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| issue date = 01/23/1981
| issue date = 01/23/1981
| title = LER 80-038/03L-0:on 801224,testing of Main Feedwater Check Valves Not Performed as Required Per Inservice Insp Program in Preparation for Startup.Caused by Misinterpreted Checkoff Sheet.Temporary Change Sheet Initiated
| title = LER 80-038/03L-0:on 801224,testing of Main Feedwater Check Valves Not Performed as Required Per Inservice Insp Program in Preparation for Startup.Caused by Misinterpreted Checkoff Sheet.Temporary Change Sheet Initiated
| author name = STEPHENS T R
| author name = Stephens T
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:NRC Cv6RhT 366, U.S.NUCLEAR REGULATORY COMMISSION 0 73)LICENSEE EVENT REPORT CONTROL BLOCK: Q (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
{{#Wiki_filter:NRC Cv6RhT 366,                                                                                                                   U. S. NUCLEAR REGULATORY COMMISSION 0 73)
I 6~oi M I D C C 2 Q2 0 P Q4 QE~Qs 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T KK soURGE~LQ<<'O O>>6 Q>>QB 0 1 8 1 Qe 7 8 60 61 DOCKET NUMBER 68 69EVENT DATE 74~75 REPbRT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO IN PREPARATION FOR START UP THE TESTING OF'W-118-1 2 3 4 AS RE VIREO BY THE IS I PROGRAM WHILE IN h10DE 3 WAS NOT DONE.(T.S.4.0.5)THE (4)MAIN FEEDWATER CHECK VALVES NOT BEING TESTED HAD NO EFFECT ON THE HEALTH AND SAFETY OF THE PUBLIC o 6 IN AS MUCH AS THERE ARE MOTOR OPERATED AND AIR OPERATED VALVES UPSTREAM OF THESE~o 6 VALVES THAT WOULD STOP REVERSE FLOW.i~O7~OB 7 8 9 80 7 8 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~o,e~CN Q11 0 Q12~Z Q13 Z Z Z Z Z Z Q4~ZQEE~Z QER 9 10 11 12 , 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LE R)RO EVENT YEAR REPORT NO.CODE TYPE NO.Q17 REPQRT~0~~7~ILJ~~IILII~~~[gJ 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT.
LICENSEE EVENT REPORT CONTROL BLOCK:
NPRDR PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS O22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER
I                                6 Q                 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
~GQER~ZQTE~ZQ23 I 2 IQ 0 N Q23~NQ24~ZQEs Z 9 9 9 QEs 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o THE FACT THAT THESE VALVES WERE NOT TESTED WAS MASKED BY THE FACT THAT SIGN OFFS FOR OTHER MODE TESTS ALSO APPEARED ON THE SAME CHECKOFF SHEET.A TEMPORARY CHANGE SHEET WAS WRITTEN TO SEPARATE THE TEST AS TO THEIR MODE RE UIREMENTS.
  ~oi 7      8    9 M     I     D     C LICENSEE CODE C     2 14 Q2 15 0     P LICENSE NUMBER                       25 Q4    26       LICENSE TYPE       30 QE~ 57 CAT 58 Qs KK 7
OTHER 3 PROCEDURES ARE BEING REVIEWED FOR SIMILIAR PROBLEMS.PUBLICITY ISSUED DESCRIPTION Q O~NQ44 B7.6609'6H'P NA 8 9 FACILITY STATUS%POWER OTHER STATUS~ls C Q23~10 0 Qss NA 7 8 9 10 12 13 44 ACTIVITY CONTENT RELEbSED OF RELEASE AMOUNT OF ACTIVITY Q 6~Q33~~Q34 7 8 9 10 44 PERSONNEL EXPOSURES 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41
CON'T 8
~TR~00 0 Q43 NA 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY 43 TYPE DESCRIPTION Z Q42 NA 7 8 9 10 80 80 80 80 80 80 NRC USE ONLY 80 ss 0 Q 68 69 EsunEEEE;.
soURGE       ~LQ<<
sss/4 f4/NIR 5'5 9'0/METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32'~AQ31 COMPLETED TEST DATA REVIEW 45 46 LOCATION OF RELEASE Q NA 45}}
60          61
                                                        '           O     O>>
DOCKET NUMBER 6
68 Q>> EVENT 69                DATE             74 QB
                                                                                                                                          ~   75 0    1 REPbRT DATE 8    1 80 Qe EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO IN PREPARATION FOR START UP THE TESTING                                         OF'W-118-1             2       3     4 AS RE VIREO BY THE IS   I   PROGRAM WHILE                 IN   h10DE 3 WAS NOT DONE .                   (T. S . 4. 0. 5)       THE       (4 ) MAIN         FEEDWATER CHECK VALVES NOT BEING TESTED HAD NO EFFECT ON THE HEALTH AND SAFETY OF THE PUBLIC o   6           IN AS         MUCH AS THERE ARE MOTOR OPERATED AND                                   AIR     OPERATED VALVES UPSTREAM OF THESE
  ~o   6           VALVES THAT WOULD STOP REVERSE FLOW.
i
  ~O7
  ~OB 7       8 9                                                                                                                                                                           80 SYSTEM             CAUSE         CAUSE                                                         COMP.           VALVE CODE               CODE         SUBCODE                 COMPONENT CODE                     SUBCODE           SUBCODE
  ~o,e                               ~CN           Q11         0   Q12   ~Z     Q13       Z   Z     Z     Z     Z   Z Q4           ~ZQEE           ~Z     QER 7        8                        9           10         11             12   ,       13                               18           19               20 SEQUENTIAL                         OCCURRENCE             REPORT                         REVISION Q17 LE R)RO REPQRT ACTION FUTURE EVENT YEAR
                                      ~0 21        22 EFFECT
                                                            ~
23 SHUTDOWN 24 REPORT NO.
                                                                            ~7~ILJ         26
                                                                                                    ~~
27             28 ATTACHMENT.
CODE IILII~    29 NPRDR
                                                                                                                                            ~ ~
TYPE 30 PRIME COMP.
31 NO.
[gJ 32 COMPONENT TAKEN ACTION                   ON PLANT           METHOD                   HOURS O22         SUBMITTED         FORM SUB.           SUPPLIER             MANUFACTURER 2
                ~GQER ~ZQTE 33          34
                                                ~ZQ23 35 I
36 IQ       37 0
40    41 N Q23         ~NQ24 42
                                                                                                                                                      ~ZQEs 43              44 Z     9   9 9 47 QEs CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o         THE FACT THAT THESE VALVES WERE NOT TESTED WAS MASKED BY THE FACT THAT SIGN OFFS FOR OTHER MODE TESTS ALSO APPEARED ON THE SAME CHECKOFF SHEET.                                                                   A TEMPORARY CHANGE SHEET WAS WRITTEN TO SEPARATE THE TEST AS TO THEIR MODE RE UIREMENTS.                                                                         OTHER 3           PROCEDURES             ARE BEING REVIEWED FOR                     SIMILIAR PROBLEMS.
8   9                                                                                                                                                                       80 FACILITY                                                                       METHOD OF STATUS               % POWER                       OTHER STATUS               DISCOVERY                                DISCOVERY DESCRIPTION Q32
  ~ls             C   Q23     ~10             0   Qss       NA                               '~AQ31          COMPLETED TEST DATA REVIEW 7       8   9               10               12     13                             44     45          46                                                                        80 ACTIVITY       CONTENT Q                                                                                Q 7
6 8
              ~
RELEbSED OF RELEASE 9
Q33   ~~Q34 10 PERSONNEL EXPOSURES AMOUNT OF ACTIVITY 44            45 NA LOCATION OF RELEASE 80 7       8   9                 11       12         13                                                                                                                               80 PERSONNEL INJURIES NUMBER               DESCRIPTIONQ41
  ~TR 7      8
              ~00             0   Q43                                 NA 9                 11       12                                                                                                                                           80 LOSS OF OR DAMAGE TO FACILITY TYPE         DESCRIPTION 43 Z   Q42                                           NA 7       8   9           10                                                                                                                                                         80 PUBLICITY O
ISSUED
              ~NQ44 DESCRIPTION      Q                NA NRC USE ONLY 68   69                           80 B7.6609'6H'P                                                                                                                    EsunEEEE;.       sss/4 f4/NIR 5'       5 9'0/
ss 0
Q}}

Latest revision as of 14:38, 22 October 2019

LER 80-038/03L-0:on 801224,testing of Main Feedwater Check Valves Not Performed as Required Per Inservice Insp Program in Preparation for Startup.Caused by Misinterpreted Checkoff Sheet.Temporary Change Sheet Initiated
ML17331A743
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 01/23/1981
From: Stephens T
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17319A927 List:
References
LER-80-038-03L, LER-80-38-3L, NUDOCS 8106090488
Download: ML17331A743 (1)


Text

NRC Cv6RhT 366, U. S. NUCLEAR REGULATORY COMMISSION 0 73)

LICENSEE EVENT REPORT CONTROL BLOCK:

I 6 Q (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

~oi 7 8 9 M I D C LICENSEE CODE C 2 14 Q2 15 0 P LICENSE NUMBER 25 Q4 26 LICENSE TYPE 30 QE~ 57 CAT 58 Qs KK 7

CON'T 8

soURGE ~LQ<<

60 61

' O O>>

DOCKET NUMBER 6

68 Q>> EVENT 69 DATE 74 QB

~ 75 0 1 REPbRT DATE 8 1 80 Qe EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO IN PREPARATION FOR START UP THE TESTING OF'W-118-1 2 3 4 AS RE VIREO BY THE IS I PROGRAM WHILE IN h10DE 3 WAS NOT DONE . (T. S . 4. 0. 5) THE (4 ) MAIN FEEDWATER CHECK VALVES NOT BEING TESTED HAD NO EFFECT ON THE HEALTH AND SAFETY OF THE PUBLIC o 6 IN AS MUCH AS THERE ARE MOTOR OPERATED AND AIR OPERATED VALVES UPSTREAM OF THESE

~o 6 VALVES THAT WOULD STOP REVERSE FLOW.

i

~O7

~OB 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~o,e ~CN Q11 0 Q12 ~Z Q13 Z Z Z Z Z Z Q4 ~ZQEE ~Z QER 7 8 9 10 11 12 , 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION Q17 LE R)RO REPQRT ACTION FUTURE EVENT YEAR

~0 21 22 EFFECT

~

23 SHUTDOWN 24 REPORT NO.

~7~ILJ 26

~~

27 28 ATTACHMENT.

CODE IILII~ 29 NPRDR

~ ~

TYPE 30 PRIME COMP.

31 NO.

[gJ 32 COMPONENT TAKEN ACTION ON PLANT METHOD HOURS O22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER 2

~GQER ~ZQTE 33 34

~ZQ23 35 I

36 IQ 37 0

40 41 N Q23 ~NQ24 42

~ZQEs 43 44 Z 9 9 9 47 QEs CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o THE FACT THAT THESE VALVES WERE NOT TESTED WAS MASKED BY THE FACT THAT SIGN OFFS FOR OTHER MODE TESTS ALSO APPEARED ON THE SAME CHECKOFF SHEET. A TEMPORARY CHANGE SHEET WAS WRITTEN TO SEPARATE THE TEST AS TO THEIR MODE RE UIREMENTS. OTHER 3 PROCEDURES ARE BEING REVIEWED FOR SIMILIAR PROBLEMS.

8 9 80 FACILITY METHOD OF STATUS  % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION Q32

~ls C Q23 ~10 0 Qss NA '~AQ31 COMPLETED TEST DATA REVIEW 7 8 9 10 12 13 44 45 46 80 ACTIVITY CONTENT Q Q 7

6 8

~

RELEbSED OF RELEASE 9

Q33 ~~Q34 10 PERSONNEL EXPOSURES AMOUNT OF ACTIVITY 44 45 NA LOCATION OF RELEASE 80 7 8 9 11 12 13 80 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41

~TR 7 8

~00 0 Q43 NA 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION 43 Z Q42 NA 7 8 9 10 80 PUBLICITY O

ISSUED

~NQ44 DESCRIPTION Q NA NRC USE ONLY 68 69 80 B7.6609'6H'P EsunEEEE;. sss/4 f4/NIR 5' 5 9'0/

ss 0

Q