ML17266A204: Difference between revisions

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| issue date = 05/12/1980
| issue date = 05/12/1980
| title = RO 335-80-25:on 800512,during Planned Secondary Plant Cooldown/Depressurization for Turbine Steam Seal Repair, Main Steam Header Would Not Depressurize Following MSIV Closure.Apparently Caused by Mispositioned Valve
| title = RO 335-80-25:on 800512,during Planned Secondary Plant Cooldown/Depressurization for Turbine Steam Seal Repair, Main Steam Header Would Not Depressurize Following MSIV Closure.Apparently Caused by Mispositioned Valve
| author name = WETHY C M
| author name = Wethy C
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
Line 14: Line 14:
| page count = 1
| page count = 1
}}
}}
=Text=
{{#Wiki_filter:cac  c ~ c'  ~ ~ I ~ ~ ~  ~ ~ ~ ~  ~ ~ Ccccvc                      0 ~  ~  ~ ~, ~ ~ ~ ~                r c ~
Q))~-PSX Ltr.    ))L. 4982 I
I  f'i ct f- r r>>  t c
c Copies tie:              Q)U, J))B, CA)l, 0.VZ,                      lou                                                                    c rc" (ct                  '>>
Df xsitc'I)S JH)3,                              CG)l, K.'iH, .fAS,      H).sU F'tci'.iT t          ic i =c>lii t  ~
                                                                                "'!0'( l2                                            ltay 1'c, 1940 TO:      Hr. J. P. O'Rail]y, Dirt.'.ctor, Hts".ion Of fico af Inspect:ion'and Eilri>l c U S            (uclear Hepulat:ory Ccit i ssion                ~
                                                                                'lt II Atlanta,              GA          30303 I:RG.'l:    lfr. C.      lf. Verity, Plant.                  l)attester                        c      )h CLKRK.
S t. Lucia                  P 1 a tat  DP)t 67  -
Plorida Potser                      6  Li')TL a      Co--pany l.limni, 1I I                                                c
==SUBJECT:==
ll)"l0 FQ)), PACSL)ILK THY'l)ISSIO;)                                    '1'0 CAl)PI)Qf PHA!)PY              )ti PARTAi3) l,"
nCC))R))3".)CE                  335-80-25 I:)OPERA))LE tlslV                        )3'CPAQQ      VALVE" I"e uo    is to confirm                        e)te telepltotla Ttotificntic'n .a'la                            vu  rli  ~  .tHC
,  doJicatod pllonc circuit                                a't 0343 an      5/12/80.
During        a  planneJ secondary plaiit.'coisl Juwtt/de)iresstirization rar riir n.".
it stcam seal            rcPair,                      was noted t')tat: t:ht tciain stoa< )ieader 4s.:<<l. iin                                    3 dcprossuriao follotsing .t)SIV c1oaure. Ar. a1".nut 3:15 P~tf on 5/l2s/80 investi~arion revealed that )sot)i:)SIV bypass valves were stucL itT tlirt
  'open'asiri.an. The st-.z nl liarli valves --crc sheared and r)ic v.ilveo worn inoperable borh electrically nnJ ...atlltal,ly                                                            t;lect:rical val z position inJicaticn in tho conrrcil r~".c."~ liaJ s)ti: nt otic valve to )ici 'siitit.'.
The ot:her was t:apped closed wir)tour. posi.t:inn indicaricn.
Since t)tc bypaa" valve is an int: gral. parr. oi i,ts rcspcctivc !)SIU, t'e plant was not in full cct=pliancc stir)i 'Recit $ pec' It shnuld he notad i~f                        t)tat t'hese are 3 lite)i ~sara iip .lines Ancl "ltattld
                                                                                                                    ~ 7 l    5 ()fSIV Qpershilikj)                  ~
Faigitificartt-saf ty filets 1 larit s)ititdci'sn't'LQ cc oMc:st tsns <:cs-.=oner-'t
                                                              ~
ar. 3:43 A)f          this date.
Xt appears that one valve was vis-'positioned                                                                dttring ttairttenancc ctiter secondary syst:en uart tip on 5/10/80 aiid t:li. s)taft shoarcd an thc at):ar when ir, was aporatccl fnz thc secondary sy t:ta;.t;sar.".;.tift.
An intsestightion is in progr~ss t:o dcaterciine the-asset cause of E)to rialfunction and final reiiu1ts including final carrecriva act:ion tsil.l )ic report:ed.
I'.
goo> 5.
H. )ht)ty, Plant                                Taper St. Lucie l'1ant Q N/HRJ/cc c}}

Latest revision as of 07:32, 24 February 2020

RO 335-80-25:on 800512,during Planned Secondary Plant Cooldown/Depressurization for Turbine Steam Seal Repair, Main Steam Header Would Not Depressurize Following MSIV Closure.Apparently Caused by Mispositioned Valve
ML17266A204
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 05/12/1980
From: Wethy C
FLORIDA POWER & LIGHT CO.
To:
References
982, NUDOCS 8005230377
Download: ML17266A204 (1)


Text

cac c ~ c' ~ ~ I ~ ~ ~ ~ ~ ~ ~ ~ ~ Ccccvc 0 ~ ~ ~ ~, ~ ~ ~ ~ r c ~

Q))~-PSX Ltr. ))L. 4982 I

I f'i ct f- r r>> t c

c Copies tie: Q)U, J))B, CA)l, 0.VZ, lou c rc" (ct '>>

Df xsitc'I)S JH)3, CG)l, K.'iH, .fAS, H).sU F'tci'.iT t ic i =c>lii t ~

"'!0'( l2 ltay 1'c, 1940 TO: Hr. J. P. O'Rail]y, Dirt.'.ctor, Hts".ion Of fico af Inspect:ion'and Eilri>l c U S (uclear Hepulat:ory Ccit i ssion ~

'lt II Atlanta, GA 30303 I:RG.'l: lfr. C. lf. Verity, Plant. l)attester c )h CLKRK.

S t. Lucia P 1 a tat DP)t 67 -

Plorida Potser 6 Li')TL a Co--pany l.limni, 1I I c

SUBJECT:

ll)"l0 FQ)), PACSL)ILK THY'l)ISSIO;) '1'0 CAl)PI)Qf PHA!)PY )ti PARTAi3) l,"

nCC))R))3".)CE 335-80-25 I:)OPERA))LE tlslV )3'CPAQQ VALVE" I"e uo is to confirm e)te telepltotla Ttotificntic'n .a'la vu rli ~ .tHC

, doJicatod pllonc circuit a't 0343 an 5/12/80.

During a planneJ secondary plaiit.'coisl Juwtt/de)iresstirization rar riir n.".

it stcam seal rcPair, was noted t')tat: t:ht tciain stoa< )ieader 4s.:<<l. iin 3 dcprossuriao follotsing .t)SIV c1oaure. Ar. a1".nut 3:15 P~tf on 5/l2s/80 investi~arion revealed that )sot)i:)SIV bypass valves were stucL itT tlirt

'open'asiri.an. The st-.z nl liarli valves --crc sheared and r)ic v.ilveo worn inoperable borh electrically nnJ ...atlltal,ly t;lect:rical val z position inJicaticn in tho conrrcil r~".c."~ liaJ s)ti: nt otic valve to )ici 'siitit.'.

The ot:her was t:apped closed wir)tour. posi.t:inn indicaricn.

Since t)tc bypaa" valve is an int: gral. parr. oi i,ts rcspcctivc !)SIU, t'e plant was not in full cct=pliancc stir)i 'Recit $ pec' It shnuld he notad i~f t)tat t'hese are 3 lite)i ~sara iip .lines Ancl "ltattld

~ 7 l 5 ()fSIV Qpershilikj) ~

Faigitificartt-saf ty filets 1 larit s)ititdci'sn't'LQ cc oMc:st tsns <:cs-.=oner-'t

~

ar. 3:43 A)f this date.

Xt appears that one valve was vis-'positioned dttring ttairttenancc ctiter secondary syst:en uart tip on 5/10/80 aiid t:li. s)taft shoarcd an thc at):ar when ir, was aporatccl fnz thc secondary sy t:ta;.t;sar.".;.tift.

An intsestightion is in progr~ss t:o dcaterciine the-asset cause of E)to rialfunction and final reiiu1ts including final carrecriva act:ion tsil.l )ic report:ed.

I'.

goo> 5.

H. )ht)ty, Plant Taper St. Lucie l'1ant Q N/HRJ/cc c