ML18030A120: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(4 intermediate revisions by the same user not shown)
Line 3: Line 3:
| issue date = 06/23/1980
| issue date = 06/23/1980
| title = Notifies of Potential Deficiencies Er 100450 & Er 100508 Re States Co Sliding Links.Failure Occurs in Form of Crack Between Threaded Screwhole & Side of U-shaped Link.Will Advise of Date of Final Rept
| title = Notifies of Potential Deficiencies Er 100450 & Er 100508 Re States Co Sliding Links.Failure Occurs in Form of Crack Between Threaded Screwhole & Side of U-shaped Link.Will Advise of Date of Final Rept
| author name = CURTIS N W
| author name = Curtis N
| author affiliation = PENNSYLVANIA POWER & LIGHT CO.
| author affiliation = PENNSYLVANIA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:REGULATORYINFORMATIONDISTRIBUTIONSYSTEM(RIDS)ACCESSIONNBR:8006270342OOC,DATE:80/06/23NOl'ARIZEO:NOFACIL:usauehannaSteamElectricStationiUnit1rPennsylva-38'ouehannaSteamElectricStationPUnit2IPennsylvaA'~AUTHORAFFILIATIO'TlCSPN.i'I~PennsylvaniaPowerilLightCo~RECIP.~A:.ERFCIPIFNTAFFILIA7IONDOCKET¹0500038705000388
{{#Wiki_filter:REGULATORY INFORMATION DISTRIBUTION SYSTEM                                      (RIDS)
ACCESSION NBR:8006270342                        OOC,DATE: 80/06/23                      NOl'ARIZEO: NO                  DOCKET  ¹ FACIL:       usauehanna                    Steam Electric Stationi Unit 1r Pennsylva                                    05000387
                -38         'ouehanna          Steam Electric StationP Unit 2I Pennsylva                                    05000388 A'     ~                     AUTHOR AFF IL I A T IO'Tl C      SPN.i'I ~             Pennsylvania          Power              il  Light    Co ~
REC IP. ~A:.E                RFC    IP IF N T  AFF  ILIA7              ION


==SUBJECT:==
==SUBJECT:==
NotifiesofPotentialOeficienciesER100450FER100508reStatesCoslidinglinks.FailureoccursinformofcrackbetweenthrcededscrewholeLsideofUshaoed1ink,&i11adviseofdateoffinalrept'ISTRISUTTUNCOOS:8019SCOPIESRECEIVES:LTRgENCLQSIZESJBTIl'LF:ConstructionDeficiencyReoort(10CFR50~55E)BOOTES:~gWM~3Q~)re~+~~RECIPIENTIODOE/i"JAETREACTION:ADI()Q~Ar~+2120rIuTlR~.'AL:AC/RCI/IEEOORSTAFF07FIELOCOOR/IE13HYD/GEOBR22-LICQUALBR<PA08VELD23PRCTSl'EVBRG01COPIESLTTRFNCLRECIPIE'TiTIOCODE/'TiA'4EBCpvry+~odd15PHAEODEQUIPQUALBR16HANAUERPS~IRE05MOOREEV~NRCPDR02,ORASSESSBR17QABR10STANORDSOEV11COPIESLTTREN11EXTERNAL'CRSNSIC24041611LPOR03due3p>F800TOTALNUi!BEROFCOPIESREQUIRED:LTTR41ENCL1 0TWONORTHNINTHSTREET,ALLENTOWN,PA.18101PHONE:(215)821-5151NORMANW.CURTISVicePresidentEngineering8Construction821-5381June23,1980Mr.BoyceH.GrierDirector,RegionIU.S.NuclearRegulatoryCommission631ParkAvenueKingofPrussia,Pennsylvania19406SUSQUEHANNASTEAMELECTRICSTATIONNOTIFICATIONOFAPOTENTIALDEFICIENCYONSTATESCOMPANYSLIDINGLINKSERs100450/100508FILE840-4PLA-499
Notifies of Potential Oef iciencies ER 100450                                        F  ER100508      re States Co sliding links. Failure occurs in form of crack between thr ceded screwhole L side of U shaoed                                        1 ink,&i    1 1 advise of date of final COPIES RECEIVES:LTR g ENCL Q                                  SIZ ESJB rept'ISTRISUT TUN COOS:         8019S T I l'LF: Cons t ruc t i on Deficiency Reoor t (10CFR50 ~ 55E)
BOOTES:     ~g          W  M~         3    Q~)re~+~~
RECIPIENT                  COP  IES                          REC IPIE'TiT              COP  IES IO      DOE/i"JA ETRE        LTTR FNCL                        IO CODE/'Ti A'4E          LTTR EN ACTION:         AD      I() Q~Ar~+21                                          BC  pvry+~od d    15          1 20                                    PH                            1 r
I uTlR~.'AL: AC/RC I/IE                                                        AEOD EOO R        STAFF      07                                    EQUIP QUAL BR 16 F I ELO      COOR/IE13                                          HANAUERPS ~
HYD/GEO BR              22                                    IRE                05 LIC    QUAL BR                                                MOOREEV  ~
                <PA                      08                                    NRC PDR            02, VELD                    23                                    OR  ASSESS    BR  17 PR    C    TS l'EV      BR                                    QA  BR            10 G                    01                                    STANORDS OEV 11 EXTERNAL'CRS                            24        16    1                    LPOR              03 NS IC                    04        1 due  3 p >F80 TOTAL NUi!BER OF COPIES                REQUIRED: LTTR                        41  ENCL 0
1


==DearMr.Grier:==
0 TWO NORTH NINTH STREET, ALLENTOWN, PA. 18101      PHONE: (215) 821-5151 NORMAN W. CURTIS Vice President Engineering 8 Construction 821-5381 June 23, 1980 Mr. Boyce H. Grier Director, Region            I U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania            19406 SUSQUEHANNA STEAM ELECTRIC STATION NOTIFICATION OF A POTENTIAL DEFICIENCY            ON STATES COMPANY SLIDING LINKS ERs 100450/100508                        FILE 840-4 PLA-499
ThisletterservestoconfirminformationprovidedbytelephonetoNRCInspectorMr.R.McGaughybyMr.A.R.SabolofPP&LonJune17,1980.Duringthatconversation,Mr.McGaughywasadvisedthatthesubjectconditionwasbeingevaluatedforreportabilityundertheprovisionsof10CFR50.55(e).ThedefectinvolvesthefailureoftheU-shapedlinkontheStatesCompanyslidinglinkterminalblock.ThefailureoccursintheformofacrackbetweenthethreadedscrewholeandthesideoftheU-shapedlink.TheU-shapedlinkandassociatedspacerformsaconnectionbetweentwoslottedbarsontheterminalblockwhenthespacerandlinkaretightenedbyascrew.Whenthescrewistightenedacrackmayresultwhichcancauseanopenorapoorelectricalconnection.Sincetheselinksareusedonsafetyrelatedequipment,thedefectiveconditionhasbeenevaluatedaspotentiallyreportableundertheprovisionsof10CFR50.55(e).ThesubjectdefecthasalsobeenpreviouslyrecogniedbytheNRCandwasdescribedinyourInformationNotice80-08issuedonMarch7,1980.BechtelhasunderdevelopmentasamplingprocedurewhichincludesguidancefortheirQualityControlfieldorganizationtoinspectthelinks.ThePP&LIntegratedStartupGroupwillalsobeinstructedtofollowtheguidanceoutlinedinthesamplingplanwhenevertheyoperatethelinksduringpreoperationaltestingactivities.Weexpectthisapproachtoprovideuswithquantitativeinformationontheextentofthedeficiency.8OO6S7o>~Sincethedetailsofthisreportprovideinformationrelevanttothereportingrequirementsof10CFR21,thiscorrespondenceisconsideredtoalsodischargeanyformalresponsibilityPP&Lmayhaveforreportingincompliancethereto.go/15PENNSYLVANIAPOWER4LIGHTCOMPANY//g Mr.BoyceH.GrierJune23,1980PP&LandBechtelarecontinuingtoanalyzetheproblemandtoestablishanacceptablecorrectiveactionplan.Baseduponthesatisfactorycompletionofourinvestigation,wewilladvisetheCommissionofthedatebywhichafinalreportwillbesubmittedshouldtheconditionsbedeterminedtobereportable.N.W.CurtisVicePresident-Engineering6Construction-NuclearFLW:mcbcc:Mr.VictorStello(15)DirectorWfficeofInspection6EnforcementU.S.NuclearRegulatoryCommissionWashington,D.C.20555Mr.G.McDonald,DirectorOfficeofManagementInformation6ProgramControlU.S.NuclearRegulatoryCommissionWashington,D.C.20555Mr.RobertM.GalloU.S.NuclearRegulatoryCommissionP.0.Box52Shickshinny,Pennsyl'vania18655}}
 
==Dear Mr.       Grier:==
 
This    letter serves to confirm information provided by telephone to NRC Inspector Mr. R. McGaughy by Mr. A. R. Sabol of PP&L on June 17, 1980. During that conversation, Mr. McGaughy was advised that the subject condition was being evaluated for reportability under the provisions of 10CFR50.55(e).
The    defect involves the failure of the U-shaped          link on the States Company sliding link terminal block.           The failure  occurs  in the form of a crack between the threaded screwhole and the side of the            U-shaped link. The U-shaped link and    associated spacer forms a connection between two slotted bars on the terminal block when the spacer and link are tightened by a screw. When the screw is tightened a crack may result which can cause an open or a poor electrical connection. Since these links are used on safety related equipment, the defective condition has been evaluated as potentially reportable under the provisions of 10CFR50.55(e).
The    subject defect has also been previously recogni ed by the NRC and                was described in your Information Notice 80-08 issued on March 7, 1980.
Bechtel has under development a sampling procedure which includes guidance for their Quality Control field organization to inspect the links. The PP&L Integrated Startup Group will also be instructed to follow the guidance outlined in the sampling plan whenever they operate the links during preoperational testing activities. We expect this approach to provide us with quantitative information on the extent of the deficiency.
Since the        details of this report provide information relevant to the reporting requirements of 10CFR21, this correspondence is considered to also discharge any formal responsibility PP&L may have for reporting in compliance thereto.
go/1 5
8OO6S7          o>~                      PENNSYLVANIA POWER  4  LIGHT COMPANY
                                                                                                    //g
 
Mr. Boyce H. Grier                                          June 23, 1980 PP&L and  Bechtel are continuing to analyze the problem and to establish an acceptable corrective action plan. Based upon the satisfactory completion of our investigation, we will advise the Commission of the date by which a final report will be submitted should the conditions be determined to be reportable.
N. W. Curtis Vice President-Engineering  6  Construction-Nuclear FLW:mcb cc: Mr. Victor Stello      (15)
DirectorWffice of Inspection    6 Enforcement U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. G. McDonald, Director Office of Management Information 6 Program    Control U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. Robert M. Gallo U. S. Nuclear Regulatory Commission P. 0. Box 52 Shickshinny, Pennsyl'vania      18655}}

Latest revision as of 16:26, 3 February 2020

Notifies of Potential Deficiencies Er 100450 & Er 100508 Re States Co Sliding Links.Failure Occurs in Form of Crack Between Threaded Screwhole & Side of U-shaped Link.Will Advise of Date of Final Rept
ML18030A120
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 06/23/1980
From: Curtis N
PENNSYLVANIA POWER & LIGHT CO.
To:
References
ER-100450, ER-100508, PLA-499, NUDOCS 8006270342
Download: ML18030A120 (4)


Text

REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:8006270342 OOC,DATE: 80/06/23 NOl'ARIZEO: NO DOCKET ¹ FACIL: usauehanna Steam Electric Stationi Unit 1r Pennsylva 05000387

-38 'ouehanna Steam Electric StationP Unit 2I Pennsylva 05000388 A' ~ AUTHOR AFF IL I A T IO'Tl C SPN.i'I ~ Pennsylvania Power il Light Co ~

REC IP. ~A:.E RFC IP IF N T AFF ILIA7 ION

SUBJECT:

Notifies of Potential Oef iciencies ER 100450 F ER100508 re States Co sliding links. Failure occurs in form of crack between thr ceded screwhole L side of U shaoed 1 ink,&i 1 1 advise of date of final COPIES RECEIVES:LTR g ENCL Q SIZ ESJB rept'ISTRISUT TUN COOS: 8019S T I l'LF: Cons t ruc t i on Deficiency Reoor t (10CFR50 ~ 55E)

BOOTES: ~g W M~ 3 Q~)re~+~~

RECIPIENT COP IES REC IPIE'TiT COP IES IO DOE/i"JA ETRE LTTR FNCL IO CODE/'Ti A'4E LTTR EN ACTION: AD I() Q~Ar~+21 BC pvry+~od d 15 1 20 PH 1 r

I uTlR~.'AL: AC/RC I/IE AEOD EOO R STAFF 07 EQUIP QUAL BR 16 F I ELO COOR/IE13 HANAUERPS ~

HYD/GEO BR 22 IRE 05 LIC QUAL BR MOOREEV ~

<PA 08 NRC PDR 02, VELD 23 OR ASSESS BR 17 PR C TS l'EV BR QA BR 10 G 01 STANORDS OEV 11 EXTERNAL'CRS 24 16 1 LPOR 03 NS IC 04 1 due 3 p >F80 TOTAL NUi!BER OF COPIES REQUIRED: LTTR 41 ENCL 0

1

0 TWO NORTH NINTH STREET, ALLENTOWN, PA. 18101 PHONE: (215) 821-5151 NORMAN W. CURTIS Vice President Engineering 8 Construction 821-5381 June 23, 1980 Mr. Boyce H. Grier Director, Region I U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania 19406 SUSQUEHANNA STEAM ELECTRIC STATION NOTIFICATION OF A POTENTIAL DEFICIENCY ON STATES COMPANY SLIDING LINKS ERs 100450/100508 FILE 840-4 PLA-499

Dear Mr. Grier:

This letter serves to confirm information provided by telephone to NRC Inspector Mr. R. McGaughy by Mr. A. R. Sabol of PP&L on June 17, 1980. During that conversation, Mr. McGaughy was advised that the subject condition was being evaluated for reportability under the provisions of 10CFR50.55(e).

The defect involves the failure of the U-shaped link on the States Company sliding link terminal block. The failure occurs in the form of a crack between the threaded screwhole and the side of the U-shaped link. The U-shaped link and associated spacer forms a connection between two slotted bars on the terminal block when the spacer and link are tightened by a screw. When the screw is tightened a crack may result which can cause an open or a poor electrical connection. Since these links are used on safety related equipment, the defective condition has been evaluated as potentially reportable under the provisions of 10CFR50.55(e).

The subject defect has also been previously recogni ed by the NRC and was described in your Information Notice 80-08 issued on March 7, 1980.

Bechtel has under development a sampling procedure which includes guidance for their Quality Control field organization to inspect the links. The PP&L Integrated Startup Group will also be instructed to follow the guidance outlined in the sampling plan whenever they operate the links during preoperational testing activities. We expect this approach to provide us with quantitative information on the extent of the deficiency.

Since the details of this report provide information relevant to the reporting requirements of 10CFR21, this correspondence is considered to also discharge any formal responsibility PP&L may have for reporting in compliance thereto.

go/1 5

8OO6S7 o>~ PENNSYLVANIA POWER 4 LIGHT COMPANY

//g

Mr. Boyce H. Grier June 23, 1980 PP&L and Bechtel are continuing to analyze the problem and to establish an acceptable corrective action plan. Based upon the satisfactory completion of our investigation, we will advise the Commission of the date by which a final report will be submitted should the conditions be determined to be reportable.

N. W. Curtis Vice President-Engineering 6 Construction-Nuclear FLW:mcb cc: Mr. Victor Stello (15)

DirectorWffice of Inspection 6 Enforcement U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. G. McDonald, Director Office of Management Information 6 Program Control U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. Robert M. Gallo U. S. Nuclear Regulatory Commission P. 0. Box 52 Shickshinny, Pennsyl'vania 18655