ML17266A158: Difference between revisions

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| issue date = 03/17/1980
| issue date = 03/17/1980
| title = LER 80-010/03L-0:on 800217,during 100% Power Operation, Control Element Assembly 65 Dropped to Full Insertion When Selected to Manual Insertion for A.S.I. Damping.Cause Undetermined.Assembly Operated Properly in Normal Position
| title = LER 80-010/03L-0:on 800217,during 100% Power Operation, Control Element Assembly 65 Dropped to Full Insertion When Selected to Manual Insertion for A.S.I. Damping.Cause Undetermined.Assembly Operated Properly in Normal Position
| author name = SCHOPPMAN M A
| author name = Schoppman M
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:NRC FORM DSBi IT 775 LlCENSEE EVENT REPORT U~S NUCLEAR'REGULATORY COVIMISSION CONTROI;BLOCK'I,'Q{PLEASE PRINT OR TYPE*I.L REQUIRED'INPORMATIONI 3i LICZtISZZ CODE Q, CON, i~o.I'lZ..I S L-.tS.I lt 2 0 7 310, I.ICZiiSE TYPE Joi$1 AT$3 LICENSE tIW48f il Ol:-Ol OIO I 0'10-0 0 i 4 1 1i ll 1Qi~lQi P~O2'i''C~O~ii>>0 61 COCKET NUMSE R.EVENT O*rs 14 15 RZPi AT Q*TZ 50 VENT OESCRIPTION'AAIO PROBABL CONSECUE.4CES Oio During.100tP power operation,CEA.
{{#Wiki_filter:NRC FORM DSBi                                                                                                               U~S NUCLEAR'REGULATORYCOVIMISSION IT 775 LlCENSEE EVENT REPORT CONTROI; BLOCK' I,'Q                     {PLEASE PRINT OR TYPE         *I.LREQUIRED'INPORMATIONI
65 dropped to full insertion when selected~o, 3.to manual insertion for A S.I damping..ACTION in accordance-with Tech Spec., 3.1 3'.f was'niefated and reactor power was reduced.CEA 65 was~o s restored to.its'ormal osition within'ne hour.The reactor was returned to 100X power.This is the si'xth occurrence.
  ~o. I   'lZ..I             S     L-.tS.I     ltQ,2     0     Ol: -   Ol OIO       I 0'10       -     0 0 0,  i 4     1       1i   ll 1Qi~lQi 7
of a dropped CEA for which~o 2 the cause is unknown.See LEP.'s 335-77-6 78-20 78-46 79-2 and 79-27.)l~OS%9 T 3 30 SYSTZAZ CAVSS CAI'Sf CQMr.YA Lv s CQOE CCOE SUSCDOf C~WPC4fN T CQOE SVSCDOA SU8C f~RB Gi~xQii~zQ ii 0 Rl 0 R v E Qw~zQii~z'9 10 11 11.IS 19 20 SECVEIITIAI OCCUAIIEMCZ REPORT S Z'I i 5 I Q N LERIRO SVZMl'YEAR CEPQRT 40, Coos TYPS NQ.Q""" LILLtI LJ...LILL'I~ID L~J L00>l'-L~J I=I 21'2 28 12 TS'7 20 2 I ACMQN PUY"Rs.3 PrifCT'tiUTQOYAV
P CON, i 31 3i          LICZtISZZ CODE 61 VENT OESCRIPTION'AAIO PROBABL CONSECUE.4CES Oio i
*l~'CRUZ NT 4PROM PSIMs COMP, TAKEN AC IQN O.'I PLANT UZTIiQO, NOVAS Q22 SUSMI~TZQ PQR'IBUS.SUSoLIZR I-'lSI-"S LJS Lar~IXS LJS LJS JJ 25 28 Jt 4'7 CAUSE OESCRIPTION ANO CORRECTIVE
COCKET NUMSE R.
~iONS Q27 No cause could be d'etermined for the CEA.drop and no other abnorm'al conditions were found.CEA 65 o crated ro erl when restored to its normal osition and has erformed normall ever since 1 8-9*11 11 LCSS Or CR DAMAGE.0 PACIuTY'c~
                                                                                      ''C~O~ii>>
TYPE Qf SCRIPTIO4 EK'ZIO2 t 3 7'O PUSLICITY KH LHM 2 9 9'IO NA NA NAME OF PREPARER M..A.Schoppman 3 9i P AC I LITY 14ZTNOO Or srAivs$1 PQYIZ R'TItf R STATUS~DISCOvERY E Qi~ll 0 0 Qi.NA+AQLi 9 10 12 12 44 45 ACTIVITY CQNTZNT RZLSASZO Or RELEASE AIZOVNT Qr Acr VITY GS'~ZQDD~ZQS.NA 7 3i9 10 If 44.45 Pf RSQAINPI, ilKPQSURE Si~0-I 0 0 Qif~ZQs NA t 11 PERSQNttf L INJI'Rif5 NUtPSZR<DZSCRIPTICIIQAI Zai~oo 0Q~NA QISCQV~aV QZ SCRIPT:"4.0 erator Observation:
LICENSE tIW48fil EVENT O*rs           14 I.ICZiiSE TYPE Joi 15     RZPi AT Q*TZ
LOCATION OPR I.EASE Q NA NRC SECNI.V!!!!'I I 6L.59 POEl~305) 552-3802 ZO 30}}
                                                                                                                                                              $1    AT $ 3 50 0
  ~O2 During.         100tP     power operation,CEA. 65 dropped to                                     full insertion                 when selected
  ~o,   3           .to manual insertion                       for A S.I               damping..           ACTION         in   accordance-             with     Tech Spec., 3.1             3'.f         was'niefated and reactor power                                     was reduced.                 CEA 65 was
  ~o     s           restored to.               its'ormal osition within'ne hour.                                             The       reactor         was   returned to 100X power.                     This is the si'xth occurrence. of a dropped                                             CEA     for   which
  ~o     2           the cause             is     unknown.             See LEP.'s 335-77-6                       78-20         78-46           79-2       and       79-27.)l
                                                                                ~ 4'7
  ~OS
            % 9                                                                                                                                                                     30 SYSTZAZ           CAVSS         CAI'Sf                                                   CQMr.           YALv s CQOE             CCOE       SUSCDOf                   C~WPC4fN T CQOE                 SVSCDOA         SU8C   f T        3
                                      ~RB 9        10 Gi     ~xQii         ~zQ ii 0                 Rl 0 R v           E     Qw     ~zQii           ~z' 11           11                                             IS         19             20 SECVEIITIAI                         OCCUAIIEMCZ         REPORT                     S Z'I i 5 I Q N SVZMl'YEAR Q "" LILLtI LERIRO                                            CEPQRT 40,                             Coos               TYPS                       NQ.
                          "                                 LJ...LILL'I~ID                                       L00>l'-
21'2PrifCT'tiUTQOYAV                            28 L~J 12           TS'7                 L~J 20 I=I 2I ACMQN PUY"Rs.                 3 UZTIiQO,                                *lSUSMI
                                                                                                              'CRUZ NT       4PROM         PSIMs COMP,
                    'lSI
                                                                                                            ~
TAKEN AC IQN                 O.'I PLANT I
JJ "S LJS Lar Jt  25              28 NOVAS Q22                ~ TZQ IXS LJS LJS PQR'IBUS.        SUSoLIZR CAUSE OESCRIPTION ANO CORRECTIVE                       ~iONS   Q27 No cause             could be d'etermined                   for the           CEA. drop and no other abnorm'al conditions were found.                               CEA 65 o           crated           ro   erl       when       restored to           its normal osition and has                                 erformed normall                       ever since 3     9i P AC I LITY srAivs E Qi
                                    $1
                                ~ll 0 PQYIZ R'TItf 0 Qi        .
NA R STATUS   ~         14ZTNOO DISCOvERY
                                                                                              +AQLi Or 0
QISCQV ~aV QZ SCRIPT:"4 erator Observation:
9                     10               12     12                           44       45 ACTIVITY         CQNTZNT                                                                                                                                             ZO RZLSASZO
                ~ZQDD ~ZQS.
Or RELEASE                  AIZOVNTQr NA AcrVITYGS' NA LOCATION OPR I.EASE        Q 7       3i9                   10           If                                       44.           45 Pf RSQAINPI,   ilKPQSURE Si
                ~0-I 0 0 Qif~ZQs                                                   NA t                               11 PERSQNttf L INJI'Rif5 NUtPSZR<             DZSCRIPTICIIQAI Zai~oo 1        8- 9*
0Q~
11      11 NA LCSS Or CR DAMAGE .0           PACIuTY'c~
TYPE        Qf SCRIPTIO4 EK'ZIO2 t        3    7        'O                                                        NA PUSLICITY NRC SECNI.V KH LHM 2        9    9            'IO NA 6L. 59
                                                                                                                                                      !!!!       '       I I 30 NAME OF PREPARER                    M.. A. Schoppman                                            POEl~305) 552-3802}}

Latest revision as of 10:04, 4 February 2020

LER 80-010/03L-0:on 800217,during 100% Power Operation, Control Element Assembly 65 Dropped to Full Insertion When Selected to Manual Insertion for A.S.I. Damping.Cause Undetermined.Assembly Operated Properly in Normal Position
ML17266A158
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 03/17/1980
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17208A358 List:
References
LER-80-010-03L, LER-80-10-3L, NUDOCS 8003310317
Download: ML17266A158 (2)


Text

NRC FORM DSBi U~S NUCLEAR'REGULATORYCOVIMISSION IT 775 LlCENSEE EVENT REPORT CONTROI; BLOCK' I,'Q {PLEASE PRINT OR TYPE *I.LREQUIRED'INPORMATIONI

~o. I 'lZ..I S L-.tS.I ltQ,2 0 Ol: - Ol OIO I 0'10 - 0 0 0, i 4 1 1i ll 1Qi~lQi 7

P CON, i 31 3i LICZtISZZ CODE 61 VENT OESCRIPTION'AAIO PROBABL CONSECUE.4CES Oio i

COCKET NUMSE R.

C~O~ii>>

LICENSE tIW48fil EVENT O*rs 14 I.ICZiiSE TYPE Joi 15 RZPi AT Q*TZ

$1 AT $ 3 50 0

~O2 During. 100tP power operation,CEA. 65 dropped to full insertion when selected

~o, 3 .to manual insertion for A S.I damping.. ACTION in accordance- with Tech Spec., 3.1 3'.f was'niefated and reactor power was reduced. CEA 65 was

~o s restored to. its'ormal osition within'ne hour. The reactor was returned to 100X power. This is the si'xth occurrence. of a dropped CEA for which

~o 2 the cause is unknown. See LEP.'s 335-77-6 78-20 78-46 79-2 and 79-27.)l

~ 4'7

~OS

% 9 30 SYSTZAZ CAVSS CAI'Sf CQMr. YALv s CQOE CCOE SUSCDOf C~WPC4fN T CQOE SVSCDOA SU8C f T 3

~RB 9 10 Gi ~xQii ~zQ ii 0 Rl 0 R v E Qw ~zQii ~z' 11 11 IS 19 20 SECVEIITIAI OCCUAIIEMCZ REPORT S Z'I i 5 I Q N SVZMl'YEAR Q "" LILLtI LERIRO CEPQRT 40, Coos TYPS NQ.

" LJ...LILL'I~ID L00>l'-

21'2PrifCT'tiUTQOYAV 28 L~J 12 TS'7 L~J 20 I=I 2I ACMQN PUY"Rs. 3 UZTIiQO, *lSUSMI

'CRUZ NT 4PROM PSIMs COMP,

'lSI

~

TAKEN AC IQN O.'I PLANT I

JJ "S LJS Lar Jt 25 28 NOVAS Q22 ~ TZQ IXS LJS LJS PQR'IBUS. SUSoLIZR CAUSE OESCRIPTION ANO CORRECTIVE ~iONS Q27 No cause could be d'etermined for the CEA. drop and no other abnorm'al conditions were found. CEA 65 o crated ro erl when restored to its normal osition and has erformed normall ever since 3 9i P AC I LITY srAivs E Qi

$1

~ll 0 PQYIZ R'TItf 0 Qi .

NA R STATUS ~ 14ZTNOO DISCOvERY

+AQLi Or 0

QISCQV ~aV QZ SCRIPT:"4 erator Observation:

9 10 12 12 44 45 ACTIVITY CQNTZNT ZO RZLSASZO

~ZQDD ~ZQS.

Or RELEASE AIZOVNTQr NA AcrVITYGS' NA LOCATION OPR I.EASE Q 7 3i9 10 If 44. 45 Pf RSQAINPI, ilKPQSURE Si

~0-I 0 0 Qif~ZQs NA t 11 PERSQNttf L INJI'Rif5 NUtPSZR< DZSCRIPTICIIQAI Zai~oo 1 8- 9*

0Q~

11 11 NA LCSS Or CR DAMAGE .0 PACIuTY'c~

TYPE Qf SCRIPTIO4 EK'ZIO2 t 3 7 'O NA PUSLICITY NRC SECNI.V KH LHM 2 9 9 'IO NA 6L. 59

!!!! ' I I 30 NAME OF PREPARER M.. A. Schoppman POEl~305) 552-3802