ Supplementary Leak Collection and Release System
    SSPS-  Solid State Protection System
    TER  ~ Technical Evaluation Report
  -TS    = Technical Specification
    TSP    Tube Support Plate
    TTS    Tubesheet
    UFSAR  Updated Final Safety Analysic Report
    URI    Unresolved item
    UT    Ultrasonic Examination
    VIO    Violation -
    VT'    Visual Examination
                                                                  ,
                                                                    ,
                                                            - . _
}}
}}

Latest revision as of 23:36, 31 December 2020

Insp Repts 50-334/97-08 & 50-412/97-08 on 971005-1115. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20203D742
Person / Time
Site: Beaver Valley
Issue date: 11/26/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20203D715 List:
References
50-334-97-08, 50-334-97-8, 50-412-97-08, 50-412-97-8, NUDOCS 9712160278
Download: ML20203D742 (36)


See also: IR 05000334/1997008

Text

_ . - . . _ ._ . ...

,

t

... _

'*

U. S. NUCLEAR REGULATORY COMMISSION

~ REGION I

e

. License' Nos. DPR 66,' NPF-73

Report Nos. 50-334/97-08, 50-412/97-08'

Docket Nos. 50-334, 50-412

Licensee: Duquesne Light Company-(DLC)_ ,

Post Office Box 4  :

Shippingport, PA 15077

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i- Facility: - _

Beaver Valley Power Station, Units 1 and 2

Inspection Period: October 5,1997 through November 15,1997

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' inspectors: D. Kern, Senior Resident inspector -

F. Lyon, Resident inspector

G. Dentel, Resident inspector

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J. Furia, Senior Radiation Specialist, DRS

L. Eckert, Radiation Specialist, DRS

S. Chaudhary, Senior Reactor Engineer, DRS

Approved by: P. Eselgroth, Chief

Reactor Projects Branch 7

9712160278 971126

PDR- ADOCK 05000334

R PDR

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EXECUTIVE SUMMARY

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Beaver Valley Power Station, Units 1 & 2

NRC Inspection Report 50-334/97-08 & 50 412/97-08

This integrated inspection included aspects of licensee operations, engineering,

maintenance, and plant support. The report covers a 6-week period of resident inspection;

in addition, it includes the results of announced inspections by regional inspectors in the

areas of radiation protection, rt riioactive effluent control, and inservice inspection.

Operations

  • Rod cluster control assembly (RCCA) R-19 was mispositioned during insert change-

outs due to inadecuate position verification by contractor personnel and inadequate

supervisory oversight of the evolution by DLC staff, inspectors assessed that the

licensee root cause analysis for the RCCA mispositioning was thorough and that

DLC took reasonable corrective actions to prevent recurrence. (Section 01.2)

out-of-service, even though the equipment was required in some emergency

response procedures, was an isolated instance due to inadequate review and

implementation of the Retired Equipment Program. (Section O3.1)

  • Operators demonstrated a strong questioning attitude in identifying a longstanding

discrepancy in the auxiliary feedwater surveillance test. (Section 04.1)

  • Operators' failure to question the acceptability of charging pump gas accumulation-

data and lack of system engineering guidance was a weakness. (Section 04.1)

testing was conservative, and operator response in the control room to the loss of

the EDG was appropriate, inspectors noted good control of event response by

control room supervisors. (Section M1.3)

Maintenance

  • Poor work practices resulted in a fuel filter leak during EDG testing and a thrust

bearing failure during post maintenance testing on an auxiliary feedwater pump.

The licensee appropriately dispositioned the failures in accordance with the

Maintenance Rule. (Sections M1.2 and M1.3)

Enaineerina

e The licensee's review and corrective actions adequately addressed the inadvertent

actuation of the Control Room Emergency Breathing Air Pressurization System

(CREBAPS) on October 6,1996. The CREBAPS Focused Design Review conducted

in response to the event was a thorough evaluation of the system and provided

good recommendations for resolving the longstanding problems. However, the

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long-term action to eliminate the spurious activation of this engineered safety

features system has not been implemented yet, showing a slow response on the

licensee's part to resolve the longstanding operator work-around. (Section 08.1)

e Engineers determined that under certain con % ions the voltage supplied to the

Unit 1 nuclear instrumentation system power supplies could potentially adversely

affect the reactor trip system protective action functions. Engineers' performance

during assessment of this issue and extent of condition reviews was conservative

and demonstrated a strong questioning attitude. Corrective actions, including

design change implementation, were timely and technically sound. (Section E1.1)

  • The licensee's team evaluating the gas binding events for the Unit 2 High Head

Safety injection (HHSI) pumps uncovered weaknesses in the original engineering

analysis performed to establish venting frequencies. Strong questioning by licensee

management and team members led to these findings. The venting frequency

established in 1988 to ensure minimal gas accumulation in the suction lines was

inadequate to prevent gas binding of the Unit 2 HHSI pumps. The inadequate

corrective actions to preclude gas binding of the pumps were addressed in NRC

Inspection Report 50 334 and 412/97-07. Further, the inspectors determined,

venting of the HHSI pump suction lines immediately prior to TS surveillances may

be a violation of NRC requirements pertaining to test validity and is unresolved.

(Section E2.1)

e The licensee's inservice inspection program plan for Unit 1, with relief requests,

was satisfactorily maintained and implemented. The non-destructive examination

personnel were properly qualified and certified, examination procedures were

adequate to assure valid examinations, and deficiencies were appropriately

evaluated and resolved. The new data management software appeared to be

effective. (Section E8)

Plant Sucoort

  • The program for control of radiological work during the Unit 1 refueling outage was

generally effective; however, one violati< of NRC requirements was identified

regarding radiation worker knowledge of radiation levels in their work and transit

areas. (Section R1)

  • Overall, the radioactive liquid and gaseous effluent control programs were good.

The Radiation Monitoring System (RMS) reliability was adequate; however, a

violation pertaining to RMS calibration practice was noted. (Section R2.1)

  • The ventilation system surveillance program for radioactive effluent control was

well implemented. (Section R2.2)

e Good quality control and quality assurance programs were established for

radi active effluent control. (Section R7)

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TABLE OF CONTENTS

EX EC U TIV E S U M M A RY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii

TAB LE O F C O NT E NT S . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv

1. Operations .................................................... 1

O1 Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01.1 General Comments (71707) . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

.................................................... 1

02 Operational Status of Facilities and Equipment . . . . . . . . . . . . . . . . . . . 3

02.1 Engineered Safety Feature System Walkdowns (71707) . . . . . . . 3

03 Operations Procedures and Documentation (92901) . . . . . . . . . . . . . . . 3

03.1 (Closed) Unresolved item 50-334 and 412/97-07-01 ......... 3

04 Operator Knowledge and Performance . . . . . . . . . . . . . . . . . . . . . . . . . 4

04.1 Questioning Attitude of Operators . . . . . . . . . . . . . . . . . . . . . . . 4

08 - Miscellaneous Operations issues . . .......................... 5

-08.1 (Closed) Licensee Event Report (LER) 50-334/96-012 . . . . . . . . . 5

08.2 (Closed) LER 50-334/97 004-01 (92901) . . . . . . . . . . . . . . . . . . 7

08.3 (Closed) LER 50-334/97-032 (92901) . . . . . . . . . . . . . . . . . . . . 7

11. M a i nt e n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

M1 Conduct of Maintenance .................................. 7

M 1.1 Routine Maintenance Observations (62707) . . . . . . . . . . . . . . . . 7

M1.2 Routino Surveillance Observations (61726) ................ 8

M1.3 Leak on Unit 1 EDG Fuel Oil Filter (71707, 92902) . . . . . . . . . . . 9

111. E ng i n e e ri n g . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

El Conduct of Engineering ................................... 9

E1.1 Vital Bus Voltage Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

E2 Engineering Support of Facilities and Equipment . . . . . . . . . . . . . . . . . 11

E2.1 (Closed) Unresolved item (URI) 50-334 and 412/97-07 04 .... 11

E8 Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

E8.1 Inservice Inspection . . . . . . . . . . . . . . . . . . . . . . . . . . ..... 14

E8.2 (Closed) VIO 50-334/96-05-02 (92903) . . . . . . . . . . . . . . . . . . 18

IV . Pl a n t S u p p o rt . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

R1 Radiological Protection and Chemistry (RP&C) Controls . . . . . . . . . . . . 19

R2 Status of RP&C Facilities and Equipment . . . . . . . . . . . . . . . . . . . . . . 21

R2.1 Calibration of Effluent / Process / Area / Accident Radiation

Monitoring Systems (RMS) . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

R2.2 Air Cleaning Systems .............................. 24

R5 Staff Training and Qualification in RP&C . . . . . . . . . . . . . . . . . . . . . . 24

R7 Quality Assurance (QA) in RP&C Activities . ................... 25

L1 Review of FS AR Commitments . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25

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Table of Contents

V. Ma nag em e nt Meeting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26

X1 Exit M e eting Summ ary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26

X2 Pre-Decisional Enforcement Conference . . . . . . . . . . . . . . . . ...... 26

PARTI AL LIST OF PERSONS CONTACTED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

INSP?.CTIO N PROCEDURES U SED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

ITEMS OPENED, CLOSED AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . _ 29

LI ST O F A C R O N Y M S U S E D . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30

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Report Details

Summary of Plant Status

Unit 1 began this inspection period in Mode 6 (refueling) for the 12th refueling outage. On

October 10, the reactor vessel was defueled. On October 20, fuel reloading commenced

and the unit re-entered Mode 6. On October 29, the reactor vessel head was tensioned

and the unit entered Mode 5 (cold shutdown).

Unit 2 operated at 100% power this inspection period.

l. Operations

01 Conduct of Operations

01.1 General Comments (71707)'

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations, in general, the conduct of operations was professional

and safety-conscious; specific events and noteworthy observations are detailed in

the sections below.

01.2 ffiscositioned Rod Cluster Control Assembiv (RCCA)

a. insoection Scone (92901)

Inspectors reviewed the licensee root cause analysis for the mispositioning of an

RCCA in the spent fuel pool. The review included interviews with selected staff -

and managers, and review of applicable refueling procedures, Nuclear Power

Division Administrative Procedures (NPDAPs) regarding vendor services, work

location conditions, and corrective actions,

b. Observations and Findinas

During RCCA eddy current testing and insert change-outs on October 12, RCCA R-

19 was incorrectly inserted into spent fuel pool (SFP) rack location M107 instead of

N107 following removal from the eddy current test stand. The RCCA movements

were being performed in accordance with Refueling Procedure Book 111 - 1RP-12R-

3.22, " Insert Changeouts, Reposition Fuel Assemblies, and Assembly Verification in

Spent Fuel Pit."

Movement of the RCCAs was conducted by two contractor personnel, a SFP bridge

operator and a spotter, and a DLC refueling engineer assistant. Shortly after the

' Topical headings such a 01, M8, etc., are used in accordance with the NRC

standardized reactor inspection report outline. Individual reports are not expected to

address all outline topics.

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movement of RCCA R 19 to its post-inspection location in the SFP, the bridge

operator realized that it had been moved to the wrong location. Contractor

supervision, the nuclear shift supervisor, and the DLC Refueling Supervisor were

immediately notified. A fuel assembly handling deviation report was prepared and

approved in accordance with procedure and R-19 was moved to its proper location.

if the positioning error had not been recognized by the bridge operator, refueling -

procedures contained additional checks later in the process which would likely have

caught the error.

DLC senior management learned of the mispositioned RCCA two days afterward

when Condition Report 971817 was reviewed during processing. All assembly,

insert, and tool movement was halted until an investigation was completed and

corrective actions were put in place to prevent recurrence. The DLC root cause

analysis highlighted the following deficiencies:

1. Poor self-verificction techniques were used by the contractor personnel.

Contributing factors were poor lighting on the index rail and the light blue

color of the lettering.

2. The refueling assistant did not perform independent verification of RCCA

position. The refueling assistant had no formal training and there was no

pre-evolution briefing.

Corrective actions for the mispositioning of R-19 included: changes were made to

enhance the refueling procedures, a formal training program was initiated for

refueling engineer assistants, the lighting was improved at the index rails, and an

ISEG review of the event was initiated.

Inspectors also reviewed the vendor oversight requirements of NPDAP 9.8, Rev.4,

" Request for Contracted Services," and the current Rev.5, and assessed that the

mispositioning did not involve a programmatic concern with vendor control. The

root cause analysis and recommended corrective actions were presented to the

Nuclear Safety Review Board. The inspectors noted that having the Plant Manager

present the analysis and recommended corrective actions diminished the

independence of the NSRB review and subsequent recommendations to the Plant

Manager. Inspectors assessed that the licensee root cause analysis for the RCCA

mispositioning was thorough and that DLC took reasonable corrective actions to

prevent recurrence.

TS 6.8.1.a requires that, " Written procedures shall be established, implemented,

and maintained covering...the applicable procedures recommended in Appendix "A"

of Regulatory Guide 1.33, Revision 2, February 1978." Regulatory Guide 1.33

includes procedures for refueling. Mispositioning RCCA R-19 was a failure to

implement refueling procedure 1RP-12R-3.22 and was a violation of TS 6.8.1.a.

This non-repetitive, licensee identified and corrected violation is being treated as a

Non-Cited Violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy

(NCV 50-334/97-08-01).

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c. Conclusion

RCCA R-19 was mispositioned during insert change-outs due to inadequate position

verification by contractor personnel and inadequate supervisory oversight of the

evolution by DLC staff. The misposition was immediately recognized by the

personnel involved and immediate corrective actions were taken to move the RCCA

to its correct position, inspectors assessed that the licensee root cause analysis for

the RCCA mispositioning was thorough and that DLC took reasonable corrective

actions to prevent recurrence.

O2 Operational Status of Facilities and Equipment

O2.1 Enoineered Safety Feature System Watkdowns (71707)

The inspectors walked down accessible portions of selected systems to assess

equipment operability, material condition, and housekeeping. Minor discrepancies

were brought to DLC staff's attention and corrected. No substantive concerns were

identified. The following systems were waWed down:

e Unit 1 Containment

03 Operations Procedures and Documentation (92901)

03.1 (Closed) Unresolved item 50-334 and 412/97-07-01: Retired Equipment Program

Inspectors reviewed the Retired Equipment Program following the licensee discovery

that some equipment was tagged as " retired in place" that was required for use in >

emergency operating procedures. The issue and the licensee's immediate corrective

actions were documented in NRC Inspection Report 50-334 and 412/97-07,

Section 03.1.

The licensee extent of condition review did not identify any additional equipment

tagged out that was required for use in emergency or abnormal operating

procedures (EOPs or AOPs). The candidate components and systems identified by

system engineers and operators for potential retirement were entered into the

evaluation process per Nuclear Power Division Administrative Procedure 8.33,

Rev.0, " Retired Equipment Program." Tha Director, System Engineering, expected

the evaluations to be completed by December 15. No additional concerns were

noted by the inspectors,

inspectors concluded that there were no safety consequences to having the

containment iodine fans and the steam generator blowdown tank (1FW-TK-1)

t igged out as " retired in place," %cause the equipment was not safety-related,pnd

was not depended upon in accident analysis. In addition, alternate methods of

emergency response other than the iodine fans and blowdown tank were

proceduralized, inspectors assessed that tagging the equipment out-of-service was

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an isolated instance due to inadequate review and implementation of the Retired

Equipment Program.

TS 6.8.1.a requires that, " Written procedures shall be established, implemented,

and maintained covering...the applicable procedures recommended in Appendix "A"

of Regulatory Guide 1.33, Revision 2, February 1978." Regulatory Guide 1.33

includes p,ocedures for combating emergencies and other significant events.

Equipment was retired-in-place without recognizing that it was required in certain

EOPs. Failure to maintain the EOPs current was a violation of TS 6.8.1.a. This

non-repetitivt licensee-identified and corrected violation is being treated as a Non-

Cited Violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy

(NCV 50-334 and 412/97-08-02).

04 Operator Knowledge and Perlormance

04.1 Questionino Attitude of Ooerators

a. insoection Scoce (71707)

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During routine control room tours, inspectors observed operator activities and

response to degraded conditions.

b. Findinos and Observations

in general, the inspectois noted that operators wera knowledgeable of plant

conditions and out-of-service equipment. The inspectors observed two particular

instances that reflected on the questioning attitude of the operators. . , .

Operators questioned steps in the surveillance test for the auxiliary feedwater

pumps. During performance of auxiliary feedwater (AFW) pump testing, the manual

discharge isolation valve is shut to prevent AFW flow to the steam generators. In

accordance with Technical Specification (TS) 4.7.1.2.a.4, an operator is stationed

at the pump and is in constant communication with the control room. if needed,

the operator is expected to open the discharge valve. The operators questioned

whether this is physically possible due to the pressure differential across the valve.

Engineering calculations show that the operator would not be able to open the

valve. The issue and corrective actions are being tracked under Condition Report

971892. The inspectors noted that operators displayed an excellent questioning

attitude in identifying this longstanding practice of stationing the operator at the

pump.

Since the beginning of September 1997, Quality Service personnel have performed

ultrasonic examinations to determine gas accumulation in the suction lines of the

charging pumps (see Section E2.1 and NRC Inspection Report 50-334 and 50-

412/97-07). The gas accumulation was reported to the control room operators in

units of inches. Based on interviews, the inspectors determined that the operators

did not have a clear understanding of what the values meant nor their impact on

operability of the charging pumps. After inspectors' questioning and discussions

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with operations and system engineering management in October, the system

engineering staff provided guidance to the operators on the quality service

examinations results. The inspectors observed that the current practice provided

the operators with a well defined gas volume limit to make an operability

determination. The lack of adequate guidance, prior to the inspectors' questioning

of the issue, resulted from poor questioning from the operators and failure of

system engineers to provide appropriate guidance to the operators,

c. Conclusion

The inspectors had mixed observations with regard to the questioning attitude of

the reactor operators. In one instance, operators using a strong questioning attitude

identified a longstanding discrepancy in an AFW pump test. However, operators'

failure to question the acceptability of charging pump gas accumulation data was a

weakness.

08 f11sc611aneous Operations issues

08.1 (Closed) Licensee Event Report (LER) 50-334/96-012: Entry into Technical

Specification 3.0.3 Due to isolation of Control Room Emergency Breathing Air

Pressurization System,

a. Insoection Scone (71707)

On October 6,1996, Unit 2 control room operators inadvertently actuated the

Control Room Emergency Breathing Air Pressurization System (CREBAPS).

CREBAPS provides pressurized air to the dual unit control room. Unit 1 operators ,

isolated CREBAPS (to mitigate the consequences) and, as a result, entered into -

Technical Specification (TS) 3.0.3. This event was previously discussed in NRC

Inspection Report 50-334 and 50-412/96-08. The inspectors reviewed LER 50-

334/96-012 and other licensee documents. The inspectors also interviewed

licensee personnel to evaluate corrective actions, the effects of the CREBAPS bottle

isolation operator work-around, and reliability of the system. The following

documents were reviewed:

  • "CREBAPS Focused Design Review Report," Rev.1
  • Problem Report 2-96-610, " Inadvertent CREBAPS Stuation"
  • Unit 1 Maintenance Rule System Basis Document, " Area Ventilation Systems

- Control Area, System 44A," Rev. 3

e 2DBD-44A2, Rev. 3, Design Basis Document for Area Ventilation Systems -

Control Area

  • Unit 2 Shift Logs for August 1997
  • Unit 1 Equipment Out of Service Log, 01/01/97 - 10/31/97
  • Unit 1 Work Around Log, dated 09/25/97.

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b. Observations and Findinas

There have been 20 LERs written at BVPS 1 and 2 since 1987 due to spurious

CREBAPS actuations and entry into TS 3.0.3. Most of the inadvertent actuations

were due to radiation monitor noise and electronic sensitivity problems. To prevent '

an inadvertent air bottle discharge during testing of the radiation monitors,

surveillance procedures were revised to isolate the CREBAPS bottles, and TS 3.7.7.1 (Unit 1) and TS 3.7.7 (Unit 2) were amended to allow isolation of the

CREBAPS bottles for up to 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. The licensee identified the isolation of the

bottles as an operator work-around in August 1995. There have been 5 spurious

actuations of the CREBAPS system this year. There were no discharges of the

system because the CREBAPS bottles were isolated through the proceduralized

operator work around.

Licensee corrective actions listed in LER 50-334/96-012 have been completed and

are appropriate to the specifics of this event. As part of the corrective actions, the

licensee performed a focused design review of the CREBAPS. The inspectors

assessed that the CREBAPS Focused Design Review Report was a very thorough

evaluation of the system, and the recommended corrective actions addressed the

root causes of the spurious actuations. Many of the recommended corrective

actions of the Focused Design Review have been implemented and have been

beneficial. The licensee installed Technical Evaluation Report (TER) 10587 in late

June for control room area radiation mor :.or RM-218A, and in September for RM-

2188. This TER improved grounding in the instrument tack, improved coaxial

shielding, installed snubbers and in-line resistor-capacitor filters, and installed a

delay modification in the radiation monitors to prevent false alarms upon startup or

following a source check. These modifications were positive improvements. *

However, several spurious actuations have occurred since the modifications.

System engineering staff concluded that additional corrective action to install a time

delay in the radiation monitor actuation circuitry is necessary; however, it has not

been scheduled yet. Therefore, the longstanding operator work-around has

continued.

Through review of the August Unit 2 operating shift togs, the inspectors determined

that portions of the CREBAPS system had been isolated 21% of the time.

Approximately 3% of the time was 'iue to the testing and surveillance operator

work around, 7% for periodic maintenance, and 11% due to unscheduled corrective

maintenance. The inspectors interviewed the licensee system engineer, the

maintenance rule program coordinator, and PRA engineer to determine the

applicability of system unavailability to the Maintenance Rule. The CREBAPS

system was considered a non-risk-significant standby system and was tracked

through plant level criteria, with a limit on maintenance preventable functional

failures (MPFFs) tracked for the standby safety-related functions. The inspectors

determined that this level of tracking was in accordance with the Maintenance Rule.

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c. Conclusions

The licensee's review and cc,rrective actions adequately addressed the inadvertent

actuation of the Control Room Emergency Breathing Air Pressurization System

(CREBAPS) on October 6,1996. The CREBAPS Focused Design Review conducted

in response to the event was a thorough evaluation of the system and provided

good recommendations for resolving the longstanding problems. However, the

long term action to eliminate the spurious activation of this engineered safety

features system has not been implemented yet, showing a slow response on the

licensee's part to resolve the longstanding operator work-around.

08.2 (Closed) LER 50-334/97-004-01 (92901): Failure to Test Post DBA Hydrogen

Control System Recombiners in Accordance with Technical Specifications.

The issue was documented in NRC Inspection Report 50-334 and 412/97-02,

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Section M8.2. No new issues were raised in the LER revision. The scheduled

completion dates for corrective actions were revised or updated.

08.3 (Closed) LER 50-334/97-032(92901): Emergency Diesel Generator (EDG)

Automatic Start During Bus Transfer from Unit to System Station Transformer.

The issue was documented in NRC Inspection Report 50-334 and 412/97-07,

Section E2.3 No new concerns were raised in the LER. Inspectors noted that the

licensee has submitted a TS arnendment request (Proposed Operating License

Change Request No.243, dated November 4,1997) for Unit 1 to revisc the

emergency bus undervoltage trip setpoint, allowable value and time delay for EDG

start. This is intended to be a permanent corrective action to prevent unnecessary..

EDG starts during fast bus tran.cfers and while starting reactor coolant pump 1 A.

The licensee also intends to review the TS amendment history associated with the

event to determine if the existing T/S amendment process has any adverse impact

and to identify and implement appropriate enhancements, if necessary, by February

27,1998.

II Maintenance

M1 Conduct of Maintenance

M 1.1 Routine Maintenance Observations (62707)

The inspectors observed selected maintenance activities on important systems and

components. The activities observed and reviewod are listed below.

  • 1PMP-13RS-P-Leak Test-1 M Recirculation Spray Pump Leak Test
  • DCP 2298 Additional Small Bore Pipe Supports Upgrade
  • DCP 2209 ARPI Electronics Upgrade

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9

8

  • MWR 061194 FW P 2 AFW Pump Terry Turbine Overhaul

The activities observed and reviewed were performed safely and in accordance with

proper procedures, except as noted below. Inspectors noted that an appropriate

level n' supervisory attention was given to the work depending on its r iority and.

difficulty.

Motor driveri auxiliary feedwater pump FW-P 3A was overhauled during the

refueling outage under MWR 067122. During post-maintenance testing, the inboard

pump bearing was destroyed. Investigation revealed that the balance drum had not

been set correctly by maintenance technicians during pump reassembly. The root

cause was attributed to poor workmanship. The issue was documented on

Condition Report 971956. Following repairs, the pump was tested satisf actorily

and returned to service. The licensee concluded that the issue was not a

maintenance preventable functional failure (MPFF) under the Maintenance Rule

because the pump was out-of service for overhaul and was not required in Mode 5

(cold shutdown), and the failure was discovered during post-maintenance testing.

Inspectors discussed the issue with system engineering staff and agreed that it was

not an MPFF. Corrective actions to prevent recurrence were under evaluation at the

end of the period.

M1.2 Routine Surveillance Observations (6172fd

The inspectors observed portions of selected surveillance tests. Operational

surveillance tests (OSTs) reviewed and observed by the inspectors are listed below.

  • 10ST-36.1, Rev.17 Diesel Generator No.1 Monthly Test
  • 10ST 36.4, Rev 9 Diesel Generator No.2 Automatic Test
  • 10ST-7.11, Rev.11 CHS and SIS Operability Test
  • 10ST-13.11, Rev.4 OS System Operability Test
  • 20ST 26.1, Rev.13 Turbine Throttle, Governor, Reheat Stop and Intercept

Valve Test

  • 10ST-47.2, Rev.18 Containment Integrity Verification

The surveillance testing was performed safely and in accordance with proper

procedures. AddiUunal observations regarding surveillance testing are discussed in

the following sections. The inspectors noted that an appropriate level of

supervisory attention was given to the testing, depending on its sensitivity.

__ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ -_________.__ _ ___-____-_ _

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M1.3 Leak on Unit 1 EDG Fuel Oil Filter (71707. 92902)

10ST-30.4 performs an automatic start of emergency diesel generator (EDG) No.2

by simulating a loss of offsite power to 4kV bus 10. Immediately after the EDG

start, a Train "B" safety injection signal is actuated to ensure proper sequencer

operation. Required loads are then verified to trip and then sequence onto

emergency bus 1DF. Following logic functional testing, EDG trips are disabled and

a load reject test of greater than 600KW is performed on the EDG.

During test performance on Novernber 8, the EDG undervoltage start and sequencer

operation was satisfactory. However, about 30 seconds into the run, operators

noted fuel oil spraying from engine mounted duplex fuel oil filter 1EE-FL-10B.

Operators shut the EDG fuel rack to stop the diesel and the leak. Loss of the EDG

resulted in loss of power to the 4kV bus 1DF, 480V bus 9P, and all "B" train

120VAC loads Vital buses 2 and 4 remained energized from their respective .

batteries. There was minimalimpact on the plant due to the initiallineup for the

test. Operators restored power to the affected buses in accordance with applicable

alarm response procedures within 45 minutes, inspectors observed the event from

the control room and toured the EDG room shortly afterward. The amount of fuel

oil spilled was small due to quick operator action in securing the EDG. Inspectors

assessed that operator response at the EDG to the fuelleak was conservative, and

operator response in the control room to the loss of the EDG was appropriate,

inspectors noted good control of event response by control room supervisors.

The fuel oil filter gasket was inspected, reseated, and tested satisf actorily.

Maintenance technicians concluded that the gasket had not been sufficiently

compressed during installation, possibly because a new gasket material was being

used. The issue was documented under Condition Report 972111 for evaluation

and corrective actions. The surveillance test on the EDG was successfully

performed on November 10.

p til. Enalneerina

E1 Conduct of Engineering

E1.1 Vital Bus Voltaae Evaluation

a. Insoection Scooe (37551. r 2700. 92903)

While reviewing plans to upgrade existing solid state protection system (SSPS)

relays, engineers identified a concern regarding the adegaacy of voltage supplied to

the nuclear instrumentation system (NIS) power supplies. The inspectors

interviewed personnel, reviewed design documents and observed design charge

implementation activities to evaluate licensee resolution of this issue.

_ _ _ . -

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b. Observations and Findinas

On October 8,1997, engineers determined that under certain conditions the voltage

supplied to the Unit 1 NIS power supplies could be outside of the vendor's

recommended range (11812.5 volts). This condition could potentially adversely

affect the reactor trip system (RTS) protective action functions that respond to

power level data from the NIS. The inspectors discussed the issue with operations

and engineering personnel and noted that the issue was properly reported to the

NRC in accordance with 10 CFR 50.72 and 10 CFR 50.73

1

The inspectors observed that engineers were conservative in assessing a cumulative

worst case scenario. Engineers applied the maximum allowable variation in the

invertor and regulating transformer output voltages combined with the worst case

voltage drop from the transformer to the NIS protection rack (due to various vital

bus and NIS protection rack loadirg). Engineers also applied the most restrictive

available tolerance band to the NIS power supplies. The Unit 2 NIS power supplies

have a vendor specified voltage tolerance of 11815% volts. Although the Unit 1

and Unit 2 NIS power supplies are very similar, the documented tolerance for Unit 1

(found in the vendor troubleshooting manual) is much more restrictive. Even though

the Unit i NIS voltages were outside of vendor recommendations, engineers believe

power supplies were likely to have functioned properly as installed, because they

were similar in design to the Unit 2 power supplies. Notwithstanding, since

documentation of acceptable NIS performance outside of the specified voltage, . sand

was not available, engineers recommended upgrading the existing Unit 1 NIS pow r

supply voltage transformers. Engineers determined that the existing Unit 2 NIS

pov'er supply was acceptable, based on design drawings, calculations, and voltage

measurements.

As an immediate action, operators verified that voltages were within the vendor

specified range each operating shift. In addition, maintenance records

demonstrated that the voltages were within the specified range when last verified

per periodic maintenance. Engineers reviewed Unit 1 operating history documents

and did not identify any actual plant conditions during which voltage was outside of

the vendor's recommendations. The unit was in cold shutdc ivn at the time of

discovery. Engineers closely communicated with the vendor, initiated a design

change to upgrade the power conditioning, and reviewed the potential extent of

condition for additional vital bus loads for both units. The inspectors determined

that initial actions were timely and technically sound.

Design change package (DCP) 2296, " Vital Bus Vo'tage Requirements", was written

to upgrade the NIS power supply regulating transformers (11811% volts) and

improve connections from the vital bus distribution panels. The inspectors reviewed

the DCP and observed portions of the field installation and testing. The DCP was

properly implemented and closely coordinated with operations personnel to establish

prerequisite plant conditions for installation and testing.

Calculation Nos. 8700-E-231(232) were initiated to model vital bus component

performance for all four vital buses and downstream components. These

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calculations were nearing completion at the end of this report period. No additional

safety related load discrepancies had been identified. Based on the results of the

completed Unit 1 calculations, engineers will determine whether a detailed Unit 2

analysis is needed.

c. Conclusions

Engineers determined that under certain conditions the voltage supplied to the Unit

1 NIS power supplies could potentially adversely affect the reactor trip system

protective action functions. Engineers' performance during ascessment of this issue

and extent of condition reviews, was conservative and demonstrated a strong

questioning attitude. Corrective actions, including design change implementation,

were timely and tv.chnically sound.

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E2 Engineering Support of Facilities and Equipment

E 2.1 (Closed) Unresolved item (URI) 50-334 and 412/97-07-04: Adequacy of the High

Head Safety injection Pump Surveillance Tests to Ensure Operability

a. Inspection Scone (37551)

The inspectors reviewed the adequacy of the surveillance procedure to determine

functionality of the high head safety injection (HHSil/ charging pumps. The

inspectors interviewed operators, system engineers, and system engineering

managcment. The inspectors reviewed the following documents:

  • Inservice Testing (IST) data for the Unit 2 HHSl pumps since 1991;
  • Completed surveillance procedures for Unit 2 HHSI pumps for 1996 and

1997;

  • The last five revisions to the surveillance proceduros for the Unit 2 HHSI

pumps;

  • Minimum operating performance curves (located in the Inservice Testing

Program for Pumps and Valves)

b. Observations and Findinas

The inspectors identified several issues in NRC inspection Report 50-334 and

412/97-07 that were related to the adequacy of the Unit 2 surveillance procedures

20ST-7.4(5)(6), " Centrifugal Charging Pump [2CHS*P21 A(B)(C))," to determine

functionality of the HHSI pumps.

Syryeillance Procedure /IST Acceotability

The surveillance procedures require that at specific flow rates (~ 200 gpm),

operators obtain IST data including pump bearing temperatures, motor bearing

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temperatures, pump vibration data, pressures, and flow rates. Af ter recordinq this

data, the procedures allow throttling of the flow to meet the Technical Spech tion

(TS) required difierential pressure. Based on review of the TS, the minimum

operating performance curves, and basis for the differential pressure values, the

inspectors determined that the procedure was acceptable to measure end determine

whether pum; performance met the TS required differential pressures.

The acceptance criteria in the surveillance procedure require that the pumps operate

within the limits of the ASME Section XIIST program. The inspectors determined

from past IST results and procedure rev;ews, that the data was collected at a

constant flow rate which ensured the data would provide meaningful trending

information. The ASME acceptance criteria for differential pressure were not clearly

linked to the flow reo due to poor procedure human factors; however, the

inspecters determined the performtnce data was properly evaluated to correlate to

the acceptanco criteria. Based on engineering memorandums and IST program

infermation reviewed, the inspectors determined that the licensee had established a

nexus between the acceptance criteria and the minimum cperating performance

curve. The minimum operating performance curve establishes the required flow for

safety analysis. This clases URI 50 334 and 412/97 07 04.

Mditional Back4NMDilBiprmation

in Ma'ch 1988, Beaver Valley experienced gas binding of the Unit 2 HHSI pump

(2CHbP21 A). NRC Information Notice 88 23, " Potential for Gas Binding of High-

Pressua Safety injection Pumps During a Loss-of-Coolant Accident," highlighted the

indus ssue. Engineering performed model testing and ultrasonic testing (UT)

exami )ns of piping to <ietermine gas growth rates. Several colutions were .

evalunt and a manual venting path was established for both units. The venting

times were established based on UT measurements of gas accumulation in 1988

and an estimated maximum gas accumulation limit (based on prior history).

The licensee did not find the Unit 2 UT examination results performed in 1988

during tecords reviews in 1997. The conclusions derived lgas accumulation rates)

from those results were documented and used to establish the pump venting

frequencies. Unit 1 gas accumulation rates were established based on 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> of

data taken in 1988. Between 1989 and August 1997, the licansee did not conduct

UT testing for Unit 1 or Unit 2 to verify gas accumulation rates were valid. Unit 2

UT examinations conducted since August 1997 showed that the majority of the gas

accumulation occurred during pump shutdown and not during steady stato

conditions. However, the overall Unit 2 gas accumulation rate, were bounded by

the 1988 conclusions. Auditional UT examinations for Unit 1 were cor' ducted on all

three Unit 1 HHSI pump suction lines in early November. The gas accumulation

rates are still under investigation.

Prior to March 1988, the licensee had experienced 21 safety injection events at

Unit 1 without failure of the HHSI pumps. The maximum gas accumulation limit

(8.1 cubic feet) was determined using past suavsful HHSI pump operation and

engineering analysis in evaluating the void size during those events. Based un this

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analysis a maximum gas accumulation limit was established for Unit 1 and Unit 2.

The use of Unit 1 data to support a Unit 2 rnaximum gas accumulation limit may

have been inappropriate due to the different piping configurations.

In October 1997, the licensee team investigating the gas binding events asse:; sed

that the maximum gas accumulation limit should be reevaluated for Unit 1 and

Unit 2. Based on preliminary evaluation, system engineers have established a

maximum gas accumulation limit of 0.5 cubic feet for Unit 2. The limit is based on

vendor recommendation to minim!ze entrained gas to 5% by volume. Daily UT

measurements on Unit 2 suction lines have been performed to verify that the limit

has been met. The Unit 1 preliminary datermination of gas accumulation lirait will

be completed prior to Mode 4 entry. The final evaluation of ge= eccumulation limit

is under investigation by the team for Unit 1 and Unit 2. Thti l'.;ensee is

reevaluating the engineering analysis for the Original values and vo.ndor information

to determine an appropriate maximum gas accumulation limit. This effort includes

construction of a model to help address cuestions on gas ccumulation and

transportation of that gas to the pump.

In addition, the established vent path was ineffective due to inmfficient driving

force to move the gas from the charging pump piping to the col 6ction tank.

Periodic venting did not always aJequately vent the Unit 2 HHSI pump suction lines.

The Unit 2 "C" HHSI pump experienced gas binding during multiple starts in June

1993 and during starts in November 1996 and August 1997. The repeated gas

binding events were the most likely cause for the pumps' degraded performance ,

and subsequent replacement in September 1997. The inadequate venting and gas  !

binding events were documented in Nf4C Inspection Report 50 334 and 412/97 07.

Based on the gas binding events that occurred on Unit 2 "C" HHSl pump, the

inspectors determined that the established vent path and venting frequencies were

inadequate to ensure proper pump performance. The inadequate venting system

and the questionable acceptable gas accumulation limits resulted in inadequate

venting frequencies. From 1988 to August 1997, the licenseo setied on the venting

i frequencies to maintain acceptable low levels of gas entrainment for operability of

the HHSI pumps. The failure to take appropriate corrective actions to preclude gas

binding of the pumps was an apparent violation documented in NRC Inspection

Report 50 334 and 412/97 07.

Ventino Prior to Manual Pumo Starts

i

( During review of the surveillance procedure and discussions with system engineers

and operations management, the inspectors determined that HHSi pump suction

'

lines were routinely vented prior to performing manual pump starts, including the

periodic surveillance test. The procedures allowed venting the HHSI pump prior to

starting the pump at the nuclear shift supervisor's discretion. Unit 1 and Unit 2

c,perators typically vented the HHSI pumps prior to performing the quarterly

surveillances, safeguards protection system testing (GO testing), and 18-month full

flow testing. The venting prior to pump start was done to eliminate any gas in the

system to enhance pump long-term reliabili'y.

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The venting frequency established to ensure minimal as accumulation in the

suction lines was inadequate to prevent gas binding or the Unit 2 HHSI pumps. 'The ,

inspectors determined that venting the suction lines immediately prior to performing i

'

the surveillance testing changed the as found condition of the system from that

which would normally be present if the system was automatically called upon to 1

perform its safety function. . Changing the as-found condition of the HHSI pump

suction lines immediately prior to performing periodic surveillance tests may

interfere with the licensee's ability to properly assass the operability of the system.

10 CFR 50, Appendix B, Criterion XI, " Test Control", requires, in part, that "... the

test is performed under suitable environmental conditions." Suitable environmental-

- conditions include conditions representative of the expseted conditions when the

aquipment is required to perform its safety function. The normal practice of venting - >

prior to surveillance testing may be a violation of NRC requirements pertaining to

the validity of the test results, depending upon the periodic venting program . ,

implemented between the surveillance tests. This is considered an unresolved item

pending further NRC review. (URI 50 334 and 412/97 08 03). ,

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c. Conclusion

The inspectors observed that the licensee's team evaluating the gas binding events

in August 1997 had uncovered weaknesses in the original engineering analysis

perfortned to establish venting frequencies. Strong questioning by licensee

management and team members led to these findings, inspectors identified

weaknesses in the licensee's oversight of gas accumulation in the safety significant

HHSI system from 1988 to 1997, in that the licensee did not verify the original gas

accumulation rate assumptions, and d!d not verify the adequacy of the periodic vent

path used during that time period.

Periodic venting practices established in 1988 to ensure minimal gas accumulation

in the suction lines was inadequate to prevent gas binding of the Unit 2 HHSI

pumps. The frequency of venting should be based on a good venting method, an

established gas accumulation limit, and an established gas accumubtion rate. Since

the venting method was not effective and the established gas accumulation rate and

limits were incorrect, the venting frequency was inadequate. The inadequate

corrective actions to preclude the gas binding of the pumps were addressed in

Inspection Report 50 33t, and 412/97 07. Acceptability of the pre surveillance test

venting that had been in effect is unresolved.

E8 Miscellaneous Engineering Issues

E8.1 Inservice Insoection

a. Insoection Scone (73753. 92903) .

An inspection of the inservice inspection (ISI) program was conducted by a regional

inspector from October 20 24,1997. The objective of this inspection was to verify

that the inservice inspection (ISI), repair, and replacement of Class 1,2, and 3

pressure retaining components are performed in accordance with the Technical

4

, ....me,,. , , , , - . - - e..,..,r .. - . . , ~ .- . . .- . . ,,,,-. _ # - + ~ , , , ,24,. ... . .,,y -v-o, ,c-,- ,.enww,,.~,.w.

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Specifications (TS), the applicable ASME Code, NRC requirements, and industry

initiatives, including any relief requests granted by the NRC.

i

The scope of the inspection included the review of the licensee's ISI program plan i

for Beaver Valby Unit 1, orocedures, qualification of inspection / examination l

personnel, schdule vi planned Isis for the refueling outage IR12, and observation l

of ISI work. '

b. Observation and Findinas

1. The ISI Prooram Plan

The ISI program plan for the third 10 year interva! was submitted to the NRC

on September 17,1997. The plan includes several relief requests and

alternate inspection methods. Although the plan has not yet been approved

by the NM, the licensee has implemented the proposed plan with the

rationale that many of these relief requests and alternate inspection methods

had been approved by the NRC for the previous plan, thus it would be

acceptable for the third interval. However, if the NRC does ' it approve nny

of tM proposed relief requests or alternates, the licensee ha two mea

scheouled " outages" to modify and implement an approved plan,

2. Steam Generator Tube Eddy Current insoection

Duquesne Light Company (DLC), the licensee for Beaver Valley Unit 1 (BV-

1), had nearly completed its steam generator (SG) tube eddy current

inspections for the current refueling outage. BV-1 has three Westinghouse

Model 51 SGs with carbon steel drilled hole tube support plates and -

WEXTEX joints in the tubesheet. DLC performed fulllength bobbin coil eddy

current inspections of all active tubes in each SG. The licensee also

performed specialized inspections using the plus point probe of the low row

U bends, hot and cold leg top of the tubesheet (TTS), most bobbin coil

indications, and rolled plugs. DLC also conducted a secondary side visual

inspection of the wrapper supports and found no degradation.

Through bobbin coil inspections, DLC identified four pluggable (i.e., greater

than 40% throughwall) wear indications due to cold lag thinning and anti-

vibration bar (AVB) wear. The licensee also detected tube support plate

(TSP) cracking through bobbin coilinspection and followed up using the plus

point probe to confirm about fifteen suc,h indications in the patch plate

region. The licensee is evaluating how to dispusition the affected tubes.

DLC inspected 100% of the TTS on the hot leg side and 20% of the TTS on

the cold leg side in each SG. The axial extent of the tubesheet inspections

included six inches above the TTS to three inches below the TTS, On the

hot leg side, the licensee reported 127 repairable indications. Most were

identified as axially-oriented outside-diameter stress corrosion cracking

(ODSCC) located above the TTS in the tube " collar" region (area of heavy

. - _. . _ - - - _ ___-- _ _ _ _

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16

tube deposits not removed through sludge lancing). A few were axial and

circumferentially-oriented indications located below the WEXTEX expansion

transition inside the tubesheet. On the cold leg side, the licensee identified

nine axially-oriented ODSCC indications located above the TTS; for this SG,

the licensee expanded its inspection scope to include 100% of the TTS

region. The longest extent for a circumferential crack was about 90' and

the longest axial crack was reported to be about 0.8 inches long. Eight

volumetric indications (some pit-like) were found in the TTS region as well.

DLC inspected 100% of the row 1 and 2 U bends and 20% of the row 3 U-

bends. The licensee reported 11 row 1 U bend indications and 1 row 2 U-

bend indication characterized as primary water stress corrosion cracking

(PWSCC) and located in the bend tangent. DLC's low row U bends have

been stress relieved.

The licensee performed a 100% inspection of dents > 5 volts, a 20% sample

of dents >205 volts, and 100% of all dents and dings (dents located in the

freespan) >2 volts located between the TTS and the 3rd TSP. No

indications were reported.

DLC inspected 100% of its inconel 600(1-600) rolled plugs and 20% of its

Inconel 690 (1690) rolled plugs. The licensee reported seven 1600 plug

indications. The licensee intends to replace these with l 690 rolled plugs

during this outage. No I 690 plug indications were reported.

For the identified degradation mechanism, the licensee has selected the most

limiting (based on length, depth and voltage) indications for insitu pressure

testing. At the time of this inspection, the pressure testing of SG tubes was

in progress. The inspector witnessed one such test from the remote test

control location.

3. Qualification /Cortification of NDE Personnel

The inspector reviewed the qualification and certification records of

approximately seven individuals engaged in non-destructive examination

(NDE) of the ISI program. The review indicated that the inspectors were

properly qualified by formal and practical training, and were certified to

proper levels of inspection / examination responsibility in different examination

methods; e.g., visual examination (VT), liquid penetrant (PT), magnetic

particle (MT), or ultrasonic examination (UT).

4. Observation of ISI Examinations

The inspector observed / witnessed several NDEs to assess the adequacy of

procedures, knowledge and proficiency of test personnel, and the validity of

the test results. The following tests were observed:

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1. Surface examination by dye penetrant: CH 23 3 5-03, and CH 23 4-

i F 06 inside containment;  ;

2. Volumetric examination by UT: 1 SA 41 FD24 in the auxiliary

building; and ,

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3. Pressure test of steam generator tube: 5A21 from the remotu

display / control test facility for SG tube examination and tests. ,

'

The tests / examinations were performed by knowledgeable and qualified i

Individuals, using approved proc?dures, materials, and calibrated equipment.

The results were properly recoroad. 7

'

5. Evaluation and Resolution of Deficiency

i

The inspector reviewed the evaluation and resolution by Engineering of three

" unsatisfactory" test results. These deficiencies were documented in

Condition Reports 970792,970793 and 970836, and were related to PT

,

surface examinations.

>

In all cases, the disposition of the indication by grinding and blending the

surface profile to established contour was appropriate. '

O. NDE Procedures

The inspector reviewed the following NDE procedure to assess the clarity

and technical adequacy of established requirements.

GP-105 Evaluation of PSl/ISI Flaw Indications, Rev. 6

LP-101 Solvent Removable Visible Dye, Rev.15

MT-201 Magnetic Particle Examination, Rev.13

UT-301 Linearity of Ultrasonic Instruments, Rev. 9

UT-303 Ultrasonic Examination of Piping Welds, 2" to 6" Thick and

Vessels Less than or Equal to 2" Wall Thickness, Rev.12

a The inspector determined that the procedures were clearly written, estbblished

technically valid requirements and were appropriately maintained, controlled, and ~

used by NDE personnel.

Additionally, the licensee has implemented a new data management software for

tracking and managing ISI program. Th' new system appears comprehensive and

has been successfully used at other utilities.

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c. ConclutdQnt

Based on the above observation, review of documentation, and discussions with

personnel responsible for ISI program, the inspector concluded that the licensee's

ISI program plan is satisfactorily maintained and implemented. The NDE personnel

are properly qualified / certified, examination procedures are adequate to assure valid

examinations, and deficiencies are appropriately evaluated and resolved. The new

data management software appears effective.

E8.2 (Closef f) VIO 50 334/96 05-02(92903): Inadequate cap'eration for UT

examinations

The above violation pertained to a failure to perform a calibration for UT

examination using a reflector perpendicular to the cound beam for examinations ,

!

with the sound beam to the weld seem (circumferential examinations) on six ASME

class 2 pipe weld examinations. Also, for two calibrations (C 96-57 and C 96-46)

sido drilled holes were not used to construct the distance amplitude correction

(DAC) curve.

In response to the Notice of Violation, the licensee initiated entrective actions to

resolve the deficiency, and to prevent similar occurrences in tue future. The

licensee's actions included the following:

1. Problem Reports 196 487,196-488 and 196 489 were submitted to the

Operations Experience Group on May 17,1996. These problem reports

identified the scope of incorrect calibrations and provided technical

assessments of the deficiencies identified during the exit meeting on

May 16,1996.

2. An independent review of the problem reports was performed by Materials

and Standards Engineering to address poter.tial operability concerns.

3. Independent root cause evaluation using the Taproot root cause evaluation

method was performed on the problems identified.

Actions Taken to Prevent Recurrence

As a result of the recommendations in the root cause evaluations, the following

corrective actions were being taken:

1. UT Procedure UT-303 was revised for clarification and to allow ID notch

calibration and was demonstrated to the authorized nuclear inservice

inspector (ANil).

2. NDE catractor training has been included in procedure OSP 2.5, which

provides procedural contrels for onsite training of contracted NDE personnel

using DLC. NDE procedures.

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3. The calibration report forms have been revised to more clearly define

calibration orientation and calibration reflectors used.

4. The dissimilar metal welds examined using only the ID notch for calibration

were re-examined using a qualified UT technique during 1R12.

The inspector verified the licensee's corrective actions by review of documentation

and discussion with cognizant personnel, and found the actions acceptable and

effective. Based on the above observation, this item is closed.

IV. Plant Support

R1 Radiological Protection and Chemistry (RP&C) Controls

a. Insnection Scone (83750)

The inspectors reviewed the licensee's program for radiation protection during a

refueling outage (1R12). Areas reviewed included high and locked high radiation

area controls, radiation worker performance indicators, including maintaining

occupational exposures as low as is reasonably achievable (ALARA), and radiation

worker practices. The inspection was accomplished by a review of plant

dncuments and procedures, interviews with personnel, and walkdowns of the

related areas,

b. Observations and Findinas

The inspectors reviewed the licensee's performance during the Unit 1 refueling

outage (1R12) which commenced in late September. Outage goals previously

established included completion of the outage in 40 days (with a challenge goal of

36 days), an occupational exposure goal of not more than 201 person rem, and a

personnel contamination event goal of not more than 180. During the period of this

specialist inspection, outage activities included eddy current testing in all three

steam generators, reactor head and upper core internals removal, and the first 36

hours of fuel removal.

The inspectors reviewed the licensee's control of high ar.d locked high radiation

areas, especially those located in the containment. All areas reviewed, which

included the entrances to the steam generator / reactor cociant pump cubicles, were

determined to be appropriately controlled, barricaded and posted in accordance with

plant technical specifications. Workers interviewed in the high radiation areas were

aware of their work area exposure rates and appropriate radiological controls to

minimize their exposures. Health physics technicians were observed providing

d3 tailed and extensive briefings to workers and providing appropriate job coverage.

Of particular note was the licensee's utilization of remote teledosimetry, closed

circuit cameras and communication fa steam generator eddy current testing. By

i utilizing this type of control, the licensee was a' ole to significantly reduce total job

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exposures, especially for the radiological cor tmis technicians, while providing real  ;

time exposure rate data so ac to minimize suam generator worker exposures.

As noted above, the licensee had established an outage ALARA goal of not more

than 201 person-rem, and through day 12 of the outage the exposures appeared to

be tracking well, although the licensee does not track exposure against percentage

of work completed and the outage was estimated to be two days behind schedule.

The inspector noted that the licensee was focused on personnel contamination

events (PCEs) and had established an outage goal of not more than 180 PCEs.

During the specialist inspection, the inspectors noted that workers entering the

radiologically controlled areas (RCAs) were not checking the posted general area

survey maps located at the primary plant staff and contractor entry points, as

specified in the licensee's radiation work permits. Since the licensee did not utilize

a direct verbal briefing system between workers and the health physics staff prior to

entries, it appeared to the inspectors that the potential existed for workers to be in

portions of the RCA without knowing the radiological conditions. On October 7th

and 8th, the inspectors conducted a random survey of workers located in the

general areas of the primary auxiliary building, especially the transit path to the

containment personnel hatch, and inside the containment, in the outer annulus

regions. None of the ten workers interviewed could identify the radiological

conditions in the areas they were standing in or had walked through. None of the

workere could identify their nearest ALARA low dose waiting area. The inspectors

further noted that workers failed to review the radiological survey maps placed at

the two main RCA entrances, as required by their RWPs. Further, the inspectors

noted that a number of the posted survey maps at the RCA access points were

outdated and did not accurately reflect current plant conditions. Failure of workers

to follow instructions contained in their RWPs is a violation of TS 6.8.1.a, which

requires that written procedures and instructions be established, implemented and

maintained regarding radiation protection procedures. (VIO 50 334/97-08-04).

On two separate occasions, the inspectors observed workers in the containment

who appeared to be unaware of their surroundings. One worker was observed lying

on the floor on the 692' elevation next to a desk and chair at the health physics

control point for that level, while another was outside the "C" steam generator

cubicle on the 718' elevation. Neither location was a designated low dose waiting

area. Both workers had their eyes closed, and did not open them cr notice the

inspector until just as the inspector passed them. The inspector notified plant

supervisors of his observations, and his concern that personnel, not actively

engaged in work in the RCA, should be outside the RCA or in posted ALARA low

dose waiting areas. The first example was subsequently documented in a plant

condition report.

During tours of the containment, the inspectors noted generally poor radiological

housekeeping. The same observation was made by the plant Health Physics

Manager, who stressed the importance of this issue at a morning management

meeting attended by the inspectors. By the end of the specialist inspection,

l housekeeping had improved but was still considered poor.

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_ . . _ _ _ . _ _ _ _= _ .. .___ . _ ..___. _ _ _ . _ _ . . _ . _ _ ._

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21

The inspectors also reviewed the license's most recent results from the National

Voluntary Laboratory Accreditation Program (NVLAP) of its thermoluminescent -

dosimetry program. During NRC Inspection Report 50 334 and 412/97-02, the

inspectors noted that the licensee had failed test criteria 1, Accideni ' ow Energy

Photon. Since that time the licensee has resubmitted 15 test dostw/.ers, five per

month for three months, and has received a passing grade from NVLAP.

c. Conclusions

Generally effective radiological controls were in place for the refueling outage,

especially for the control of work in high and locked high radiation areas. However;

radiological housekeeping was poor, some posted survey maps of the RCA were out

of date, and two workers were observed in the RCA who were not aware of their

surroundings. One violation of NRC requirements was also identified concerning

workers failing to follow the RWP requirement to review the applicable survey maps

of the RCA prior to entry.

R2 Status of RP&C Facilities and Equipment

R2.1 Calibration of Effluent / Process / Area / Accident Radiation Monitorino Svstems (RMS)

a. Insoection Scope (84750)

,

The inspector reviewed the most recent radiological and electronic calibration

results and calibration procedures for the effluent / process RMS. The inspector also

held discussions with Health Physics and instrumentation and Controls staff, and

the RMS System Engineer.

The inspector utilized the following documents as a basis to determine whether the

calibration procedures contained sufficient detail and guidance to verify conversion

factors (calibration factors) and monitoring capability for the intended range

(linearity):

o Regulatory Guide 1.21, " Measuring, Evaluating, and Reporting Radioactivity

in Solid Wastes and Releases of Radioactive Materials in Liquid and Gaseous

Effluents from Light Water Cooled Nuclear Power Plants, February 1979"

, o Regulatory Guide 4.15, " Quality Assurance for Radiological Monitoring

Programs (Normal Operations)- Effluent Streams r, rid the Environment.

February 1979"

e ANSI N42.18,1980, " Specification and Performance of On-Site

Instrumentation for Continuously Monitoring Radioactivity in Effluents"

e EPRI TR-102644, " Calibration of Radiation Monitors at Nuclear Power r)lants,

March 1994"

_ -_

. - . - . - - - .- --

- - - - . .. . _- -. - - . . . . . . . - -- .-_ . . _ . . .-

4

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  • - Victoreen Installation, Operation, and Maintenance Instruction Manual Beta

'

Scintillation Detectors Models 843 20,843 20A, and 843 20B *

  • Victoreen Instruction Manual Gamma Scintillation Detector Model 843 30 l

The following Unit 1 RMS were reviewed.

  • Liquid Waste Effluent

'

  • Component Cooling Recirculation Spray Heat Exchange
  • Process Vent Noble Gas
  • Auxiliary. Building Noble Gas
  • Supplementary Leak Collection Noble Gas
  • Containment Air

. * Containment Purge

The following Unit 2 RMS were reviewed.

  • Liquid Waste Effluent
  • Ventilation System Noble Gas
  • Elevated Release Noble Gas
  • Decontamination Building Noble Gas
  • Waste Gas Storage Vault
  • Condensate Polishing Building Noble Gas

'

  • Containment Purge Noble Gas

b. Observations and Findinas

Electronic calibrations were appropriate. Linearity checking was appropriate. Good

tracking and trending of the RMS was noted. The inspector noted that despite the

age of RMS, reliability has been good. There were few open work orders at the

time of the inspection.

The inspector did note that the licensee typically used supervisory discretion

(permitted by procedure) rather than using the detailed guidance within the Health

Physics Department procedure 5.11 for establishing a high voltage setting. Of the

22 channels of RMS reviewed, only 3 channels met EPRI guidance for establishing

the operating high voltage. The inspector noted that the practice was contrary to

existing standards and industry guidance documents.

RM-1RM 215A (Unit 1 containment particulate; Victorcen detector type 843-20A)

operating voltage was established at 650 volts. Per licensee calibration data, the

4 percent change over 50 volts at 650 volts on a operating voltage vs. count rate

curve was 365% The inspector noted that the vendor instruction manual directed

the user to generate a plateau curve and noted that at 1100 volts the count rate

should reach the lower end of the plateau. Contrary to the vendor instruction

manual and the above noted guidance documents that operating high voltage be set

on the plateau, the licensee established operating high voltage by changing high

. _~- - . -,

. ..-. . - -- --- - - . . _- . -. . - - ..-.-. - ~ ~ .. -

- .- - --

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- voltage to a point at.which actual counts equalled expected counts with a National

Institute of Standards and Technology (NIST) traceable source.

RM 1LW-104 (Unit 1 liquid waste effluent; Victoreen detector type 843 30)

operating voltage was established at 450 volts. Per licensee calibration data, the

percent change over 50 volts at 450 volts on a operating voltage vs. count rate

curve was 133% The inspector noted that the vendor instruction manual

specifications for operating voltage were 500 to 1400 volts. The inspector also

noted that the vendor manual recommended that the operating high voltage be

established by generating a signal to noise ratio curve and setting high voltage to

the peak value on the curve (this method is also described in EPRI TR 102644).

Contrary to the vendor instruction manual and the above noted guidance

documents, the licensee established operating high voltage by changing high -

voltage to a point at which actual counts equalled expected counts with a NIST  !

traceable source.

TS 6.8.1.a requires, in part, that written procedures shall be established,

implemented, and maintained covering the activities recommended in Appendix A of

Regulatory Guide 1.33 (RG 1.33), Revision 2, February 1978. Appendix A of the

RG 1.33, " Typical Procedures for Pressurized Water Reactors and Boiling Water

Reactors," describes typical procedures for the control of radioactivity, including

procedures involving radiation monitoring systems.

Contrary to the above, the licensee failed to establish adequate RMS calibration

instructions in regard to determining RMS operating high voltage. Specifically,

operating high voltage was not established on a plateau for RM 1RM 215A (Unit 1

Containment Particulate) and RM 1LW-104 (Unit 1 Liquid Waste Effluent). This was

contrary to vendor manual "Victoreen Installation,- Operation, and Maintenance, ~

Instruction Manual Beta Scintillation Detectors Models 843 20, 843-20A, and 843-

20B" and "Victoreen instructional Manual Gamma Scintillation Detectors Model

843-30" respectively; and was contrary to RMS calibration standards and industry

guidance documents. This is a violation of NRC requirements (VIO 50-334/97-08-

05).

In reviewing as found and as left high voltages for the above noted RMS calibrations

- and a synopsis of similar data provided by the RMS Health Physicist, the inspecte."

noted that typically there was little if any high voltage drift. In one case, a drift of

30 volts was noted. For this particular RMS, the operating high voltage had been

set close to the plateau and, as a result, this relatively large drif t in operating high

voltage had very little impact on the accuracy of RMS output. While the technique

used to establish operating high voltage was technically deficient, the inspector did

not identify any case in which high voltage drift had led to error such that the

validity of data provided in the annual effluent report was questionable. During the

inspection and at the exit meeting, licensee representatives indicated that prior to a

planned batra release a sample is taken, thereby providing a check on RMS

operability.

.

f

_ ,

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24

The inspector questioned the licensee as to whether they could provide any

information pertaining to new/ refurbished detector failures. The Health Physics I

Marager informed the inspector that if BVPS identified a faulty detector, it was I

replaced; but, the f ailure cause may not be documented. This matter will be l

reviewed further (IFl 50-334/97 08-06).

c. Conclusion

RMS reliability has generally been good. Electronic alignment and linearity checking

were good. The inspector noted that the licensee had failed to implement industry

guidance (EPRI TR 102644 and ANSI N42.18) which specifically direct that the

operating voltage be set on a plateau and, in two cases, had failed to implement

vendor manual instructions for establishing operating high voltage. The inspector

concluded that this was a poor calibration practice which has the potential for ,

leading to instrument error. Instrument error could impede or prevent an accurate

assessment of public exposures and environmental impact in the case of an

inadvertent release of radioactive materials.

R2.2 Air Cleanino Systems

a. Insoection Scoco (84750)

The inspectors reviewed the licensee's most recent surveillance test results,

including visual inspections, in-place High Efficiency Particulate Air (HEPA) leak

tests, in-place charcoal leek tests, air capacity tests, pressure drop tests, and

laboratory tests for the iodine collection efficiencies for the Supplementary Leak

Collection and Release Systems (SLCRS).

b. Observations and Findinas

All test results were within the licensee's acceptance criteria. No procedural

inadequacies were noted. Unsatisfactory test results were analyzed and corrective

actions were implemented in a timely manner. The inspectors noted that attention

given to the air cleaning systems was good. System Engineers monitored and

trended the performance of the air cleaning systems.

c. Conclusions

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Those portions of the test program reviewed were wellimplemented with strong

monitoring and trending of air cleaning system performance parameters.

R5 Staff Training and Qualification in RP&C

l

a. Insoection Scone (83750)

+

The inspectors reviewed the qualifications of 23 contractor health physics

technicians to ensure they were appropriately classified as junior or senior

technicians. The records were selected by the inspectors at random.

._ _ _ _ _ _ _ . _ _ _ . . _ _ _

_ _ _ _ _ _ ___.. _ ._.. _ .. _ _

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b. Observations l

8

The licensee hired 86 contractor health physics technicians (66 senior and 20

junior) in ordet to support the Unit 1 refueling outage. The inspectors selected 23 i

records at random and reviewed the licensee's calculations for technician  !

experience. All calculations reviewed were determined to be appropriate, and in

general, the inspectors determined that the licensee was conservative in reviewing

technician qualifications. ,

c. Conclusions

,

The licens9e appropriately classified contractor health physics technicians with

~

'l

regards to previous experience.

. R7 Quality Assurance (QA)in RP&C Activities ,

a. Inspection Scope (84750)

'

The inspection consisted of: (1) review of the 1996 Quality Services Unit (OSU)-

audit of the Site Radiological Effluent and Environmental Monitoring Programs, (2) '

QSU surveillances and (3) self assessments.

b. Observations and Findinas

Audit team members included a technical specialist from another utility. The depth

>

of the audit was good. The audit team identified several minor discrepancies and

matters for enhancing the radioactive liquid and gaseous effluent control programs..

No items were of regulatory significance. l

! Surveillances and self assessments were also well-targeted arcl helped to augment

the audit.~

!

c. Conclusion

This program area was wellimplemented.

L1 Review of FSAR Commitments

l

l_ - While performing the inspections discussed in this report, the inspectors leviewed

'

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the applicable parts of the UFSAR that related to the areas inspected. The

inspectors verified that the UFSAR wording was consistent with the observed plant

practices, procedures and/or parameters.

.

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__ . _ _ - . - _ _ _. __ ._ _ . _ - . - - _ . _ . _ . - . . _ . - - _ - _ _ . __ _ _ . _ _ _ . _

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26

V. Mananoment Meetinas

X1 Exh Meeting Summery

The inspectors presented the results of the radiation protection and radioactive effluent ~i

control inspections to Mr. R. Vento on October 10,1997. The results of the ISl program

inspection were presented to Mr. S. Jain and Mr. R. LeGrand on October 24. The licensee

acknowledged the findings presented. After further in office review of information

pertaining to the RMS calibration, the inspector concluded that a violation of NRC

requirements had occurred. '

The inspectors conducted an interim exit with Mr. S. Jain on November 10,1997, to

discuss the apparent violation documented in this report. The inspectors presented the

remainder of the inspection results in a meeting with Mr. J. Cross and members of his staff

at the conclusion of the inspection on November 21,1997. The licensee acknowledged i

the findings presented with one exception, i

. -

'

The licensee disagreed with the NRC's position that venting the HHSl pumps immediately

prior to surveillance test preconditioned the pumps. The licensee stated that the purpose ,

of venting the suction lines on the HHSl pumps prior to surveillance testing was to ensure

long term reliability of the pumps. The venting was not performed to create an enhanced l

test environment.~ The licensee stated that venting the pump would not change the <

environment such that it could be considered preconditioning.

The inspectors asked the licensee whether any materials examined during the inspection

!

should be considered proprietary. No proprietary information was identified.

X2 Pre-Decisional Enforcement Conference

'

The pre-decisional enforcement conference referred to in NRC Inspection Report 50-334

and 50-412/97 07 has been scheduled for December 10 at the NRC Region i office to 3

discuss the apparent violation documented in that report and URI 50 334 and 412/97-08- ,

03 of this report.

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_ .. -_ _ . _ . -, _ _ . - . . - . - . - . _ . ._ _- ._ .~_-__,_.- - _ ,._- _ - _ .

.. . . -. . . . . -- - - - . - . . - - _ - _ . - - - - - . . - -- .

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PARTIAL. LIST OF PERSONS CONTACTED

QLG

J. Cross, President,' Generation Group ,

R. LeGrand, Vice President, Nuclear Operations / Plant Manager

S. Jain, Vice President, Nuclear Services

M. Pergar, Acting Manager, Quality Services Unit

B. Tulte, General Manager, Nuclear Operations

R. Hansen, General Manager, Maintenance Programs Unit

R. Vento, Manager, Health Physics

D. Orndorf, Manager, Chemistry

F. Curl, Manager, Nuclear Construction

J. Matsko, Manager, Outage Management Department

T. Lutkehaus, Manager, Maintenance Planning & Administration

.T. McGhee, Coordinator, Onsite Safety Committee

Ji Macdonald, Manager, System & Performance Engineering

K. Beatty, General Manager, Nuclear Support Unit

J. Arias, Director, Safety & Licensing

W. Kline, Manager, Nuclear Engineering Department

R. Brosi, Manager, Management Services

O. Arredondo, Manager, Nuclear Procurement

NBC

D. Kern, SRI

G. Dentel, Ri

F. Lyon, RI -

,

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-. - . - - . . . .-. - _ _= - - - - - ._-_.-- - -.-- ._ .-. - - - -_ _-_ .

4

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INSPECTION PROCEDURES USED

.

IP 37551: Onsite Engineering

IP 61726: Surveillance Observation

IP 62707: Maintenance Observation l

lP 71707: Plant Operations .

IP 71750:- Plant Support  !

!

IP 73753: Inservice inspection

IP 83750: Occupational Exposure

IP 84750: Radioactive Waste Treatment, and Effluent and Environmental

Monitoring

IP 92700: Onsite Follow up of Written Reports of Nontoutine Events at Power  ;

Reactor Facilities

IP 92901: Follow up - Operations

IP 92902: Follow up - Maintenance i

IP 92903: Follow up - Engineering

,

t

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. . _ . _ _ _ _ _ _ _. _ _ - _ - _ . _ _ _ _ _ _ _ _ _ . . _ _ _ _ _ _ . _ - - _ _ _ . _ _ _

.-

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29 i

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ITEMS OPENED, CLOSED AND DISCUSSED

>

Ooened

50 412/97 08-03 URI Test Control High Head Safsty injection Pumps

(Section E2.1)

!

50-334/97-08-04 VIO Workers were Unaware of Radiological Conditione in i

their Work and Transit Areas in the RCA (Section R1)

50 334/97 08-05 VIO Failure to Calibrate RMS in Accordance with Propor

Procedures (Section R2.1)

,

50 334/97 08-06 IFl Documentation of RMS Detector Failures (Section R2.1) ,

Ooened/ Closed

50 334/97 08 01 NCV Mispositioning of RCCA in the SFP (Section 01.2)

50 334 and 312/97 08 02 NCV implementation of the Retired Equipment Program

(Section 03.1)

Closed

50 334/96-012 LER Entry into Technical Specification 3.0.3 Due to Isolation

of Control Room Emergency Breathing Air Pressurization

System (Section 08.1)

50 334/97-004-01 LER Failure to Test Post DBA Hydrogen Control System

Recombiners in Accordance With Technical

Specifications (Section 08.2) ,

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50 334/97-032 LER EDG Automatic Start During Bus Transfer from Unit to

System Station Transformer (Section 08.3)

50 334 and 412/97-07 04 URI Adequacy of the High Head Safety injection Pump

! Surveillance Tests to Ensure Operability (Section E2.1)

50 334/96-05 02 VIO Inadequate Calibration for UT examinations

,

(Section E8.2)

50 334 and 412/97-07-01 URI implementation of the Retired Equipment Program

(Section 03.1)

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LIST OF ACRONYMS USED

1R12 Unit 112th Refueling Outage

AFW Auxiliary Feedwater Pump

ALARA As Low As is Reasonably Achievable

ANil Authorized Nuclear Inservice inspector

AOP Abnormal Operating Procedure

l

AVB Anti Vibration Bar i

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BVPS Bebver Valley Power Station

CR Condition Report

CREBAPS Control Room Emergency Breathing Air Pressurization System

DCP Design Change Package

DLC Duquesne Light Company

EDG Emergency Diesel Generator ,

eel Est stated Enforcement issue ,

EOP Emergency Operating Procedure

.ESF Engineered Safety Feature

HEPA High efficiency Particulate Air

HHSl High Head Safety injection

l&C Instrumentation and Controls

ISI Inservice Inspection '

IST Inservice Surveillance Test

LER Licensee Event Report

MPFF Maintenance Preventable Functional Failures

MSP Maintenance Surveillance Procedure

MT Magnetic Particulate

NCV Non-Cited Violation

NDE Nondestructive Examination

NIS Nuclear Instrumentation System

NIST National Institute of Standards and Technology

NPDAPS Nuclear Power Division Administrative Procedure ,

NVLAP Nuclear Voluntary Laboratory Accreditation Program

ODCM Offsite Dose Calculation Manual

ODSCC Outside Diameter Stress Corrosion Cracking

OST Operational Surveillance Test

PCE Personnel Contamination Event

PDR Public Document Room

PMP Preventive Maintenance Procedure

PT Liquid Penetrant

PWSCC Primary Water Stress Corrosion Cracking

QA Cuality Assurance

OC Quality Control

OSU Quality Services Unit

RCA- Radiological Controlled Area

RCCA Rob Jiuster Control Assembly

RMS Radiation Monitoring System

RP&C Radiological Protection and Chemistry

RTS Reactor Trip System

. . _ _ _ _ _ _ . _ _ . _ _ _ _ _. __ _ _ . _ _ __ .- . . . _

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31

RWP Radiological Work Permit

SFP Spent Fuel Pool

SG Steam Generator

SLCRS _ Supplementary Leak Collection and Release System

SSPS- Solid State Protection System

TER ~ Technical Evaluation Report

-TS = Technical Specification

TSP Tube Support Plate

TTS Tubesheet

UFSAR Updated Final Safety Analysic Report

URI Unresolved item

UT Ultrasonic Examination

VIO Violation -

VT' Visual Examination

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