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| {{#Wiki_filter:}} | | {{#Wiki_filter:EDO Principal Correspondence Control FROM: DUE: 04/06/05 EDO CONTROL: G20050160 DOC DT: 03/02/05 FINAL REPLY: |
| | Barry Quigley Rockford, Illinois TO: |
| | Reyes, EDO FOR SIGNATURE OF - ** GRN ** CRC NO: |
| | Dyer, NRR DESC: ROUTING: |
| | 2.206 - Byron Station/IC RCS Cold Leg Loop Stop Reyes Isolation Valve Virgilio Kane Merschoff Silber Dean DATE: 03/07/05 Burns Congel, OE ASSIGNED TO: CONTACT: Caputo, OI Caldwell, RIII NRR Dyer Cyr, OGC Skay, NRR SPECIAL INSTRUCTIONS OR REMARKS: Goldberg, OGC lzqLIoQ £ QboLooQ1 -- etl~s: a0-1 |
| | |
| | March 2, 2005 |
| | |
| | ==Dear Mr. Reyes,== |
| | |
| | This is a request for enforcement action (under 10CFR2.206) against Exelon Nuclear's Byron Station for failure to comply with 10CFR50 Appendix B, Criterion XVI. |
| | Specifically, the 1C RCS Cold Leg Loop Stop Isolation valve (lRC8002C) has been broken for at least 6 years and has not been repaired. |
| | The Byron Reactor Coolant System is equipped with Motor Operated Loop Stop Isolation Valves. These are sometimes difficult to close to the point of protective features of the motor actuating. Our current practice is to reopen the valve and keep attempting to close it until it goes all the way closed. The failure mechanism is metal-to-metal contact between the valve disc and a misaligned valve guide. A repair is available. |
| | We are currently in refueling outage BIR13. Plans had been made for the last year to implement the repair; a high cost, high dose job. Two days before the outage, our senior management got together and started "sharpshooting" the schedule in an attempt to reduce dose. It was decided that if the valve closed without too much trouble, the repair would be pulled from the outage. This morning, the first closing attempt resulted in the protective feature actuating. However on the second attempt the valve closed completely and the repair for this outage cancelled. |
| | I have several concerns: |
| | : 1. The cultural aspect of accepting actuation of a protective function, |
| | : 2. Failure to correct a longstanding equipment issue, |
| | : 3. The excessive emphasis on dose reduction is compromising plant safety. To the uninitiated dose reduction sounds noble, in our case it is allowing the valve to continue to grind metal to metal, leaving debris in the RCS. |
| | : 4. I would like to point out that a significant portion of the site executives' (and my) bonus is tied to meeting aggressive dose goals. This is similar to Davis-Besse where dose prevented adequate head inspections and focus on monetary bonuses by executives caused other major issues. Note that the Institute of Nuclear Power Operations sets these dose goals, so this may be an industry concern. |
| | Due to the small time window available to repair this valve, I am requesting immediate NRC action. |
| | Respectfully, Barry Quigley 3512 Louisiana Rockford, IL 61108 815-397-3392 815-222-4745 EDO -- G20050160 |
| | |
| | ..- :-- I l c:\temD\AWVI00001.TMP F- -- I-- ---- |
| | i Page 1 Mail Envelope Properties (4226373A.562:13: 58722) |
| | |
| | ==Subject:== |
| | Exelon 2.206 Petition Creation Date: 3/2/05 4:59PM From: <barry.quigleygexeloncorp.qom> |
| | Created By: barry.quigley(exeloncorp.com Recipients nrc.gov owf4 o.OWFNDO SDW2 (Sandra Walker) |
| | Post Office Route owf4po.OWFNDO nrc.gov Files Size Date & Time MESSAGE 1184 03/02/05 04:59PM Exelon 2.206 Petition.doc 23040 Mime.822 34671 Options Expiration Date: None-Priority: Standard Reply Requested: No Return Notification: None Concealed |
| | |
| | ==Subject:== |
| | No Security: Standard}} |
Latest revision as of 21:52, 11 January 2020
Letter Sequence Request |
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MONTHYEARML0506802552005-03-0202 March 2005 G20050160 - Barry Quigley Ltr Re 2.206 - Byron Station/1C RCS Cold Leg Loop Stop Isolation Valve Project stage: Request ML0516701922005-03-18018 March 2005 E-mail, Byron #2 Project stage: Request ML0516605342005-03-18018 March 2005 E-mail Re Byron Lsiv Drawing Project stage: Request ML0516605412005-03-18018 March 2005 E-mail Re Byron #3 Project stage: Request ML0516605272005-03-18018 March 2005 E-mail from Chrzanowski to NRC, Documents 2, 7 and 8 (Attached) Project stage: Request ML0516605292005-03-18018 March 2005 E-mail from Chrzanowski to NRC, Byron Lsv Info 1 Project stage: Request ML0516605442005-03-19019 March 2005 Fwd: 1C Lsiv Data Project stage: Request ML0508205302005-04-20020 April 2005 Summary of Meeting with Exelon Nuclear Regarding the Performance of the 1C Loop Stop Isolation Valve at Byron Station, Unit 1 Project stage: Meeting ML0509701182005-05-0404 May 2005 RAI, 1C Loop Stop Isolation Valve Project stage: RAI RS-05-070, Response to Request for Additional Information Regarding the Plant Loop Stop Isolation Valve2005-05-27027 May 2005 Response to Request for Additional Information Regarding the Plant Loop Stop Isolation Valve Project stage: Response to RAI ML0519403522005-07-29029 July 2005 G20050160 - Barry Quigley Ltr 2.206 Proposed Director'S Decision Regarding Loop Stop Isolation Valve - Byron Station, Unit 1 Project stage: Other ML0519401792005-08-0101 August 2005 G20050160 - Christopher M. Crane Ltr. 2.206 Draft Director'S Decision Regarding Loop Stop Isolation Valve - Byron Station, Unit 1 Project stage: Draft Other ML0525002412005-08-12012 August 2005 Comments on Proposed Director'S Decision by Exelon Regarding 2.206 Petition Re Byron Station Project stage: Request ML0525002442005-08-14014 August 2005 Comments by Barry Qugley Re Proposed Director'S Decision on 2.206 Petition for Byron Station Project stage: Request ML0528602852005-10-19019 October 2005 G20050160 - Herbert N. Berkow, Memo to Address Comments on Proposed Director'S Decision Regarding Byron Station, Unit 1 LOOP Stop Isolation Valve 2.209 Petition Project stage: Request ML0529400912005-11-0808 November 2005 G20050160 - Director'S Decision Under 10 CFR 2.206 in the Matter of Exelon Generation Company, LLC, Byron Station, Unit 1 LOOP Stop Isolation Valve Project stage: Other ML0528601592005-11-0808 November 2005 G20050160 - Barry Quigley Ltr Re. Byron 2.206 Petition Regarding Station/1C RCS Cold Leg Loop Stop Isolation Valve Project stage: Other 2005-04-20
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Text
EDO Principal Correspondence Control FROM: DUE: 04/06/05 EDO CONTROL: G20050160 DOC DT: 03/02/05 FINAL REPLY:
Barry Quigley Rockford, Illinois TO:
Reyes, EDO FOR SIGNATURE OF - ** GRN ** CRC NO:
Dyer, NRR DESC: ROUTING:
2.206 - Byron Station/IC RCS Cold Leg Loop Stop Reyes Isolation Valve Virgilio Kane Merschoff Silber Dean DATE: 03/07/05 Burns Congel, OE ASSIGNED TO: CONTACT: Caputo, OI Caldwell, RIII NRR Dyer Cyr, OGC Skay, NRR SPECIAL INSTRUCTIONS OR REMARKS: Goldberg, OGC lzqLIoQ £ QboLooQ1 -- etl~s: a0-1
March 2, 2005
Dear Mr. Reyes,
This is a request for enforcement action (under 10CFR2.206) against Exelon Nuclear's Byron Station for failure to comply with 10CFR50 Appendix B, Criterion XVI.
Specifically, the 1C RCS Cold Leg Loop Stop Isolation valve (lRC8002C) has been broken for at least 6 years and has not been repaired.
The Byron Reactor Coolant System is equipped with Motor Operated Loop Stop Isolation Valves. These are sometimes difficult to close to the point of protective features of the motor actuating. Our current practice is to reopen the valve and keep attempting to close it until it goes all the way closed. The failure mechanism is metal-to-metal contact between the valve disc and a misaligned valve guide. A repair is available.
We are currently in refueling outage BIR13. Plans had been made for the last year to implement the repair; a high cost, high dose job. Two days before the outage, our senior management got together and started "sharpshooting" the schedule in an attempt to reduce dose. It was decided that if the valve closed without too much trouble, the repair would be pulled from the outage. This morning, the first closing attempt resulted in the protective feature actuating. However on the second attempt the valve closed completely and the repair for this outage cancelled.
I have several concerns:
- 1. The cultural aspect of accepting actuation of a protective function,
- 2. Failure to correct a longstanding equipment issue,
- 3. The excessive emphasis on dose reduction is compromising plant safety. To the uninitiated dose reduction sounds noble, in our case it is allowing the valve to continue to grind metal to metal, leaving debris in the RCS.
- 4. I would like to point out that a significant portion of the site executives' (and my) bonus is tied to meeting aggressive dose goals. This is similar to Davis-Besse where dose prevented adequate head inspections and focus on monetary bonuses by executives caused other major issues. Note that the Institute of Nuclear Power Operations sets these dose goals, so this may be an industry concern.
Due to the small time window available to repair this valve, I am requesting immediate NRC action.
Respectfully, Barry Quigley 3512 Louisiana Rockford, IL 61108 815-397-3392 815-222-4745 EDO -- G20050160
..- :-- I l c:\temD\AWVI00001.TMP F- -- I-- ----
i Page 1 Mail Envelope Properties (4226373A.562:13: 58722)
Subject:
Exelon 2.206 Petition Creation Date: 3/2/05 4:59PM From: <barry.quigleygexeloncorp.qom>
Created By: barry.quigley(exeloncorp.com Recipients nrc.gov owf4 o.OWFNDO SDW2 (Sandra Walker)
Post Office Route owf4po.OWFNDO nrc.gov Files Size Date & Time MESSAGE 1184 03/02/05 04:59PM Exelon 2.206 Petition.doc 23040 Mime.822 34671 Options Expiration Date: None-Priority: Standard Reply Requested: No Return Notification: None Concealed
Subject:
No Security: Standard