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 Issue dateTitleTopic
ML20202F91629 January 1998Special Rept:On 980128,two of Three Fire Protection Pumps Were Removed from Svc as Result of Sys Configuration Necessary to Support Planned Maintenance.Fire Pumps Were Returned to Svc on 980128
ML20138F58029 April 1997Special Rept:On 970402,declared Reactor Bldg Wide Range Gas Monitor Inoperable.Caused by Ruptured Pump Diaphragm. Initiated Work Order,Installed Replacement Pump & Declared Pump Operable
ML20137Y21715 April 1997Special Rept:On 961220,util Rail Car Was Released to Burlington Northern Railroad from Monticello Nuclear Plant. Rail Car Was Delayed in Chicago as Result of Problems W/Bill of Lading on Computer Sys.Rail Car Was Delivered on 970131
ML20101E83215 March 1996Special Rept:On 960314,two of Three Fire Pumps Removed from Svc for Planned Mod Work.Returned Both Fire Pumps to Svc Same Day
ML20094E43731 October 1995Special Rept:On 951010,sys Engineer & Technicians Reintiated Work on B Channel of Reactor Bldg Vent Radiation Monitor, After Providing Proper Notification to Main Control Room. Caused by Incorrect Channels Removed from Svc
ML20082R66019 April 1995Special Rept:On 950404,discovered That Manual Isolation Valves for 'A' Channel in Closed Position.Cause of Failure to Correctly Position Valves Will Be Assessed.Valves Placed in Required Position & Demonstrated Operability
ML20082E5666 April 1995Special Rept:On 950326,pump Discharge Relief Valve for Electric Screen Wash/Fire Pump Became Inoperable.Valve Had to Be Secured to Permit Installation of an Isolation Device. Pump Returned to Operational Status After Device Installed
ML20080G4731 February 1995Special Rept:On 950119,two of Three Fire Protection Pumps Out of Svc for Period of Approx 15 H.Action Taken for Planned Preventative Maint on Two Check Valves & Drain Valve in Fire Suppression Sys.Roving Fire Watch EstablishedFire Watch
ML20067D13523 February 1994Special Rept:On 940126,fire Door 105 Declared Inoperable Due to Inability to Close Properly.Caused by Higher than Normal Differential Pressure Between Plant Administration Bldg & Turbine Bldg.Cause of Failure CorrectedFire Barrier
Hourly Fire Watch
ML20117A58024 November 1992Special Rept:On 921020,determined That RHR Sample Supply Loops a & B Excess Flow Check Valves Not Included in ASME Section XI Program.Caused by Lack of Proven Test Procedure. Valves Incorporated Into Third 10-yr ASME Program
ML20082G92615 August 1991Special Rept:On 910719,potential for Inoperable Penetration Fire Barrier Identified.Caused by Use of Less Conservative, But Technically Acceptable,Design Alternatives in Plant Const.Vents Will Be ReroutedFire Barrier
Fire Watch
Hourly Fire Watch
ML20244E59416 June 1989Special Rept:On 890603,two Out of Three Diesel Fire Pumps Were Inoperable for Less than 12 H.Caused by Diesel Fire Pump Day Tank Outlet Valve Being Closed Instead of Fill Valve During Performance Test 1158.Test Revised
ML20081G95625 October 1983Ro:On 831024,trip Coil for Reactor Recirculation Motor Generator Set 11 Drive Breaker Failed to Trip Automatically. Investigation Ongoing.Trip Coil Replaced
ML20066E0131 November 1982Ro:On 821031,thru Wall Defect Found on C 12-inch Recirculation safe-end to Pipe Weld Joint.Resolution Under Investigation
ML20064E51421 October 1982Ro:On 821020,thru Wall Defect Found on E 12-inch Recirculation Sys Safe End to Pipe Weld Joint.Indications Will Be Documented as Revision to RO 82-16 Reported on 820928.Resolution Being Investigated
ML20064E47611 October 1982Ro:On 821009,linear Indications Confirmed to Exist on Three Addl Welds in Recirculation Sys.Indications Will Be Documented as Revision to RO 82-16 Reported on 820928. Resolution Being Investigated
ML20071N43628 September 1982Ro:On 820928,crack Indication in End Cap of a Recirculation Riser Confirmed by Radiography.Indications Initially Detected by Ultrasonic Exam During Normal Inservice Insp. Remedial Measures Under Investigation
ML20071L82616 September 1982Ro:On 820915,leak Discovered on Primary Containment Suppression Chamber Nitrogen Control Sys Inboard Isolation Valve (AO-2378).Leakage Less than Tech Spec Allowable Leakage
ML20053E8072 June 1982RO Iii:On 810224,failure of Discharge Valve on Instrument & Svc Air Compressor Resulted in Loss of Instrument Air Sys Pressure Causing Plant Scram.Failed Check Valve Replaced W/Similar UnitSafe Shutdown
Systematic Assessment of Licensee Performance
ML20058L34331 July 1978Ro:On 780728,control Rod Drive 30-47 Delayed Approx 1.4 Before Scramming.Buna N Disk in Plunger Broken in Pieces.Plungers on 242 Scram Pilot Valves & Two Backup Scram Pilot Valves Removed & Replaced
ML20090L8312 June 1978Ro:On 780505,steam Leak Noted in RCIC Inlet Steam Line & Drain Line to Condenser.Caused by Pinhole Failure on Weld on 300 Lb Socket Weld.Hole Temporarily Patched
ML20091A99410 March 1978Ro:On 780309,smear Survey of Chem Nuclear Sys Inc Model 4-45 Shipping Cask Disclosed Max Surface Contamination of 25,900 Disintegrations Per Min Per 100 Square Centimeters.Cask Will Be Decontaminated
ML20127G6172 February 1978Advises That on 780202,during Surveillance Test,One Suppression Chamber to Drywell Vacuum Breaker Failed to Reclose Following Exercise.Plant Shutdown Initiated
ML20086D5146 January 1978Telecopy Ro:On 780105,discovered That One of Two Nuclear Engineering Co Model B3-1 Shipping Casks Provided w/1-inch Diameter Lid Bolts Rather than 1-1/4 Inch Size Specified in Certificate of Compliance 6058
ML20086D52014 December 1977Telecopy Ro:Heating Steam Coil Leak in Reactor Bldg Ventilation Supply Unit V-AH-4A Resulted in Freezing of Condensate at Inlet to Unit & Subsequent Inoperability of Associated Secondary Containment Isolation Dampers
ML20086D53714 October 1977Telecopy Ro:Insp of Internal Torus Catwalk Support Structure Revealed That Catwalk Mitered Sections Not All Attached to Horizontal Catwalk Support Plates in Some Manner.Attachment Locations Will Be Upgraded
ML20086D55013 October 1977Telecopy Ro:On 771012,local Leak Rate Testing of MSIV AO-2-80A & Nitrogen Instrument Air Sys Isolation Valve CV-7436 Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation
ML20086D5545 October 1977Telecopy Ro:On 771004,local Leak Rate Testing of HPCI Sys Discharge Isolation Check Valve HPCI-9 Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation
ML20086D55729 September 1977Telecopy Ro:On 770929,local Leak Rate Testing of Core Spray Inboard Isolation Check Valve AO-14-13A Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation
ML20086D56114 September 1977Telecopy Ro:On 770913,local Leak Rate Testing of Core Spray Inboard Isolation Check Valve AO 14-13B Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Related Event on 770914
ML20086D56712 September 1977Telecopy Ro:Main Steam Drain Isolation Valve MD 2373 & Main Steam Outboard Isolation Valve AO 2-86A Exceeded Tech Spec Acceptance Criteria for Local Leak Rate Tests
ML20086D64211 July 1977Telecopy Ro:On 770709,determined That Recombiner Sys a Offgas Flow Control Valve PCV 7489A Could Be Opened W/ Controlling Solenoid Valve Deenergized.Valve Held from Svc Pending Investigation
ML20058K6119 March 1977Ro:On 770223,discovered Withdrawal of in-sequence Control Rod Resulted in Period Less than 5-s & IRM Scram
ML20086D6912 March 1977Telecopy Ro:On 770301,torus Water Vol Found to Be Slightly Below Min Vol Established by Tech Specs.Water Vol Restored to Normal Operating Level
ML20086D70324 February 1977Telecopy Ro:On 770223,while Withdrawing in-sequence Control Rod to Bring Reactor Critical,Reactor Period of Less than 5 Obtained
ML20086D78810 September 1976Telecopy Ro:On 760909,discovered That Torus Water Vol Several Hundred Cubic Ft Below 68,000 Cubic Ft Min Required by Tech Specs.Caused by Failure to Correct for Vol Vs Level Correlation
ML20056B85421 May 1976Informs of 760520 Event Involving TIP Bell Valve Which Failed to Properly Close During Operation of TIP Sys.Valve Cleaned,Relubricated & Closure Spring Tension Increased
ML20086D8235 May 1976Telecopy Ro:On 760504,during Routine Surveillance Test, Primary Containment Oxygen Concentration Found to Be in Excess of Tech Spec Limit.Caused by Leakage from Drywell Instrument Air Sys Into Containment Nitrogen Supply Line
ML20127L26122 September 1975Informs of 750921 Incident Re Countrate Decreasing Below 3 Counts Per While Performing Refueling Core Alterations. Countrate Increased & Refueling Operations Recommenced. Further Investigation Continuing
ML20127L27522 September 1975Informs of 750920 Incident Re Drywell Equipment Drain Sump Isolation Valves AO 2561A & B Exceeding TS Acceptance Criteria.Further Investigation Continuing
ML20127L25519 September 1975Informs That on 750919,during Local Leak Rate Testing of MSIVs 2-86A & 2-88A,combined Leakage of Valves Exceeded Acceptance Criteria.Further Investigation Continuing
ML20127L23915 September 1975Informs of 750914 Incident Re Discovery That Hydraulic Shock Suppressor Located Inside Primary Containment on Loop B HPCI Line Inoperable Due to Loss of Oil.Reactor in Cold Shutdown for Refueling.Further Investigation Underway
ML20127L17421 August 1975Discusses 750818 Incident Re Broken Seal Cooling Line at Threaded Connection on Reactor Water Cleanup Pump 12.Pump Immediately Isolated & Line Repaired.Investigation Into Cause of Failure Continuing
ML20127L26528 July 1975Ro:On 750727,operator Motor Failed & Stalled Due to Stalled Rotor Current Overheating Windows.Investigation Pending
ML20127L25214 July 1975Ro:On 750713,small Leak Developed on Local Pressure Gauge Monitoring Reactor Pressure.Root Valve for Pressure Gauge Closed,Allowing Ref Leg to Refill & Water Level Indication to Return to Normal
ML20058L17611 July 1975Ro:On 750624 & 25,10 Initial Core Fuel Assemblies Which Had Been Identified as Leakers & Removed from Core at End of Cycles 2 & 3 Inspected Using Underwater Television
ML20058K6753 July 1975Notifies That on 750703,during Routine Surveillance Testing, Reactor High Pressure Scram Switches Found Inoperable
ML20127B73727 May 1975Ro:On 750525 Core Spray Sys Motor Operated Valve Failed to Reopen by Means of Motorized Operator.Valve Was Returned to Normal Open Position by Local Handwheel
ML20058K6955 May 1975Ro:On 750505,discovered That Control Circuit for Valve Steam Supply to RCIC Turbine Was Deenergized by Motor Control Unit Undervoltage Relay Coil Opening.Coil Replaced & Remote Operability of Valve Demonstrated
ML20127L1471 May 1975RO 75-12:on 750429,surveillance Test for Exercising Unit 2 Containment Vacuum Breaker Isolation Valve CV-31628 Showed Valve to Be Inoperable