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| issue date = 04/17/1991
| issue date = 04/17/1991
| title = Special Rept:On 910320,1B Emergency Diesel Generator (DG) Nonvalid Failure Occurred Due to Circuitry Failure of DG Synchronizing Circuitry.Relay Exhibiting Binding Calibr & Will Be Replaced
| title = Special Rept:On 910320,1B Emergency Diesel Generator (DG) Nonvalid Failure Occurred Due to Circuitry Failure of DG Synchronizing Circuitry.Relay Exhibiting Binding Calibr & Will Be Replaced
| author name = SAGER D A
| author name = Sager D
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:ACCELERATED DISUTIONDEMONSTRATION SYSTEMtrREGULATORY INFORMATXON DISTRIBUTION SYSTEM(RIDS)ACCESSION NBR:9104240135 DOC.DATE:91/04/17NOTARIZED:
{{#Wiki_filter:ACCELERATED DIS                        UTION DEMONSTRATION SYSTEM t
NOFACIL:50-335 St.LuciePlant,Unit.1,FloridaPower6LightCo.AUTH.NAMEAUTHORAFFILIATXON SAGER,D.A.
r REGULATORY INFORMATXON DISTRIBUTION SYSTEM (RIDS)
FloridaPowerSLightCo.RECIP.NAME RECIPIENT AFFXLIATION DocumentControlBranch(Document ControlDesk)
ACCESSION NBR: 9104240135             DOC. DATE: 91/04/17    NOTARIZED: NO          DOCKET FACIL:50-335 St. Lucie Plant, Unit. 1, Florida Power              6  Light  Co. 05000335 AUTH. NAME            AUTHOR AFFILIATXON SAGER,D.A.            Florida      Power S Light Co.
RECIP.NAME           RECIPIENT AFFXLIATION Document Control Branch (Document           Control Desk)           R


==SUBJECT:==
==SUBJECT:==
Specialrept:on910320,1B emergency dieselgenerator non-valid duringsurveillance testing.Sys protection testedrelayelectriclly 6foundoperable&plamsavailable toreplaceengineering dedication.W/910417 ltr.DISTRIBUTION CODE:ROOIDCOPIESRECEIVED:LTR
Special rept:on 910320,1B emergency diesel generator non-valid during surveillance testing.Sys protection tested relay electriclly 6 found operable & plams available to replace engineering dedication.W/910417 ltr.                                     D DISTRIBUTION CODE: ROOID            COPIES RECEIVED:LTR     )
)ENCLISIZE:TITLE:ORSubmittal:
ENCL    I  SIZE:
GeneralDistribution NOTES:DOCKET05000335RDARECIPIENT IDCODE/NAME PD2-2LANORRIS,JXNTERNAL:
TITLE: OR  Submittal: General Distribution NOTES:
ACRSNRR/DET/ESGB NRR/DSTSE2NRR/DST/SICB 7ENUDOCS-ABSTRACT OGC/HDS3RES/DSXR/EIB EXTERNAL:
A RECIPIENT                COPIES          RECIPIENT          COPIES ID  CODE/NAME             LTTR ENCL      ID CODE/NAME        LTTR ENCL          D PD2-2 LA                      1    1    PD2-2 PD                1    1 NORRIS,J                      2    2                                              D XNTERNAL: ACRS                          6    6    NRR/DET/ECMB 9H        1    1 NRR/DET/ESGB                 1    1    NRR/DOEA/OTSB1 1        1    1 NRR/DST          SE2          1    1    NRR/DST/SELB SD        1    1 NRR/DST/SICB 7E              1    1    NRR/DST/SRXB 8E        1    1 NUDOCS-ABSTRACT               1    1    OC                      1    0 OGC/HDS3                      1    0    KE  FXLE      Ol      1    1 RES/DSXR/EIB                 1    1 EXTERNAL: NRC PDR                        1    1    NSIC                    1    1 R
NRCPDRCOPIESLTTRENCL11226611111111101111RECIPIENT IDCODE/NAME PD2-2PDNRR/DET/ECMB 9HNRR/DOEA/OTSB1 1NRR/DST/SELB SDNRR/DST/SRXB 8EOCKEFXLEOlNSICCOPIESLTTRENCL1111111111101111DDRDNOTETOALL"RIDS"RECIPIENTS:
D D
PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMP1-37(EXT.20079)TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!TOTALNUMBEROFCOPIESREQUIRED:
D NOTE TO ALL "RIDS" RECIPIENTS:
LTTR24ENCL22DD P.O.Box,Ft.Pierce,FL34954-0128 April17,1991L-91-12210CFR50.36 U.SNuclearRegulatory Commission Attn:DocumentControlDeskWashington, DC20555Gentlemen:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
Re:St.LucieUnit1DocketNo.50-335SpecialReportDateofEvent:March20,1991EmerencDieselGenerator FailureTheattachedSpecialReportisbeingtransmitted pursuanttotherequirements ofSt.LucieUnit1Technical Specifications 4.8.1.1.3 and6.9.2.Thereportprovidesnotification ofa1BEmergency DieselGenerator non-valid failureduringsurveillance testing.Shouldtherebeanyquestions onthisinformation, pleasecontactuseVerytrulyyours,D.A.VicegersidentSt.LuciePlantDAS:GRM:kw DAS/PSL5416Attachment cc:StewartD.Ebneter,RegionalAdministrator, RegionII,USNRCSeniorResidentInspector, USNRC,St.LuciePlant9104240135 910417PDRADOCK05000335SPDRP,$~,g~9QnFPLGroupcompany NRCSPECIALREPORTDIESELGENERATOR NON-VALID FAILUREAt0904onMarch20,1991,theSt.LucieUnitOne1BEmergency DieselGenerator wasstartedforitsmonthlysurveillance run.Severalattemptsweremadetosynchronize thedieselgenerator ontothegrid;however,theD/Goutputbreakerwouldnotclose.Electrical Maintenance wascalledintotroubleshoot thesynchronizing circuitry, andthe1Bdieselgenerator wasshutdownanddeclaredoutofserviceat0947.Corrective Actions:Electrical Maintenance Personnel determined thattheD/Gsynchronizing relaywasmalfunctioning.
TOTAL NUMBER OF COPIES REQUIRED: LTTR              24  ENCL    22
SystemProtection personnel testedtherelayelectrically andfoundittobeoperable.
 
However,mechanical manipulation ofthecontactarmscausedbinding.Acalibration oftherelaywasperformed anditwasnotedthattherelayexhibited intermittent bindingofthecontacts.
P.O. Box, Ft. Pierce, FL 34954-0128 April 17, 1991 L-91-122 10CFR50.36 U. S  Nuclear Regulatory Commission Attn:   Document Control Desk Washington,         DC      20555 Gentlemen:
Noreplacement relayswereavailable atthetimeofthisfailure.Plansareinplacetoreplacetherelayfollowing anengineering dedication ofareplacement, andPC/Mpackage.The1Bdieselgenerator wasrestarted at1248andtheoutputbreakerwasclosedat1255.Thesurveillance wassuccessfully completed at1407andthedieselwasdeclaredbackinservice.Thedieselwasdeclaredoutofserviceforatotalof4hoursand20minutes.Theproblemwasevaluated tobeanon-valid failureperRegulatory Guide1~108C.2.e.2,inthattheaffectedcircuitry wastheD/Gsynchronizing circuitry.
Re:     St. Lucie Unit          1 Docket No. 50-335 Special Report Date of Event: March 20, 1991 Emer enc Diesel Generator Failure The attached          Special Report is being transmitted pursuant to the requirements of St. Lucie Unit 1 Technical Specifications 4.8.1.1.3 and 6.9.2.             The report provides notification of a 1B Emergency Diesel Generator non-valid failure during surveillance testing.
Thiscircuitry isusedforsurveillance purposesonly,whenthedieselmustbetiedontothelivebus.DuringaLossofOffsitePowerevent,thiscircuitry isbypassedandtheD/Gwillautomatically pickuptheplantsafetybus.Atnotimeduringthiseventwasthedieselgenerator unabletoperformitsintendedsafetyfunction.
Should there be any questions on          this information, please contact use Very    truly yours, D. A.       ger Vice          sident St. Lucie Plant DAS:GRM:kw DAS/PSL 5416 Attachment cc:     Stewart D. Ebneter, Regional Administrator, Region                    II, USNRC Senior Resident Inspector, USNRC, St. Lucie Plant 9104240135 910417 PDR    ADOCK 05000335 S                          PDR P,$ ~, g ~9 Qn FPL Group company
FailureSummary:Withtherecentincorporation ofamendments toTechnical Specification 3.8.1.1(July1990),therehavebeennorecordedvalidfailuresofthe1BEmergency DieselGenerator andnine(9)successful starts.Thesurveillance frequency remainsonceper31daysasperTechSpec3.8.1.1.}}
 
NRC SPECIAL REPORT DIESEL GENERATOR NON-VALID FAILURE At 0904 on March 20, 1991, the St. Lucie Unit One 1B Emergency Diesel Generator was started for its monthly surveillance run. Several attempts were made to synchronize the diesel generator onto the grid; however, the D/G output breaker would not close. Electrical Maintenance was called in to troubleshoot the synchronizing circuitry, and the 1B diesel generator was shut down and declared out of service at 0947.
Corrective Actions: Electrical Maintenance Personnel determined that the D/G synchronizing relay was malfunctioning. System Protection personnel tested the relay electrically and found it to be operable. However, mechanical manipulation of the contact arms caused binding. A calibration of the relay was performed and it was noted that the relay exhibited intermittent binding of the contacts. No replacement relays were available at the time of this failure. Plans are in place to replace the relay following an engineering dedication of a replacement, and PC/M package. The 1B diesel generator was restarted at 1248 and the output breaker was closed at 1255. The surveillance was successfully completed at 1407 and the diesel was declared back in service. The diesel was declared out of service for a total of 4 hours and 20 minutes.
The problem was evaluated to be a non-valid failure per Regulatory Guide 1 108 C.2.e.2, in that the affected circuitry was the D/G synchronizing
  ~
circuitry. This circuitry is used for surveillance purposes only, when the diesel must be tied onto the live bus. During a Loss of Offsite Power event, this circuitry is bypassed and the D/G will automatically pick up the plant safety bus. At no time during this event was the diesel generator unable to perform its intended safety function.
Failure Summary: With the recent incorporation of amendments to Technical Specification 3.8.1.1 (July 1990), there have been no recorded valid failures of the 1B Emergency Diesel Generator and nine (9) successful starts. The surveillance frequency remains once per 31 days as per Tech Spec 3.8.1.1.}}

Latest revision as of 22:45, 29 October 2019

Special Rept:On 910320,1B Emergency Diesel Generator (DG) Nonvalid Failure Occurred Due to Circuitry Failure of DG Synchronizing Circuitry.Relay Exhibiting Binding Calibr & Will Be Replaced
ML17223B168
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 04/17/1991
From: Sager D
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-91-122, NUDOCS 9104240135
Download: ML17223B168 (3)


Text

ACCELERATED DIS UTION DEMONSTRATION SYSTEM t

r REGULATORY INFORMATXON DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR: 9104240135 DOC. DATE: 91/04/17 NOTARIZED: NO DOCKET FACIL:50-335 St. Lucie Plant, Unit. 1, Florida Power 6 Light Co. 05000335 AUTH. NAME AUTHOR AFFILIATXON SAGER,D.A. Florida Power S Light Co.

RECIP.NAME RECIPIENT AFFXLIATION Document Control Branch (Document Control Desk) R

SUBJECT:

Special rept:on 910320,1B emergency diesel generator non-valid during surveillance testing.Sys protection tested relay electriclly 6 found operable & plams available to replace engineering dedication.W/910417 ltr. D DISTRIBUTION CODE: ROOID COPIES RECEIVED:LTR )

ENCL I SIZE:

TITLE: OR Submittal: General Distribution NOTES:

A RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL D PD2-2 LA 1 1 PD2-2 PD 1 1 NORRIS,J 2 2 D XNTERNAL: ACRS 6 6 NRR/DET/ECMB 9H 1 1 NRR/DET/ESGB 1 1 NRR/DOEA/OTSB1 1 1 1 NRR/DST SE2 1 1 NRR/DST/SELB SD 1 1 NRR/DST/SICB 7E 1 1 NRR/DST/SRXB 8E 1 1 NUDOCS-ABSTRACT 1 1 OC 1 0 OGC/HDS3 1 0 KE FXLE Ol 1 1 RES/DSXR/EIB 1 1 EXTERNAL: NRC PDR 1 1 NSIC 1 1 R

D D

D NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 22

P.O. Box, Ft. Pierce, FL 34954-0128 April 17, 1991 L-91-122 10CFR50.36 U. S Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 Gentlemen:

Re: St. Lucie Unit 1 Docket No. 50-335 Special Report Date of Event: March 20, 1991 Emer enc Diesel Generator Failure The attached Special Report is being transmitted pursuant to the requirements of St. Lucie Unit 1 Technical Specifications 4.8.1.1.3 and 6.9.2. The report provides notification of a 1B Emergency Diesel Generator non-valid failure during surveillance testing.

Should there be any questions on this information, please contact use Very truly yours, D. A. ger Vice sident St. Lucie Plant DAS:GRM:kw DAS/PSL 5416 Attachment cc: Stewart D. Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, St. Lucie Plant 9104240135 910417 PDR ADOCK 05000335 S PDR P,$ ~, g ~9 Qn FPL Group company

NRC SPECIAL REPORT DIESEL GENERATOR NON-VALID FAILURE At 0904 on March 20, 1991, the St. Lucie Unit One 1B Emergency Diesel Generator was started for its monthly surveillance run. Several attempts were made to synchronize the diesel generator onto the grid; however, the D/G output breaker would not close. Electrical Maintenance was called in to troubleshoot the synchronizing circuitry, and the 1B diesel generator was shut down and declared out of service at 0947.

Corrective Actions: Electrical Maintenance Personnel determined that the D/G synchronizing relay was malfunctioning. System Protection personnel tested the relay electrically and found it to be operable. However, mechanical manipulation of the contact arms caused binding. A calibration of the relay was performed and it was noted that the relay exhibited intermittent binding of the contacts. No replacement relays were available at the time of this failure. Plans are in place to replace the relay following an engineering dedication of a replacement, and PC/M package. The 1B diesel generator was restarted at 1248 and the output breaker was closed at 1255. The surveillance was successfully completed at 1407 and the diesel was declared back in service. The diesel was declared out of service for a total of 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> and 20 minutes.

The problem was evaluated to be a non-valid failure per Regulatory Guide 1 108 C.2.e.2, in that the affected circuitry was the D/G synchronizing

~

circuitry. This circuitry is used for surveillance purposes only, when the diesel must be tied onto the live bus. During a Loss of Offsite Power event, this circuitry is bypassed and the D/G will automatically pick up the plant safety bus. At no time during this event was the diesel generator unable to perform its intended safety function.

Failure Summary: With the recent incorporation of amendments to Technical Specification 3.8.1.1 (July 1990), there have been no recorded valid failures of the 1B Emergency Diesel Generator and nine (9) successful starts. The surveillance frequency remains once per 31 days as per Tech Spec 3.8.1.1.