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=Text=
=Text=
{{#Wiki_filter:REGULATORY INFORMATION DISTRIBUTION SYSTEM<RIDS)DISTRIBUTION FOR INCOMING MATERIAL 50-220 REC'RIER B H NRC ORG: SCHNEIDER R R NIAGARA MOHAWK PWR DOCDATE: 02/24/78 DATE RCVD: 03/07/78 DOCTYPE: LETTER NOTARIZED:
{{#Wiki_filter:REGULATORY INFORMATION DISTRIBUTION SYSTEM <RIDS)
NO COPIES RECEIVED  
DISTRIBUTION FOR INCOMING MATERIAL                             50-220 REC'RIER     B H                     ORG: SCHNEIDER R R               DOCDATE: 02/24/78 NRC                                  NIAGARA MOHAWK PWR              DATE RCVD: 03/07/78 DOCTYPE: LETTER     NOTARIZED: NO                                       COPIES RECEIVED


==SUBJECT:==
==SUBJECT:==
LTR 0 ENCL 1 LICENSEE EVENT REPT<RO 50-220/78-06)
LTR 0   ENCL 1 LICENSEE EVENT REPT <RO 50-220/78-06) ON 01/27/78 CONCERNING PERFORMANCE OF SURVEILLANCE TEST IC-75 FOUND A TRIP SETPOINT OF
ON 01/27/78 CONCERNING PERFORMANCE OF SURVEILLANCE TEST IC-75 FOUND A TRIP SETPOINT OF 22.5 INCHES WATER ON ONE VACUUM SWITCH IN THE VACUUM RELIEF SYSTEM FROM THE PRESSURE SUPPRESSION CHAMBER TO THE RX BLDG (68-12B>.PLANT NAME: NINE MILE PT-UNIT 1 REVIEWER INITIAL: X JM DISTRIBUTOR.
: 22. 5 INCHES WATER ON ONE VACUUM SWITCH IN THE VACUUM RELIEF SYSTEM FROM THE PRESSURE   SUPPRESSION       CHAMBER TO THE RX BLDG (68-12B>.
INITIAL: gQ DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS INCIDENT REPORTS<DISTRIBUTION CODE A002)FOR ACTION: INTERNAL: EXTERNAL:/4 ENCL EG ILE~~~~W/ENCL I 8.E%~%SCHROEDER/I PPOL I T044 W/ENCL NOVAK/CHECK++W/ENCL KNI GHT++W/ENCL HANAUER+4W/ENCL E I SENHUT++W/ENCL SHAO++W/ENCL KREGER/J.COLLINS44W/ENCL K SEYFRIT/IE++W/ENCL LPDR'S OSWEGO'Y++W/ENCL TIC++W/ENCL NS I C+4 W/ENCL ACRS CAT B++W/16 ENCL NRC PDR44W/ENCL MIPC++W/3 ENCL HOUSTON4+W/ENCL GR IMES++W/ENCL BUTLER++W/ENCL TEDESCO++W/ENCL BAER44W/ENCL VOLLMER/BUNCH>~W/ENCL ROSA++W/ENCL DISTRIBUTION:
PLANT NAME: NINE MILE PT UNIT         1                       REVIEWER INITIAL: X JM DISTRIBUTOR. INITIAL:gQ DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS INCIDENT REPORTS
LTR 45 ENCL 45 SI ZE: iP+iP THE END CONTROL NB: 780680044
    <DISTRIBUTION CODE A002)
~4.I~Ihh Ih h J t'V;.>'1:,"',"t,', 4~*khh'I t',"V I I I I I kl hh Ik h~l'~I, k k~h,PV"k htt"I 4'h h h 4 4 ,'I~Vk I h,b I,K H((LQRE MMH teI'F(NMP-0124 NIAGARA MOHAWK POWER CORPORATION/300 ERIE BOULEVARD WEST, SYRACUSE, N.Y.13202/TELEPHONE (315)474-1511 Febeuucg 24, 1978 A..Bogce H.G/L4.et, Mn.ecto/I.
FOR ACTION:                             /4 ENCL INTERNAL:          EG     ILE~~~~W/ENCL              NRC PDR44W/ENCL I   8. E%~%                         MIPC++W/3 ENCL SCHROEDER/I PPOL I T044 W/ENCL        HOUSTON4+W/ENCL NOVAK/CHECK++W/ENCL                   GR IMES++W/ENCL KNIGHT++W/ENCL                        BUTLER++W/ENCL HANAUER+4W/ENCL                      TEDESCO++W/ENCL E I SENHUT++W/ENCL                    BAER44W/ENCL SHAO++W/ENCL                          VOLLMER/BUNCH>~W/ENCL KREGER/J. COLLINS44W/ENCL            ROSA++W/ENCL K   SEYFRIT/IE++W/ENCL EXTERNAL:        LPDR'S OSWEGO'Y++W/ENCL TIC++W/ENCL I
U~ed Staf:e5 NueLea/1.ReguZato/I.y Commission Region I 631 Pa/I.k Avenue King o(Pm56~, PA.19406 RE: Socket No.50-220 Pea/I.(k.G/Iie/I,: 9~f//pe'+~,t@ZAN c W/~Ay~~/In acco/u(ance uIith Nine NLe Point Nuct'.ea/I.
NS C+4 W/ENCL ACRS CAT B++W/16 ENCL DISTRIBUTION:     LTR 45         ENCL 45                       CONTROL NB  :  780680044 SI ZE: iP+ iP THE END
S~on Unit>1 Technicat'.
Speci.+cation/, me he/1eby sub~Licensee Event Repo/Lt LER 78-06, IvhichLe in v~o~n o(Section 3.3.6.F o)Ae Technicat'pecigcations.
Th&aepoM uIm completed in She JotuIat designated in NUREG-0161, dated JId'(g 1977.Ve/I.y~g go~, ORIGINAL SIGNEP BY R.R.SCHNEISER R.R.Schneide/I, Vice P/I.u&e<-ELecttu.c P/I,odu~on n4n Attachments (3)xc: Nrce&on.,'0(I(ice o(18E (30 copiu)Si/Iecto/L, 0(pce o(h(IPC (3 copim)78pggo NRC FORM 3GG (7 77)U.S.NUCLEAR REGULATORY COMMISSION
~o 7 8 CON'T~01 7 8 Qs.0 2 2 4 7 8 Qg soURGE MLQG 5 0 0 0 2 2 0 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 Durin stead state o eration erformance of surveillance test IC-75 LICENSEE EVENT REPOR~~~CONTROL BLOCK: QI (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
I 6 N Y N N P 1 QE 0 0-0 0 0 0 0-0 0 Q34 1 1 1 1 QE~QE LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58~03 found a tri set oint of 22.5 inches water on one vacuum swi tch in the~o 4 vacuum relief s stem from the ressure su ression chamber to the Rx~o 5 Buildin (68-12B).T.S.3.3.64F re uires a set oint less than or equal~o G to 0.5 si 13.85 inches water.This condition resulted in minimal~o 7 safet im lications.
A redundant switch was available to initiate~o s o eration of the vacuum relief valve.7 8 9 80~Os SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~SA Q>>E Q13~6Q13 I N S T R 0 04~SQPE~Z QPE 7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LEAPPAO EVENT YEAR REPORT NO.CODE TYPE NO.Q17 REPQRT~78~~00 6~~~03~L~0 21 22 23 24 26 27 28 29 30 31 32 ACTION 4 FUTURE EFFECT SHUTDOWN ATTACHh'IENT NPADP PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS 22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER gJQ~Q gJ gJQ o" Q33~Q34~QEE QEE 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o The cause of the failure was instrument drift in a mercoid model CP4122 vacuum switch.Trip setpoint was reset to 6.8 inches water.Current surveillance testing schedules are adequate to ensure early detection of future instrument drifts.7 8 9 FACILITY STATUS 66POWEA OTHER STATUS Q 1 5 E 2S 9 6 29 NA Q~0Q ACTIVITY CONTENT RELEASED OF AEI.EASE AMOUNT OF ACTIVITY Q Z Q33~ZQ34 nA 7 8 9 10 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39 7~00 0 Q37 Z Q33 NA 7 8 9 11 12 13 PEASONNEL IN3URIES METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q2~BQ31 Survei 1 1 ance Testing 45 46 LOCATION OF RELEASE Q 45 80 80 80 80 7 8 7 8 n ,7 NAMF-OF PREPARER Dennis MacVittie 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43 TYPE DESCRIPTION
~ZQ42 NA 9 10 PUBLICITY ISSUED DESCRIPTION l N IWnI NA 80 NRC USE ONLY I t i i 1J.L.LLL..Li I'7 J'''315-343-2110 ext.]558 0 , PHONE: a NRC FORh1'366 I7 77)U.b.NVCLFAR HEUULATOHY CL7<IIP Ilb>ICJEN I IPLEASE PRINT OR TYPE ALL REOUIREO INFORMATIONI 6 1 020 01 0 0 0 0 0 14 15 LICENSE NUAIBER 0 0 Q24 I I I I QE~QE 25 26 LICENSE TYPE'0 57 CAT 58 ICENSEE EVENT REPORT P (ONTROL BLOCK: I~or N I Y N.I'I P 7 8 9 I.ICENSEE CODE CON'T~or Eov'REE~LQE 0 5 0.0 0 2 2 QT.O8022 478 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74~75 REPORT DATE 80 EVEITIT DESCRIPTION ANO PROBABI.E CONSEQUENCES 10~oz Burin stead state o eration erformance of surveillance test IC-75~o 2 found a trip setpoint of 22.5 inches water on one vacuum switch in the~o R vacuum relief s stem from the ressure su ression chamber to the Rx~o s Buildin (68-128.T.S.3.3.6.F requires a setpoint less than or equ'al~o 8 to 0.5 si 13.85 inches ivater.This condition resulted in minimal~o T safet im Iications.
A redundant switch was available to initiate~o 8 o aration of the vacuum relief valve.7 8 9 80 7 8 SYSTES1 CAUSE CAUSE COMP.VALVE CODE CODE"SUBCODE COMPONFNT CODE SUBCOOE SUBCODE~SA Q~EQ~EQ I N S T R 0 Q~SQ~2cl 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LEREPRO EVENT YEAR REPORT NO.CODE>YPE NO.Qir REPQRT~78~~00 6~m~03~L~~0 21 22 23, 24 26 27 28 29 30 31 32 ACTION, FUTURE EFFECT SHUTDOWN ATTACHA1ENT NPROK PRIME COMP COMPONcNT TAKEN ACTION ON PLANT METHOD~OURS 22 SUBS11 TTED FORM SUB, SUPPLIER MANUFACTURER Q18 LIEO>>~2O20~2Q21 0 0 0~~NQ22~TOTE~NQzs N 2 3 5 Q28 33 34 35 36 37 40 41 42 43 44 47 CAUSF DESCRIPTION AND CORRECTIVE ACTIONS'27 o The cause of the failure was instrument drift in a mercoid model CP4122 vacuum switch.Trip setpoint was reset to 6.8 inches water.Current surveillance testing schedules are adequate to ensure early detection of future instrument drifts.4 7 8 9 FACILITY~STATUS<<8 POWER OTHER STATUS S E 28 0 9 6 29 NA 7 8 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43 TYPE DESCRIPTION 2 Q42 NA 9 10 PUBLICITY ISSUED~DESCRIPTION
~6)E~EE IEA Dennis t 1acVi tti e NAME OF PREPARER CO LJO~O ACTIVITY CONTENT REI.EASED OF RELEASE AMOUNT OF ACTIVITY Q 8~2 Qzz~2QEE NA 7 8 9 10 11 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION
~I7~00 0 QTT~L Q28 N A 7 8 9 11 12 13 PERSOiNiNEL INJURIES NUMBER O'ESCRIPTIONQ
~00 0 Qio NA I,IETHQD OF DISCOVERY~BQSI 45 46 NA DISCOVERY OESCRIPTIQi'4 Q3 Surveillance Testing LOCATION OF RELEASE QB 80 80 80 80 80 80 NRC IJSE ONLY I I I I I I.I.I..I.I I I"", 315-343-2110 ext.1558 PHONE:


To: PIB-39~)~)rooN.3fa-gQ 2 lg~or<TL/To r Y<i&#x17d;(lil~~.riG l'w:;b~:r', lel ephonc lou::il~ci TO: Director of Pco>>lat<<ry Operation OSl;lK l.-.:ir,n I 63l Pari: l:;en c l:in@nf Pros'ia, Ph.19406 Frooi: Hiirgara lTol:a';cl; Po.jcr Corporation bine hilt.Point, Duel cdr Station U>>lt fiT P 0.Bor.i<32 Lp'colllin9, hcl'I York 13093 SUPiilECT:
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OCD).J)El'CE DOC):l'.T l'0."0-220 LICLl!SE l!0.DPR-G3 ASSJ(islED LER HO.'8-09 CYGNET DATE: 78022E REPORT Df<TE: 78022I EVErlT DFSCRIPTTnrl:
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SEE ATTACHED.CO:(POlKliTS Il'OL"ED: TIP machine shear va'1ve squfb devices , CAUSE l(t!D RKr':ENf(L ACTIDIL circuit per GE revisi'on Institution of modiffcation in squib FE(CILITV STATUS=c)Routine Startop d)Routln~Sll:: dc"n e)stea<ry s:.iie opLl-~f)Load Cl'.-.age S;TllEt:Wnt.
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bi(1840 Slwit<foi~o refuel lng Other l(ot lippj'IcBI>IL IL i'riticn follow-up rcport will be sent v;itbin i<io v.'ccl:s.vr..roon ro 35 7 6.H:i ll.roo~rV: P.~~a" owL a 2.i llM H.
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ATTACHMENT TO LER 78-09 Event
H((LQRE MMH teI'F(
NMP-0124 NIAGARA MOHAWK POWER CORPORATION/300 ERIE BOULEVARD WEST, SYRACUSE, N.Y. 13202/TELEPHONE (315) 474-1511 Febeuucg  24, 1978 9
A.. Bogce    H. G/L4.et,              Commission Mn.ecto/I.                                                                                    ~f//pe U~ed Staf:e5 NueLea/1. ReguZato/I.y Region I                                                                                '+~,t    @ZAN c
631 Pa/I.k Avenue W/~Ay~~
King o( Pm56~, PA.          19406
                                                                                                          /
RE:    Socket No. 50-220 Pea/I. (k. G/Iie/I,:
In acco/u(ance uIith Nine NLe Point Nuct'.ea/I. S~on Unit >1 Technicat'. Speci.+cation/, me he/1eby sub~ Licensee Event Repo/Lt LER 78-06, IvhichLe in      v~o~n    o( Section 3.3.6.F o) Ae Technicat'pecigcations.
Th& aepoM uIm completed      in She    JotuIat designated      in NUREG-0161,    dated JId'(g 1977.
Ve/I.y ~g go~,
ORIGINAL SIGNEP BY R.R. SCHNEISER R.R. Schneide/I, Vice  P/I.u&e<-
ELecttu.c P/I,odu~on n4n Attachments      (3) xc:    Nrce&on., '0(I(ice o( 18E (30 copiu)
Si/Iecto/L, 0(pce o( h(IPC (3 copim) 78pggo
 
NRC FORM 3GG                                                                                                                              U. S. NUCLEAR REGULATORY COMMISSION (7 77)
LICENSEE EVENT REPOR
                                      ~
                                                                                                                                                                                            ~ ~
CONTROL BLOCK:                                                      QI                  (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
I                                    6
  ~o              N    Y    N      N      P      1      QE    0    0    -    0      0    0      0    0    -    0    0    Q34            1    1    1    1    QE~QE 7        8            LICENSEE CODE                14      15                      LICENSE NUMBER                        25        26        LICENSE TYPE      30      57 CAT 58 CON'T
  ~01                  soURGE      MLQG                    5    0    0    0    2      2    0                                              Qs. 0    2    2      4    7      8    Qg 7        8                      60            61                DOCKET NUMBER                  68    69        EVENT DATE                74      75      REPORT DATE              80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                                    Q10 Durin          stead            state        o  eration              erformance of surveillance                            test IC-75
  ~03                found        a    tri      set oint of 22. 5 inches water                                on one vacuum swi tch                      in the
  ~o    4          vacuum        relief          s stem          from the            ressure su            ression chamber to the                          Rx
  ~o    5          Buildin (68-12B). T.S. 3.3.64F re uires                                                a  set oint less than or equal
  ~o    G          to 0.5            si        13.85 inches water                      . This condition resulted in minimal
  ~o    7          safet          im      lications.              A  redundant switch was available to                                  initiate
  ~o    s          o  eration of the                      vacuum        relief      valve.
7        8 9                                                                                                                                                                                    80 SYSTEM                CAUSE          CAUSE                                                            COMP.            VALVE CODE                CODE        SUBCODE                    COMPONENT CODE                      SUBCODE          SUBCODE
  ~Os                                ~SA              Q>>          E    Q13    ~6Q13                I    N    S    T    R      0 04            ~SQPE            ~Z      QPE 7        8                        9            10            11              12              13                              18            19              20 SEQUENTIAL                            OCCURRENCE                REPORT                        REVISION Q17 LEAPPAO REPQRT ACTION FUTURE 4
EVENT YEAR
                                        ~78 21        22 EFFECT
                                                                ~
23 SHUTDOWN
                                                                                ~00 24 REPORT NO.
6 26
                                                                                                            ~~
27
                                                                                                                          ~03 28 CODE ATTACHh'IENT 29 NPADP TYPE
                                                                                                                                                    ~L 30 PRIME COMP.
31 NO.
                                                                                                                                                                                    ~0 32 COMPONENT TAKEN ACTION                    ON PLANT            METHOD                    HOURS      22      SUBMITTED        FORM SUB.            SUPPLIER              MANUFACTURER gJQ~Q gJ 33          34                  35 gJQ 36              37 o
40
                                                                                                                        "
41 Q33          ~Q34 42
                                                                                                                                                              ~QEE 43                44              47 QEE CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o          The cause              of the failure                  was    instrument            drift in        a    mercoid model CP4122 vacuum        switch. Trip setpoint                          was      reset to 6.8 inches water. Current surveillance testing schedules are adequate to ensure early detection of future instrument drifts.
7        8    9                                                                                                                                                                              80 Q
                                ~0Q FACILITY                                                                              METHOD OF STATUS              66POWEA                          OTHER STATUS                  DISCOVERY                                DISCOVERY DESCRIPTION            Q2 1  5        E    Q2S                  9 6        29                  NA                          ~BQ31 45        46 Survei        1 1 ance Testing 80 ACTIVITY        CONTENT RELEASED OF AEI.EASE Z
AMOUNT OF ACTIVITY nA Q                                                    LOCATION OF RELEASE          Q Q33    ~ZQ34 7        8    9              10                                                            44            45                                                                                80 PERSONNEL EXPOSURES NUMBER                TYPE          DESCRIPTION Q39 7
8
                ~00            0    Q37      Z  Q33            NA 7            9                11        12            13                                                                                                                                    80 PEASONNEL IN3URIES 7        8    9                11        12 LOSS OF OR DAMAGE TO FACILITY TYPE        DESCRIPTION                      Q43
                ~ZQ42                  NA 7        8    9            10                                                                                                                                                                80 PUBLICITY                                                                                                                                          NRC USE ONLY ISSUED        DESCRIPTION n      l N IWnI            NA                                                                                                                          I t    i i  1J.L.LLL..Li      I'7
,7                                                                                                                                                          J NAMF- OF PREPARER Dennis MacVittie                                                              '''315-343-2110 ext. ]558                            0 a
                                                                                                                                        ,
PHONE:
 
NRC FORh1'366                                                                                                                                  U. b. NVCLFAR HEUULATOHY CL7<IIP Ilb>ICJEN I7 77)
ICENSEE EVENT REPORT P
( ONTROL BLOCK:                                                          I                    IPLEASE PRINT OR TYPE ALL REOUIREO INFORMATIONI I                                    6
~or              N    I  Y      N.        I'I    P      1    020          01        0      0    0      0      0        0    0    Q24            I    I    I I        QE~QE 7        8    9          I.ICENSEE CODE                  14      15                      LICENSE NUAIBER                        25      26        LICENSE    TYPE'0        57 CAT 58 CON'T
~or 7        8 Eov'REE      ~LQE 60 0      5      0  .0    0    2      2 68 QT.
69      EVENT DATE              74 O8022 478 75      REPORT DATE            80 61              DOCKET NUMBER                                                                  ~
EVEITIT DESCRIPTION ANO PROBABI.E CONSEQUENCES                                      10
~oz                Burin stead                          state        o  eration            erformance of surveillance                              test      IC-75
~o    2              found        a        trip setpoint of 22.5                        inches water on one vacuum switch in the
~o    R            vacuum          relief s stem from the                                ressure          su    ression chamber to the                        Rx
~o    s            Buildin (68-128                          . T.S. 3.3.6.F requires                        a  setpoint less than or                        equ'al
~o  8              to 0.5              si          13.85 inches ivater                    . This condition resulted in minimal
~o    T            safet          im        Iications.              A  redundant switch was available to                                    initiate
~o 8              o    aration of the                        vacuum        relief valve.
7      8    9                                                                                                                                                                                      80 SYSTES1              CAUSE          CAUSE                                                              COMP.          VALVE CODE                CODE        "SUBCODE                      COMPONFNT CODE                      SUBCOOE          SUBCODE 7        8
                                      ~SA Q ~EQ ~EQ 9              10          11            12                13 I      N    S    T    R    0 18 Q ~SQ ~2cl 19              20 SEQUENTIAL                              OCCURRENCE              REPORT                      REVISION Qir LEREPRO REPQRT ACTION, FUTURE EVENT YEAR
                                          ~78 21          22 EFFECT
                                                                  ~
23, SHUTDOWN
                                                                                  ~00 24 REPORT NO.
6 26
                                                                                                                ~m 27
                                                                                                                              ~03 28 ATTACHA1ENT CODE 29 NPROK
                                                                                                                                                        >YPE
                                                                                                                                                        ~L 30 PRIME COMP
                                                                                                                                                                      ~
31 NO.
                                                                                                                                                                                    ~0 32 COMPONcNT TAKEN 33 Q18 ACTION LIEO>>
34 ON PLANT
                                                      ~2O20 35 METHOD
                                                                          ~2Q21 36              37 0
                                                                                                  ~OURS 0      0  ~
22 40 SUBS11 TTED
                                                                                                                          ~NQ22 41 FORM SUB,
                                                                                                                                            ~TOTE SUPPLIER
                                                                                                                                                                ~NQzs MANUFACTURER N    2      3    5  Q28 42                  43              44                    47 CAUSF DESCRIPTION AND CORRECTIVE ACTIONS '27 o            The cause                  of the failure                was    instrument              drift in        a  mercoid model CP4122 vacuum          switch. Trip setpoint                            was      reset to 6.8 inches water. Current surveillance testing schedules are adequate to ensure early detection of future instrument drifts.
4
                                ~O 7      8    9                                                                                                                                                                                      80 FACILITY              ~                                                                  I,IETHQD OF STATUS                <<8  POWER                          OTHER STATUS                  DISCOVERY                                DISCOVERY OESCRIPTIQi'4        Q3 CO LJOS          E    28          0        9 6        29                NA                            ~BQSI 45        46 Surveillance Testing 80 ACTIVITY          CONTENT REI.EASED OF RELEASE                                AMOUNT OF ACTIVITY        Q                                                    LOCATION OF RELEASE QB 8        ~2        Qzz    ~2QEE                          NA                                                      NA 7      8    9                10              11                                              44                                                                                                  80 PERSONNEL EXPOSURES NUMBER                    TYPE          DESCRIPTION
~I7 ~00                        0    QTT      ~L      Q28            NA 7        8    9                  11          12            13                                                                                                                                      80 PERSOiNiNEL INJURIES NUMBER                    O'ESCRIPTIONQ 8
              ~00 9
0 Qio 12 NA 7                                11                                                                                                                                                                  80 LOSS OF OR DAMAGE TO FACILITY TYPE          DESCRIPTION                        Q43 2    Q42                NA 7      8    9            10                                                                                                                                                                      80 ISSUED~
PUBLICITY
: 6) E~EE DESCRIPTION IEA
                                                  ~                                                                                                                  I  I NRC IJSE ONLY I I  I  I .I .I..I. I I  I "",
NAME OF PREPARER Dennis      t 1acVi    ttie                                          PHONE:
315-343-2110 ext. 1558
 
To:  PIB      -39~)~) ',
Y<i'(lil~~.riG l'w:;b~:r rooN  .3fa -gQ 2 lg~
lel ephonc  lou::il~ci or<TL/To  r TO:                                                      Frooi:      Hiirgara lTol:a';cl; Po.jcr Corporation Director of Pco>>lat<<ry Operation                              bine hilt. Point, Duel cdr Station OSl;lK l. -.:ir,n I                                          U>>lt  fiT 63l Pari: l:;en c                                            P  0. Bor. i<32 l:in@ nf Pros'ia, Ph.            19406                      Lp'colllin9, hcl'I York    13093 SUPiilECT:            PP.Ol',1'T Rl.PO.,TN)].!! OCD).J)El'CE DOC):l'.T ASSJ(islED LER HO.      '8-09 l'0. "0-220 LICLl!SE l!0.          DPR-G3 CYGNET  DATE:                78022E                    REPORT Df<TE:              78022I EVErlT DFSCRIPTTnrl:
SEE ATTACHED.
CO:(POlKliTS    Il 'OL"ED:              TIP machine shear va'1ve squfb devices
, CAUSE    l(t!D RKr':ENf(L ACTIDIL              Institution of modiffcation in squib circuit per      GE  revisi'on
                                    ~
FE(CILITV STATUS=                                                S;  TllEt:Wnt. bi( 1840 c) Routine Startop                                            Slwit<foi~o d) Routln~ Sll:: dc"n                                        refuel lng e) stea<ry s:.iie opLl-                                      Other f)  Load Cl'.-.age                                            l(ot lippj'IcBI>IL IL i'riticn follow-up rcport will be              sent v;itbin i<io v.'ccl:s.
vr..roon ro 35          7 H:i ll.
: 6.                  roo~    rV: P.~~a" llMH.
owL a 2.i
 
ATTACHMENT TO LER   78-09 Event


== Description:==
== Description:==


During routine station operation with the TIP detectors.
During routine station operation with the TIP detectors. withdrawn, repTacement explosive charges in the TIP system shear valves were replcaed with new charges. Following replacement,             it was found that the ohmneter contlnuity test for acceptable eTectric           contact   was unsatisfactory.
withdrawn, repTacement explosive charges in the TIP system shear valves were replcaed with new charges.Following replacement, it was found that the ohmneter contlnuity test for acceptable eTectric contact was unsatisfactory.
The normal TIP tube tsoTaticm system       was. operabTe   at   this time.
The normal TIP tube tsoTaticm system was.operabTe at this time.I It was found thart the.actual etectricaV connections to the.explosive charges were net as-described
I It was found thart the. actual etectricaV connections to the. explosive The shear charges were net as-described -4n the maStenance-procedure.             -             .
-4n the maStenance-procedure.
valves would not have operated to       5solate   the   TIP guide. tuba   witlr the TIp inserted     Dectrical   connections   vill   be checked described in the and tested   to assure.
-The shear.valves would not have operated to 5solate the TIP guide.tuba witlr the TIp inserted Dectrical connections vill be checked and tested to assure.that the explosive.va7.ves wAl operate as described in the operatic procedures."..Station records;including.
that the explosive.va7.ves wAl operate as                               operatic procedures."..Station records; including. the au6ntenance.-.procedures,-wfTT             =
the au6ntenance.-.procedures,-wfTT
be corrected to reflect the correct. wiriny connections               An end-ta-end demonstration-at'he. explosive     shear   va7ves=will   be performed'ith       the explosive charge   removed. from..the, system..   'orrective     action   wfll be compTeted before the TIP system is again used r
=be corrected to reflect the correct.wiriny connections An end-ta-end demonstration-at'he.
The explosive operated TIP shear tsolation valves are a back-up system to be used for isa'Eatioe of the TIP tubes in the event detectnr      the it is i.soTation not possible. te wfthdrwr   the.           se       normaT automat%a.
explosive shear va7ves=will be performed'ith the explosive charge removed.from..the, system..'orrective action wfll be compTeted before the TIP system is again used r The explosive operated TIP shear tsolation valves are a back-up system to be used for isa'Eatioe of the TIP tubes in the event it is not possible.te wfthdrwr the.detectnr se the normaT automat%a.
system may function}}
i.soTation system may function}}

Revision as of 04:30, 22 October 2019

LER 78-006-00 for Nine Mile Point, Unit 1 Re During Steady State Operation, Performance of Surveillance Test IC-75 Found a Trip Setpoint of 22.5 Inches Water on One Vacuum Switch in the Vacuum Relief System from the Pressure Suppression Cha
ML18018B265
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 02/24/1978
From: Schneider R
Niagara Mohawk Power Corp
To: Grier B
Office of Nuclear Reactor Regulation, NRC Region 1
References
NMP-0124 LER 78-006-00
Download: ML18018B265 (10)


Text

REGULATORY INFORMATION DISTRIBUTION SYSTEM <RIDS)

DISTRIBUTION FOR INCOMING MATERIAL 50-220 REC'RIER B H ORG: SCHNEIDER R R DOCDATE: 02/24/78 NRC NIAGARA MOHAWK PWR DATE RCVD: 03/07/78 DOCTYPE: LETTER NOTARIZED: NO COPIES RECEIVED

SUBJECT:

LTR 0 ENCL 1 LICENSEE EVENT REPT <RO 50-220/78-06) ON 01/27/78 CONCERNING PERFORMANCE OF SURVEILLANCE TEST IC-75 FOUND A TRIP SETPOINT OF

22. 5 INCHES WATER ON ONE VACUUM SWITCH IN THE VACUUM RELIEF SYSTEM FROM THE PRESSURE SUPPRESSION CHAMBER TO THE RX BLDG (68-12B>.

PLANT NAME: NINE MILE PT UNIT 1 REVIEWER INITIAL: X JM DISTRIBUTOR. INITIAL:gQ DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS INCIDENT REPORTS

<DISTRIBUTION CODE A002)

FOR ACTION: /4 ENCL INTERNAL: EG ILE~~~~W/ENCL NRC PDR44W/ENCL I 8. E%~% MIPC++W/3 ENCL SCHROEDER/I PPOL I T044 W/ENCL HOUSTON4+W/ENCL NOVAK/CHECK++W/ENCL GR IMES++W/ENCL KNIGHT++W/ENCL BUTLER++W/ENCL HANAUER+4W/ENCL TEDESCO++W/ENCL E I SENHUT++W/ENCL BAER44W/ENCL SHAO++W/ENCL VOLLMER/BUNCH>~W/ENCL KREGER/J. COLLINS44W/ENCL ROSA++W/ENCL K SEYFRIT/IE++W/ENCL EXTERNAL: LPDR'S OSWEGO'Y++W/ENCL TIC++W/ENCL I

NS C+4 W/ENCL ACRS CAT B++W/16 ENCL DISTRIBUTION: LTR 45 ENCL 45 CONTROL NB  : 780680044 SI ZE: iP+ iP THE END

~ 4 .I Ihh

~

Ih h

J t'V;.>'1:," ',"t,', 4 ~

  • khh' I t', "V I I I I kl I

hh Ik

~ l' 4' I,

h

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H((LQRE MMH teI'F(

NMP-0124 NIAGARA MOHAWK POWER CORPORATION/300 ERIE BOULEVARD WEST, SYRACUSE, N.Y. 13202/TELEPHONE (315) 474-1511 Febeuucg 24, 1978 9

A.. Bogce H. G/L4.et, Commission Mn.ecto/I. ~f//pe U~ed Staf:e5 NueLea/1. ReguZato/I.y Region I '+~,t @ZAN c

631 Pa/I.k Avenue W/~Ay~~

King o( Pm56~, PA. 19406

/

RE: Socket No. 50-220 Pea/I. (k. G/Iie/I,:

In acco/u(ance uIith Nine NLe Point Nuct'.ea/I. S~on Unit >1 Technicat'. Speci.+cation/, me he/1eby sub~ Licensee Event Repo/Lt LER 78-06, IvhichLe in v~o~n o( Section 3.3.6.F o) Ae Technicat'pecigcations.

Th& aepoM uIm completed in She JotuIat designated in NUREG-0161, dated JId'(g 1977.

Ve/I.y ~g go~,

ORIGINAL SIGNEP BY R.R. SCHNEISER R.R. Schneide/I, Vice P/I.u&e<-

ELecttu.c P/I,odu~on n4n Attachments (3) xc: Nrce&on., '0(I(ice o( 18E (30 copiu)

Si/Iecto/L, 0(pce o( h(IPC (3 copim) 78pggo

NRC FORM 3GG U. S. NUCLEAR REGULATORY COMMISSION (7 77)

LICENSEE EVENT REPOR

~

~ ~

CONTROL BLOCK: QI (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6

~o N Y N N P 1 QE 0 0 - 0 0 0 0 0 - 0 0 Q34 1 1 1 1 QE~QE 7 8 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T

~01 soURGE MLQG 5 0 0 0 2 2 0 Qs. 0 2 2 4 7 8 Qg 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 Durin stead state o eration erformance of surveillance test IC-75

~03 found a tri set oint of 22. 5 inches water on one vacuum swi tch in the

~o 4 vacuum relief s stem from the ressure su ression chamber to the Rx

~o 5 Buildin (68-12B). T.S. 3.3.64F re uires a set oint less than or equal

~o G to 0.5 si 13.85 inches water . This condition resulted in minimal

~o 7 safet im lications. A redundant switch was available to initiate

~o s o eration of the vacuum relief valve.

7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~Os ~SA Q>> E Q13 ~6Q13 I N S T R 0 04 ~SQPE ~Z QPE 7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION Q17 LEAPPAO REPQRT ACTION FUTURE 4

EVENT YEAR

~78 21 22 EFFECT

~

23 SHUTDOWN

~00 24 REPORT NO.

6 26

~~

27

~03 28 CODE ATTACHh'IENT 29 NPADP TYPE

~L 30 PRIME COMP.

31 NO.

~0 32 COMPONENT TAKEN ACTION ON PLANT METHOD HOURS 22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER gJQ~Q gJ 33 34 35 gJQ 36 37 o

40

"

41 Q33 ~Q34 42

~QEE 43 44 47 QEE CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o The cause of the failure was instrument drift in a mercoid model CP4122 vacuum switch. Trip setpoint was reset to 6.8 inches water. Current surveillance testing schedules are adequate to ensure early detection of future instrument drifts.

7 8 9 80 Q

~0Q FACILITY METHOD OF STATUS 66POWEA OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION Q2 1 5 E Q2S 9 6 29 NA ~BQ31 45 46 Survei 1 1 ance Testing 80 ACTIVITY CONTENT RELEASED OF AEI.EASE Z

AMOUNT OF ACTIVITY nA Q LOCATION OF RELEASE Q Q33 ~ZQ34 7 8 9 10 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39 7

8

~00 0 Q37 Z Q33 NA 7 9 11 12 13 80 PEASONNEL IN3URIES 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Q43

~ZQ42 NA 7 8 9 10 80 PUBLICITY NRC USE ONLY ISSUED DESCRIPTION n l N IWnI NA I t i i 1J.L.LLL..Li I'7

,7 J NAMF- OF PREPARER Dennis MacVittie 315-343-2110 ext. ]558 0 a

,

PHONE:

NRC FORh1'366 U. b. NVCLFAR HEUULATOHY CL7<IIP Ilb>ICJEN I7 77)

ICENSEE EVENT REPORT P

( ONTROL BLOCK: I IPLEASE PRINT OR TYPE ALL REOUIREO INFORMATIONI I 6

~or N I Y N. I'I P 1 020 01 0 0 0 0 0 0 0 Q24 I I I I QE~QE 7 8 9 I.ICENSEE CODE 14 15 LICENSE NUAIBER 25 26 LICENSE TYPE'0 57 CAT 58 CON'T

~or 7 8 Eov'REE ~LQE 60 0 5 0 .0 0 2 2 68 QT.

69 EVENT DATE 74 O8022 478 75 REPORT DATE 80 61 DOCKET NUMBER ~

EVEITIT DESCRIPTION ANO PROBABI.E CONSEQUENCES 10

~oz Burin stead state o eration erformance of surveillance test IC-75

~o 2 found a trip setpoint of 22.5 inches water on one vacuum switch in the

~o R vacuum relief s stem from the ressure su ression chamber to the Rx

~o s Buildin (68-128 . T.S. 3.3.6.F requires a setpoint less than or equ'al

~o 8 to 0.5 si 13.85 inches ivater . This condition resulted in minimal

~o T safet im Iications. A redundant switch was available to initiate

~o 8 o aration of the vacuum relief valve.

7 8 9 80 SYSTES1 CAUSE CAUSE COMP. VALVE CODE CODE "SUBCODE COMPONFNT CODE SUBCOOE SUBCODE 7 8

~SA Q ~EQ ~EQ 9 10 11 12 13 I N S T R 0 18 Q ~SQ ~2cl 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION Qir LEREPRO REPQRT ACTION, FUTURE EVENT YEAR

~78 21 22 EFFECT

~

23, SHUTDOWN

~00 24 REPORT NO.

6 26

~m 27

~03 28 ATTACHA1ENT CODE 29 NPROK

>YPE

~L 30 PRIME COMP

~

31 NO.

~0 32 COMPONcNT TAKEN 33 Q18 ACTION LIEO>>

34 ON PLANT

~2O20 35 METHOD

~2Q21 36 37 0

~OURS 0 0 ~

22 40 SUBS11 TTED

~NQ22 41 FORM SUB,

~TOTE SUPPLIER

~NQzs MANUFACTURER N 2 3 5 Q28 42 43 44 47 CAUSF DESCRIPTION AND CORRECTIVE ACTIONS '27 o The cause of the failure was instrument drift in a mercoid model CP4122 vacuum switch. Trip setpoint was reset to 6.8 inches water. Current surveillance testing schedules are adequate to ensure early detection of future instrument drifts.

4

~O 7 8 9 80 FACILITY ~ I,IETHQD OF STATUS <<8 POWER OTHER STATUS DISCOVERY DISCOVERY OESCRIPTIQi'4 Q3 CO LJOS E 28 0 9 6 29 NA ~BQSI 45 46 Surveillance Testing 80 ACTIVITY CONTENT REI.EASED OF RELEASE AMOUNT OF ACTIVITY Q LOCATION OF RELEASE QB 8 ~2 Qzz ~2QEE NA NA 7 8 9 10 11 44 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION

~I7 ~00 0 QTT ~L Q28 NA 7 8 9 11 12 13 80 PERSOiNiNEL INJURIES NUMBER O'ESCRIPTIONQ 8

~00 9

0 Qio 12 NA 7 11 80 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Q43 2 Q42 NA 7 8 9 10 80 ISSUED~

PUBLICITY

6) E~EE DESCRIPTION IEA

~ I I NRC IJSE ONLY I I I I .I .I..I. I I I "",

NAME OF PREPARER Dennis t 1acVi ttie PHONE:

315-343-2110 ext. 1558

To: PIB -39~)~) ',

Y<i'(lil~~.riG l'w:;b~:r rooN .3fa -gQ 2 lg~

lel ephonc lou::il~ci or<TL/To r TO: Frooi: Hiirgara lTol:a';cl; Po.jcr Corporation Director of Pco>>lat<<ry Operation bine hilt. Point, Duel cdr Station OSl;lK l. -.:ir,n I U>>lt fiT 63l Pari: l:;en c P 0. Bor. i<32 l:in@ nf Pros'ia, Ph. 19406 Lp'colllin9, hcl'I York 13093 SUPiilECT: PP.Ol',1'T Rl.PO.,TN)].!! OCD).J)El'CE DOC):l'.T ASSJ(islED LER HO. '8-09 l'0. "0-220 LICLl!SE l!0. DPR-G3 CYGNET DATE: 78022E REPORT Df<TE: 78022I EVErlT DFSCRIPTTnrl:

SEE ATTACHED.

CO:(POlKliTS Il 'OL"ED: TIP machine shear va'1ve squfb devices

, CAUSE l(t!D RKr':ENf(L ACTIDIL Institution of modiffcation in squib circuit per GE revisi'on

~

FE(CILITV STATUS= S; TllEt:Wnt. bi( 1840 c) Routine Startop Slwit<foi~o d) Routln~ Sll:: dc"n refuel lng e) stea<ry s:.iie opLl- Other f) Load Cl'.-.age l(ot lippj'IcBI>IL IL i'riticn follow-up rcport will be sent v;itbin i<io v.'ccl:s.

vr..roon ro 35 7 H:i ll.

6. roo~ rV: P.~~a" llMH.

owL a 2.i

ATTACHMENT TO LER 78-09 Event

Description:

During routine station operation with the TIP detectors. withdrawn, repTacement explosive charges in the TIP system shear valves were replcaed with new charges. Following replacement, it was found that the ohmneter contlnuity test for acceptable eTectric contact was unsatisfactory.

The normal TIP tube tsoTaticm system was. operabTe at this time.

I It was found thart the. actual etectricaV connections to the. explosive The shear charges were net as-described -4n the maStenance-procedure. - .

valves would not have operated to 5solate the TIP guide. tuba witlr the TIp inserted Dectrical connections vill be checked described in the and tested to assure.

that the explosive.va7.ves wAl operate as operatic procedures."..Station records; including. the au6ntenance.-.procedures,-wfTT =

be corrected to reflect the correct. wiriny connections An end-ta-end demonstration-at'he. explosive shear va7ves=will be performed'ith the explosive charge removed. from..the, system.. 'orrective action wfll be compTeted before the TIP system is again used r

The explosive operated TIP shear tsolation valves are a back-up system to be used for isa'Eatioe of the TIP tubes in the event detectnr the it is i.soTation not possible. te wfthdrwr the. se normaT automat%a.

system may function