And LER 78-015-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump in 102 D/G Would Not Fill the Day Tank and Discovery That 12 Control Room Air Treatment Fan Would Not Run| ML18018B262 |
| Person / Time |
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| Site: |
Nine Mile Point  |
|---|
| Issue date: |
03/28/1978 |
|---|
| From: |
Schneider R Niagara Mohawk Power Corp |
|---|
| To: |
Grier B NRC Region 1 |
|---|
| References |
|---|
| LER 78-014-00, LER 78-015-00 |
| Download: ML18018B262 (8) |
|
LER-1978-015, And LER 78-015-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump in 102 D/G Would Not Fill the Day Tank and Discovery That 12 Control Room Air Treatment Fan Would Not Run |
| Event date: |
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| Report date: |
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| 2201978015R00 - NRC Website |
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text
.r REGULATORY DISTRIBUTION FOR REC:
GRIER B
H NRC INFORMATION DISTRIBUTION SYSTEM
< RIDS)
INCOMING MATERIAL 50-220 tl ORG:
SCHNEIDER R
R DOCDATE: 03f28/78 NIAGARA MOHAWK PWR DATE RCVD: 04/03/78 DOCTYPE:
LETTER NOTARIZED:
NO, COPIES RECEIVED
SUBJECT:
LTR 1
ENCL 1
LICENSEE EVENT REPT (RO 50-220f78-14)
ON 03/07/78 CONCERNING PEFORMANCE OF SURVEILLANCE TEST Ni-ST-I"l4 FOUND THAT THE FUEL 'TRANSFER PUMP ON 102 D/G WOULD NOT FILL THE DAY TANK>
DUE TO FOOT VALVE UNSEATED DURING ATTEMPT TO SAMPLE FUEL OIL... W/ATT LER 78-14 PLANT NAl"IE:NINE I'fILE PT UNIT 1
REVIEWER INlTIAL:
XJM DISTRIBUTOR INITIAL:
~~W/4 ENCL DISTRIBUTlON OF THIS MATERIAL IS AS FOLLOWS INCIDENT REPORTS (DISTRIBUTION CODE A002)
FOR ACTION:
BR INTERNAL:
REG FILE~~W/EN SCHROEDER/I PPOL ITO+4 WfENCL NOVAK/CHECK~+W/ENCL KNIGHTS 4 W/ENCL HANAUER44W/ENCL EISENHUT44 W/ENCL SHAO>+W/ENCL KREGER/J.
COLLINS+4 W/ENCL K SEYFRIT/IE++W/ENCL NRC PDR+~W/ENCL MIPC++W/3 ENCL HOUSTON44W/ENCL GR IMES~+W/ENCL BUTLER~~W/ENCL TEDESCO++W/ENCL BAER++W/ENCL VOLLMER/BUNCH+4W/ENCL ROSA+4 WfENCL EXTERNAL:
LPDR S OSWEGO'Y++W/ENCL TIC++W/ENCL NSIC4~+W/ENCL ACRS CAT B+~W/16 ENCL COPIES ilOT SUB".lITTED PER REGULATORY GUIDE 10.1 DISTRIBUTION:
LTR 45 ENCL 45 SIZE:
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Nh(P-0140 NIAGARAMOHAWKPOWER CORPORATION/300 ERIE BOULEVARDWEST, SYRACUSE. N.Y. 13202/TELEPHONE (315) 474-1511 h4,.
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%Recto/L Un&ted S~e5 Nuclea/L Regulators'omInQ amn Region I 631 Pa/I.k Avenue King og PuL5am, PA.
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LER 78-14, I0fuch m wI. violation of Section 3.6.3, and LER 78-15, I0Mch m ~n volation o( Se~n 3.4.5, olI We Tech'.cd Speci; g,~nb, Thee rcepo~
I0e/Ie complied in She (o/UIIat de5~gnated in NUREG-0161, dated July 1977.
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~os N4 found that the fuel transfer PumP on 102 0/G would not fill the day tank.
In accordance with T.S. 4.6.3e operability of D/G 103 was demon-strated.
This condition resulted in minimal safety implications.
The LICENSEE EVENT REPORT CONTROL BLOCK:
QI (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION)
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LICENSEE CODE 14 IS LICENSE NUMBER CON'T
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0 Qz 0
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8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74
'76 REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10
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Durin stead state o aration erformanc f
QB
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redundant D/G was operational and both 115 KV external lines were
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available.
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SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCOOE COMPONENTCODE SUBCODE SUBCODE
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10 11 12 13 18 19 20 SEOUENTIAL OCCURRENCE REPORT LER/AO EVENT YEAR REPORT NO.
CODE TYPE Q'z
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~L 2'I 22 23 24 26 27 28 29 30 31 ACTION. FUTURE EFFECT SHUTOOtVN ATTACHMENT NPRD'4 PRIME CONIP, TAKEN ACTION ON PLANT METHOD HOURS Q22 SU811ITTED FORM SUB.
SUPPLIER
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LJOz'JO CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 The fuel transfer pump lost its prime when the A.Y. IICDonald foot valve 80 REVISION NO.
0 32 COMPONENT hIANUFACTURER (zo
,'7 44 assembly was mistakenly unseated during an attempt to sample the fuel oil. The foot valve was removed, inspected, and replaced.
Transfer pump functioned properly.
Sampling procedure is being revised to more readily identify the proper sample point.
9 11 12 LOSS OF OA OAhIACE TO FACILITYQ43 TYPE
DESCRIPTION
2 Q42 NA 9
10 PUBLICITY ISSUED DESCRIPTION LP9 NA ~
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8 7
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D.K; I/IacVittie NAME OF PREPARER 7
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FACILITY STATUS SG PO1VER OTHER STATUS Q
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10 12 13 44 ACTIVITY CONTENT AELEASEO OF RELEASE AhiOUNT OF ACTIVITYQB
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10 11 44 PERSONNEL EXPOSURES NUMBER TYPE OESCAIPTION
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11 12 13 PERSONNEL INJURIES
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NA METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32
~AQ3I Operational Event 45 46 LOCATIONOF RELEASE Q36 5
NA NRC USE ONLY 315-343-2110 x 1558 PHONE:
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LICENSEE CODE 14 15 LICENSE NULIBEB 25 2G LICENSE TYPE Jo 57 CAT 58 CON'T IZKI soo<<RRR~LQRO 5
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60 Gi DOCKET NUMBER 68 G9 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABI.E CONSEQUENCES QIO
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Durin stead state o eration erf rm Hg found that 812 Control Room Air Treatment Fan would not run.
The
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redundant fan was shown to be operable.
This condition resulted in
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minimal safety implications.
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8 SYSTEM CAUSE'AUSE COMP.
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10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIBO EVENTYEAR REPORT NO.
CODE TYPE NO.
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SUPPLIER MANUFACTURER
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0 Qs 33 34 35 3G 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS o
A G.E. Hotor, Hodel 5K145AL226A, shorted when a conduit box screw came loos'e and wedged into the windings. Hotor was rewound and tested.
In
- addition, al'1 screws were tightened, and lock washers installed.
7 8
9 FACILITY STATUS
'4 POWER OTHER STATUS 0
~l5
~EQ23 ~09 9
Qss NA 7
8 9
10 12 13 44 ACTIVITY CONTENT RELEASED OF RELEASE AhIOUNTOF ACTIVITYQG G
~Z 03 Z
034 HA 7
8 9
10 44 PERSONNEL EXPOSURES NUMBER TYPE DCSCBIPTION 039
~77
~00 0
Q37 Z
Q33 NA 7
8 9
11 12 13 PERSONNEL INJURIES
~00 O
Qo
""N'A"'"
7 8
METHOD OF DISCOVCBY DISCOVERY DESCRIPTION Q32
~8031 Sur vei 1 1 ance Test 45 46 LOCATIONOF RELEASE QG 45 80 80 80 80 7
8 O
7 8
9 11 12 LOSS OF OR DAMAGETO FACILITYQ43 TYPE
DESCRIPTION
Z 042
~A 9
10 PUBLICITY ISSUED DESCRIPTION~
MNO
~A 9
10 D.K. HacVittie NAME OF, PREPARER 80 80 NRC USE ONLY 68 69 80 o 315-343-2110 x 1558 o
PHONE:
I c
~w>o~
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| | | Reporting criterion |
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| 05000220/LER-1978-001, Submittal of Licensee Event Report LER 78-01 Concerning Delta Temperature of the Discharge Water Exceeded Environmental Tech. Spec | Submittal of Licensee Event Report LER 78-01 Concerning Delta Temperature of the Discharge Water Exceeded Environmental Tech. Spec | | | 05000220/LER-1978-003, Regarding Drywell High Pressure Switch RE04A Setpoint Drift and LER 78-003-00 | Regarding Drywell High Pressure Switch RE04A Setpoint Drift and LER 78-003-00 | | | 05000220/LER-1978-005, And LER 78-005-00 for Nine Mile Point, Unit 1 Re During Unit Shutdown, Reserve Power Breaker on Power Board II Failed to Close in After Loss of Normal Power and During Plant Outage While Marking Up Outside MSIV 01-03 Discovered | And LER 78-005-00 for Nine Mile Point, Unit 1 Re During Unit Shutdown, Reserve Power Breaker on Power Board II Failed to Close in After Loss of Normal Power and During Plant Outage While Marking Up Outside MSIV 01-03 Discovered That Valve | | | 05000220/LER-1978-006, Re During Steady State Operation, Performance of Surveillance Test IC-75 Found a Trip Setpoint of 22.5 Inches Water on One Vacuum Switch in the Vacuum Relief System from the Pressure Suppression Chamber to the | Re During Steady State Operation, Performance of Surveillance Test IC-75 Found a Trip Setpoint of 22.5 Inches Water on One Vacuum Switch in the Vacuum Relief System from the Pressure Suppression Chamber to the | | | 05000220/LER-1978-009-01, For Nine Mile Point Unit 1 Regarding Replacement of Explosive Charges in the TIP Shear Valves with New Charges and the Resulting Unsatisfactory Ohmmeter Continuity Test for Acceptable Electric Contact | For Nine Mile Point Unit 1 Regarding Replacement of Explosive Charges in the TIP Shear Valves with New Charges and the Resulting Unsatisfactory Ohmmeter Continuity Test for Acceptable Electric Contact | | | 05000220/LER-1978-009, And LER 78-010-00 for Nine Mile Point, Unit 1 Re Technical Specification Violations of Listed Sections | LER 78-009-00 and LER 78-010-00 for Nine Mile Point, Unit 1 Re Technical Specification Violations of Listed Sections | | | 05000220/LER-1978-013, And LER 78-013-00 for Nine Mile Point, Unit 1 Re Technical Specification Violations of Section 3.6.2 | And LER 78-013-00 for Nine Mile Point, Unit 1 Re Technical Specification Violations of Section 3.6.2 | | | 05000220/LER-1978-014, LERs 78-014,00, 78-016-00, and 78-016-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump on 102 D/G Would Not Fill the Day Tank, Discovery of RE18C with a Setpoint of 129 Inches Wc, and | LERs 78-014,00, 78-016-00, and 78-016-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump on 102 D/G Would Not Fill the Day Tank, Discovery of RE18C with a Setpoint of 129 Inches Wc, and RE04B | | | 05000220/LER-1978-015, And LER 78-015-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump in 102 D/G Would Not Fill the Day Tank and Discovery That 12 Control Room Air Treatment Fan Would Not Run | And LER 78-015-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump in 102 D/G Would Not Fill the Day Tank and Discovery That 12 Control Room Air Treatment Fan Would Not Run | | | 05000220/LER-1978-018, For Nine Mile Point Unit 1 Regarding Discovery of Main Steam High Flow Switch with a Setpoint of 106.2 PSI, Which Is Above the Technical Specification | For Nine Mile Point Unit 1 Regarding Discovery of Main Steam High Flow Switch with a Setpoint of 106.2 PSI, Which Is Above the Technical Specification | | | 05000220/LER-1978-019, For Nine Mile Point Unit 1 Regarding Discovery That Hydraulic Snubber 31-HS-1 Had Failed and Was Empty of Hydraulic Fluid and Disconnected from Its Anchor at the Feedwater Pipe | For Nine Mile Point Unit 1 Regarding Discovery That Hydraulic Snubber 31-HS-1 Had Failed and Was Empty of Hydraulic Fluid and Disconnected from Its Anchor at the Feedwater Pipe | | | 05000220/LER-1978-020, LERs 78-020-00, 78-021-00, 78-022-00, and 78-023-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery of RE18A with a Setpoint of 135 Inches Wc, Discovery of RE04A and RE04B with a Setpoint of 3.65 PSIG, Discovery o | LERs 78-020-00, 78-021-00, 78-022-00, and 78-023-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery of RE18A with a Setpoint of 135 Inches Wc, Discovery of RE04A and RE04B with a Setpoint of 3.65 PSIG, Discovery of Turbine . | | | 05000220/LER-1978-024, For Nine Mile Point Unit 1 Regarding Discovery That Test N1-St-Q2,4,5,7,8,9, and 10 Had Not Been Performed During a Review of Quarterly Surveillance Test Results | For Nine Mile Point Unit 1 Regarding Discovery That Test N1-St-Q2,4,5,7,8,9, and 10 Had Not Been Performed During a Review of Quarterly Surveillance Test Results | | | 05000220/LER-1978-025, LERs 78-025-00, 78-026-00, and 78-027-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery of RE04D with a Setpoint of 3.70 PSIG, Discovery of Numerous Small Leaks in Small Sample and Instrument Pipes, and Discovery | LERs 78-025-00, 78-026-00, and 78-027-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery of RE04D with a Setpoint of 3.70 PSIG, Discovery of Numerous Small Leaks in Small Sample and Instrument Pipes, and Discovery of RE22D Wit | | | 05000220/LER-1978-028, For Nine Mile Point Unit 1 Regarding Discovery of the Allowable Test Interval of TS 4.1.4c for the Core Spray Power-Operated Valves Had Been Exceeded | For Nine Mile Point Unit 1 Regarding Discovery of the Allowable Test Interval of TS 4.1.4c for the Core Spray Power-Operated Valves Had Been Exceeded | | | 05000220/LER-1978-029, Regarding Discovery of High Drywell Pressure Switches RE04A, RE04B, and RE04C with Setpoints Less Conservative than the Technical Specifications | Regarding Discovery of High Drywell Pressure Switches RE04A, RE04B, and RE04C with Setpoints Less Conservative than the Technical Specifications | | | 05000220/LER-1978-030, 78-031-00, and 78-032-00 for Nine Mile Point Unit 1 Regarding, Respectively, Unavailability of Feedwater Pump 29-03 While Its Pump Seals Were Replaced, Unavailability of Liquid Poison Pump NP02A While a Frozen Valve | 78-031-00, and 78-032-00 for Nine Mile Point Unit 1 Regarding, Respectively, Unavailability of Feedwater Pump 29-03 While Its Pump Seals Were Replaced, Unavailability of Liquid Poison Pump NP02A While a Frozen Valve | | | 05000220/LER-1978-033-03, /03L-0 on 780916:Surveillance Tests on Barton Model 289 Pressure Indicating Switches Showed Changes in Setpoints Due to Instru Drift.Rev Surveillance Test Scheds Now Adequate to Ensure Early Detection of Drifts | /03L-0 on 780916:Surveillance Tests on Barton Model 289 Pressure Indicating Switches Showed Changes in Setpoints Due to Instru Drift.Rev Surveillance Test Scheds Now Adequate to Ensure Early Detection of Drifts | | | 05000220/LER-1978-034, Regarding an Environmental Contractor Obtaining 22 Hourly Fish Impingement Samples, and One Two-Hour Sample, Which Is Contrary to the Technical Specification Requiring 24 Hourly Samples | Regarding an Environmental Contractor Obtaining 22 Hourly Fish Impingement Samples, and One Two-Hour Sample, Which Is Contrary to the Technical Specification Requiring 24 Hourly Samples | | | 05000220/LER-1978-035, Forwards LER 78-035/01T-0 | Forwards LER 78-035/01T-0 | | | 05000220/LER-1978-035-01, /01T-0 on 781020:all Main Steam High Flow Pressure Indicating Instr Were Found W/Setpoints Less than Tech Specs.Heise 0-200 PSIG Test Gauge Calibrated & Used in Test Had Loose Screw & Was Recalibrated | /01T-0 on 781020:all Main Steam High Flow Pressure Indicating Instr Were Found W/Setpoints Less than Tech Specs.Heise 0-200 PSIG Test Gauge Calibrated & Used in Test Had Loose Screw & Was Recalibrated | | | 05000220/LER-1978-036-04, /04T-0 on 781025:improper Appl of Brook Model 9456 Oval Gear Flowmeter Combined W/Failed Seal on Caustic Addition Pump Caused High Concentration of Sodium & Sulfate & Degraded Capability to Control Rate of Discharge | /04T-0 on 781025:improper Appl of Brook Model 9456 Oval Gear Flowmeter Combined W/Failed Seal on Caustic Addition Pump Caused High Concentration of Sodium & Sulfate & Degraded Capability to Control Rate of Discharge | | | 05000220/LER-1978-036, Forwards LER 78-036/04T-0 | Forwards LER 78-036/04T-0 | | | 05000220/LER-1978-037, Forwards LER 78-037/03L-0, 78-038/03L-0 & 78-039/03L-0 | Forwards LER 78-037/03L-0, 78-038/03L-0 & 78-039/03L-0 | | | 05000220/LER-1978-037-03, /03L-0 on 781027:test Revealed Trip Setpoint of 26.5 Inches Water on One Vacuum Switch in Vacuum Relief Sys from Pressure Supression Chamber to Rx Bldg.Caused by Instru Drift in a Mercoid Model CP4122 Vacuum Switch | /03L-0 on 781027:test Revealed Trip Setpoint of 26.5 Inches Water on One Vacuum Switch in Vacuum Relief Sys from Pressure Supression Chamber to Rx Bldg.Caused by Instru Drift in a Mercoid Model CP4122 Vacuum Switch | | | 05000220/LER-1978-038-03, /03L-0 on 781025:review of N1-ISP-RE22 Test Results Found 12 Instances Where Procedure Was Violated. Caused by Carelessness in Procedure Implementation. Re-instruction & Closer Supervision Instituted | /03L-0 on 781025:review of N1-ISP-RE22 Test Results Found 12 Instances Where Procedure Was Violated. Caused by Carelessness in Procedure Implementation. Re-instruction & Closer Supervision Instituted | | | 05000220/LER-1978-039-03, /03L-0 on 781103:surveillance Test N1-ISP-RE02 Revealed Rx Lo-Lo Water Level Switch W/Trip Setpoint of +2 Inches Water.Caused by Instru Drift.Setpoint Reset | /03L-0 on 781103:surveillance Test N1-ISP-RE02 Revealed Rx Lo-Lo Water Level Switch W/Trip Setpoint of +2 Inches Water.Caused by Instru Drift.Setpoint Reset | | | 05000220/LER-1978-040-03, /03L-0 on 781113: 112 Core Spray Topping Pump Motor Breaker Closed Starting Pump But Breaker Closing Spring Motor Was Running Continuously & Not Charging Closing Spring.Caused by Misaligned Motor Assembly at Latching Pawl | /03L-0 on 781113: 112 Core Spray Topping Pump Motor Breaker Closed Starting Pump But Breaker Closing Spring Motor Was Running Continuously & Not Charging Closing Spring.Caused by Misaligned Motor Assembly at Latching Pawl | | | 05000220/LER-1978-040, Forwards LER 78-040/03L-0 | Forwards LER 78-040/03L-0 | | | 05000220/LER-1978-041, Forwards LER 78-041/04T-0 | Forwards LER 78-041/04T-0 | | | 05000220/LER-1978-041-04, /04T-0 on 781220:during Impingement Sampling Only 23 Samples (22 Hourly Samples & One 2-hr Sample) Were Collected Instead of 24 Required Samples,Caused by one-time Personnel Scheduling Change | /04T-0 on 781220:during Impingement Sampling Only 23 Samples (22 Hourly Samples & One 2-hr Sample) Were Collected Instead of 24 Required Samples,Caused by one-time Personnel Scheduling Change | |
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