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{{#Wiki_filter:03/21/2011                    U.S. Nuclear Regulatory Commission OperationsCenter Event Report                          Pare I Power Reactor                                                                                      Event#        46688 Site: FORT CALHOUN                                Notification Date I Time: 03/21/2011      13:19  (EDT)
Unit:  1            Region: 4        State: NE          Event Date/ Time: 03/18/2011                (CDT)
Reactor Type:  (1) CE                                            Last Modification: 03/21/2011 Containment Type:      DRY AMB NRC Notified by: DONNA GUINN                                      Notifications: GREG PICK                      R4DO HQ Ops Officer: CHARLES TEAL                                                        PART 21 GROUP Emergency Class: NON EMERGENCY 10 CFR Section:
21.21                UNSPECIFIED PARAGRAPH Unit Scram Code      RX Crit Init Power    Initial RX Mode                Curr Power    Current RX Mode 1        N            Yes    100          Power Operation                100          Power Operation DEFECTIVE KPR-14DG-125 RELAYS DISCOVERED DURING BENCH TESTING "The following event description is based on information currently available. The condition is reported under 10 CFR 21.21(d)(3)(i).
"Part 21 Report - Potter Brumfield KRP-14DG-125 Relays, supplied by Southern Testing Services (STS) division of Argo Turboserve Corporation (ATC).
"On March 17, 2011, during bench testing of the KRP-14DG-125 Relays, Fort Calhoun Station (FCS) discovered that some of these relays were defective in that one of the contacts would not close properly after energizing and de-energizing the relay coils. If installed in the plant, the improper closure of this contact could defeat the safety function of the relays that provide a signal to the component supported by that contact. This deviation from the design specifications is reportable per 10 CFR 21. FCS does not have any of the affected relays installed in the plant.
"FCS returned the batch of relays to the vendor for further failure modes and effects evaluation and reporting.
"FCS has not provided any of these relays from our stock to any other licensee.
"The vendor and the [NRC] resident inspector have been notified."
PAGE 1 OF 2 NRC FORM 361                                                                                                                                  U.S. NUCLEAR REGULATORY COMMISSION (12-2000)                                                                              REACTOR PLANT                                                          OPERATIONS CENTER EVENT NOTIFICATION WORKSHEET                                                            EN #
NRC OPERATION TELEPHONE NUMBER: PRIMARY - 301-816-5100 or 800-532-3469*, BACKUPS - [1st] 301-951-0550 or 800-449-3694*,
  ,*,rli*  -Ai*--*n      n d rA',r1        -Air        1                                                -1i        *      ;*  ;  .  . ,,+    r-TQ    ,    fl,
* 40      *.1.        fl6 NOTIFICATIONR  liE        _    AILOODR-MANIZA1IObL.                                  UNIT        ~      IM  EAL        ~CALL                                            BACK #
Ft. Calhoun Station                                    17~        Donna Guinn                              ~42537337 EVENT lIME & ZONE            EVENT DAM                                                                            7                  PCINERMODE AFTER                                  -
L      03/18/2011                            =          10%          1                                                          10 0%l EVENT CLASSIFICATIONS                                    1-Hr. Non-Emergency 10 CFR 50.72(b)(1) I                            I v)(A)      Safe SID Capability                      AMA GENERALEMERGENCY                                GENEC        r              TS Deviation                            ADEV      E    (v)(B)    RHR Capability                            AINB SITE AEEERGENCY                                  Srr/AAEC      4-Hr. Non-Emergency 10 CFR 50.72(b)(2)                          __j(v)(C)        Control of Rad Release                    AINC ALERT                                          ALEIAAEC          WI        TS Required SIT)                        ASHU              v)D        c    idetitaio                        AIN)
UNUSUAL EVENT                                  LN,,EC            J(iv)(A)  ECCS Discharge to RCS                    ACCS        -(xii)          Offsite Medical                          NvED
:    50.72 NON-EMERGENCY                    (see next columns)        .(iv)(B)    RPS Actuation (scram)                    AJ4-S        [(,dii)      Loss Comm/AsmtlResp                      ACOM PHYSICAL SECURITY (73.71)                            ___    - I((x)        Ofisite Notification                      APRE              60-Day Optional 10 CFR 50.73(a)(1)
MATEI Ai          RE                                  Bfn      8-Hr. Non-Emergency 10 CFR 50.72(b)(3)                                            Invalid Specified System Actuation        ANV FITNESS FOR DUTY                                      HR1T 1(ii)(A)        Degraded Condition                      ADEG        Other Unspecified Requirement (Identify)
      -OTHERUNSPECIIED            .            (seelastcolumn)          (iiXB)    Unanalyzed Condition                    AUNA                  10 CFR 21. 21 (d) (3) (i)
INFORMATION ONLY                                      NIMF      [Iiv)(A)  Specified System Actuation                ASFl DESCRIPTION Include: Systems affected, actuations and their initiating signals, causes, effect of event on plant, actions taken or planned, etc. (Continue on back)
The following event description is based on information currently available.                                                                                                    The condition is reported under 10 CFR 21.21(d) (3) (i).
Part 21 Report - Potter Brumfield KRP-14DG-125 Relays, supplied by Southern Testing Services (STS) division of Argo Turboserve Corporation (ATC).
On March 17, 2011, during bench testing of the KRP-14DG-125 Relays, Fort Calhoun Station (FCS) discovered that some of these relays were defective in that one of the contacts would not close properly after                                          energizing and de-energizing the relay coils.                                                          If installed          in the plant, the improper closure of this                                                      contact could defeat the safety function of the relays that provide a signal to the component supported by that contact.
This deviation from the design specifications is reportable per 10 CFR 21.                                                                                                FCS does not have any of the affected relays installed                                                        in the plant.
FCS returned the batch of relays to the vendor for further                                                                        failure modes and effects evaluation and reporting.
FCS has not provided any of these relays from our stock to any other licensee.
The vendor and the resident                                    inspector have been notified.
NOTIFICATIONS                        YES        NO        WILL BE        ANYTHING UNUSUAL OR                        YES (Explain above)                  ~      NO NOTIFICATIONS                            YES        NO        WILL BE        ANYTHING UNUSUAL OR NRC RESIDENT                                                                  NOT UNDERSTOOD?                            YES (Explain above)                        NO STATE(s)                                                                      ]DID ALL SYSTEMS LOCAL                                                                          FUNCTION AS REQUIRED?                []    YES                                        NO (Explain above)
OTHER GOV AGENCIES                                    ______ODE              M    OF OPERATION                  ESTIMATED                  n/a          ADDITONAL INFO ON BACK MEDIAIPRESS RELEASE                    i*-                                    UNTIL CORRECTED:            1      RESTART DATE:                n/a          UYES                  MNO
____ ____ _                                                                                                                    YS                  N NRC FORM 361 (12-2000)                                                                                                                                                      PRINTED ON RECYCLED PAPER}}

Latest revision as of 02:50, 13 November 2019

Notification of Potential Part 21 Re Defective KPR-14G-125 Relays Discovered During Bench Testing
ML110810064
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 03/21/2011
From: Guinn D
Omaha Public Power District
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
46688
Download: ML110810064 (2)


Text

03/21/2011 U.S. Nuclear Regulatory Commission OperationsCenter Event Report Pare I Power Reactor Event# 46688 Site: FORT CALHOUN Notification Date I Time: 03/21/2011 13:19 (EDT)

Unit: 1 Region: 4 State: NE Event Date/ Time: 03/18/2011 (CDT)

Reactor Type: (1) CE Last Modification: 03/21/2011 Containment Type: DRY AMB NRC Notified by: DONNA GUINN Notifications: GREG PICK R4DO HQ Ops Officer: CHARLES TEAL PART 21 GROUP Emergency Class: NON EMERGENCY 10 CFR Section:

21.21 UNSPECIFIED PARAGRAPH Unit Scram Code RX Crit Init Power Initial RX Mode Curr Power Current RX Mode 1 N Yes 100 Power Operation 100 Power Operation DEFECTIVE KPR-14DG-125 RELAYS DISCOVERED DURING BENCH TESTING "The following event description is based on information currently available. The condition is reported under 10 CFR 21.21(d)(3)(i).

"Part 21 Report - Potter Brumfield KRP-14DG-125 Relays, supplied by Southern Testing Services (STS) division of Argo Turboserve Corporation (ATC).

"On March 17, 2011, during bench testing of the KRP-14DG-125 Relays, Fort Calhoun Station (FCS) discovered that some of these relays were defective in that one of the contacts would not close properly after energizing and de-energizing the relay coils. If installed in the plant, the improper closure of this contact could defeat the safety function of the relays that provide a signal to the component supported by that contact. This deviation from the design specifications is reportable per 10 CFR 21. FCS does not have any of the affected relays installed in the plant.

"FCS returned the batch of relays to the vendor for further failure modes and effects evaluation and reporting.

"FCS has not provided any of these relays from our stock to any other licensee.

"The vendor and the [NRC] resident inspector have been notified."

PAGE 1 OF 2 NRC FORM 361 U.S. NUCLEAR REGULATORY COMMISSION (12-2000) REACTOR PLANT OPERATIONS CENTER EVENT NOTIFICATION WORKSHEET EN #

NRC OPERATION TELEPHONE NUMBER: PRIMARY - 301-816-5100 or 800-532-3469*, BACKUPS - [1st] 301-951-0550 or 800-449-3694*,

,*,rli* -Ai*--*n n d rA',r1 -Air 1 -1i *  ;*  ; . . ,,+ r-TQ , fl,

  • 40 *.1. fl6 NOTIFICATIONR liE _ AILOODR-MANIZA1IObL. UNIT ~ IM EAL ~CALL BACK #

Ft. Calhoun Station 17~ Donna Guinn ~42537337 EVENT lIME & ZONE EVENT DAM 7 PCINERMODE AFTER -

L 03/18/2011 = 10% 1 10 0%l EVENT CLASSIFICATIONS 1-Hr. Non-Emergency 10 CFR 50.72(b)(1) I I v)(A) Safe SID Capability AMA GENERALEMERGENCY GENEC r TS Deviation ADEV E (v)(B) RHR Capability AINB SITE AEEERGENCY Srr/AAEC 4-Hr. Non-Emergency 10 CFR 50.72(b)(2) __j(v)(C) Control of Rad Release AINC ALERT ALEIAAEC WI TS Required SIT) ASHU v)D c idetitaio AIN)

UNUSUAL EVENT LN,,EC J(iv)(A) ECCS Discharge to RCS ACCS -(xii) Offsite Medical NvED

50.72 NON-EMERGENCY (see next columns) .(iv)(B) RPS Actuation (scram) AJ4-S [(,dii) Loss Comm/AsmtlResp ACOM PHYSICAL SECURITY (73.71) ___ - I((x) Ofisite Notification APRE 60-Day Optional 10 CFR 50.73(a)(1)

MATEI Ai RE Bfn 8-Hr. Non-Emergency 10 CFR 50.72(b)(3) Invalid Specified System Actuation ANV FITNESS FOR DUTY HR1T 1(ii)(A) Degraded Condition ADEG Other Unspecified Requirement (Identify)

-OTHERUNSPECIIED . (seelastcolumn) (iiXB) Unanalyzed Condition AUNA 10 CFR 21. 21 (d) (3) (i)

INFORMATION ONLY NIMF [Iiv)(A) Specified System Actuation ASFl DESCRIPTION Include: Systems affected, actuations and their initiating signals, causes, effect of event on plant, actions taken or planned, etc. (Continue on back)

The following event description is based on information currently available. The condition is reported under 10 CFR 21.21(d) (3) (i).

Part 21 Report - Potter Brumfield KRP-14DG-125 Relays, supplied by Southern Testing Services (STS) division of Argo Turboserve Corporation (ATC).

On March 17, 2011, during bench testing of the KRP-14DG-125 Relays, Fort Calhoun Station (FCS) discovered that some of these relays were defective in that one of the contacts would not close properly after energizing and de-energizing the relay coils. If installed in the plant, the improper closure of this contact could defeat the safety function of the relays that provide a signal to the component supported by that contact.

This deviation from the design specifications is reportable per 10 CFR 21. FCS does not have any of the affected relays installed in the plant.

FCS returned the batch of relays to the vendor for further failure modes and effects evaluation and reporting.

FCS has not provided any of these relays from our stock to any other licensee.

The vendor and the resident inspector have been notified.

NOTIFICATIONS YES NO WILL BE ANYTHING UNUSUAL OR YES (Explain above) ~ NO NOTIFICATIONS YES NO WILL BE ANYTHING UNUSUAL OR NRC RESIDENT NOT UNDERSTOOD? YES (Explain above) NO STATE(s) ]DID ALL SYSTEMS LOCAL FUNCTION AS REQUIRED? [] YES NO (Explain above)

OTHER GOV AGENCIES ______ODE M OF OPERATION ESTIMATED n/a ADDITONAL INFO ON BACK MEDIAIPRESS RELEASE i*- UNTIL CORRECTED: 1 RESTART DATE: n/a UYES MNO

____ ____ _ YS N NRC FORM 361 (12-2000) PRINTED ON RECYCLED PAPER