ML092800205: Difference between revisions

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| number = ML092800205
| number = ML092800205
| issue date = 10/07/2009
| issue date = 10/07/2009
| title = E-mail, Request for Additional Information Regarding Steam Generator Tube Inservice Inspections During the 2008 Rfo(Tac ME0313)
| title = E-mail, Request for Additional Information Regarding Steam Generator Tube Inservice Inspections During the 2008 RFO
| author name = Wilkins L E
| author name = Wilkins L
| author affiliation = NRC/NRR/DORL/LPLIV
| author affiliation = NRC/NRR/DORL/LPLIV
| addressee name = Edwards M L
| addressee name = Edwards M
| addressee affiliation = Omaha Public Power District
| addressee affiliation = Omaha Public Power District
| docket = 05000285
| docket = 05000285
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:From: Wilkins, Lynnea Sent: Wednesday, October 07, 2009 10:51 AM To: EDWARDS, MICHAEL L Cc: HANSHER, BILL R; HUTCHINSON, TEDDY J; Lent, Susan; Burkhardt, Janet  
{{#Wiki_filter:From:                           Wilkins, Lynnea Sent:                           Wednesday, October 07, 2009 10:51 AM To:                             EDWARDS, MICHAEL L Cc:                             HANSHER, BILL R; HUTCHINSON, TEDDY J; Lent, Susan; Burkhardt, Janet


==Subject:==
==Subject:==
Request for Additional Information Regarding Steam Generator Tube Inservice Inspections During the 2008 RFO Mike, By letter dated December 9, 2008, (Agencywide Documents Access & Management System (ADAMS) Accession No. ML083440629), Omaha Public Power District (the licensee), submitted information summarizing the results of steam generator tube inspections performed at Fort Calhoun Station Steam Generator during the 2008 Refueling Outage.
Request for Additional Information Regarding Steam Generator Tube Inservice Inspections During the 2008 RFO
The US Nuclear Regulatory Commission (NRC) staff has determined that the following additional information is needed to complete the evaluation. This request was discussed with Teddy Hutchinson of your staff on October 6, 2009, and it was agreed that a response would be provided within 7 days of receipt of this email. If circumstances result in the need to revise the requested response date, please contact me at (301) 415-1377 or via e-mail at Lynnea.Wilkins@nrc.gov. Thanks, Lynnea Lynnea Wilkins Project Manager NRR/DORL/LPL4 301-415-1377 301-415-1222(fax)  
: Mike, By letter dated December 9, 2008, (Agencywide Documents Access & Management System (ADAMS) Accession No. ML083440629), Omaha Public Power District (the licensee), submitted information summarizing the results of steam generator tube inspections performed at Fort Calhoun Station Steam Generator during the 2008 Refueling Outage.
 
The US Nuclear Regulatory Commission (NRC) staff has determined that the following additional information is needed to complete the evaluation. This request was discussed with Teddy Hutchinson of your staff on October 6, 2009, and it was agreed that a response would be provided within 7 days of receipt of this email. If circumstances result in the need to revise the requested response date, please contact me at (301) 415-1377 or via e-mail at Lynnea.Wilkins@nrc.gov.
---------------------------------------------------------------------------------------------------------------- REQUEST FOR ADDITIONAL INFORMATION
: Thanks, Lynnea Lynnea Wilkins Project Manager NRR/DORL/LPL4 301-415-1377 301-415-1222(fax)
REQUEST FOR ADDITIONAL INFORMATION
: 1. Please provide the following information pertaining to your steam generators (SGs):
: 1. Please provide the following information pertaining to your steam generators (SGs):
* a tubesheet map depicting the row and column numbers
* a tubesheet map depicting the row and column numbers
* a sketch of the SG depicting the tube support naming convention
* a sketch of the SG depicting the tube support naming convention
* the thickness of the tubesheet with and without cladding
* the thickness of the tubesheet with and without cladding
* the design/size of the anti-vibration bars (i.e., rectangular shape, 2 inches wide, 0.1 inches thick) 2. On page 3 of your report, it states that the broached supports are chamfered at both the top and bottom edges. Please describe the exact design. 3. Please discuss whether the two bulges identified in two different tubes in SG RC-2B were present in the baseline inspection and discuss the cause of the bulges. 4. On page 9 of your report, it states that three dents/dings were identified in three different tubes in SG RC-2A and one new dent was identified in SG RC-2B. Please discuss the cause and the severity (voltage) of the dents.  
* the design/size of the anti-vibration bars (i.e., rectangular shape, 2 inches wide, 0.1 inches thick)
: 2. On page 3 of your report, it states that the broached supports are chamfered at both the top and bottom edges. Please describe the exact design.
: 3. Please discuss whether the two bulges identified in two different tubes in SG RC-2B were present in the baseline inspection and discuss the cause of the bulges.
: 4. On page 9 of your report, it states that three dents/dings were identified in three different tubes in SG RC-2A and one new dent was identified in SG RC-2B. Please discuss the cause and the severity (voltage) of the dents.


This e-mail contains Omaha Public Power District's confidential and proprietary information and is for use only by the intended recipient. Unless explicitly stated otherwise, this e-mail is not a contract offer, amendment, nor acceptance. If you are not the intended recipient you are notified that disclosing, copying, distributing or taking any action in reliance on the contents of this information is strictly prohibited.
This e-mail contains Omaha Public Power District's confidential and proprietary information and is for use only by the intended recipient. Unless explicitly stated otherwise, this e-mail is not a contract offer, amendment, nor acceptance. If you are not the intended recipient yo u are notified that disclosing, copying, distributing or taking any action in reliance on the content s of this information is strictly prohibited.
This e-mail contains Omaha Public Power District's confidential and proprietary information and is for use only by the intended recipient. Unless explicitly stated otherwise, this e-mail is not a contract offer, amendment, nor acceptance. If you are not the intended recipient you are notified that disclosing, copying, distributing or taking any action in reliance on the contents of this information is strictly prohibited.
This e-mail contains Omaha Public Power District's confidential and proprietary information and is for use only by the intended recipient. Unless explicitly stated otherwise, this e-mail is not a contract offer, amendment, nor acceptance. If you are not the intended recipient yo u are notified that disclosing, copying, distributing or taking any action in reliance on the content s of this information is strictly prohibited.
E-mail Properties Mail Envelope Properties (F371D08C516DE74F81193E6D891DC4AF1EBFB5AF7D)  
E-mail Properties Mail Envelope Properties (F371D08C516DE74F81193E6D891DC4AF1EBFB5AF7D)


==Subject:==
==Subject:==
Request for Additional Information Regarding Steam Generator Tube Inservice Inspections During the 2008 RFO  
Request for Additional Information Regarding Steam Generator Tube Inservice Inspections During the 2008 RFO Sent Date:       10/7/2009 10:51:11 AM Received Date:        10/7/2009 10:51:11 AM From:           Wilkins, Lynnea Created By:       Lynnea.Wilkins@nrc.gov Recipients:
 
Sent Date:       10/7/2009 10:51:11 AM Received Date:        10/7/2009 10:51:11 AM From:               Wilkins, Lynnea  
 
Created By:         Lynnea.Wilkins@nrc.gov  
 
Recipients:
medwards@oppd.com (EDWARDS, MICHAEL L)
medwards@oppd.com (EDWARDS, MICHAEL L)
Tracking Status: None bhansher@oppd.com (HANSHER, BILL R)
Tracking Status: None bhansher@oppd.com (HANSHER, BILL R)
Tracking Status: None tjhutchinson@oppd.com (HUTCHINSON, TEDDY J)
Tracking Status: None tjhutchinson@oppd.com (HUTCHINSON, TEDDY J)
Tracking Status: None Susan.Lent@nrc.gov (Lent, Susan)
Tracking Status: None Susan.Lent@nrc.gov (Lent, Susan)
Tracking Status: None Janet.Burkhardt@nrc.gov (Burkhardt, Janet)                Tracking Status: None
Tracking Status: None
 
Post Office:
HQCLSTR02.nrc.gov
 
Files                Size        Date & Time
 
MESSAGE        18325        10/7/2009
 
Options Expiration Date:
Priority:                        olImportanceNormal ReplyRequested:        False Return Notification:        False


Sensitivity:         olNormal Recipients received:}}
Janet.Burkhardt@nrc.gov (Burkhardt, Janet)
Tracking Status: None Post Office:
HQCLSTR02.nrc.gov Files          Size      Date & Time MESSAGE          18325      10/7/2009 Options Expiration Date:
Priority:              olImportanceNormal ReplyRequested:      False Return Notification:      False Sensitivity:     olNormal Recipients received:}}

Latest revision as of 09:12, 12 March 2020

E-mail, Request for Additional Information Regarding Steam Generator Tube Inservice Inspections During the 2008 RFO
ML092800205
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 10/07/2009
From: Lynnea Wilkins
Plant Licensing Branch IV
To: Edwards M
Omaha Public Power District
Wilkins, L E, NRR/DORL/LPL4, 415-1377
References
TAC ME0313
Download: ML092800205 (3)


Text

From: Wilkins, Lynnea Sent: Wednesday, October 07, 2009 10:51 AM To: EDWARDS, MICHAEL L Cc: HANSHER, BILL R; HUTCHINSON, TEDDY J; Lent, Susan; Burkhardt, Janet

Subject:

Request for Additional Information Regarding Steam Generator Tube Inservice Inspections During the 2008 RFO

Mike, By letter dated December 9, 2008, (Agencywide Documents Access & Management System (ADAMS) Accession No. ML083440629), Omaha Public Power District (the licensee), submitted information summarizing the results of steam generator tube inspections performed at Fort Calhoun Station Steam Generator during the 2008 Refueling Outage.

The US Nuclear Regulatory Commission (NRC) staff has determined that the following additional information is needed to complete the evaluation. This request was discussed with Teddy Hutchinson of your staff on October 6, 2009, and it was agreed that a response would be provided within 7 days of receipt of this email. If circumstances result in the need to revise the requested response date, please contact me at (301) 415-1377 or via e-mail at Lynnea.Wilkins@nrc.gov.

Thanks, Lynnea Lynnea Wilkins Project Manager NRR/DORL/LPL4 301-415-1377 301-415-1222(fax)

REQUEST FOR ADDITIONAL INFORMATION

1. Please provide the following information pertaining to your steam generators (SGs):
  • a tubesheet map depicting the row and column numbers
  • a sketch of the SG depicting the tube support naming convention
  • the thickness of the tubesheet with and without cladding
  • the design/size of the anti-vibration bars (i.e., rectangular shape, 2 inches wide, 0.1 inches thick)
2. On page 3 of your report, it states that the broached supports are chamfered at both the top and bottom edges. Please describe the exact design.
3. Please discuss whether the two bulges identified in two different tubes in SG RC-2B were present in the baseline inspection and discuss the cause of the bulges.
4. On page 9 of your report, it states that three dents/dings were identified in three different tubes in SG RC-2A and one new dent was identified in SG RC-2B. Please discuss the cause and the severity (voltage) of the dents.

This e-mail contains Omaha Public Power District's confidential and proprietary information and is for use only by the intended recipient. Unless explicitly stated otherwise, this e-mail is not a contract offer, amendment, nor acceptance. If you are not the intended recipient yo u are notified that disclosing, copying, distributing or taking any action in reliance on the content s of this information is strictly prohibited.

This e-mail contains Omaha Public Power District's confidential and proprietary information and is for use only by the intended recipient. Unless explicitly stated otherwise, this e-mail is not a contract offer, amendment, nor acceptance. If you are not the intended recipient yo u are notified that disclosing, copying, distributing or taking any action in reliance on the content s of this information is strictly prohibited.

E-mail Properties Mail Envelope Properties (F371D08C516DE74F81193E6D891DC4AF1EBFB5AF7D)

Subject:

Request for Additional Information Regarding Steam Generator Tube Inservice Inspections During the 2008 RFO Sent Date: 10/7/2009 10:51:11 AM Received Date: 10/7/2009 10:51:11 AM From: Wilkins, Lynnea Created By: Lynnea.Wilkins@nrc.gov Recipients:

medwards@oppd.com (EDWARDS, MICHAEL L)

Tracking Status: None bhansher@oppd.com (HANSHER, BILL R)

Tracking Status: None tjhutchinson@oppd.com (HUTCHINSON, TEDDY J)

Tracking Status: None Susan.Lent@nrc.gov (Lent, Susan)

Tracking Status: None

Janet.Burkhardt@nrc.gov (Burkhardt, Janet)

Tracking Status: None Post Office:

HQCLSTR02.nrc.gov Files Size Date & Time MESSAGE 18325 10/7/2009 Options Expiration Date:

Priority: olImportanceNormal ReplyRequested: False Return Notification: False Sensitivity: olNormal Recipients received: