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| issue date = 12/09/1980
| issue date = 12/09/1980
| title = Interim Deficiency Rept Re Unsupported Anchors Between Concrete Floors & Equipment Base Plates,Initially Reported 801107.Caused by Unfilled Annular Space Between Pipe Shim & Anchor.Use of Shims Around Anchors Will Be Discontinued
| title = Interim Deficiency Rept Re Unsupported Anchors Between Concrete Floors & Equipment Base Plates,Initially Reported 801107.Caused by Unfilled Annular Space Between Pipe Shim & Anchor.Use of Shims Around Anchors Will Be Discontinued
| author name = CURTIS N W
| author name = Curtis N
| author affiliation = PENNSYLVANIA POWER & LIGHT CO.
| author affiliation = PENNSYLVANIA POWER & LIGHT CO.
| addressee name = GRIER B H
| addressee name = Grier B
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
| docket = 05000387, 05000388
| docket = 05000387, 05000388
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:REGULATURr>>FOR'>ATIOttDISTRIBU1IO<SYiE"I(RIOS)ACCESSIU'tfR:8012190573OuC.r(ATE:80/12/09NOTARIEEO:NOFACIL'"-SusqirehannaSteamElectricStation~unit1rPennsylva0-3HsouehannaStea(nElectricStationsi!nit2iPennsylvaAr!THuRAt-FlLIATIONTI3g.'4~'v(~PennsylvaniaPower8,LightCo.RECIPei(A<<cRECIr'Ie,i<1AFFILI'ATIOttGR1ERi8~H~ReqronliPni1aaelphia<OfficeoftheOirector
{{#Wiki_filter:REGULA TUR      r>>FOR'>AT IOtt    DISTR IBU1IO< SY      i E "I   (RIOS)
ACCESS    IU't f R:8012190573                          OuC. r(ATE:   80/12/09      NOTARI EEO:       NO FACIL'" -                   Susqirehanna          Steam    Electric Station~ unit 1r Pennsylva              05000387 0-3 H              souehanna        Stea(n  Electric Stations i!nit 2i Pennsyl va            0500u388 Ar!THuR    At-FlLIATION T I 3 g.'4 ~
                    'v( ~               Pennsylvania        Power 8, Light Co.
REC  IP e i(A<<c                      REC Ir'Ie,i<1 AFF ILI'ATIOtt GR1ERi8      ~ H   ~                     Reqron    li    Pni aaelphia<
1            Of f ice  of the Oir ector


==SUBJECT:==
==SUBJECT:==
Interimdeficiencyreptreunsuppartedancharsbetweenconcretefloors8equiomentbaseplates>ini-tiallyreported801107~Causedby-un'l1edannularspacebetweenpipeshimanchor.useofSnimsaroundanchorswi11oediscontinued~OISTHIbiJTIONCCOc,:R019SCOYIESRECEIVEi):LTDE4CLSIZE:TITLE:ConstructionOeticiencyReport(10CFR50.55E)NOTES:SendI(t,E3copiest-S'AR8a'll'amends,SendIt(E3copies,FSAR'llallamends'OCKET050003870500u3880500038705000388DECI'PIE"1IOCO()E/ttA>iEAC1'Ot'iA/0LICEiiStvG04RUSdbR(rOK.H.OeIWTERt~AL:AO/RCI/IE17ASL8P/J.~(a<ROOIKOIVOFLICEikuIPDUALRR11IQE09NPA20OELO21QARR14aurHERFO~O,"r.It-COl'I.ESLT1'REtlCL111111111.1111111l11RECIPIEeTIOCOOE/ilAtlEYOUiYGBLOOOg805STARKqR~07AEnOr)/OIRHU>tFAC15EonISTAFF198YO/GEORR22LICUALOR12(vRCPOR02P13OlOi)EV21COPIESLTTR'~tCL1111EXTER(AAL'CHSruSIC1o0trle16110311DEC22=l989)r5TOTAL.ti!<<BEDOFCOPIESHFuUIRt.n:LTTR~E(~CL TWONORTHNINTHSTREET,ALLENTOWN,PA.18101PHONErt215I821~5151NORMANW.CURTISVicePresiaent-Engineering8Conslructlcn-Nuclear821-5381December9,1980Mr.BoyceH.GrierDirector,RegionIU.S.NuclearRegulatoryCommission631ParkAvenueKingofPrussia,Pennsylvania19406SUSQUEHANNASTEAMELECTRICSTATIONINTERIMREPORTOFADEFICIENCYRELATINGTOSHIMMINGOFBASEPLATESERs100450/100508FILES840-4/900-10PLA-586nwrCAro
Interim deficiency rept re unsupparted anchars between
                                    ~                          1      amends'OCKET concr ete floors 8 equioment base plates> ini-tial ly reported 801107 Caused by- un' l ed annul ar space between pipe shim anchor.use of Snims around anchor s wi1 oe discontinued ~       1 OISTH IbiJTION CCOc,: R019S                        COYIES RECEI VEi):LTD            E4CL            SIZE:
TITLE: Construction Oeticiency                              Repor t (10CFR50.55E)
NOTES:Send              I(t,E 3      copies t-S'AR 8 a'll 'amends,                                           05000387 Send          It(E    3    copies, FSAR'll all                                                    05000388 DECI'PIE"         1          C Ol'I.ES            REC  IP IEe T              COPIES IO CO()E/ttA>iE                  LT 1'R EtlCL        IO  COOE/ilAtlE            LTTR'~tCL AC 1'Ot'i        A/0        L I CEiiStvG 04                      1    YOUiYGBLOOOg8 05                1    1 RUSdbR(rOK.H. Oe                        1        1    STARKqR ~          07            1    1 I WTERt~AL: AO/RC I/IE                        17        1        1    AEnO A S L8 P    / J. ~ (a < R O            1        1    r)/OI R  HU>t FAC 15 OIK OIV OF LIC                          1        1. Eon  I  STAFF    19 EikuIP DUAL RR11                        1        1    8YO/GEO RR        22 IQE                          09        1        1    LIC    UAL OR    12 NPA                          20        1        1    (vRC  POR          02 OELO                        21          1      l    P                  13 QA      RR                  14        1                                Ol aurHERFO~O,"r. It-                               1              Oi )EV    21 EXTER(AAL'CHS                                  1o        le      16                        03            1    1 ruS    IC                    0tr        1        1 DEC 2    2= l989 TOTAL .ti!<<BED OF COPIES                      HFuUIRt.n: LTTR       ~)r5  E(~CL


==DearMr.Grier:==
TWO NORTH NINTH STREET, ALLENTOWN, PA. 18101      PHONEr t215I 821 ~ 5151 NORMAN W. CURTIS Vice Presiaent-Engineering  8 Conslructlcn-Nuclear 821-5381 December 9, 1980 Mr. Boyce H. Grier Director, Region I U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania 19406 SUSQUEHANNA STEAM ELECTRIC STATION n
ThisletterservestoprovidetheCommissionwithaninterimreportofadeficiencyregardingtheuseofpipeshimsaroundanchorsbetweenconcretefloorsandequipmentbaseplates.ThedeficiencywasoriginallyreportedbytelephonetoNRCRegionIInspectorMr.L.NarrowbyMr.R.A.SchwanofPPGLonNovember7,1980.Duringthatconversation,Mr.Narrowwasadvisedthattheconditionwasunderevaluationforreportabilityundertheprovisionsof10CFR50.55(e).ThedeficiencyhasbeendocumentedbyBechtelunderMCAR1-64issuedonNovember4,1980;andPPaLhassubsequentlyconcludedthattheconditionisreportableunder10CFR50.55(e).Theattachmenttothislettercontainsthedescriptionoftheproblems,theapproachtoresolutionalongwiththebasi.s.forreportability.Sincethedetailsofthisreport-provideinformationrelevanttothereportingrequirementsof10CFR21,thiscorrespondenceisconsideredtoalsodischargeanyformalresponsibili.tyPPGLmayhaveforreportingincompliancethereto.Weexpecttoprovideafi.nalreportonthedeficiencyinFebruary,1981.Verytrulyyours,N.W.CurtisVicePresident-EngineeringaConstruction-NucleartLC(V5AttachmentFLW:mcbPENNSYLVANIAPOWERILLIGHTCOMPANY 0''r.BoyceH.GrierDecember9,1980cc:Mr.VictorStello(15)..Director,RegionIU.S.Nuc'learRegulatoryCommissionWashington,D.C.,20555IOfficeof'ManagementInformationaProgramControlU.S.NuclearRegulatoryCommissionWashington,D.C.20555Mr.RobertM;Gall'oU.S.NuclearRegulatoryCommissionP.0.Box52,Shickshinny,Pennsylvania18655 0'TTACHMENT'OPLA-586DESCRIPTIONOFTHEPOTENTIALPROBLEMSBechtelEngineeringbecameawarethatpipe.shimshavebeenusedaroundanchorsbetweenconcretefloors-and,base.plates.Thesewereusedfearsettingandlevelingofthebaseplatesofvarioustypesofsupports.Themajorityof.theexisting.baseplates,havebeenalreadygrouted,however,theannularspacebetween.pipeshimandtheanchorisnotfilled'S'eeFigure'l.').Thegrout,thickne'ss(and.also.theheightofthepipeshim)generallyr'angesbetweenoneandtwoinches.As.theanchorsareunsupported'ithintheheightofpipe.shims,,their,shearcapacitiesmayb'esignificantly.reduced.IFurthercommunicationbyBechtel.EngineeringwithBechtelField.Engineeringindicatedthatthisaondition~ists-..typicallyonthefollowingtypesoffloormountedsupports:a.Largeandsmallpipesupports.b.Instrument.supportsc.ElectricalsupportsZnaddition.totheabovecondition,onafewfloormountedpipesupports,itwasobserved'hatanutwasplaced'withinthepipeshimandtackwelded.(SeeFigure'2')This'conditionmay-haveanadverseimpactindevelopingandverifyingrequiredinstallationtorque/prestressintheanchors.'PPROACH"TORESOLUTIONOFTHE.PROBLEMS(Ondiscoveryof.theproblenrs,BechtelFieldEngineeringwasinstructedbyBechtelEngineeringtodiscontinueuseofpipeshimsaroundanchors.Aninspectionprogramisplannedtoidentifyanddeterminethescopeofthisproblem;,Basedupontheinformationobtained,adequacyofanchorswillbeaccordinglyevaluated.Fortheresolutionoftheproblem>thefollowingoptionsarebeingconsidered.a.Developinganarialyticalmethodforengineeringevaluation.,b.Removingpipeshims,wherebaseplatesarenotgrouted.c.Fillingtheannularspacewithanapprovedmaterial.STATUSOF'ROPOSEDRESOLUTIONSBechtel.fieldpersonnelarecurrentlydevelopingafieldprocedureforunder<<takingtheinspectionprogramnecessarytoresolvetheuseofpipeshimsaroundanchors.TheinspectionisscheduledtocommenceinDecember1980.Additionally,thefieldhasestablishedthefeasibilityoffillingthevoidshowninFigure1withgroutingmaterial.BechtelEngineeringisintheprocessofevaluatingthisconditionbyanalyticalmethod.rAninspectionandremedialprogramispresentlybeingplannedwhichwilldealwiththetackweldingoflevelingnutsinsidepipeshims(Figure2).
wr CA        ro INTERIM REPORT OF A DEFICIENCY RELATING TO SHIMMING OF BASE PLATES ERs    100450/100508              FILES 840-4/900-10 PLA-586
ATTACM:-?KTOPLA-586(Pae2)REPORTABZLXTYPPsLEngineeringhasdeterminedthese-problemstobereportabletoNRCunderlOCPR50.55(e)forthefollowingreasons.a.Theconditions,hadtheygoneunnoticed,mighthaveadverseimpactonthesafeoperation/shutdownoftheplantastheseanchorssupportsafetyrelatedsystemsand/orpiping.b.Baseduponthe-availableinformation,theseconditionsmayrequireextensiveevaluation.and/orrepairtomeetstructuralrequirements.  
 
'Z9Pd/WNRoo7PIPESHIT.~\4~~~~0~~t'r~re\~o~~r4~0h~~~~~~~~~a~~~~~'I(gl"C':~~~.~(g]cegr~>~,~erdSHIMNIAIG.OFBASE'PEATED~1Z
==Dear Mr.       Grier:==
~~'oo@.~Oi~,~0~~gt~~~~~~F.:Ex]sv-wccome.EXPANsldNANCHORpypssHl
 
}}
This      letter serves to provide the Commission with an interim report of a deficiency regarding the use of pipe shims around anchors between concrete floors and equipment base plates.
The deficiency was originally reported by                telephone to NRC Region        I  Inspector Mr. L. Narrow by Mr. R. A. Schwan of PPGL                on November 7, 1980. During that conversation, Mr. Narrow was advised that                the condition  was under      evaluation for reportability under the provisions of              10CFR50.55(e).
The deficiency has been documented by Bechtel under MCAR 1-64 issued on November 4, 1980; and PPaL has subsequently concluded that the condition                        is reportable under 10CFR50.55(e). The attachment to this letter contains the description of the problems, the approach to resolution along with the basi.s.for reportability.
Since the        details of this report- provide information relevant to the reporting requirements of 10CFR21, this correspondence is considered to also discharge any formal responsibili.ty PPGL may have for reporting in compliance thereto.
We expect to provide a fi.nal report on the deficiency in February, 1981.
Very      truly yours, tLC (V 5
N. W.       Curtis Vice President-Engineering              a Construction-Nuclear Attachment FLW:mcb PENNSYLVANIA POWER    IL LIGHT COMPANY
 
0     '
                                                          'r.
Boyce H. Grier                                    December 9, 1980 cc: Mr. Victor Stello      (15)
  .. Director, Region  I U. S. Nuc'lear Regulatory Commission Washington, D.C.,     20555 I
Office of'Management Information  a Program Control U. S. Nuclear Regulatory Commission Washington, D.C.       20555 Mr. Robert M; Gall'o U. S. Nuclear  Regulatory Commission P. 0. Box 52, Shickshinny, Pennsylvania    18655
 
              'O    PLA-586 0'TTACHMENT DESCRIPTION OF THE POTENTIAL PROBLEMS Bechtel Engineering became aware that pipe.shims have been used around anchors between concrete floors-and, base. plates. These were used fear setting and leveling of the base plates of various types of supports. The majority of.
the existing. base plates, have been already grouted, however, the annular space between. pipe shim and the anchor is not filled'S'ee Figure 'l.'). The grout, thickne'ss (and. also. the height of the pipe shim) generally r'anges between one and two inches. As. the anchors are unsupported'ithin the height of pipe.shims,, their, shear capacities      may b'e significantly. reduced.
I Further communication by Bechtel. Engineering with Bechtel Field. Engineering indicated that this aondition ~ists-..typically on the following types of floor mounted supports:
: a. Large and small pipe supports.
: b. Instrument. supports
: c. Electrical supports Zn addition. to the above condition, on a few floor mounted pipe supports, was observed'hat a nut was placed'within the pipe shim and tack welded.
it (See Figure '2') This'condition may -have an adverse impact in developing and verifying required installation torque/prestress        in the anchors.
'PPROACH"TO RESOLUTION OF THE. PROBLEMS
(
On  discovery of. the problenrs, Bechtel Field Engineering was instructed by Bechtel Engineering to discontinue use of pipe shims around anchors.
An  inspection program is planned to identify and determine the scope of this problem;,   Based upon the information obtained, adequacy of anchors will be accordingly evaluated.
For the resolution of the problem> the following options are being considered.
: a. Developing an arialytical method for engineering evaluation.
                , b. Removing pipe shims, where base plates are not grouted.
: c. Filling the annular space with an approved material.
STATUS OF'ROPOSED RESOLUTIONS Bechtel. field  personnel are currently developing a    field procedure for  under<<
taking the inspection program necessary to resolve the use of pipe shims around anchors. The inspection is scheduled to commence in December 1980. Additionally, the field has established the feasibility of filling the void shown in Figure 1 with grouting material.
Bechtel Engineering is    in the  process of evaluating    this condition  by analytical method.
r An inspection and remedial program is        presently being planned which    will deal with the tack welding of leveling nuts inside pipe shims (Figure 2).
 
ATTACM:-?K TO PLA-586 (Pa e 2)
REPORTABZ LXTY PPsL Engineering has determined these- problems to be reportable to NRC under lOCPR50.55(e) for the following reasons.
: a. The conditions, had they gone unnoticed, might have adverse impact on the safe operation/shutdown of the plant as these anchors support safety related systems and/or piping.
: b. Based upon the-available information, these conditions may require extensive evaluation. and/or repair to meet structural requirements.
 
  'Z 9
Pd/W                                                                      NRoo7 PIPE SHIT.
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Latest revision as of 00:49, 22 October 2019

Interim Deficiency Rept Re Unsupported Anchors Between Concrete Floors & Equipment Base Plates,Initially Reported 801107.Caused by Unfilled Annular Space Between Pipe Shim & Anchor.Use of Shims Around Anchors Will Be Discontinued
ML18030A024
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 12/09/1980
From: Curtis N
PENNSYLVANIA POWER & LIGHT CO.
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
10CFR-050.55E, 10CFR-50.55E, ER-100450-10050, PLA-586, NUDOCS 8012190573
Download: ML18030A024 (7)


Text

REGULA TUR r>>FOR'>AT IOtt DISTR IBU1IO< SY i E "I (RIOS)

ACCESS IU't f R:8012190573 OuC. r(ATE: 80/12/09 NOTARI EEO: NO FACIL'" - Susqirehanna Steam Electric Station~ unit 1r Pennsylva 05000387 0-3 H souehanna Stea(n Electric Stations i!nit 2i Pennsyl va 0500u388 Ar!THuR At-FlLIATION T I 3 g.'4 ~

'v( ~ Pennsylvania Power 8, Light Co.

REC IP e i(A<<c REC Ir'Ie,i<1 AFF ILI'ATIOtt GR1ERi8 ~ H ~ Reqron li Pni aaelphia<

1 Of f ice of the Oir ector

SUBJECT:

Interim deficiency rept re unsupparted anchars between

~ 1 amends'OCKET concr ete floors 8 equioment base plates> ini-tial ly reported 801107 Caused by- un' l ed annul ar space between pipe shim anchor.use of Snims around anchor s wi1 oe discontinued ~ 1 OISTH IbiJTION CCOc,: R019S COYIES RECEI VEi):LTD E4CL SIZE:

TITLE: Construction Oeticiency Repor t (10CFR50.55E)

NOTES:Send I(t,E 3 copies t-S'AR 8 a'll 'amends, 05000387 Send It(E 3 copies, FSAR'll all 05000388 DECI'PIE" 1 C Ol'I.ES REC IP IEe T COPIES IO CO()E/ttA>iE LT 1'R EtlCL IO COOE/ilAtlE LTTR'~tCL AC 1'Ot'i A/0 L I CEiiStvG 04 1 YOUiYGBLOOOg8 05 1 1 RUSdbR(rOK.H. Oe 1 1 STARKqR ~ 07 1 1 I WTERt~AL: AO/RC I/IE 17 1 1 AEnO A S L8 P / J. ~ (a < R O 1 1 r)/OI R HU>t FAC 15 OIK OIV OF LIC 1 1. Eon I STAFF 19 EikuIP DUAL RR11 1 1 8YO/GEO RR 22 IQE 09 1 1 LIC UAL OR 12 NPA 20 1 1 (vRC POR 02 OELO 21 1 l P 13 QA RR 14 1 Ol aurHERFO~O,"r. It- 1 Oi )EV 21 EXTER(AAL'CHS 1o le 16 03 1 1 ruS IC 0tr 1 1 DEC 2 2= l989 TOTAL .ti!<<BED OF COPIES HFuUIRt.n: LTTR ~)r5 E(~CL

TWO NORTH NINTH STREET, ALLENTOWN, PA. 18101 PHONEr t215I 821 ~ 5151 NORMAN W. CURTIS Vice Presiaent-Engineering 8 Conslructlcn-Nuclear 821-5381 December 9, 1980 Mr. Boyce H. Grier Director, Region I U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, Pennsylvania 19406 SUSQUEHANNA STEAM ELECTRIC STATION n

wr CA ro INTERIM REPORT OF A DEFICIENCY RELATING TO SHIMMING OF BASE PLATES ERs 100450/100508 FILES 840-4/900-10 PLA-586

Dear Mr. Grier:

This letter serves to provide the Commission with an interim report of a deficiency regarding the use of pipe shims around anchors between concrete floors and equipment base plates.

The deficiency was originally reported by telephone to NRC Region I Inspector Mr. L. Narrow by Mr. R. A. Schwan of PPGL on November 7, 1980. During that conversation, Mr. Narrow was advised that the condition was under evaluation for reportability under the provisions of 10CFR50.55(e).

The deficiency has been documented by Bechtel under MCAR 1-64 issued on November 4, 1980; and PPaL has subsequently concluded that the condition is reportable under 10CFR50.55(e). The attachment to this letter contains the description of the problems, the approach to resolution along with the basi.s.for reportability.

Since the details of this report- provide information relevant to the reporting requirements of 10CFR21, this correspondence is considered to also discharge any formal responsibili.ty PPGL may have for reporting in compliance thereto.

We expect to provide a fi.nal report on the deficiency in February, 1981.

Very truly yours, tLC (V 5

N. W. Curtis Vice President-Engineering a Construction-Nuclear Attachment FLW:mcb PENNSYLVANIA POWER IL LIGHT COMPANY

0 '

'r.

Boyce H. Grier December 9, 1980 cc: Mr. Victor Stello (15)

.. Director, Region I U. S. Nuc'lear Regulatory Commission Washington, D.C., 20555 I

Office of'Management Information a Program Control U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. Robert M; Gall'o U. S. Nuclear Regulatory Commission P. 0. Box 52, Shickshinny, Pennsylvania 18655

'O PLA-586 0'TTACHMENT DESCRIPTION OF THE POTENTIAL PROBLEMS Bechtel Engineering became aware that pipe.shims have been used around anchors between concrete floors-and, base. plates. These were used fear setting and leveling of the base plates of various types of supports. The majority of.

the existing. base plates, have been already grouted, however, the annular space between. pipe shim and the anchor is not filled'S'ee Figure 'l.'). The grout, thickne'ss (and. also. the height of the pipe shim) generally r'anges between one and two inches. As. the anchors are unsupported'ithin the height of pipe.shims,, their, shear capacities may b'e significantly. reduced.

I Further communication by Bechtel. Engineering with Bechtel Field. Engineering indicated that this aondition ~ists-..typically on the following types of floor mounted supports:

a. Large and small pipe supports.
b. Instrument. supports
c. Electrical supports Zn addition. to the above condition, on a few floor mounted pipe supports, was observed'hat a nut was placed'within the pipe shim and tack welded.

it (See Figure '2') This'condition may -have an adverse impact in developing and verifying required installation torque/prestress in the anchors.

'PPROACH"TO RESOLUTION OF THE. PROBLEMS

(

On discovery of. the problenrs, Bechtel Field Engineering was instructed by Bechtel Engineering to discontinue use of pipe shims around anchors.

An inspection program is planned to identify and determine the scope of this problem;, Based upon the information obtained, adequacy of anchors will be accordingly evaluated.

For the resolution of the problem> the following options are being considered.

a. Developing an arialytical method for engineering evaluation.

, b. Removing pipe shims, where base plates are not grouted.

c. Filling the annular space with an approved material.

STATUS OF'ROPOSED RESOLUTIONS Bechtel. field personnel are currently developing a field procedure for under<<

taking the inspection program necessary to resolve the use of pipe shims around anchors. The inspection is scheduled to commence in December 1980. Additionally, the field has established the feasibility of filling the void shown in Figure 1 with grouting material.

Bechtel Engineering is in the process of evaluating this condition by analytical method.

r An inspection and remedial program is presently being planned which will deal with the tack welding of leveling nuts inside pipe shims (Figure 2).

ATTACM:-?K TO PLA-586 (Pa e 2)

REPORTABZ LXTY PPsL Engineering has determined these- problems to be reportable to NRC under lOCPR50.55(e) for the following reasons.

a. The conditions, had they gone unnoticed, might have adverse impact on the safe operation/shutdown of the plant as these anchors support safety related systems and/or piping.
b. Based upon the-available information, these conditions may require extensive evaluation. and/or repair to meet structural requirements.

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