ML17331A700: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(One intermediate revision by the same user not shown)
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:NRC FORIVL366 l7.77)I~~V.S.NUCI.EAR REGULATORY COMMISSION LlCENSEE EVENT REPORT CONTROL BLOCK: (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
{{#Wiki_filter:NRC FORIVL366 l7.77)
I 6 N I 0 C C 2 QE 0 0 0 0 0 0 0 0 0 Q34 1 1 1 1 QE~QE 8 9 LICENSEE'ODE 14 15 LICENSE NUMBER 26 26 LICENSE TYPE 30 57 CAT 58 CON'T 0 I soURcE LJO 0 5 0 0 0 3 1 6 7 0 3 1 5 8 1 Q OB DOCKET NUMBER 68 69 EVENT DATE 74/5 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10~02 DURING OPERATION OF 2CD EMERGENCY DIESEL IN PREPARATION FOR 18 MONTH SURVfILLANCE, A~03~04~OS~os HOT STARTING AIR LINE WAS OBSERVED.THE fNGINE WAS REMOVED FROM SERVICE AND DECLARED INOPfRABLE PER T.S.3.8.1.1 THE ACTION REQUIREMENTS WfRE MET.THE UNIT WAS BEING COOLED DOWN FOR A SCHEDULED REFUELING OUTAGE.THE 2AB DIESEL REMAINED OPERABLE.PUB-LIC HEALTH AND SAFETY WAS NOT AFFECTED BY THIS EVENT.A SIMILAR OCCURfNCE WAS REPORTED~07 AS RO 78-~OB 7 8 9~Os 03L-O.80 7 8 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~EE QLI L~JQ LJQI3 V A L V E X QE LBGE~Go 9 10 11 12 13 18 19 20 SEOUENTIAL OCCURRENCE REPORT REVISION LER/RO EVENT YEAR REPORT NO.CODE TYPE NO.QI7 REPORT~01~~00 7~m~03 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ PRIME COMP.*COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER
CONTROL BLOCK:
~CQIB~X Q19~ZQ20~Z Q21 0 0 0 0~Y Q23~YQ24~A Q25 W 3 1 5 Q2B 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTION Q27 T TART G AIR VALVE FOR 4 REAR BANK CYLINDER WORTHINGTON PART NO.56000001, STUCK OPEN EXPOSING THE STEM TO FLUCTUATING HIGH PRESSURE AND TEMPERATURE OUE TO COMBUSTION
I I           LlCENSEE EVENT REPORT 6
.IN THE CYLINDER AND RESULTING IN FATIGUE FAILURE.ALL CYLINDER HEADS WERE REMOVED 3 AND THE CYLINDERS INSPECTED.
S. NUCI.EAR REGULATORY COMMISSION (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
METAL PIECES WERE REMOVED FROM¹2 AND¹4 REAR BANK CYL-4 INDERS.¹2 REAR BANK PISTON CYLINDER HEAD AND SLEEVf WERE REPLACED.(CONTINUED) 80 N A 80 80 80 80 NRC USE ONLY o 80~o 0 PHONE 7 8 9 FACILITY~3P METHOD OF STATUS%POWER OTHER STATUS Q DISCOVERY DISCOVERY DESCRIPTION Q32~ls~OQ23~00 0 Qss N/A~AQSI OPERATOR OBSERVATION 7 8 9 10 12 13 44 45 46 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q3S LOCATION OF RELEASE Q EK LZJ Q3 IZlQ-7 8 9 10 11 44 45 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39~l7~00 0 Q37~ZQSs N A 7 8 9 11 12 13 P ER5 0NNE L IN JURIES NUMBER DESCRIPTIONQ41 EK~~OQ4o N A 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43 TYPE DESCRIPTION 9~ZQ42 N A 8 9 10 PUBLICITY IssUED UEEERIPTIUN~o 8 106PNX(/3'
N     I   0 C C                 2     QE 15 0     0       0   0   0 LICENSE NUMBER 0     0         0     0 26 Q34 26 1   1   1 LICENSE TYPE 1
~NQ44 N/A 7 8 9 10 68 69 NAME OF PREPARER DAVID G.W Z SUPPLEMENT TO LER¹81-007/03L-0 SUPPLEMENT TO CAUSE DESCRIPTION:
30 QE~QE 57 CAT 58 8   9         LICENSEE'ODE               14 CON'T 0   I           soURcE       LJO               0     5     0     0 0 DOCKET NUMBER 3   1   6 68 7
THE INTAKE AND EXHAUST VALVES IN¹4 REAR BANK CYLINDER HEAD WERE REPLACED.ALL STARTING AIR VALVES WERE INSPECTED.
69 0   3     1 EVENT DATE 5     8     1 74 Q /5         REPORT DATE           80 OB EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                             Q10
TWO ADDITIONAL STARTING AIR VALVES WERE FOUND STUCK OPEN.THf¹4 REAR BANK,¹2 FRONT BANK AND¹5 REAR BANK STARTING AIR VALVES WERE REPLACED.THE REAR BANK STARTING AIR DISTRIBUTOR WAS REPLACED.INSPECTION OF STARTING AIR VALVES WILL BE A PART OF THE 18 MONTH SURVEILLANCE IN BOTH UNITS.INSPECTION OF THE TURBOCHARGER REVEALfD THAT IT WAS DAMAGED BY SMALL PARTS OF THE FAILfD STARTING AIR VALVf AND FAILURE OF THE EXHAUST EXPANSION JOINT INNfR LINERS.THE TURBOCHARGER ROTOR WAS REPLACED.ALL OF THE LINERS HAVE BEEN RfMOVED FROM 2CD DIESEL.LINERS ON THE THREE REMAINING DIESEL ENGINES WILL BE REMOVfD DURING'UBSEQUENT 18 MONTH SURVEILLANCE INSPECTIONS.}}
~02             DURING OPERATION OF 2CD EMERGENCY                                   DIESEL IN PREPARATION FOR 18 MONTH SURVfILLANCE, A
~03             HOT STARTING               AIR LINE             WAS OBSERVED.           THE fNGINE WAS REMOVED FROM SERVICE AND DECLARED T.S. 3.8.1.1             THE ACTION REQUIREMENTS WfRE MET.                                 THE UNIT WAS BEING
~04              INOPfRABLE PER THE 2AB DIESEL REMAINED OPERABLE.                                PUB-
~OS              COOLED DOWN FOR A SCHEDULED REFUELING OUTAGE.
HEALTH AND SAFETY WAS NOT AFFECTED BY THIS EVENT.                                                 A   SIMILAR OCCURfNCE               WAS REPORTED
~os              LIC
~07             AS RO     78-             03L-O.
~OB                                                                                                                                                                                80 7         8 9 SYSTEM               CAUSE         CAUSE                                                         COMP.         VALVE CODE                 CODE       SUBCODE                 COMPONENT CODE                     SUBCODE         SUBCODE
~Os                                ~EE             QLI       L~JQ LJQI3                 13 V     A   L   V     E     X 18 QE       LBGE 19
                                                                                                                                                      ~Go 20 7        8                      9           10           11           12 SEOUENTIAL                         OCCURRENCE             REPORT                     REVISION QI7 LER/RO REPORT ACTION FUTURE EVENT YEAR
                                    ~01 21          22 EFFECT
                                                            ~23 SHUTDOWN 24 REPORT NO.
                                                                          ~00         7 26
                                                                                                    ~m 27
                                                                                                                  ~03 28 ATTACHMENT CODE 29 NPRDQ TYPE 30 PRIME COMP.
31 NO.
32 COMPONENT TAKEN ACTION                   ON PLANT             METHOD                 HOURS Q22         SUBMITTED         FORM SUB.       SUPPLIER             MANUFACTURER
                                                                    ~Z             0     0     0   0       ~Y               ~YQ24           ~A                 W   3   1 5
              ~CQIB ~X            Q19          ~ZQ20                  Q21 37                          41 Q23                                Q25 44                47 Q2B 33         34                   35                 36                                 40                       42               43 CAUSE DESCRIPTION AND CORRECTIVE ACTION Q27 T       TART         G     AIR VALVE             FOR   4 REAR BANK CYLINDER WORTHINGTON PART NO. 56000001,                                               STUCK OPEN EXPOSING THE STEM TO FLUCTUATING HIGH PRESSURE                                                 AND TEMPERATURE OUE TO COMBUSTION                             .
IN THE CYLINDER                   AND RESULTING             IN FATIGUE FAILURE.                   ALL CYLINDER HEADS                   WERE REMOVED 3         AND THE CYLINDERS INSPECTED.                                 METAL PIECES WERE REMOVED FROM                             ¹2   AND   ¹4     REAR BANK       CYL-4         INDERS.         ¹2     REAR BANK PISTON                   CYLINDER HEAD AND SLEEVf WERE REPLACED. (CONTINUED) 7       8   9 FACILITY STATUS             % POWER                         OTHER STATUS   Q
                                                                                  ~3P      METHOD OF DISCOVERY                               DISCOVERY DESCRIPTION Q32
~ls           ~OQ23         ~00 10 0
12 Qss       N/A 44
                                                                                              ~AQSI 45          46 OPERATOR OBSERVATION 80 7       8     9                                         13 ACTIVITY       CONTENT RELEASED OF RELEASE                         AMOUNTOF ACTIVITYQ3S                                                      LOCATION OF RELEASE       Q EK LZJ Q3 7       8   9 IZlQ-10           11                                         44           45 N A 80 PERSONNEL EXPOSURES NUMBER               TYPE           DESCRIPTION Q39
~l7 ~00                     0   Q37   ~ZQSs 12            13 N     A 80 7       8   9               11 P ER5 0NNE L   INJURIES NUMBER               DESCRIPTIONQ41 EK ~~OQ4o 7       8   9               11       12 N A 80 LOSS OF OR DAMAGE TO FACILITY TYPE       DESCRIPTION                     Q43 9       ~ZQ42           N   A 8   9         10                                                                                                                                                       80 PUBLICITY                                                                                                                                 NRC USE ONLY IssUED
              ~NQ44 UEEERIPTIUN~o N/A 8   106PNX(/3'                                                                                                           o 7       8   9         10                                                                                                                   68   69                           80 o
                                                                                                                                                                                      ~
0 NAME OF PREPARER                     DAVID G.     W Z                                               PHONE
 
SUPPLEMENT TO LER ¹81-007/03L-0 SUPPLEMENT TO CAUSE DESCRIPTION:
THE INTAKE AND EXHAUST VALVES IN ¹4 REAR BANK CYLINDER HEAD WERE REPLACED. ALL STARTING AIR VALVES WERE INSPECTED. TWO ADDITIONAL STARTING AIR VALVES WERE FOUND STUCK OPEN. THf ¹4 REAR BANK, ¹2 FRONT BANK AND ¹5 REAR BANK STARTING AIR VALVES WERE REPLACED.
THE REAR BANK STARTING AIR DISTRIBUTOR WAS REPLACED. INSPECTION OF STARTING AIR VALVES WILL BE A PART OF THE 18 MONTH SURVEILLANCE IN BOTH UNITS.
INSPECTION OF THE TURBOCHARGER REVEALfD THAT IT WAS DAMAGED BY SMALL PARTS OF THE FAILfD STARTING AIR VALVf AND FAILURE OF THE EXHAUST EXPANSION JOINT INNfR LINERS. THE TURBOCHARGER ROTOR WAS REPLACED. ALL OF THE LINERS HAVE BEEN RfMOVED FROM 2CD DIESEL. LINERS ON THE THREE REMAINING DIESEL ENGINES WILL BE REMOVfD DURING'UBSEQUENT 18 MONTH SURVEILLANCE INSPECTIONS.}}

Latest revision as of 01:32, 4 February 2020

LER 81-007/03L-0:on 810315 During Operation of 2CD Emergency Diesel in Preparation for Surveillance,Hot Starting Air Line Observed.Caused by Valve Damage & Exhaust Expansion Joint Inner Liner Failure.Intake & Exhaust Valves Replaced
ML17331A700
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 04/14/1981
From: Wizner D
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17326A873 List:
References
LER-81-007-03L-01, LER-81-7-3L-1, NUDOCS 8104210363
Download: ML17331A700 (2)


Text

NRC FORIVL366 l7.77)

CONTROL BLOCK:

I I LlCENSEE EVENT REPORT 6

S. NUCI.EAR REGULATORY COMMISSION (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

N I 0 C C 2 QE 15 0 0 0 0 0 LICENSE NUMBER 0 0 0 0 26 Q34 26 1 1 1 LICENSE TYPE 1

30 QE~QE 57 CAT 58 8 9 LICENSEE'ODE 14 CON'T 0 I soURcE LJO 0 5 0 0 0 DOCKET NUMBER 3 1 6 68 7

69 0 3 1 EVENT DATE 5 8 1 74 Q /5 REPORT DATE 80 OB EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10

~02 DURING OPERATION OF 2CD EMERGENCY DIESEL IN PREPARATION FOR 18 MONTH SURVfILLANCE, A

~03 HOT STARTING AIR LINE WAS OBSERVED. THE fNGINE WAS REMOVED FROM SERVICE AND DECLARED T.S. 3.8.1.1 THE ACTION REQUIREMENTS WfRE MET. THE UNIT WAS BEING

~04 INOPfRABLE PER THE 2AB DIESEL REMAINED OPERABLE. PUB-

~OS COOLED DOWN FOR A SCHEDULED REFUELING OUTAGE.

HEALTH AND SAFETY WAS NOT AFFECTED BY THIS EVENT. A SIMILAR OCCURfNCE WAS REPORTED

~os LIC

~07 AS RO 78- 03L-O.

~OB 80 7 8 9 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~Os ~EE QLI L~JQ LJQI3 13 V A L V E X 18 QE LBGE 19

~Go 20 7 8 9 10 11 12 SEOUENTIAL OCCURRENCE REPORT REVISION QI7 LER/RO REPORT ACTION FUTURE EVENT YEAR

~01 21 22 EFFECT

~23 SHUTDOWN 24 REPORT NO.

~00 7 26

~m 27

~03 28 ATTACHMENT CODE 29 NPRDQ TYPE 30 PRIME COMP.

31 NO.

32 COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER

~Z 0 0 0 0 ~Y ~YQ24 ~A W 3 1 5

~CQIB ~X Q19 ~ZQ20 Q21 37 41 Q23 Q25 44 47 Q2B 33 34 35 36 40 42 43 CAUSE DESCRIPTION AND CORRECTIVE ACTION Q27 T TART G AIR VALVE FOR 4 REAR BANK CYLINDER WORTHINGTON PART NO. 56000001, STUCK OPEN EXPOSING THE STEM TO FLUCTUATING HIGH PRESSURE AND TEMPERATURE OUE TO COMBUSTION .

IN THE CYLINDER AND RESULTING IN FATIGUE FAILURE. ALL CYLINDER HEADS WERE REMOVED 3 AND THE CYLINDERS INSPECTED. METAL PIECES WERE REMOVED FROM ¹2 AND ¹4 REAR BANK CYL-4 INDERS. ¹2 REAR BANK PISTON CYLINDER HEAD AND SLEEVf WERE REPLACED. (CONTINUED) 7 8 9 FACILITY STATUS  % POWER OTHER STATUS Q

~3P METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32

~ls ~OQ23 ~00 10 0

12 Qss N/A 44

~AQSI 45 46 OPERATOR OBSERVATION 80 7 8 9 13 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITYQ3S LOCATION OF RELEASE Q EK LZJ Q3 7 8 9 IZlQ-10 11 44 45 N A 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39

~l7 ~00 0 Q37 ~ZQSs 12 13 N A 80 7 8 9 11 P ER5 0NNE L INJURIES NUMBER DESCRIPTIONQ41 EK ~~OQ4o 7 8 9 11 12 N A 80 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Q43 9 ~ZQ42 N A 8 9 10 80 PUBLICITY NRC USE ONLY IssUED

~NQ44 UEEERIPTIUN~o N/A 8 106PNX(/3' o 7 8 9 10 68 69 80 o

~

0 NAME OF PREPARER DAVID G. W Z PHONE

SUPPLEMENT TO LER ¹81-007/03L-0 SUPPLEMENT TO CAUSE DESCRIPTION:

THE INTAKE AND EXHAUST VALVES IN ¹4 REAR BANK CYLINDER HEAD WERE REPLACED. ALL STARTING AIR VALVES WERE INSPECTED. TWO ADDITIONAL STARTING AIR VALVES WERE FOUND STUCK OPEN. THf ¹4 REAR BANK, ¹2 FRONT BANK AND ¹5 REAR BANK STARTING AIR VALVES WERE REPLACED.

THE REAR BANK STARTING AIR DISTRIBUTOR WAS REPLACED. INSPECTION OF STARTING AIR VALVES WILL BE A PART OF THE 18 MONTH SURVEILLANCE IN BOTH UNITS.

INSPECTION OF THE TURBOCHARGER REVEALfD THAT IT WAS DAMAGED BY SMALL PARTS OF THE FAILfD STARTING AIR VALVf AND FAILURE OF THE EXHAUST EXPANSION JOINT INNfR LINERS. THE TURBOCHARGER ROTOR WAS REPLACED. ALL OF THE LINERS HAVE BEEN RfMOVED FROM 2CD DIESEL. LINERS ON THE THREE REMAINING DIESEL ENGINES WILL BE REMOVfD DURING'UBSEQUENT 18 MONTH SURVEILLANCE INSPECTIONS.