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| issue date = 06/07/1979
| issue date = 06/07/1979
| title = LER 79-017/03L-0 on 790509:1B Charging Pump Casing Block Contained Several Internal Cracks Centered Around Pressure Chambers.Caused by Suction Cavitation Resulting in Vibration.Pump Block Replaced
| title = LER 79-017/03L-0 on 790509:1B Charging Pump Casing Block Contained Several Internal Cracks Centered Around Pressure Chambers.Caused by Suction Cavitation Resulting in Vibration.Pump Block Replaced
| author name = SCHOPPMAN M A
| author name = Schoppman M
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:NRC PQRIrI 544 IT TTI LlCEIVSEE FVHIVT REPORT V.S NVCt 6AR RSOVLATOAY CO>>!MISSION
{{#Wiki_filter:NRC PQRIrI 544                                                                                                                     V. S NVCt 6AR RSOVLATOAY CO>>!MISSION IT TTI LlCEIVSEE FVHIVT REPORT I                    (PLEASS PRINT QR TYPS AI.L REQVIRSQ INPORMATIONI Q~
~o 3 CQN'T~O p 2 CQNTRQL, SLCCKI I I I I FILIS L ISI1Q20 0-9 UCLrr$44 CQCS I Ql" (PLEASS PRINT QR TYPS AI.L REQVIRSQ INPORMATIONI OI OIOI OIO-010 Qrt II Qi~IQi UCSIisa'i'IUM44R
CQNTRQL, SLCCKI                         I     I         I         Ql  "
'15 15 I aa-'454 TVPS i4 51~T 53!6 I I I I Qg 74 75 ilaPCrIT QAT4 0 Pum.casin block it was";;~lrQ 0 0 0>>Q~40 41 QQCK4 i HUMSSR 43 49 SVS>>T QATS 6VSNT QSSCRIPTIQN ANQ PRQIABL6 CQNS6QVSNC'6S QIQ Durin 1 armed re 1acement of the 1B Char in~02 found that the ol d block, contained several internal cracks centered around the um's ressure'hambers.
I
The cracks did not enetrate the block.This char in um block was bein re laced due to recent failures of the~as A an 1~pg T 3 9 Ia svsTau cAU54 cAU54 caMP.yALys CQQ4 cQQS suacaoa ccMpo>>SHTcaoa suacaoa suacaos S L<JS L~JS~+<"'r rS MES LrrS 9'0 II 11 11 1$'19 10$4CUa>>TIAI OCCUR IISNCS RSPQRT~.RSVISIQH 11 Ts 14 12, 15 11 11 ACTION PUTVRS SPPSCi sriUTQOWH+'TTACNM4>>T 4PRQW PRIMS COMP CQMPOHSHT TAKSH ACTICH CH PLANT A!4TIICO, NOVAS+22 SUSMITTSO PORlMSU8 SV JPLI4R MANUPAC VRrIR LrrS~xS.~iS MzS Lraoo.r EYES~YS~IQ~Ea 4 5 Q 14 15 14 3I S0 4 I 41 44 47'AVSS O6scRIPT!ON ANO CORRSCnv6 ACTIONS Q23 o.The cause.a ears to have-been-.vibration ca e b the um s.Suction dam enin devices accumulators will be install d all three um s to reduce cavitation.
    ~o              FILIS             L     ISI1Q20 0-                               OI OIOI OIO UCSIisa'i'IUM44R 010 15 Qrt II 15       I aa-'454 TVPS       i4 Qi~IQi 51 ~T   53 0>>
Preliminar installation work to install these accumulators at ower is com lete'and these accumulators will be installed shortl after deliver.The 1B um block was re laced.I 4 9 P Ac I LI.Y.IQ MSTIICO QP ST*IUS'5 PCWSR QTIISR STATVS p/01$CQVSRY i LtuQrr~00 Qi NA~C(Dr 1 10'$11 SS 45 Ja ACTIVITY COHTSRT RSLSASSO 01 RSLSA54 AAIQUNI'QP
3    9        UCLrr$44 CQCS CQN'T
~iVITY QS 6~Z Q22~ZQ25 NA I 3 9 14 11 IA 49 psA50>>HSL axpa5VA45 r Loooo rQ>>2 Q>>'A 5 11 11 11 Psil$0>>>>SL IHIU>143~o'" o"o 8" NA 9 I I 11 LC5$QP CR QAMAC'4 ia SACIUTY Q42 VPS CSSCRIPTIQH Z'Q 1'0 pvaLIC.T.:ssuao 04$CRI pT!c>>Qas LN ISA 01$CQVSRY 045CIIIPTICH Q2 S ecial Ins ection LQCATIQV OP RSLSA$4 Q26 NA 30 g I 4!0~NBA!6 QP PRSPARSR>906'Z 80~~&NA NA H.A.Scho man ao 30 NRC LCK ONLY I-'ll 44,49 IO 305 552-3802 REPORTABLE OCCURRENCE 335-79-17 LICENSEE EVENT REPORT PAGE TWO Additional Cause Descri tion and Corrective Action An engineering evaluation of the Charging and Volume Contro1 System (CVCS)operation and vibration was performed in September of 1977.This evaluation suggested that suction cavitation may be the cause of vibration within the system.Based on this,-plans were made to install pulsation dampening devices (accumulators) on the suction of each charging pump.Installation was scheduled to be performed during the 1980 refueling shutdown.On 9-2-78, the 1A charging pump was found to have a cracked casing (see LER 335-78-34).
    ~O                  ";;~lrQ 0   40             41 0
The procurement of materials to install the suction pulsation dampening devices was placed on.an expedited basis.The cracked casing was replaced with a new casing on 1-9-79.On 3-16-79, the 1C charging pump was found to have'cracked casing (see LER 335-79-11).
QQCK4 i HUMSSR                 43     49       SVS>>T QATS             74 0
Presently, the plant is shut down in the final stages of the 1979 refueling outage.Preliminary work on the CVCS was performed during this refueling outage'to enable installation of the pulsation dampening devices during full power operation later this year.During power operation, only one charging pump at a time will be removed from servic'e to install the pulsation dampening device on that pump.This allows install ation during power operation while still fulfilling Technical Specification requirements for the CVCS.Delivery of the pulsation dampening devices is presently scheduled for September, 1979.The devices will be installed shortly after delivery.Both the 1C and 18 Charging Pump Blocks were replaced during the 1979 refueling outage.The replacement blocks for all three pumps were of an improved design with fewer stress riser points (which reduces susceptability to cracking).}}
                                                                                                                                            !6 75 I      I    I ilaPCrIT QAT4 I            Qg p  2 6VSNT QSSCRIPTIQN ANQ PRQIABL6 CQNS6QVSNC'6S Durin               1 armed re 1acement                         of the QIQ 1B     Char       in     Pum      .casin block                    it    was
    ~02             found that the ol d block, contained several internal cracks centered around the um 's ressure'hambers.                                                 The cracks did not enetrate the block.
This char in                           um block was bein                             re laced due to recent failures of the
    ~as               A an           1 T       3 9 Ia svsTau             cAU54           cAU54                                                         caMP.           yALys
                                            '0 S                                                                      'r rS CQQ4               cQQS       suacaoa                     ccMpo>>SHTcaoa                   suacaoa           suacaos
      ~pg                                                        L<JS           L~JS ~+<                       "                           MES LrrS 9                       II             11               11                             1$         '19               10
                                                                                    $ 4CUa>>TIAI                           OCCUR IISNCS         RSPQRT         ~       . RSVISIQH 11                       Ts             14         12,           15                                     11           11 ACTION PUTVRS TAKSH ACTICH LrrS~xS.
SPPSCi CH PLANT
                                                    ~iS sriUTQOWH A!4TIICO, MzS NOVAS +22 Lraoo. r EYES
                                                                                                            +    'TTACNM4>>T SUSMITTSO 4PRQW PORlMSU8
                                                                                                                                      ~YS ~IQ ~Ea PRIMS COMP SV JPLI4R CQMPOHSHT MANUPAC VRrIR 4 5   Q 14                   15               14               3I                     S0     4I              41                                 44               47
                'AVSS O6scRIPT!ON                   ANO CORRSCnv6 ACTIONS                 Q23
: o.       The cause. a                       ears to have- been-.vibration ca                                       e     b the         um       s.         Suction           dam     enin           devices             accumulators                 will be install                   d all three um s to reduce cavitation. Preliminar installation work to install these accumulators at ower is com lete'and these accumulators will be installed shortl                                 after deliver . The 1B um block was re laced.
I 4   9 P Ac LI Y I   . .
QTIISR STATVS p/
IQ MSTIICO         QP 1
i ST*IUS LtuQrr ACTIVITY COHTSRT
                                  ~00 Qi 10
                                      '5 PCWSR 11 NA SS 01$ CQVSRY
                                                                                                        ~C(Dr 45         Ja S
01$ CQVSRY 045CIIIPTICH Q2 ecial Ins ection RSLSASSO 01 RSLSA54                           AAIQUNI'QP~iVITYQS                                                          LQCATIQV OP RSLSA$ 4 Q26 6     ~Z       Q22   ~ZQ25                             NA                                                              NA I     3   9               14             11                                           IA           49 psA50>>HSL axpa5VA45 r     Loooo             rQ>>     2     Q>>
                                                                                                      'A 5                     11       11         11                                                                                                                               30
                  ~o'" o"o 9                II 8"
Psil$ 0>>>>SL IHIU>143 11 NA ao LC5$ QP CR QAMAC'4 ia SACIUTY VPS       CSSCRIPTIQH                   Q42 g        Z'Q '0                                                                               NA 1                                                                                                                                                                        30 pvaLIC.T.                                                                                                                                     NRC LCK ONLY I      4
:ssuao LN ISA 04$ CRI pT!c>> Qas
                                !0 NA 44,49 I-'ll                    IO
                      ~         NBA!6 QP PRSPARSR                         H. A. Scho                   man                                             305         552-3802
>906'Z 80        ~~&
 
REPORTABLE OCCURRENCE     335-79-17 LICENSEE EVENT REPORT PAGE TWO Additional   Cause   Descri tion and Corrective Action An engineering evaluation of the Charging and Volume Contro1 System (CVCS) operation and vibration was performed in September of 1977. This evaluation suggested that suction cavitation may be the cause of vibration within the system. Based on this,-plans were made to install pulsation dampening devices (accumulators) on the suction of each charging pump. Installation was scheduled to be performed during the 1980 refueling shutdown.
On 9-2-78, the   1A charging pump was found to have a cracked casing (see LER 335-78-34). The procurement of materials to install the suction pulsation dampening devices was placed on. an expedited basis. The cracked casing was replaced with a new casing on 1-9-79. On 3-16-79, the 1C charging pump was found to have'     cracked casing (see LER 335-79-11).
Presently, the plant is shut down in the final stages of the 1979 refueling         '
outage. Preliminary work on the CVCS was performed during this refueling outage to enable installation of the pulsation dampening devices during full power operation later this year. During power operation, only one charging pump at a time will be removed from servic'e to install the pulsation dampening device on that pump. This allows install ation during power operation while still fulfilling Technical Specification requirements for the CVCS. Delivery of the pulsation dampening devices is presently scheduled for September, 1979. The devices will be installed shortly after delivery.
Both the   1C and 18   Charging Pump Blocks were replaced during the 1979 refueling outage. The replacement blocks for all three pumps were of an improved design with fewer stress riser points (which reduces susceptability to cracking).}}

Latest revision as of 10:06, 4 February 2020

LER 79-017/03L-0 on 790509:1B Charging Pump Casing Block Contained Several Internal Cracks Centered Around Pressure Chambers.Caused by Suction Cavitation Resulting in Vibration.Pump Block Replaced
ML17266A073
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 06/07/1979
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17206A852 List:
References
LER-79-017-03L, LER-79-17-3L, NUDOCS 7906180555
Download: ML17266A073 (2)


Text

NRC PQRIrI 544 V. S NVCt 6AR RSOVLATOAY CO>>!MISSION IT TTI LlCEIVSEE FVHIVT REPORT I (PLEASS PRINT QR TYPS AI.L REQVIRSQ INPORMATIONI Q~

CQNTRQL, SLCCKI I I I Ql "

I

~o FILIS L ISI1Q20 0- OI OIOI OIO UCSIisa'i'IUM44R 010 15 Qrt II 15 I aa-'454 TVPS i4 Qi~IQi 51 ~T 53 0>>

3 9 UCLrr$44 CQCS CQN'T

~O ";;~lrQ 0 40 41 0

QQCK4 i HUMSSR 43 49 SVS>>T QATS 74 0

!6 75 I I I ilaPCrIT QAT4 I Qg p 2 6VSNT QSSCRIPTIQN ANQ PRQIABL6 CQNS6QVSNC'6S Durin 1 armed re 1acement of the QIQ 1B Char in Pum .casin block it was

~02 found that the ol d block, contained several internal cracks centered around the um 's ressure'hambers. The cracks did not enetrate the block.

This char in um block was bein re laced due to recent failures of the

~as A an 1 T 3 9 Ia svsTau cAU54 cAU54 caMP. yALys

'0 S 'r rS CQQ4 cQQS suacaoa ccMpo>>SHTcaoa suacaoa suacaos

~pg L<JS L~JS ~+< " MES LrrS 9 II 11 11 1$ '19 10

$ 4CUa>>TIAI OCCUR IISNCS RSPQRT ~ . RSVISIQH 11 Ts 14 12, 15 11 11 ACTION PUTVRS TAKSH ACTICH LrrS~xS.

SPPSCi CH PLANT

~iS sriUTQOWH A!4TIICO, MzS NOVAS +22 Lraoo. r EYES

+ 'TTACNM4>>T SUSMITTSO 4PRQW PORlMSU8

~YS ~IQ ~Ea PRIMS COMP SV JPLI4R CQMPOHSHT MANUPAC VRrIR 4 5 Q 14 15 14 3I S0 4I 41 44 47

'AVSS O6scRIPT!ON ANO CORRSCnv6 ACTIONS Q23

o. The cause. a ears to have- been-.vibration ca e b the um s. Suction dam enin devices accumulators will be install d all three um s to reduce cavitation. Preliminar installation work to install these accumulators at ower is com lete'and these accumulators will be installed shortl after deliver . The 1B um block was re laced.

I 4 9 P Ac LI Y I . .

QTIISR STATVS p/

IQ MSTIICO QP 1

i ST*IUS LtuQrr ACTIVITY COHTSRT

~00 Qi 10

'5 PCWSR 11 NA SS 01$ CQVSRY

~C(Dr 45 Ja S

01$ CQVSRY 045CIIIPTICH Q2 ecial Ins ection RSLSASSO 01 RSLSA54 AAIQUNI'QP~iVITYQS LQCATIQV OP RSLSA$ 4 Q26 6 ~Z Q22 ~ZQ25 NA NA I 3 9 14 11 IA 49 psA50>>HSL axpa5VA45 r Loooo rQ>> 2 Q>>

'A 5 11 11 11 30

~o'" o"o 9 II 8"

Psil$ 0>>>>SL IHIU>143 11 NA ao LC5$ QP CR QAMAC'4 ia SACIUTY VPS CSSCRIPTIQH Q42 g Z'Q '0 NA 1 30 pvaLIC.T. NRC LCK ONLY I 4

ssuao LN ISA 04$ CRI pT!c>> Qas

!0 NA 44,49 I-'ll IO

~ NBA!6 QP PRSPARSR H. A. Scho man 305 552-3802

>906'Z 80 ~~&

REPORTABLE OCCURRENCE 335-79-17 LICENSEE EVENT REPORT PAGE TWO Additional Cause Descri tion and Corrective Action An engineering evaluation of the Charging and Volume Contro1 System (CVCS) operation and vibration was performed in September of 1977. This evaluation suggested that suction cavitation may be the cause of vibration within the system. Based on this,-plans were made to install pulsation dampening devices (accumulators) on the suction of each charging pump. Installation was scheduled to be performed during the 1980 refueling shutdown.

On 9-2-78, the 1A charging pump was found to have a cracked casing (see LER 335-78-34). The procurement of materials to install the suction pulsation dampening devices was placed on. an expedited basis. The cracked casing was replaced with a new casing on 1-9-79. On 3-16-79, the 1C charging pump was found to have' cracked casing (see LER 335-79-11).

Presently, the plant is shut down in the final stages of the 1979 refueling '

outage. Preliminary work on the CVCS was performed during this refueling outage to enable installation of the pulsation dampening devices during full power operation later this year. During power operation, only one charging pump at a time will be removed from servic'e to install the pulsation dampening device on that pump. This allows install ation during power operation while still fulfilling Technical Specification requirements for the CVCS. Delivery of the pulsation dampening devices is presently scheduled for September, 1979. The devices will be installed shortly after delivery.

Both the 1C and 18 Charging Pump Blocks were replaced during the 1979 refueling outage. The replacement blocks for all three pumps were of an improved design with fewer stress riser points (which reduces susceptability to cracking).