ML17266A217: Difference between revisions

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| issue date = 06/10/1980
| issue date = 06/10/1980
| title = LER 80-023/03L-0:on 800511,during Power Ascension,Control Element Assemblies 19 & 58 Dropped to Full Insertion.Caused by Failure of 15-volt Power Supply Units.Both Control Element Assemblies Were Restored
| title = LER 80-023/03L-0:on 800511,during Power Ascension,Control Element Assemblies 19 & 58 Dropped to Full Insertion.Caused by Failure of 15-volt Power Supply Units.Both Control Element Assemblies Were Restored
| author name = SCHOPPMAN M A
| author name = Schoppman M
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  

Revision as of 02:50, 19 June 2019

LER 80-023/03L-0:on 800511,during Power Ascension,Control Element Assemblies 19 & 58 Dropped to Full Insertion.Caused by Failure of 15-volt Power Supply Units.Both Control Element Assemblies Were Restored
ML17266A217
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 06/10/1980
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17208A733 List:
References
LER-80-023-03L, LER-80-23-3L, NUDOCS 8006230495
Download: ML17266A217 (2)


Text

~~-+,~e~I e NRC PORM SSS IT 771 LICENSEE EVENT REPORT U S NUCLEAR RlfCULATORY COIIIIIIISSIOH

~[001]7 CON Y~o 0 i CON YROL SLOCICI l I I I.ls L Si1 lQz 9 LICENSEE CQQE Ql IPLEAsK PRINT OR TYP AI L, O'EcvIAKo IHPORI4ATIQNI 0f OI0 I Ot-'i I II..ill IQeI~Qe 15 6 LIC~seef 4 TTPS Jo 51~e 56 UCSNSK:IIeMd KA f 1 1t 8 I 0'QK 0 6 1 I 0 I8 10 Qs RKPCAT QA.3 30 I4 15 4VKNT QATK in ful'":*iL'0~""'O~60 61 COCEATNUMSKII 66 67 sVKNYOKSCRIPY!ON

'NO PROSAgl K CC,'IscCU~VCES QIP ower a c.a'n 1a corda le was initiated with reactor ower a The ow"r su ly, unit for CHA 19 had failed.The ower su77.v T a~os re'l c CEA 19 was ali ned with its CEA roun hei ht.On 5-11-80 CEA 58 drc77oed.Ao ro riate act on was taken a d E 8 1 P~07 I.6-.c rouTI osition.Similar occurrences were re or ed as I,EP~ps 335-76-37.

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