Semantic search

Jump to navigation Jump to search
 Issue dateTitleTopic
ML20042E2269 April 1990Special Rept:On 900227,fire Protection Alarm Reporting Sys Inoperable for More than 14 Days.Compensatory Fire Watches Instituted in Affected Areas & Failure & Malfunction Rept 90-44 Written to Document ProblemFire Watch
ML19325E9026 November 1989Special Rept:On 890929,fire Water Supply Sys Storage Tanks Declared Inoperable.Caused by Drained Storage Tank. Fwst (T-107A) Refilled & Declared Operable on 891007
ML20052E18027 April 1982RO 82-011/01X-0:on 820427,review of Water Level Anomaly, Determined That Facility Entered Limiting Condition for Operation W/O Insertion of Control Rods.Special Order 82-04 Will Be Issued 820428 to Prevent RecurrenceHalf scram
ML20050D5851 April 1982Ro 82-008/01x-0:on 820331,HPCI Sys Declared Inoperable Due to Failure of HPCI Injection Valve Mo 2301-8 to Go Full Open During Performance of Surveillance Test 8.I.13. Cause Not Stated.Priority a Maint Request Issued
ML20042A4589 March 1982Telecopy RO 82-006/01X-0:on 820309,HPCI Stop Valve Main Disc Flange Which Should Be Attached to Main Disc by Four Cap Screws Found W/Three Cap Screws Broken.Cause Not Stated. Engineering Support Requested
ML20039E07715 December 1981RO 81-1:on 811208,util Received Analysis Rept from Yankee Atomic Environ Lab Indicating Potentially Reportable Concentration of Co-60 in Irish Moss Sample from Indicator Station.Calculated Doses Not Considered Significant
ML20050C21225 March 1981RO 82-07/01X-0:on 810325,HPCI,reactor Core Isolation Cooling & Reactor Water Cleanup Pipe Excess Flow Isolation Setpoints Set Unconservatively.Caused by Exclusion of plant-specific Parameters from Original Calculation
ML20049A33614 November 1980RO 80-084/01X-0:on 801113,during Repairs to D Msn Discovered Water Leaking from 2 Inch Vessel Drain Line Which Connects to Rwcv Sys.Caused by Defective 2 Inch Pipe Coupling Weld. Leak Isolated & Coupling Rewelded
ML19340B16115 October 1980RO 80-072/01X-0:on 801014,during Steady State Operation,Mgt Review Revealed That Reactor Protection Sys Trip Level Setting Was Miscalibrated to Nonconservative Level.Caused by Calculation Error.Monitors Were Immediately Recalibrated
ML19340B16214 October 1980RO 80-070/01X-0:on 801010,during Steady State operation,480 Volt Breaker B204 Tripped Twice within 10 Minutes, de-energizing 480 Volt Bus B14.Cause Unknown.Bus B14 Was Immediately Returned to Svc by Closing Breaker B204
ML19351D6753 October 1980RO 80-067/01X-0:on 801002,NRC Was Notified That Analytical Reanalysis of RHR Sys B Indicated That as-built Configuration Would Not Remain Functional During Sse.Caused by Design Error.Seismic Anchor Is Being ModifiedSafe Shutdown Earthquake
ML19343A41911 September 1980RO 80-050/01X-0:on 800907,during Surveillance Testing,Diesel Generator Removed from Svc When RBCCW Pump P202D Found Inoperable.Caused by Ambiguous Tech Specs.Tech Specs Will Be Revised to Clarify Limiting Condition of OperationSafe Shutdown
ML19338C4287 August 1980RO 80-036/01X-0:on 800807,found Hourly Fire Check of Auxiliary Offgas Bldg Was Not Performed on Continuous Basis After 800707.Hourly Fire Check Reinitiated,Surveillance Testing Completed & Sys Returned to SvcFire Watch
Hourly Fire Watch
ML19330C51217 July 1980RO 80-29/01X-0:on 800701,during Surveillance Testing to Verify Operability of Oxygen Analyzer Isolation Valves, SV-5065-23 Failed to Meet Acceptance Criteria for Closing Time,Impacting on Operability of Panel C-19Pressure boundary leak
ML19309G6638 March 1980RO 80-008/01X-0:on 800308,two Irradiated Fuel Assemblies Relocated in Spent Fuel Pool,W/Diesel Generators Inoperable & Secondary Containment Not Intact.Caused by Lack of Knowledge Re Core Drilling for Mods.Fuel Movements Stopped
ML19260D4021 February 1980LER 80-004/012-0:during Visual Examination of Core Spray Sparger,Seven Linear Indications Were Recorded.Cause Unstated.Analysis Initiated
ML19257C65624 January 1980RO 80-002/01X-0:during Investigation Following Review of IE Info Notice 79-32,several 125-volt Dc Automatic Depressurization Sys Supply Cables Found Routed in Cable Trays Containing HPCI Control Cables.Problem Being Resolved
ML19257C64723 January 1980RO 80-001/01X-0:fire Hazards Rept Indicated That Fire in Raceways of Facility Cannot Be Tolerated Because Safe Shutdown Would Be Jeopardized.Cause Unstated.Fire Protection Measures Proposed or Being CompletedSafe Shutdown
ML19262B56924 December 1979RO-79-048 on 791224:backup Battery Charger,In Use Due to Main Battery Charger 791223 Failure,Tripped & Could Not Be Reset.Cause Under Investigation.Spare Battery Charger Will Be in Svc by 791224
ML19270H62720 December 1979Ro:On 791211,while Transferring Fuel Assembly LTL-656,crane Lifted Assembly Out of Spent Fuel Pool.Caused by Failure to Monitor Hook While Withdrawing from Pool.Assembly Returned to Proper Position
ML19322C02417 December 1979RO 79-01/OR:on 791217,while Lowering New Fuel Assembly Into Fuel Pool,Rice Hook Holding Assembly Failed,Resulting in Assembly Falling Onto Spent Fuel.Cause Not Yet Determined. Investigation Underway Re Recovery of Assembly
ML19254C72710 October 1979Ro:On 791009,Bechtel Notified Util That Reanalysis of Reactor Bldg Component Cooling Water Sys as-built Configuration Indicated Sys Would Not Remain Functional During Sse.Caused by Design Error.Mods Underway
ML19209B6972 October 1979RO 79-036/01X-0:on 791001,util Was Informed That Portion of Loop Piping Does Not Meet SSE Criteria.Caused by Failure to Include Pipe Flange Weights in Design CalculationsSafe Shutdown Earthquake
ML19249B57328 August 1979RO 79-032/01X-0 on 790828:during Evaluation Performed Per IE Bulletin 79-01,dry Well Sump Containment Isolation Valves AO-7011A & B & AO-7017A & B Were Found Unqualified for Svc. Caused by High Radiation Exposure to Solenoid Valve
ML19249B57828 August 1979RO 79-033/01X-0:on 790828,lightning Struck Station Switchyard,Causing Loss of Offsite Power & Reactor Scram. Offsite Power Restored & Reactor Startup Initiated
ML19242C77627 July 1979RO 79-027/01X-0 on 790727:lightning Struck Station Switchyard,Causing Loss of Offsite Power & Reactor Scram. HPCI Was Started for Injecting Water Into Vessel.Relief Valve 203-3A Will Be Replaced & Tested Prior to Restart