ML20010C862: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
 
(StriderTol Bot change)
 
Line 56: Line 56:
E $l )N i @ oescaintioN @
E $l )N i @ oescaintioN @
l 10 NA            S                            PDR          ;
l 10 NA            S                            PDR          ;
68 69 IllltI{{liIil}
68 69 IllltI((liIil}
33 %
33 %
N AstE cr paE*Aa :n R. A. PALMER                                                                                    ~
N AstE cr paE*Aa :n R. A. PALMER                                                                                    ~
7HCNE:                                                    .}}
7HCNE:                                                    .}}

Latest revision as of 02:02, 27 February 2020

LER 81-027/03L-0:on 810717,three Containment Isolation Valves Were Identified to Be Leaking & Repaired Before Having Been Quantified.Cause Not Stated.Updated Rept Will Be Submitted Upon Receipt of Insp Rept
ML20010C862
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 08/14/1981
From: Palmer R
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20010C859 List:
References
LER-81-027-03L, LER-81-27-3L, NUDOCS 8108210114
Download: ML20010C862 (1)


Text

- - - - -

accasce evcni neroni 4 CONTROL BLOCK: l l l l I l

.h l (PLEASE PRINT OR TYPE ALL REQUlf ED INFORMATION)

> Iif4*lJM1 II D l C l CJ 1 UCENsit COOC 14 l@l O l 0 l 01010 15 l 01010 l 010 l oM i@l26 41 UCENSE uCENSE NVM8EM I l 111 TY,E l 140 l@l57 jail sd l

ON T E d

"un[ l I j@l0 l 5 l 0l 01013 l 1 l5 l@l 64 61 oOCK ET NVM8ER 66 69 0 EVE'AT l 7 loATE 1 171811 @loInllla19 14 75 REPoAr o ATE li l@

80 EVENT DESCalPTION AND PROBA8LE CONSEQUENCES h g l DURING STABILIZATION PERIOD PRIOR TO STARTING 24 HOUR ILRT TYPE "A" TEST, THREE CONTAINMENTi ,

gi ISOLATION VALVES WERE IDENTIFIED TO BE LEAKING AND REPAIRED. THE NRC INSPECTOR INTERI'lET-l 3;,, i ED THIS TO BE CONTRARY TO 10 CFR-50 APPENDIX J. THE LEAKS FROM THESE VALVES SHOULD HAVE l 3, q g BEEN QUANTIFIED BEFORE REPAIRS, AS PER THE NRC INSPECTOR. l o 16 l l l TI Tl I _

l o 181 l _

as 80 E Coot sueC E CoMPoNGNT CocE SueCco'E su E E ULI D l@ Lxj@ I z l@ l Z I z I z Iz I ZI z l@ I ZI@ LZJ @

u

.v.Nrv[4a S'c31'a'r' a

C d**' 'r%' "'"S' *

(gj

@ ,a g,,,o Ial11

, 21 22

[-j 23 l 0 12 1 71 24 Je 27 10131 28 23 l Ll 30 l-l 36 l0 l 32 N AC Q oNP Nr ME 3 HOURS 22 s8 t PoR S. SuPet MANUFAC RER LLJ@l 33 x 1@

34 I z j@

34 I z l@

l 0101010 l 31 40 l41 Nl@ lNl@

42 l43 Zl@ lZl9l9l9l@

44 47 CAU$E DESCRIPTION AND CORRECTIVE ACTIONS h i l o I l UI' DATED LER WILL BE SUBillTTED WHEN I.E. INSPECTION REPORT IS RECEIVED AND ANSWERED. l t Iii l I

@l l EI I i i4 I I l

's #2E7 rowea orwen status @ Es'*o 18v' oiscoveny oesCnierioN l

i I s* I* di @ l 0l 0 l 0 ' l@l" NA l l B l@l SURVEILLANCE TERT l

4Criviry Co'0 TENT

=strasso er asLarss i.oCArios on aetsass @

NA AucuNr on Activery @l l NA E L.Z.J

@ l zl@l'* " '

l

.ensoNuct exposuAss suunta tves orsCniertoN@

ITil'[0* l 0 l 0 l@[Z_J@l

NA l

,. m so~ N.'c' i N3u'n'i c s suune, cesCnierioN@

E 1010101@l NA l tos,s s ca o ACf a MClurV

] l 'Z* l@l NA l

ausuNrv 91')8210114 810814 NRC WE ONLY issuso PDR ADOCK 05000315 ,

E $l )N i @ oescaintioN @

l 10 NA S PDR  ;

68 69 IllltI((liIil}

33 %

N AstE cr paE*Aa :n R. A. PALMER ~

7HCNE: .