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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20076M086 + (ML20076M086)
- ML20076M094 + (ML20076M094)
- ML20076M099 + (ML20076M099)
- ML20076M100 + (ML20076M100)
- ML20076M103 + (ML20076M103)
- ML20076M107 + (ML20076M107)
- ML20076M114 + (ML20076M114)
- ML20076M122 + (ML20076M122)
- 05000237/LER-1983-020-03, Core Spray Injection Valve Mo 1402-25B Remained Open When Close Signal Given. Caused by Breaker Incorrectly Set Due to Procedure Inadequacy.Breaker Reset + (ML20076M140)
- ML20076M144 + (ML20076M144)
- 05000237/LER-1983-046-03, /03L-0:on 830615,after Using LPCI Sys to Lower Suppression Pool Level,Mo 2-1501-13A Failed to Reopen Upon LPCI Sys Shutdown.Caused by Valve Motor Operator Mounting Bolts Snapping Off.Bolts Replaced & Retorqued + (ML20076M155)
- ML20076M183 + (ML20076M183)
- ML20076M186 + (ML20076M186)
- ML20076M199 + (ML20076M199)
- 05000237/LER-1983-048-03, /03L-0:on 830616,during Reactor Vessel Low Water Level ECCS Initiation (DIS-500-3),level Indicating Switch 2-263-72B Tripped at 111.3 Inches Delta P.Caused by Setpoint Drift.Setpoint Adjusted + (ML20076M210)
- 05000454/LER-1994-010, Informs That LER Number 94-010 from Plant Will Not Be Used + (ML20076M214)
- 05000454/LER-1994-011, Informs That LER Number 94-011 from Plant Will Not Be Used + (ML20076M218)
- ML20076M219 + (ML20076M219)
- ML20076M237 + (ML20076M237)
- ML20076M241 + (ML20076M241)
- ML20076M245 + (ML20076M245)
- ML20076M255 + (ML20076M255)
- ML20076M258 + (ML20076M258)
- ML20076M259 + (ML20076M259)
- ML20076M263 + (ML20076M263)
- ML20076M265 + (ML20076M265)
- ML20076M273 + (ML20076M273)
- ML20076M277 + (ML20076M277)
- ML20076M278 + (ML20076M278)
- ML20076M279 + (ML20076M279)
- ML20076M282 + (ML20076M282)
- ML20076M284 + (ML20076M284)
- 05000249/LER-1983-024-03, /03L-0:on 830615,while Performing Component Cooling Svc Water Pump Test,Pressure Regulating Valve Mo 3-1501-3B Could Not Be Opened Past 50% Using Differential Pressure Controller.Caused by High Resistance + (ML20076M286)
- ML20076M291 + (ML20076M291)
- ML20076M299 + (ML20076M299)
- ML20076M304 + (ML20076M304)
- ST-HL-AE-4917, Submits Eight Responses to RAI Re Compliance W/Station Blackout Requirements + (ML20076M305)
- ML20076M313 + (ML20076M313)
- 05000289/LER-1994-006-01, :on 941002,inadvertent Actuation of EG-Y-1B Occurred Due to Personnel Error.Lead replaced,86B/E Relay Reset & EG-Y-1B Breaker Automatically Closed + (ML20076M316)
- ML20076M330 + (ML20076M330)
- ML20076M335 + (ML20076M335)
- ML20076M337 + (ML20076M337)
- NRC-94-0102, Provides Status of Detroit Edison Initiatives on Pressure Locking & Thermal Binding of Gate Valves + (ML20076M341)
- ML20076M345 + (ML20076M345)
- ML20076M347 + (ML20076M347)
- LIC-94-0198, Discusses Info Re Use of Cecor Power Peaking Uncertainties at Fort Calhoun Station + (ML20076M348)
- ML20076M352 + (ML20076M352)
- ML20076M364 + (ML20076M364)
- ML20076M366 + (ML20076M366)
- ML20076M367 + (ML20076M367)
- ML20076M368 + (ML20076M368)