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Category:Deficiency Report (per 10CFR50.55e and Part 21)
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[Table view] Category:Deficiency Correspondence (per 10CFR50.55e and Part 21)
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Text
10CFR21.21 April 15, 2013
U.S. Nuclear Regulatory Commission ATTN: Document Control Desk
Washington, DC 20555-0001
Limerick Generating Station, Units 1 and 2 Facility Operating Licens e Nos. NPF-39 and NPF-85 NRC Docket Nos. 50-352 and 50-353
Subject:
Part 21 Notification Due To Pump Defect
This 10 CFR Part 21 30-day written report no tification is due to receipt of a pump assembly with incorrectly sized impellers.
The impellers of the replacement pump assembly were not machined to the purchase order specifications.
On Thursday, February 21, 2013, the post maintenance test was performed following replacement of the 0C RHR Service Water pump. Hydraulic performance
of the new pump was approx imately 16% (40 feet) greater than the design specification and resulted in motor current exceeding the motor full load rating by approximately 6.5% at the system design flow rate.
The initial notification to the NRC Operat ions Center (Event Number 48824) was completed on March 15, 2013. This repor t is being submitted pursuant to the requirements of 10CFR21.21(d)(3)(ii).
There are no regulatory commitments contained in this letter.
If you have any questions, please contact Robert B. Dickinson at (610) 718-3400.
Respectfully, Original signed by
Thomas J. Dougherty
Vice President - Lime rick Generating Station Exelon Generation Company, LLC
cc: Administrator Region I, USNRC USNRC Senior Resident Inspector, LGS
- Thirty-Day Part 21 Repor t In Accordance With 10 CFR 21.21(d)(3)(ii)
Thirty-Day Part 21 Report In Accordance Attachment 1 With 10CFR21.21(d)(3)(ii) Page 1 of 3 (i) Name and address of the individual or individuals informing the Commission.
Thomas J. Dougherty Vice President - Lime rick Generating Station 3146 Sanatoga Road Pottstown, PA. 19464
(ii) Identification of the fac ility, the activity, or the bas ic component supplied for such facility or such activity within the United St ates which fails to comply or contains a defect.
Limerick Generating Station, Units 1 and 2 Facility Operating Licens e Nos. NPF-39 and NPF-85 NRC Docket Nos. 50-352 and 50-353
Basic component Cont aining Defect:
Flowserve Corporation Pump Model Number 28KXL - 2 STG Replacement RHRSW pump assembly (minus discharge head).
(iii) Identification of the fi rm constructing the facility or supplying the basic component which fails to comply or contains a defect.
Purchase Order Location Flowserve Corporation Pump Parts Regional Services
Scranton, PA
Manufacturing Facility Location
Flowserve Corporation
Vernon, CA
(iv) Nature of the defect or failure to co mply and the safety hazar d which is created or could be created by such defect or failure to comply.
Nature of the defect:
Replacement RHRSW pump assembly was furnished with incorrectly sized
impellers. Following the failed post inst allation test for the replacement pump, the pump manufacturer, Flowserve, c onfirmed that the replacement pump had been furnished with impellers at full diam eter (20-11/16 inches) versus the required trim diameter (19-1/16 inches). This deviation to the RHRSW pump purchase specification is defined as the basic component defect.
Thirty-Day Part 21 Report In Accordance Attachment 1 With 10CFR21.21(d)(3)(ii) Page 2 of 3 Safety Hazard:
Ability of RHRSW loop to mitigate a design basis accident could be compromised by the replacement RHRSW pump, if installed.
(v) The date on which the information of such defect or failure to comply was obtained.
The defective pump assembly was receiv ed from Flowserve in December 2012. The post maintenance test that reveal ed the defect occurred on February 21, 2013.
(vi) In the case of a basic component which contains a defect or fails to comply, the number and location of these components in use at, supplied for, being supplied for, or may be supplied for, manufactured, or being m anufactured for one or more facilities or activities subject to the regulations in this part.
At the time of discovery, in addition to the tested r eplacement pump, there were two additional replacement RHRSW pump assemblies that were confirmed to be defective (incorrect size impellers). One of the additional pumps was removed from storage in a Virginia warehouse, reworked by Flowserve to eliminate the defect and supplied to Limerick on Februar y 28, 2013. The other additional pump had not yet been shipped from Flowse rve's Vernon, CA facility.
(vii) The corrective action which has been, is being, or will be taken; the name of the individual or organization responsible for t he action; and the length of time that has been or will be taken to complete the action.
Following discovery of the defective pump assembly during post maintenance testing on February 21, 2013, the defecti ve pump assembly was removed and returned to the manufacturer. One of the two additional pump assemblies bearing the same defect was reworked by the manufacturer to install correctly sized impellers and was furnished to Limerick to support the site's Technical Specification Limiting Condition for Operation completion ti me. The 0C RHRSW pump was returned to operable status on March 2, 2013.
The supplier entered this event into their internal corrective action system and
determined root causes and resolutions wit h detailed actions that are focused on precluding recurrence of this condition. Additional Quality Control checks will be added by the supplier and additional purchase order technical requirements will be added by Limerick for future pump orders in order to prevent reoccurrence.
Thirty-Day Part 21 Report In Accordance Attachment 1 With 10CFR21.21(d)(3)(ii) Page 3 of 3 (viii) Any advice related to the defect or failure to comply about the facility, activity, or basic component that has been, is being, or will be given to purchasers or licensees.
None (ix) In the case of an early site permit, the entities to whom an early site permit was transferred.
This event does not involve an early site permit.