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| issue date = 12/20/1978
| issue date = 12/20/1978
| title = LER#78-094/03L-0 on 781202:halon Sys for Cable Spreading Area Was Discharged & Therefore Inoperable.Caused by Operator Error
| title = LER#78-094/03L-0 on 781202:halon Sys for Cable Spreading Area Was Discharged & Therefore Inoperable.Caused by Operator Error
| author name = SMITH J K
| author name = Smith J
| author affiliation = INDIANA MICHIGAN POWER CO.
| author affiliation = INDIANA MICHIGAN POWER CO.
| addressee name =  
| addressee name =  
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:NRC FORM 366{7.77}LICENSEE EVENT REPORT LL S.NUCLEAR REGULATORY COMMISSION 4 CONTROL BLOCK: I Ql" (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 25 26 I.ICENSE TYPF 30 57 CAT 58 Q 3 0~O Q M I D C C 7 8 9 LICENSEE'CODE CON'T 14 15 LICENSE NUMBER QB>>20 QB 80 74 75 REPORT DATE 7 8 A soURGE LLJO 0 5 0 0 0 3 1 6 0 60 61 DOCKET NUMBER 68 69 EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 UNIT OPERATING IN MODE 1.OPERATOR ERROR RESULTED I~O3 4 SPREADING AREA BEING DISCHARGED AND THEREFORE INOPERABLE IN VIOLATION OF SPEC 3.7.9.4.ACTION ITEM 3.7.9.4a WAS COMPLIED.WITH HALON SYS.'RESTOR
{{#Wiki_filter:NRC FORM 366                                                                                                                         LL S. NUCLEAR REGULATORY COMMISSION
~OS~OB OPERABLE STATUS ON DECEMBER 4, 19784 NO" PROBABLE CONSE UENCES.THIS WAS FIRST EVENT OF THIS TYPE.0 7~OB 80 7 8 7 8 SYSTEM CAUSE CAUSE COMP VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~ZZ Q77 A Q>>~BQ>>Z Z Z Z Z Z Q4 UZQ>>UZ Q'5 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIRP EVENT YEAR REPORT NO.CODE TYPE NO.Q17 REPoRT MB U~09 4 L~l LU~UL U Uo 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN, ATTACHMENT NPRDR PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER UNQ75 UZQER~ZO20 UZQ 0 0 0 0 UNQ23 UNQ24 UZQ25 Z 9 9 9 Q25 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o HALON SYS DISCHARGED WHEN OPERATOR PUSHED AC HAVE PUSHED CO RESET BUTTON.OPERATO SURE HE PUSHED CORRECT PUSH BUTTON:-7SINCE PUSH BUTTONS ARE CLOSE TO EACH OTHER.3 PROTECTIVE COVERS TO BE INSTALLED OVER PUSH BUTTONS TO CAUSE OPERATOR TO TAKE TIME TO BE SURE HE IS CORRECT.45 7 8 9 FACILITY~3P METHOD OF STATUS 9I'7 POWER OTHER STATUS~'ISCOVERY DISCOVERY DESCRIPTION 32~l5 UB Qss~10 0 Qss NA~AQ31 OPERATOR OBSERVATION 7 8 9 10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q LOCATION OF RELEASE Q[i>~]~Q33 IZJQ34 7 8 9 10 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION 7~00 0 Q37 UZQ35 NA 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTION~41 5~00 0 Q45 NA 80 80 80 80 9 11 12 LOSS OF OR DAMAGE TO FACILITY 43 TYPE DESCRIPTION Z Q2 NA 9 10 PUBLICITY ISSUED DESCRIPTION
{7.77}
~QUQ44 9 10 7 8 zz 8 O 7 8 NAME (~JIZ PREPARER L.K SMITH 80 80 NRC LISE ONLY 68 69 80 o (616)465 5901 K.L 0 0 I I 1~0'l~K., fl}}
LICENSEE EVENT REPORT 4
CONTROL BLOCK:                                                     Ql                 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 7      8    9 M    I    D      C LICENSEE'CODE C
I 14 Q    15                    LICENSE NUMBER                      25 Q 3 26       I.ICENSE TYPF     30 0~O 57 CAT 58 CON'T 7       8 soURGE     LLJO 60              61 0     5     0     0   0 DOCKET NUMBER 3   1   6 68 0   69       EVENT DATE             74 QB>> 20 75      REPORT DATE            80 QB EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                                 Q10 UNIT OPERATING IN                       MODE       1. OPERATOR           ERROR RESULTED             I       A
~O3               SPREADING AREA BEING DISCHARGED AND THEREFORE INOPERABLE IN VIOLATION OF 4            SPEC     3.7.9.4.             ACTION ITEM             3.7.9.4a       WAS     COMPLIED. WITH HALON SYS.'RESTOR
~OS               OPERABLE STATUS ON DECEMBER                                 4,   19784       NO" PROBABLE CONSE UENCES.                         THIS     WAS     FIRST
~OB              EVENT OF THIS TYPE.
0 7
~OB                                                                                                                                                                                   80 7       8 SYSTEM               CAUSE           CAUSE                                                       COMP           VALVE CODE                 CODE         SUBCODE                 COMPONENT CODE                     SUBCODE           SUBCODE
                                  ~ZZ         10 Q77         A     Q>>     ~BQ>>
12            13 Z     Z     Z   Z   Z     Z 18 Q4       UZQ>>
19 UZ 20 Q'5 7      8                      9                           11 SEQUENTIAL                           OCCURRENCE             REPORT                       REVISION REPORT NO.                             CODE                 TYPE                           NO.
Q17 LERIRP REPoRT EVENT YEAR MB 21          22 U
23
                                                                            ~09 24 4
26 L~l 27 LU~
28         29 UL 30 U
31 Uo 32 ACTION FUTURE                     EFFECT             SHUTDOWN,                                 ATTACHMENT           NPRDR         PRIME COMP.             COMPONENT TAKEN ACTION                     ON PLANT             METHOD                 HOURS Q22         SUBMITTED         FORM SUB.         SUPPLIER             MANUFACTURER UNQ75 UZQER 33        34
                                                ~ZO20 35 UZQ 36            37 0     0     0     0 40 UNQ23 41 UNQ24 42 UZQ25 43              44 Z   9   9 9 47 Q25 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o           HALON SYS DISCHARGED WHEN OPERATOR PUSHED AC HAVE PUSHED CO                       RESET BUTTON. OPERATO SURE HE PUSHED CORRECT PUSH BUTTON:-7SINCE PUSH BUTTONS ARE CLOSE TO EACH OTHER.
3           PROTECTIVE COVERS TO BE INSTALLED OVER PUSH BUTTONS TO CAUSE OPERATOR TO TAKE TIME TO BE SURE HE                   IS CORRECT.
80 7       8   9 FACILITY STATUS
                            ~10 9I'7 POWER                         OTHER STATUS     ~
                                                                                      ~3P      METHOD OF
                                                                                            'ISCOVERY                                 DISCOVERY DESCRIPTION           32
~l5         UB   Qss 10 0
12 Qss 13 NA 44
                                                                                                  ~AQ31 OPERATOR OBSERVATION 45          46                                                                      80 7     8     9 ACTIVITY       CONTENT Q                                                                             Q
[i>~]
7      8
              ~
RELEASED OF RELEASE 9
Q33   IZJQ34 10 PERSONNEL EXPOSURES AMOUNT OF ACTIVITY 44            45 LOCATION OF RELEASE 80 NUMBER                 TYPE         DESCRIPTION 7       ~00         0     Q37     UZQ35 12          13 NA 80 7       8   9             11 PERSONNEL INJURIES NUMBER                 DESCRIPTION~41 5       ~00         0     Q45 12 NA 80 7    8    9             11 LOSS OF OR DAMAGE TO FACILITY                 43 zz          TYPE       DESCRIPTION Z Q2       NA 10                                                                                                                                                          80 8    9 O
PUBLICITY ISSUED QUQ44 DESCRIPTION         ~                                                                                                                 NRC LISE ONLY 68   69                           80 o 7      8    9          10 L. K    SMITH                                                              (616) 465 5901               K .         L NAME (~JIZ PREPARER
 
0                     0 I I 1
              ~ 0' l ~
K., fl}}

Latest revision as of 02:14, 4 February 2020

LER#78-094/03L-0 on 781202:halon Sys for Cable Spreading Area Was Discharged & Therefore Inoperable.Caused by Operator Error
ML17317A827
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 12/20/1978
From: James Smith
INDIANA MICHIGAN POWER CO.
To:
Shared Package
ML17317A823 List:
References
LER-78-094-03L, LER-78-94-3L, NUDOCS 7812270268
Download: ML17317A827 (2)


Text

NRC FORM 366 LL S. NUCLEAR REGULATORY COMMISSION

{7.77}

LICENSEE EVENT REPORT 4

CONTROL BLOCK: Ql (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 7 8 9 M I D C LICENSEE'CODE C

I 14 Q 15 LICENSE NUMBER 25 Q 3 26 I.ICENSE TYPF 30 0~O 57 CAT 58 CON'T 7 8 soURGE LLJO 60 61 0 5 0 0 0 DOCKET NUMBER 3 1 6 68 0 69 EVENT DATE 74 QB>> 20 75 REPORT DATE 80 QB EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 UNIT OPERATING IN MODE 1. OPERATOR ERROR RESULTED I A

~O3 SPREADING AREA BEING DISCHARGED AND THEREFORE INOPERABLE IN VIOLATION OF 4 SPEC 3.7.9.4. ACTION ITEM 3.7.9.4a WAS COMPLIED. WITH HALON SYS.'RESTOR

~OS OPERABLE STATUS ON DECEMBER 4, 19784 NO" PROBABLE CONSE UENCES. THIS WAS FIRST

~OB EVENT OF THIS TYPE.

0 7

~OB 80 7 8 SYSTEM CAUSE CAUSE COMP VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~ZZ 10 Q77 A Q>> ~BQ>>

12 13 Z Z Z Z Z Z 18 Q4 UZQ>>

19 UZ 20 Q'5 7 8 9 11 SEQUENTIAL OCCURRENCE REPORT REVISION REPORT NO. CODE TYPE NO.

Q17 LERIRP REPoRT EVENT YEAR MB 21 22 U

23

~09 24 4

26 L~l 27 LU~

28 29 UL 30 U

31 Uo 32 ACTION FUTURE EFFECT SHUTDOWN, ATTACHMENT NPRDR PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER UNQ75 UZQER 33 34

~ZO20 35 UZQ 36 37 0 0 0 0 40 UNQ23 41 UNQ24 42 UZQ25 43 44 Z 9 9 9 47 Q25 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o HALON SYS DISCHARGED WHEN OPERATOR PUSHED AC HAVE PUSHED CO RESET BUTTON. OPERATO SURE HE PUSHED CORRECT PUSH BUTTON:-7SINCE PUSH BUTTONS ARE CLOSE TO EACH OTHER.

3 PROTECTIVE COVERS TO BE INSTALLED OVER PUSH BUTTONS TO CAUSE OPERATOR TO TAKE TIME TO BE SURE HE IS CORRECT.

80 7 8 9 FACILITY STATUS

~10 9I'7 POWER OTHER STATUS ~

~3P METHOD OF

'ISCOVERY DISCOVERY DESCRIPTION 32

~l5 UB Qss 10 0

12 Qss 13 NA 44

~AQ31 OPERATOR OBSERVATION 45 46 80 7 8 9 ACTIVITY CONTENT Q Q

[i>~]

7 8

~

RELEASED OF RELEASE 9

Q33 IZJQ34 10 PERSONNEL EXPOSURES AMOUNT OF ACTIVITY 44 45 LOCATION OF RELEASE 80 NUMBER TYPE DESCRIPTION 7 ~00 0 Q37 UZQ35 12 13 NA 80 7 8 9 11 PERSONNEL INJURIES NUMBER DESCRIPTION~41 5 ~00 0 Q45 12 NA 80 7 8 9 11 LOSS OF OR DAMAGE TO FACILITY 43 zz TYPE DESCRIPTION Z Q2 NA 10 80 8 9 O

PUBLICITY ISSUED QUQ44 DESCRIPTION ~ NRC LISE ONLY 68 69 80 o 7 8 9 10 L. K SMITH (616) 465 5901 K . L NAME (~JIZ PREPARER

0 0 I I 1

~ 0' l ~

K., fl