NRC-94-0025, LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr

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LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr
ML20029C767
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 04/25/1994
From: Gipson D, Tibai J
DETROIT EDISON CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
CON-NRC-94-0025, CON-NRC-94-25 LER-93-014, LER-93-14, NUDOCS 9404290114
Download: ML20029C767 (8)


Text

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Dougies H. Glpson

[ c<uer yo F rewjert Nuclear Ge . n100 Detroit r.,m a MO Nort

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Edison on()aw~h ;n D u<e H4)huri 10CFR50.73 April 25, 1994 NRC-94-0025 U. S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555

References:

1) Fermi 2 NRC Docket No. 50-341 NRC License No. NPF-43
2) NRC-94-0006, Licensing Event Report (LER) No.93-014, dated January 24, 1994

Subject:

Licensee Event Report (LER) No.93-014, Revision 1 Please find enclosed LER No.93-014, Revision 1, dated April 25, 1994, for a reportable event that occurred on December 25, 1993 A copy of this LER is also being sent to the Regional Administrator, USNRC Region III.

If you have any questions, please contact John A. Tibal, Principal Compliance Engineer, at (313) 586-4289 Sincerely, 1 Y'

Enclosure:

NRC Forms 366, 366A cc: T. G. Colburn J. B. Martin M. P. Phillips K. R. Riemer P. L. Torpey Wayne County Emergency Management Division 9404290114 940425 ,l PDR ADOCK 05000341 S PDR

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4 NRC F ORM 366 U.S. NUCL5AR REGULATORY COMMISSION APPROVED BY OMO NO. 3150-0104 6%

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DOCM L I NUMBL R (2) PAGI (3)

Fermi 2 05000 341 1 OF 7 TITLE ly Automatic Reactor Shutdown Following Failure of the Main Turbine EVENT DATE (5)~ LER HUMBER (6' REPORT NUMBER (7) OTHER F ACILITIES INVOLVED (8)

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DOCKET NUMai R 12 25 , 93 93 ~ 014 01 04 25 94 5 0 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 6: (Check one or more) (11)

MODE (9) 1 20 402(b) 20 405(c) X 50 73faH2)(iv) 73 71(b)

POWER 20 405(a)(1)0) 50 30(cH1) 50 73(a)(2)(v) 73.71(c)

L EVEL (10) 93% 20 405(a)(1)(n) 50 36(c)(2) 50.73(a)(2)(vil) OTHER 20 405(a)D)(in) 50 73(aH2)0) 50.73(a)(2)(vin)(A) M "*/'^^M"ad 20 40S(a)(f)0v) 50.73(a)(2)(n) 50.73(a)(2)(voi)(B) 20 405(a)(1)(v) 50.73(a)(2)(m) 50.73(a)(2)(x)

LICENSEE CONTACT FOR THIS LER (12) s M.n numou NuYat H pnuuc. A<.a coa.n John A. Tibai, Compliance Engineer (313) 586-4289 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) cAusE sem u couPmi N T MANuf Actunt H

[ CAUM SYS R AA COMPONENT MANUF AGURf R B TA TRB E275 Y SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MON TH DAY RAH yt s

" SUBMISSION p r.. www rwrcrco w.urdoN Data X DATE (15)

ABSTRACT (Limrt to 1400 tpaces i e., approximately 15 single 4 paced typewntten bnes) (16) s On December 25, 1993 at 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br /> an automatic reactor shutdown occurred when the main turbine tripped off line. The turbine generator tripped when the mechanical overspeed device was activated. This was due to high l vibration levels and was not due to an actual overspeed condition. The turbine generator unit and associated support systems sustained significant damage. All safety systems and isolations performed as designed during the event. An Unusual Event was declared at 1352 hours0.0156 days <br />0.376 hours <br />0.00224 weeks <br />5.14436e-4 months <br />. This was upgraded to an Alert at 1357 hours0.0157 days <br />0.377 hours <br />0.00224 weeks <br />5.163385e-4 months <br />. A fire at the main generator brush rig area was j extinguished by the plant fire brigade using hand held extinguishers.

The cause of the high turbine vibration was due to the failure of the number 9 blade, on the 8th stage, turbine end of the low pressure section number 3 The root cause or this failure continues to be under investigation.

Turbine / generator repairs will be determined based on the results of the investigation. Other corrective actions needed to return the plant to power operation are being formulated and implemented.

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REOUIRED NUMBER OF DIGITS / CHARACTERS FOR EACH BLOCK BLOCK NUMBER OF NUMDER DIGITS / CHARACTERS 1 UP TO 46 FACILITY NAME 3 IN ADDITION TO 05000 DOC E M BER-3 VARIES PAGE NUMBER 4 UP TO 76 TITLE 5 EVENT DATE-2 PER BLOCK 7 TOTAL 2 FOR YEAR 6 LER NUMBER 3 FOR SEQUENTIAL NUMBER 2 FOR REVISION NUMBER 7 ^

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UP TO 18 -- FACILITY NAME OTHER FACluTIES INVOLVED B TOTAL - DOCKET NUMBER 3 IN ADDITION TO 05000 9 1 OPERATING MODE 10 3 POWER LEVEL l' REQUIREMENTS OF 10 CFR CHECK BOX THAT APPLIES UP TO 50 FOR NAME 12 LICENSEE CONTACT 14 FOR TELEPHONE CAUSE VARIES -

2 FOR SYSTEM 13 4 FOR COMPONENT EACH COMPONENT FAILURE 4 FOR MANUFACTURER NPRDS VARIES I# SUPPLEMENTAL REPORT EXPECTED CHECK BOX THAT APPLIES 15 2 PE BLOCK i

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NRC FORM 366A u.S. NUCLEAR REGULATORY CoMMISSloN APPROVED BY UMB NO. 31bo-0104 m 92)

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THE PAPEAwoAK REDUCTION PACUECY (31500104h OFFICE OF MANAGhMENT AND BUDGET, WASH NGTON, DC 20503 FACILITY hAME (1) DOCKET NUMBEH (2) LE H NUMBER (6) PAGE g3) ygg blOVENhAu hey @oN Fermi 2 05000 341 2 oF 7 93 - 014 -

01 ru, tu -. aoa. . , w.a. m. . maw n., a unc 1,,, wm o n Initial Plant Conditions:

Operational Condition: 1 - Power Operation Reactor Power: 93 5 Percent Reactor Pressure: 1020 psig Reactor Temperature: 535 degrees Fahrenheit Description of Event:

On December 25, 1993 at 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br /> an automatic reactor shutdown [JC]

occurred in response to a main turbine [TA] trip. The specific cause of the reactor automatic shutdown was fast closure of the turbine control [JJ) valves. The main turbine generator [TB] tripped off line due to activation of the mechanical overspeed trip device. This was caused by very high vibration levels and not by an actual overspeed condition. Control room operators [ Utility-Licensed] heard a loud noise from the turbine deck followed by heavy rumbling. A number of alarms were received in the control room [NA] including the seismic monitoring alarm, turbine vibration alarms

[VA], turbine tripped alarm and alarms from turbine auxiliary systems.

Control Room operators noted that the oil supply pressure to the main turbine indicated 0 psig.

Twenty five (25) seconds into the event the main steam isolation valves (MSIV)[ISV) automatically closed due to high condenser [SG) pressure (Group 1 isolation). A Group 13 isolation (Drywell Sumps) [WK] occurred when '

reactor water level decreased to level 3, which normally occurs during an automatic shutdown from power operation. Reactor pressure was controlled by manually opening safety relief valves [RV) and water level was controlled by manual operation of the reactor core isolation cooling (RCIC)[BN] and standby feedwater (SBFW)[SK] systems.

The Nuclear Shift Supervisor [ Utility-Licensed] declared an Unusual Event at 1352 hours0.0156 days <br />0.376 hours <br />0.00224 weeks <br />5.14436e-4 months <br /> based on fire alarms and potential fire hazards from turbine lubricating oil. The emergency classification was upgraded to an Alert at 1357 hours0.0157 days <br />0.377 hours <br />0.00224 weeks <br />5.163385e-4 months <br /> based on a report of a fire on the second floor of the turbine building in the area of the lubricating oil reservoir. The fire brigade was assembled and assistance, although not utilized, was requested from the-local fire department. At 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> it was determined that a fire in the lubricat.ing oil area had not occurred. The previous communication to the control room operators had been misunderstood. The misunderstood communication was attributed to the difficulty of communicating with hand held radios while wearing self contained breathing equipment. At 1405 hours0.0163 days <br />0.39 hours <br />0.00232 weeks <br />5.346025e-4 months <br /> a small fire was identified in the generator brush rig area. This was l extinguished with portable fire extinguishers.

NRC FORM 366A (5 92)

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'NRc FORM 366A U.S. NUCLEAR REGULATORY CoMMISSloN APPROVED BY oMB No. 3150-0104 m2;

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F ACluTY NAME p) DOCKET NUMBER (2) LIR NUMBER (t) pAog g3; g LEQutNTiA. HLv3CN NUMBER NUMBER Fermi 2 05000 341 93 -

014 3oF7 01 rvT w ma, so ca v w.w. .ama,a an., a mc 1a,n m o n A review of the event determined that the initial fire alarms v .*e caused by a rapid hydrogen burn around the generator. The source of hyorogen was that used to cool the Internals of the generator. The automatic fire supnression systems operated as designed.

Significant damage was sustained by the turbine / generator and the auxiliary systems. The exciter rotor (TL] had become disconnected from the turbine / generator shaft. A hole measuring approximately 18" x 30" was found  ;

in the northwest corner of the number 3 low pressure turbine hood. General Service Water [KG) and Turbine Building Closed Cooling Water [KB] Systems, which cool hydrogen [LJ] in the main generator and air within the exciter, respectively, were breached. Approximately 550,000 gallons of water from these two systems and the fire suppression system flooded the radwaste building [NE] and turbine building [NM] basement areas disabling the radwaste systems.

The turbine lubricating oil system [TD] also suffered significant damap.

An estimated 17,000 gallons of turbine lubricating oil was spilled onta the turbine building floor areas and mixed with water in these areas.

The main condenser also sustained damage. An unknown number of condenser tubes were severed resulting in approximately 250,000 gallons of circulating water flowing into the condenser hotwell. This water was subsequently discharged through the condensate polishing demineralizers, compromising the effectiveness of the demineralizers. The water was discharged to the condensate storage tank [KA] as the hotwell level control system functioned >

to compensate for increasing hotwell water level. Reactor water quality deteriorated as the RCIC and SBFW systems utilized water from the condensate storage tank to maintain reactor water level.

All safety systems [JE] and isolations performed as designed. All safety systems were available throughout the event. Standby gas treatment [WF] was manually started in response to the loss of the reactor building HVAC [VA]

system.

At 1722 hours0.0199 days <br />0.478 hours <br />0.00285 weeks <br />6.55221e-4 months <br /> the Emergency Director downgraded the emergency status to an Unusual Event based on stable plant conditions. The Unusual Event was terminated at 2052 hours0.0238 days <br />0.57 hours <br />0.00339 weeks <br />7.80786e-4 months <br /> based on the plant being in a stable condition.

On December 26, 1993, while preparing to place the reactor into cold shutdown, reactor recirculation discharge [AD] valve B3105-F031B failed to close. Had the reactor coolant level dropped to level 2 during the December 25, 1993 event, the low pressure coolant injection [(LPCI)(BO)]

full flow may not have been available. LER 93-015 was submitted to address this valve failure.

NRC FORM 366A p 92} ,

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MRC FORM 366A U.S. NUCLEAR REGULATORY CoMMISSloN 5 93 APPROVED BY oMD No. 3150 0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER FiESPONSE TO COMPLY W'TH TMS LICENSEE EVENT REPORT (LER) E CT*2SE E T 1"RIE E L TUO E d CT$ ,

TEXT CONTINUATION E"$" S cy^uM"7 8MC"rfSj 72;M@l o J THE PAPERWORK REDUCTION PRCUECT (3150C0% OFFICE OF (

M ANAGEMENT AND BVDGET, WASH lNGTON. DC 20503 l f ACILITY NAME (1) l DOCKET NUMBER (2) LE R NUMBER (4) PAGE (3)

M QuLN11A. HEWuGN NLJMBER NUMBER Fermi 2 05000 341 - -

93 014 01 itxT or more space as reqwrea. uso esorsonar cones or NRc Form assa) (17) 1 The plant was placed in cold shutdown at 2251 hours0.0261 days <br />0.625 hours <br />0.00372 weeks <br />8.565055e-4 months <br /> on December 26, 1993 Cause of Event The reactor scram was caused by the closure of the turbine control valves when the main turbine generator (HTG) tripped off line. The turbine trip was caused by the activation of the mechanical overspeed trip device.

Activation of the mechanical overspeed trip device was due to severe vibration and not from an actual overspeed condition. The high vibration of the main turbine was the result of the failure of the number 9 blade on the 8th stage, turbine end of low pressure section number 3 The root cause of the blade failure has not yet been determined.

Analysis of Event: '

An automatic reactor shutdown was initiated by the closure of the main turbine control valves. A turbine trip was initiated by the activation of the mechanical overspeed trip mechanism. Analysis of the turbine vibration data determined that this trip was initiated due to high vibration on the main turbine unit and was not due to an actual overspeed condition. ,

Reactor and safety system responses following the automatic shutdown, including the low level 3 actuation were normal. The turbine failure did '

not result in any abnormal release of radioactive material. i A comparison of the event against the UFSAR turbine missile analysis was made by Engineering and it was determined that this event was bounded by the UFSAR analysis.

The dynamic response of the reactor / auxiliary building to the MTG failure induced excitation was measured by earthquake recording devices located in  ;

the reactor / auxiliary building. The data from these devices show that the l reactor / auxiliary building was not significantly excited or displaced by the I MTG failure event.

There are three triaxial passive peak shock recorders installed in the following reactor / auxiliary building locations; High Pressure Coolant i Injection (HPCI) room floor (El. 540'-0"), relay room floor (El. 613'-6"), l and refueling floor (El. 684'-6"). These devices are capable of recording {

accelerations in the frequency range of 2-25 Hz and fully characterize the I structural dynamic environment in the reactor / auxiliary building. Data from l

NRC FORM 366A (S.92)

. . 1 NRC FORM 366A u.S. NUCLEAR REGULATORY CoMMISSloN APPROVED BY oMB No. 3150-0104 la2, EXPIRES 5/31/95 ESTlMATED DURDEN PER RESPONSE TO COMPLY W'TH THl3

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NUMBER NUMBER i 05000 Fermi 2 341 93 -

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01 runa n, ,o.c. ,, ,.e<.a. u.. . sana n., a unc r- um <m the relay room and refueling room recorders show no significant response resulted from the turbine event.

There are also two triaxial accelerometers located on the HPCI room floor  ;

and at the top of the reactor pedestal. The accelographs indicated three  ;

short duration acceleration excursions. The first and second were separated by approximately 2 seconds and the second and third were separated by approximately one minute. Engineering analysis determined these were not l

structurally significant. Further, there is no evidence that the four inch seismic isolation gap between the turbine and auxiliary building was infringed on during the turbine event.

An independent review of the data was conducted by an outside consultant.

They determined that the instrumentation response was due to a shock impulse. A shock impulse imparts short duration, high amplitude, and low energy into a structure, whereas, an earthquake imparts long duration, broad frequencies, and high energy into a structure. Industry standards recognize shock impulses do not cause significant structural stresses. The report concluded that the shock wave length resulting from the turbine event was small compared to the building, and therefore produced local high accelerations, but the short duration, low energy, and small deformations associated with these high frequency accelerations did not compromise the structural integrity of the Reactor / Auxiliary building or che equ!pment therein.

Although planned walkdowns to examine the plant structures have not been fully completed, those structural items which have been inspected did not exhibit any evidence of loss of structural integrity.

  • Engineering has examint;d all accessible areas of the turbine pedestal. -3 Based on their examination they have concluded that the turbine pedestal I structural integrity remains intact.

Engineering is also examining the turbine support steel structure. Initial results found some cracks and tear of base metal in stiffeners in the low -

pressure section number 3 bearing box. These will be repaired.

The fire protection system performance during the event was reviewed by Engineering. Although there was some damage to the fire suppression system, the system responded as designed.

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M#Ub h b^*' Nb* BON YEAR NUMBER NUMBER 05000 341 6 OF 7 Fermi 2 93 014 -

01 m T g, ,,,o,. .,.c. ,.y,.a ,,.. . ,,o, . or wC F ,,,, m, o 7, An assessment of the effects of poor reactor water quality on fuel and vessel internals is in progress. Preliminary results indicate that there is no immediate or short term impact on vessel structural integrity. Long term affects on the vessel structual integrity are being assessed. The interim report also noted that there may be future problems associated with the Jet Pump Holddown Beams. Detroit Edison has decided to replace these during the current outage. In addition, preliminary review of the impact of poor water

.iality indicates that the zircaloy components of fuel, including fuel rod cladding, spacers and channels, should be insignificant. Inspection of some fuel assemblies, control rod drives, and control rod blades will be conducted to further assess for water chemistry concerns.

Corrective Actions:

An assessment of the structural integrity of the turbin'e pedestal was conducted. The structural integrity of the pedestal was verified to be intact. No structural repairs will be necessary.

Flood water located in the turbine building basement and radwaste building basement floors has been removed. Approximately 1.5 million gallons of water has been processed and discharged. This includes stored, high quality water which deteriorated in quality when it mixed with untreated water during the event.

betroit Edison will complete those actions agreed to by the NRC and Detroit 5',11 son management and specified in the Confirmatory Action Letter dated December 28, 1993 These actions will be completed prior to returning the unit to power operations.

Engineering has completed an inspection of the turbine building structure.

They have concluded that the turbine building was not structurally compromised (i.e., it maintained its structural integrity) as a result of the turbine event. Some cosmetic repairs will be made. However, these repairs have no impact on structural integrity.

An investigation of the event was initiated by the Plant Manager. A turbine-generator assessment team (TGAT) was given the responsibility to determine the root cause of the main turbine generator trip and develop a plan for damage assessment, repair options, reassembly, startup, and monitoring turbine performance following implementation of the corrective action. Specifically the TGAT will:

NRC FORM 366A ($ S2)

NRC FORM 366A U.S. NUCLEAR REGULA1oRY COMMISSloN APPROVED BY oMB No. 3150-0104 i 15-92>

EXPIRES 5/31/95 j 4 (STIMATED 'URDEN PER RESPONSE TO COMPi,Y WITH TMTS LICENSEE EVENT REPORT (LER) E 0 @"J L tf8Fn'fG Unli s $ $ 0 0 ,NrOF% ? 2 TEXT CONTINUATION ^' "' " 8 "*"^"'"' "" " (MNoa mn u s NUCtEAR REGULATORY COMM SSf0N. WASH NGTON. DC 20555 CD01c AND TO THE FAPERWORK REDUCTION PRCUECT p1534904h OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20SC3 FACILITY NAME (1) DOCKt'T NUMBER (2) LER HUMBER (5) PAGE p)

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01 7N7 iLx1 pt more spece a regwed, use adstronar copies or Mtc f orm 36&y (17)

Develop a sequence of events leading to the failure.

Determine the root cause of the turbine / generator failure.

Develop lessons learned Publish a final report.

The assessment of the effects of the poor water quality on the fuel and reactor vessel internals is in progress. Preliminary results indicate that it would be prudent to replace the jet pump hold down beams. This will be done during the current outage. In addition, inspection of some fuel assemblies, control rod drives, and control rod blades will be done to further assess water chemistry concerns.

Walkdown of systems located in the turbine building to as'sess any damage and identify needed repairs is in progress.

A review of the response of the Emergency Response Organization and the Fire Brigade is being conducted and lessons learned are being developed.

Previous Similar Events:

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NAC FORM 366A (5-02) k