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=Text=
=Text=
{{#Wiki_filter:REGULATORY INFORNATION DISTRIBUTION SYSTEM (RIDS)DISTRIBUTION FOR INCOMING MATERIAL 50-260 REC: OREILLY J P NRC ORG: FOX H S.TN VALLEY AUTH DOCDATE: 05/05/78 DATE RCVD: 05/09/78 DOCTYPE: LETTER NOTARIZED:
{{#Wiki_filter:REGULATORY INFORNATION DISTRIBUTION SYSTEM (RIDS)
NO COPIES RECEIVED  
DISTRIBUTION FOR INCOMING MATERIAL                       50-260 REC: OREILLY     J P               ORG: FOX H S.                   DOCDATE: 05/05/78 NRC                                TN VALLEY AUTH                DATE RCVD: 05/09/78 DOCTYPE:     LETTER     NOTARIZED: NO                                 COPIES RECEIVED


==SUBJECT:==
==SUBJECT:==
LTR i ENCL i LICENSEE EVENT REPT 078-006 ON 3/25/78 CONCERNING CHECK VALVE 2-73-603 IN HIGH-PRESSURE COOLANT INJECTION SYSTEI"l WAS FOUND IN OPEN POSITION RESULTS NO HAZARD TO PUBLIC HEALTH OR SAFETY.PLANT NAME: BROWNS FERRY-UNIT 2 INCIDENT REPORTS (DISTRIBUTION CODE A002)REVIEWER INITIAL: XRS DISTRIBUTOR INITIAL: ssss+w+++>++~~++w+4~~~
LTR i LICENSEE EVENT REPT 078-006 ON 3/25/78 CONCERNING CHECK VALVE 2-73-603 IN ENCL  i HIGH-PRESSURE COOLANT INJECTION SYSTEI"l WAS FOUND IN OPEN POSITION RESULTS           NO HAZARD TO PUBLIC HEALTH OR SAFETY.
DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS FOR ACTION: INTERNAL: BR CHIEF LEAR 4W/4 ENCL EG FILE++M/E CL SCHROEDER/I PPOL I TO4+W/ENCL NOVAK/CHECK++M/ENCL KN I GHT<4 W/ENCL HANAUER4+W/ENCL E I SENHUT+4 W/ENCL SHAG+>W/ENCL KREGER/J.COLL INS~4l VENCL K SEYFRIT/IE++W/ENCL NRC PDR+4M/ENCL NIPC++W/3 ENCL HOUSTON++M/ENCL EEB+~~W/ENCL BUTLER+4W/ENCI TEDESCO>~W/ENCL BAER++W/ENCL VOLLEYER/BUNCH++W/ENCL ROSA++M/ENCL EXTERNAL: LPDR S ATHENS AL+<W/ENCL TIC++W/ENCL NS I C4~4~W/ENCL ACRS CAT B+>W/ih ENCL COPIES NOT SUB~IITXED PFR~REGULATORY GUIDE 10.1 DISTRIBUTION:
PLANT NAME: BROWNS FERRY UNIT 2                           REVIEWER   INITIAL: XRS DISTRIBUTOR   INITIAL:
LTR 45 ENCL 45 SIZE: iP+2P CONTROL NBR: 78i300004 HHf+%0l+%%%%+SHHM%%%%%%%%%%%%%%%%%%%%
ssss+w+++>++~~++w+4~~~ DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS INCIDENT REPORTS
THE END I I-e>>
( DISTRIBUTION CODE A002)
l c TENNESSEE VALLEY AUTHORITY GHATTANooGA.
FOR ACTION:       BR   CHIEF LEAR 4W/4 ENCL INTERNAL:            EG   FILE++M/E CL             NRC PDR+4M/ENCL NIPC++W/3 ENCL SCHROEDER/I PPOL I TO4 +W/ENCL  HOUSTON++M/ENCL NOVAK/CHECK++M/ENCL            EEB+~~W/ENCL KN I GHT<4 W/ENCL               BUTLER+4W/ENCI HANAUER4+W/ENCL                TEDESCO>~W/ENCL E I SENHUT+4 W/ENCL            BAER++W/ENCL SHAG+>W/ENCL                    VOLLEYER/BUNCH++W/ENCL KREGER/J. COLL INS~4l VENCL     ROSA++M/ENCL K  SEYFRIT/IE++W/ENCL EXTERNAL:         LPDR S ATHENS AL+<W/ENCL TIC++W/ENCL I
TENNEssEE 37401 MAY q)978 Mr.J'ames P.O'Really, Director U.S.Nuclear Regulatory Commission Office of Xnspection and Enforcement Region XX 230 Peachtree Street~Ef.>Suite 12l7 AtLanta, Georgia 30303 CC j~: O'C MOP~~cn;a j>1 Kl C7 rcc CA r v:, CD Deax Mr.O'Re~: I'KINESSEE VAXL1K AVKORXTY BEES XZRHY IjlUCLEAR PXAIG UNXT 2-DOCKET NO 50 260+PACXXZTY OPEHATIKr LICENSE DPR+52 REPORTAKE OCCURRENCE REPORT 3PRO 50-260/786 ghe enclosed report provides details concerning check valve 2-73-603 in the high-pressure coolant injection system that was found in open position during the maintenance inspection after failing a local leds rate test.Tbis xeport is submitted in accox'dance srlth 3h'cans Perry unit 2 Technical Spec9.fications, Section 6.7.2.'b.(2).Very tr~yours, TENNESSEE VAIZZY AUTHORXTY E.8.Pox Director of Power Production Enclosure (3}cc (Enclosure):
NS C4~4~W/ENCL ACRS     CAT B+>W/ih ENCL PFR COPIES NOT SUB~IITXED
Director Office of Management Xnformation and Program Control U.S.Nuclear Regulatory Commission Washington, DC 20555 Director{40}Office of Xnspection and.Enforcement U.S.Nuclear Regulator Comission Washington,'DC 20555 781300004 An Equal Opportunity Employer  
                                                                                    ~
.4 EL P I L ca 34'I'I r~P V I'4 4.4~'~~'Vt m~L I'LL-'I 11 14 P 4 Il QL  
REGULATORY GUIDE 10.1 DISTRIBUTION:         LTR 45       ENCL 45                   CONTROL NBR:    78i300004 SIZE: iP+2P HHf+%0l+%%%%+SHHM%%%%%%%%%%%%%%%%%%%%         THE END
.771 LfCENSEE EVENT REPORT , p CONTRO'-.SLOE: IPLEASE PRINT OR TYPE EQUIRED INFORMATION) 6 O 1 A L B R P 2 P2 0 0-0 0 0 0 0-0 0 Qs fp 1 1 1 1 Qn~Q 8 9 LICENSEE CODE 14 15 LICENSE NUhlBER 26 26 LICENSE TYPE 30 57 CAT 68 CON'T o 1""~LQs 0 5 0 0 0 2 6 0 07 0 3 2 5 7 8 8 0 5 0 5 7 8 09 SOURCE 8 60 61 DOCK ET N V hi 8 E R 68 69 EVENT DATE 74 76 REPORT DATE 80 EVENT DESCRIPTION ANO PROBABI.E CONSEQUENCES 010 o 2 Following failure of local leak x'ate test (Reference Technical Specifications
 
~O3 4.7.A.2.g and h)va lve maintenance was performed~
I I -e>>
.During the maintenance inspection~
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check valve 2"73-603pin high~zesu se zcoolant injection systempwas Bound in open position.A redundant valve was operable.'Zhere was no hazard to the T7ublic health 6 or safety.(See attached sheet.)~O8 80 7 8 9 SYSTEM CAUSE CAUSE COMP.VALV E CODE CODE SUBCODE, COMPONENT CODE SVBCODE SUBCODC~CE Q11~B Q12~C Q13 V A L V E E Q14~C Qns~A Qs 7 8 9 1O 12 13 18 I9 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIRO EVENT YEAR REPORT NO.CODE'YPE NO.QET REPoRT~7/~~00 6~~~03~L~0 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHhlENT NPRD4 PRIhlE COMP, COMPONENT TAKEN ACTION GN PLANT hIETHOD HOURS 022 SUBMITTED FORM BVB.SUPPLIER hlANUFACTURER
TENNESSEE VALLEY AUTHORITY GHATTANooGA. TENNEssEE 37401 MAY q     )978 r v:,
~Bpls~Zpfs~ZQ20'~ZQ21 0 0 0 0~Yfp23~NQ24~NQ29 0 2 6 Qs 33 34 35 36 31 40 41 42 43'4 47 CAUSE OESCRIPTION ANO CORRECTIVE ACTIONS 27 o The cause of the open position was a dimensional errox in component interference clearance.
Mr. J'ames P. O'Really, Director U.S. Nuclear Regulatory Commission                                 j~:
The corrective action t'aken was to machine the valve component to provide interference clearance.
MOP~
~I 3 The valve data is: Nf g: Crane Chapman.'ize;20 inch.Type: Swing check;4 Rating l50 lb~7 8 9 FACILITY STATUS'POWER OTHER STATUS 1 5 28 0 0 0 9 N/A NQ~ps ACTIVITY CONTENT RELEAS'EO OF RELEASE AMOUNT OF ACTIVITY EKI~Q ufp 7 8 9 IO 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION A3~00 0 Q31 Z Qss N/0 7&9 11 12 13 PERSONNEI.
CC O'C Office of Xnspection and Enforcement                               ~cn;a Region XX                                                           j>1 Kl 230 Peachtree Street~ Ef.> Suite 12l7 CD AtLanta, Georgia 30303                                               C7 rcc CA Deax Mr. O'Re~:
INJURIES 45 N/A ,f LOCATION OF RELEASE h'IETHOD DF DISCOVERY DISCOVERY DESCRIPTION
2-I
~BQ31 Nozmal maintenance 45 46 80 80 80 7 8 9 7 8 o 8 9 11 12 LOSS OF OR DAMAGE TO FACIUTY 43 9 Io PUBLICITY IS" UED DESCRIPTION
  'KINESSEE VAXL1KAVKORXTY          BEES     XZRHY IjlUCLEAR PXAIG UNXT DOCKET NO   50 260 + PACXXZTY OPEHATIKr LICENSE DPR+52         REPORTAKE OCCURRENCE REPORT 3PRO   50-260/786 ghe enclosed   report provides details concerning check valve 2-73-603 in the high-pressure coolant injection system that was found in open position during the maintenance inspection after failing a local leds rate test.
~5~N Qnn 9 10 NAME OF PREPARER N/A 68 69 PHONE: NRC USE ONLY 80 BO 2 80 0
Tbis xeport is submitted in accox'dance srlth 3h'cans Perry unit 2 Technical Spec9.fications, Section 6.7.2.'b. (2) .
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Very tr~ yours, TENNESSEE VAIZZY AUTHORXTY E. 8. Pox Director of   Power Production Enclosure (3}
BFBO-50~260 786+a a+~~~II~y  
cc (Enclosure):
Director Office of Management Xnformation       and Program Control U.S. Nuclear Regulatory Commission Washington, DC 20555 Director {40}
Office of Xnspection and. Enforcement U.S. Nuclear Regulator Comission Washington,'DC     20555 781300004 An Equal Opportunity Employer
 
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      .771 LfCENSEE EVENT REPORT
              , p CONTRO'-. SLOE:                                                                 IPLEASE PRINT OR TYPE                         EQUIRED INFORMATION) 6 O     1 8      9 A   L     B     R LICENSEE CODE P     2 14 P2 15 0     0   -     0     0     0 LICENSE NUhlBER 0   0         0     0 26 Qs 26 fp   1     1 LICENSE TYPE 1     1 30 Qn~ Q 57 CAT 68 CON'T
                          "     "                       0     5     0     0   0     2     6     0 07       0   3     2     5     7     8             0       5     0   5   7     8 09 o    1 SOURCE       ~LQs                                                                                                          8 8                      60           61             DOCK ET N Vhi 8 E R           68     69         EVENT DATE                 74     76         REPORT DATE         80 EVENT DESCRIPTION ANO PROBABI.E CONSEQUENCES 010 o     2           Following failure of local leak x'ate test (Reference Technical Specifications performed
  ~O3                   4. 7 .A. 2 . g and h) va lve maintenance                               was                         . During the maintenance inspection~
check valve 2"73-603pin                           high~       zesusezcoolant                injection             systempwas               Bound     in   open position.             A   redundant valve was operable.                               'Zhere was no hazard                       to the         T7ublic     health 6           or safety.               (See attached               sheet. )
  ~O8 7           8 9                                                                                                                                                                               80 SYSTEM               CAUSE         CAUSE                                                               COMP.             VALVE CODE                 CODE       SUBCODE,                   COMPONENT CODE                       SVBCODE             SUBCODC
                                        ~CE             Q11       ~B     Q12   ~C       Q13       V     A   L V           E   E     Q14       ~C     Qns       ~A Qs 7           8                         9           1O                         12               13                                   18           I9               20 SEQUENTIAL                               OCCURRENCE
                                                                                                                                            'YPE    REPORT                       REVISION QET LERIRO REPoRT EVENT YEAR
                                          ~7/                     ~             ~00 REPORT NO.
6           ~~               ~03 CODE
                                                                                                                                                      ~L NO.
                                                                                                                                                                                    ~0
                                                                                                                                                                      '4 21         22         23           24               26         27               28         29           30               31           32 ACTION FUTURE                   EFFECT           SHUTDOWN                                     ATTACHhlENT               NPRD4         PRIhlE COMP,               COMPONENT TAKEN ACTION                   GN PLANT           hIETHOD                   HOURS 022         SUBMITTED             FORM BVB.           SUPPLIER             hlANUFACTURER
                    ~Bpls ~Zpfs                     ~ZQ20             '~ZQ21               0   0     0   0         ~Yfp23               ~NQ24             ~NQ29               0 2       6 Qs 33         34                 35                 36               31                   40     41                   42                 43                               47 CAUSE OESCRIPTION ANO CORRECTIVE ACTIONS 27 o           The cause           of the         open     position         was a     dimensional errox in component interference clearance.               The     corrective action t'aken                       was   to machine the valve component to provide interference clearance.                                                                     ~   I 3
The   valve data is: Nfg: Crane                             Chapman       .'ize;           20     inch. Type: Swing check; 4             Rating l50 lb               ~
7           8     9                                                                                                                                                                           80
                                  ~ps FACILITY '                                                                          h'IETHOD DF STATUS                 POWER                         OTHER STATUS                 DISCOVERY                                    DISCOVERY DESCRIPTION 1     5         NQ    28       0     0     0         9           N/A                             ~BQ31 45        46 Nozmal maintenance 80 ACTIVITY         CONTENT                                                                                                                         ,f RELEAS'EO OF RELEASE                           AMOUNTOF ACTIVITY                                                                LOCATION OF RELEASE EKI 7          8      9
                      ~
Q ufp   IO                                                         44             45 N/A PERSONNEL EXPOSURES NUMBER               TYPE         DESCRIPTION A3
                  ~00             0   Q31     Z   Qss                 N/0 7           &     9                 11       12           13                                                                                                                                   80 PERSONNEI. INJURIES 7           8     9                 11       12                                                                                                                                               80 LOSS OF OR DAMAGE TO FACIUTY 43 9
7          8    9            Io                                                                                                                                                             BO PUBLICITY
                                                ~5                                                                                                                          NRC USE ONLY IS" UED       DESCRIPTION                             N/A o        ~N     Qnn 2
8    9           10                                                                                                                           68      69                        80 0
NAME OF PREPARER                                                                                             PHONE:
 
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==SUMMARY==
==SUMMARY==
OF VALVE 2-73-603 ON UNIT 2 FAILURE TO CLOSE Following failure of local leak rate test (Reference Technical Specifications 4.7.A.2.g and h)valve maintenance was performed.
OF VALVE     2-73-603 ON UNIT 2 FAILURE TO CLOSE Following failure of local leak rate test             (Reference Technical Specifications 4.7.A.2.g     and h) valve maintenance     was performed. During maintenance inspection of high-pressure injection coolant system,           check valve 2-73-603 was found   in open position.       Investigation found the       cause of failuxe to   be a mechanical interference between       t'e end caps and   t'e hinge pin.
During maintenance inspection of high-pressure injection coolant system, check valve 2-73-603 was found in open position.Investigation found the cause of failuxe to be a mechanical interference between t'e end caps and t'e hinge pin.Coxrective action was taken by machining the end caps to provide an interference clearance.
Coxrective action       was taken by machining the end caps to provide an interference clearance.       Following corrective action, the valve operability was checked and found wi.thin acceptable       limi,ts.
Following corrective action, the valve operability was checked and found wi.thin acceptable limi,ts.It should be noted another valve FCV 2-73-23, which was operable, is upstream of the valve in question.Under this consideration no apparent safety function was inhibi.ted.
It should     be noted another valve     FCV 2-73-23, which was operable, is upstream of the valve in question.           Under this consideration     no apparent safety function was   inhibi.ted.
JGD: SGS s/s/78}}
JGD: SGS s/s/78}}

Revision as of 13:55, 20 October 2019

LER 1978-006-00 for Browns Ferry Nuclear Plant, Unit 2, Check Valve 2-73-603 in High-Pressure Coolant Injection System Was Found in Open Position During Maintenance Inspection After Failing Local Leak Rate Test
ML18283A992
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 05/05/1978
From: Fox H
Tennessee Valley Authority
To: O'Reilly J
NRC/IE, NRC/RGN-II
References
LER 1978-006-00
Download: ML18283A992 (8)


Text

REGULATORY INFORNATION DISTRIBUTION SYSTEM (RIDS)

DISTRIBUTION FOR INCOMING MATERIAL 50-260 REC: OREILLY J P ORG: FOX H S. DOCDATE: 05/05/78 NRC TN VALLEY AUTH DATE RCVD: 05/09/78 DOCTYPE: LETTER NOTARIZED: NO COPIES RECEIVED

SUBJECT:

LTR i LICENSEE EVENT REPT 078-006 ON 3/25/78 CONCERNING CHECK VALVE 2-73-603 IN ENCL i HIGH-PRESSURE COOLANT INJECTION SYSTEI"l WAS FOUND IN OPEN POSITION RESULTS NO HAZARD TO PUBLIC HEALTH OR SAFETY.

PLANT NAME: BROWNS FERRY UNIT 2 REVIEWER INITIAL: XRS DISTRIBUTOR INITIAL:

ssss+w+++>++~~++w+4~~~ DISTRIBUTION OF THIS MATERIAL IS AS FOLLOWS INCIDENT REPORTS

( DISTRIBUTION CODE A002)

FOR ACTION: BR CHIEF LEAR 4W/4 ENCL INTERNAL: EG FILE++M/E CL NRC PDR+4M/ENCL NIPC++W/3 ENCL SCHROEDER/I PPOL I TO4 +W/ENCL HOUSTON++M/ENCL NOVAK/CHECK++M/ENCL EEB+~~W/ENCL KN I GHT<4 W/ENCL BUTLER+4W/ENCI HANAUER4+W/ENCL TEDESCO>~W/ENCL E I SENHUT+4 W/ENCL BAER++W/ENCL SHAG+>W/ENCL VOLLEYER/BUNCH++W/ENCL KREGER/J. COLL INS~4l VENCL ROSA++M/ENCL K SEYFRIT/IE++W/ENCL EXTERNAL: LPDR S ATHENS AL+<W/ENCL TIC++W/ENCL I

NS C4~4~W/ENCL ACRS CAT B+>W/ih ENCL PFR COPIES NOT SUB~IITXED

~

REGULATORY GUIDE 10.1 DISTRIBUTION: LTR 45 ENCL 45 CONTROL NBR: 78i300004 SIZE: iP+2P HHf+%0l+%%%%+SHHM%%%%%%%%%%%%%%%%%%%% THE END

I I -e>>

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TENNESSEE VALLEY AUTHORITY GHATTANooGA. TENNEssEE 37401 MAY q )978 r v:,

Mr. J'ames P. O'Really, Director U.S. Nuclear Regulatory Commission j~:

MOP~

CC O'C Office of Xnspection and Enforcement ~cn;a Region XX j>1 Kl 230 Peachtree Street~ Ef.> Suite 12l7 CD AtLanta, Georgia 30303 C7 rcc CA Deax Mr. O'Re~:

2-I

'KINESSEE VAXL1KAVKORXTY BEES XZRHY IjlUCLEAR PXAIG UNXT DOCKET NO 50 260 + PACXXZTY OPEHATIKr LICENSE DPR+52 REPORTAKE OCCURRENCE REPORT 3PRO 50-260/786 ghe enclosed report provides details concerning check valve 2-73-603 in the high-pressure coolant injection system that was found in open position during the maintenance inspection after failing a local leds rate test.

Tbis xeport is submitted in accox'dance srlth 3h'cans Perry unit 2 Technical Spec9.fications, Section 6.7.2.'b. (2) .

Very tr~ yours, TENNESSEE VAIZZY AUTHORXTY E. 8. Pox Director of Power Production Enclosure (3}

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Director Office of Management Xnformation and Program Control U.S. Nuclear Regulatory Commission Washington, DC 20555 Director {40}

Office of Xnspection and. Enforcement U.S. Nuclear Regulator Comission Washington,'DC 20555 781300004 An Equal Opportunity Employer

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.771 LfCENSEE EVENT REPORT

, p CONTRO'-. SLOE: IPLEASE PRINT OR TYPE EQUIRED INFORMATION) 6 O 1 8 9 A L B R LICENSEE CODE P 2 14 P2 15 0 0 - 0 0 0 LICENSE NUhlBER 0 0 0 0 26 Qs 26 fp 1 1 LICENSE TYPE 1 1 30 Qn~ Q 57 CAT 68 CON'T

" " 0 5 0 0 0 2 6 0 07 0 3 2 5 7 8 0 5 0 5 7 8 09 o 1 SOURCE ~LQs 8 8 60 61 DOCK ET N Vhi 8 E R 68 69 EVENT DATE 74 76 REPORT DATE 80 EVENT DESCRIPTION ANO PROBABI.E CONSEQUENCES 010 o 2 Following failure of local leak x'ate test (Reference Technical Specifications performed

~O3 4. 7 .A. 2 . g and h) va lve maintenance was . During the maintenance inspection~

check valve 2"73-603pin high~ zesusezcoolant injection systempwas Bound in open position. A redundant valve was operable. 'Zhere was no hazard to the T7ublic health 6 or safety. (See attached sheet. )

~O8 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE, COMPONENT CODE SVBCODE SUBCODC

~CE Q11 ~B Q12 ~C Q13 V A L V E E Q14 ~C Qns ~A Qs 7 8 9 1O 12 13 18 I9 20 SEQUENTIAL OCCURRENCE

'YPE REPORT REVISION QET LERIRO REPoRT EVENT YEAR

~7/ ~ ~00 REPORT NO.

6 ~~ ~03 CODE

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'4 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHhlENT NPRD4 PRIhlE COMP, COMPONENT TAKEN ACTION GN PLANT hIETHOD HOURS 022 SUBMITTED FORM BVB. SUPPLIER hlANUFACTURER

~Bpls ~Zpfs ~ZQ20 '~ZQ21 0 0 0 0 ~Yfp23 ~NQ24 ~NQ29 0 2 6 Qs 33 34 35 36 31 40 41 42 43 47 CAUSE OESCRIPTION ANO CORRECTIVE ACTIONS 27 o The cause of the open position was a dimensional errox in component interference clearance. The corrective action t'aken was to machine the valve component to provide interference clearance. ~ I 3

The valve data is: Nfg: Crane Chapman .'ize; 20 inch. Type: Swing check; 4 Rating l50 lb ~

7 8 9 80

~ps FACILITY ' h'IETHOD DF STATUS POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION 1 5 NQ 28 0 0 0 9 N/A ~BQ31 45 46 Nozmal maintenance 80 ACTIVITY CONTENT ,f RELEAS'EO OF RELEASE AMOUNTOF ACTIVITY LOCATION OF RELEASE EKI 7 8 9

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Q ufp IO 44 45 N/A PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION A3

~00 0 Q31 Z Qss N/0 7 & 9 11 12 13 80 PERSONNEI. INJURIES 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACIUTY 43 9

7 8 9 Io BO PUBLICITY

~5 NRC USE ONLY IS" UED DESCRIPTION N/A o ~N Qnn 2

8 9 10 68 69 80 0

NAME OF PREPARER PHONE:

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SUMMARY

OF VALVE 2-73-603 ON UNIT 2 FAILURE TO CLOSE Following failure of local leak rate test (Reference Technical Specifications 4.7.A.2.g and h) valve maintenance was performed. During maintenance inspection of high-pressure injection coolant system, check valve 2-73-603 was found in open position. Investigation found the cause of failuxe to be a mechanical interference between t'e end caps and t'e hinge pin.

Coxrective action was taken by machining the end caps to provide an interference clearance. Following corrective action, the valve operability was checked and found wi.thin acceptable limi,ts.

It should be noted another valve FCV 2-73-23, which was operable, is upstream of the valve in question. Under this consideration no apparent safety function was inhibi.ted.

JGD: SGS s/s/78