ML17317B031: Difference between revisions

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| issue date = 03/20/1979
| issue date = 03/20/1979
| title = LER 79-011/03L-0 on 790223:auxiliary Feedwater Discharge Valve Would Not Close from Control Room.Caused by Loose Connection in Hot Shutdown Panel.Connection Tightened & Correct Valve Operation Verified
| title = LER 79-011/03L-0 on 790223:auxiliary Feedwater Discharge Valve Would Not Close from Control Room.Caused by Loose Connection in Hot Shutdown Panel.Connection Tightened & Correct Valve Operation Verified
| author name = BEILMAN T P
| author name = Beilman T
| author affiliation = INDIANA MICHIGAN POWER CO.
| author affiliation = INDIANA MICHIGAN POWER CO.
| addressee name = KEPPLER J G
| addressee name = Keppler J
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
| docket = 05000315
| docket = 05000315
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=Text=
=Text=
{{#Wiki_filter:U.S.NUCLEARREGULATORY COMMISSION NRC.FORM366I7-77)LICENSEEfVENTREPORTCONTROLBLOCK:Q1{PLEASEPRINTORTYPEALLREQUIREDINFORMATION)
{{#Wiki_filter:NRC.FORM 366                                                                                                                      U. S. NUCLEAR REGULATORY COMMISSION I7-77)
I6~oiMIDCCIQo00000000000Qo41111ps~ps,789LICENSEE.
LICENSEE          fVENT REPORT CONTROL BLOCK:                                                 Q1                 {PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
CODE1415LICENSENUMBER2526LICENSETYPE3057CAT58CON'T~o1~LQBO5OOO315Q7022379QsO32O709786061DOCKETNUMBER69EVENTDATE7475REPORTDATE80EVENTDESCRIPTION ANDPROBABLECONSEQUENCES Q10WHILEPERFORMING ASURVEILLANCE TESTONAUXILIARY FEEDWATER DISCHARGE VALVEFMO-212ITWASDISCOVERED THATTHEVALVEWOULDNOTCLOSEFROMTHECONTROLROOM.ALTHOUGHTHEVALVEFAILEDINTHECONSERVATIVE POSITIONTHEREQUIREMENTS OF~osT.S.4.7.1.2.a.4 IIERENOTFULFILLED UNTILREPAIRSIIERECOMPLETED.
I                                    6
THETIME~o6LIMITIMPOSEDBYT.S3712WASOBSERVEDWITHREPAIRSCOMPLETED WITHINELEVENHOURSOFDISCOVERY.
  ~oi 7      8    9 M    I    D    C LICENSEE. CODE C  I Qo0 14      15 0    0      0    0    0    0 LICENSE NUMBER 0    0    0    0Qo 25      26 4    1      1 LICENSE TYPE 1    1 30 ps~ps 57 CAT 58 CON'T
ASIMILAROCCURRENCE WASREPORTEDUNDER315/78-018.
  ~o1                           ~LQB        O        5      O    O    O      3    1    5  Q7      0    2    2    3    7      9 Qs        O    3    2    O    7      09 7        8                    60        61              DOCKET NUMBER                          69      EVENT DATE              74      75        REPORT DATE          80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                              Q10 WHILE PERFORMING A SURVEILLANCE                                    TEST ON AUXILIARY FEEDWATER DISCHARGE VALVE FMO-212        IT    WAS DISCOVERED                THAT THE VALVE WOULD NOT CLOSE FROM THE CONTROL ROOM.
~OS78980~09CONNECTION WASTIGHTENED ANDCORRECTVALVEOPERATION WASVERIFIED.
ALTHOUGH THE VALVE FAILED IN THE CONSERVATIVE POSITION THE REQUIREMENTS OF
THELOOSECONNECTIONS WEREATTRIBUTED TOCONSTRUCTION INSTALLATION, ANDFOLLOWING THISEVENT,ALLTERMINALBOARDCONNECTIONS INTHEUNITONEANDTWOHOTSHUTDOWNPANELSlOEREVERIFIEDTOBETIGHT.SYSTEMCAUSECAUSEg,Q~>>aoVALV0PQl4~l(Qis~kQs78910111213181920SEQUENTIAL OCCURRENCE REPORTREVISION21222324262728293031ACTIONFUTUREEFFECTSHUTDOWNATTACHMENT, NPRDPPRIMECOMP.COMPONENT
  ~os            T.S. 4.7.1.2.a.4                   IIERE NOT FULFILLED UNTIL REPAIRS IIERE COMPLETED.                                                   THE TIME
"~~pls~~Qo~poo~Q>>~PJQ>>PJQ4PJQsQs3334353637404142434447CAUSEDESCRIPTION ANDCORRECTIVE ACTIONSQ27oTHECAUSEWASDETERMINED TOBEALOOSECONNECTION INTHEHOTSHUTDOWNPANELTHE789FACILITYQs~IO0P>>78910121344ACTIVITYCONTENTRELFASEDOFRFfEASEAMOUlggFACTIVITYQ36CZLJQ>>Lips78910PERSONNEL EXPOSURES OŽ'"''Q'"'"'""
  ~o6            LIMIT IMPOSED              BY    T.S        3 7    1    2 WAS OBSERVED WITH REPAIRS COMPLETED WITHIN ELEVEN HOURS OF DISCOVERY.                             A    SIMILAR OCCURRENCE                WAS REPORTED                UNDER        315/78-018.
"789111213PERSONNEL INJURIESEZLoools"-QNAMETHODOF4546NA45LOCATIONOFRELEASEQ808080807891112LOSSOFORDAMAGETOFACILITY4378910PUBLICITY ISQIEDDESCRIPTION
  ~OS                                                                                                                                                                                  80 7      8 9 SYSTEM              CAUSE          CAUSE
~KZ<Q448910NAMEOFPREPARERPeilman806869616-.465.,5gO]
  ~09 7        8                      9        10 g,
80NRCUSEONI.YssO80o0 vs~'4}}
11 Q ~>>ao  12              13 V    A    L    V    0    P 18 Ql4      ~l(
19 Qis     ~k 20 Qs SEQUENTIAL                          OCCURRENCE             REPORT                        REVISION 21        22          23            24              26        27            28        29          30              31 ACTION FUTURE                EFFECT            SHUTDOWN                                      ATTACHMENT,NPRDP                    PRIME COMP.               COMPONENT
                ~~pls ~~
33        34 Qo       ~poo 35
                                                                ~
36 Q>>
37
                                                                                          ~
40 PJ 41 Q>>         PJQ4 42 PJ Qs 43              44                47 Qs CAUSE DESCRIPTION AND CORRECTIVE ACTIONS                            Q27 o        THE CAUSE WAS DETERMINED TO BE A LOOSE CONNECTION IN THE HOT SHUTDOWN PANEL                                                                              THE CONNECTION WAS TIGHTENED AND CORRECT VALVE OPERATION WAS                                                          VERIFIED.              THE LOOSE CONNECTIONS WERE ATTRIBUTED TO CONSTRUCTION INSTALLATION, AND FOLLOWING THIS EVENT, ALL TERMINAL BOARD CONNECTIONS IN THE UNIT ONE AND TWO HOT SHUTDOWN PANELS lOERE    VERIFIED TO BE TIGHT.
7      8  9                                                                                                                                                                        80 FACILITY                                                                        METHOD OF Qs      ~IO          0 P>>
7      8    9              10            12      13                                44      45        46                                                                        80 ACTIVITY      CONTENT RELFASED OF      RFf EASE                AMOUlggF ACTIVITYQ36                                                          LOCATION OF RELEASE          Q CZ      8 LJQ>>
9 Lips 10                                                                      45 NA 80 O''"''Q'"'"'"""
7 PERSONNEL EXPOSURES 7      8    9              11      12          13                                                                                                                                  80 PERSONNEL INJURIES
                                                "-Q EZ Loools 7      8    9              11      12 NA 80 LOSS OF OR DAMAGE TO FACILITY            43 7      8    9          10                                                                                                                                                          80 KZ <Q44 ISQIED PUBLICITY DESCRIPTION      ~                                                                                                                      NRC USE ONI.Y ss O
8    9          10                                                                                                                        68    69                          80 o 0
NAME OF PREPARER                            P        eilman                                                                616-.465.,5gO]
 
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Latest revision as of 03:11, 4 February 2020

LER 79-011/03L-0 on 790223:auxiliary Feedwater Discharge Valve Would Not Close from Control Room.Caused by Loose Connection in Hot Shutdown Panel.Connection Tightened & Correct Valve Operation Verified
ML17317B031
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 03/20/1979
From: Beilman T
INDIANA MICHIGAN POWER CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317B029 List:
References
LER-79-011-03L, LER-79-11-3L, NUDOCS 7903290033
Download: ML17317B031 (2)


Text

NRC.FORM 366 U. S. NUCLEAR REGULATORY COMMISSION I7-77)

LICENSEE fVENT REPORT CONTROL BLOCK: Q1 {PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6

~oi 7 8 9 M I D C LICENSEE. CODE C I Qo0 14 15 0 0 0 0 0 0 LICENSE NUMBER 0 0 0 0Qo 25 26 4 1 1 LICENSE TYPE 1 1 30 ps~ps 57 CAT 58 CON'T

~o1 ~LQB O 5 O O O 3 1 5 Q7 0 2 2 3 7 9 Qs O 3 2 O 7 09 7 8 60 61 DOCKET NUMBER 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 WHILE PERFORMING A SURVEILLANCE TEST ON AUXILIARY FEEDWATER DISCHARGE VALVE FMO-212 IT WAS DISCOVERED THAT THE VALVE WOULD NOT CLOSE FROM THE CONTROL ROOM.

ALTHOUGH THE VALVE FAILED IN THE CONSERVATIVE POSITION THE REQUIREMENTS OF

~os T.S. 4.7.1.2.a.4 IIERE NOT FULFILLED UNTIL REPAIRS IIERE COMPLETED. THE TIME

~o6 LIMIT IMPOSED BY T.S 3 7 1 2 WAS OBSERVED WITH REPAIRS COMPLETED WITHIN ELEVEN HOURS OF DISCOVERY. A SIMILAR OCCURRENCE WAS REPORTED UNDER 315/78-018.

~OS 80 7 8 9 SYSTEM CAUSE CAUSE

~09 7 8 9 10 g,

11 Q ~>>ao 12 13 V A L V 0 P 18 Ql4 ~l(

19 Qis ~k 20 Qs SEQUENTIAL OCCURRENCE REPORT REVISION 21 22 23 24 26 27 28 29 30 31 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT,NPRDP PRIME COMP. COMPONENT

~~pls ~~

33 34 Qo ~poo 35

~

36 Q>>

37

~

40 PJ 41 Q>> PJQ4 42 PJ Qs 43 44 47 Qs CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o THE CAUSE WAS DETERMINED TO BE A LOOSE CONNECTION IN THE HOT SHUTDOWN PANEL THE CONNECTION WAS TIGHTENED AND CORRECT VALVE OPERATION WAS VERIFIED. THE LOOSE CONNECTIONS WERE ATTRIBUTED TO CONSTRUCTION INSTALLATION, AND FOLLOWING THIS EVENT, ALL TERMINAL BOARD CONNECTIONS IN THE UNIT ONE AND TWO HOT SHUTDOWN PANELS lOERE VERIFIED TO BE TIGHT.

7 8 9 80 FACILITY METHOD OF Qs ~IO 0 P>>

7 8 9 10 12 13 44 45 46 80 ACTIVITY CONTENT RELFASED OF RFf EASE AMOUlggF ACTIVITYQ36 LOCATION OF RELEASE Q CZ 8 LJQ>>

9 Lips 10 45 NA 80 O"Q'"'"'"""

7 PERSONNEL EXPOSURES 7 8 9 11 12 13 80 PERSONNEL INJURIES

"-Q EZ Loools 7 8 9 11 12 NA 80 LOSS OF OR DAMAGE TO FACILITY 43 7 8 9 10 80 KZ <Q44 ISQIED PUBLICITY DESCRIPTION ~ NRC USE ONI.Y ss O

8 9 10 68 69 80 o 0

NAME OF PREPARER P eilman 616-.465.,5gO]

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