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| {{#Wiki_filter:OPSEG* Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit AUG 131996 LR-N96237 U. s. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen: | | {{#Wiki_filter:OPSEG* Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit AUG 131996 LR-N96237 U. s. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen: |
| LER 272/96-014-004 SALEM GENERATING STATION -UNIT 1 FACILITY OPERATING LICENSE NO. DPR-70 DOCKET NO. 50-272 This Licensee Event Report entitled Hydrogen Embrittlement on 4KV Breaker Parts" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50.73(a) | | LER 272/96-014-004 SALEM GENERATING STATION -UNIT 1 FACILITY OPERATING LICENSE NO. DPR-70 DOCKET NO. 50-272 This Licensee Event Report entitled Hydrogen Embrittlement on 4KV Breaker Parts" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50.73(a) |
| (2) (i) (B). Attachment SORC Mtg. 96-106 DVH/tcp c LER File 3.7 1 .:* ,1 n '""' 9 .l. 0 \_, '-' ( 9608200207 PDR ADOCK s 960816 05000272 PDR TI1C power is in hands. Sincerely, ao (. Jfv)m-v David F. | | (2) (i) (B). Attachment SORC Mtg. 96-106 DVH/tcp c LER File 3.7 1 .:* ,1 n '""' 9 .l. 0 \_, '-' ( 9608200207 PDR ADOCK s 960816 05000272 PDR TI1C power is in hands. Sincerely, ao (. Jfv)m-v David F. |
| General Manager -Salem Operations | | General Manager -Salem Operations |
| _..:, . 95-2168 REV. 6 '94 Document Control Desk LR-N96237 Attachment A The following represents the commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (272/96-014-004). | | _..:, . 95-2168 REV. 6 '94 Document Control Desk LR-N96237 Attachment A The following represents the commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (272/96-014-004). |
| The commitments are as follows: 1. Removed all NL! refurbished breakers, except 2B4D, from vital loads. Breaker 2B4D will be removed when its loads are available to be transferred to another bus. 2. A QA stop work order was issued to NL! on July 26, 1996. 3. The circuit breakers will be removed for replacement and refurbishment. | | The commitments are as follows: 1. Removed all NL! refurbished breakers, except 2B4D, from vital loads. Breaker 2B4D will be removed when its loads are available to be transferred to another bus. 2. A QA stop work order was issued to NL! on July 26, 1996. 3. The circuit breakers will be removed for replacement and refurbishment. |
| This will be completed for each breaker prior to that breaker being required to be operable. | | This will be completed for each breaker prior to that breaker being required to be operable. |
| : 4. Further corrective actions will be taken as a result of the root cause evaluation currently being conducted. | | : 4. Further corrective actions will be taken as a result of the root cause evaluation currently being conducted. |
| Significant corrective actions that affect the discussion in this LER, if any, will be reported in a supplement to this LER. | | Significant corrective actions that affect the discussion in this LER, if any, will be reported in a supplement to this LER. |
| NRCFORM 366 U.S.NU AR REGULATORY COMMISSION ROVED BY OMB NO. 3150-0104 (4-95) EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS. LtCENSEE EVENT REPORT (LER) REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY. | | NRCFORM 366 U.S.NU AR REGULATORY COMMISSION ROVED BY OMB NO. 3150-0104 (4-95) EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS. LtCENSEE EVENT REPORT (LER) REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY. |
| FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION reverse for re"qulred number of AND RECORDS MANAGEMENT BRANCH (T-G NUCLEAR REGULATORY 0 COMMISSION, WASHINGTON, DC . , AND TO digits/characters for each block) THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. FACILITY NAllE (1) DOCKET NUllBER (2) PAGE(3) SALEM GENERATING STATION, UNIT 1 05000272 1 OF 4 TITLE (4) Potential Hydrogen Embrittlement on 4KV Breaker Parts EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) YEAR I FACILITY NAME DOCKET NUMBER MONTH DAY YEAR SEQUENTIAL I REVISION MONTH DAY YEAR NUMBER NUMBER Salem unit2 05000311 07 17 96 96 014 00 08 16 96 FACILITY NAME DOCKET NUMBER --05000 OPERATING N THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11) MODE(9) 20.2201(b) 20.2203(a)(2)(v) x 50. 73(a)(2)(i) | | FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION reverse for re"qulred number of AND RECORDS MANAGEMENT BRANCH (T-G NUCLEAR REGULATORY 0 COMMISSION, WASHINGTON, DC . , AND TO digits/characters for each block) THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. FACILITY NAllE (1) DOCKET NUllBER (2) PAGE(3) SALEM GENERATING STATION, UNIT 1 05000272 1 OF 4 TITLE (4) Potential Hydrogen Embrittlement on 4KV Breaker Parts EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) YEAR I FACILITY NAME DOCKET NUMBER MONTH DAY YEAR SEQUENTIAL I REVISION MONTH DAY YEAR NUMBER NUMBER Salem unit2 05000311 07 17 96 96 014 00 08 16 96 FACILITY NAME DOCKET NUMBER --05000 OPERATING N THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11) MODE(9) 20.2201(b) 20.2203(a)(2)(v) x 50. 73(a)(2)(i) |
| : 50. 73(a)(2)(viii) | | : 50. 73(a)(2)(viii) |
| POWER 0 20.2203(a)(1) 20.2203(a)(3)(i) | | POWER 0 20.2203(a)(1) 20.2203(a)(3)(i) |
| : 50. 73(a)(2)(ii) | | : 50. 73(a)(2)(ii) |
| : 50. 73(a)(2)(x) | | : 50. 73(a)(2)(x) |
| LEVEL (10) 20.2203(a)(2)(i) 20.2203(a)(3)(ii) | | LEVEL (10) 20.2203(a)(2)(i) 20.2203(a)(3)(ii) |
| : 50. 73(a)(2)(iii) 73.71 -20.2203(a)(2)(ii) 20.2203(a)(4) | | : 50. 73(a)(2)(iii) 73.71 -20.2203(a)(2)(ii) 20.2203(a)(4) |
| : 50. 73(a)(2)(iv) x OTHER 20.2203(a)(2)(iii) 50.35( c )( 1) 50. 73(a)(2)(v) | | : 50. 73(a)(2)(iv) x OTHER 20.2203(a)(2)(iii) 50.35( c )( 1) 50. 73(a)(2)(v) |
| Abstnict below or in C Form 366A 20.2203(a)(2)(iv) 50.36(c)(2) | | Abstnict below or in C Form 366A 20.2203(a)(2)(iv) 50.36(c)(2) |
| : 50. 73(a)(2)(vii) | | : 50. 73(a)(2)(vii) |
| Part 21 LICENSEE CONTACT FOR THIS LER (12) NAME TELEPHONE NUMBER (Include Area Coda) Dennis v. Hassler, LER Coordinator 609-339-1989 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE I CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS TONPRDS !llllll1:illl:iii: | | Part 21 LICENSEE CONTACT FOR THIS LER (12) NAME TELEPHONE NUMBER (Include Area Coda) Dennis v. Hassler, LER Coordinator 609-339-1989 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE I CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS TONPRDS !llllll1:illl:iii: |
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| The health and safety of the public were not affected by this occurrence. | | The health and safety of the public were not affected by this occurrence. |
| CORRECTIVE ACTIONS 1. Removed all NLI refurbished breakers, except 2B4D, from vital loads. Breaker 2B4D will be removed when its loads are available to be transferred to another bus. 2. A QA stop work order was issued to NLI on July 26, 1996. 3. The circuit breakers will be sent for replacement and refurbishment. | | CORRECTIVE ACTIONS 1. Removed all NLI refurbished breakers, except 2B4D, from vital loads. Breaker 2B4D will be removed when its loads are available to be transferred to another bus. 2. A QA stop work order was issued to NLI on July 26, 1996. 3. The circuit breakers will be sent for replacement and refurbishment. |
| This will be completed for each breaker prior to that breaker being required to be operable. | | This will be completed for each breaker prior to that breaker being required to be operable. |
| : 4. Further corrective actions will be taken as a result of the root cause evaluation currently being conducted. | | : 4. Further corrective actions will be taken as a result of the root cause evaluation currently being conducted. |
| Significant corrective actions that affect the discussion irthis LER, if any, will be reported in a supplement to this LER. 10CFR21 REPORTING 10CFR21 reporting requirements are met by this LER. NRC FORM 366A (4-95) J}} | | Significant corrective actions that affect the discussion irthis LER, if any, will be reported in a supplement to this LER. 10CFR21 REPORTING 10CFR21 reporting requirements are met by this LER. NRC FORM 366A (4-95) J}} |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
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[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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OPSEG* Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit AUG 131996 LR-N96237 U. s. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
LER 272/96-014-004 SALEM GENERATING STATION -UNIT 1 FACILITY OPERATING LICENSE NO. DPR-70 DOCKET NO. 50-272 This Licensee Event Report entitled Hydrogen Embrittlement on 4KV Breaker Parts" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50.73(a)
(2) (i) (B). Attachment SORC Mtg.96-106 DVH/tcp c LER File 3.7 1 .:* ,1 n '""' 9 .l. 0 \_, '-' ( 9608200207 PDR ADOCK s 960816 05000272 PDR TI1C power is in hands. Sincerely, ao (. Jfv)m-v David F.
General Manager -Salem Operations
_..:, . 95-2168 REV. 6 '94 Document Control Desk LR-N96237 Attachment A The following represents the commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (272/96-014-004).
The commitments are as follows: 1. Removed all NL! refurbished breakers, except 2B4D, from vital loads. Breaker 2B4D will be removed when its loads are available to be transferred to another bus. 2. A QA stop work order was issued to NL! on July 26, 1996. 3. The circuit breakers will be removed for replacement and refurbishment.
This will be completed for each breaker prior to that breaker being required to be operable.
- 4. Further corrective actions will be taken as a result of the root cause evaluation currently being conducted.
Significant corrective actions that affect the discussion in this LER, if any, will be reported in a supplement to this LER.
NRCFORM 366 U.S.NU AR REGULATORY COMMISSION ROVED BY OMB NO. 3150-0104 (4-95) EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS. LtCENSEE EVENT REPORT (LER) REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION reverse for re"qulred number of AND RECORDS MANAGEMENT BRANCH (T-G NUCLEAR REGULATORY 0 COMMISSION, WASHINGTON, DC . , AND TO digits/characters for each block) THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. FACILITY NAllE (1) DOCKET NUllBER (2) PAGE(3) SALEM GENERATING STATION, UNIT 1 05000272 1 OF 4 TITLE (4) Potential Hydrogen Embrittlement on 4KV Breaker Parts EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) YEAR I FACILITY NAME DOCKET NUMBER MONTH DAY YEAR SEQUENTIAL I REVISION MONTH DAY YEAR NUMBER NUMBER Salem unit2 05000311 07 17 96 96 014 00 08 16 96 FACILITY NAME DOCKET NUMBER --05000 OPERATING N THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11) MODE(9) 20.2201(b) 20.2203(a)(2)(v) x 50. 73(a)(2)(i)
- 50. 73(a)(2)(viii)
POWER 0 20.2203(a)(1) 20.2203(a)(3)(i)
- 50. 73(a)(2)(ii)
- 50. 73(a)(2)(x)
LEVEL (10) 20.2203(a)(2)(i) 20.2203(a)(3)(ii)
- 50. 73(a)(2)(iii) 73.71 -20.2203(a)(2)(ii) 20.2203(a)(4)
- 50. 73(a)(2)(iv) x OTHER 20.2203(a)(2)(iii) 50.35( c )( 1) 50. 73(a)(2)(v)
Abstnict below or in C Form 366A 20.2203(a)(2)(iv) 50.36(c)(2)
- 50. 73(a)(2)(vii)
Part 21 LICENSEE CONTACT FOR THIS LER (12) NAME TELEPHONE NUMBER (Include Area Coda) Dennis v. Hassler, LER Coordinator 609-339-1989 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE I CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS TONPRDS !llllll1:illl:iii:
SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY YEAR IYES XINO SUBMISSION (tfyes, complete EXPECTED SUBMISSION DATE). DATE (15) ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) On July 17, 1996 a failure of a roll pin securing a spring for a latch pawl on a 4KV breaker was reviewed and a determination made that the failure of this pin could cause the breaker to fail. Further investigation revealed that the roll pin failed as a result of hydrogen errbrittlement.
The roll pin failure was an unexpected occurrence and consequently determined that this condition could place the plant in an unanalyzed condition.
Later, an issue involving permanently applied lubricant which was inadvertently removed from the breakers was identified.
This also could potentially affect breaker operation.
The cause of the cracked roll pin was the lack of knowledge of plating induced hydrogen errbrittlement.
The Nuclear Logistics Incorporated (NLI) personnel involved in the NLI procedure develoµnent were not aware that zinc plating of hardened steel parts could produce hydrogen embrittlement and subsequent cracking.
The cause of the lubricant being inadvertently rerroved from breaker parts is also due to the lack of knowledge by NLI personnel.
NLI is a PSE&G approved vendor for safety related work. Corrective actions include issuance of a stop work order on NLI's breaker activities and replacement of the affected parts and reapplication of the lubricant.
This event is reportable in accordance with 10 CFR 50.73(a) (2) (ii); any event or condition that resulted in the plant being in an unanalyzed condition and in accordance with 10 CFR 21.2 (c). NRC FORM 366 (4-95)
- NRC FORM 366A (4-95) U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) LER NUMBER (6) 05000272 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER Salem Generating station, Unit 1 96 -014 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) PLANT AND SYSTEM IDENTIFICATION Westinghouse
-Pressurized Water Reactor 4KV Breakers {-/BKR}* PAGE (3) 2 OF 4
- Energy Industry Identification System (EIIS) codes and component function identifier codes appear as (SS/CCC) CONDITIONS PRIOR TO OCCURRENCE At the time of identification, Salem Units 1 and 2 were and defueled.
DESCRIPTION OF OCCURRENCE On July 17, 1996 a failure of a roll pin securing a latch pawl on a 4KV breaker was reviewed and a determination made that the failure of this pin could cause the breaker to fail. Further investigation revealed that the roll pin failed as a result of hydrogen embrittlement.
The roll pin failure was an unexpected occurrence, and consequently determined that this condition could place the plant in an unanalyzed condition.
Public Service Electric & Gas (PSE&G) contracted with Nuclear Logistics Incorporated (NLI) to overhaul/refurbish 4 KV breakers for Salem Units 1 and 2. NLI is a PSE&G approved vendor for safety related work. NLI utilized clear zinc plating on a number of breaker parts that had been heat treated to a hardness of RC 60. The plated areas should have been masked off so that the hardened surfaces were not subjected to the acid and zinc plate baths. Acid cleaning and electroplating generates hydrogen, which can diffuse into the metal. This can result in instant cracking or delayed cracking.
The cracking is not normally dependent on the operating load. On May 1, 1996 a lockwasher holding the breaker lower arc chutes cracked and broke on site. The remainder of the breaker washers were visually checked and no other similar washers were found. The crack appeared to have been caused by hydrogen embrittlement induced when the lockwasher was zinc plated. This condition was reported to the industry through INPO OE 7875 dated June 5, 1996. During the first week of May, the circuit breakers which were at the Texas facility of NLI were inspected and no problems related to plating or lockwashers were found. PSE&G then asked for a corrplete list of breaker parts that were zinc plated. The list was developed but it did not include the roll pins used on the breakers, including the ratchet drive pawl roll pins. During the same time frame, the vendor reported that the ratchet drive pawl in some circuit breakers was chipping.
Efforts then were started to remove all hardened steel parts which were zinc plated by NLI with the intention of replacing them with new unplated parts. When the new parts became unavailable, NLI and PSE&G agreed on an alternate solution to the plating problem: the parts would be heat treated to relieve hydrogen induced stress and reinstalled in the circuit breakers; Both NLI and PSE&G agreed that no further zinc plating would be performed.
Circuit breakers were then delivered to Salem and some were installed in the plant. NRC FORM 366A {4-95)
NRC FORM 366A (4-95) U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) LER NUMBER (6) 05000272 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER Salem Generating Station, Unit 1 96 -014 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) DESCRIPTION OF OCCURRENCE (CONT'D) PAGE (3) 3 OF 4 On July 16, 1995, a ;ircuit breaker in the Salem breaker shop was being tested prior to installation in the plant. A circuit breaker was found to have its inner latch pawl spring hanging down. The latch pawl itself was not engaging -
ratchet wheel. Further inspection revealed that the roll pin that fits inside the bottom of the pawl return spring had broken along its longitude axis. The roll pin that broke normally serves to keep the bottom of the pawl return spring in the proper position.
The support plate in which the roll pin is mounted and the roll pin itself appear to have been plated. Subsequent to the above, an issue involving inadvertently removed lubricant was identified.
This was identified during a visual inspection of an NLI rebuilt circuit breaker. The procedures for refurbishment of 4KV circuit breakers included acid cleaning and zinc plating of some mechanical parts. The original equipment manufacturer design included a lubricant which was baked-on some moving parts. The baked-on lubricant (molybdenum disulfide) was meant to last the life of* the circuit breaker. The molybdenum disulfide is a dry baked-on lubricant that is applied to various rotating and rubbing surfaces on the breaker. This lubricant is applied to mini.rf'ize component wear. The acid cleaning and zinc plating performed by NLI removed the original baked on lubricant.
After the zinc plating of parts was discontinued, the cleaning/polishing process used by NLI still resulted in the removal of the original baked on lubricant.
The effect of the above described problems is that all NLI circuit breakers which had parts zinc plated must be removed from the plant for parts replacement.
There were 15 breakers that were involved in the plating issue, and an additional four breakers involving the inadvertent removal of the lubricant.
Eleven of the 19 breakers were installed in the plant in vital load cubicles.
The buses where these breakers were installed were not operable but were considered available.
One of the 11 installed breakers, 2B4D, is currently installed in a vital application and is supplying loads (e.g. spent fuel pool cooling pump) . At the time the broken roll pins were found, it was not considered prudent, based on existing plant conditions, to remove this breaker. Also, an evaluation determined that failure of the plated roll pins in the breaker would not preclude this breaker from opening/tripping.
A contingency plan has been approved for replacement of this breaker and it is expected to be removed in the near future. CAUSE OF OCCURRENCE The cause of the cracked roll pin was the lack of knowledge of plating induced hydrogen embrittl-=rnent.
The NLI procedure development and ,ent reviews failed to associate zinc plating of hardened steel parts with hydrogen embrittlement.
The NLI personnel involved in the NLI procedure were not aware that zinc plating of hardened steel parts could produce hydrogen embrittlement and the subsequent cracking.
The cause of the lubricant being inadvertently removed from breaker parts is also due to the lack of knowledge by NLI personnel.
NRC FORM 366A (4-95)
!+iRC FORM 366A (4-95) * .,. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) 05000272 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER Salem Generating Station, Unit 1 96 -014 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) PRIOR SIMILAR cx:::cuRRENCES PAGE (3) 4 OF 4 In the past two years, there has been one Salem LER that addressed breaker failures.
LER 272/96-009-00 addressed a potential common mode failure mechanism for 4KV breakers due to of the breaker mechanism.
The plating and lubrication issues discussed in this LER (272/96-014-00) were discovered as a result of the same overhaul work that identified the plating problem discussed above. SAFE'I'Y CONSEQUENCES AND IMPLICATIONS There were no safety consequences for this occurrence since the breaker failures were found while the plant was in a defueled condition and the buses are not operable.
However, the irrplications are that this is a potential common mode failure which could jeopardize the operability of safety related circuit breakers.
The operability of the AC Power Sources insures power will be available to supply safety related equipment.
In the event safety related equipment is required to start, but is prevented from starting due to a single circuit breaker failing, redundant safety equipment would be available.
However, it is possible that during an event, more than one channel of safety related equipment could be affected.
The breaker installed in 2B4D was in the closed position and the roll pin was not cracked or missing. The capability to open or trip the circuit breaker was reviewed and was determined not to be compromised.
The health and safety of the public were not affected by this occurrence.
CORRECTIVE ACTIONS 1. Removed all NLI refurbished breakers, except 2B4D, from vital loads. Breaker 2B4D will be removed when its loads are available to be transferred to another bus. 2. A QA stop work order was issued to NLI on July 26, 1996. 3. The circuit breakers will be sent for replacement and refurbishment.
This will be completed for each breaker prior to that breaker being required to be operable.
- 4. Further corrective actions will be taken as a result of the root cause evaluation currently being conducted.
Significant corrective actions that affect the discussion irthis LER, if any, will be reported in a supplement to this LER. 10CFR21 REPORTING 10CFR21 reporting requirements are met by this LER. NRC FORM 366A (4-95) J